ML17304B326: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(One intermediate revision by the same user not shown)
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:AC CELERATED DIFIMBUTION DEMONSTRATION SYSTEM.~0 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)R I ACCESSION NBR:8907200409 DOC.DATE: 89/07/14 NOTARIZED:
{{#Wiki_filter:AC CELERATED                 DIFIMBUTION DEMONSTRATION                                       SYSTEM
NO DOCKET FACIL:STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi 05000529 AUTH.NAME AUTHOR AFFILIATION HAYNES,,J.G.
                                . ~                                             0 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
Arizona Public Service Co.(formerly Arizona.Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
ACCESSION NBR:8907200409                   DOC.DATE:         89/07/14     NOTARIZED: NO               DOCKET FACIL:STN-50-529 Palo Verde Nuclear Station,                             Unit 2, Arizona Publi 05000529 AUTH. NAME                 AUTHOR AFFILIATION HAYNES,,J.G.               Arizona Public Service Co. (formerly Arizona. Nuclear Power RECIP.NAME                 RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)                                   R


==SUBJECT:==
==SUBJECT:==
Special R 2-SR-89-005:on 890712,notification of unusual event declared on low pressurizer pressure.D DISTRIBUTION CODE: IE22D'COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), nciden Rpt, etc.8~lg~I a~s~l~I NOTES Standardized plant'.i,"'"-"-'"-'.'-'''5000529 j I RECIPIENT ,ID CODE/NAME PD.5 LA CHAN, T INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DS P/TPAB DEDRO NRR/DEST/ADE SH NRR/DEST/CEB SH NRR/DEST/ICSB 7 NRR/DEST/MTB 9H NRR/DEST/RSB SE'NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NUDOCS-ABSTRACT RES/DSIR/EIB RGN5 FILE 01 EXTERNAL EG&G WILLIAMS~S L ST LOBBY WARD NRC PDR NSIC MURPHY,G.A NOTES COOIES LTTR ENCL 1 1 1 1 1 1~1 1 1.1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1.1 1-1 1 1 4 4 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD5 PD DAVIS,M ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP IRM/DCTS/DAB NRR/DEST/A'DS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB SD NRR/DEST/SGB SD NRR/DLPQ/PEB 10 ERR/DREP/RPB 10~EG FI~RES/DSR/PRAB FORD BLDG HOY,A LPDR NSIC MAYS,G COPIES LTTR ENCL 1 1 1 1 2 2 1 1 2 2 1 1 1 0 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1"-1 1 1 1 1 1 1 R I" D S NCTE M ALL r RZDSn RECZPIEKIS PZEASE HELP US'ZO REDOCE KLSZE!~~~DOCX3MEPZ CXNZROL DESK IZSTS FOR DOCOMEaMXS VXJ DCSERT NEEDt TOTAL NUMBER OF COPIES REQUIRED: LTTR 45 ENCL 44 D D S il Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O, BOX 52034~PHOENIX, ARIZONA 85072-2034 192-00498-JGH/TDS/JJN July 14, 1989 U.S.Nuclear Regulatory Commission NRC Document Control Desk Washington, D.C.20555
Special R 2-SR-89-005:on 890712,notification of unusual                                               I event declared on low pressurizer pressure.
D DISTRIBUTION CODE: IE22D 'COPIES RECEIVED:LTR                                   ENCL       SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER),                               nciden     Rpt, etc.             8 NOTES I
Standardized plant'. i, "
          ~ lg     ~ I s a~
                                                                ~ l
                                                                              ~ I
                                                                                        "-'.   '- '''5000529   j RECIPIENT               COOIES                      RECIPIENT              COPIES
                ,ID CODE/NAME             LTTR ENCL                  ID CODE/NAME          LTTR ENCL PD.5     LA                     1          1      PD5 PD                        1      1 CHAN, T                         1          1      DAVIS,M                      1      1 INTERNAL: ACRS MICHELSON                     1          1      ACRS MOELLER                  2      2 ACRS WYLIE                     ~
1          1      AEOD/DOA                      1      1 AEOD/DS P/TPAB                   1    . 1      AEOD/ROAB/DSP                2      2 DEDRO                           1          1      IRM/DCTS/DAB                  1      1 NRR/DEST/ADE SH                 1          1      NRR/DEST/A'DS        7E      1      0 NRR/DEST/CEB SH                  1          1      NRR/DEST/ESB        8D      1      1 NRR/DEST/ICSB 7                  1          1      NRR/DEST/MEB        9H      1     1 NRR/DEST/MTB 9H                  1          1      NRR/DEST/PSB        SD      1      1 NRR/DEST/RSB SE                  1          1      NRR/DEST/SGB        SD       1      1
            'NRR/DLPQ/HFB 10                  1          1      NRR/DLPQ/PEB         10       1      1 NRR/DOEA/EAB 11                  1          1      ERR/DREP/RPB         10       2      2 NUDOCS-ABSTRACT RES/DSIR/EIB 1
1  -
                                                      . 1 1
                                                              ~EG       FI~
RES/DSR/PRAB 1
1 "-  1 1
RGN5          FILE 01          1         1 R
EXTERNAL    EG&G      WILLIAMS~ S            4          4      FORD BLDG HOY,A              1     1         I" L ST LOBBY        WARD          1         1       LPDR                          1     1 NRC PDR                          1         1       NSIC MAYS,G                  1     1 NSIC MURPHY,G.A                  1         1                                                       D NOTES                                          1         1                                                     S D
D NCTE     M ALL r RZDSn   RECZPIEKIS PZEASE HELP US 'ZO REDOCE KLSZE!               ~~ ~         DOCX3MEPZ CXNZROL DESK S
IZSTS FOR   DOCOMEaMXS   VXJ     DCSERT NEEDt TOTAL NUMBER OF COPIES REQUIRED: LTTR                             45   ENCL     44


==Dear Sirs:==
il Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O, BOX 52034 ~ PHOENIX, ARIZONA85072-2034 192-00498-JGH/TDS/JJN July  14, 1989 U. S. Nuclear Regulatory Commission NRC  Document Control Desk Washington, D.C. 20555
 
==Dear   Sirs:==


==Subject:==
==Subject:==
Palo Verde Nuclear Generating Station (PVNGS)Unit 2 Docket No.STN 50-529 (License No.NPF-51)Special Report 2-SR-89-005 File: 89-020-404 Attached please find Special Report 2-SR-89-005 prepare'd and submitted pursuant to,Emergency Plan Implementing Procedure-03.This report discusses a NOTIFICATION OF UNUSUAL EVENT due to a Safety Injection System Actuation.
Palo Verde Nuclear Generating Station (PVNGS)
If you have any questions, please contact T.D.Shriver, Compliance Hanager at (602)393-2521.Very tr ly yours, JGH/TDS/JJN/kj Attachment (all w/a)cc: W.F.Conway D.B.Karner J.B.Hartin T.J.Polich H.J.Davis A.C.Gehr INPO Records Center R.T.Hilstead C.F.Tedford F.L.Russo T.J.Agnos R.Colson J.G.Ha nes Vice President.
Unit 2 Docket No. STN 50-529 (License No. NPF-51)
Nuclear Production swy07)0I)409 8907 1 4 PDR ADOCK 05000529 PDC~g2L II I 4k Palo Verde Nuclear Generating Station Unit 2 Notification of Unusual Event Docket No.50-529 License No.NPF-51 Special Report No.2-SR-89-005 This Special Report is being provided pursuant to Emergency Plan Implementing Procedure (EPIP)-03,"Notification of Unusual Event Implementing Actions" to report the declaration of a Notification of Unusual Event (NUE)for Palo Verde Unit 2.The NUE was declared pursuant to EPIP-02,"Emergency Classification" as.a result of the initiation of a Safety Injection Actuation Signal (SIAS)on low pressurizer pressure.On July 12, 1989 Palo Verde Unit 2 was operating at 100 percent power in Hode 1 (POMER OPERATION) when a load shed signal on 13.8 KV Bus, 2E-NAN-S02, resulted in Reactor Coolant Pumps (RCPs)1B and 2B being deenergized.
Special Report 2-SR-89-005 File: 89-020-404 Attached please find Special Report 2-SR-89-005 prepare'd and submitted pursuant to,Emergency Plan Implementing Procedure -03. This report discusses a NOTIFICATION OF UNUSUAL EVENT due to a Safety Injection System Actuation.
As a result of the partial loss of forced circulation, at approximately 2212 HST the reactor tripped on low DNBR which resulted in a turbine trip.Following the reactor and turbine trip, the Reactor Coolant System (RCS),pressure decreased as expected.However, additional depresurization occurred due to less than nominal decay heat and RCP heat generation, greater than nominal pressurizer spray valve leakage, and three pressurizer heaters being out of service.At approximately 2213 HST the RCS pressure decreased to the Safety Injection and Containment Isolation setpoint.The Safety Injection and, Containment Isolation Actuation resulted in the actuation of the"A" and"B" Diesel Generator Start Sequencer.
If you   have any questions,     please contact T. D. Shriver, Compliance Hanager at (602) 393-2521.
All Engineered Safety Features actuated as designed.At approximately 2223 HST on July 12, 1989, a Notification of Unusual Event (NUE)was declared.At approximately 2237 HST on July 12, 1989, the appropriate state and local agencies were notified via the Notification and Alert Network (NAN).The Nuclear Regulatory Commission (NRC)Operations Center was notified at approximately 2308 HST on July 12, 1989.Stable conditions were achieved and the NUE was terminated at approximately 2322 HST on July 12, 1989.The event did not result in any challenges to fission product barriers or result in any releases of radioactive materials.
Very tr ly yours, J. G. Ha nes Vice President.
Nuclear Production JGH/TDS/JJN/kj Attachment cc:   W. F. Conway       (all    w/a)
D. B. Karner J. B. Hartin T. J. Polich H. J. Davis A. C. Gehr INPO Records Center R. T. Hilstead C. F. Tedford F. L. Russo T. J. Agnos R. Colson swy07 )0I )409 PDR    ADOCK 8907 1 4 05000529 PDC
                                                                                  ~g2L III
 
4k Palo Verde Nuclear Generating Station Unit   2 Notification of Unusual Event Docket No. 50-529 License No. NPF-51 Special Report No. 2-SR-89-005 This Special Report is being provided pursuant to Emergency Plan Implementing Procedure (EPIP)-03, "Notification of Unusual Event Implementing Actions" to report the declaration of a Notification of Unusual Event (NUE) for Palo Verde Unit 2. The NUE was declared pursuant to EPIP-02, "Emergency Classification" as. a result of the initiation of a Safety Injection Actuation Signal (SIAS) on low pressurizer pressure.
On July 12, 1989 Palo Verde   Unit 2 was operating at 100 percent power in Hode 1 (POMER OPERATION) when a   load shed signal on 13.8 KV Bus, 2E-NAN-S02, resulted in Reactor Coolant Pumps (RCPs) 1B and 2B being deenergized. As a result of the partial loss of forced circulation, at approximately 2212 HST the reactor tripped on low DNBR which resulted in a turbine trip. Following the reactor and turbine trip, the Reactor Coolant System (RCS),pressure decreased as expected. However, additional depresurization occurred due to less than nominal decay heat and RCP heat generation, greater than nominal pressurizer spray valve leakage, and three pressurizer heaters being out of service. At approximately 2213 HST the RCS pressure decreased to the Safety Injection and Containment Isolation setpoint. The Safety Injection and, Containment Isolation Actuation resulted in the actuation of the "A" and "B" Diesel Generator Start Sequencer.     All Engineered Safety Features actuated as designed.
At approximately 2223 HST on July 12, 1989, a Notification of Unusual Event (NUE) was declared. At approximately 2237 HST on July 12, 1989, the appropriate state and local agencies were notified via the Notification and Alert Network (NAN). The Nuclear Regulatory Commission (NRC) Operations Center was notified at approximately 2308 HST on July 12, 1989.
Stable conditions were achieved and the NUE was terminated at approximately 2322 HST on July 12, 1989. The event did not result in any challenges to fission product barriers or result in any releases of radioactive materials.
A Licensee Event Report will be submitted within 30 days of the event in accordance with 10CFR50.73 which will provide further details concerning the load shed from 2E-NAN-S02, the decrease of RCS pressure below the safety injection and containment isolation actuation setpoint, and the greater than nominal pressurizer spray valve leakage.}}
A Licensee Event Report will be submitted within 30 days of the event in accordance with 10CFR50.73 which will provide further details concerning the load shed from 2E-NAN-S02, the decrease of RCS pressure below the safety injection and containment isolation actuation setpoint, and the greater than nominal pressurizer spray valve leakage.}}

Latest revision as of 05:14, 4 February 2020

Special Rept 2-SR-89-005:on 890712,load Shed Signal of 13.8 Kv Bus 2E-NAN-S02 Resulted in Deenergizing Reactor Coolant Pumps 1B & 2B & Reactor Trip.Caused by Less than Nominal Decay Heat.Unusual Event Declared.Ler Will Be Submitted
ML17304B326
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 07/14/1989
From: Haynes J
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
192-00498-JGH-T, 192-498-JGH-T, 2-SR-89-005, 2-SR-89-5, NUDOCS 8907200409
Download: ML17304B326 (6)


Text

AC CELERATED DIFIMBUTION DEMONSTRATION SYSTEM

. ~ 0 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8907200409 DOC.DATE: 89/07/14 NOTARIZED: NO DOCKET FACIL:STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi 05000529 AUTH. NAME AUTHOR AFFILIATION HAYNES,,J.G. Arizona Public Service Co. (formerly Arizona. Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk) R

SUBJECT:

Special R 2-SR-89-005:on 890712,notification of unusual I event declared on low pressurizer pressure.

D DISTRIBUTION CODE: IE22D 'COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), nciden Rpt, etc. 8 NOTES I

Standardized plant'. i, "

~ lg ~ I s a~

~ l

~ I

"-'. '- 5000529 j RECIPIENT COOIES RECIPIENT COPIES

,ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD.5 LA 1 1 PD5 PD 1 1 CHAN, T 1 1 DAVIS,M 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE ~

1 1 AEOD/DOA 1 1 AEOD/DS P/TPAB 1 . 1 AEOD/ROAB/DSP 2 2 DEDRO 1 1 IRM/DCTS/DAB 1 1 NRR/DEST/ADE SH 1 1 NRR/DEST/A'DS 7E 1 0 NRR/DEST/CEB SH 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB SD 1 1 NRR/DEST/RSB SE 1 1 NRR/DEST/SGB SD 1 1

'NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/PEB 10 1 1 NRR/DOEA/EAB 11 1 1 ERR/DREP/RPB 10 2 2 NUDOCS-ABSTRACT RES/DSIR/EIB 1

1 -

. 1 1

~EG FI~

RES/DSR/PRAB 1

1 "- 1 1

RGN5 FILE 01 1 1 R

EXTERNAL EG&G WILLIAMS~ S 4 4 FORD BLDG HOY,A 1 1 I" L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 D NOTES 1 1 S D

D NCTE M ALL r RZDSn RECZPIEKIS PZEASE HELP US 'ZO REDOCE KLSZE! ~~ ~ DOCX3MEPZ CXNZROL DESK S

IZSTS FOR DOCOMEaMXS VXJ DCSERT NEEDt TOTAL NUMBER OF COPIES REQUIRED: LTTR 45 ENCL 44

il Arizona Public Service Company PALO VERDE NUCLEAR GENERATING STATION P.O, BOX 52034 ~ PHOENIX, ARIZONA85072-2034 192-00498-JGH/TDS/JJN July 14, 1989 U. S. Nuclear Regulatory Commission NRC Document Control Desk Washington, D.C. 20555

Dear Sirs:

Subject:

Palo Verde Nuclear Generating Station (PVNGS)

Unit 2 Docket No. STN 50-529 (License No. NPF-51)

Special Report 2-SR-89-005 File: 89-020-404 Attached please find Special Report 2-SR-89-005 prepare'd and submitted pursuant to,Emergency Plan Implementing Procedure -03. This report discusses a NOTIFICATION OF UNUSUAL EVENT due to a Safety Injection System Actuation.

If you have any questions, please contact T. D. Shriver, Compliance Hanager at (602) 393-2521.

Very tr ly yours, J. G. Ha nes Vice President.

Nuclear Production JGH/TDS/JJN/kj Attachment cc: W. F. Conway (all w/a)

D. B. Karner J. B. Hartin T. J. Polich H. J. Davis A. C. Gehr INPO Records Center R. T. Hilstead C. F. Tedford F. L. Russo T. J. Agnos R. Colson swy07 )0I )409 PDR ADOCK 8907 1 4 05000529 PDC

~g2L III

4k Palo Verde Nuclear Generating Station Unit 2 Notification of Unusual Event Docket No. 50-529 License No. NPF-51 Special Report No. 2-SR-89-005 This Special Report is being provided pursuant to Emergency Plan Implementing Procedure (EPIP)-03, "Notification of Unusual Event Implementing Actions" to report the declaration of a Notification of Unusual Event (NUE) for Palo Verde Unit 2. The NUE was declared pursuant to EPIP-02, "Emergency Classification" as. a result of the initiation of a Safety Injection Actuation Signal (SIAS) on low pressurizer pressure.

On July 12, 1989 Palo Verde Unit 2 was operating at 100 percent power in Hode 1 (POMER OPERATION) when a load shed signal on 13.8 KV Bus, 2E-NAN-S02, resulted in Reactor Coolant Pumps (RCPs) 1B and 2B being deenergized. As a result of the partial loss of forced circulation, at approximately 2212 HST the reactor tripped on low DNBR which resulted in a turbine trip. Following the reactor and turbine trip, the Reactor Coolant System (RCS),pressure decreased as expected. However, additional depresurization occurred due to less than nominal decay heat and RCP heat generation, greater than nominal pressurizer spray valve leakage, and three pressurizer heaters being out of service. At approximately 2213 HST the RCS pressure decreased to the Safety Injection and Containment Isolation setpoint. The Safety Injection and, Containment Isolation Actuation resulted in the actuation of the "A" and "B" Diesel Generator Start Sequencer. All Engineered Safety Features actuated as designed.

At approximately 2223 HST on July 12, 1989, a Notification of Unusual Event (NUE) was declared. At approximately 2237 HST on July 12, 1989, the appropriate state and local agencies were notified via the Notification and Alert Network (NAN). The Nuclear Regulatory Commission (NRC) Operations Center was notified at approximately 2308 HST on July 12, 1989.

Stable conditions were achieved and the NUE was terminated at approximately 2322 HST on July 12, 1989. The event did not result in any challenges to fission product barriers or result in any releases of radioactive materials.

A Licensee Event Report will be submitted within 30 days of the event in accordance with 10CFR50.73 which will provide further details concerning the load shed from 2E-NAN-S02, the decrease of RCS pressure below the safety injection and containment isolation actuation setpoint, and the greater than nominal pressurizer spray valve leakage.