IR 05000321/2010002: Difference between revisions
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| issue date = 04/29/2010 | | issue date = 04/29/2010 | ||
| title = IR 05000321-10-002, 05000366-10-002; 01/01/2010 - 03/31/2010; Edwin I. Hatch Nuclear Plant, Units 1 & 2, Event Follow-Up | | title = IR 05000321-10-002, 05000366-10-002; 01/01/2010 - 03/31/2010; Edwin I. Hatch Nuclear Plant, Units 1 & 2, Event Follow-Up | ||
| author name = Shaeffer S | | author name = Shaeffer S | ||
| author affiliation = NRC/RGN-II/DRP/RPB2 | | author affiliation = NRC/RGN-II/DRP/RPB2 | ||
| addressee name = Madison D | | addressee name = Madison D | ||
| addressee affiliation = Southern Nuclear Operating Co, Inc | | addressee affiliation = Southern Nuclear Operating Co, Inc | ||
| docket = 05000321, 05000366 | | docket = 05000321, 05000366 | ||
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=Text= | =Text= | ||
{{#Wiki_filter: | {{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II MARQUIS ONE TOWER 245 PEACHTREE CENTER AVENUE, NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 April 29, 2010 Mr. Dennis Vice President Southern Nuclear Operating Company, Inc. Edwin I. Hatch Nuclear Plant 11028 Hatch Parkway North Baxley, GA 31513 | ||
Mr. Dennis Vice President Southern Nuclear Operating Company, Inc. Edwin I. Hatch Nuclear Plant 11028 Hatch Parkway North Baxley, GA 31513 | |||
SUBJECT: EDWIN I. HATCH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000321/2010002 AND 05000366/2010002 | SUBJECT: EDWIN I. HATCH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000321/2010002 AND 05000366/2010002 | ||
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In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosures, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the SNC 2 NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosures, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the SNC 2 NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | ||
Sincerely,/RA/ Scott M. Shaeffer, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos.: 50-321, 50-366 License Nos.: DPR-57 and NPF-5 | Sincerely, | ||
/RA/ Scott M. Shaeffer, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos.: 50-321, 50-366 License Nos.: DPR-57 and NPF-5 | |||
===Enclosure:=== | ===Enclosure:=== | ||
Inspection Report 05000321/2010002, 05000366/2010002 | Inspection Report 05000321/2010002, 05000366/2010002 w/Attachment: Supplemental Information | ||
Supplemental Information | |||
REGION II== | |||
Docket Nos.: 50-321, 50-366 License Nos.: DPR-57 and NPF-5 | Docket Nos.: 50-321, 50-366 License Nos.: DPR-57 and NPF-5 | ||
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No findings of significance were identified. | No findings of significance were identified. | ||
===Cornerstone:=== | ===Cornerstone: Emergency Preparedness=== | ||
1EP6 Drill Evaluation | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Line 562: | Line 521: | ||
===Closed=== | ===Closed=== | ||
: 05000321,366/2515/180 TI Inspection of Procedures and Processes for Managing Fatigue (Section 4OA5.2) | : 05000321,366/2515/180 TI Inspection of Procedures and Processes for Managing Fatigue (Section 4OA5.2) | ||
: 05000366/2009-003 LER Main Generator Runback Due to High Stator Cooling Water Temperature (Section 4OA3) | |||
Opened & | |||
===Closed=== | ===Closed=== | ||
: 05000366/2010002-02 FIN Failure to implement adequate configuration control on Unit 2 main generator stator water cooling temperature control instrument loop, 2N43-F100 (Section 4OA3) | |||
===Discussed=== | ===Discussed=== | ||
None | None | ||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
}} | }} |
Revision as of 09:40, 11 July 2019
ML101200162 | |
Person / Time | |
---|---|
Site: | Hatch |
Issue date: | 04/29/2010 |
From: | Scott Shaeffer NRC/RGN-II/DRP/RPB2 |
To: | Madison D Southern Nuclear Operating Co |
References | |
FOIA/PA-2010-0209 IR-10-002 | |
Download: ML101200162 (42) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II MARQUIS ONE TOWER 245 PEACHTREE CENTER AVENUE, NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 April 29, 2010 Mr. Dennis Vice President Southern Nuclear Operating Company, Inc. Edwin I. Hatch Nuclear Plant 11028 Hatch Parkway North Baxley, GA 31513
SUBJECT: EDWIN I. HATCH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000321/2010002 AND 05000366/2010002
Dear Mr. Madison:
On March 31, 2010, U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your Edwin I. Hatch Nuclear Plant, Units 1 and 2. The enclosed integrated inspection report documents the inspection results, which were discussed on April 16, 2010, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities and interviewed personnel.
Based on the results of this inspection one self-revealing finding of very low safety significance (Green) was identified. The finding did not involve a violation of NRC requirements. If you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the Hatch facility. The information you provide will be considered in accordance with Inspection Manual Chapter 0305.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosures, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the SNC 2 NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/ Scott M. Shaeffer, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos.: 50-321, 50-366 License Nos.: DPR-57 and NPF-5
Enclosure:
Inspection Report 05000321/2010002, 05000366/2010002 w/Attachment: Supplemental Information
REGION II==
Docket Nos.: 50-321, 50-366 License Nos.: DPR-57 and NPF-5
Report Nos.: 05000321/2010002 and 05000366/2010002 Licensee: Southern Nuclear Operating Company, Inc.
Facility: Edwin I. Hatch Nuclear Plant Location: Baxley, Georgia 31513
Dates: January 1 - March 31, 2010 Inspectors: E. Morris, Senior Resident Inspector P. Niebaum, Resident Inspector S. Rose, Senior Project Engineer L. Pressley, Project Engineer B. Collins, Reactor Inspector (Section 1R08) W. Loo, Senior Health Physicist (Sections 2RS5, 2RS6, 4OA1) L. Mahlahla, Health Physicist (Section 2RS5) A. Nielsen, Health Physicist (Sections 2RS5, 2RS7) H. Gepford, Senior Health Physicist (Sections 2RS1, 4OA1)
Approved by: Scott M. Shaeffer, Chief Reactor Projects Branch 2 Division of Reactor Projects Enclosure
SUMMARY OF FINDINGS
IR 05000321/2010-002, 05000366/2010-002; 01/01/2010-03/31/2010; Edwin I. Hatch Nuclear Plant, Units 1 and 2, Event Follow-up
The report covered a three-month period of inspection by two resident inspectors, two project engineers, one reactor inspector, and four health physicists. One self-revealing Green finding was identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). The cross-cutting aspect was determined using IMC 0305, Operating Reactor Assessment Program. Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review.
A. NRC-Identified and Self-Revealing Findings
Cornerstone: Initiating Events
- Green.
A self-revealing finding was identified for the licensee's failure to create, implement, and make available to maintenance personnel, quality processes or documents for configuration control. Specifically, the licensee failed to maintain the correct configuration of the stator water cooling (SWC) temperature control instrument loop air-operated valve, 2N43-F100, as required by licensee procedure NMP-ES-014, Air Operated Valve Program. The failure to implement adequate configuration control on the SWC temperature control instrument loop directly resulted in a Unit 2 reactor scram on June 20, 2009. The licensee has addressed this issue in their Corrective Action Program (CAP) and developed corrective actions in CR 2009106326. As part of the licensee's immediate corrective actions the Unit 2 SWC instrument loop was reconfigured to the correct alignment, and changes were made to procedure NMP-ES-014.
This performance deficiency was more than minor because it was associated with the Configuration Control attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of those events that upset plant stability. Specifically, inadequate configuration control resulted in a Unit 2 reactor scram on June 20, 2009. The significance of this finding was screened using the Phase 1 of the Significance Determination Process (SDP) in accordance with NRC Inspection Manual Chapter 0609 Attachment 4. Because the finding contributed to a reactor scram, but did not affect mitigation equipment availability, the finding screened as
- Green.
This finding had a cross-cutting aspect in the Resources component of the Human Performance area, because the licensee did not provide complete, accurate and up-to-date design documentation, procedures, and work packages, and correct labeling of components. Specifically, the licensee did not implement a means of configuration control of the SWC temperature control instrument loop. (H.2(c)). (Section 4OA3.1)
REPORT DETAILS
Summary of Plant Status
Unit 1 began the inspection period at or near 100% Rated Thermal Power (RTP) and shutdown for a refueling outage on February 8, 2010. A reactor startup began on March 18 and the main generator was placed online on March 21. Unit 1 returned to 100% on March 27.
Unit 2 began the inspection period at or near 100% RTP. On February 16, a load reduction to approximately 60% was necessary to replace a main generator stator water cooling valve. Unit 2 returned to 100% on February 20 and remained at or near 100% for the remainder of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather
a. Inspection Scope
Readiness for Impending Adverse Weather Conditions: Freezing. The inspectors performed a review of licensee readiness to cope with freezing weather experienced at the site January 1 - 8. The inspectors performed walk downs to verify that equipment was in place to mitigate the potential impacts from freezing conditions. The inspectors reviewed licensee procedure DI-OPS-36-0989, Cold Weather Checks, to verify actions were taken by the licensee to cope with freezing conditions. Documents reviewed are listed in the Attachment.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment
a. Inspection Scope
Partial Walkdowns. The inspectors performed partial walkdowns of the following three systems when the opposite train was removed from service, a remaining operable system/train with high risk significance for the plant configuration exists, or a system/train that was recently realigned following an extended system outage or a risk significant single train system exists. The inspectors checked system valve positions, electrical breaker positions, and operating switch positions to evaluate the operability of the opposite trains or components by comparing the position listed in the system operating procedure to the actual position. Documents reviewed are listed in the Attachment.
- Unit 1 Reactor Core Isolation Cooling (RCIC) while Unit 1 High Pressure Cooling Injection (HPCI) was out of service (OOS) on January 5.
- Unit 2A Emergency Diesel Generator (EDG) while the 1B Swing EDG was OOS on February 26.
- Common Main Control Room (MCR) 1A and 1B Air Handling Units (AHU) while the 1C MCR AHU was OOS on March 22.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
a. Inspection Scope
Fire Area Tours. The inspectors toured the following five risk significant plant areas to assess the material condition of the fire protection and detection equipment, verify fire protection equipment was not obstructed and that transient combustibles were properly controlled. The inspectors reviewed the site Fire Hazards Analysis to verify that the necessary fire fighting equipment, such as fire extinguishers, hose stations, ladders, and communications equipment, was in place. Documents reviewed are listed in the Attachment.
- Unit 1/Unit 2 600V switchgear rooms
- Unit 1/Unit 2 Annunciator rooms
- Unit 1/Unit 2 Station Service Battery Rooms 112'
- Unit 1/Unit 2 RPS and Cable Tray Rooms
- Unit 1 Torus Room and Steam Chase
b. Findings
No findings of significance were identified.
1R08 Inservice Inspection Activities
From February 15, 2010 through February 19, 2010, the inspectors conducted a review of the implementation of the licensee's Inservice Inspection (ISI) Program for monitoring degradation of the reactor coolant system, steam generator tubes, emergency feedwater systems, risk-significant piping and components and containment systems.
The inspections described in Sections 1R08.1 and 1R08.2 below constituted one inservice inspection sample as defined in Inspection Procedure 71111.08-05.
.1 Piping Systems ISI
a. Inspection Scope
The inspectors evaluated the following non-destructive examinations mandated by the ASME Code Section XI to verify compliance with the ASME Code Section XI and Section V requirements and, if any indications and defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement.
- Ultrasonic Testing (UT) examination of weld 1C11-1CRD-3-R-18A-OL, ASME Class 1, Reactor Coolant System, 6-inch diameter overlay weld (Nozzle N9) - Direct Observation
- UT examination of weld 1B21-1MS-24B-14, ASME Class 2, Main Steam System, 24-inch Category B-J weld - Direct Observation
- Phased Array UT exam of weld 1B31-1RC-12BR-D-5, ASME Class 1, Reactor Coolant System, 12-inch Category B-F dissimilar metal weld - Direct Observation The inspectors reviewed the following examination records (volumetric or surface) with recordable indications that were analytically evaluated and accepted for continued service against the ASME Code Section XI or an NRC-approved alternative.
- Indication found during UT of weld 1B21-1MS-24B-14, Main Steam System pipe-to-valve weld The inspectors reviewed documentation for the following pressure boundary welds completed for risk-significant systems during the outage to evaluate if the licensee applied the pre-service non-destructive examinations and acceptance criteria required by ASME Code Section XI. In addition, the inspectors reviewed the welding procedure specification, welder qualifications, welding material certification and supporting weld procedure qualification records, to evaluate if the weld procedures were qualified in accordance with the requirements of Construction Code and the ASME Code Section IX.
- Work Order 1081999513, 20-inch hemispherical end cap-to-pipe weld #12797-1-1 for assembly of Residual Heat Removal (RHR) Acoustic Resonator
- Work Order 1081999513, 3-inch flange-to-pipe weld #12797-3A for assembly of RHR Acoustic Resonator
b. Findings
No findings of significance were identified.
.2 Identification and Resolution of Problems
a. Inspection Scope
The inspectors performed a review of ISI-related problems entered into the licensee's corrective action program and conducted interviews with licensee staff to determine if;
- the licensee had established an appropriate threshold for identifying ISI-related problems;
- the licensee had performed a root cause (if applicable) and taken appropriate corrective actions; and
- the licensee had evaluated operating experience and industry generic issues related to ISI and pressure boundary integrity.
The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requirements. The corrective action documents reviewed by the inspectors are listed in the Attachment.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification
a. Inspection Scope
Resident Quarterly Observation The inspectors observed the performance of licensee simulator scenario conducted on January 13 which included damage to irradiated fuel during core offload, an un-isolable steam break on the "C" main steam line, an anticipated transient without scram, trip of the reactor core isolation cooling, and failure of an emergency diesel to start. The inspectors reviewed the classification in accordance with the Emergency Plan and licensee procedures 10AC-MGR-019-0, Procedure Use and Adherence, and DI-OPS-59-0896, Operations Management Expectations, to verify formality of communication, procedure usage, alarm response, control board manipulations, group dynamics, and supervisory oversight. The inspectors attended the post-exercise critique of operator performance to assess if the licensee identified performance issues were comparable to those identified by the inspectors. In addition, the inspectors reviewed the critique results from previous training sessions to assess performance improvement.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed the following sample associated with structures, systems, and components to assess the licensee's implementation of the Maintenance Rule (10 CFR 50.65) with respect to the characterization of failures and the appropriateness of the associated (a)
- (1) or (a)
- (2) classification. The inspectors reviewed operator logs, associated Condition Reports (CRs), Maintenance Work Orders (MWO), and the licensee's procedures for implementing the Maintenance Rule to determine if equipment failures were being identified, properly assessed, and corrective actions established to return the equipment to a satisfactory condition. Documents reviewed are listed in the Attachment.
- Unit 1 and 2 CRD Pumps
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Evaluation
a. Inspection Scope
The inspectors reviewed the following five Plan of the Day (POD) documents listed below to verify that risk assessments were performed prior to components being removed from service. The inspectors reviewed the risk assessment and risk management controls implemented for these activities to verify they were completed in accordance with licensee procedure 90AC-OAM-002-0, Scheduling Maintenance, and 10 CFR 50.65 (a)(4). For emergent work, the inspectors assessed whether any increase in risk was promptly assessed and that appropriate risk management actions were implemented.
- January 2 - 8, 1A EDG OOS for corrective maintenance, U1 HPCI OOS for planned maintenance, U1/U2 MCR exhaust damper corrective maintenance, U2 reactor manual scram functional test
- January 16 - 22, 2A EDG OOS for temperature switch replacement, 2B Plant Service Water Pump OOS for preventative maintenance, 2A Station Service Battery charger OOS for corrective maintenance, 1A CRD Pump replacement
- January 30 - February 5, 1A RHR train OOS for surveillance, 2A Plant Service Water OOS for preventative maintenance, 1A Train of Main Control Room A/C system for maintenance
- February 16 - 19, Unit 1 B RHR shutdown cooling with A RHR out of service, switchyard maintenance activities, HPCI pump testing, and control rod drive exercises, 1A EDG out of service
- March 8 - 12, Unit 1 outage safety assessments with transition from Mode 5 to Mode 4
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
a. Inspection Scope
The inspectors reviewed the following six operability evaluations and compared the evaluations to the system requirements identified in the TS and the FSAR to ensure operability was adequately assessed and the system or component remained available to perform its intended function. Also, the inspectors assessed the adequacy of compensatory measures implemented as a result of the condition. Documents reviewed are listed in the Attachment.
- Unit 1 condensate storage tank level switches with heat trace unavailable and temperatures below 32F
- Unit 1A EDG low jacket cooling water pressure
- Reduced plant service water flows to 1A, 1B and 1C MCR A/C units
- 2A station service battery charger output with an AC voltage ripple
- 1B EDG 'A' start circuit inoperable
- 2A EDG air coolant heat exchanger pipe vibration
b. Findings
No findings of significance were identified.
1R18 Plant Modifications
a. Inspection Scope
The inspectors reviewed the following plant temporary modifications (TM) to ensure that safety functions of important safety systems have not been affected. Also, the inspectors verified that the design bases, licensing bases and performance capability of risk significant structures, systems and components have not been degraded through modifications. The inspectors verified that any modifications performed during increased risk-significant configurations did not place the plant in an unsafe condition. Documents reviewed are listed in the Attachment.
- U1 RHRSW flume discharge to Unit 2 circulating water flume
b. Findings
No findings of significance were identified.
1R19 Post Maintenance Testing
a. Inspection Scope
For the following five post maintenance tests, the inspectors reviewed the test scope to verify the test demonstrated the work performed was completed correctly and the affected equipment was functional and operable in accordance with TS requirements. The inspectors also reviewed equipment status and alignment to verify the system or component was available to perform the required safety function. Documents reviewed are listed in the Attachment.
- 34SV-E41-002-1, "HPCI Pump Operability," replacement of the Unit 2 HPCI electro-mechanical EG-R hydraulic actuator, January 19
- 34SV-R43-001-2, "Diesel Generator 2A Monthly Test," replace 2A EDG lube oil temperature switch, January 19
- WO 1100014501, "1Z41-F018A repair," repair MCR exhaust damper 1Z41-F018A, January 20
- WO 1100475801, "1A residual heat removal service water pump," repair high indicated bearing temperature, March 10
- 34SV-T22-001-0, "Secondary Containment Test," repairs to U2 Reactor building air-lock door, February 10
b. Findings
No findings of significance were identified.
1R20 Refueling and Outage Activities
.1 Unit-1 Refueling Outage
a. Inspection Scope
The inspectors reviewed the licensee's shutdown risk monitoring program and the outage schedule to verify the licensee's use of risk management techniques, incorporation of operating experience, and past lessons learned for the refueling outage beginning February 8, 2010. Additionally, the inspectors reviewed the shutdown safety assessment to verify the licensee had contingency plans and these plans included sufficient equipment to maintain a defense-in-depth approach to safety. The inspectors routinely verified the licensee was correctly maintaining required equipment in service in accordance with the overall outage safety assessment. During the refueling outage, the inspectors monitored licensee control over the outage activities listed below. Documents reviewed are listed in the Attachment.
- Reactor Coolant System cooldown following shutdown
- 3 clearances to verify implementation of the clearance process and the associated equipment was properly configured to support the function of the clearance
- Fuel movement during core reload
- Technical Specifications (TS) and licensee procedures to verify mode change requirements were met
- Walkdown of the torus proper and other areas to verify material conditions supported plant operations
- Shutdown Margin determination
- Drywell containment closeout inspection activities and performed an independent walkdown prior to closeout
- Licensee identification and resolution of problems related to outage activities
- Outage work hour controls
- Reactor startup and power ascension
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors reviewed eight licensee surveillance test procedures and either witnessed the test or reviewed test records for the following surveillances to determine if the scope of the test adequately demonstrated the affected equipment was operable. The inspectors reviewed these activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance. The inspectors reviewed licensee procedure AG-MGR-21-0386, Evolution and Pre-and Post-Job Brief Guidance, and attended selected briefings to determine if procedure requirements were met. Documents reviewed are listed in the Attachment.
Surveillance Tests
- 34SV-R43-011-2, Diesel Generator 2A 24 Month Operability Test, Rev. 2.20
- 42SV-T46-003-1, Testing of SGT Filter Trains, Ver. 9.23
- 57IT-MIC-004-2, Testing of the LOCA/LOSP Timer Cards, Ver. 1.9 Reactor Coolant System Leak Detection Test
- 34SV-SUV-019-2, Surveillance Checks, Ver. 34.23 Containment Isolation Valves
- 42SV-TET-001-0, Local Leak Rate Test (LLRT) Testing Methodology for 1B21-F010A
- 42SV-TET-001-0, Local Leak Rate Test (LLRT) Testing Methodology for 1E41-F049 In-Service Test
- 34SV-E41-002-2, High Pressure Coolant Injection Pump Operability, Rev. 30.21
- 34SV-E51-002-1, RCIC Pump Operability, Ver. 20.14
b. Findings
No findings of significance were identified.
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
a. Inspection Scope
The inspectors observed the following emergency plan evolution. The inspectors observed licensee activities in the simulator and Technical Support Center to verify implementation of licensee procedure 10AC-MGR-006-0, Hatch Emergency Plan. The inspectors reviewed the classification of the simulated events and the development of protective action recommendations to verify these activities were conducted in accordance with licensee procedure 73EP-EIP-001-0, Emergency Classification and Initial Actions. The inspectors also reviewed licensee procedure 73EP-EIP-073-0, Onsite Emergency Notification, to verify the proper offsite notifications were made. The inspectors attended the post-exercise critique to assess the licensee's effectiveness in identifying areas of improvement. Documents reviewed are listed in the Attachment.
- Emergency Preparedness (EP) drill on January 13
b. Findings
No findings of significance were identified.
RADIATION SAFETY
Cornerstones: Occupational Radiation Safety and Public Radiation Safety
2RS1 Radiological Hazard Assessment and Exposure Control
a. Inspection Scope
Radiological Hazard Assessment. The inspectors reviewed a number of radiological surveys, including those performed for airborne areas, of locations throughout the facility including the Unit 1 (U1) drywell, U1 and Unit 2 (U2) reactor buildings, and the independent spent fuel storage installation (ISFSI). The inspectors also walked down those same areas and radioactive material storage locations with a survey instrument, evaluating material condition, postings, and radiological controls. The inspectors observed jobs in radiologically risk-significant areas including high radiation areas and areas with, or with the potential for, airborne activity. The inspectors determined that the surveys were adequate in thoroughness and frequency for the identified hazards.
Instructions to Workers. During plant walk downs, the inspectors observed labeling and radiological controls on containers of radioactive material. The inspectors also reviewed radiation work permits (RWP) used for accessing high radiation areas and airborne areas, verifying that appropriate work control instructions and electronic dosimeter (ED) setpoints had been provided and to assess the communication of radiological control requirements to workers. For selected tasks, the inspectors attended pre-job briefings that reviewed RWP details with the workers. The inspectors reviewed selected ED dose and dose rate alarms, to verify workers properly responded to the alarms and that the licensee's review of the events was appropriate. Through observation of pre-job RWP briefings and health physics technician coverage of workers, the inspectors determined the licensee had established adequate means to notify workers of changing radiological conditions.
Contamination and Radioactive Material Control: The inspectors observed the release of potentially contaminated items from the radiologically controlled area (RCA) and from contaminated areas such as the drywell. The inspectors also reviewed the procedural requirements for, and equipment used to perform, the radiation surveys for release. During plant walk downs, the inspectors evaluated radioactive material storage areas and containers, including satellite RCAs, assessing material condition, posting/labeling, and control of materials/areas. In addition, the inspectors reviewed the sealed source inventory and verified labeling, storage conditions, and leak testing of selected sources.
The inspectors walked-down the ISFSI facility, observing the physical condition of the casks, radiological postings, and barriers. The inspectors performed independent gamma radiation surveys of the area and reviewed gamma radiation surveys of the ISFSI facility performed by licensee personnel. Inspectors compared the independent survey results to previous surveys and against procedural and Technical Specification (TS) limits. The inspectors evaluated implementation of radiological controls, including labeling and posting, and discussed controls with health physics staff. Environmental monitoring results for direct radiation from the ISFSI were reviewed and inspectors observed the placement and physical condition of thermoluminescent dosimeters around the facility.
Radiological Hazards Control and Work Coverage. The inspectors evaluated licensee performance in controlling worker access to radiologically significant areas and monitoring jobs in-progress associated with the U1 refueling outage. Established radiological controls were evaluated for selected tasks including main steam isolation valve work, safety-relief valve work, scaffolding, and control rod drive hydraulic control unit maintenance. The inspectors evaluated the effectiveness of radiation exposure controls, including air sampling, barrier integrity, engineering controls, and postings through a review of both internal and external exposure results.
During walk downs with a radiation survey meter, the inspectors independently verified ambient radiological conditions were consistent with licensee performed surveys, RWPs, and pre-job briefings; observed the adequacy of radiological controls; and observed controls for radioactive materials stored in the spent fuel pool. The inspectors also reviewed the procedural guidance for multi- and extremity badging. Select multi-badge packets were reviewed to verify consistency with procedural and regulatory guidance. For high radiation area tasks involving significant dose rate gradients, the inspectors evaluated the use and placement of whole body and extremity dosimetry to monitor worker exposure. The inspectors also reviewed and discussed selected whole-body count analyses conducted during 2009 and the current U1 refueling outage. The inspectors reviewed RWPs for use in airborne areas, ensuring the prescribed controls were appropriate for the conditions as identified in radiological surveys and air samples. ED alarm set points and worker stay times were evaluated against area radiation survey results for drywell and refueling floor activities.
Risk-Significant High Radiation Area and Very High Radiation Area Controls. The inspectors discussed the controls and procedures for locked-high radiation areas (LHRAs) and very high radiation areas (VHRAs) with health physics supervisors and the radiation protection manager. The inspectors observed the issuance of LHRA keys and evaluated the storage, inventory, and handling of LHRA/VHRA keys. During plant walk downs, the inspectors verified the posting/locking of LHRA/VHRA areas.
Radiation Worker Performance and Radiation Protection Technician Proficiency. The inspectors observed radiation worker performance through direct observation and in the remote monitoring center. Jobs observed included main steam isolation valve work, safety-relief valve work, scaffolding, and control rod drive hydraulic control unit maintenance. These jobs were performed in high radiation, airborne, and/or contaminated areas. The inspectors also observed health physics technicians providing field coverage of jobs and providing remote coverage from the central monitoring center.
Problem Identification & Resolution. Licensee Corrective Action Program (CAP) documents associated with access control to radiologically significant areas were reviewed and assessed. This included review of selected Condition Reports (CRs) related to radworker and health physics technician performance. The inspectors evaluated the licensee's ability to identify, characterize, prioritize, and resolve the identified issues in accordance with procedure NMP-GM-002, Corrective Action Program, Ver. 9.0. The inspectors also evaluated the scope of the licensee's internal audit program and reviewed recent assessment results. Licensee CAP documents reviewed are listed in Section
2RS1 of the report Attachment.
Radiation protection activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 12; TS Sections 5.4 and 5.7; 10 Code of Federal Regulations (CFR) Parts 19 and 20; and approved licensee procedures. Radiological control activities for ISFSI areas were evaluated against 10 CFR Part 20, 10 CFR Part 72, and TS details. Records reviewed are listed in Section
2RS1 of the Attachment.
The inspectors completed 1 sample, as described in Inspection Procedure (IP) 71124.01. The inspectors also completed the radiation protection line-item sample activities specified in IP 60855.1.
b. Findings
No findings of significance were identified.
2RS5 Radiation Monitoring Instrumentation
a. Inspection Scope
Radiation Monitoring Instrumentation. During tours of the Unit 1 (U1) and Unit 2 (U2) Reactor Buildings, Spent Fuel Pool Areas, U2 Turbine Building and Radwaste Building, the inspectors observed installed radiation detection equipment including the following instrument types: Area Radiation Monitors (ARMs), Continuous Air Monitors (CAMs), Personnel Contamination Monitors (PCMs), Portal Monitors (PMs), Small Article Monitors (SAMs). The inspectors observed the physical location of the components, noted the material condition, and compared sensitivity ranges with UFSAR requirements. Select ARMs with local readouts were compared with actual radiological conditions for consistency.
In addition to equipment walk-downs, the inspectors observed functional checks and alarm set point testing of various fixed and portable detection instruments, including portable ion chambers, AMP-100s, teletectors, PCMs, PMs and small article monitors (SAMs). Select calibration records for PCMs, PMs, SAMs, portable survey instruments, air samplers, ARMs and electronic personnel dosimeters were reviewed.
The inspectors reviewed calibration records, source check data and the material condition of instruments in the licensee's radiation protection instrument issue area, including portable ion chambers, underwater survey meters, neutron survey meters and portable GM detectors. The inspectors reviewed records of portable survey instruments that failed to meet the source acceptance criteria to verify the appropriateness of corrective actions. Daily performance checks and calibration data for HP laboratory equipment used for alpha and beta counting were reviewed.
The most recent 10 CFR Part 61 analyses and Whole Body Counter Calibration were reviewed to determine if calibration and check sources were representative of the plant isotopic mix. The inspectors reviewed records for the licensee's portable survey and ARM instrument calibrator and verified measuring devices were calibrated with NIST traceable sources. The last two calibration records for the U1 low range (1D11-K622) and the U1 High-range (1D11-K621) post accident monitors were reviewed.
The inspectors reviewed performance records and calibration results for selected process and effluent radiation monitors. The inspectors verified that the channel calibration and functional tests were performed consistent with radiological effluent technical specifications and National Institute of Standards and Technology (NIST)traceable standards. During the inspection, the inspectors observed the calibration of POST-LOCA monitors 1D11-K624, 1D11-K625, and 1D11-K626.
The inspectors reviewed selected laboratory analytical instruments used for radiological analysis in the chemistry lab areas. The inspectors observed the daily performance checks of those counting instruments used in the chemistry lab areas and discussed those results with cognizant licensee representatives.
Operability and reliability of selected radiation detection instruments were reviewed against 10 CFR Part 20; TS Section 5.4, Procedures; UFSAR Chapters 11 and 12; and applicable licensee procedures. Documents reviewed during the inspection are listed in Section
2RS5 of the Attachment.
Electronic Dosimetry. The inspectors reviewed the licensee's calibration methodology for Electronic Personal Dosimeters (EPDs) that included the radioactive sources, traceable standards, and tolerance levels used during EPD calibration.
Problem Identification and Resolution. Selected Condition Reports (CRs) associated with effluent release activities and radiation protection instrumentation were reviewed and assessed. The inspectors evaluated the licensee's ability to identify, characterize, prioritize, and resolve selected issues in accordance with procedure NMP-GM-002, Corrective Action Program, Rev 9.0. The inspectors also evaluated the scope of the licensee's internal audit program and reviewed recent assessment results. Reviewed documents are listed in Section
2RS5 of the Attachment.
The inspectors completed 1 of the 1 required samples detailed in IP 71124.05. All samples have now been completed for this IP.
b. Findings
The inspectors reviewed calibration records for EPDs at the licensee's facility. The licensee's EPDs were found to be capable of measuring Deep Dose Equivalent (DDE) and Shallow Dose Equivalent (SDE). The SDE feature was disabled and not used during routine radiological monitoring. EPDs were primarily used to estimate worker exposure for DDE, but were also used as a method of controlling worker exposure for entries in High Radiation Areas in accordance with TS 5.7.1b.
The inspectors identified three different methods used to calibrate EPDs. New EPDs purchased directly from the manufacturer were calibrated to a tolerance level of +/-10%
of a known Cs-137 source traceable to a United Kingdom National Standard. Subsequent calibrations were performed by the licensee's Environmental Laboratory to respond to a tolerance level of +/- 15% of a known Cs-137 source traceable to NIST. EPDs that required repair were sent to a calibration vendor located in West Columbia, South Carolina for repair and subsequently calibrated at that facility to a tolerance level of +/-10% using an Am-241 source traceable to NIST.
Licensee procedure 60AC-HPX-017-0, Radiation Protection Instrumentation Program, required radiation survey instruments used to assign or control worker exposure be initially and subsequently calibrated to read within +/-10% of the actual calibration source dose rates using radiation sources traceable to NIST. Additionally, 10 CFR 20.1501
- (b) requires licensees to ensure that instruments and equipment used for quantitative radiation measurements (e.g., dose rate and effluent monitors) are calibrated periodically for the radiation measured. Although the EPD is not generally used as a substitute for typical dose rate survey meters, it is used to initiate worker actions in lieu of a survey meter in accordance with TS 5.7.1.b which requires incorporation of the EPD into the routine instrument calibration program.
From a review of licensee records and discussions with cognizant licensee representatives, the inspectors determined that the licensee had not established a site specific standard for calibrating EPDs or compared the response of the EPDs using the different sources. The use of an Am-241 source, a low level gamma emitter was not representative of the energy ranges in the licensee's isotopic mix. In addition, the inspectors determined that the calibrations performed by the licensee's environmental laboratory were not consistent with the licensee's calibration methods for other instruments used to control worker exposure.
This item is unresolved pending NRC review of the licensee's evaluation of the EPDs response using NIST traceable sources representative of the energy spectrum of radiation fields at the licensee's facility and a review of the licensee's specific calibration method for EPDs. URI 05000321, 366/2010002-01, Review Licensee's EPD Calibration Methodology.
2RS6 Radioactive Gaseous and Liquid Effluent Treatment
Effluent Monitoring and Radwaste Equipment. During inspector walkdowns, accessible sections of the U1 and U2 liquid and gaseous radioactive waste (radwaste) and effluent systems were assessed for material condition and conformance with the UFSAR. The inspection included the Waste Sample Tanks, Floor Drain Sample Tanks, Chemical Waste Sample Tanks, Liquid Radwaste Discharge Monitors (1/2D11-N007), U1 Off-gas System Post-Treatment Monitor (1D11-K615A and B), U1 Recombiner Building Vent Monitor (1D11-R763A and B), Reactor Building Vent Monitors (D11-K619A and B / 2D11-K636A and B), Main Stack Monitor (D11-K600A and B), and associated airborne effluent sample lines. The inspectors interviewed chemistry and engineering staff regarding radwaste effluent monitor operation and equipment configuration requirements for representative sampling. The inspectors observed collection of particulate, iodine, and tritium samples from the main stack and recombiner release pathway, and assessed those activities for procedural adherence.
The inspectors reviewed out-of-service monitors from December 2008 to December 2009, and verified that required compensatory sampling was performed. The most recent surveillances on the Off-Gas High-Efficiency Particulate Air Filter Systems were reviewed. Performance and operations of the systems were reviewed and discussed with cognizant licensee personnel.
Current licensee programs for monitoring, tracking, and documenting the results of both routine and abnormal liquid releases to onsite and offsite surface environs were reviewed and discussed in detail. Current licensee capabilities and routine surveillances to minimize and rapidly identify abnormal leaks from liquid radioactive waste tanks, processing lines, and spent fuel pools were reviewed and discussed in detail.
Installed configuration, material condition, operability, and reliability of selected effluent sampling and monitoring equipment were reviewed against details documented in the following: 10 CFR Part 20; RG 1.21, Measuring, Evaluating and Reporting Radioactivity in Solid Wastes and Releases of Radioactive Materials In Liquid and Gaseous Effluents from Light-Water Cooled Nuclear Power Plants; TS, Section 5.0; the Offsite Dose Calculation Manual (ODCM), Rev. 17; and UFSAR. Procedures and records reviewed during the inspection are listed in Section
2RS6 of the Attachment.
Effluent Release Processing and Quality Control (QC) Activities. The inspector evaluated the methods used to determine the isotopes that are included in the source term to ensure all applicable radionuclides are included, within detectability standards. The inspector reviewed the Part 61 analyses to ensure hard-to-detect radionuclides are included in the source term.
The inspector reviewed the results of the inter-laboratory comparison program to verify the quality of radioactive effluent sample analyses. The inspector reviewed assessments of any identified bias in the sample analysis results and the overall effect on calculated projected doses to members of the public.
The inspector verified that the licensee was maintaining adequate effluent sampling records [sampling locations, sample analyses results, flow rates, and source term for radioactive liquid and gaseous effluent (i.e., information needed to satisfy the requirements of 10 CFR 20.1501)].
Selected portions of procedures for effluent sampling, processing, and release were evaluated for consistency with licensee actions. Selected gaseous release permits were reviewed against ODCM specifications for pre-release sampling and effluent monitor setpoints. The inspectors discussed performance of pre-release sampling and analysis, release permit generation, and radiation monitor setpoint adjustment with chemistry technicians and radwaste control room operators. The inspectors reviewed the 2007 and 2008 Annual Radiological Effluent Release Reports to evaluate reported doses to the public and ODCM changes. Public dose calculations were reviewed and discussed with cognizant licensee personnel.
Observed task evolutions, count room activities, and offsite dose results were evaluated against details and guidance documented in the following: 10 CFR Part 20 and Appendix I to 10 CFR Part 50; ODCM; RG 1.21; RG 1.109, Calculation of Annual Doses to Man from Routine Releases of Reactor Effluents for the Purpose of Evaluating Compliance with 10 CFR Part 50 Appendix I; RG 1.33, Quality Assurance Program Requirements; and TS Section 5.0. Procedures and records reviewed during the inspection are listed in Section
2RS6 of the Attachment.
Problem Identification and Resolution. Selected CRs and self-assessments associated with effluent release activities were reviewed. The inspectors evaluated the licensee's ability to identify, characterize, prioritize, and resolve selected issues in accordance with NMP-GM-002-GL02. Reviewed documents are listed in Section
2RS6 of the Attachment.
Groundwater Monitoring. The inspectors will evaluate the licensee's groundwater monitoring program during performance of Temporary Instruction (TI) 2515/173, "Review of the Implementation of the Industry Ground Water Protection Voluntary Initiative". This TI is scheduled to be completed prior to August 30, 2010.
The inspectors completed 1 of the required 1 sample for IP 71124.06. All samples have now been completed for this IP.
b. Findings
No findings of significance were identified.
2RS7 Radiological Environmental Monitoring Program (REMP)
a. Inspection Scope
REMP Implementation. The inspectors observed routine sample collection and surveillance activities as required by the licensee's environmental monitoring program. The inspectors noted the material condition and operability of airborne particulate filter and iodine cartridge sample stations and observed collection of weekly air samples, vegetation, and milk at selected monitoring locations. Environmental thermoluminescent dosimeters at selected sites were checked for material condition. In addition, an automatic water sampler on the Altamaha River was inspected for material condition upstream of the plant (control location). The inspectors determined the current location of selected sample points using NRC global positioning system instrumentation. Land use census results, changes to the ODCM, and sample collection/processing activities were discussed with environmental technicians and licensee staff.
The inspectors reviewed the last two calibration records for selected environmental air sample flowmeters and the 2009 maintenance log for automated water samplers. The inspectors also reviewed the 2008 Radiological Environmental Operating Report, the 2008 Annual Radioactive Effluent Report, an audit of the Georgia Power Environmental Laboratory, results of the 2008 interlaboratory cross-check program, and procedural guidance for environmental sample collection and processing. Selected environmental measurements were reviewed for consistency with licensee effluent data, evaluated for radionuclide concentration trends, and compared with detection level sensitivity requirements.
Procedural guidance, program implementation, and environmental monitoring results were reviewed against: 10 CFR Part 20; Appendix I to 10 CFR Part 50; TS Section 5.0; ODCM; RG 4.15, "Quality Assurance for Radiological Monitoring Programs (Normal Operation) - Effluent Streams and the Environment," and the Branch Technical Position, "An Acceptable Radiological Environmental Monitoring Program" - 1979. Documents reviewed are listed in Section
2RS7 of the Attachment.
Meteorological Monitoring Program. The inspectors observed a weekly surveillance on the primary meteorological tower and local data collection equipment. The inspectors observed the physical condition of the tower and its instrumentation and discussed equipment operability and maintenance history with licensee staff. The inspectors evaluated transmission of locally generated meteorological data to other licensee groups such as emergency operations personnel and main control room operators. For the meteorological measurements of wind speed, wind direction, and temperature, the
inspectors reviewed the last two calibration records for applicable tower instrumentation. The inspectors also evaluated measurement data recovery for 2008.
Licensee procedures and activities related to meteorological monitoring were evaluated against: ODCM; UFSAR Chapter 2; and proposed revision 1 to RG 1.23, Meterological Programs in Support of Nuclear Power Plants (1980). Documents reviewed are listed in Section
2RS7 of the Attachment.
Contaminated Leak Monitoring Program. The inspectors will evaluate the licensee's leak monitoring program during performance of Temporary Instruction (TI) 2515/173, "Review of the Implementation of the Industry Ground Water Protection Voluntary Initiative". This TI is scheduled to be completed prior to August 30, 2010.
Problem Identification and Resolution. The inspectors reviewed selected CRs in the areas of radiological environmental monitoring and meteorological tower maintenance. The inspectors evaluated the licensee's ability to identify and resolve the issues in accordance with procedure NMP-GM-002, "Corrective Action Program," Ver. 9.0. Documents reviewed are listed in Section
2RS7 in the Attachment.
The inspectors completed 1 of the required 1 sample for IP 71124.07. All samples have now been completed for this IP.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
a. Inspection Scope
The inspectors sampled licensee submittals for the Performance Indicators (PI) documented below. To verify the accuracy of the PI data reported during that period, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, were used to verify the basis in reporting for each data element. Occupational Radiation Safety Cornerstone. The inspectors reviewed PI data collected from January 1, 2009, through December 31, 2009, for the Occupational Exposure Control Effectiveness PI. For the reviewed period, the inspectors assessed CAP records to determine whether high radiation area, VHRA, or unplanned exposures, resulting in TS or 10 CFR 20 non-conformances, had occurred during the review period. In addition, the inspectors reviewed selected personnel contamination event data, internal dose assessment results, and ED alarms for cumulative doses and/or dose rates exceeding established set-points. The reviewed data were assessed against guidance contained in NEI 99-02. The reviewed documents relative to these PI reviews are listed in Sections 2RS01 and
4OA1 of the Attachment.
Public Radiation Safety Cornerstone. The inspectors reviewed the Radiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences PI results from February through December 2009. The inspectors reviewed CAP documents, effluent dose data, and licensee procedural guidance for classifying and reporting PI events. The inspectors also interviewed licensee personnel responsible for collecting and reporting the PI data. Reviewed documents are listed in Section
4OA1 of the Attachment.
The inspectors completed one of the required samples for IP 71151. One sample for the Public Radiation Safety Cornerstone PI.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
Daily Screening of Corrective Action Items
a. Inspection Scope
As required by Inspection Procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's corrective action program. This review was accomplished by either attending daily screening meetings that briefly discussed major CRs, or accessing the licensee's computerized corrective action database and reviewing each CR that was initiated.
b. Findings and Observations
No findings of significance were identified
4OA3 Event Follow-up
(Closed) LER 05000366/2009-003 Main Generator Runback Due to High Stator Cooling Water Temperature
a. Inspection Scope
On June 20, 2009, a Unit 2 automatic reactor scram was initiated on high reactor pressure when a main generator runback due to high stator water cooling outlet temperature occurred. The licensee identified that the cause of the main generator high stator cooling outlet temperature was due to improper set-up of the stator cooling water temperature control instrument loop. The inspectors reviewed this LER, the licensee's root cause report and associated corrective actions.
b. Findings
Introduction
- A Green self-revealing finding was identified for the licensee's failure to create, implement, and make available to maintenance personnel, quality processes or documents for configuration control. Specifically, the licensee failed to maintain the correct configuration of the stator water cooling (SWC) temperature control instrument loop air-operated valve, 2N43-F100, as required by licensee procedure NMP-ES-014, Air Operated Valve Program. The failure to implement adequate configuration control on the SWC temperature control instrument loop directly resulted in a Unit 2 reactor scram on June 20, 2009. (LER 05000366/2009-003)
Description
- On June 20, 2009, Unit 2 was in mode 1 at approximately 100% reactor power. Protective circuitry initiated a main generator runback due to high SWC outlet temperature. As a result, the electro-hydraulic control (EHC) processor began reducing turbine load by closing the turbine control valves and subsequently opening the turbine bypass valves. Operations personnel immediately began reducing reactor power in response to the main generator runback by reducing recirculation flow. The reactor power was reduced to approximately 66% reactor thermal power and could not be reduced any further without the insertion of control rods. As a result of turbine load reducing faster than the manual actions taken to reduce reactor power, reactor pressure began to increase. Pressure reached the setpoint to actuate the Reactor Protection System, and an automatic reactor scram was initiated due to high reactor pressure.
The cause of high SWC outlet temperature on the main generator was a result of improper set-up of the SWC temperature control instrument loop during the previous outage, (2R20). Air Operated Valve (AOV) 2N43-F100, which controls temperature by directing flow to the SWC heat exchangers, was on full bypass when it should have been providing flow through the heat exchanger given the system operating temperature at the time. Since Unit 1 SWC positioner is configured the same, Unit 1 was inspected to ensure that the positioner and controller were set up correctly.
During the 2R20 refueling outage on Unit 2, maintenance personnel performed preventive maintenance (PM) on the SWC temperature control instrument loop. This PM consisted of a calibration of 2N43-R310 (temperature controller), performed every 2 years and refurbishment of 2N43-F100 (actuator), performed every 12 years. AOV 2N43-F100 was a reverse design, spring return, three way valve. The proper configuration should have been "Direct" action for the temperature controller (2N43-R310) and "Reverse" action for the actuator (2N43-F100). Under a "Direct/Reverse" configuration set-up, the temperature controller (2N43-R310) would have sent maximum "open signal" to the actuator (2N43-F100). During the 2R20 PM's, the actuator (2N43-F100) was incorrectly set-up as "Direct" action. The "Direct/Direct" configuration would not allow the valve to function per design, essentially increasing the bypass flow around the heat exchanger.
Southern Nuclear Operating Company, NMP-ES-014, Air Operated Valve Program, Version 5.0, provides program requirements for all AOV's onsite. Per this program all AOV's are to be categorized as either 1, 2, or 3 based upon its contribution to safe plant operation or accident mitigation. Depending on the category this program will define the extent of design review and testing activities to be performed. Contrary to the requirements of NMP-ES-014 the licensee failed to create, implement, and make available to maintenance, quality processes or documents that would control and identify the correct configuration of the SWC temperature control instrument loop as required for CAT 3 AOV's such as 2N43-F100. The licensee has addressed this issue in their Corrective Action Program (CAP) and developed corrective actions in CR 2009106326. As part of the licensee's immediate corrective actions the Unit 2 SWC instrument loop was reconfigured to the correct alignment, and changes were made to procedure NMP-ES-014.
Analysis:
Failure to implement adequate configuration control of the SWC temperature control instrument loop as required per licensee procedure NMP-ES-014, was a performance deficiency. This performance deficiency was more than minor because it was associated with the Configuration Control attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of those events that upset plant stability. Specifically inadequate configuration control resulted in a Unit 2 reactor scram on June 20, 2009. The significance of this finding was screened using the Phase 1 of the Significance Determination Process (SDP) in accordance with NRC Inspection Manual Chapter 0609 Attachment 4. Because the finding contributed to a reactor scram, but did not affect mitigation equipment availability, the finding screened as Green.
The inspectors determined this performance deficiency was indicative of current licensee performance, in that this event occurred during the last refueling outage (2R20). Also, as indicated in the Root Cause Investigation for CR 2009106326, work packages that controlled the set-up of the SWC temperature control instrument loop have been inconsistent or incorrect since 2000. Therefore, this finding had a cross-cutting aspect in the Resources component of the Human Performance area, because the licensee failed to provide complete, accurate and up-to-date design documentation, procedures, work packages, and correct labeling of components. Specifically, the licensee failed to implement a means of configuration control of the SWC temperature control instrument loop (H.2(c)).
Enforcement
- Enforcement action did not apply because the performance deficiency did not involve a violation of regulatory requirements due to it being associated with the non-safety related Main Generator Stator Water Cooling system. Because this finding did not involve a violation of regulatory requirements and had very low safety significance, it was identified as FIN 05000366/2010002-02, "Failure to implement adequate configuration control on Unit 2 main generator stator water cooling temperature control instrument loop, 2N43-F100."
4OA5 Other Activities
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities
a. Inspection Scope
During the inspection period, the inspectors conducted the following observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours.
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities.
b. Findings
No findings of significance were identified.
.2 (Closed) Temporary Instruction (TI) 2515/180 Inspection of Procedures and Processes
for Managing Fatigue
a. Inspection Scope
The objective of this TI was to determine if licensees' implementation procedures and processes required by 10 CFR 26, Subpart I, "Managing Fatigue" are in place to reasonably ensure the requirements specified in Subpart I are being addressed. The TI applies to all operating nuclear power reactor licensees but is intended to be performed for one site per utility. The inspector interfaced with the appropriate staff to obtain and review station policies, procedures, and processes necessary to complete all portions of this TI.
b. Findings
No findings of significance were identified.
4OA6 Meetings, Including Exit
On April 16, 2010, the resident inspectors presented the inspection results to you and other members of your staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- S. Bargeron, Plant Manager
- G. Brinson, Operations Manager
- J. Dixon, Health Physics Manager
- G. Fechter, Site Welding/Repair & Replacement Coordinator
- B. Hulett, Engineering Design Manager
- G. Johnson, Engineering Director
- J. Lewis, Site Support Manager
- D. Madison, Hatch Vice President
- S. Soper, Engineering Support Manager
- J. Merritt, Nuclear Security Manager
- S. Tipps, Licensing
- R. Varnadore, Maintenance Manager
- D. Willyard, Programs Supervisor
NRC Eddie Morris, Senior Resident Inspector Phil Niebaum, Resident Inspector
LIST OF ITEMS
OPENED AND CLOSED
Opened
Closed
- 05000321,366/2515/180 TI Inspection of Procedures and Processes for Managing Fatigue (Section 4OA5.2)
- 05000366/2009-003 LER Main Generator Runback Due to High Stator Cooling Water Temperature (Section 4OA3)
Opened &
Closed
- 05000366/2010002-02 FIN Failure to implement adequate configuration control on Unit 2 main generator stator water cooling temperature control instrument loop, 2N43-F100 (Section 4OA3)
Discussed
None