IR 05000366/2022003

From kanterella
Jump to navigation Jump to search
Integrated Inspection Report 05000321 /2022003 and 05000366/2022003
ML22311A470
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 11/08/2022
From: Alan Blamey
NRC/RGN-II
To: Gayheart C
Southern Nuclear Operating Co
References
IR 2022003
Download: ML22311A470 (22)


Text

SUBJECT:

EDWIN I. HATCH - INTEGRATED INSPECTION REPORT 05000321/2022003 AND 05000366/2022003

Dear Cheryl A. Gayheart:

On September 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Edwin I. Hatch. On October 19, 2022, the NRC inspectors discussed the results of this inspection with Johnny Weissinger, Site Vice President, and other members of your staff.

The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

A licensee-identified violation which was determined to be of very low safety significance is documented in this report. We are treating this violation as an NCV consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Edwin I. Hatch.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC Resident Inspector at Edwin I. Hatch.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document November 8, 2022 Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Alan J. Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos. 05000321 and 05000366 License Nos. DPR-57 and NPF-5

Enclosure:

As stated,

Inspection Report

Docket Numbers:

05000321 and 05000366

License Numbers:

DPR-57 and NPF-5

Report Numbers:

05000321/2022003 and 05000366/2022003

Enterprise Identifier:

I-2022-003-0018

Licensee:

Southern Nuclear Operating Company, Inc.

Facility:

Edwin I. Hatch

Location:

Baxley, GA

Inspection Dates:

July 01, 2022 to September 30, 2022

Inspectors:

A. Alen, Senior Project Engineer

T. Fanelli, Senior Reactor Inspector

J. Hickman, Resident Inspector

M. Magyar, Reactor Inspector

T. Morrissey, Senior Resident Inspector

C. Safouri, Senior Project Engineer

R. Smith, Senior Resident Inspector

Approved By:

Alan J. Blamey, Chief

Reactor Projects Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Edwin I. Hatch, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified non-cited violation (NCV) is documented in report section: 71111.0

List of Findings and Violations

Failure to Periodically Test Molded Case Circuit Breakers Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000321,05000366/2022003-01 Open/Closed

[H.14] -

Conservative Bias 71152A An NRC-identified Green NCV, involving two examples of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, for the licensees failure to implement corrective actions to periodically test molded case circuit breakers (MCCBs) in order to promptly identify and correct performance degradation, including potential age-related degradation, of MCCBs.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period at 100 percent rated thermal power (RTP). On September 3, 2022, the operators reduced power to 65 percent RTP for a rod pattern adjustment and quarterly turbine valve testing. On September 5, 2022, the operators returned the unit to 100 percent RTP. The unit operated there for the remainder of the inspection period.

Unit 2 began the inspection period at 100 percent RTP. On August 20, 2022, the operators reduced power to 75 percent RTP for a rod pattern adjustment and returned the unit to 100 percent RTP the same day. On September 10, 2022, the operators reduced power to 65 percent RTP for a rod pattern adjustment and quarterly turbine valve testing. On September 11, 2022, the operators returned the unit to 100 percent RTP. On September 23, 2022, the operators reduced power to 87 percent RTP for a rod pattern adjustment and returned the unit to 100 percent RTP the same day. The unit operated there for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 C emergency diesel generator (EDG) system following testing, using 34SO-R43-001-2, on August 22-24, 2022.
(2) Unit 1 control rod drive (CRD) hydraulic system following repairs to the 1B CRD pump seal leak, using 34SO-C11-005-1, on August 25-26, 2022.
(3) Unit 2 B loop residual heat removal service water (RHRSW) system following the replacement of 2D RHRSW pump and motor, using 34SO-E11-010-2, on September 26, 2022.

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the Unit 2 core spray (CS) system from July 12 through 14, 2022.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Intake structure on 111-foot elevation on July 18, 2022.
(2) Unit 2 reactor building 158 and 164-foot elevations on July 20, 2022.
(3) Unit 1 condensate storage tank, fire pump house, and units 1 and 2 service water valve pits on August 4, 2022.
(4) Unit 1 reactor building 185-foot elevation on August 12, 2022.
(5) Control building 147-foot elevation, including units 1 and 2 cable spreading room and plant computer room on August 18, 2022.
(6) Unit 2 radiological waste building 132-foot elevation on September 16, 2022.

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Units 1 and 2 reactor buildings emergency core cooling corner rooms, units 1 and 2 west cable way, and a review of licensee actions to NRC-issued information notices addressing internal flooding at nuclear plants.

71111.07SIX - Heat Exchanger/Sink Performance Ultimate Heat Sink Containment Device and Dam (IP Section 03.05)

The inspectors evaluated the ultimate heat sink performance containment device and dam on the following:

(1) Service water intake structure and Altamaha River

71111.07T - Heat Exchanger/Sink Performance Heat Exchanger (Service Water Cooled) (IP Section 03.02)

The inspectors evaluated heat exchanger performance on the following:

(1) Unit 1 A high pressure coolant injection (HPCI) pump room cooler (1T41B005A)
(2) Unit 2 B residual heat removal (RHR) heat exchanger (2E11B001B)
(3) Unit 2 B reactor core isolation cooling (RCIC) system room cooler (2T41B004B)

Ultimate Heat Sink (IP Section 03.04) (1 Sample)

The inspectors evaluated the ultimate heat sink performance on the following:

(1) Service water intake structure and Altamaha River

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the main control room during a unit 2 rod pattern adjustment, on August 20, 2022.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operators respond to License Operator Requalification Program scenario H-LT-AF-CPE-00112, "Crew Performance Evaluation Design - Electrohydraulic Control, Reactor Feed Pump Turbine Oil Temperature Controller, Condenser Vacuum, Adjustable Speed Drive Cell, Scram Discharge Volume, and Anticipated Transient Without Scram," on July 11, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:

(1) Unit 2 hydrogen/oxygen analyzer system, P33-01, due to maintenance rule condition monitoring events being exceeded, on August 2, 2022.
(2) Review of Hatchs living (i.e., continuous) 10CFR50.65 a(3) documentation package with emphasis on unit 1 A plant service water pump, unit 2 primary containment isolation valves, and containment cooling system being monitored under 10CFR50.65 under a(1) status, on August 1, 2022.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Unit 1 elevated risk due to HPCI system maintenance, on July 14, 2022.
(2) Units 1 and 2 elevated risk due to performance of fire main system surveillance with existing system failures, on July 22, 2022.
(3) Unit 2 elevated risk due to the A CS system maintenance outage, on August 30, 2022.
(4) Unit 1 elevated risk due to emergency lighting relay fire in main control room, on September 14, 2022.
(5) Units 1 and 2 elevated risk due to Hurricane Ian, the week of September 26, 2022.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (8 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Condition report (CR) 10897512, loud knocking sound in bay 12 of unit 2 torus potentially caused by leak-by of the E safety relief valve.
(2) CR 10899243, unit 2 "Diesel Gen B Loading Timer Failure," resulting in potential inoperability of the 1B (swing) EDG for a loss of coolant accident (LOCA) or loss of offsite power (LOSP) or LOCA/LOSP.
(3) CR 10895096, unit 1 torus to drywell vacuum breaker, 1T48-F323F, would not close during testing.
(4) CR 10895145, unit 1 RHRSW pump seal water piping detaching; and CRs 10898218 and10898626 for units 1 and 2 RHRSW piping degradation.
(5) CR 10899388, unit 2 RHRSW pump flow dropped from 4300 gallons per minute (gpm) to 2700 gpm during torus cooling operations.
(6) CR 10905959, unit 1 B EDG relays exceeded 10-year replacement criteria.
(7) CR 10905054, unit 1 reactor pressure low analog transmitter trip system (ATTS)instrument failed to the lower end of the scale.
(8) CR 10910753, unit 2 RHR minimum flow valve, 2E11-F007B, did not operate properly.

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Temporary modification to install a temporary supplemental cooling on the unit 2 CRD piping supplying the seal purge flow to the shaft seal cavity of the 2B reactor recirculation pump.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:

(1)57SV-SUV-012-1, ATTS Panel 1H11-P926 Channel FT&C, following the replacement of the HPCI exhaust diaphragm high pressure ATTS card, on July 28, 2022.

(2)34SO-R42-001-2, "125 Volts Direct Current (VDC) and 125/250 VDC System,"

following cleaning, calibration, and fan replacement of the unit 2 division II station service battery charger F, on July 29, 2022.

(3)57SV-R43-001-2, "Testing the LOCA/LOSP Timer Card," following replacement of the

==2R43 N782B card, on August 11, 2022.

(4)==

42SP-07-20-22-RS-1-1, "Diesel Fire Pump Engine Replacement Functional Test,"

following the replacement of the 1X43-C002B engine, the weeks of August 15, 22, and 29, 2022.

(5)34SO-E21-001-2, "Core Spray System", section 4.3.1, B loop CS manual startup, following unit 2 A CS system maintenance outage, on August 31, 2022.

(6)57SV-R43-001-2, "Testing The LOCA/LOSP Timer Cards," following the K7 relay replacement on the unit 2 B EDG loading timer, on September 2, 2022.

(7) Work Order SNC1340018, computer processing unit replacement in the unit 2 B recirculation adjustable speed drive, on September 10, 2022.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (2 Samples)

(1)34SV-P41-001-1, "Plant Service Water Pump Operability," Version 15.3 (section 7.2, "PSW 'A' Loop"), on July 12, 2022.

(2)34SV-E11-004-2, "RHR Service Water Pump Operability", Version 19.2, on September 7, 2022.

Inservice Testing (IP Section 03.01) (1 Sample)

(1)34SV-E51-002-1, "RCIC Pump Operability," Version 29.2 (sections 4.2, "Operability Test" and 4.3, "RCIC IST Test"), on July 6, 2022

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

(1) Emergency preparedness off-year exercise involving a LOCA, on July 26,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS06: Emergency AC Power Systems (IP Section 02.05)===

(1) Unit 1 (July 1, 2021-June 30, 2022)
(2) Unit 2 (July 1, 2021-June 30, 2022)

MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)

(1) Unit 1 (July 1, 2021-June 30, 2022)
(2) Unit 2 (July 1, 2021-June 30, 2022)

MS08: Heat Removal Systems (IP Section 02.07) (2 Samples)

(1) Unit 1 (July 1, 2021-June 30, 2022)
(2) Unit 2 (July 1, 2021-June 30, 2022)

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Testing and replacement schedule for safety related molded case circuit breakers were not being followed in accordance with Institute of Electrical and Electronics Engineers (IEEE) 308-1971 standards (CR 10625944).

INSPECTION RESULTS

Licensee-Identified Non-Cited Violation 71111.05 This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program (CAP) and is being treated as a non-cited violation (NCV), consistent with Section 2.3.2 of the Enforcement Policy.

Violation: The licensee identified an NCV of Technical Specification 5.4.1.a which required applicable procedures per Regulatory Guide 1.33 Appendix A section 1.l, shall be established, implemented, and maintained covering Fire Protection Program activities. Contrary to this, prior to identifying the issue on August 19, 2022, the licensee failed to establish and maintain fire protection program procedure 42SV-FPX-021-0, Surveillance Of Swinging Fire Doors, Revision 1.20, for inspecting fire doors. Specifically, the licensees procedure did not ensure the flush bolts for the inactive leaf of a double fire door were properly engaged. As a result, the unit 2 A emergency diesel generator (EDG) room door, 1L48-D135, was identified as non-functional on August 17, 2022. The licensee initiated hourly roving fire watches for this fire door and placed the door in their corrective maintenance process to restore the affected fire door. The issue was placed in the CAP on August 19, 2022.

Significance/Severity: Green. The inspectors assessed the significance of the finding using guidance in IMC 0609, Appendix F, Fire Protection Significance Determination Process, and determined the finding to be of very low safety significance because there was an adequate automatic suppression system inside the EDG room.

Corrective Action References: Condition reports (CRs) 10901837, 10902255 Failure to Periodically Test Molded Case Circuit Breakers Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000321,05000366/2022003-01 Open/Closed

[H.14] -

Conservative Bias 71152A An NRC-identified Green non-cited violation (NCV), involving two examples of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, for the licensees failure to implement corrective actions to periodically test molded case circuit breakers (MCCBs) in order to promptly identify and correct performance degradation, including potential age-related degradation, of MCCBs.

Description:

The updated final safety analysis report (UFSAR) for Hatchs unit 1 (Section 8.3.7) and unit 2 (Section 8.3.1.2.1.C Part 3) states that periodic equipment tests (applicable to MCCBs) are performed at scheduled intervals to detect deterioration of the system toward an unacceptable condition and to demonstrate that standby power equipment and other components that are not exercised during normal operation of the station are operable.

Additionally, the licensee committed to (in the UFSAR for unit 2) testing and surveillances of MCCBs in accordance with the Institute of Electrical and Electronics Engineers (IEEE)standards 308-1971, IEEE Standard Criteria for Class 1E Power Systems for Nuclear Power Generating Stations. Sections 5.2.2 and 5.3.2 for alternating current and direct current distribution systems, respectively, specify in part, that the distribution systems shall be monitored to the extent that it is shown to be ready to perform its intended function. Also, Section 5.4, Vital Instrumentation and Control Power Systems, specifies in part, that dependable power supplies are required for the vital instrumentation and control systems of the unit(s), and Section 6, Surveillance Requirements, specifies in part, that tests shall demonstrate that the equipment operates within design limits and that the system is operational and can meet its performance specifications. Testing can reveal whether degradation has occurred or is occurring that could potentially impact the operability of the load served by the MCCB. Additionally, testing can also identify age-related degradation of the MCCB, such as the potential for hardening of the lubricant used internally to the MCCB as identified by industry operating experience.

Example 1:

In March 2012, during an engineering assessment, the licensee identified that it did not have a test program for the majority (approximately 750 breakers) of its safety-related MCCBs in accordance with the UFSAR and IEEE standards identified above. Many breakers were beyond their 20-year life expectancy, installed in the early 1970s during initial construction, and had not been tested since installation. The licensee identified this issue as a condition adverse to quality (i.e., nonconformance condition) and captured it in the corrective action program (CAP) under condition report (CR) 431380. The licensee initiated a corrective action technical evaluation (TE) 351918 where it documented corrective action plans to replace obsolete breakers and then replace breakers periodically instead of testing. This TE was subsequently closed in May 2012 to a new TE (TE413574) to track and initiate activities to replace the affected breakers. In April 2015, during a second engineering self-assessment, the licensee initiated CR10059075 after identifying that the corrective actions from 2012 (CR431380 and TE413574) were not implemented. The licensee initiated a series of new TEs to establish a testing program, establish PMs to perform the testing, and replace obsolete breakers and distribution panels. TE 930308 tracked actions to ensure all safety related MCCBs located in motor control centers (MCC) were tested within 6 years (complete by 2021), TEs 939734 and 939740 tracked the development of maintenance instructions to test MCCBs in both MCCs and distribution panels, and TE 930309 tracked the replacement of distribution panels planned to begin in 2017. In July 2019, during a third engineering self-assessment, the licensee identified that the corrective actions from 2015 had not been implemented, specifically, no preventive maintenance testing or work orders (WOs) had been created and no replacement distribution panels had been designed or procured. The licensee again entered the failure to take corrective actions in their CAP under CR 10625944. The inspectors determined that between 2012 and 2019 the licensee failed to develop and implement a test program (i.e., corrective actions) for MCCBs. These were corrective actions the licensee acknowledged and documented were needed after identifying the periodic testing nonconformance in 2012 and again in 2015.

Example 2:

The inspectors reviewed the licensees progress towards restoring compliance with the MCCB test requirements since it last identified it in 2019. The inspectors noted that as of September 2022 the licensee had only tested 33 (of approximately 750) in-service MCCBs.

When the licensee began testing in 2019 it deferred testing of in-service MCCBs due to a high number of spare MCCB failures (WOs SNC898390, SNC900113, SNC915932). These failures meant that replacements were not available for in-service MCCB test failures.

Although the licensee determined that the cause of the spare failures may not affect the in-service failure rate, which was not as high as the spares (December 2021 - CR 10845767),the licensee stopped testing in-service MCCBs despite having adverse trend data suggesting MCCBs were in an age degraded state due to being in operation far beyond their design life.

The licensee resumed testing in 2022 after determining the cause of the high failure rate of the spare MCCBs. However, the inspectors noted that in subsequent testing, documented in WOs: SNC900103, SNC900100, and SNC900095, the licensee continued to defer testing of in-service MCCBs. Specifically, 9 out of 35 MCCBs scheduled to be tested in the referenced WOs were not tested due to not having a replacement available.

The licensees Quality Assurance Program is described in topical report SNC-1, Quality Assurance Topical Report (QATR). The QATR describes the quality assurance program and administrative control requirements established to meet 10 CFR 50 Appendix B, Quality Assurance Criteria for Nuclear Power Plants and Fuel Reprocessing Plants. In establishing provisions for corrective action, and compliance with Criterion XVI of 10 CFR Appendix B, SNC commits to comply with Basic Requirement 16, Corrective Action, of ASME NQA-1-1994, Quality Assurance Requirements for Nuclear Facility Applications. Basic Requirement 16 requires, in part, that conditions adverse to quality shall be identified promptly and corrected as soon as practical. The inspectors determined that deferring MCCB testing due to parts availability (particularly considering the long-standing nature and awareness of this issue) was inadequate and inconsistent with correcting a CAQ (lack of testing) as soon as practical.

Corrective Actions: The licensee entered the issue into their CAP as CR 10915674 to ensure testing is conducted regardless of breaker replacement availability. Also, CR10915161 was initiated to create WOs to test MCCBs for which testing has been deferred. Lastly, TE 1112637 will develop and support a test plan to ensure MCCBs are tested at the next available opportunity.

Corrective Action References: CRs 10915674, 10915161, 10916115, and TE 1112637

Performance Assessment:

Performance Deficiency: The failure to implement corrective actions to test MCCBs in accordance with IEEE 308 standards in order to promptly identify and correct degradation, including aging degradation, of MCCBs was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The failure to establish a test program and use it to detect and correct degradation in safety related MCCBs adversely affects the reliability and availability of mitigating systems and could cause undesirable consequences.

Significance: Although the MCCBs associated with this performance deficiency affected systems and components in both the Mitigating Systems and the Containment Barrier Cornerstones, the number of mitigating systems affected was significantly higher than the systems associated with the Containment Barrier; therefore, the Mitigating Systems Cornerstone was used to evaluate the significance of the finding. In accordance with NRC Inspection Manual Chapter (IMC) 0609, Attachment 4, Initial Characterization of Findings, the inspectors assessed the significance of the finding using the mitigating systems screening questions from Exhibit 2 of IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power. The finding screened as very low safety significance (Green) because the finding was a qualification deficiency that did not result in loss of operability or functionality. Specifically, the licensee determined it had reasonable assurance of operability (CR10852218) regarding untested MCCBs based on results of MCCB tested to-date, operating experience, and the determination that the cause for the high failure rate of spare breakers did not impact in-service breakers.

Cross-Cutting Aspect: H.14 - Conservative Bias: Individuals use decision making-practices that emphasize prudent choices over those that are simply allowable. A proposed action is determined to be safe in order to proceed, rather than unsafe in order to stop. The licensees decision making did not act prudently to ensure MCCBs were tested to be safe to use in order to proceed, rather they allowed the use of untested MCCBs, which were beyond their design life, simply because spares were unavailable and work instructions allowed it.

Enforcement:

Violation: 10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, requires in part, that measures shall be established to assure that conditions adverse to quality, such as a nonconformances, are promptly identified and corrected.

In SNC-1, Quality Assurance Topical Report (QATR), Version 25.0, the licensee committed to implement Basic Requirement 16, Corrective Action, of the American Society of Mechanical Engineers (ASME) NQA-1-1994, Quality Assurance Requirements for Nuclear Facility Applications, to comply with 10 CFR 50, Appendix B, Criterion XVI. Basic Requirement 16, Corrective Action, of ASME NQA-1-1994 requires in part, that conditions adverse to quality shall be identified promptly and corrected as soon as practical.

Contrary to the above, since March 2012, the licensee identified a condition adverse to quality associated with the lack of MCCB testing, a nonconforming condition, but failed to implement measures to assure the condition was promptly identified and corrected.

Specifically, as identified in 2015 and 2019, the licensee repeatedly failed to establish a test program for MCCBs. Furthermore, since the licensee began testing in 2019, the deferral to test MCCBs, which were beyond their service life, due to parts availability was inadequate and inconsistent with correcting the nonconformance as soon as practical. Approximately 10 years after the licensee identified (March 2012) the nonconforming condition only a small population of MCCBs have been tested.

Enforcement Action: This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On July 27, 2022, the inspectors presented the heat sink performance inspection results to Johnny Weissingner, Site Vice President (SVP) and other members of the licensee staff.

On October 19, 2022, the inspectors presented the integrated inspection results to Johnny Weissinger, SVP, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Corrective Action

Documents

Condition Reports (CR)

10628284, 10632635, 10635610, 10644674,

10661058, 10694204, 10695300, 10705032,

10706311, 10706501, 10709640, 10713284,

10713434, 10713709, 10714302, 10729116,

10733813, 10734322, 10739735, 10755977,

10756457, 10767210, 10771203, 10772070,

10773140, 10773366, 10774313, 10774993,

10776756, 10776800, 10776816, 10777640,

10778063, 10778614, 10778614, 10778635,

10778819, 10778940, 10778979, 10779210,

10780003, 10782516, 10782790, 10785605,

10786941, 10786942, 10789793, 10801026,

10803252, 10807247, 10808377, 10826311,

10829392, 10831704, 10839522, 10846527,

10847035, 10861205, 10871869, 10877955,

10885863, 10887149, 10889038, 10889039

71111.04

Corrective Action

Documents

Condition Reports (CR)

10823143, 10835132, 10835365, 10838266,

10840019, 10847448, 10847489, 10847705,

10848122, 10855525, 10866214, 10868463,

10868678, 10868924, 10869381, 10869482,

10869566, 10869866, 10870090, 10870117,

10870147, 10870156, 10870165, 10876258,

10876581, 10879799, 10884793, 10892133,

10896398

71111.04

Drawings

H-24739

Unit 2 Core Spray System Logic Diagrams Sheet 1 of

6.0

71111.04

Drawings

H-24740

Unit 2 Core Spray System Logic Diagrams Sheet 2 of

71111.04

Drawings

H-26018

Unit 2 Core Spray System P&ID

40.0

71111.04

Drawings

H-26046

Reactor & Radwaste Buildings - Condensate Storage

& Transfer System Diagram

50.0

71111.04

Drawings

H16065

Control Rod Drive Hydraulic System P&ID Sheet 2

50.0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Procedures

34SO-C11-005-1

Control Rod Drive Hydraulic System

34.0

71111.04

Procedures

34SO-E11-010-2

Residual Heat Removal System

45.0

71111.04

Procedures

34SO-E21-001-2

Core Spray System

26.6

71111.04

Procedures

34SO-R43-001-2

Diesel Generator Standby AC System

30.8

71111.04

Procedures

NMP-ES-012-001

Inspection of Heat Exchangers (2R43-B002C - 2C

EDG Lube Oil Heat Exchanger)

2.1

71111.04

Work Orders

Work Orders (SNC)

1145215, 1145516, 1078706

71111.05

Corrective Action

Documents

Resulting from

Inspection

Condition Report (CR)

10895572

71111.05

Fire Plans

NMP-ES-035-019-GL02-

F03

Control Building 147-foot Elevation

1.0

71111.05

Fire Plans

NMP-ES-035-019-GL02-

F15

Unit 1 Reactor Building 185' Elevation

1.0

71111.05

Fire Plans

NMP-ES-035-019-GL02-

F31

U2 Reactor Building El. 158/164

1.0

71111.05

Fire Plans

NMP-ES-035-019-GL02-

F35

Unit 2 Rad Waste Building 132' elevation

1.0

71111.05

Fire Plans

NMP-ES-035-019-Gl02-

F52

U1 Condensate Storage Tank

1.0

71111.05

Fire Plans

NMP-ES-035-019-GL02-

F70

Fire Pump House

1.0

71111.05

Fire Plans

NMP-ES-035-019-GL02-

F84

Service Water Valve Pits

1.0

71111.05

Procedures

NMP-ES-035-017

Fleet Fire Doors Functional Inspection Governance

and Acceptance Criteria

1.1

71111.06

Calculations

SMNH 99-014 (REV 1)

Water Hammer Evaluation for Fire Protection Piping

06/25/2012

71111.06

Corrective Action

Documents

Resulting from

Inspection

Condition Reports (CR)

10904792, 10904824

71111.06

Drawings

H-16039

Leak Detection System-Instrument & Drainage Sump

P&ID

8.0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.06

Drawings

H-16110

Types of Penetration Seals For Non Fire Rated Wall

Pipe & Duct

2.0

71111.06

Drawings

H-16176

Radwaste System P&ID

2.0

71111.06

Engineering

Evaluations

LR-REG-001-1098

SER 3-98 Recurring Events Flooding of ECCS

Rooms Caused by Fire Protection System Water

Hammer

10/05/1998

71111.06

Engineering

Evaluations

REA HT98703

Hatch Nuclear Plant - Units 1 & 2-Water Hammer

Analysis for Fire Protection

2/17/2000

71111.06

Engineering

Evaluations

Technical Evaluations (TE)

390614, 78139

71111.06

Miscellaneous

Response to NRC IN 2007-001

Recent Operating Experience Concerning Hydrostatic

Barriers

04/18/2007

71111.06

Miscellaneous

Response to NRC IN-

2003-008

Potential Flooding through Unsealed Concrete Floor

Cracks

09/16/2003

71111.06

Miscellaneous

Response to NRC IN-

2005-011 and IN-2005-30

Internal Flooding/Spraying-Down of Safety-Related

Equipment Due to Unsealed Equipment Hatch Floor

Plugs and/or Blocked Floor Drains

Safe Shutdown Potentially Challenged by Unanalyzed

Internal Flooding Events and Inadequate Design

06/29/2005

71111.06

Procedures

34AB-T22-003-1/2

Secondary Containment Control

5.18/4.5

71111.06

Procedures

34AB-T23-004-1/2

Torus Water Level

1.2/1.4

71111.06

Procedures

34AR-657-901-1/2

ARP's For Control Panel 1H11-P657 (2H11-P657)

25.18/23.10

71111.11Q

Miscellaneous

Emergency Preparedness Observation Form

07/11/2022

71111.11Q

Miscellaneous

H-LT-AF-CPE-00112

CPE Design - EHC, RFPT Oil Temperature

Controller, Condenser Vacuum, ASD Cell, SDV,

ATWS

1.0

71111.11Q

Procedures

NMP-RE-008-F02

Simplified Reactivity Management Plan (Hatch - Unit

Cycle 27, H2C27-082022-040

2.1

71111.12

Corrective Action

Documents

Condition Reports (CR)

10895237, 10889783, 10627699, 10636561,

10644291, 10648471, 10649056, 10644291,

10649128, 10653060, 10661059, 10665465,

10671968, 10683877, 10698757, 10700915,

10702813, 10702936, 10707324, 10709100,

10709104, 10709119, 10716168, 10717046,

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

10723279, 10723451, 10726191, 10727321,

10729088, 10730446, 10730448, 10730527,

10733168, 10733904, 10734223, 10735427,

10737276, 10741057, 10742768, 10743777,

10743835, 10750160, 10753242, 10764198,

10767536, 10771598, 10774779, 10776884,

10779262, 10779523, 10780594, 10781036,

10781693, 10782597, 10782937, 10783554,

10786049, 10786052, 10790129, 10791368,

10791498, 10793147, 10794840, 10800016,

10803039, 10803106, 10803107, 10807477,

10814592, 10814961, 10814961, 10815628

71111.12

Engineering

Evaluations

Technical Evaluations (TE)

1107681, 1075210

71111.12

Miscellaneous

H-1(2) - P33 - Sampling

Primary Containment Hydrogen and Oxygen

Analyzers

71111.12

Miscellaneous

P33-01 Sampling

Hydrogen and Oxygen Analyzers (Maintenance Rule

Function Scoping Sheet)

71111.13

Calibration

Records

Condition Report (CR)

10910325

71111.13

Corrective Action

Documents

Resulting from

Inspection

Condition Reports (CR)

10910484,10910972, 10910974

71111.13

Miscellaneous

Hatch Unit 2 R8 On-Line Configuration Risk Monitor

Current

Risk Summary Report

08/30/2022

71111.13

Miscellaneous

Hatch U1 R8 On-Line Configuration Risk Monitor -

Current Risk Summary Report

07/14/2022

71111.13

Procedures

NMP-GM-031-001

Online Maintenance Rule (a)(4) Risk Calculations

8.0

71111.13

Procedures

NMP-OS-010-002

Hatch Protective Equipment Logs

2.2

71111.13

Procedures

NMP-OS-010-002

Hatch Protected Equipment Logs

11.1

71111.13

Procedures

NMP-OS-017

Severe Weather

3.0

71111.13

Procedures

NMP-OS-017

Severe Weather (Attachments 1 through 9 for Site

09/27/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Preps for Hurricane Ian)

71111.15

Corrective Action

Documents

Condition Report (CR)

10895096

71111.15

Corrective Action

Documents

Condition Reports (CR)

10899243, 10627205

71111.15

Corrective Action

Documents

Condition Reports (CR)

10895145, 10898218, 10898626, 10901485

71111.15

Drawings

H-26833

RHR Service Water at River Intake Structure -

Isometric

4.0

71111.15

Drawings

S-00768, 00769, 00770

RHR Service Water system E-11-HGR-1, E-11-HGR-

2, E-11-HGR-3

2.0/1.0/3.0

71111.15

Engineering

Evaluations

DOEJ-HRSNC1358910-

S001

Minimum Pipe Wall Thickness for 18 Inch RHRSW

Piping Structures at the Intake

08/08/2022

71111.15

Engineering

Evaluations

NMP-AD-012-F01

Operability Determination Support Bases (CRs

10898218, 10898626, 10895145)

08/18/2022

71111.15

Engineering

Evaluations

Prompt Determination of

Operability (CR 10730343)

Unit 2 RHRSW Division 2 Pumps

08/17/2020

71111.15

Miscellaneous

1-LCO-22-00152

1T48-F323F Vacuum Breaker Failure to Close

71111.15

Procedures

34AB-P41-001-2

Loss of Plant Service Water

13.13

71111.15

Procedures

34AR-652-207-2

Diesel Gen B Loading Timer Failure Alarm

3.3

71111.15

Procedures

34SO-T48-002-1

Containment Atmosphere Control and Dilution

System

26.4

71111.15

Work Orders

Work Orders (WO)

1358911, 1358154

71111.18

Engineering

Changes

SNC1334334

Design Equivalent Change Package for the 2B

Recirculation Pump Seal Purge Supplemental

Cooling

06/06/2022

71111.18

Miscellaneous

NMP-OS-028

Adverse Condition Monitoring and Contingency Plan

for the 2B Recirculation Seal Monitoring

07/06/2022

71111.19

Corrective Action

Documents

Condition Report (CR)

10897221

71111.19

Corrective Action

Documents

Condition Report (CR)

10897312

71111.19

Drawings

DECP SNC1225505J001

Fire Protection P&ID

1.0

71111.19

Drawings

DECP

Program Fire Protection House Equipment

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

SNC125505E100_FCR004

71111.19

Drawings

H-58109

Fire Pump Diesel Engine Mounting Details (1X43-

C002A and 1X43-C002B)

1.0

71111.19

Miscellaneous

S-78101

Installation and Maintenance Manual for Diesel

Engine Fire Pump Controllers Model GPD

2.0

71111.19

Procedures

34SO-R42-001-2

25 VDC and 125/250 VDC System

20.3

71111.19

Procedures

2SP-07-20-22-RS-1-1

Diesel Fire Pump Engine Replacement Functional

Test

1.0

71111.19

Work Orders

Work Order (SNC)

1359845

08/11/2022

71111.19

Work Orders

Work Order (SNC)

1356086

07/28/2022

71111.19

Work Orders

Work Orders (SNC)

1012444, 1012446, 1356128, 1295880, 1296244,

1342764, 1368174, 1366668, 1321585, 1323434,

23466, 1297079, 1302202, 1297079, 1302202,

1303107, 1304289, 1305582, 1325361, 1325378,

25378, 1325787, 1326726, 1328511, 1329001,

1337341, 1345820, 1352434

07/29/2022

71111.22

Corrective Action

Documents

Condition Reports

10892714, 10892718

71111.22

Drawings

H-16334

RCIC System P&ID (Sheet No. 1)

51.0

71111.22

Drawings

H-16335

RCIC System P&ID (Sheet No. 2)

36.0

71111.22

Miscellaneous

34SV-E51-002-1S

1E51-C001 Existing Reference Data Page

3.0

71111.22

Procedures

34SV-E51-002-1

RCIC Pump Operability, completed on

7/6/2022

71111.22

Procedures

34SV-P41-001-1

Plant Service Water Pump Operability

15.3

71114.06

Corrective Action

Documents

Condition Reports (CR)

10897008, 10897010, 10897011

71114.06

Miscellaneous

Classification Evaluation for Hatch Off Year Exercise

22

71114.06

Miscellaneous

Hatch Off Year Exercise 2022

07/26/2022

71114.06

Miscellaneous

Emergency Preparedness Observation Form

07/26/2022

71114.06

Procedures

NMP-EP-142-F10

Alert/Site Area/General Area Emergency Public

Address Announcement Scripts (July 26, 2022)

2.0

71114.06

Procedures

NMP-EP-303-F05

Drill and Exercise Objectives (Section E.1 - Off-Site

Notification)

7.0

71152A

Corrective Action

Corrective Action Report

2959

03/20/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

Determination