IR 05000321/2021002

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Integrated Inspection Report 05000321/2021002 and 05000366/2021002
ML21216A201
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 08/04/2021
From: Alan Blamey
NRC/RGN-II
To: Gayheart C
Southern Nuclear Operating Co
T Francis
References
IR 2021002
Download: ML21216A201 (17)


Text

August 04, 2021

SUBJECT:

EDWIN I. HATCH NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000321/2021002 AND 05000366/2021002

Dear Ms. Gayheart:

On June 30, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Edwin I. Hatch Nuclear Plant. On July 23, 2021, the NRC inspectors discussed the results of this inspection with Sonny Dean and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Alan J. Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects

Docket Nos. 05000321 and 05000366 License Nos. DPR-57 and NPF-5

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000321 and 05000366

License Numbers:

DPR-57 and NPF-5

Report Numbers:

05000321/2021002 and 05000366/2021002

Enterprise Identifier: I-2021-002-0015

Licensee:

Southern Nuclear Operating Company, Inc.

Facility:

Edwin I. Hatch Nuclear Plant

Location:

Baxley, GA

Inspection Dates:

April 01, 2021 to June 30, 2021

Inspectors:

C. Curran, Project Engineer

J. Hickman, Senior Resident Inspector

N. Peterka, Fuel Facility Inspector

R. Smith, Senior Resident Inspector

Approved By:

Alan J. Blamey, Chief

Reactor Projects Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Edwin I. Hatch Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period at 100 percent rated thermal power (RTP). On June 11, 2021, the unit was shut down to investigate a step change increase in drywell unidentified leakage. The licensee determined the cause of the increase leakage to be a packing and pressure seal leak on the inboard high pressure coolant injection (HPCI) steam supply valve (1E41-F002). After repairs to the valve, the unit was restarted on June 16, 2021, and reached 100 percent RTP on June 20, 2021. On June 21, 2021, the unit was down powered to 85 percent RTP to perform the final rod pattern adjustment after startup and was returned to 100 percent RTP on the same day. On June 30, 2021, the unit commenced a shutdown to repair turbine temperature switches that were causing half group I signals on the A2 channel.

Unit 2 began the inspection period at 100 percent RTP. On April 8, 2021, the unit reduced power to 20 percent RTP to repair a main generator hydrogen cooler valve. After repairs were completed, the unit was returned to 100 RTP on April 13, 2021. On June 5, 2021, the unit was down powered to 70 percent RTP to perform turbine control valve testing and was returned to 100 percent RTP the same day. On June 26, 2021, the unit was down powered to 91 percent RTP due to fourth stage high pressure feedwater heater isolating. After repairs to the fourth stage high pressure feedwater heater level switch, the unit was returned to 100 percent RTP on June 27, 2021. On June 29, 2021, the unit was down powered to 96 percent RTP to perform the final rod pattern adjustment after the down power and was returned to 100 percent RTP on the same day. The unit operated there for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident and regional inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week, increasing the amount of time on site as local COVID-19 conditions permitted.

As part of their onsite activities, resident inspectors conducted plant status activities as described in IMC 2515, Appendix D; observed risk significant activities; and completed on site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on site. The inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of Summer Readiness for the following systems:

1. Offsite and alternate alternating current (AC) power systems on May 24, 2021.

2. Residual heat removal service water on May 26, 2021.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Alignment of the Unit 1 HPCI system while the reactor core isolation cooling (RCIC)system was inoperative for maintenance, using 34SO-E41-001-1, Version 30.4 on May 4, 2021.
(2) Alignment of the Unit 2 residual heat removal (RHR) system 'A' and 'C' pumps, using 34SO-E11-010-2, Version 44.5 on May 5, 2021.
(3) Alignment of the Unit 1 RHR system 'B' pump following emergent repair work on the pump piping, using 34SO-E41-010-1, Version 45.3, on May 12, 2021.
(4) Alignment of the main control ventilation system following maintenance on the 'C' train, using 34SO-Z41-001-1, Version 24.0, on May 19, 2021.

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the Unit 1 plant service water (PSW) system on June 22, 2021.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Unit 2 RCIC pump and turbine room, on April 21, 2021
(2) Unit 2 NE RHR and core spray pump room, on April 21, 2021
(3) Unit 1 working floor and adjustable speed drive (ASD) area, on April 27, 2021
(4) Unit 1/2 control room, on April 28, 2021
(5) Unit 1/2 control room roof, on May 5, 2021
(6) Unit 1 600-volt switchgear rooms 1C/1D, and Unit 1 DC switchgear rooms 1A/1B, on May 19, 2021.

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the onsite live fire brigade training and performance during an announced fire drill on April 15, 2021.

71111.06 - Flood Protection Measures

Cable Degradation (IP Section 03.02) (1 Sample)

The inspectors evaluated cable submergence protection in:

(1) Safety related cables in pull boxes PB1-BJ and PB2-BJ on April 7, 2021.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during shutdown of Unit 1 caused by a step change increase of drywell unidentified leakage, the inspectors observed reduction of power via decrease in recirculation flow, insertion of control rods followed by a reactor scram from 32 percent power and post scram activities to stabilize the plant in Mode 3 (Hot Shutdown). They also observed transfer of house loads, hourly updates of unidentified leakage calculations, de-inerting the drywell and preps for shutdown cooling on June 11-12, 2021.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated License Requalification Operator Training for the following training scenario: CPE-EOP: Main Turbine Bypass Valve Monthly, Steam Flow Instrument Failure, Fire in the Protected Area, Lowering Vacuum, Scram, Loss of High Pressure Feed, RCIC Steam Line break, RCIC failed to Isolate, Anticipated Emergency Depress, and Emergency Depress on May 5, 2021.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Safety related cables exposed to adverse environmental conditions.

(2)1A PSW pump surveillance test results placed the differential pressure ratio in the required action range, which was previously in the alert range. Additionally, the axial vibration level and calculated vibration ratio both increased to the alert range on June 3, 2021.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Emergent risk associated with Unit 2 following unplanned system outage of the 2D RHR pump for an extended period from April 16 to April 30, 2021.
(2) Risk associated with the Unit 1 RCIC system outage from May 4 to May 7, 2021.
(3) Emergent risk associated with Unit 1 following unplanned piping repair on the 1B RHR pump from May 10 to May 12, 2021.
(4) Emergent risk associated with the following unplanned equipment failures, Unit 1C emergency diesel generator (EDG), automatic start light failed to illuminate after a monthly run, 1D RHR service water pump tripped from overcurrent, and Unit 2 vital AC inverter failure, from May 28, to June 11, 2021.
(5) Unit 1 elevated risk for forced outage due to step change increase in drywell unidentified leakage, from June 12 and 18, 2021.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Condition Report (CR) 10788308, while performing semi-annual sampling of 2A EDG fuel oil storage tank, water and sediment failed at 2.5 percent on the bottom sample and CR 10788395, water found in 2A fuel oil day tank flush on April 8, 2021.
(2) CR 10789017, During performance of 34SV-R43-010-0 EDG Fuel Oil Transfer Pump Surveillance, the 2Y52C001A 2A EDG Fuel Oil Transfer Pump was in the alert range for high vibrations and in the action range for high flow on April 09, 2021.
(3) CR 10790963, While running the 2D Residual Heat Removal (RHR) Pump, alarm RHR Pump D OVLD/Lockout Relay Trip was received and the pump was manually secured. Following alarm relay replacement, the pump was restarted and tripped on Phase 2 overcurrent on April 16, 2021.
(4) CR 10796694, leak was identified on the 1B Residual Heat Removal pump casing drain line on May 10, 2021.
(5) CR 10782516, in leakage was seen on Unit 2 Core Spray 'B' loop as observed by increase pressure above jockey pump pressure on March 15, 2021.
(6) CR 10799968, while performing the 1A Plant Service Water IST Quarterly surveillance, the ratio of the test dP value to reference dP value was calculated to be 0.9189, in the required action range. Axial vibration level was also measured at 0.206 in/sec with a calculated vibration ratio of 2.58, which places it in the alert range on May 23, 2021.

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering Change (EC) SNC 1118966 for the complete replacement of the Unit 2 turbine building chillers due to obsolete equipment.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:

(1)34SV-E11-001-2, Residual Heat Removal Pump Operability, Version 22.2 following the overhaul of 2D RHR pump on April 30, 2021.

(2)34SV-E51-001-1 Reactor Core Isolation Cooling (RCIC) Pump Operability, Version 29.2, and 34SV-E51-001-1 RCIC Valve Operability, Version 18.7, after a Unit 1 RCIC system outage on May 7, 2021.

(3) NMP-ES-024-301, Liquid Penetrant Examination Color Contrast and Fluorescent, Version 14.0 and 34SO-E11-010-1, Residual Heat Removal (RHR) System section 4.2.5, Version 45.3, after the replacement of 1B RHR pump casing drainpipe on May 12, 2021.

(4)34SV-E41-002-2 High Pressure Coolant Injection Pump (HPCI) Operability, Version 39.2, and 34SV-E41-001-2 HPCI Valve Operability, Version 13.7, after a Unit 2 HPCI system outage on May 13, 2021.

(5) SNC1133912 Replacement of the Analog Trip and Testing System (ATTS) Power Supply 1E21K401B due to the original power supply failing previously, this work was completed on May 20, 2021.

(6)34SV-P41-001-1, Plant Service Water Pump Operability - 1B Preservice Test Section, Version 15.2 following the 1B pump replacement on May 30, 2021.

(7)34SV-E11-004-1, RHR Service Water Pump Operability - 1D RHRSW Pump Preservice Test Section, version 22.1, following the replacement of the pump and motor, on June 14, 2021.

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated Unit 1 forced outage activities due to increase in drywell unidentified leakage caused by a packing leak and pressure seal leak on the HPCI inboard steam isolation valve 1E41-F002, from June 11 to June 18.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1)34SV-P41-001-1, Plant Service Water Pump Operability, Version 15.2 on April 8, 2021.

(2)34SV-R43-002-2, Diesel Generator 1B Monthly Test, Version 26.4 on April 15, 2021.

(3)34SV-E11-004-1, RHR Service Water Pump Operability, Version 22.1 on April 19, 2021.

(4)57SV-C51-012-1, Average Power Range Monitor (APRM) Two-Out-Of-Four Time Response Testing Channel D, Version 0.6 on May 17, 2021.

Inservice Testing (IP Section 03.01) (1 Sample)

(1)34SV-E51-002-1, Reactor Core Isolation Cooling System Pump Operability IST, Version 29.2 on April 8, 2021.

RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)

(1) CR 10789452 noted an increase in Unit 1 Drywell Floor Drain leakage, on April 10, 2021

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

(1) Emergency Preparedness Drill 21EX02, Loss of Coolant Accident on April 13, 2021.

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Licensed reactor operators respond to a RCIC steam line break in the simulator and the inspectors observed the crew make an emergency declaration and notification. This represented a drill and exercise performance opportunity on May 19,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 03.10)===

(1) Unit 1 (April 1, 2020 to March 31, 2021)
(2) Unit 2 (April 1, 2020 to March 31, 2021)

BI02: RCS Leak Rate Sample (IP Section 03.11) (2 Samples)

(1) Unit 1 (April 1, 2020 to March 31, 2021)
(2) Unit 2 (April 1, 2020 to March 31, 2021)

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends in the maintenance of FLEX equipment that might be indicative of a more significant safety issue.

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) CRs 10800377 and 10799775; pertaining to radiation protection (RP) technicians assigned to the Operations Support Center (OSC) that are not required to have specific training for the Emergency Response Organization (ERO) position. CRs addressing this issue by a licensee's senior RP technician who questioned whether the site is implementing the high standards to support OSC duties.
(2) Operator Work Arounds, OS-BP-001, Operations Performance Indicators, Ver. 5.1 on June 14,

INSPECTION RESULTS

No findings were identified.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On July 23, 2021, the inspectors presented the integrated inspection results to Sonny Dean and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Corrective Action

Documents

10763660, 1076427, 10765536, 10765906, 10766273,

10767122, 10767220, 10768440, 10768453, 10768454,

10768471, 10769701, 10769718, 10771873, 10772188,

10772360, 10772649, 10773111, 10774071, 10775427,

10775872, 10776196, 10776585, 10776712, 10776960,

10777662, 10777755, 10777876, 10778741, 10778745,

10782781, 10782932, 10783001, 10783711, 10784268,

10785362, 10785619, 10785935, 10789039, 10789486,

10792073 and 10796411

Various

10716238, 10717331, 10724811, 10725085, 10728553,

10729316, 10734089, 10739860, 10741950, 10744866,

10750143, 10754860, 10756890, 10759996, 10760944,

10765581, 10765925, 10770167, 10772281, 10773104,

10776508, 10784735, 10792705, 10794164, 10799968

Various

Corrective Action

Documents

Resulting from

Inspection

10795361

05/04/2021

Drawings

BASES PLANT

SYSTEMS B 3.7

B 3.7.2 Plant Service Water (PSW) System and Ultimate

Heat Sink (UHS)

D-11001

SERVICE WATER PIPING AT INTAKE STRUCTURE

91.0

H-11024

SERVICE WATER PIPING

67.0

H-11600

SERVICE WATER AT DIESEL GENERATOR

37.0

H-11609

SERVICE WATER PIPING

2.0

Miscellaneous

HNP-1-FASR-10

10.7 Plant Service Water System

TECH SPEC

PLANT

SYSTEMS 3.7

3.7.2 Plant Service Water

281

Procedures

34SO-E11-010-1

Residual Heat Removal System

45.3

34SO-E11-010-2

Residual Heat Removal System

44.5

34SO-E41-001-1

High Pressure Coolant Injection (HPCI) System

30.4

34SO-P41-001-1

Plant Service Water System

36.19

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

34SO-Z41-001-1

Control Room Ventilation System

24.0

71111.05

Drawings

A-43965 Sheets

28B, 29B, 30B

and 32B

600V Switchgear Rooms 1C/1D and DC Switchgear Rooms

1A/1B

6.0

Fire Plans

A43965, Sheet

100

Unit 2 RCIC Pump and Turbine Room

2.0

A43965, Sheet 48 Unit 1 and 2 Control Room

4.0

A43965, Sheet 50 Unit 1 and 2 Control Room Roof

1.0

A43965, Sheet 60 Unit 1 Working Floor South Reactor Building Elevation 158'

5.0

A43965, Sheet 99 Unit 2 NE RHR and Core Spray Pump Room

3.0

Procedures

NMP-ES-035-014

Fleet Transient Combustible Controls

5.0

71111.11Q Miscellaneous

H-LR-AF-CPE003 CPE-EOP: Main Turbine Bypass Valve Monthly, Steam

Flow Instrument Failure, Fire in the Protected Area,

Lowering Vacuum, Scram, Loss of High Pressure Feed,

Reactor Core Isolation Cooling (RCIC) Steam Line break,

RCIC failed to Isolate, Anticipated Emergency Depress, and

Emergency Depress

05/02/2021

Procedures

34GO-OPS-014-1 Fast Reactor Shutdown

14.2

71111.12

Corrective Action

Documents

CR 10795220

05/04/2021

CR 10799968

06/03/2021

NDE Reports

HVA TD Report

Summary 2017-

2-14_2R23-

S004

Tan Delta Test Results for RHE202M02

2/14/2017

HVA TD Report

Summary R22-

S007-ES2-M06

Tan Delta Test Results for R22-S007-ES2-M06

2/25/2020

Procedures

2IT-EEL-001-0

Insulated Cables and Connections Program

1.1

NMP-ES-051

Cable Monitoring Program

9.2

NMP-ES-051-002

Tan Delta Testing

10.2

NMP-ES-051-003

Adverse Localized Equipment Environment Walkdown

2.5

NMP-ES-051-004

Pull Box Inspection

6.0

71111.13

Corrective Action

Documents

10797456

05/12/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Resulting from

Inspection

Drawings

H-13414

Elementary Diagram Diesel Generation 1C

55.0

Procedures

34AB-Y22-002-0

Naturally Occurring Phenomena

20.0

34GO-OPS-007-0 Shutdown/Refueling Mode Preparation Strategy For Flex

1.2

NMP-OS-010-002 Hatch Protected Equipment Logs

11.1

NMP-OS-019-253 Hatch Unit C Sig-12, Mode 4/5 RPV Inventory Control

2.3

71111.15

Corrective Action

Documents

10782516

03/15/2021

Drawings

H-26018

Unit 2 Core Spray System

40.0

Engineering

Evaluations

NMP-AD-012-F01 Prompt Determination of Operability for Unit Core Spray

Loop 'B'

05/18/2020

Miscellaneous

2R26 Hatch

Appendix J

Summarization

03/09/2021

Procedures

34AR-601-125-2

Cores Spray B Discharge Pressure High

4.4

34SO-E21-001-2,

Section 4.16

Core Spray System - System Pressure Control Due to In

leakage

26.5

2SV-TET-001-2

Unit 2 LLRT for 2E21-F006B & 2E21-F037B

2/20/2021

2SV-TET-001-2

Summarized LLRT Test Results for 2R26 Refueling Outage

03/09/2021

71111.18

Engineering

Changes

SNC1118966

05/05/2021

Miscellaneous

H-15-0079

Unit 2 Turbine building Chiller Replacement - Project Status

Report

2/18/2020

Procedures

2SP-02-15-21-

RR-1-2

Unit 2 Turbine Building Chillers 2P63-B019B & D Functional

Test

1.1

71111.19

Corrective Action

Documents

10797252,

10797254

and10797255

05/12/2021

10797478

05/12/2021

10797539

05/12/2021

Miscellaneous

Unit 1 TRM

Mater Equipment Cross Reference - table T10.1-1 (Sheets

3, 4, 5, 11, 12, 13, and 14)

113.0

Procedures

34IT-E51-003-1

RCIC Turbine Speed Control Test

05/07/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

34SV-E11-004-1

RHR Service Water Pump Operability

2.1

34SV-E41-001-2

HPCI Valve Operability

05/13/2021

34SV-E41-002-2

HPCI Pump Operability

05/13/2021

34SV-E51-001-1

RCIC Valve Operability

05/07/2021

34SV-E51-002-1

RCIC Pump Operability

05/07/2021

34SV-P41-001-1

Plant Service Water Pump Operability

15.2

57CP-CAL-102-1

Analog Master/Slave Trip Unit Calibration

16.8

57CP-CAL-302-0

Datametrics Voltage Converter Calibration

1.1

Work Orders

SNC1061116

05/07/2021

SNC11133912

05/20/2021

SNC115720

Repair of 1B RHR pump leak

05/12/2021

SNC1160130

6/14/2021

SNC1161391

06/11/2021

SNC614849

05/06/2021

SNC792312

05/04/2021

SNC833995

05/06/2021

SNC843513,

SNC842419,

SNC555959,

SNC636522,

SNC553993, and

SNC698526

05/12/2021

SNC845342

05/04/2021

SNC966362

05/04/2021

71111.20

Miscellaneous

Unit 1: Initial Drywell entry Walkdown Briefing

06/07/2021

Hatch Unit 1: H12021A Drywell Leakage Outage Safety

Assessment

0.0

Procedures

31GO-OPS-024-0 Outage Safety Assessment

5.5

34GO OPS-001-1

Plant Startup

46.1

34GO-OPS-003-1 Startup System Status Checklist

14.8

34SV-E51-001-1

REACTOR CORE ISOLATION COOLING SYSTEM 1E51-

F008

06/17/2021

34SV-SUV-016-1

COLD SHUTDOWN VALVE OPERABILITY 1E41-F002

06/16/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

34SV-SUV-016-1

Cold Shutdown Valve Operability 1E21-F005B

6/17/2021

2SV-TET-001-0

UNIT 1 LLRT 1E21-F005B

6-15-2021

2SV-TET-001-0

UNIT 1 LLRT 1E41-F002 & F003

06/16/2021

2SV-TET-001-0

UNIT 1 LLRT 1E51-F008

06/15/2021

71111.22

Corrective Action

Documents

10789452

04/10/2021

Corrective Action

Documents

Resulting from

Inspection

10795064

05/03/2021

Miscellaneous

Unit 1 Chemistry

Drywell Floor

Drain Sump Data

04/14/2021

Unit 1 Increase

Drywell Floor

Drain Leakage

Fault Tree

04/12/2021

Procedures

34SO-G11-013-1

Drywell & Reactor Building Sumps System

15.0

34SV-E11-004-1

RHR Service Water Pump Operability

2.1

57SV-C51-012-1

APRM Two-Out-Of-Four Time Response D

0.6

NMP-OS-028

ACMP - U1 DWFD Leakage Elevated

04/14/2021

Work Orders

SNC1102716

05/17/2021

71114.06

Miscellaneous

Observation

Summary

Emergency Preparedness Observation Form

05/19/2021

71151

Procedures

2CH-SAM-025-0

Reactor Coolant Weekly

04/28/2020

71152

Corrective Action

Documents

10714850, 10714599, 10784312, 10573812, 10781885,

10506986, 10527703, 10781885, 1084501 TE, 1087473 TE,

10796465

Various

Miscellaneous

Compensatory

Actions Requiring

Manipulations

Unit 2 Compensatory Actions List

Current List

Compensatory

Actions Requiring

Manipulations

Unit 1 Compensatory Actions

Current List

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Procedures

31GO-OPS-014-0

APC Sheet Number: 2-21-018P

03/16/2021

31GO-OPS-014-0 Annunciator and Plant Component Control

3.3

31GO-OPS-014-0 APC Sheet Number: 2-21-021

03/20/2021

31GO-OPS-014-0 APC Sheet Number: 2-21-020

03/20/2021

31GO-OPS-014-0 APC Sheet Number: 2-13-028P

09/12/2013

31GO-OPS-014-0 APC Sheet Number: 2-13-028P

06/12/2015

NMP-GM-002-

001

Corrective Action Program Instructions

40.0

NMP-OS-019-059 FLEX Storage Building Operating Instructions

2.1

NMP-OS-028

1B SJAE Monitoring Unit 1

2/04/2020

NMP-OS-028

U1 DWFD Leakage Elevated

04/16/2021

NMP-OS-028

Unit 1 Turbine Building Chilled Water System

04/30/2021

NMP-OS-028

1E51-F008 Packing Leak

2/14/2021

NMP-OS-028

1B Core Spray Inboard Injection Valve (1E21F005B) Bonnet

Leak

05/04/2021

NMP-OS-028

1A ASD Process Trouble and 1A ASD Trouble

2/03/2020

NMPS-OS-006-

2

Aggregate Operator Impact Review Instruction

3.0

OS-BP-001

Operations Performance Indicators

5.1