IR 05000354/2009002: Difference between revisions

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{{Adams|number = ML091170613}}
{{Adams
| number = ML091170613
| issue date = 04/27/2009
| title = IR 05000354-09-002 on 01/01/09 - 03/31/09 for Hope Creek
| author name = Burritt A L
| author affiliation = NRC/RGN-I/DRP/PB3
| addressee name = Joyce T
| addressee affiliation = PSEG Nuclear, LLC
| docket = 05000354
| license number = NPF-057
| contact person = burritt al
| case reference number = FOIA/PA-2010-0209
| document report number = IR-09-002
| document type = Inspection Report, Letter
| page count = 27
}}


{{IR-Nav| site = 05000354 | year = 2009 | report number = 002 }}
{{IR-Nav| site = 05000354 | year = 2009 | report number = 002 }}
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==Dear Mr. Joyce:==
==Dear Mr. Joyce:==
On March 31, 2009, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at the Hope Creek Generating Station. The enclosed inspection report documents the inspection results discussed on April 8, 2009, with Mr. George Barnes and other members of your staff. The inspections examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, no findings of significance were identified.
On March 31, 2009, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at the Hope Creek Generating Station. The enclosed inspection report documents the inspection results discussed on April 8, 2009, with Mr. George Barnes and other members of your staff.
 
The inspections examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
Based on the results of this inspection, no findings of significance were identified.


In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/
Sincerely,/RA/  
 
Arthur L. Burritt, Chief Projects Branch 3 Division of Reactor Projects Docket No: 50-354 License No: NPF-57  
Arthur L. Burritt, Chief Projects Branch 3 Division of Reactor Projects Docket No: 50-354 License No: NPF-57  


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=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
......................................................................................................... 3
IR 05000354/2009002; 01/01/2009 - 03/31/2009; Hope Creek Generating Station; Routine
 
Integrated Inspection Report.
 
This report covers a three-month period of inspection by resident inspectors and announced inspections by regional specialist inspectors. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
 
No findings of significance were identified.
 
4


=REPORT DETAILS=
=REPORT DETAILS=
===Summary of Plant Status===
The Hope Creek Generating Station operated at or near full power for the duration of the inspection period with the following exceptions. On January 9, operators reduced power to approximately 76 percent for planned testing and maintenance. The unit was restored to full power on January 10. On January 17, operators performed a manual scram in response to a turbine runback caused by a loss of stator cooling to the main generator. The unit was restarted on January 18, and reached full power on January 19. Additionally, on February 28, operators reduced power to approximately 81 percent to repair a condenser tube leak. The unit was restored to full power on March 1. On March 23, the unit entered end-of-cycle coastdown. The unit was operating at approximately 97 percent power at the end of the inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
.............................................................................................................. 4 1R01 Adverse Weather Protection .................................................................................... 4 1R04 Equipment Alignment .............................................................................................. 4 1R05 Fire Protection ......................................................................................................... 5 1R06 Flood Protection Measures ...................................................................................... 6 1R11 Licensed Operator Requalification Program ............................................................ 6 1R12 Maintenance Effectiveness ...................................................................................... 7 1R13 Maintenance Risk Assessments and Emergent Work Control ................................. 7 1R15 Operability Evaluations ............................................................................................ 8 1R18 Plant Modifications .................................................................................................. 8 1R19 Post-Maintenance Testing ....................................................................................... 9 1R22 Surveillance Testing ................................................................................................ 9 1EP2 Alert and Notification System (ANS) Evaluation .................................................... 10 1EP3 Emergency Response Organization (ERO) Staffing and Augmentation System .... 10 1EP4 Emergency Action Level (EAL) and Emergency Plan Changes ............................. 10 1EP5 Correction of Emergency Preparedness Weaknesses ........................................... 11 1EP6 Drill Evaluation
Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness
 
{{a|1R01}}
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01|count=1}}
 
===.1 Evaluate Readiness for Impending Adverse Weather Conditions===
 
====a. Inspection Scope====
The inspectors completed one adverse weather preparation sample. The inspectors reviewed PSEG's preparation activities for river grass intrusion conditions that may impact the station service water system. Inspectors assessed implementation of PSEG's grassing readiness plan through service water system walkdowns, corrective action program review, and discussions with cognizant managers and engineers. Documents reviewed are listed in the Attachment.
 
====b. Findings====
No findings of significance were identified.
{{a|1R04}}
==1R04 Equipment Alignment (71111.04 - 3 samples, 71111.04S - 1 sample)==
 
===.1 Partial Walkdown===
 
====a. Inspection Scope====
The inspectors completed three partial system walkdown inspection samples. For the systems listed below the inspectors verified the operability of redundant or diverse trains and components when the listed safety equipment was unavailable. The inspectors completed walkdowns to determine whether there were discrepancies in the system's alignment that could impact the function of the system, and therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, walked down control system components, and verified that selected breakers, valves, and support 5equipment were in the correct position to support system operation. The inspectors also verified that PSEG had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program. Documents reviewed are listed in the Attachment.
* A emergency diesel generator (EDG) during B EDG maintenance on February 9, 2009
* A, B, and D service water (SW) system with C SW system out of service on March 9, 2009
* B safety auxiliary cooling system (SACS) loop with A SACS loop 2522 C valve maintenance on March 23, 2009
 
===.2 Complete Walkdown===
 
====a. Inspection Scope====
The inspectors completed one complete walkdown inspection of accessible portions of the standby liquid control system. The inspectors used PSEG procedures and other documents listed in the Attachment to verify proper system alignment and functional capability. The inspectors independently verified the alignment and status of standby liquid control system valves, labeling, hangers and supports, and associated support systems. The walkdown also included checks that oil reservoir levels were normal, pump rooms and pipe chases were adequately ventilated, system parameters were within established ranges, and equipment deficiencies were appropriately identified.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R05}}
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05Q|count=6}}
 
===.1 Fire Protection - Tours===
 
====a. Inspection Scope====
The inspectors completed six quarterly fire protection inspection samples. The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that combustibles and ignition sources were controlled in accordance with PSEG's administrative procedures; fire detection and suppression equipment was available for use; that passive fire barriers were maintained in good material condition; and that compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with PSEG's fire plan. The six areas toured are listed below with their associated pre-fire plan designator. Other documents reviewed are listed in the Attachment.
* FRH-II-713, A/C SW Bay
* FRH-II-713, B/D SW Bay
* FRH-II-713, SW Intake Screen Room 6* FRH-II-434, Reactor Building MCC Area
* FRH-II-542, Lower Control Equipment Area
* FRH-II-541, 1E Switchgear 130'
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R06}}
==1R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06|count=1}}
 
====a. Inspection Scope====
The inspectors completed one flood protection measure inspection sample. The inspectors reviewed selected risk-important plant design features and PSEG procedures intended to protect the plant and its safety-related equipment from internal flooding events. Specifically, the inspectors focused on internal flood mitigation features for the 54' elevation of the reactor building that contains significant portions of the core spray, residual heat removal, high pressure coolant injection, reactor core isolation cooling, and reactor building sump systems. The inspectors reviewed flood analysis and design documents, including the Updated Final Safety Analysis Report (UFSAR), engineering calculations, and abnormal operating procedures. The inspectors observed the condition of wall penetrations, watertight doors, flood alarm switches, and drains to assess their readiness to contain flow from an internal flood in accordance with the design basis.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R11}}
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11Q|count=1}}
 
===.1 Requalification Activities Review By Resident Staff===
 
====a. Inspection Scope====
The inspectors observed a licensed operator annual requalification simulator scenario on February 10, 2009, to assess operator performance and training effectiveness. The scenario involved a safety relief valve failing open, a loss of primary condensate pumps, a mode switch failure, a failure of the high pressure coolant injection system to initiate, and event classification. The inspectors verified that control room staff correctly identified and declared emergency action levels in a timely manner. The inspectors assessed simulator fidelity and observed the simulator instructor's critique of operator performance. The inspectors also observed control room activities with emphasis on simulator-identified areas for improvement. Finally, the inspectors reviewed applicable documents associated with licensed operator requalification as listed in the Attachment.
 
====b. Findings====
No findings of significance were identified.
 
71R12 Maintenance Effectiveness (71111.12 - 3 samples)
 
====a. Inspection Scope====
The inspectors completed three maintenance effectiveness inspection samples. For the systems listed below the inspectors evaluated items such as:  appropriate work practices; identifying and addressing common cause failures; scoping in accordance with 10 CFR 50.65(b) of the maintenance rule (MR); characterizing reliability issues for performance; trending key parameters for condition monitoring; charging unavailability for performance; classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2); and appropriateness of performance criteria for structures, systems, and components (SSCs) functions classified as (a)(2) and/or appropriateness and adequacy of goals and corrective actions for SSCs/functions classified as (a)(1). Documents reviewed are listed in the Attachment.
* Feedwater system
* High pressure coolant injection (HPCI) pump
* Service water pumps
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13|count=4}}
 
====a. Inspection Scope====
The inspectors completed four maintenance risk assessment and emergent work control inspection samples. The inspectors reviewed on-line risk management evaluations through direct observation and document reviews for the following four configurations:
* A control rod drive pump and C SACS pump out of service on January 6, 2009;
* B EDG and one offsite line out of service on February 10, 2009;
* C EDG and B reactor building ventilation system out of service on February 3, 2009; and
* B reactor protection system motor generator set and one of two supply breakers for the B 4kV bus out of service on March 10, 2009.
 
The inspectors reviewed the applicable risk evaluations, work schedules and control room logs for these configurations to verify that concurrent planned and emergent maintenance and test activities did not adversely affect the plant risk already incurred with these configurations. PSEG's risk management actions were reviewed during shift turnover meetings, control room tours, and plant walkdowns. The inspectors also used PSEG's on-line risk monitor (Equipment Out-Of-Service workstation) to gain insights into the risk associated with these plant configurations. Finally, the inspectors reviewed notifications documenting problems associated with risk assessments and emergent work evaluations. Documents reviewed are listed in the Attachment.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R15}}
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15|count=6}}
 
====a. Inspection Scope====
The inspectors completed six operability evaluation inspection samples. The inspectors reviewed the operability determinations for degraded or non-conforming conditions associated with:
* Degraded control rods due to channel distortion;
* HPCI booster pump wear particles in oil;
* SW strainer differential pressure increase;
* B EDG jacket water leak;
* Condensate storage tank to torus swapover for high pressure coolant injection/reactor core isolation cooling; and
* EDG fuel oil transfer pump cross-connect flow path.
 
The inspectors reviewed the technical adequacy of the operability determinations to ensure the conclusions were justified. The inspectors also walked down accessible equipment to corroborate the adequacy of PSEG's operability determinations.
 
Additionally, the inspectors reviewed other PSEG identified safety-related equipment deficiencies during this report period and assessed the adequacy of their operability screenings. Documents reviewed are listed in the Attachment.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R18}}
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18|count=1}}
 
===.1 Temporary Modifications===
 
====a. Inspection Scope====
The inspectors completed one plant modification inspection sample. The inspectors reviewed the temporary plant modification package for temporary power feeds from offsite power supply substation #9. This review verified that the design bases, licensing bases, and performance capability of the system was not degraded by the modification. The inspectors verified the new configuration was accurately reflected in the design documentation, and the post-modification testing was adequate to ensure the structures, systems, and components would function properly. The inspectors interviewed plant staff, and reviewed issues that had been entered into the corrective action program to determine whether PSEG had been effective in identifying and resolving problems associated with temporary modifications. The 10 CFR 50.59 evaluation associated with this temporary modification was also reviewed. Documents reviewed are listed in the Attachment.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R19}}
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=6}}
 
====a. Inspection Scope====
The inspectors completed six post-maintenance testing inspection samples. The inspectors reviewed the post-maintenance tests for the maintenance items listed below to verify that test activities confirmed system operability and functional capability following completion of maintenance. The inspectors reviewed applicable test procedures to verify that they tested all safety functions potentially affected by the associated maintenance activities. The inspectors verified that for each potentially affected safety function the acceptance criteria stated in the procedure was consistent with the UFSAR and other design documentation. The inspectors also witnessed completion of the testing or reviewed the completed test results to verify satisfactory restoration of all safety functions affected by the maintenance activities. Documents reviewed are listed in the Attachment.
* A control rod drive pump motor replacement on January 8, 2009
* CD482 inverter card replacement on January 5, 2009
* D EDG SACS cooling water valve 2395 D relay replacement on January 12, 2009
* C EDG scheduled maintenance on March 9, 2009
* B, C, and D EDG day tank level switch calibrations on March 11, 2009
* B control room chiller scheduled maintenance on March 19, 2009
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R22}}
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22|count=6}}
 
====a. Inspection Scope====
The inspectors completed six surveillance testing (ST) inspection samples. The inspectors witnessed performance of and/or reviewed test data for the risk-significant STs listed below to assess whether the SSCs tested satisfied technical specification, UFSAR, and procedure requirements. The inspectors verified that test acceptance criteria were clear, demonstrated operational readiness and were consistent with design documentation; that test instrumentation had current calibrations and the range and accuracy for the application; and that tests were performed, as written, with applicable prerequisites satisfied. Upon ST completion, the inspectors verified that equipment was returned to the status required to perform its safety function. Documents reviewed are listed in the Attachment.
* Nuclear instrumentation intermediate range monitor testing on January 18, 2009
* B EDG monthly operability test on February 11, 2009
* D EDG 24-hour surveillance test on February 18, 2009 10* Control room envelope filtration surveillance test on February 19, 2009
* Reactor core isolation cooling surveillance test on February 19, 2009
* High pressure coolant injection in-service test on February 24, 2009
 
====b. Findings====
No findings of significance were identified.
 
{{a|1EP2}}
==1EP2 Alert and Notification System (ANS) Evaluation==
{{IP sample|IP=IP 71114.02|count=1}}
 
====a. Inspection Scope====
An onsite review was conducted to assess the maintenance and testing of the Salem and Hope Creek ANS. During this inspection, the inspectors interviewed Emergency Preparedness (EP) staff responsible for implementation of the ANS testing and maintenance and reviewed corrective action program notifications pertaining to the ANS for causes, trends, and PSEG's corrective actions. The inspector reviewed the ANS procedures and the ANS design report to ensure PSEG's compliance with system maintenance and testing commitments. The inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment
 
===.02. Planning Standard, 10 CFR 50.47(b) (5) and the related requirements of 10 CFR 50, Appendix E, were used as reference criteria.===
 
====b. Findings====
No findings of significance were identified.
 
1EP3 Emergency Response Organization (ERO) Staffing and Augmentation System (71114.03 - 1 sample)
 
====a. Inspection Scope====
The inspectors conducted a review of Salem/Hope Creeks' ERO augmentation staffing requirements and the process for notifying and augmenting the ERO. This was performed to ensure the readiness of key staff for responding to an event and to ensure timely facility activation. The inspectors reviewed the ERO roster, training records, applicable procedures, drill reports for augmentation, quarterly EP drills and corrective action program notifications related to the ERO staffing augmentation system. The inspectors also reviewed the implementation of the change in the ERO augmentation time from 60 to 90 minutes. The inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment
 
===.03. Planning Standard, 10 CFR 50.47(b)(2) and related requirements of 10 CFR 50, Appendix E, were used as reference criteria.===
 
====b. Findings====
No findings of significance were identified.
 
{{a|1EP4}}
==1EP4 Emergency Action Level (EAL) and Emergency Plan Changes==
{{IP sample|IP=IP 71114.04|count=1}}
 
====a. Inspection Scope====
11Prior to this inspection, the NRC had received and acknowledged changes made to  the Salem/Hope Creek Emergency Plan and its implementing procedures. PSEG developed these changes in accordance with 10 CFR 50.54(q), and determined that the changes did not result in a decrease in effectiveness of the Plan. PSEG also determined that the Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR 50. During this inspection, the inspectors conducted a review of Salem's and Hope Creek's 10 CFR 50.54(q) screenings for all changes made to the EALs, and for a sample of the changes made to the Plan, from May 2008 through March 2009, that could have potentially resulted in a decrease in effectiveness. This review of the EAL, Plan, and EPIP changes did not constitute NRC approval of the changes and, as such, the changes remain subject to future NRC inspection. In addition, the inspectors reviewed notifications written related to this area. The inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment
 
===.04. The requirements in 10 CFR 50.54(q) were used as reference criteria.===
 
====b. Findings====
No findings of significance were identified.
 
{{a|1EP5}}
==1EP5 Correction of Emergency Preparedness Weaknesses==
{{IP sample|IP=IP 71114.05|count=1}}
 
====a. Inspection Scope====
The inspectors reviewed a sampling of self-assessment procedures and reports to assess PSEG
=s ability to evaluate their EP performance and programs. The inspectors reviewed a sampling of notifications written between January 2008 and March 2009 that were initiated by PSEG at Salem and Hope Creek for issues identified during drills, self-assessments and audits. Additionally, the inspectors reviewed:  Nuclear Oversight audits; the event report for the August 2008 Unusual Event declaration at Hope Creek; and, the 2007 and 2008 50.54(t) audit reports. This inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment
 
===.05. Planning Standard, 10 CFR 50.47(b) (14) and the related requirements of 10 CFR 50 Appendix E were used===
 
as reference criteria.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1EP6}}
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06|count=1}}
 
====a. Inspection Scope====
The inspectors completed one drill evaluation inspection sample. The inspectors observed control room operator emergency plan response actions during a licensed operator requalification training scenario on February 10, 2009. The inspectors verified that emergency classification declarations and notifications were completed in accordance with 10 CFR 50.72, 10 CFR 50, Appendix E, and the Hope Creek emergency plan implementing procedures. Documents reviewed for this inspection are listed in the Attachment.
 
====b. Findings====
No findings of significance were identified.


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
............................................................................................................ 12
 
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification ......................................................................... 12 4OA2 Identification and Resolution of Problems .............................................................. 12 4OA3 Event Followup ...................................................................................................... 13 4OA5 Other Activities ...................................................................................................... 13 4OA6 Meetings, Including Exit......................................................................................... 15==
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151|count=6}}
 
====a. Inspection Scope====
The inspectors reviewed PSEG's program for gathering, evaluating and reporting information for the performance indicators (PIs) listed below. The inspectors used the definitions and guidance contained in NEI (Nuclear Energy Institute) 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, to assess the accuracy of PSEG's collection and reporting of PI data. The documents reviewed by the inspectors are listed in the Attachment.
 
===Cornerstone:===
Initiating Events
* Unplanned Scrams per 7000 Critical Hours
* Unplanned Scrams with Complications
* Unplanned Power Changes per 7000 Critical Hours The inspectors reviewed the data reported for these PIs for the period January 1 through December 31, 2008. The records reviewed included PI data summary reports, licensee event reports, monthly operating reports, and operator narrative logs. The inspectors verified the accuracy of the number of critical hours reported, and interviewed the system engineers responsible for data collection and evaluation.
 
===Cornerstone:===
Emergency Preparedness
* Drill and Exercise Performance
* ERO Drill Participation
* ANS Reliability For the PIs listed above, to verify the accuracy of the reported data, the inspectors reviewed the PI data, supporting documentation and the information PSEG reported, from the second quarter through the fourth quarter of 2008
 
====b. Findings====
No findings of significance were identified.
 
{{a|4OA2}}
==4OA2 Identification and Resolution of Problems==
 
(71152)
 
===.1 Review of Items Entered into the Corrective Action Program:===
 
As required by Inspection Procedure 71152, "Identification and Resolution of Problems," and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into 13PSEG's corrective action program. This was accomplished by reviewing the description of each new notification and attending daily management review committee meetings.
 
{{a|4OA3}}
==4OA3 Event Followup==
{{IP sample|IP=IP 71153|count=1}}
 
===.1 (Closed) LER 05000354/2009-001, Reactor Manual Scram Due to Turbine Runback===
 
On January 17, 2009, operators initiated a manual reactor scram in response to a main turbine runback caused by a loss of main generator stator cooling. The loss of stator cooling occurred due to a turbine auxiliary cooling system isolation valve that failed shut. The solenoid for the valve was determined to have a detached lead. This lead had been replaced approximately one week prior to the event. This condition was not caused by a performance deficiency associated with the maintenance activity.
 
The resident inspectors responded to the site and verified that plant systems responded as designed to the transient and operator response was consistent with plant procedures. The inspectors reviewed control board indications, plant logs, computer alarm data, and other post-transient records and data. The inspectors also reviewed PSEG's prompt investigation, apparent cause evaluation, and root cause evaluation for this event.
 
The inspectors reviewed LER 05000354/2009-001 and determined that the direct cause, the solenoid failure, was not within PSEG's ability to foresee and correct, and therefore would not meet the screening criteria for a finding. The inspectors identified no findings of significance and determined there was no violation of NRC requirements. This LER is closed.  
{{a|4OA5}}
==4OA5 Other Activities==
 
===.1 Quarterly Resident Inspector Observations of Security Personnel and Activities===
 
====a. Inspection Scope====
During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with PSEG security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours. These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities.
 
====b. Findings====
No findings of significance were identified.
 
===.2 TI 2515/173, Review of the Implementation of the Industry Ground Water Protection Voluntary Initiative===
 
====a. Inspection Scope====
14On March 9-13, 2009, the inspectors assessed PSEG's ground water protection program to verify that PSEG implemented the voluntary industry Ground Water Protection Initiative (GPI). The GPI was unanimously approved by a formal vote of the Nuclear Energy Institute (NEI) member utility chief nuclear officers. This established the industry's commitment to implement the initiative. The GPI identifies the actions the industry deemed necessary for implementation of a timely and effective ground water protection program.
 
The inspectors verified that the following objectives for the GPI were contained in PSEG's program:
1.1 Site Hydrology and Geology 1.2 Site Risk Management 1.3 On-Site Ground Water Monitoring 1.4 Remediation Process 1.5 Record Keeping 2.1 Stakeholder Briefing 2.2 Voluntary Communication 2.3 Thirty-Day Reports 2.4 Annual Reporting 3.1 Perform a Self-Assessment 3.2 Review the Program Under the Auspices of NEI Unit 2 Emergency Sump The inspectors reviewed documentation and PSEG actions related to the identification of tritium in the Unit 2 emergency sump, located below the 54' elevation in the turbine building. The inspectors discussed with PSEG the testing and reviews conducted to determine the source of the tritium. PSEG's investigation determined that the source of the tritium was condensation from the turbine building administrative area heating ventilation and air conditioning (HVAC) unit, and that the tritium from the condensation came from the Technical Specification/Offsite Dose Calculation Manual authorized effluent releases from the plant vents being drawn into the HVAC intake. The inspectors confirmed that the information developed from PSEG's investigation, including various system testing and data collection, supported this conclusion.
 
The inspectors also reviewed PSEG's investigation efforts and actions taken to determine the cause of frequent makeup of water volume to the condensate storage tank. While investigation is still continuing, PSEG's efforts did provide basis to conclude that there were no leaks to ground water in associated underground piping, valving, or the tank.
 
====b. Findings====
No findings of significance were identified.
 
===.3 Correction to NRC Cross-Cutting Aspect Coding of NRC Finding NCV 05000354/2009006-03, Failure to Follow Procedures Contributes to Emergency Diesel Generator Inoperability===
 
15NRC Inspection Report 05000354/2009006 dated March 16, 2009, documented a Green finding associated with PSEG's failure to follow a surveillance test procedure. The finding had a cross-cutting aspect in the area of human performance and the aspect of work practices, procedural compliance, because PSEG personnel did not follow procedures. However, the finding documentation in Inspection Report 05000354/2009006 contained a typographical error. Specifically, in analysis section for the finding and the summary of findings section for the report the cross-cutting aspect code for this finding was incorrectly listed as H.2(b). The correct cross-cutting aspect code for this finding was H.4(b).
 
===.4 TI 2515/175, Emergency Response Organization, Drill/Exercise Performance Indicator Program Review===
 
The inspectors performed TI 2515/175, ensured the completeness of PSEG's completed Attachment 1 from the TI, and then forwarded the data to NRC, HQ.
 
{{a|4OA6}}
==4OA6 Meetings, Including Exit==
 
The resident inspectors presented the inspection results to Mr. George Barnes and other members of PSEG staff on April 8, 2009. The inspectors verified that proprietary material reviewed by the inspectors during this period was properly controlled and the content of the report includes no proprietary information.
 
ATTACHMENT:   
ATTACHMENT:   


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==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
.................................................................................................. A-1
 
===Licensee Personnel===
: [[contact::G. Barnes]], Site Vice President
: [[contact::B. Booth]], Operations Director
: [[contact::D. Burgin]], Corporate Emergency Preparedness Manager
: [[contact::R. Canziani]], Maintenance Director
: [[contact::E. Casulli]], Shift Operations Superintendent
: [[contact::K. Chambliss]], Assistant Plant Manager 
: [[contact::P. Duca]], Senior Engineer, Regulatory Assurance
: [[contact::K. Knaide]], Engineering Director
: [[contact::M. Gaffney]], Regulatory Assurance Manager 
: [[contact::J. Perry]], Plant Manager
: [[contact::J. Sears]], Chemistry Manager
: [[contact::H. Trimble]], Radiation Protection Manager
 
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
  ....................................................... A-1
 
===Closed===
: [[Closes LER::05000354/LER-2009-001]] LER Reactor Manual Scram Due to Turbine Runback (Section 4OA3.1)
 
===Discussed===
: 05000354/2009006-03  NCV  Failure to Follow Procedures Contributes        to Emergency Diesel Generator        Inoperability (Section 4OA5.3)
 
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
...................................................................................... A-1
In addition to the documents identified in the body of this report, the inspectors reviewed the following documents and records:
==LIST OF ACRONYMS==
: Hope Creek Generating Station (HCGS) Updated Final Safety Analysis Report Technical Specification Action Statement Log (SH.OP-AP.ZZ-108) HCGS NCO Narrative Logs HCGS Plant Status Reports Weekly Reactor Engineering Guidance to Hope Creek Operations Hope Creek Operations Night Orders and Temporary Standing Orders Attachment
: [[......]] [[...................................................................................................... A-9]]
 
: [[3SUMMAR]] [[Y]]
==Section 1R01: Adverse Weather Protection==
: [[OF]] [[]]
 
: [[FINDIN]] [[]]
===Procedures===
GS
: WC-AA-107, Seasonal Readiness, Revision 8 
IR 05000354/2009002; 01/01/2009 - 03/31/2009; Hope Creek Generating Station; Routine
===Notifications===
Integrated Inspection Report. This report covers a three-month period of inspection by resident inspectors and announced
*NRC identified
inspections by regional specialist inspectors. The
: 20319618
: [[NRC]] [['s program for overseeing the safe operation of commercial nuclear power reactors is described in]]
: 20319616
NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
: 20346435
No findings of significance were identified.
: 20329266 *20403377 *20403912 
: [[4REPORT]] [[]]
===Other Documents===
DETAILS  Summary of Plant Status  The Hope Creek Generating Station operated at or near full power for the duration of the
: HWM-08-0013, 2008 Site Winter/Grassing Readiness - Hope Creek Generating Station,
inspection period with the following exceptions. On January 9, operators reduced power to approximately 76 percent for planned testing and maintenance. The unit was restored to full power on January 10. On January 17, operators performed a manual scram in response to a turbine runback caused by a loss of stator cooling to the main generator. The unit was restarted on January 18, and reached full power on January 19. Additionally, on February 28, operators
: 10/31/2008 Hope Creek Winter/Grassing Readiness Report and Weekly Information Update
reduced power to approximately 81 percent to repair a condenser tube leak. The unit was restored to full power on March 1. On March 23, the unit entered end-of-cycle coastdown. The unit was operating at approximately 97 percent power at the end of the inspection period. 1.
 
: [[REACTO]] [[R]]
==Section 1R04: Equipment Alignment==
: [[SAFETY]] [[Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness  1R01 Adverse Weather Protection (71111.01 - 1 sample)  .1 Evaluate Readiness for Impending Adverse Weather Conditions  a. Inspection Scope The inspectors completed one adverse weather preparation sample. The inspectors reviewed]]
 
: [[PS]] [[]]
===Procedures===
: [[EG]] [['s preparation activities for river grass intrusion conditions that may impact the station service water system. Inspectors assessed implementation of]]
: HC.OP-SO.KJ-0001, Emergency Diesel Generators Operation, Revision 46
: [[PS]] [[]]
: HC.OP-SO.EA-0001, Service Water System Operation, Revision 34
EG's grassing readiness plan through service water system walkdowns, corrective action program review, and discussions with cognizant managers and engineers. Documents reviewed are listed in the Attachment. b. Findings  No findings of significance were identified. 1R04 Equipment Alignment (71111.04 - 3 samples, 71111.04S - 1 sample) 
: HC.OP-SO.EG-0001, Safety and Turbine Auxiliaries Cooling Water System Operation, Revision
.1 Partial Walkdown  a. Inspection Scope  The inspectors completed three partial system walkdown inspection samples. For the systems listed below the inspectors verified the operability of redundant or diverse trains and components when the listed safety equipment was unavailable. The inspectors
: HC.OP-IS.BH-0001, Standby Liquid Control Valve Operability Test - Monthly, Revision 42
completed walkdowns to determine whether there were discrepancies in the system's alignment that could impact the function of the system, and therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, walked down control system components, and verified that selected breakers, valves, and support
: HC.OP-IS.BH-0101, Standby Liquid Control System Valves - Inservice Test, Revision 9
5equipment were in the correct position to support system operation. The inspectors also verified that
: HC.OP-ST.BH-0002, Standby Liquid Control Flow Test - 18 Months, Revision 25
: [[PSEG]] [[had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program. Documents reviewed are listed in the Attachment.  * A emergency diesel generator (]]
: HC.OP-SO.BH-0001, Standby Liquid Control System Operation, Revision 10 
: [[EDG]] [[) during B]]
===Drawings===
: [[EDG]] [[maintenance on February 9, 2009 * A, B, and D service water (]]
: M-11-1, Safety Auxiliaries Cooling Reactor Building, Revision 40
: [[SW]] [[) system with C]]
: M-48-1, Standby Liquid Control, Revision 15
: [[SW]] [[system out of service on March 9, 2009 * B safety auxiliary cooling system (]]
 
: [[SACS]] [[) loop with A]]
==Section 1R05: Fire Protection==
: [[SACS]] [[loop 2522 C valve maintenance on March 23, 2009    .2 Complete Walkdown a. Inspection Scope  The inspectors completed one complete walkdown inspection of accessible portions of the standby liquid control system. The inspectors used]]
 
PSEG procedures and other documents listed in the Attachment to verify proper system alignment and functional capability. The inspectors independently verified the alignment and status of standby liquid control system valves, labeling, hangers and supports, and associated support systems. The walkdown also included checks that oil reservoir levels were normal, pump rooms and pipe chases were adequately ventilated, system parameters were
===Procedures===
within established ranges, and equipment deficiencies were appropriately identified. b. Findings  No findings of significance were identified. 1R05 Fire Protection (71111.05Q - 6 samples)  .1 Fire Protection - Tours  a. Inspection Scope  The inspectors completed six quarterly fire protection inspection samples. The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that combustibles
: NC.FP-AP.ZZ-0005, Fire Protection Surveillance and Periodic Test Program, Revision 14
and ignition sources were controlled in accordance with
: NC.FP-AP.ZZ-0025, Operational Fire Protection Program, Revision 7
: [[PSEG]] [['s administrative procedures; fire detection and suppression equipment was available for use; that passive fire barriers were maintained in good material condition; and that compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with]]
: OP-AA-201-009, Control of Transient Combustible Material, Revision 1
PSEG's fire plan. The six areas toured are listed below
: HC.FP-SV.ZZ-0026(F), Flood and Fire Barrier Penetration Seal Inspection, Revision 4
with their associated pre-fire plan designator. Other documents reviewed are listed in the Attachment.  *
: NC.FP-AP.ZZ-0009, Fire Protection Training Program, Revision 5  
: [[FRH]] [[-]]
===Notifications===
: [[II]] [[-713, A/C]]
*NRC-identified
: [[SW]] [[Bay *]]
*20406254 
: [[FRH]] [[-II-713, B/D]]
===Other Documents===
: [[SW]] [[Bay *]]
: FRH-II-541, 1E Switchgear, Revision 7
FRH-II-713, SW Intake Screen Room
: FRH-II-542, Control Equipment Mezzanine Area, Revision 9
6*
: FRH-II-713, Service Water Intake Structure, Revision 4
: [[FRH]] [[-]]
: FRH-II-434, MCC Area, Revision 3
: [[II]] [[-434, Reactor Building]]
: Attachment
: [[MCC]] [[Area *]]
 
: [[FRH]] [[-II-542, Lower Control Equipment Area *]]
==Section 1R06: Flood Protection Measures==
: [[FRH]] [[-]]
 
: [[II]] [[-541, 1E Switchgear 130'  b. Findings  No findings of significance were identified. 1R06 Flood Protection Measures (71111.06 - 1 sample)  a. Inspection Scope  The inspectors completed one flood protection measure inspection sample. The inspectors reviewed selected risk-important plant design features and]]
===Procedures===
: [[PS]] [[]]
: OP-HC-103-102-1005, High Energy and Internal Flooding Barrier Control Program, Revision 0 Drawings A-4641-1, Reactor Building Unit 1 Floor Plan at Elevation 54'
EG procedures intended to protect the plant and its safety-related equipment from internal flooding events. Specifically, the inspectors focused on internal flood mitigation features for the 54' elevation of the reactor building that contains significant portions of the core spray,
: 2-1, Reactor Building Unit 1 Floor Plan at Elevation 77'  
residual heat removal, high pressure coolant injection, reactor core isolation cooling, and reactor building sump systems. The inspectors reviewed flood analysis and design documents, including the Updated Final Safety Analysis Report (UFSAR), engineering calculations, and abnormal operating procedures. The inspectors observed the condition of wall penetrations, watertight doors, flood alarm switches, and drains to assess their readiness to contain flow from an internal flood in accordance with the design basis.
===Other Documents===
b. Findings  No findings of significance were identified.
: Calculation 11-92, Reactor Building Flooding - El. 54' and 77', Revision 5
1R11 Licensed Operator Requalification Program (71111.11Q - 1 sample)  .1 Requalification Activities Review By Resident Staff a. Inspection Scope The inspectors observed a licensed operator annual requalification simulator scenario on February 10, 2009, to assess operator performance and training effectiveness. The scenario involved a safety relief valve failing open, a loss of primary condensate pumps, a mode switch failure, a failure of the high pressure coolant injection system to initiate,
 
and event classification. The inspectors verified that control room staff correctly identified and declared emergency action levels in a timely manner. The inspectors assessed simulator fidelity and observed the simulator instructor's critique of operator performance. The inspectors also observed control room activities with emphasis on simulator-identified areas for improvement. Finally, the inspectors reviewed applicable
==Section 1R11: Licensed Operator Requalification Program==
documents associated with licensed operator requalification as listed in the Attachment. b. Findings  No findings of significance were identified.
 
71R12 Maintenance Effectiveness (71111.12 - 3 samples)  a. Inspection Scope  The inspectors completed three maintenance effectiveness inspection samples. For the systems listed below the inspectors evaluated items such asappropriate work
===Procedures===
practices; identifying and addressing common cause failures; scoping in accordance with
: HC.OP-AB.ZZ-0001, Transient Plant Conditions, Revision 16
: [[10 CFR]] [[50.65(b) of the maintenance rule (]]
: HC.OP-AB.RPV-0006, Safety Relief Valve, Revision 3
MR); characterizing reliability issues for performance; trending key parameters for condition monitoring; charging unavailability for performance; classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2); and appropriateness of performance criteria for structures,
: HC.OP-AB.RPV-0004, Reactor Level Control, Revision 6
systems, and components (SSCs) functions classified as (a)(2) and/or appropriateness and adequacy of goals and corrective actions for
: HC.OP-AB.ZZ-0000, Reactor Scram, Revision 3 
: [[SSC]] [[s/functions classified as (a)(1). Documents reviewed are listed in the Attachment. * Feedwater system * High pressure coolant injection (]]
===Other Documents===
HPCI) pump * Service water pumps    b. Findings  No findings of significance were identified. 1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 4 samples)  a. Inspection Scope  The inspectors completed four maintenance risk assessment and emergent work control inspection samples. The inspectors reviewed on-line risk management evaluations
: Hope Creek Generating Station Emergency Classification Guide Simulator Scenario Guide
through direct observation and document reviews for the following four configurations: * A control rod drive pump and C
: SG-654, SRV fails open / Loss of Primary Condensate Pumps / Mode Switch Failure / Failure of HPCI to Auto-initiate
: [[SACS]] [[pump out of service on January 6, 2009; * B]]
 
: [[EDG]] [[and one offsite line out of service on February 10, 2009; * C]]
==Section 1R12: Maintenance Effectiveness==
: [[EDG]] [[and B reactor building ventilation system out of service on February 3, 2009; and * B reactor protection system motor generator set and one of two supply breakers for the B 4kV bus out of service on March 10, 2009. The inspectors reviewed the applicable risk evaluations, work schedules and control room logs for these configurations to verify that concurrent planned and emergent maintenance and test activities did not adversely affect the plant risk already incurred with these configurations.]]
 
PSEG's risk management actions were reviewed during shift
===Procedures===
turnover meetings, control room tours, and plant walkdowns. The inspectors also used
: HC.OP-AB.COOL-001, Station Service Water, Revision 17
: [[PS]] [[]]
: HC.OP-SO.EA-0001, Service Water System Operation, Revision 34
EG's on-line risk monitor (Equipment Out-Of-Service workstation) to gain insights into the risk associated with these plant configurations. Finally, the inspectors reviewed notifications documenting problems associated with risk assessments and emergent work evaluations. Documents reviewed are listed in the Attachment.
: HC.OP-SO.BJ-0001, High Pressure Coolant Injection Operation, Revision 37
b. Findings  No findings of significance were identified. 1R15 Operability Evaluations (71111.15 - 6 samples)
: WC-AA-101, On-line Work Management Process, Revision 16
a. Inspection Scope  The inspectors completed six operability evaluation inspection samples. The inspectors reviewed the operability determinations for degraded or non-conforming conditions associated with:  * Degraded control rods due to channel distortion; *
: ER-AA-310, Implementation of the Maintenance Rule, Revision 6
: [[HPCI]] [[booster pump wear particles in oil; *]]
: ER-AA-310-1001, Maintenance Rule - Scoping, Revision 3
: [[SW]] [[strainer differential pressure increase; * B]]
: ER-AA-310-1003, Maintenance Rule - Performance Criteria Selection, Revision 3
: [[EDG]] [[jacket water leak; * Condensate storage tank to torus swapover for high pressure coolant injection/reactor core isolation cooling; and *]]
: ER-AA-310-1004, Performance Monitoring, Revision 7 
: [[EDG]] [[fuel oil transfer pump cross-connect flow path. The inspectors reviewed the technical adequacy of the operability determinations to ensure the conclusions were justified. The inspectors also walked down accessible equipment to corroborate the adequacy of]]
===Drawings===
: [[PS]] [[]]
: PN1-E41-C002-0050, Oil Piping Diagram, Revision 0 M-55-1, HPCI P&ID Mech/Cont, Revision 39 
EG's operability determinations.
===Notifications===
Additionally, the inspectors reviewed other
: 20373393
: [[PS]] [[]]
: 20383071
EG identified safety-related equipment deficiencies during this report period and assessed the adequacy of their operability screenings. Documents reviewed are listed in the Attachment. b. Findings    No findings of significance were identified. 1R18 Plant Modifications (71111.18 - 1 sample)  .1 Temporary Modifications
: 20382963
a. Inspection Scope The inspectors completed one plant modification inspection sample. The inspectors reviewed the temporary plant modification package for temporary power feeds from offsite power supply substation #9. This review verified that the design bases, licensing
: 20389013
bases, and performance capability of the system was not degraded by the modification. The inspectors verified the new configuration was accurately reflected in the design documentation, and the post-modification testing was adequate to ensure the structures, systems, and components would function properly. The inspectors interviewed plant staff, and reviewed issues that had been entered into the corrective action program to
: 20356470
determine whether
: 20402660
: [[PSEG]] [[had been effective in identifying and resolving problems associated with temporary modifications. The 10]]
: 20402671
CFR 50.59 evaluation associated with this temporary modification was also reviewed. Documents reviewed are listed in the Attachment.
: 20402908
b. Findings  No findings of significance were identified. 1R19 Post-Maintenance Testing (71111.19 - 6 samples)
: 20402662
a. Inspection Scope  The inspectors completed six post-maintenance testing inspection samples. The inspectors reviewed the post-maintenance tests for the maintenance items listed below to verify that test activities confirmed system operability and functional capability
: 20402661
following completion of maintenance. The inspectors reviewed applicable test procedures to verify that they tested all safety functions potentially affected by the associated maintenance activities. The inspectors verified that for each potentially affected safety function the acceptance criteria stated in the procedure was consistent with the
: 20402653
: [[UFS]] [[]]
: 20401726
AR and other design documentation. The inspectors also witnessed completion of the testing or reviewed the completed test results to verify satisfactory restoration of all safety functions affected by the maintenance activities. Documents
: Orders
reviewed are listed in the Attachment.  * A control rod drive pump motor replacement on January 8, 2009 *
: 70086290
: [[CD]] [[482 inverter card replacement on January 5, 2009 * D]]
: 70070456  
: [[EDG]] [[]]
: Attachment  
: [[SACS]] [[cooling water valve 2395 D relay replacement on January 12, 2009 * C]]
===Other Documents===
: [[EDG]] [[scheduled maintenance on March 9, 2009 * B, C, and D]]
: Hope Creek Maintenance Rule Status and Projections, dated February 5, 2009 Hope Creek SHIP System Summary Report, 4
: [[EDG]] [[day tank level switch calibrations on March 11, 2009 * B control room chiller scheduled maintenance on March 19, 2009    b. Findings  No findings of significance were identified. 1R22 Surveillance Testing (71111.22 - 6 samples)    a. Inspection Scope  The inspectors completed six surveillance testing (]]
th Quarter 2008 System Function Level Maintenance Rule Scoping Information Maintenance Rule System Function and Risk Information
: [[ST]] [[) inspection samples. The inspectors witnessed performance of and/or reviewed test data for the risk-significant]]
 
: [[ST]] [[s listed below to assess whether the]]
==Section 1R13: Maintenance Risk Assessments and Emergent Work Control==
: [[SSC]] [[s tested satisfied technical specification,]]
 
: [[UFS]] [[]]
===Procedures===
AR, and procedure requirements. The inspectors verified that test acceptance
: OP-AA-101-112-1002, On-Line Risk Assessment, Revision 2
criteria were clear, demonstrated operational readiness and were consistent with design documentation; that test instrumentation had current calibrations and the range and accuracy for the application; and that tests were performed, as written, with applicable prerequisites satisfied. Upon ST completion, the inspectors verified that equipment was returned to the status required to perform its safety function. Documents reviewed are
: WC-AA-101, On-Line Work Management Process, Revision 16  
listed in the Attachment. * Nuclear instrumentation intermediate range monitor testing on January 18, 2009 * B
===Notifications===
: [[EDG]] [[monthly operability test on February 11, 2009 * D]]
*NRC-identified
EDG 24-hour surveillance test on February 18, 2009
*20400675
10* Control room envelope filtration surveillance test on February 19, 2009 * Reactor core isolation cooling surveillance test on February 19, 2009 * High pressure coolant injection in-service test on February 24, 2009    b. Findings    No findings of significance were identified.
: 20403118
: [[1EP]] [[2 Alert and Notification System (]]
: Orders 70094278
: [[ANS]] [[) Evaluation (71114.02 - 1 sample)    a. Inspection Scope  An onsite review was conducted to assess the maintenance and testing of the Salem and Hope Creek]]
 
: [[ANS.]] [[During this inspection, the inspectors interviewed Emergency Preparedness (]]
==Section 1R15: Operability Evaluations==
: [[EP]] [[) staff responsible for implementation of the]]
 
: [[ANS]] [[testing and maintenance and reviewed corrective action program notifications pertaining to the]]
===Procedures===
: [[ANS]] [[for causes, trends, and]]
: HC.OP-SO.BJ-0001, High Pressure Coolant Injection Operation, Revision 37
: [[PSEG]] [['s corrective actions. The inspector reviewed the]]
: HC.OP-IS.BJ-0001, HPCI Main and Booster Pump Set - In-service Test, Revision 51
: [[ANS]] [[procedures and the]]
: HC.OP-AR.ZZ-0023, CRIDS Computer Points Book 4, Revision 6
: [[ANS]] [[design report to ensure]]
: HC.OP-AR.ZZ-0022, CRIDS Computer Points Book 3, Revision 5
: [[PSEG]] [['s compliance with system maintenance and testing commitments. The inspection was conducted in accordance with]]
: HC.OP-AR.AP-0001, Condensate and Refuel Storage and Transfer Local Panel, Revision 8
: [[NRC]] [[Inspection Procedure 71114, Attachment .02. Planning Standard, 10]]
: OP-AA-108-115, Operability Determinations, Revision 1
: [[CFR]] [[50.47(b) (5) and the related requirements of]]
: HC.OP-AB.COOL-001, Station Service Water, Revision 17
: [[10 CFR]] [[50, Appendix E, were used as reference criteria. b. Findings  No findings of significance were identified. 1]]
: HC.OP-SO.EA-0001, Service Water System Operation, Revision 34
: [[EP]] [[3 Emergency Response Organization (ERO) Staffing and Augmentation System (71114.03 - 1 sample)    a. Inspection Scope  The inspectors conducted a review of Salem/Hope Creeks']]
: HC.RE-RA.BF-0002, Channel Distortion Testing, Revision 5 
: [[ERO]] [[augmentation staffing requirements and the process for notifying and augmenting the]]
===Calculations===
ERO. This was
: SC-AP-0001, Condensate Storage Tank Low Level Switch to HPCI & Tank 135,000 Gal
performed to ensure the readiness of key staff for responding to an event and to ensure timely facility activation. The inspectors reviewed the
: Reserve, Revision 6
: [[ERO]] [[roster, training records, applicable procedures, drill reports for augmentation, quarterly]]
: SC-AP-0003, Condensate Storage Tank Low Level to RCIC, Revision 7
: [[EP]] [[drills and corrective action program notifications related to the]]
: AP-0004, Condensate Storage Tank Level Set Points - EPU, Revision 7
: [[ERO]] [[staffing augmentation system. The inspectors also reviewed the implementation of the change in the]]
: PN0-E41-4010-0072, High Pressure Coolant Injection, Revision 10 22A6237, High Pressure Coolant Injection 
ERO augmentation
===Drawings===
time from 60 to 90 minutes. The inspection was conducted in accordance with
: M-55-1, HPCI P&ID Mech/Cont, Revision 39 M-30-1, Diesel Engine Auxiliary Systems Fuel Oil, Revision 26  
: [[NRC]] [[Inspection Procedure 71114, Attachment .03. Planning Standard, 10]]
===Notifications===
: [[CFR]] [[50.47(b)(2) and related requirements of]]
*NRC-identified *20405785 *20406260 *20405617 *20407300
: [[10 CFR]] [[50, Appendix E, were used as reference criteria. b. Findings  No findings of significance were identified. 1]]
: 20396692
EP4 Emergency Action Level (EAL) and Emergency Plan Changes (71114.04 - 1 sample)    a. Inspection Scope
: 20198545
11Prior to this inspection, the
: 20400785
: [[NRC]] [[had received and acknowledged changes made to  the Salem/Hope Creek Emergency Plan and its implementing procedures.]]
: 20401222
: [[PSEG]] [[developed these changes in accordance with]]
: 20400174
: [[10 CFR]] [[50.54(q), and determined that the changes did not result in a decrease in effectiveness of the Plan.]]
: 20399809
: [[PSEG]] [[also determined that the Plan continued to meet the requirements of]]
: 20399810
: [[10 CFR]] [[50.47(b) and Appendix E to 10]]
: 20400121
CFR 50. During this inspection, the inspectors conducted a review of
: 20406048
Salem's and Hope Creek's
: 20404376
: [[10 CFR]] [[50.54(q) screenings for all changes made to the]]
: 20399912
: [[EAL]] [[s, and for a sample of the changes made to the Plan, from May 2008 through March 2009, that could have potentially resulted in a decrease in effectiveness. This review of the]]
: 20367624
: [[EAL]] [[, Plan, and]]
: Orders
: [[EPIP]] [[changes did not constitute]]
: 50097446
: [[NRC]] [[approval of the changes and, as such, the changes remain subject to future]]
: 50104249
NRC inspection. In addition, the
: 50106733
inspectors reviewed notifications written related to this area. The inspection was conducted in accordance with
: 50093625
: [[NRC]] [[Inspection Procedure 71114, Attachment .04. The requirements in 10]]
: 70093928 
: [[CFR]] [[50.54(q) were used as reference criteria. b. Findings  No findings of significance were identified.]]
: Attachment 
: [[1EP]] [[5 Correction of Emergency Preparedness Weaknesses (71114.05 - 1 sample)    a. Inspection Scope  The inspectors reviewed a sampling of self-assessment procedures and reports to assess]]
===Other Documents===
PSEG=s ability to evaluate their EP performance and programs. The inspectors reviewed a sampling of notifications written between January 2008 and March 2009 that
: Hope Creek Generating Station Human Reliability Analysis, Revision 3 GE/Hitachi 10
were initiated by
: CFR 21 Communication SC08-05, Updated Surveillance Program for Channel - Control Blade Interference Monitoring, Revision 1
: [[PSEG]] [[at Salem and Hope Creek for issues identified during drills, self-assessments and audits. Additionally, the inspectors reviewed: Nuclear Oversight audits; the event report for the August 2008 Unusual Event declaration at Hope Creek; and, the 2007 and 2008 50.54(t) audit reports. This inspection was conducted in accordance with]]
 
: [[NRC]] [[Inspection Procedure 71114, Attachment .05. Planning Standard,]]
==Section 1R18: Plant Modifications==
: [[10 CFR]] [[50.47(b) (14) and the related requirements of 10]]
 
CFR 50 Appendix E were used
===Procedures===
as reference criteria. b. Findings  No findings of significance were identified.
: CC-AA-112, Temporary Configuration Changes, Revision 11
: [[1EP]] [[6 Drill Evaluation (71114.06 - 1 sample)    a. Inspection Scope  The inspectors completed one drill evaluation inspection sample. The inspectors observed control room operator emergency plan response actions during a licensed operator requalification training scenario on February 10, 2009. The inspectors verified that emergency classification declarations and notifications were completed in accordance with 10]]
: CC-AA-112-1001, Temporary Configuration Change Implementation T&RM, Revision 1
CFR 50.72, 10 CFR 50, Appendix E, and the Hope Creek
: LS-AA-104-1001, 50.59 Review Coversheet Form, Revision 2
emergency plan implementing procedures. Documents reviewed for this inspection are listed in the Attachment.
: LS-AA-104-1002, 50.59 Applicability Review Form, Revision 2
2  b. Findings  No findings of significance were identified.
: LS-AA-104-1003, 50.59 Screening Form, Revision 1
4.
: Orders
: [[OTHER]] [[]]
: 80097753
: [[ACTIVI]] [[TIES]]
===Other Documents===
: [[4OA]] [[1 Performance Indicator Verification (71151 - 6 samples)  a. Inspection Scope  The inspectors reviewed]]
: 4HT-09-001, Temporary Power Feeds From Substation #9, Revision 1
PSEG's program for gathering, evaluating and reporting
 
information for the performance indicators (PIs) listed below. The inspectors used the definitions and guidance contained in
==Section 1R19: Post-Maintenance Testing==
: [[NEI]] [[(Nuclear Energy Institute) 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, to assess the accuracy of]]
 
: [[PSEG]] [['s collection and reporting of]]
===Procedures===
: [[PI]] [[data. The documents reviewed by the inspectors are listed in the Attachment. Cornerstone: Initiating Events  * Unplanned Scrams per 7000 Critical Hours * Unplanned Scrams with Complications * Unplanned Power Changes per 7000 Critical Hours  The inspectors reviewed the data reported for these]]
: HC.IC-FT.JE-0003, Emergency Diesel Generator C Day Tank Level Switches, Revision 3
PIs for the period January 1 through
: HC.IC-GP.ZZ-0067, General Instrument Calibration, Revision 13
December 31, 2008. The records reviewed included
: HC.MD-GP.ZZ-0055, Magnetrol Liquid Level Detector P.M. and Calibration, Revision 7
: [[PI]] [[data summary reports, licensee event reports, monthly operating reports, and operator narrative logs. The inspectors verified the accuracy of the number of critical hours reported, and interviewed the system engineers responsible for data collection and evaluation. Cornerstone:  Emergency Preparedness  * Drill and Exercise Performance *]]
: MA-AA-716-012, Post Maintenance Testing, Revision 12
: [[ERO]] [[Drill Participation *]]
: HC.OP-ST.KJ-0003, Emergency Diesel Generator Operability Test - Monthly, Revision 66 
: [[ANS]] [[Reliability  For the]]
===Calculations===
: [[PI]] [[s listed above, to verify the accuracy of the reported data, the inspectors reviewed the]]
: SC-JE-0059, Diesel Fuel Oil Day Tank Level, Revision 6 10855-JE-13, Volume of Diesel Fuel Oil in Diesel Fuel Oil Day Tank at Setpoints, Revision 3 
: [[PI]] [[data, supporting documentation and the information]]
===Drawings===
PSEG reported, from the second quarter through the fourth quarter of 2008 b. Findings  No findings of significance were identified. 4OA2 Identification and Resolution of Problems (71152) 
: PM018Q-0087, Tank 550 Gallon Fuel Oil Day ASME III, 8/31/94 
.1 Review of Items Entered into the Corrective Action Program: As required by Inspection Procedure 71152, "Identification and Resolution of Problems," and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into
===Notifications===
: [[13PSEG]] [['s corrective action program. This was accomplished by reviewing the description of each new notification and attending daily management review committee meetings. 4]]
*NRC-identified
OA3 Event Followup (71153 - 1 sample)  .1 (Closed) LER 05000354/2009-001, Reactor Manual Scram Due to Turbine Runback  On January 17, 2009, operators initiated a manual reactor scram in response to a main turbine runback caused by a loss of main generator stator cooling. The loss of stator cooling occurred due to a turbine auxiliary cooling system isolation valve that failed shut. The solenoid for the valve was determined to have a detached lead. This lead had been
*20404345 *20397661 *20397987
replaced approximately one week prior to the event. This condition was not caused by a performance deficiency associated with the maintenance activity. The resident inspectors responded to the site and verified that plant systems responded as designed to the transient and operator response was consistent with plant procedures. The inspectors reviewed control board indications, plant logs, computer alarm data, and other post-transient records and data. The inspectors also reviewed
*20402772 *20402389 *20407000
: [[PSEG]] [['s prompt investigation, apparent cause evaluation, and root cause evaluation for this event. The inspectors reviewed]]
: 20393065
: [[LER]] [[05000354/2009-001 and determined that the direct cause, the solenoid failure, was not within]]
: 20403928
: [[PS]] [[]]
: 20088715
EG's ability to foresee and correct, and therefore
: 20379530
would not meet the screening criteria for a finding. The inspectors identified no findings of significance and determined there was no violation of
: Orders
: [[NRC]] [[requirements. This]]
: 30134833
LER is closed. 4OA5 Other Activities  .1 Quarterly Resident Inspector Observations of Security Personnel and Activities  a. Inspection Scope  During the inspection period, the inspectors conducted observations of security force
: 50120642
personnel and activities to ensure that the activities were consistent with
: 70035038
: [[PS]] [[]]
: 60078265
EG security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours. These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an
: 60080169
integral part of the inspectors' normal plant status review and inspection activities. b. Findings  No findings of significance were identified.  .2 TI 2515/173, Review of the Implementation of the Industry Ground Water Protection Voluntary Initiative    a. Inspection Scope
: 60080750
14On March 9-13, 2009, the inspectors assessed
: 70093493
: [[PSEG]] [['s ground water protection program to verify that]]
: 70091844 50120642
: [[PSEG]] [[implemented the voluntary industry Ground Water Protection Initiative (GPI). The]]
 
: [[GPI]] [[was unanimously approved by a formal vote of the Nuclear Energy Institute (]]
==Section 1R22: Surveillance Testing==
NEI) member utility chief nuclear officers. This established the industry's commitment to implement the initiative. The GPI identifies the actions the industry deemed necessary for implementation of a timely and effective ground water
 
protection program. The inspectors verified that the following objectives for the
===Procedures===
: [[GPI]] [[were contained in]]
: OP-HC-103-102-1005, High Energy and Internal Flooding Barrier Control Program, Revision 0
PSEG's program: 1.1 Site Hydrology and Geology 1.2 Site Risk Management 1.3 On-Site Ground Water Monitoring 1.4 Remediation Process 1.5 Record Keeping 2.1 Stakeholder Briefing 2.2 Voluntary Communication
: Completed Surveillances
2.3 Thirty-Day Reports 2.4 Annual Reporting 3.1 Perform a Self-Assessment 3.2 Review the Program Under the Auspices of
: HC.IC-FT.SE-0006, Nuclear Instrumentation Intermediate Range Monitor Test, 1/19/09
: [[NEI]] [[Unit 2 Emergency Sump  The inspectors reviewed documentation and]]
: HC.OP-ST.KJ-0002, Emergency Diesel Generator 1BG400 Operability Test, 2/11/09 
: [[PSEG]] [[actions related to the identification of tritium in the Unit 2 emergency sump, located below the 54' elevation in the turbine building. The inspectors discussed with]]
: Attachment
: [[PS]] [[]]
: HC.OP-IS.BJ-0001, HPCI Main and Booster Pump Set - In-service Test, 2/24/09
EG the testing and reviews conducted to
: HC.OP-ST.KJ.0017, Emergency Diesel Generator 1DG400 - 24 Hour Operability Run and Hot
determine the source of the tritium.
: Restart Test, 2/18/09
: [[PSEG]] [['s investigation determined that the source of the tritium was condensation from the turbine building administrative area heating ventilation and air conditioning (]]
: HC.OP-IS.BD-0001, Reactor Core Isolation Cooling Pump, 2/19/09
: [[HVAC]] [[) unit, and that the tritium from the condensation came from the Technical Specification/Offsite Dose Calculation Manual authorized effluent releases from the plant vents being drawn into the]]
: HC.OP-ST.GK-0005, Control Room Emergency Air Supply Fan Operability Test, 3/19/09
: [[HV]] [[]]
: Orders
AC intake. The inspectors
: 50120468
confirmed that the information developed from
===Notifications===
: [[PSEG]] [['s investigation, including various system testing and data collection, supported this conclusion. The inspectors also reviewed]]
: 20406899
PSEG's investigation efforts and actions taken to determine the cause of frequent makeup of water volume to the condensate storage
 
tank. While investigation is still continuing,
==Section 1EP2: Alert and Notification System (ANS) Evaluation==
: [[PS]] [[]]
: American Signal Corporation Final
EG's efforts did provide basis to conclude that there were no leaks to ground water in associated underground piping, valving, or the tank. b. Findings  No findings of significance were identified.
: REP-10 Design Review Report, PSEG Salem and Hope Creek Generating Stations
.3 Correction to
: EP-AA-121, Emergency Response Facilities and Equipment Readiness, Revision 0
: [[NRC]] [[Cross-Cutting Aspect Coding of]]
: EP-AA-121-1002, PSEG Alert Notification System (ANS) Program, Revision 0
: [[NRC]] [[Finding NCV 05000354/2009006-03, Failure to Follow Procedures Contributes to Emergency Diesel Generator Inoperability]]
: EP-AA-121-1004, PSEG ANS Corrective Maintenance, Revision 0
: [[15NRC]] [[Inspection Report 05000354/2009006 dated March 16, 2009, documented a Green finding associated with]]
: EP-AA-121-1005, PSEG ANS Preventive Maintenance Program, Revision 1
: [[PSEG]] [['s failure to follow a surveillance test procedure. The finding had a cross-cutting aspect in the area of human performance and the aspect of work practices, procedural compliance, because]]
: EP-AA-121-1006, PSEG ANS Siren Monitoring, Troubleshooting, and Testing, Revision 0 ANS-related Condition Reports, dated January 2008 -
: [[PS]] [[]]
: March 2009
EG personnel did not follow procedures. However, the finding documentation in Inspection Report 05000354/2009006 contained a typographical error. Specifically, in analysis section for
 
the finding and the summary of findings section for the report the cross-cutting aspect code for this finding was incorrectly listed as
==Section 1EP3: Emergency Response Organization (ERO) Staffing and Augmentation System==
: [[H.]] [[2(b). The correct cross-cutting aspect code for this finding was H.4(b).  .4]]
: PSEG Nuclear LLC Emergency Plan, Revision 62
: [[TI]] [[2515/175, Emergency Response Organization, Drill/Exercise Performance Indicator Program Review  The inspectors performed]]
: EP-AA-121-1001, Automated Call-Out System Maintenance
: [[TI]] [[2515/175, ensured the completeness of]]
: NC.EP-AP.ZZ-1011 (Z), Maintenance of Emergency Response Organization, Revision 9 EPIP 204S, Emergency Response Callout/Personnel Recall, Revision 70 EPIP 204H, Emergency Response Callout/Personnel Recall, Revision 70
: [[PSEG]] [['s completed Attachment 1 from the]]
: January Monthly Callout Check (pagers) February Monthly Callout Check (pagers)  
: [[TI]] [[, and then forwarded the data to]]
: ERO Roster ERO Assignment ERO Qualifications
: [[NRC]] [[,]]
 
: [[HQ.]] [[4]]
==Section 1EP4: Emergency Action Level (EAL) and Emergency Plan Changes==
: [[OA]] [[6 Meetings, Including Exit  The resident inspectors presented the inspection results to Mr. George Barnes and other members of]]
: PSEG Nuclear LLC Emergency Plan, Revision 62
: [[PSEG]] [[staff on April 8, 2009. The inspectors verified that proprietary material reviewed by the inspectors during this period was properly controlled and the content of the report includes no proprietary information.]]
: EP-AA-120, Emergency Plan Administration, Revision 0
: [[ATTACH]] [[MENT:]]
: EP-AA-120-1001, 10CFR50.54(q) Change Evaluation, Revision 0
: [[SUPPLE]] [[]]
: EP-AA-120-1003, Emergency Preparedness Document Processing, Revision 0
: [[MENTAL]] [[]]
: EP-AA-120-1005, Emergency Plan and Event Classification Guide Content/Format, Revision 1
: [[INFORM]] [[]]
: EP-AA-124, Inventories and Surveillances, Revision 0
: [[ATION]] [[Attachment]]
: EP-AA-124-1001, Facilities Inventories and Equipment Tests, Revision 0
: [[SUPPLE]] [[]]
: LS-AA-104, Exelon 50.59 Review Process, Revision 5
: [[MENTAL]] [[]]
: LS-AA-104-1000, 50.59 Resource Manual, Revision 4
: [[INFORM]] [[]]
: LS-AA-104-1007, Emergency Plan Guidance for Salem and Hope Creek Stations, Revision 0 Emergency Preparedness 10CFR50.54(q) screenings performed between May 2008 - March
: [[ATION]] [[]]
: 2009 
: [[KEY]] [[]]
: Attachment
: [[POINTS]] [[]]
 
: [[OF]] [[]]
==Section 1EP5: Correction of Emergency Preparedness Weaknesses==
CONTACT
: LS-AA-120, Issue Identification and Screening Process, Revision 8
Licensee Personnel  G. Barnes, Site Vice President B. Booth, Operations Director D. Burgin, Corporate Emergency Preparedness Manager R. Canziani, Maintenance Director
: LS-AA-125, Corrective Action Program (CAP) Procedure, Revision 12
: [[E.]] [[Casulli, Shift Operations Superintendent K. Chambliss, Assistant Plant Manager  P. Duca, Senior Engineer, Regulatory Assurance K. Knaide, Engineering Director M. Gaffney, Regulatory Assurance Manager  J. Perry, Plant Manager J. Sears, Chemistry Manager]]
: EP-AA-122, Drills and Exercises, Revision 0
: [[H.]] [[Trimble, Radiation Protection Manager]]
: EP-AA-122-1001-F10, Drill and Exercise Post Event Critique and Report Development Guidance, Revision 0
: [[LIST]] [[]]
: EP-AA-121-1001, Automated Call-Out System Maintenance, Revision 0 Nuclear Oversight Audits:
: [[OF]] [[]]
: NOSA-HPC-08-02
: [[ITEMS]] [[]]
: NOSA-HPC-07-04
: [[OPENED]] [[,]]
: NOSA-HPC-06-03 Event Follow-up Report for the Hope Creek August 2008 Unusual Event Declaration ERO Common Cause Analysis Report ERO Common Cause Analysis Report, Revision 1
: [[CLOSED]] [[,]]
: Emergency Preparedness Drill Reports, dated January 2008 - March 2009 Emergency Preparedness-related Condition Reports, dated January 2008 - March 2009
: [[AND]] [[]]
 
: [[DISCUS]] [[SED  Closed  05000354/2009-001]]
==Section 1EP6: Drill Evaluation==
: [[LER]] [[Reactor Manual Scram Due to Turbine Runback (Section 4]]
 
OA3.1)
===Procedures===
Discussed  05000354/2009006-03
: HC.OP-AB.ZZ-0001, Transient Plant Conditions, Revision 16
: [[NCV]] [[Failure to Follow Procedures Contributes        to Emergency Diesel Generator        Inoperability (Section 4]]
: HC.OP-AB.RPV-0006, Safety Relief Valve, Revision 3
: [[OA]] [[5.3)]]
: HC.OP-AB.RPV-0004, Reactor Level Control, Revision 6
: [[LIST]] [[]]
: HC.OP-AB.ZZ-0000, Reactor Scram, Revision 3 
: [[OF]] [[]]
===Other Documents===
: [[DOCUME]] [[]]
: Hope Creek Generating Station Emergency Classification Guide
: [[NTS]] [[]]
 
: [[REVIEW]] [[]]
==Section 4OA1: Performance Indicator Verification==
: [[ED]] [[In addition to the documents identified in the body of this report, the inspectors reviewed the following documents and records:  Hope Creek Generating Station (HCGS) Updated Final Safety Analysis Report Technical Specification Action Statement Log (SH.OP-AP.ZZ-108)]]
 
: [[HCGS]] [[]]
===Procedures===
: [[NCO]] [[Narrative Logs]]
: LS-AA-2001, Collecting and Reporting of NRC Performance Indicator Data, Revision 10
: [[HC]] [[]]
: LS-AA-2010, Monthly Data Elements for NRC/WANO Unit/Reactor Shutdown Occurrences,
GS Plant Status Reports
: Revision 6
Weekly Reactor Engineering Guidance to Hope Creek Operations Hope Creek Operations Night Orders and Temporary Standing Orders
: LS-AA-2030, Monthly Data Elements for NRC Unplanned Power Changes per 7000 Critical
Attachment      Section 1R01: Adverse Weather Protection  Procedures
: Hours, Revision 6
: [[WC]] [[-]]
: EP-AA-125-1001, EP Performance Indicator Guidance, Revision 0
AA-107, Seasonal Readiness, Revision 8  Notifications  *NRC identified 20319618 20319616 20346435  20329266 *20403377 *20403912
: DEP PI data, April 2008 - December 2008 ERO Drill Participation PI data, April 2008 - December 2008 ANS Reliability PI data, April 2008 - December 2008 
Other Documents
===Other Documents===
: [[HWM]] [[-08-0013, 2008 Site Winter/Grassing Readiness - Hope Creek Generating Station,  10/31/2008 Hope Creek Winter/Grassing Readiness Report and Weekly Information Update  Section 1R04: Equipment Alignment  Procedures]]
: Hope Creek Integrated Inspection Reports
: [[HC.OP]] [[-SO.KJ-0001, Emergency Diesel Generators Operation, Revision]]
: 2008002 ,
: [[46 HC.OP]] [[-]]
: 2008003,
: [[SO.EA]] [[-0001, Service Water System Operation, Revision]]
: 2008004,
: [[34 HC.OP]] [[-]]
: 2008005 NRC Performance Indicators for 1
: [[SO.EG]] [[-0001, Safety and Turbine Auxiliaries Cooling Water System Operation, Revision]]
st quarter, 2
: [[40 HC.OP]] [[-]]
nd quarter, 3
: [[IS.BH]] [[-0001, Standby Liquid Control Valve Operability Test - Monthly, Revision]]
rd quarter, and 4
: [[42 HC.OP]] [[-]]
th quarter
: [[IS.BH]] [[-0101, Standby Liquid Control System Valves - Inservice Test, Revision]]
: NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5
: [[9 HC.OP]] [[-]]
: [[ST.BH]] [[-0002, Standby Liquid Control Flow Test - 18 Months, Revision]]
: [[25 HC.OP]] [[-]]
SO.BH-0001, Standby Liquid Control System Operation, Revision 10  Drawings M-11-1, Safety Auxiliaries Cooling Reactor Building, Revision 40
M-48-1, Standby Liquid Control, Revision 15  Section 1R05: Fire Protection  Procedures
: [[NC.FP]] [[-]]
: [[AP.ZZ]] [[-0005, Fire Protection Surveillance and Periodic Test Program, Revision]]
: [[14 NC.FP]] [[-]]
: [[AP.ZZ]] [[-0025, Operational Fire Protection Program, Revision 7]]
: [[OP]] [[-]]
: [[AA]] [[-201-009, Control of Transient Combustible Material, Revision]]
: [[1 HC.FP]] [[-]]
: [[SV.ZZ]] [[-0026(F), Flood and Fire Barrier Penetration Seal Inspection, Revision]]
: [[4 NC.FP]] [[-]]
: [[AP.ZZ]] [[-0009, Fire Protection Training Program, Revision 5  Notifications *NRC-identified *20406254  Other Documents]]
: [[FRH]] [[-]]
: [[II]] [[-541, 1E Switchgear, Revision]]
: [[7 FRH]] [[-]]
: [[II]] [[-542, Control Equipment Mezzanine Area, Revision]]
: [[9 FRH]] [[-]]
: [[II]] [[-713, Service Water Intake Structure, Revision]]
: [[4 FRH]] [[-]]
II-434, MCC Area, Revision 3


Attachment    Section 1R06: Flood Protection Measures
==Section 4OA3: Event Followup==
Procedures
: [[OP]] [[-]]
HC-103-102-1005, High Energy and Internal Flooding Barrier Control Program, Revision 0 Drawings A-4641-1, Reactor Building Unit 1 Floor Plan at Elevation 54'
2-1, Reactor Building Unit 1 Floor Plan at Elevation 77'  Other Documents Calculation 11-92, Reactor Building Flooding - El. 54' and 77', Revision 5  Section 1R11: Licensed Operator Requalification Program  Procedures
: [[HC.OP]] [[-]]
: [[AB.ZZ]] [[-0001, Transient Plant Conditions, Revision 16]]
: [[HC.OP]] [[-]]
: [[AB.RPV]] [[-0006, Safety Relief Valve, Revision]]
: [[3 HC.OP]] [[-]]
: [[AB.RPV]] [[-0004, Reactor Level Control, Revision]]
: [[6 HC.OP]] [[-]]
: [[AB.ZZ]] [[-0000, Reactor Scram, Revision 3  Other Documents Hope Creek Generating Station Emergency Classification Guide Simulator Scenario Guide]]
: [[SG]] [[-654,]]
: [[SRV]] [[fails open / Loss of Primary Condensate Pumps / Mode Switch Failure / Failure of]]
: [[HPCI]] [[to Auto-initiate  Section 1R12: Maintenance Effectiveness  Procedures]]
: [[HC.OP]] [[-AB.COOL-001, Station Service Water, Revision]]
: [[17 HC.OP]] [[-]]
: [[SO.EA]] [[-0001, Service Water System Operation, Revision 34]]
: [[HC.OP]] [[-]]
: [[SO.BJ]] [[-0001, High Pressure Coolant Injection Operation, Revision]]
: [[37 WC]] [[-]]
: [[AA]] [[-101, On-line Work Management Process, Revision]]
: [[16 ER]] [[-]]
: [[AA]] [[-310, Implementation of the Maintenance Rule, Revision]]
: [[6 ER]] [[-]]
: [[AA]] [[-310-1001, Maintenance Rule - Scoping, Revision]]
: [[3 ER]] [[-]]
: [[AA]] [[-310-1003, Maintenance Rule - Performance Criteria Selection, Revision 3]]
: [[ER]] [[-]]
: [[AA]] [[-310-1004, Performance Monitoring, Revision 7  Drawings]]
: [[PN]] [[1-E41-C002-0050, Oil Piping Diagram, Revision 0 M-55-1,]]
: [[HPCI]] [[]]
: [[P&]] [[]]
ID Mech/Cont, Revision 39
Notifications 20373393 20383071 20382963 20389013 20356470 20402660 20402671 20402908 20402662 20402661 20402653 20401726
Orders 70086290 70070456 


Attachment    Other Documents Hope Creek Maintenance Rule Status and Projections, dated February 5, 2009 Hope Creek
===Procedures===
: [[SHIP]] [[System Summary Report, 4th Quarter 2008 System Function Level Maintenance Rule Scoping Information Maintenance Rule System Function and Risk Information  Section 1R13: Maintenance Risk Assessments and Emergent Work Control  Procedures]]
: OP-AA-108-114, Post Transient Review, Revision 3  
: [[OP]] [[-AA-101-112-1002, On-Line Risk Assessment, Revision 2]]
: Attachment
: [[WC]] [[-]]
: OP-HC-108-114-1001, Hope Creek Post-Trip Data Collection Guidelines, Revision 2  
AA-101, On-Line Work Management Process, Revision 16 Notifications *NRC-identified *20400675 20403118
===Notifications===
Orders 70094278  Section 1R15: Operability Evaluations  Procedures
: 20398232
: [[HC.OP]] [[-]]
: 20398234
: [[SO.BJ]] [[-0001, High Pressure Coolant Injection Operation, Revision]]
: 20308825
: [[37 HC.OP]] [[-]]
: 20402784
: [[IS.BJ]] [[-0001,]]
: Orders
: [[HPCI]] [[Main and Booster Pump Set - In-service Test, Revision 51]]
: 70093613
: [[HC.OP]] [[-AR.ZZ-0023,]]
: 70064952  
: [[CRIDS]] [[Computer Points Book 4, Revision 6]]
===Other Documents===
: [[HC.OP]] [[-AR.ZZ-0022,]]
: Prompt Investigation for
: [[CRIDS]] [[Computer Points Book 3, Revision 5]]
: 20398232
: [[HC.OP]] [[-AR.AP-0001, Condensate and Refuel Storage and Transfer Local Panel, Revision]]
: LER 05000354/2009001, dated 3/16/2009
: [[8 OP]] [[-]]
: Training diagram 080-01, Safety and Turbine Auxiliaries Cooling System Post-transient alarm data
: [[AA]] [[-108-115, Operability Determinations, Revision]]
: [[1 HC.OP]] [[-]]
: [[AB.COO]] [[L-001, Station Service Water, Revision 17]]
: [[HC.OP]] [[-]]
: [[SO.EA]] [[-0001, Service Water System Operation, Revision]]
: [[34 HC.RE]] [[-]]
: [[RA.BF]] [[-0002, Channel Distortion Testing, Revision 5 Calculations]]
: [[SC]] [[-]]
: [[AP]] [[-0001, Condensate Storage Tank Low Level Switch to]]
: [[HPCI]] [[& Tank 135,000 Gal  Reserve, Revision 6]]
: [[SC]] [[-AP-0003, Condensate Storage Tank Low Level to]]
: [[RCIC]] [[, Revision 7]]
: [[AP]] [[-0004, Condensate Storage Tank Level Set Points -]]
: [[EPU]] [[, Revision 7]]
PN0-E41-4010-0072, High Pressure Coolant Injection, Revision 10 22A6237, High Pressure Coolant Injection
Drawings M-55-1,
: [[HPCI]] [[P&]]
ID Mech/Cont, Revision 39 M-30-1, Diesel Engine Auxiliary Systems Fuel Oil, Revision 26
Notifications *NRC-identified *20405785 *20406260 *20405617 *20407300 20396692 20198545 20400785 20401222 20400174 20399809 20399810 20400121 20406048 20404376 20399912 20367624
Orders 50097446 50104249 50106733 50093625 70093928
Attachment    Other Documents Hope Creek Generating Station Human Reliability Analysis, Revision
: [[3 GE]] [[/Hitachi 10]]
: [[CFR]] [[21 Communication]]
: [[SC]] [[08-05, Updated Surveillance Program for Channel - Control Blade Interference Monitoring, Revision 1    Section 1R18: Plant Modifications Procedures]]
: [[CC]] [[-AA-112, Temporary Configuration Changes, Revision]]
: [[11 CC]] [[-]]
: [[AA]] [[-112-1001, Temporary Configuration Change Implementation]]
: [[T&]] [[]]
: [[RM]] [[, Revision 1]]
: [[LS]] [[-]]
: [[AA]] [[-104-1001, 50.59 Review Coversheet Form, Revision]]
: [[2 LS]] [[-]]
: [[AA]] [[-104-1002, 50.59 Applicability Review Form, Revision]]
: [[2 LS]] [[-]]
: [[AA]] [[-104-1003, 50.59 Screening Form, Revision 1  Orders 80097753  Other Documents]]
: [[4HT]] [[-09-001, Temporary Power Feeds From Substation #9, Revision 1  Section 1R19: Post-Maintenance Testing  Procedures]]
: [[HC.IC]] [[-FT.JE-0003, Emergency Diesel Generator C Day Tank Level Switches, Revision]]
: [[3 HC.IC]] [[-]]
: [[GP.ZZ]] [[-0067, General Instrument Calibration, Revision]]
: [[13 HC.MD]] [[-]]
: [[GP.ZZ]] [[-0055, Magnetrol Liquid Level Detector]]
: [[P.M.]] [[and Calibration, Revision 7]]
: [[MA]] [[-AA-716-012, Post Maintenance Testing, Revision]]
: [[12 HC.OP]] [[-]]
ST.KJ-0003, Emergency Diesel Generator Operability Test - Monthly, Revision 66
Calculations
: [[SC]] [[-]]
: [[JE]] [[-0059, Diesel Fuel Oil Day Tank Level, Revision 6 10855-JE-13, Volume of Diesel Fuel Oil in Diesel Fuel Oil Day Tank at Setpoints, Revision 3 Drawings]]
: [[PM]] [[018Q-0087, Tank 550 Gallon Fuel Oil Day]]
: [[ASME]] [[]]
: [[III]] [[, 8/31/94  Notifications *]]
NRC-identified *20404345 *20397661 *20397987 *20402772 *20402389 *20407000 20393065 20403928 20088715 20379530
Orders 30134833 50120642 70035038 60078265 60080169 60080750 70093493 70091844 50120642  Section 1R22: Surveillance Testing  Procedures
: [[OP]] [[-]]
HC-103-102-1005, High Energy and Internal Flooding Barrier Control Program, Revision 0
Completed Surveillances
: [[HC.IC]] [[-]]
: [[FT.SE]] [[-0006, Nuclear Instrumentation Intermediate Range Monitor Test, 1/19/09]]
: [[HC.OP]] [[-]]
ST.KJ-0002, Emergency Diesel Generator 1BG400 Operability Test, 2/11/09
Attachment
: [[HC.OP]] [[-]]
: [[IS.BJ]] [[-0001,]]
: [[HPCI]] [[Main and Booster Pump Set - In-service Test, 2/24/09]]
: [[HC.OP]] [[-ST.KJ.0017, Emergency Diesel Generator]]
: [[1DG]] [[400 - 24 Hour Operability Run and Hot  Restart Test, 2/18/09]]
: [[HC.OP]] [[-IS.BD-0001, Reactor Core Isolation Cooling Pump, 2/19/09]]
: [[HC.OP]] [[-]]
ST.GK-0005, Control Room Emergency Air Supply Fan Operability Test, 3/19/09
Orders 50120468  Notifications 20406899


Section
==Section 4OA5: Other Activities==
: [[1EP]] [[2:  Alert and Notification System (]]
ANS) Evaluation
American Signal Corporation Final
: [[REP]] [[-10 Design Review Report,]]
: [[PSEG]] [[Salem and Hope Creek Generating Stations]]
: [[EP]] [[-]]
: [[AA]] [[-121, Emergency Response Facilities and Equipment Readiness, Revision]]
: [[0 EP]] [[-]]
: [[AA]] [[-121-1002,]]
: [[PSEG]] [[Alert Notification System (]]
: [[ANS]] [[) Program, Revision 0]]
: [[EP]] [[-]]
: [[AA]] [[-121-1004,]]
: [[PSEG]] [[]]
: [[ANS]] [[Corrective Maintenance, Revision]]
: [[0 EP]] [[-]]
: [[AA]] [[-121-1005,]]
: [[PSEG]] [[]]
: [[ANS]] [[Preventive Maintenance Program, Revision]]
: [[1 EP]] [[-]]
: [[AA]] [[-121-1006,]]
: [[PSEG]] [[]]
: [[ANS]] [[Siren Monitoring, Troubleshooting, and Testing, Revision]]
: [[0 ANS]] [[-related Condition Reports, dated January 2008 -  March 2009  Section 1]]
: [[EP]] [[3:  Emergency Response Organization (ERO) Staffing and Augmentation System]]
: [[PSEG]] [[Nuclear]]
: [[LLC]] [[Emergency Plan, Revision]]
: [[62 EP]] [[-]]
: [[AA]] [[-121-1001, Automated Call-Out System Maintenance]]
: [[NC.EP]] [[-]]
: [[AP.ZZ]] [[-1011 (Z), Maintenance of Emergency Response Organization, Revision]]
: [[9 EPIP]] [[204S, Emergency Response Callout/Personnel Recall, Revision 70]]
: [[EPIP]] [[204H, Emergency Response Callout/Personnel Recall, Revision 70  January Monthly Callout Check (pagers) February Monthly Callout Check (pagers)]]
: [[ERO]] [[Roster]]
: [[ERO]] [[Assignment]]
: [[ERO]] [[Qualifications  Section 1]]
: [[EP]] [[4:  Emergency Action Level (EAL) and Emergency Plan Changes]]
: [[PSEG]] [[Nuclear]]
: [[LLC]] [[Emergency Plan, Revision]]
: [[62 EP]] [[-]]
: [[AA]] [[-120, Emergency Plan Administration, Revision]]
: [[0 EP]] [[-]]
: [[AA]] [[-120-1001,]]
: [[10CFR]] [[50.54(q) Change Evaluation, Revision 0]]
: [[EP]] [[-AA-120-1003, Emergency Preparedness Document Processing, Revision]]
: [[0 EP]] [[-]]
: [[AA]] [[-120-1005, Emergency Plan and Event Classification Guide Content/Format, Revision]]
: [[1 EP]] [[-]]
: [[AA]] [[-124, Inventories and Surveillances, Revision 0]]
: [[EP]] [[-]]
: [[AA]] [[-124-1001, Facilities Inventories and Equipment Tests, Revision]]
: [[0 LS]] [[-]]
: [[AA]] [[-104, Exelon 50.59 Review Process, Revision]]
: [[5 LS]] [[-]]
: [[AA]] [[-104-1000, 50.59 Resource Manual, Revision]]
: [[4 LS]] [[-]]
AA-104-1007, Emergency Plan Guidance for Salem and Hope Creek Stations, Revision 0 Emergency Preparedness 10CFR50.54(q) screenings performed between May 2008 - March
2009
Attachment      Section
: [[1EP]] [[5:  Correction of Emergency Preparedness Weaknesses]]
: [[LS]] [[-AA-120, Issue Identification and Screening Process, Revision]]
: [[8 LS]] [[-]]
: [[AA]] [[-125, Corrective Action Program (CAP) Procedure, Revision]]
: [[12 EP]] [[-]]
: [[AA]] [[-122, Drills and Exercises, Revision 0]]
: [[EP]] [[-]]
: [[AA]] [[-122-1001-F10, Drill and Exercise Post Event Critique and Report Development Guidance, Revision]]
: [[0 EP]] [[-]]
: [[AA]] [[-121-1001, Automated Call-Out System Maintenance, Revision 0 Nuclear Oversight Audits:]]
: [[NOSA]] [[-]]
: [[HPC]] [[-08-02]]
: [[NOSA]] [[-]]
: [[HPC]] [[-07-04]]
: [[NOSA]] [[-]]
: [[HPC]] [[-06-03 Event Follow-up Report for the Hope Creek August 2008 Unusual Event Declaration]]
: [[ERO]] [[Common Cause Analysis Report]]
ERO Common Cause Analysis Report, Revision 1  Emergency Preparedness Drill Reports, dated January 2008 - March 2009 Emergency Preparedness-related Condition Reports, dated January 2008 - March 2009


Section
===Procedures===
: [[1EP]] [[6: Drill Evaluation  Procedures]]
: CY-AA-170-400, Revision 3, Radiological Ground Water Protection Program
: [[HC.OP]] [[-AB.ZZ-0001, Transient Plant Conditions, Revision]]
: ER-AA-5400, Revision 1, Buried Piping Program Guide
: [[16 HC.OP]] [[-]]
: ER-AA-5400-1002, Revision 1, Buried Piping Examination Guide
: [[AB.RPV]] [[-0006, Safety Relief Valve, Revision]]
: SH.RA-IS.ZZ-0109(Q), Revision 4, Storage Tank Integrity Testing
: [[3 HC.OP]] [[-]]
: OP-SH-111-101-1001, Revision 1, Use and Development of Operating Logs
: [[AB.RPV]] [[-0004, Reactor Level Control, Revision 6]]
: LS-AA-125, Revision 12, Corrective Action Program Procedure
: [[HC.OP]] [[-]]
: HC.MD-DG.ZZ-0091(Z), Revision 1, Desktop Guide Leak Management Coordination
: [[AB.ZZ]] [[-0000, Reactor Scram, Revision 3  Other Documents Hope Creek Generating Station Emergency Classification Guide  Section]]
: CY-AA-170-4000, Revision 6, Radiological Ground Water Protection Program Implementation
: [[4OA]] [[1: Performance Indicator Verification  Procedures]]
: CY-AA-170-4160, Revision 1, Station RGPP Controlled Sample Point Parameters
: [[LS]] [[-AA-2001, Collecting and Reporting of NRC Performance Indicator Data, Revision 10]]
: CY-AA-170-000, Revision 3, Radioactive Effluent and Environmental Monitoring Programs
: [[LS]] [[-]]
: RP-AA-228, Revision 0, 10CFR50.75(G) and 10CFR72.30(D) Documentation Requirements
: [[AA]] [[-2010, Monthly Data Elements for]]
: NC.CH-AP.ZZ-8011(Q), Revision 1, Unplanned Radiological Effluent Releases
: [[NRC]] [[/]]
: CY-AA-170-100, Revision 2, Radiological Environmental Monitoring Program
: [[WANO]] [[Unit/Reactor Shutdown Occurrences,  Revision]]
: LA-AA-126-1005, Revision 3, Check-In Self-Assessment   
: [[6 LS]] [[-]]
===Other Documents===
: [[AA]] [[-2030, Monthly Data Elements for]]
: Preliminary Assessment and Site Investigation Work Plan - Hope Creek Generating Station, April 2006 Site Investigation Report, Hope Creek Generating Station, July 2006 Updated Final Safety Analysis Report, Section 2.4 - Hydrology American Nuclear Insurers Nuclear Liability Insurance Inspection - Report L071108.230, Salem/Hope Creek Nuclear Power Plant, July 23, 2008
: [[NRC]] [[Unplanned Power Changes per 7000 Critical  Hours, Revision 6]]
: Memorandum from E. Keating to J. Shelton, March 6, 2009, Subject:
: [[EP]] [[-AA-125-1001, EP Performance Indicator Guidance, Revision 0]]
: NEI 07-07 Objective 2.1.a and 2.1.b Maplewood Testing Services, Work Instruction
: [[DEP]] [[]]
: HBLF-68, Groundwater Sampling Procedure Off-Site Dose Calculation Manual, Revision 22 Check-In Self-Assessment, Tritium Ground Water, SAP Order
: [[PI]] [[data, April 2008 - December]]
: 70087553  
: [[2008 ERO]] [[Drill Participation]]
: Attachment
: [[PI]] [[data, April 2008 - December]]
==LIST OF ACRONYMS==
: [[2008 ANS]] [[Reliability]]
: [[PI]] [[data, April 2008 - December 2008  Other Documents Hope Creek Integrated Inspection Reports 2008002 , 2008003, 2008004,]]
: [[2008005 NRC]] [[Performance Indicators for 1st quarter, 2nd quarter, 3rd quarter, and 4th quarter]]
: [[NEI]] [[99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5  Section]]
: [[4OA]] [[3: Event Followup  Procedures]]
OP-AA-108-114, Post Transient Review, Revision 3
Attachment
: [[OP]] [[-]]
HC-108-114-1001, Hope Creek Post-Trip Data Collection Guidelines, Revision 2  Notifications 20398232 20398234 20308825 20402784  Orders 70093613 70064952  Other Documents Prompt Investigation for 20398232 LER 05000354/2009001, dated 3/16/2009
Training diagram 080-01, Safety and Turbine Auxiliaries Cooling System Post-transient alarm data  Section
: [[4OA]] [[5: Other Activities  Procedures]]
: [[CY]] [[-AA-170-400, Revision 3, Radiological Ground Water Protection Program]]
: [[ER]] [[-]]
: [[AA]] [[-5400, Revision 1, Buried Piping Program Guide]]
: [[ER]] [[-]]
: [[AA]] [[-5400-1002, Revision 1, Buried Piping Examination Guide]]
: [[SH.RA]] [[-]]
: [[IS.ZZ]] [[-0109(Q), Revision 4, Storage Tank Integrity Testing]]
: [[OP]] [[-]]
: [[SH]] [[-111-101-1001, Revision 1, Use and Development of Operating Logs]]
: [[LS]] [[-]]
: [[AA]] [[-125, Revision 12, Corrective Action Program Procedure]]
: [[HC.MD]] [[-]]
: [[DG.ZZ]] [[-0091(Z), Revision 1, Desktop Guide Leak Management Coordination]]
: [[CY]] [[-]]
: [[AA]] [[-170-4000, Revision 6, Radiological Ground Water Protection Program Implementation]]
: [[CY]] [[-]]
: [[AA]] [[-170-4160, Revision 1, Station]]
: [[RGPP]] [[Controlled Sample Point Parameters]]
: [[CY]] [[-AA-170-000, Revision 3, Radioactive Effluent and Environmental Monitoring Programs]]
: [[RP]] [[-]]
: [[AA]] [[-228, Revision 0,]]
: [[10CFR]] [[50.75(G) and 10]]
: [[CFR]] [[72.30(D) Documentation Requirements]]
: [[NC.CH]] [[-]]
: [[AP.ZZ]] [[-8011(Q), Revision 1, Unplanned Radiological Effluent Releases]]
: [[CY]] [[-]]
: [[AA]] [[-170-100, Revision 2, Radiological Environmental Monitoring Program]]
: [[LA]] [[-]]
AA-126-1005, Revision 3, Check-In Self-Assessment  Other Documents Preliminary Assessment and Site Investigation Work Plan - Hope Creek Generating Station, April 2006 Site Investigation Report, Hope Creek Generating Station, July 2006 Updated Final Safety Analysis Report, Section 2.4 - Hydrology
American Nuclear Insurers Nuclear Liability Insurance Inspection - Report L071108.230, Salem/Hope Creek Nuclear Power Plant, July 23, 2008 Memorandum from
: [[E.]] [[Keating to J. Shelton, March 6, 2009, Subject:]]
: [[NEI]] [[07-07 Objective 2.1.a and 2.1.b Maplewood Testing Services, Work Instruction]]
: [[HB]] [[]]
LF-68, Groundwater Sampling Procedure
Off-Site Dose Calculation Manual, Revision 22 Check-In Self-Assessment, Tritium Ground Water, SAP Order 70087553
Attachment
: [[LIST]] [[]]
: [[OF]] [[]]
: [[ACRONY]] [[]]
: [[MS]] [[]]
: [[ANS]] [[Alert and Notification System]]
: [[ANS]] [[Alert and Notification System]]
: [[CFR]] [[Code of Federal Regulations]]
: [[CFR]] [[Code of Federal Regulations]]
Line 648: Line 738:
: [[EP]] [[Emergency Preparedness]]
: [[EP]] [[Emergency Preparedness]]
: [[EPIP]] [[Emergency Plan Implementing Procedure]]
: [[EPIP]] [[Emergency Plan Implementing Procedure]]
: [[ERO]] [[Emergency Response Organization GPI Ground Water Protection Initiative]]
: [[ERO]] [[Emergency Response Organization]]
: [[GPI]] [[Ground Water Protection Initiative]]
: [[HCGS]] [[Hope Creek Generating Station]]
: [[HCGS]] [[Hope Creek Generating Station]]
: [[HPCI]] [[High Pressure Coolant Injection]]
: [[HPCI]] [[High Pressure Coolant Injection]]
Line 654: Line 745:
: [[MCC]] [[Motor Control Center]]
: [[MCC]] [[Motor Control Center]]
: [[MR]] [[Maintenance Rule]]
: [[MR]] [[Maintenance Rule]]
: [[NCV]] [[Non-cited Violation NEI Nuclear Energy Institute]]
: [[NCV]] [[Non-cited Violation]]
: [[NEI]] [[Nuclear Energy Institute]]
: [[NRC]] [[Nuclear Regulatory Commission]]
: [[NRC]] [[Nuclear Regulatory Commission]]
: [[PI]] [[Performance Indicators]]
: [[PI]] [[Performance Indicators]]
: [[PS]] [[Planning Standard]]
: [[PS]] [[Planning Standard]]
: [[PSEG]] [[Public Service Enterprise Group Nuclear]]
: [[PSEG]] [[Public Service Enterprise Group Nuclear]]
Line 664: Line 756:
: [[SSC]] [[Structures, Systems, and Components]]
: [[SSC]] [[Structures, Systems, and Components]]
: [[ST]] [[Surveillance Testing]]
: [[ST]] [[Surveillance Testing]]
: [[SW]] [[Service Water TI Temporary Instruction]]
: [[SW]] [[Service Water]]
: [[UFS]] [[]]
: [[TI]] [[Temporary Instruction]]
: [[AR]] [[Updated Final Safety Analysis Report]]
: [[UFSAR]] [[Updated Final Safety Analysis Report]]
}}
}}

Revision as of 20:33, 26 August 2018

IR 05000354-09-002 on 01/01/09 - 03/31/09 for Hope Creek
ML091170613
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 04/27/2009
From: Burritt A L
Reactor Projects Branch 3
To: Joyce T
Public Service Enterprise Group
burritt al
References
FOIA/PA-2010-0209 IR-09-002
Download: ML091170613 (27)


Text

April 27, 2009

Mr. Thomas Joyce President and Chief Nuclear Officer PSEG Nuclear LLC - N09 P. O. Box 236 Hancocks Bridge, NJ 08038

SUBJECT: HOPE CREEK GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000354/2009002

Dear Mr. Joyce:

On March 31, 2009, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at the Hope Creek Generating Station. The enclosed inspection report documents the inspection results discussed on April 8, 2009, with Mr. George Barnes and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, no findings of significance were identified.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/

Arthur L. Burritt, Chief Projects Branch 3 Division of Reactor Projects Docket No: 50-354 License No: NPF-57

Enclosure:

Inspection Report 05000354/2009002

w/Attachment:

Supplemental Information

SUMMARY OF FINDINGS

IR 05000354/2009002; 01/01/2009 - 03/31/2009; Hope Creek Generating Station; Routine

Integrated Inspection Report.

This report covers a three-month period of inspection by resident inspectors and announced inspections by regional specialist inspectors. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

No findings of significance were identified.

4

REPORT DETAILS

Summary of Plant Status

The Hope Creek Generating Station operated at or near full power for the duration of the inspection period with the following exceptions. On January 9, operators reduced power to approximately 76 percent for planned testing and maintenance. The unit was restored to full power on January 10. On January 17, operators performed a manual scram in response to a turbine runback caused by a loss of stator cooling to the main generator. The unit was restarted on January 18, and reached full power on January 19. Additionally, on February 28, operators reduced power to approximately 81 percent to repair a condenser tube leak. The unit was restored to full power on March 1. On March 23, the unit entered end-of-cycle coastdown. The unit was operating at approximately 97 percent power at the end of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness

1R01 Adverse Weather Protection

.1 Evaluate Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

The inspectors completed one adverse weather preparation sample. The inspectors reviewed PSEG's preparation activities for river grass intrusion conditions that may impact the station service water system. Inspectors assessed implementation of PSEG's grassing readiness plan through service water system walkdowns, corrective action program review, and discussions with cognizant managers and engineers. Documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04 - 3 samples, 71111.04S - 1 sample)

.1 Partial Walkdown

a. Inspection Scope

The inspectors completed three partial system walkdown inspection samples. For the systems listed below the inspectors verified the operability of redundant or diverse trains and components when the listed safety equipment was unavailable. The inspectors completed walkdowns to determine whether there were discrepancies in the system's alignment that could impact the function of the system, and therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, walked down control system components, and verified that selected breakers, valves, and support 5equipment were in the correct position to support system operation. The inspectors also verified that PSEG had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program. Documents reviewed are listed in the Attachment.

  • A, B, and D service water (SW) system with C SW system out of service on March 9, 2009
  • B safety auxiliary cooling system (SACS) loop with A SACS loop 2522 C valve maintenance on March 23, 2009

.2 Complete Walkdown

a. Inspection Scope

The inspectors completed one complete walkdown inspection of accessible portions of the standby liquid control system. The inspectors used PSEG procedures and other documents listed in the Attachment to verify proper system alignment and functional capability. The inspectors independently verified the alignment and status of standby liquid control system valves, labeling, hangers and supports, and associated support systems. The walkdown also included checks that oil reservoir levels were normal, pump rooms and pipe chases were adequately ventilated, system parameters were within established ranges, and equipment deficiencies were appropriately identified.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Fire Protection - Tours

a. Inspection Scope

The inspectors completed six quarterly fire protection inspection samples. The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that combustibles and ignition sources were controlled in accordance with PSEG's administrative procedures; fire detection and suppression equipment was available for use; that passive fire barriers were maintained in good material condition; and that compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with PSEG's fire plan. The six areas toured are listed below with their associated pre-fire plan designator. Other documents reviewed are listed in the Attachment.

  • FRH-II-713, A/C SW Bay
  • FRH-II-713, B/D SW Bay
  • FRH-II-713, SW Intake Screen Room 6* FRH-II-434, Reactor Building MCC Area
  • FRH-II-542, Lower Control Equipment Area
  • FRH-II-541, 1E Switchgear 130'

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors completed one flood protection measure inspection sample. The inspectors reviewed selected risk-important plant design features and PSEG procedures intended to protect the plant and its safety-related equipment from internal flooding events. Specifically, the inspectors focused on internal flood mitigation features for the 54' elevation of the reactor building that contains significant portions of the core spray, residual heat removal, high pressure coolant injection, reactor core isolation cooling, and reactor building sump systems. The inspectors reviewed flood analysis and design documents, including the Updated Final Safety Analysis Report (UFSAR), engineering calculations, and abnormal operating procedures. The inspectors observed the condition of wall penetrations, watertight doors, flood alarm switches, and drains to assess their readiness to contain flow from an internal flood in accordance with the design basis.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1 Requalification Activities Review By Resident Staff

a. Inspection Scope

The inspectors observed a licensed operator annual requalification simulator scenario on February 10, 2009, to assess operator performance and training effectiveness. The scenario involved a safety relief valve failing open, a loss of primary condensate pumps, a mode switch failure, a failure of the high pressure coolant injection system to initiate, and event classification. The inspectors verified that control room staff correctly identified and declared emergency action levels in a timely manner. The inspectors assessed simulator fidelity and observed the simulator instructor's critique of operator performance. The inspectors also observed control room activities with emphasis on simulator-identified areas for improvement. Finally, the inspectors reviewed applicable documents associated with licensed operator requalification as listed in the Attachment.

b. Findings

No findings of significance were identified.

71R12 Maintenance Effectiveness (71111.12 - 3 samples)

a. Inspection Scope

The inspectors completed three maintenance effectiveness inspection samples. For the systems listed below the inspectors evaluated items such as: appropriate work practices; identifying and addressing common cause failures; scoping in accordance with 10 CFR 50.65(b) of the maintenance rule (MR); characterizing reliability issues for performance; trending key parameters for condition monitoring; charging unavailability for performance; classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2); and appropriateness of performance criteria for structures, systems, and components (SSCs) functions classified as (a)(2) and/or appropriateness and adequacy of goals and corrective actions for SSCs/functions classified as (a)(1). Documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors completed four maintenance risk assessment and emergent work control inspection samples. The inspectors reviewed on-line risk management evaluations through direct observation and document reviews for the following four configurations:

  • A control rod drive pump and C SACS pump out of service on January 6, 2009;
  • B EDG and one offsite line out of service on February 10, 2009;

The inspectors reviewed the applicable risk evaluations, work schedules and control room logs for these configurations to verify that concurrent planned and emergent maintenance and test activities did not adversely affect the plant risk already incurred with these configurations. PSEG's risk management actions were reviewed during shift turnover meetings, control room tours, and plant walkdowns. The inspectors also used PSEG's on-line risk monitor (Equipment Out-Of-Service workstation) to gain insights into the risk associated with these plant configurations. Finally, the inspectors reviewed notifications documenting problems associated with risk assessments and emergent work evaluations. Documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors completed six operability evaluation inspection samples. The inspectors reviewed the operability determinations for degraded or non-conforming conditions associated with:

  • HPCI booster pump wear particles in oil;
  • SW strainer differential pressure increase;
  • B EDG jacket water leak;
  • Condensate storage tank to torus swapover for high pressure coolant injection/reactor core isolation cooling; and
  • EDG fuel oil transfer pump cross-connect flow path.

The inspectors reviewed the technical adequacy of the operability determinations to ensure the conclusions were justified. The inspectors also walked down accessible equipment to corroborate the adequacy of PSEG's operability determinations.

Additionally, the inspectors reviewed other PSEG identified safety-related equipment deficiencies during this report period and assessed the adequacy of their operability screenings. Documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R18 Plant Modifications

.1 Temporary Modifications

a. Inspection Scope

The inspectors completed one plant modification inspection sample. The inspectors reviewed the temporary plant modification package for temporary power feeds from offsite power supply substation #9. This review verified that the design bases, licensing bases, and performance capability of the system was not degraded by the modification. The inspectors verified the new configuration was accurately reflected in the design documentation, and the post-modification testing was adequate to ensure the structures, systems, and components would function properly. The inspectors interviewed plant staff, and reviewed issues that had been entered into the corrective action program to determine whether PSEG had been effective in identifying and resolving problems associated with temporary modifications. The 10 CFR 50.59 evaluation associated with this temporary modification was also reviewed. Documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors completed six post-maintenance testing inspection samples. The inspectors reviewed the post-maintenance tests for the maintenance items listed below to verify that test activities confirmed system operability and functional capability following completion of maintenance. The inspectors reviewed applicable test procedures to verify that they tested all safety functions potentially affected by the associated maintenance activities. The inspectors verified that for each potentially affected safety function the acceptance criteria stated in the procedure was consistent with the UFSAR and other design documentation. The inspectors also witnessed completion of the testing or reviewed the completed test results to verify satisfactory restoration of all safety functions affected by the maintenance activities. Documents reviewed are listed in the Attachment.

  • A control rod drive pump motor replacement on January 8, 2009
  • CD482 inverter card replacement on January 5, 2009
  • D EDG SACS cooling water valve 2395 D relay replacement on January 12, 2009
  • C EDG scheduled maintenance on March 9, 2009
  • B, C, and D EDG day tank level switch calibrations on March 11, 2009
  • B control room chiller scheduled maintenance on March 19, 2009

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors completed six surveillance testing (ST) inspection samples. The inspectors witnessed performance of and/or reviewed test data for the risk-significant STs listed below to assess whether the SSCs tested satisfied technical specification, UFSAR, and procedure requirements. The inspectors verified that test acceptance criteria were clear, demonstrated operational readiness and were consistent with design documentation; that test instrumentation had current calibrations and the range and accuracy for the application; and that tests were performed, as written, with applicable prerequisites satisfied. Upon ST completion, the inspectors verified that equipment was returned to the status required to perform its safety function. Documents reviewed are listed in the Attachment.

  • B EDG monthly operability test on February 11, 2009
  • D EDG 24-hour surveillance test on February 18, 2009 10* Control room envelope filtration surveillance test on February 19, 2009

b. Findings

No findings of significance were identified.

1EP2 Alert and Notification System (ANS) Evaluation

a. Inspection Scope

An onsite review was conducted to assess the maintenance and testing of the Salem and Hope Creek ANS. During this inspection, the inspectors interviewed Emergency Preparedness (EP) staff responsible for implementation of the ANS testing and maintenance and reviewed corrective action program notifications pertaining to the ANS for causes, trends, and PSEG's corrective actions. The inspector reviewed the ANS procedures and the ANS design report to ensure PSEG's compliance with system maintenance and testing commitments. The inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment

.02. Planning Standard, 10 CFR 50.47(b) (5) and the related requirements of 10 CFR 50, Appendix E, were used as reference criteria.

b. Findings

No findings of significance were identified.

1EP3 Emergency Response Organization (ERO) Staffing and Augmentation System (71114.03 - 1 sample)

a. Inspection Scope

The inspectors conducted a review of Salem/Hope Creeks' ERO augmentation staffing requirements and the process for notifying and augmenting the ERO. This was performed to ensure the readiness of key staff for responding to an event and to ensure timely facility activation. The inspectors reviewed the ERO roster, training records, applicable procedures, drill reports for augmentation, quarterly EP drills and corrective action program notifications related to the ERO staffing augmentation system. The inspectors also reviewed the implementation of the change in the ERO augmentation time from 60 to 90 minutes. The inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment

.03. Planning Standard, 10 CFR 50.47(b)(2) and related requirements of 10 CFR 50, Appendix E, were used as reference criteria.

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level (EAL) and Emergency Plan Changes

a. Inspection Scope

11Prior to this inspection, the NRC had received and acknowledged changes made to the Salem/Hope Creek Emergency Plan and its implementing procedures. PSEG developed these changes in accordance with 10 CFR 50.54(q), and determined that the changes did not result in a decrease in effectiveness of the Plan. PSEG also determined that the Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR 50. During this inspection, the inspectors conducted a review of Salem's and Hope Creek's 10 CFR 50.54(q) screenings for all changes made to the EALs, and for a sample of the changes made to the Plan, from May 2008 through March 2009, that could have potentially resulted in a decrease in effectiveness. This review of the EAL, Plan, and EPIP changes did not constitute NRC approval of the changes and, as such, the changes remain subject to future NRC inspection. In addition, the inspectors reviewed notifications written related to this area. The inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment

.04. The requirements in 10 CFR 50.54(q) were used as reference criteria.

b. Findings

No findings of significance were identified.

1EP5 Correction of Emergency Preparedness Weaknesses

a. Inspection Scope

The inspectors reviewed a sampling of self-assessment procedures and reports to assess PSEG

=s ability to evaluate their EP performance and programs. The inspectors reviewed a sampling of notifications written between January 2008 and March 2009 that were initiated by PSEG at Salem and Hope Creek for issues identified during drills, self-assessments and audits. Additionally, the inspectors reviewed: Nuclear Oversight audits; the event report for the August 2008 Unusual Event declaration at Hope Creek; and, the 2007 and 2008 50.54(t) audit reports. This inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment

.05. Planning Standard, 10 CFR 50.47(b) (14) and the related requirements of 10 CFR 50 Appendix E were used

as reference criteria.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors completed one drill evaluation inspection sample. The inspectors observed control room operator emergency plan response actions during a licensed operator requalification training scenario on February 10, 2009. The inspectors verified that emergency classification declarations and notifications were completed in accordance with 10 CFR 50.72, 10 CFR 50, Appendix E, and the Hope Creek emergency plan implementing procedures. Documents reviewed for this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed PSEG's program for gathering, evaluating and reporting information for the performance indicators (PIs) listed below. The inspectors used the definitions and guidance contained in NEI (Nuclear Energy Institute) 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, to assess the accuracy of PSEG's collection and reporting of PI data. The documents reviewed by the inspectors are listed in the Attachment.

Cornerstone:

Initiating Events

  • Unplanned Scrams per 7000 Critical Hours
  • Unplanned Scrams with Complications
  • Unplanned Power Changes per 7000 Critical Hours The inspectors reviewed the data reported for these PIs for the period January 1 through December 31, 2008. The records reviewed included PI data summary reports, licensee event reports, monthly operating reports, and operator narrative logs. The inspectors verified the accuracy of the number of critical hours reported, and interviewed the system engineers responsible for data collection and evaluation.

Cornerstone:

Emergency Preparedness

  • Drill and Exercise Performance
  • ERO Drill Participation
  • ANS Reliability For the PIs listed above, to verify the accuracy of the reported data, the inspectors reviewed the PI data, supporting documentation and the information PSEG reported, from the second quarter through the fourth quarter of 2008

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

(71152)

.1 Review of Items Entered into the Corrective Action Program:

As required by Inspection Procedure 71152, "Identification and Resolution of Problems," and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into 13PSEG's corrective action program. This was accomplished by reviewing the description of each new notification and attending daily management review committee meetings.

4OA3 Event Followup

.1 (Closed) LER 05000354/2009-001, Reactor Manual Scram Due to Turbine Runback

On January 17, 2009, operators initiated a manual reactor scram in response to a main turbine runback caused by a loss of main generator stator cooling. The loss of stator cooling occurred due to a turbine auxiliary cooling system isolation valve that failed shut. The solenoid for the valve was determined to have a detached lead. This lead had been replaced approximately one week prior to the event. This condition was not caused by a performance deficiency associated with the maintenance activity.

The resident inspectors responded to the site and verified that plant systems responded as designed to the transient and operator response was consistent with plant procedures. The inspectors reviewed control board indications, plant logs, computer alarm data, and other post-transient records and data. The inspectors also reviewed PSEG's prompt investigation, apparent cause evaluation, and root cause evaluation for this event.

The inspectors reviewed LER 05000354/2009-001 and determined that the direct cause, the solenoid failure, was not within PSEG's ability to foresee and correct, and therefore would not meet the screening criteria for a finding. The inspectors identified no findings of significance and determined there was no violation of NRC requirements. This LER is closed.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with PSEG security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours. These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities.

b. Findings

No findings of significance were identified.

.2 TI 2515/173, Review of the Implementation of the Industry Ground Water Protection Voluntary Initiative

a. Inspection Scope

14On March 9-13, 2009, the inspectors assessed PSEG's ground water protection program to verify that PSEG implemented the voluntary industry Ground Water Protection Initiative (GPI). The GPI was unanimously approved by a formal vote of the Nuclear Energy Institute (NEI) member utility chief nuclear officers. This established the industry's commitment to implement the initiative. The GPI identifies the actions the industry deemed necessary for implementation of a timely and effective ground water protection program.

The inspectors verified that the following objectives for the GPI were contained in PSEG's program:

1.1 Site Hydrology and Geology 1.2 Site Risk Management 1.3 On-Site Ground Water Monitoring 1.4 Remediation Process 1.5 Record Keeping 2.1 Stakeholder Briefing 2.2 Voluntary Communication 2.3 Thirty-Day Reports 2.4 Annual Reporting 3.1 Perform a Self-Assessment 3.2 Review the Program Under the Auspices of NEI Unit 2 Emergency Sump The inspectors reviewed documentation and PSEG actions related to the identification of tritium in the Unit 2 emergency sump, located below the 54' elevation in the turbine building. The inspectors discussed with PSEG the testing and reviews conducted to determine the source of the tritium. PSEG's investigation determined that the source of the tritium was condensation from the turbine building administrative area heating ventilation and air conditioning (HVAC) unit, and that the tritium from the condensation came from the Technical Specification/Offsite Dose Calculation Manual authorized effluent releases from the plant vents being drawn into the HVAC intake. The inspectors confirmed that the information developed from PSEG's investigation, including various system testing and data collection, supported this conclusion.

The inspectors also reviewed PSEG's investigation efforts and actions taken to determine the cause of frequent makeup of water volume to the condensate storage tank. While investigation is still continuing, PSEG's efforts did provide basis to conclude that there were no leaks to ground water in associated underground piping, valving, or the tank.

b. Findings

No findings of significance were identified.

.3 Correction to NRC Cross-Cutting Aspect Coding of NRC Finding NCV 05000354/2009006-03, Failure to Follow Procedures Contributes to Emergency Diesel Generator Inoperability

15NRC Inspection Report 05000354/2009006 dated March 16, 2009, documented a Green finding associated with PSEG's failure to follow a surveillance test procedure. The finding had a cross-cutting aspect in the area of human performance and the aspect of work practices, procedural compliance, because PSEG personnel did not follow procedures. However, the finding documentation in Inspection Report 05000354/2009006 contained a typographical error. Specifically, in analysis section for the finding and the summary of findings section for the report the cross-cutting aspect code for this finding was incorrectly listed as H.2(b). The correct cross-cutting aspect code for this finding was H.4(b).

.4 TI 2515/175, Emergency Response Organization, Drill/Exercise Performance Indicator Program Review

The inspectors performed TI 2515/175, ensured the completeness of PSEG's completed Attachment 1 from the TI, and then forwarded the data to NRC, HQ.

4OA6 Meetings, Including Exit

The resident inspectors presented the inspection results to Mr. George Barnes and other members of PSEG staff on April 8, 2009. The inspectors verified that proprietary material reviewed by the inspectors during this period was properly controlled and the content of the report includes no proprietary information.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

G. Barnes, Site Vice President
B. Booth, Operations Director
D. Burgin, Corporate Emergency Preparedness Manager
R. Canziani, Maintenance Director
E. Casulli, Shift Operations Superintendent
K. Chambliss, Assistant Plant Manager
P. Duca, Senior Engineer, Regulatory Assurance
K. Knaide, Engineering Director
M. Gaffney, Regulatory Assurance Manager
J. Perry, Plant Manager
J. Sears, Chemistry Manager
H. Trimble, Radiation Protection Manager

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Closed

05000354/LER-2009-001 LER Reactor Manual Scram Due to Turbine Runback (Section 4OA3.1)

Discussed

05000354/2009006-03 NCV Failure to Follow Procedures Contributes to Emergency Diesel Generator Inoperability (Section 4OA5.3)

LIST OF DOCUMENTS REVIEWED

In addition to the documents identified in the body of this report, the inspectors reviewed the following documents and records:

Hope Creek Generating Station (HCGS) Updated Final Safety Analysis Report Technical Specification Action Statement Log (SH.OP-AP.ZZ-108) HCGS NCO Narrative Logs HCGS Plant Status Reports Weekly Reactor Engineering Guidance to Hope Creek Operations Hope Creek Operations Night Orders and Temporary Standing Orders Attachment

Section 1R01: Adverse Weather Protection

Procedures

WC-AA-107, Seasonal Readiness, Revision 8

Notifications

  • NRC identified
20319618
20319616
20346435
20329266 *20403377 *20403912

Other Documents

HWM-08-0013, 2008 Site Winter/Grassing Readiness - Hope Creek Generating Station,
10/31/2008 Hope Creek Winter/Grassing Readiness Report and Weekly Information Update

Section 1R04: Equipment Alignment

Procedures

HC.OP-SO.KJ-0001, Emergency Diesel Generators Operation, Revision 46
HC.OP-SO.EA-0001, Service Water System Operation, Revision 34
HC.OP-SO.EG-0001, Safety and Turbine Auxiliaries Cooling Water System Operation, Revision
HC.OP-IS.BH-0001, Standby Liquid Control Valve Operability Test - Monthly, Revision 42
HC.OP-IS.BH-0101, Standby Liquid Control System Valves - Inservice Test, Revision 9
HC.OP-ST.BH-0002, Standby Liquid Control Flow Test - 18 Months, Revision 25
HC.OP-SO.BH-0001, Standby Liquid Control System Operation, Revision 10

Drawings

M-11-1, Safety Auxiliaries Cooling Reactor Building, Revision 40
M-48-1, Standby Liquid Control, Revision 15

Section 1R05: Fire Protection

Procedures

NC.FP-AP.ZZ-0005, Fire Protection Surveillance and Periodic Test Program, Revision 14
NC.FP-AP.ZZ-0025, Operational Fire Protection Program, Revision 7
OP-AA-201-009, Control of Transient Combustible Material, Revision 1
HC.FP-SV.ZZ-0026(F), Flood and Fire Barrier Penetration Seal Inspection, Revision 4
NC.FP-AP.ZZ-0009, Fire Protection Training Program, Revision 5

Notifications

  • NRC-identified
  • 20406254

Other Documents

FRH-II-541, 1E Switchgear, Revision 7
FRH-II-542, Control Equipment Mezzanine Area, Revision 9
FRH-II-713, Service Water Intake Structure, Revision 4
FRH-II-434, MCC Area, Revision 3
Attachment

Section 1R06: Flood Protection Measures

Procedures

OP-HC-103-102-1005, High Energy and Internal Flooding Barrier Control Program, Revision 0 Drawings A-4641-1, Reactor Building Unit 1 Floor Plan at Elevation 54'
2-1, Reactor Building Unit 1 Floor Plan at Elevation 77'

Other Documents

Calculation 11-92, Reactor Building Flooding - El. 54' and 77', Revision 5

Section 1R11: Licensed Operator Requalification Program

Procedures

HC.OP-AB.ZZ-0001, Transient Plant Conditions, Revision 16
HC.OP-AB.RPV-0006, Safety Relief Valve, Revision 3
HC.OP-AB.RPV-0004, Reactor Level Control, Revision 6
HC.OP-AB.ZZ-0000, Reactor Scram, Revision 3

Other Documents

Hope Creek Generating Station Emergency Classification Guide Simulator Scenario Guide
SG-654, SRV fails open / Loss of Primary Condensate Pumps / Mode Switch Failure / Failure of HPCI to Auto-initiate

Section 1R12: Maintenance Effectiveness

Procedures

HC.OP-AB.COOL-001, Station Service Water, Revision 17
HC.OP-SO.EA-0001, Service Water System Operation, Revision 34
HC.OP-SO.BJ-0001, High Pressure Coolant Injection Operation, Revision 37
WC-AA-101, On-line Work Management Process, Revision 16
ER-AA-310, Implementation of the Maintenance Rule, Revision 6
ER-AA-310-1001, Maintenance Rule - Scoping, Revision 3
ER-AA-310-1003, Maintenance Rule - Performance Criteria Selection, Revision 3
ER-AA-310-1004, Performance Monitoring, Revision 7

Drawings

PN1-E41-C002-0050, Oil Piping Diagram, Revision 0 M-55-1, HPCI P&ID Mech/Cont, Revision 39

Notifications

20373393
20383071
20382963
20389013
20356470
20402660
20402671
20402908
20402662
20402661
20402653
20401726
Orders
70086290
70070456
Attachment

Other Documents

Hope Creek Maintenance Rule Status and Projections, dated February 5, 2009 Hope Creek SHIP System Summary Report, 4

th Quarter 2008 System Function Level Maintenance Rule Scoping Information Maintenance Rule System Function and Risk Information

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

OP-AA-101-112-1002, On-Line Risk Assessment, Revision 2
WC-AA-101, On-Line Work Management Process, Revision 16

Notifications

  • NRC-identified
  • 20400675
20403118
Orders 70094278

Section 1R15: Operability Evaluations

Procedures

HC.OP-SO.BJ-0001, High Pressure Coolant Injection Operation, Revision 37
HC.OP-IS.BJ-0001, HPCI Main and Booster Pump Set - In-service Test, Revision 51
HC.OP-AR.ZZ-0023, CRIDS Computer Points Book 4, Revision 6
HC.OP-AR.ZZ-0022, CRIDS Computer Points Book 3, Revision 5
HC.OP-AR.AP-0001, Condensate and Refuel Storage and Transfer Local Panel, Revision 8
OP-AA-108-115, Operability Determinations, Revision 1
HC.OP-AB.COOL-001, Station Service Water, Revision 17
HC.OP-SO.EA-0001, Service Water System Operation, Revision 34
HC.RE-RA.BF-0002, Channel Distortion Testing, Revision 5

Calculations

SC-AP-0001, Condensate Storage Tank Low Level Switch to HPCI & Tank 135,000 Gal
Reserve, Revision 6
SC-AP-0003, Condensate Storage Tank Low Level to RCIC, Revision 7
AP-0004, Condensate Storage Tank Level Set Points - EPU, Revision 7
PN0-E41-4010-0072, High Pressure Coolant Injection, Revision 10 22A6237, High Pressure Coolant Injection

Drawings

M-55-1, HPCI P&ID Mech/Cont, Revision 39 M-30-1, Diesel Engine Auxiliary Systems Fuel Oil, Revision 26

Notifications

  • NRC-identified *20405785 *20406260 *20405617 *20407300
20396692
20198545
20400785
20401222
20400174
20399809
20399810
20400121
20406048
20404376
20399912
20367624
Orders
50097446
50104249
50106733
50093625
70093928
Attachment

Other Documents

Hope Creek Generating Station Human Reliability Analysis, Revision 3 GE/Hitachi 10
CFR 21 Communication SC08-05, Updated Surveillance Program for Channel - Control Blade Interference Monitoring, Revision 1

Section 1R18: Plant Modifications

Procedures

CC-AA-112, Temporary Configuration Changes, Revision 11
CC-AA-112-1001, Temporary Configuration Change Implementation T&RM, Revision 1
LS-AA-104-1001, 50.59 Review Coversheet Form, Revision 2
LS-AA-104-1002, 50.59 Applicability Review Form, Revision 2
LS-AA-104-1003, 50.59 Screening Form, Revision 1
Orders
80097753

Other Documents

4HT-09-001, Temporary Power Feeds From Substation #9, Revision 1

Section 1R19: Post-Maintenance Testing

Procedures

HC.IC-FT.JE-0003, Emergency Diesel Generator C Day Tank Level Switches, Revision 3
HC.IC-GP.ZZ-0067, General Instrument Calibration, Revision 13
HC.MD-GP.ZZ-0055, Magnetrol Liquid Level Detector P.M. and Calibration, Revision 7
MA-AA-716-012, Post Maintenance Testing, Revision 12
HC.OP-ST.KJ-0003, Emergency Diesel Generator Operability Test - Monthly, Revision 66

Calculations

SC-JE-0059, Diesel Fuel Oil Day Tank Level, Revision 6 10855-JE-13, Volume of Diesel Fuel Oil in Diesel Fuel Oil Day Tank at Setpoints, Revision 3

Drawings

PM018Q-0087, Tank 550 Gallon Fuel Oil Day ASME III, 8/31/94

Notifications

  • NRC-identified
  • 20404345 *20397661 *20397987
  • 20402772 *20402389 *20407000
20393065
20403928
20088715
20379530
Orders
30134833
50120642
70035038
60078265
60080169
60080750
70093493
70091844 50120642

Section 1R22: Surveillance Testing

Procedures

OP-HC-103-102-1005, High Energy and Internal Flooding Barrier Control Program, Revision 0
Completed Surveillances
HC.IC-FT.SE-0006, Nuclear Instrumentation Intermediate Range Monitor Test, 1/19/09
HC.OP-ST.KJ-0002, Emergency Diesel Generator 1BG400 Operability Test, 2/11/09
Attachment
HC.OP-IS.BJ-0001, HPCI Main and Booster Pump Set - In-service Test, 2/24/09
HC.OP-ST.KJ.0017, Emergency Diesel Generator 1DG400 - 24 Hour Operability Run and Hot
Restart Test, 2/18/09
HC.OP-IS.BD-0001, Reactor Core Isolation Cooling Pump, 2/19/09
HC.OP-ST.GK-0005, Control Room Emergency Air Supply Fan Operability Test, 3/19/09
Orders
50120468

Notifications

20406899

Section 1EP2: Alert and Notification System (ANS) Evaluation

American Signal Corporation Final
REP-10 Design Review Report, PSEG Salem and Hope Creek Generating Stations
EP-AA-121, Emergency Response Facilities and Equipment Readiness, Revision 0
EP-AA-121-1002, PSEG Alert Notification System (ANS) Program, Revision 0
EP-AA-121-1004, PSEG ANS Corrective Maintenance, Revision 0
EP-AA-121-1005, PSEG ANS Preventive Maintenance Program, Revision 1
EP-AA-121-1006, PSEG ANS Siren Monitoring, Troubleshooting, and Testing, Revision 0 ANS-related Condition Reports, dated January 2008 -
March 2009

Section 1EP3: Emergency Response Organization (ERO) Staffing and Augmentation System

PSEG Nuclear LLC Emergency Plan, Revision 62
EP-AA-121-1001, Automated Call-Out System Maintenance
NC.EP-AP.ZZ-1011 (Z), Maintenance of Emergency Response Organization, Revision 9 EPIP 204S, Emergency Response Callout/Personnel Recall, Revision 70 EPIP 204H, Emergency Response Callout/Personnel Recall, Revision 70
January Monthly Callout Check (pagers) February Monthly Callout Check (pagers)
ERO Roster ERO Assignment ERO Qualifications

Section 1EP4: Emergency Action Level (EAL) and Emergency Plan Changes

PSEG Nuclear LLC Emergency Plan, Revision 62
EP-AA-120, Emergency Plan Administration, Revision 0
EP-AA-120-1001, 10CFR50.54(q) Change Evaluation, Revision 0
EP-AA-120-1003, Emergency Preparedness Document Processing, Revision 0
EP-AA-120-1005, Emergency Plan and Event Classification Guide Content/Format, Revision 1
EP-AA-124, Inventories and Surveillances, Revision 0
EP-AA-124-1001, Facilities Inventories and Equipment Tests, Revision 0
LS-AA-104, Exelon 50.59 Review Process, Revision 5
LS-AA-104-1000, 50.59 Resource Manual, Revision 4
LS-AA-104-1007, Emergency Plan Guidance for Salem and Hope Creek Stations, Revision 0 Emergency Preparedness 10CFR50.54(q) screenings performed between May 2008 - March
2009
Attachment

Section 1EP5: Correction of Emergency Preparedness Weaknesses

LS-AA-120, Issue Identification and Screening Process, Revision 8
LS-AA-125, Corrective Action Program (CAP) Procedure, Revision 12
EP-AA-122, Drills and Exercises, Revision 0
EP-AA-122-1001-F10, Drill and Exercise Post Event Critique and Report Development Guidance, Revision 0
EP-AA-121-1001, Automated Call-Out System Maintenance, Revision 0 Nuclear Oversight Audits:
NOSA-HPC-08-02
NOSA-HPC-07-04
NOSA-HPC-06-03 Event Follow-up Report for the Hope Creek August 2008 Unusual Event Declaration ERO Common Cause Analysis Report ERO Common Cause Analysis Report, Revision 1
Emergency Preparedness Drill Reports, dated January 2008 - March 2009 Emergency Preparedness-related Condition Reports, dated January 2008 - March 2009

Section 1EP6: Drill Evaluation

Procedures

HC.OP-AB.ZZ-0001, Transient Plant Conditions, Revision 16
HC.OP-AB.RPV-0006, Safety Relief Valve, Revision 3
HC.OP-AB.RPV-0004, Reactor Level Control, Revision 6
HC.OP-AB.ZZ-0000, Reactor Scram, Revision 3

Other Documents

Hope Creek Generating Station Emergency Classification Guide

Section 4OA1: Performance Indicator Verification

Procedures

LS-AA-2001, Collecting and Reporting of NRC Performance Indicator Data, Revision 10
LS-AA-2010, Monthly Data Elements for NRC/WANO Unit/Reactor Shutdown Occurrences,
Revision 6
LS-AA-2030, Monthly Data Elements for NRC Unplanned Power Changes per 7000 Critical
Hours, Revision 6
EP-AA-125-1001, EP Performance Indicator Guidance, Revision 0
DEP PI data, April 2008 - December 2008 ERO Drill Participation PI data, April 2008 - December 2008 ANS Reliability PI data, April 2008 - December 2008

Other Documents

Hope Creek Integrated Inspection Reports
2008002 ,
2008003,
2008004,
2008005 NRC Performance Indicators for 1

st quarter, 2

nd quarter, 3

rd quarter, and 4

th quarter

NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5

Section 4OA3: Event Followup

Procedures

OP-AA-108-114, Post Transient Review, Revision 3
Attachment
OP-HC-108-114-1001, Hope Creek Post-Trip Data Collection Guidelines, Revision 2

Notifications

20398232
20398234
20308825
20402784
Orders
70093613
70064952

Other Documents

Prompt Investigation for
20398232
LER 05000354/2009001, dated 3/16/2009
Training diagram 080-01, Safety and Turbine Auxiliaries Cooling System Post-transient alarm data

Section 4OA5: Other Activities

Procedures

CY-AA-170-400, Revision 3, Radiological Ground Water Protection Program
ER-AA-5400, Revision 1, Buried Piping Program Guide
ER-AA-5400-1002, Revision 1, Buried Piping Examination Guide
SH.RA-IS.ZZ-0109(Q), Revision 4, Storage Tank Integrity Testing
OP-SH-111-101-1001, Revision 1, Use and Development of Operating Logs
LS-AA-125, Revision 12, Corrective Action Program Procedure
HC.MD-DG.ZZ-0091(Z), Revision 1, Desktop Guide Leak Management Coordination
CY-AA-170-4000, Revision 6, Radiological Ground Water Protection Program Implementation
CY-AA-170-4160, Revision 1, Station RGPP Controlled Sample Point Parameters
CY-AA-170-000, Revision 3, Radioactive Effluent and Environmental Monitoring Programs
RP-AA-228, Revision 0, 10CFR50.75(G) and 10CFR72.30(D) Documentation Requirements
NC.CH-AP.ZZ-8011(Q), Revision 1, Unplanned Radiological Effluent Releases
CY-AA-170-100, Revision 2, Radiological Environmental Monitoring Program
LA-AA-126-1005, Revision 3, Check-In Self-Assessment

Other Documents

Preliminary Assessment and Site Investigation Work Plan - Hope Creek Generating Station, April 2006 Site Investigation Report, Hope Creek Generating Station, July 2006 Updated Final Safety Analysis Report, Section 2.4 - Hydrology American Nuclear Insurers Nuclear Liability Insurance Inspection - Report L071108.230, Salem/Hope Creek Nuclear Power Plant, July 23, 2008
Memorandum from E. Keating to J. Shelton, March 6, 2009, Subject:
NEI 07-07 Objective 2.1.a and 2.1.b Maplewood Testing Services, Work Instruction
HBLF-68, Groundwater Sampling Procedure Off-Site Dose Calculation Manual, Revision 22 Check-In Self-Assessment, Tritium Ground Water, SAP Order
70087553
Attachment

LIST OF ACRONYMS

ANS Alert and Notification System
CFR Code of Federal Regulations
DEP Drill and Exercise Performance
EAL Emergency Action Level
EDG Emergency Diesel Generator
EP Emergency Preparedness
EPIP Emergency Plan Implementing Procedure
ERO Emergency Response Organization
GPI Ground Water Protection Initiative
HCGS Hope Creek Generating Station
HPCI High Pressure Coolant Injection
HVAC Heating Ventilation and Air Conditioning
MCC Motor Control Center
MR Maintenance Rule
NCV Non-cited Violation
NEI Nuclear Energy Institute
NRC Nuclear Regulatory Commission
PI Performance Indicators
PS Planning Standard
PSEG Public Service Enterprise Group Nuclear
LLC [[]]
PSID Pounds per Square Inch Differential
SACS Safety Auxiliaries Cooling System
SSC Structures, Systems, and Components
ST Surveillance Testing
SW Service Water
TI Temporary Instruction
UFSAR Updated Final Safety Analysis Report