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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
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Text
LICENSEE EVENT REPORT (LER)
FACILITYNAME(1) DOCKET NUMBER(2) PAGE (3)
Palo Verde Unit 1 0 5 0 0 0 5 2 8 1OF8 TLE (4)
Letdown Line Break Due To Pressure Transients EVENT DATE 5 LER NUMBER 6) REPORT DATE 7 OTHER FACIUTIES INVOLVED 6 MONTH DAY YEAR YEAR SEQUENTIAL REVI T NUMBERS NUMBER NUMBER N/A N/A 0 5 2 0 9 8 9 8 - 0 0 7 - 0 0 0 6 1 9 9 8 OPERATING HIS REPORT IS SUBMITTED PURSUAN1'O THE REQUIREMENTS OF 10 CFR S: (Check one or more ot the foaovnng) (11)
MODE (9) 20.402(b) 20.405(c) 50.73(aX2Xrv) 73.71(b)
POWER 20.405(aXI X') 50.36(cX I) 50.73(aX2Xv) 73.71(c)
LEvEL(to) 204os(aXIXi) 50.36(cX2) 50.73(a X2Xv's) OTHER (SPecrfy at Abstract 1 Q 0 20.405(aXI Xii) 50.73(aX2XO 50.73(aX2XvisXA) below arxf al Text. NRC Fohn 20.405(a X I Xiv) so.73(aX2Xsq 50.73(aX2X~XB) 366A) 20405(aXIXv) 5073(aX2XB) 50.73(aX2Xx)
LICENSEE CONTACT FOR THIS LER (12)
NUMBER EA CODE Daniel G. Marks, Section Leader, Regulatory Affairs REPORl'LEPHONE 6 0 2 3 9 3 - 6 4 9 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS (13)
CAUSE SYSTEM COMPONENT MANUFAC. REPORTABLE CAUSE SYSTEM COMPONENT MANUFAC REPORTABLE TURER TO NPRDS TURER TO NPRDS C 8 p s p YES SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH OAY YEAR SUBMISSION X YES (Ifyes, complete EXPECTED SUBMISSION DATE) No DATE (15) 0 8 1 9 On May 20, 1998, at approximately 0100 MST, Palo Verde Unit 1 was in Mode 1 (POWER OPERATION), operating at 100') power when control room personnel (utility licensed) observed flow and pressure perturbations on the Chemical and Volume Control system (CVCS) letdown system. Radiation monitor alert alarms from area monitors RU-9 and RU-8 were annunciated at approximately 01:06 and 01:09, respectively, indicating a potential letdown system leak in the Auxiliary Building. A subsequent walk-down of the letdown valve gallery area confirmed that a leak had developed on the 2" letdown line just upstream of the pressure relief valve PSV 345. Approximately 325 gallons of letdown flow was routed to the equipment drain tank via pressure relief valve (PSV-345) and 175 gallons of letdown flow was released into the valve gallery.
Prior to this evolution, at approximately 1259, Unit 1 was completing surveillance test (ST) 40ST-9CH06, Charging Pump Operability and started the "A" Charging Pump to restore from the ST, commencing two pump operation. Shortly after i.ncreasing letdown flow, operations noted abnormal flow and pressure perturbations. Control room personnel (utility licensed) isolated letdown at approximately Ol:23 using letdown isolation valve UV-515. Control room personnel (utility licensed) initiated entry into procedure 40AO-9ZZ05, Loss of Letdown. The plant remained operating in mode 1 at 100% power. The apparent cause (preliminary) of the letdown line piping failure was determined to be cyclic fatigue due to dynamic pressure transients.
As an interim troubleshooting action, visual inspections were performed on selected portions of the letdown piping in Units one, two and three. The Unit 1 piping was replaced and the damaged piping section was sent off-site for analysis and no problems noted in unit's .2 and 3.
No previous similar events have been reported by Palo Verde pursuant to 10CFR50.73.
'7)806300552 'I)80619 PDR ADOCK 05000528 8 PDR
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION RAG ILITYNAME DOCKET NUMBER LER NUMBER PAGE SEQUENTIAL REVISION NUMBER NUMBER Paio Verde Unit 1 0 5 0 0 0 5 2 8 9 8 - 0 0 7 - 0 0 0 2 of 0'
- 1. REPORTING REQUIREMENT:
This LER (528/98-007-00) is being submitted pursuant to 10 CFR 50.73(a)(2)(i)(B), operating in a condition prohibited by the plant' Technical Specifications (TS), where Unit 1 wasTrequired to .enter TS
- 3. 0. 3'.
Specifically, on May 20, 1998 at approximately 0100 MST', Unit 1 was in Mode 1 (POWER OPERATION) at normal operating temperature and pressure at approximately 100% power when control room personnel (utility licensed) determined that a leak had developed in the ASME Code Class 2 letdown line and isolated the leak in accordance with abnormal operations procedure 40A0-9ZZ05, Loss of Letdown. The letdown piping failure resulted in control room personnel(utility licensed) entering Technical Specification LCO 3.4.9 for structural integrity of ASME Code Class 2 components.
Specifically, LCO 3.4.9 action (b) was entered which requires restoration of structural integrity of the affected component(s) to within its limit or isolate the affected component(s) prior to increasing reactor coolant system temperature above 210'F.
Compliance with LCO 3.4.9 action(b) could not be achieved since Unit 1 was operating at 100% power with reactor coolant system temperature greater than 210'F therefore, control room personnel(utility licensed) subsequently entered Technical Specification LCO 3.0.3. Approximately 22 minutes into the event corrective measures were established by isolating letdown, which allowed control room personnel to exit LCO 3.0.3 and return to compliance with Technical Specification 3.4.9 action (b). Compliance with Technical Specifications was maintained throughout the event.
As described in the PVNGS UFSAR Chapter 5, Section 5.2.5.1.5, "Intersystem.
Leakage", CVCS leakage is not considered when determining operational RCS leakage in accordance with Technical Specification 3.4.5.2. If any leakage of reactor coolant exists outside of the RCS barrier (i.e., intersystem leakage), and it is capable of being isolated, then the leakage is not operational RCS leakage. Continued operation under Technical Specification 3.4.5.2 for RCS Leakage does not apply in this case.
EVENT DESCRIPTION:
On May 20, 1998 at approximately 0100 MST, Unit 1 was in Mode 1 operating at 100% power (POWER OPERATION) when indications of flow and pressure perturbations were observed on the Chemical and Volume Control system (CVCS) letdown system. Auxiliary Building Area Radiation monitor alert alarms from RU-9 and RU-8 were annunciated at 01:06 and 01:09, respectively, indicating a,potential letdown leak in the Auxiliary Building.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ACIEITY NAME DOCKET NUMBER LER NUMBER PAGE SEQUENTIAI. REVISION NUMBER NUMBER Palo Verde Unit 1 EXT 0 5 0 0 0 5 2 8 9.8-007-0003 of 0 8 EVENT DESCRIPTION Continued:
With assistance from Radiation Protection, an Auxiliary Operator (AO)
(utility non-licensed) entered the 100'ux.'ldg. and observed steam and water in the letdown valve gallery area.
Subsequent investigation determined that a leak had developed on the 2" letdown line piping as a result of a circular crack at a weld where a 1" pipe stanchion of a spring can support was connected to the letdown 1'ine.
Approximately 325 gallons of letdown flow was routed to the equipment
'drain tank via pressure safety valve (PSV-345) and approximately 175 gallons was released into the valve gal'lery room from the cracked letdown line.
Prior to this evolution, at approximately 1259, Unit 1 was completing quarterly surveillance test 40ST-9CH06, Charging Pump. Operability and started the "A" Charging Pump to restore the plant into its normal two-pump operation. Letdown flow was increased using letdown flow control RCN-LIC-110 in manual.
Subsequently, operations observed indications of letdown flow mismatch and that PSV-345 may have lifted which resulted in letdown flow and pressure perturbations. At 01:06, RU-9 alert alarm was received. The backpressure control valve controller (CHN-PIC-201) was placed in manual and demand increased to ) 50%. This caused oscillations to dampen.
Controller CHN-PIC-201 was then placed, back in auto. Approximately two minutes later; pressure oscillations began to recur. At 01:09, RU-8 alert alarm was received and at 01:10, RU-9 high alarm .was annunciated.
Operations believed at this time that a valve-packing leak had developed in the Auxiliary building. The appropriate alarm response procedures were used and an AO (utility non-licensed) dispatched to walkdown the letdown system for any leaks or abnormalities.
The Control Room was notified by the Area Operator that steam, and water was coming from the letdown valve gallery area'. Subsequent to this notification, letdown was isolated at approximately 01:23 using letdown isolation valve CHB-UV-515. Procedure 40AO-9ZZOS, Loss of'etdown, was entered. The plant remained operating in mode 1 at 100% power.
The shift manager determined that no event declaration was required per the Emergency Plan classification criteria.
There were no safety system actuations and none were required.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ACIUTYNAME DOCKET NUMBER LER NUMBER PAGE SEQUENTIAL REVISION NUMBER NUMBER Palo Verde Unit 1 0 .5 0 0 0 5 2 8 -9 8 - 0 0 7 -, 0 0 0 4 of 0 8
- 3. 'ASSESSMENT OF THE SAFETY CONSEQUENCES AND IMPLICATIONS OF THIS EVENT:
Although this event did result in an integrated leak of approximately 175 gallons of reactor coolant in a radiological controlled area, there were no challenges to fission product barriers. 'Therefore there were no adverse safety consequences or implications as a result of this event.. This event did not adversely impact the safe operation of the plant or the health and safety of the public.
A safety assessment was conducted on May 21, 1998 to determine the, safety implications of continued operation of Unit 1 with the letdown line isolated. The assessment concluded that the bounding safety analysis results would not be adversely impacted by operating the unit with letdown isolated, provided that no more than two charging pumps are simultaneously in service. Therefore, continued operation of Unit 1 with letdown isolated was all'owed under Technical Specification 3.4.9(b).
An additional nuclear safety assessment was conducted to determine any impact the event may have caused on assumptions in the safety analysi's.
The assessment concluded that the consequences of the letdown line leak in Unit 1 were bounded by the consequences identified in UFSAR Chapter 15, specifically section 15.6.2.1, "Double-Ended Break Of A Letdown Line Outside Containment." The assessment also included an analysis of the letdown leak rate during the event. The investigation of the event.
determined that system leakage was approximately 175 gallons which approximates to 12 gpm of system leakage over the duration of the event.
This safety assessment considered off-site dose consequences based on a conservative leak rate. The dose consequence for off-site was 0.4 Rem which was well within the 22.4 Rem reported in UFSAR 15.6.2. In addition a dose assessment was performed for effluent release from the plant vent.
Plant vent monitor (RU-143) data indicated no significant increase in dose rate to on-site personnel as well as offsite.
41 I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITYNAME DOCKET NUMBER LER NUMBER PAGE SEOUENTIAL REVISION NUMSER NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 8 - 0 0 7 - 0'0 05of08
- 4. CAUSE OF THE EVENT:
The root cause of the event is still under evaluation pending results from the metallurgical report from off-site laboratory analysis and from the development of hydraulic and I&C models. The investigation of this event has determined the apparent cause to be cyclic fatigue of the letdown piping due to dynamic pressure transients. The following contributing factors are under investigation and will be addressed by engineering during equipment root cause of failure (ERCFA) activities.
The probable cause(s) listed below are factors that are believed to be potential contributors to the event.
- 1. System response to some transient conditions (Relative slow response of the backpressure control valve control loop and actuation of the relief valve) 2 ~ Contribution of hanger design to increased stresses on system.
- 3. The rate that the letdown control valve is opened The final root cause will be submitted in a supplement to this LER.
- 5. STRUCTURES, SYSTEMS, OR COMPONENTS INFORMATION:
During this event, operations manually throttled the letdown control valve open to increase letdown flow with the backpressure control valve in auto to maintain backpressure at setpoint. Due to the delay in the backpressure control loop, a pressure spike was experienced in the letdown system, which rapidly increased backpressure, to the set pressure of the pressure relief valve PSV-345.
It is not known precisely when the letdown line failed, during the first pressure spike, or soon thereafter. Cycling of pressure relief valve PSV-345 is indicated as a potential contributing factor to the dynamic pressure transient experienced during this event.
Engineering has determined that the spring can pipe support with the 1" diameter stanchion connected to the letdown piping was not an optimal design for the estimated loading conditions during the event. Based on damage assessment, an enhanced Pipe support design to account for all postulated loading (i.e., axial, lateral) was installed to provide additional piping integrity protection and eliminate the piping stanchion and associated high local stresses.
- 9
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION ACILI1YNAME DOCKET NUMBER LER NUMBER PAGE SEQUENTIAL REVISION NUMBER NUMBER Palo Verde lJnit 1 0 5 0 0 0 5 2 8 9 8 - 0 0 7 - 0 0 0 6 of 0 8 EXT Continued:
STRUCTURES, SYSTEMS, OR COMPONENTS INFORMATION The affected portion of the letdown system piping and components are ASME Section III class 2 piping rated for 650psi. Review of the data plots indicated a maximum pressure was reached in the system of 600.1 psig.
Pressure relief valve PSV-345 valve is designed to lift at 600psi and has a relieving capacity of 180 gpm. It was determined that the relief valve did not exceed the proper lift pressure setpoint and had sufficient capacity to keep pressure below the design pressure.
Effects of the event for impact against Equipment Qualification, RCP seal extended operation without seal injection and Appendix R considerations were reviewed by engineering. The conclusion of each evaluation determined that this event does not impact or have a significant affect on equipment operability nor jeopardize the ability to safely shutdown the unit during a postulated fire.
There are no indications that any structures systems or components were inoperable prior to the event that contributed to this event.
CORRECTIVE ACTIONS TO PREVENT RECURRENCE:
The following actions were taken as immediate and interim corrective action until final corrective actions are developed from the equipment root cause of failure.
- 1. Letdown was isolated using CHB-UV-515 on May 20, 1998.
- 2. A,night order was issued to heighten operations personnel awareness of the Unit 1 event and to exercise precaution associated with activities that will possibly challenge the control characteristics of the backpressure control valves.
- 3. The Unit 1 letdown piping was replaced and the pipe support .and hangers were optimized. The system was returned to service on May 22, 1998. The failed letdown line was cut out of the system and subsequently quarantined in the Hot Machine Shop. Inservice Inspection (ISI) engineers performed a visual examination of the support-to-pipe weld and determined the apparent cause to be cyclic overload of the line/hanger due to a dynamic pressure transient.
' t(
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AGILITYNAME DOCKET NUMBER LER NUMBER PAGE SEQUENTIAL REVISION NUMBER NUMBER Palo Verde Unit 1 0 5 0 0 0 5 2 8 9 8 - 0 0 7 - 0 0 0 7 of 0 8 EXT CORRECTIVE ACTIONS TO,PREVENT RECURRENCE Continued:
- 4. Operating procedures were enhanced to minimize hydraulic transients.
Procedure 4xOP-xCH01, CVCS Normal Operations, was revised to lower letdown backpressure to 200 to 350 p i, preferably as close to 200 psi as practical. Decreasing letdown backpressure to 200 psi was emphasized prior to starting the desired charging pump. Procedure 400P-9CH13, Charging Pump Pulsation Dampener Operation, was revised to reference procedure 4xOP-xCH01, CVCS Normal Operations.
- 5. Transportability has been evaluated for Units 2 and 3 to allow continued operation while root cause and final corrective actions are determined.
Walkdown of the piping system in Unit 1 revealed that the failed letdown line had apparently experienced a dynamic transient of sufficie'nt magnitude to cause observable pipe support deformation.
Piping in the proximity of the dynamic failure, including fittings, supports and weld between the letdown line and stanchion, were inspected in all three units. Visual inspection of the affected letdown piping was performed in Unit's 2 and 3 without disturbing insulation. No damage or signs of cracking were observed. In addition to the above, high stress points in Unit 2 letdown piping, with all insulation removed, were also inspected. No deficiencies were identified.'.
Diagnostic testing of the in-service backpressure control valve (201P) was performed subsequent to this event. Test results indicate that the positioner was found to have a high zero (valve would initially open at approximately 6.5 ma control signal versus 4 ma) and that the stroke length was found to be slightly short at 0.6 inches, versus the nominal travel of 0.75 inches. 'reliminary evaluation indicates that this was not a contributing factor to the event. However, the investigation team determined that this concern warrants further investigation.
II Ol P
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AGILITY NAME DOCKET NUMBER LER NUMBER PAGE SEQUENTIAI. REVISION NUMBER NUMBER Palo verde Unit 1 EXT 0 5 0 0 0 5 2 8 98-00'7-0008 0 8 CORRECTIVE ACTIONS TO PREVENT RECURRENCE Continued:
Valve travel, bench set; spring rate and packing load for letdown control valve 110(Q) were all acceptable and consistent with the as-left test results ollowing the Unit 1 refueling outage valve repack. The volume booster gain was also noted as not having excessive gain. The valve positioner was found to have a low zero (the valve may not fully close at the 4 ma control signal).
Calibration of the instrumentation loop for the Letdown Back Pressure Valve was verified on May 20, 1998. The components included pressure transmitter 1JCHNPT0201, indicator 1JCHNPI0201, controller 1JCHNPIC0201 and alarm cards 1JCHNPSHL0210 (hi & low). All as found data was satisfactory. No adjustments were necessary.
It is expected that additional corrective actions wil'1 result from the 1'aboratory analysis of the damaged pipe and final corrective actions along with the results from the equipment root cause of failure will be documented in a supplement to this LER.
- 7. PREVIOUS SIMILAR EVENTS:
Although no other previous simil'ar events have been reported at Palo Verde pursuant to 10 CFR 50.73 in the last three years, operating history indicates that previous concerns with the responsiveness .of the backpressure control system have occurred and are under investigation.
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