ML19263D205: Difference between revisions

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[iTil 8i P 7            9 l A LICENSEE l B l VCODE      l S l 114 l@l                15 0 l 0 l- l 0 LICENSE l 0 l 0NUMdERl 0 l 0 l- l0 l 0 25l@l4          26 1LICENSE l1 11TYPt  l1JJ@l5 7 CAl T bdl@
[iTil 8i P 7            9 l A LICENSEE l B l VCODE      l S l 114 l@l                15 0 l 0 l- l 0 LICENSE l 0 l 0NUMdERl 0 l 0 l- l0 l 0 25l@l4          26 1LICENSE l1 11TYPt  l1JJ@l5 7 CAl T bdl@
CON'T O    i g,"c7 l L l@l 0 l 5 l 0 l 010 l 3 l 3 l 4 @l 01310] 5l 7l 9@l075 l 3 l1 l 9 l 7 l 9dol@
CON'T O    i g,"c7 l L l@l 0 l 5 l 0 l 010 l 3 l 3 l 4 @l 01310] 5l 7l 9@l075 l 3 l1 l 9 l 7 l 9dol@
                            "
74 I          8                      60                61                    DOCKET NUM8ER                  68      69      EVENT DATE                                    REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 1012l lon 3/3/79 at 0230 hours, the steam driven auxiliary feedwater pump was declared                                                                                                                          l 1
74 I          8                      60                61                    DOCKET NUM8ER                  68      69      EVENT DATE                                    REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 1012l lon 3/3/79 at 0230 hours, the steam driven auxiliary feedwater pump was declared                                                                                                                          l 1
    '
O a l inoperable because the 1B steam supply trip valve would not close.                                                                                                  The valve was                      l
O a l inoperable because the 1B steam supply trip valve would not close.                                                                                                  The valve was                      l
[O 141 ldisassembled and a nut and washor were discovered in the line.                                                                                                The numn was then                          i 10151 Ireturned t o service.                                                  An investigation was commenced and, on 3/5/79, it was                                                                            l
[O 141 ldisassembled and a nut and washor were discovered in the line.                                                                                                The numn was then                          i 10151 Ireturned t o service.                                                  An investigation was commenced and, on 3/5/79, it was                                                                            l O 6 l determined the nut and washer came from one of the three check valves upstream of                                                                                                                      l O    7      the trip valve.                                At 1828 hours on 3/5/79, the steam driven auxiliary feedwater pump [
  .
O 6 l determined the nut and washer came from one of the three check valves upstream of                                                                                                                      l O    7      the trip valve.                                At 1828 hours on 3/5/79, the steam driven auxiliary feedwater pump [
                                                                                                                                          '
ITITl            was anain isolated and declared inoperable.
ITITl            was anain isolated and declared inoperable.
83 l
83 l
   '    7        89 SYSTEM                          CAUSE              CAUSE                                                            COMP.          VALV E CODE                          CODE          SUBCODE                    COMPONENT CODE                        SUSCOCl          SUBCODE
   '    7        89 SYSTEM                          CAUSE              CAUSE                                                            COMP.          VALV E CODE                          CODE          SUBCODE                    COMPONENT CODE                        SUSCOCl          SUBCODE O 9                                l C l H l@ l E l@ W@ l V l A l L l V l E Xl@ lC[@ y @
  ,
O 9                                l C l H l@ l E l@ W@ l V l A l L l V l E Xl@ lC[@ y @
7        8                          9                to                11                12            13                                18            19              20
7        8                          9                to                11                12            13                                18            19              20
   '                                                                                                                                      CCCURRENCE                                                R EVISION SEQUENTIAL                                                    REPORT LE R /RO      IVENT YEAR                                              REPORT NO.                                CODE                  TYPE                              NO.
   '                                                                                                                                      CCCURRENCE                                                R EVISION SEQUENTIAL                                                    REPORT LE R /RO      IVENT YEAR                                              REPORT NO.                                CODE                  TYPE                              NO.
  ,
  '
h ,RE QRT p l9 l                                          [-.]
h ,RE QRT p l9 l                                          [-.]
23 l0 24 l0 l 7l              y            l0l1l M
23 l0 24 l0 l 7l              y            l0l1l M
Line 45: Line 36:
36 l0l0l0 0l 21                      40 l Yl@
36 l0l0l0 0l 21                      40 l Yl@
41 l42 Yl@            l43A l@          lCl6l6 5l@
41 l42 Yl@            l43A l@          lCl6l6 5l@
44                  47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS
44                  47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS L'_1.OJ lIbe three upstrean check valves were disassenblai and inspected.                                                                                                The nuts and                          I i i Iwashers on the 1A and 1B check valves were intact. However, the nut and washer on                                                                                                                        I I
    '
L'_1.OJ lIbe three upstrean check valves were disassenblai and inspected.                                                                                                The nuts and                          I i i Iwashers on the 1A and 1B check valves were intact. However, the nut and washer on                                                                                                                        I I
1 2      'Ithe IC steam generator steam supply check valve to the auxiliary feedwater pump were j
1 2      'Ithe IC steam generator steam supply check valve to the auxiliary feedwater pump were j
,        1i13lImissinc.                        The nut and washer were replaced and the nut was pinned per vendor i 4          recommendation.                                                                                                                                                                                I 7        8 9                                                                                                                                                                                                80 STA                    % POWER                                      OTF.ER STATUS              OS          HY                              DISCOVERY DESCRIPTION
,        1i13lImissinc.                        The nut and washer were replaced and the nut was pinned per vendor i 4          recommendation.                                                                                                                                                                                I 7        8 9                                                                                                                                                                                                80 STA                    % POWER                                      OTF.ER STATUS              OS          HY                              DISCOVERY DESCRIPTION
[A,_j@l Operator observation
[A,_j@l Operator observation
   ~
   ~
i s C l@ l0 l0 l0 l@l                                                N/A                    l                                                                                                    l 1                  A TtvlTY CO TENT RELEASED OF RELEASE                                    AMOUNT OF ACTIVITY                                                                  LOCATION OF HELEASE
i s C l@ l0 l0 l0 l@l                                                N/A                    l                                                                                                    l 1                  A TtvlTY CO TENT RELEASED OF RELEASE                                    AMOUNT OF ACTIVITY                                                                  LOCATION OF HELEASE i    6 W @ l Zl@l                                                        N/A                    l            l                                          N/A                                          l
  ,
   !    7        8 9                  to            11                                                      44              45                                                                                    80 PERSONNEL EXPOSURES NUMBER                TYPE                DESCRIPTION 39 i 7 l0l0l0l@lZl@l      '                          ''
i    6 W @ l Zl@l                                                        N/A                    l            l                                          N/A                                          l
N/A l
   !    7        8 9                  to            11                                                      44              45                                                                                    80 PERSONNEL EXPOSURES
  '
NUMBER                TYPE                DESCRIPTION 39
        '
i 7
                  ' '
l0l0l0l@lZl@l      '                          ''
N/A
                                                                                                                                                                                                                    '
l
                           ,ERsO~~E'L mu'R'ie$
                           ,ERsO~~E'L mu'R'ie$
  '
NuusER                oESCmPriON@
NuusER                oESCmPriON@
1 a        l0l0 0 l@l _                                                      N/A 7          8 9                  11      12                                                                                                                                                                80 LOSS OF OR DAMAGE TO FACILtTY TYPE        DESCRIPTION 1 9 lZl@l                                                              N/A 7        8 9              to                                                                                                                                                                              80
1 a        l0l0 0 l@l _                                                      N/A 7          8 9                  11      12                                                                                                                                                                80 LOSS OF OR DAMAGE TO FACILtTY TYPE        DESCRIPTION 1 9 lZl@l                                                              N/A 7        8 9              to                                                                                                                                                                              80 2 0        ,SSuE        l @L'SCm, TION                                        N/A @
                            '""" "                                                                                                                                                        ""
2 0        ,SSuE        l @L'SCm, TION                                        N/A @
7903260279                                                        l      lllbllll
7903260279                                                        l      lllbllll
                                                                                                                                                                                                   'S ' "'"
                                                                                                                                                                                                   'S ' "'"
Line 76: Line 52:
7        8 9              to                                                                                                                                      68 69                                    80 5 NAME OF PREPARER ng                                              PHONE:
7        8 9              to                                                                                                                                      68 69                                    80 5 NAME OF PREPARER ng                                              PHONE:
412-643-1258                              2
412-643-1258                              2
  ,
              ._              _ . _ _                          _ _ _ _ _ _ _ _ . __                        ..                                                                .
      ,                                                                                                                                                  . . _                                .. _. _ _____


  . . -
Attachment To LER 79-007/0lT
Attachment To LER 79-007/0lT
*      ,.'                          Beaver Valley Power Station
*      ,.'                          Beaver Valley Power Station oDuquesne Light Company.
* oDuquesne Light Company.
Docket No. 50-334 On March 3, 1979 at 0230 hours, the steam driren auxiliary feedwater pump was declared inoperable because the 1B steam supply trip valve would not close. The valve was isolated and disassembled and a nut and washer were discovered in the line. The trip valve was reassembled and the pump was returned to operable condition. The plant was then returned to power. An investigation was commenced to determine the orie,in of the components. On March 5, 1979, it was determined the nut and washer came from one of the three check valves upstream of the trip valve.      In the event of a ruptured steam line, these check valves control backflow from the operating steam generators to the ruptured line. Operation with an inoperable check valve was in a manner less conservative than described in the SAR. Therefore, at 1828 hours on March 5, the steam driven auxiliary feedwater pump was again isolated and declared inoperable.      Station shutdown was commenced at 2000 hours.
Docket No. 50-334 On March 3, 1979 at 0230 hours, the steam driren auxiliary feedwater pump was declared inoperable because the 1B steam supply trip valve would not close. The valve was isolated and disassembled and a nut and washer were discovered in the line. The trip valve was reassembled and the pump was returned to operable condition. The plant was then returned to power. An investigation was commenced to determine the orie,in of the components. On March 5, 1979, it was determined the nut and washer came from one of the three check valves upstream of the trip valve.      In the event of a ruptured steam line, these check valves control backflow from the operating steam generators to the ruptured line. Operation with an inoperable check valve was in a manner less conservative than described in the SAR. Therefore, at 1828 hours on March 5, the steam driven auxiliary feedwater pump was again isolated and declared inoperable.      Station shutdown was commenced at 2000 hours.
The three upstream check valves were disassembled and inspected. The nuts and washers on the 1A and 1B check valves were intact. However, the nut and washer on the IC steam generator steam supply check valve to the auxiliary feedwater pump were missing. Following discussions with the valve vendor, the nut and washer were replaced and the nut was pinned per vendor recommendation.
The three upstream check valves were disassembled and inspected. The nuts and washers on the 1A and 1B check valves were intact. However, the nut and washer on the IC steam generator steam supply check valve to the auxiliary feedwater pump were missing. Following discussions with the valve vendor, the nut and washer were replaced and the nut was pinned per vendor recommendation.
                                                    .
         -          - - . - ,}}
         -          - - . - ,}}

Latest revision as of 20:37, 1 February 2020

LER 79-007/01T-0 on 790305:steam Driver Auxiliary Feedwater Pump Declared Inoperable Because 1B Steam Supply Trip Valve Would Not Close.Caused by Missing Nut & Washer on 1C Steam Generator Supply Check Valve.Nut & Washer Replaced
ML19263D205
Person / Time
Site: Beaver Valley
Issue date: 03/19/1979
From: Werling J
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19263D203 List:
References
LER-79-007-01T, LER-79-7-1T, NUDOCS 7903260279
Download: ML19263D205 (2)


Text

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NRC FORM 366 . U.S. NUCLEAR REGULATORY COMMtSSLON (7 7M* '

- LICENSEE EVENT REPORT CONTROL BLOCK: l l l l l l l (PLEASE PRINT OR TYPE ALL REQUIREO INFORIV# TION) 1 6

[iTil 8i P 7 9 l A LICENSEE l B l VCODE l S l 114 l@l 15 0 l 0 l- l 0 LICENSE l 0 l 0NUMdERl 0 l 0 l- l0 l 0 25l@l4 26 1LICENSE l1 11TYPt l1JJ@l5 7 CAl T bdl@

CON'T O i g,"c7 l L l@l 0 l 5 l 0 l 010 l 3 l 3 l 4 @l 01310] 5l 7l 9@l075 l 3 l1 l 9 l 7 l 9dol@

74 I 8 60 61 DOCKET NUM8ER 68 69 EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 1012l lon 3/3/79 at 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br />, the steam driven auxiliary feedwater pump was declared l 1

O a l inoperable because the 1B steam supply trip valve would not close. The valve was l

[O 141 ldisassembled and a nut and washor were discovered in the line. The numn was then i 10151 Ireturned t o service. An investigation was commenced and, on 3/5/79, it was l O 6 l determined the nut and washer came from one of the three check valves upstream of l O 7 the trip valve. At 1828 hours0.0212 days <br />0.508 hours <br />0.00302 weeks <br />6.95554e-4 months <br /> on 3/5/79, the steam driven auxiliary feedwater pump [

ITITl was anain isolated and declared inoperable.

83 l

' 7 89 SYSTEM CAUSE CAUSE COMP. VALV E CODE CODE SUBCODE COMPONENT CODE SUSCOCl SUBCODE O 9 l C l H l@ l E l@ W@ l V l A l L l V l E Xl@ lC[@ y @

7 8 9 to 11 12 13 18 19 20

' CCCURRENCE R EVISION SEQUENTIAL REPORT LE R /RO IVENT YEAR REPORT NO. CODE TYPE NO.

h ,RE QRT p l9 l [-.]

23 l0 24 l0 l 7l y l0l1l M

lTl 30 l-l l0 l

_ 21 22 26 27 28 31 32 N A T ON ON PLANT HOURS S B ITT O FORT B. St PPLIER N' ANU F CTURER lA 33 l@l34 Zl@ l35C l@ lAl@

36 l0l0l0 0l 21 40 l Yl@

41 l42 Yl@ l43A l@ lCl6l6 5l@

44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS L'_1.OJ lIbe three upstrean check valves were disassenblai and inspected. The nuts and I i i Iwashers on the 1A and 1B check valves were intact. However, the nut and washer on I I

1 2 'Ithe IC steam generator steam supply check valve to the auxiliary feedwater pump were j

, 1i13lImissinc. The nut and washer were replaced and the nut was pinned per vendor i 4 recommendation. I 7 8 9 80 STA  % POWER OTF.ER STATUS OS HY DISCOVERY DESCRIPTION

[A,_j@l Operator observation

~

i s C l@ l0 l0 l0 l@l N/A l l 1 A TtvlTY CO TENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF HELEASE i 6 W @ l Zl@l N/A l l N/A l

! 7 8 9 to 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION 39 i 7 l0l0l0l@lZl@l '

N/A l

,ERsO~~E'L mu'R'ie$

NuusER oESCmPriON@

1 a l0l0 0 l@l _ N/A 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILtTY TYPE DESCRIPTION 1 9 lZl@l N/A 7 8 9 to 80 2 0 ,SSuE l @L'SCm, TION N/A @

7903260279 l lllbllll

'S ' "'"

l l l l :;

7 8 9 to 68 69 80 5 NAME OF PREPARER ng PHONE:

412-643-1258 2

Attachment To LER 79-007/0lT

  • ,.' Beaver Valley Power Station oDuquesne Light Company.

Docket No. 50-334 On March 3, 1979 at 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br />, the steam driren auxiliary feedwater pump was declared inoperable because the 1B steam supply trip valve would not close. The valve was isolated and disassembled and a nut and washer were discovered in the line. The trip valve was reassembled and the pump was returned to operable condition. The plant was then returned to power. An investigation was commenced to determine the orie,in of the components. On March 5, 1979, it was determined the nut and washer came from one of the three check valves upstream of the trip valve. In the event of a ruptured steam line, these check valves control backflow from the operating steam generators to the ruptured line. Operation with an inoperable check valve was in a manner less conservative than described in the SAR. Therefore, at 1828 hours0.0212 days <br />0.508 hours <br />0.00302 weeks <br />6.95554e-4 months <br /> on March 5, the steam driven auxiliary feedwater pump was again isolated and declared inoperable. Station shutdown was commenced at 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br />.

The three upstream check valves were disassembled and inspected. The nuts and washers on the 1A and 1B check valves were intact. However, the nut and washer on the IC steam generator steam supply check valve to the auxiliary feedwater pump were missing. Following discussions with the valve vendor, the nut and washer were replaced and the nut was pinned per vendor recommendation.

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