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Supplemental Information | Supplemental Information | ||
Distribution via ListServ | Distribution via ListServ | ||
ML17216A345 OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP NAME BBishop BCollins RTaylor SNinh SSeaton RRodriguez /RA FJE/ DATE 7/25/2017 7/17/2017 7/25/2017 7/21/2017 8/4/2017 8/4/2017 OFFICE RII:DRP NAME FEhrhardt DATE 8/4/2017 Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION II Docket Nos.: 50-327, 50-328 License Nos.: DPR-77, DPR-79 | |||
Report Nos.: 05000327/2017009 and 05000328/2017009 Licensee: Tennessee Valley Authority (TVA) | |||
Facility: Sequoyah Nuclear Plant, Units 1 and 2 Location: Sequoyah Access Road Soddy-Daisy, TN 37379 Dates: June 5, 2017 through June 22, 2017 | |||
Inspectors: S. Seaton, Project Engineer, Team Leader R. Taylor, Senior Project Inspector S. Ninh, Senior Project Engineer B. Bishop, Project Engineer B. Collins, Reactor Inspector Approved by: R. Rodriguez, Chief Reactor Projects Branch 7 Division of Reactor Projects | |||
=SUMMARY= | =SUMMARY= |
Revision as of 05:56, 10 May 2018
ML17216A345 | |
Person / Time | |
---|---|
Site: | Sequoyah |
Issue date: | 08/04/2017 |
From: | Reinaldo Rodriguez NRC/RGN-II |
To: | Shea J W Tennessee Valley Authority |
References | |
IR 2017009 | |
Download: ML17216A345 (14) | |
Text
August 4, 2017
Mr. Joseph Vice President, Nuclear Regulatory Affairs and Support Services Tennessee Valley Authority 1101 Market Street, LP 3R-C Chattanooga, TN 37402-2801
SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000327/2017009, 05000328/2017009
Dear Mr. Shea:
On June 22, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution biennial inspection at your Sequoyah Nuclear Plant Units 1 and 2 and discussed the results of this inspection with Mr. Anthony Williams and other members of your staff. The inspection team documented the results of this inspection in the enclosed inspection report.
The NRC inspection team reviewed the plant's corrective action program and the plant's implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the plant was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staff's performance in each of these areas adequately supported nuclear safety.
The team also evaluated the plant's processes for use of industry and NRC operating experience information and the effectiveness of the plant's audits and self-assessments. Based on the samples reviewed, the team determined that your staff's performance in each of these areas adequately supported nuclear safety.
Finally, the team reviewed the plant's programs to establish and maintain a safety-conscious work environment, and interviewed plant personnel to evaluate the effectiveness of these programs. Based on the team's observations and the results of these interviews the team found no evidence of challenges to your organization's safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available. The NRC inspectors did not identify any findings or violations of more than minor significance.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Witholding."
Sincerely,/RA Frank Ehrhardt Acting for/ Reinaldo Rodriguez, Chief Reactor Projects Branch 7 Division of Reactor Projects Docket Nos.: 50-327, 50-328 License Nos.: DPR-77, DPR-79
Enclosure:
IR 05000327/2017009 and 05000328/2017009
w/Attachment:
Supplemental Information
Distribution via ListServ
ML17216A345 OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP NAME BBishop BCollins RTaylor SNinh SSeaton RRodriguez /RA FJE/ DATE 7/25/2017 7/17/2017 7/25/2017 7/21/2017 8/4/2017 8/4/2017 OFFICE RII:DRP NAME FEhrhardt DATE 8/4/2017 Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION II Docket Nos.: 50-327, 50-328 License Nos.: DPR-77, DPR-79
Report Nos.: 05000327/2017009 and 05000328/2017009 Licensee: Tennessee Valley Authority (TVA)
Facility: Sequoyah Nuclear Plant, Units 1 and 2 Location: Sequoyah Access Road Soddy-Daisy, TN 37379 Dates: June 5, 2017 through June 22, 2017
Inspectors: S. Seaton, Project Engineer, Team Leader R. Taylor, Senior Project Inspector S. Ninh, Senior Project Engineer B. Bishop, Project Engineer B. Collins, Reactor Inspector Approved by: R. Rodriguez, Chief Reactor Projects Branch 7 Division of Reactor Projects
SUMMARY
IR 05000327/2017009 and 05000328/2017009; June 5, 2017 - June 22, 2017; Sequoyah Nuclear Plant Units 1 and 2; Biennial Problem Identification and Resolution report.
The inspection was conducted by a senior project inspector, a senior project engineer, two project engineers, and a reactor inspector. No findings were identified. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 6. Identification and Resolution of Problems The inspectors concluded that, in general, problems were properly identified, evaluated, prioritized, and corrected. The licensee was effective at identifying problems and entering them into the corrective action program (CAP) for resolution, as evidenced by the relatively few number of deficiencies identified by external organizations (including the NRC) that had not been previously identified by the licensee, during the review period. Generally, prioritization and evaluation of issues were adequate, formal root cause evaluations for significant problems were adequate, and corrective actions specified for problems were acceptable. Overall, corrective actions developed and implemented for issues were generally effective and implemented in a timely manner.
The inspectors determined that overall, audits and self-assessments were adequate in identifying deficiencies and areas for improvement in the CAP, and appropriate corrective actions were developed to address the issues identified. Operating experience (OE) usage was found to be generally acceptable and integrated into the licensee's processes for performing and managing work and plant operations.
Based on discussions and interviews conducted with plant employees from various departments, the inspectors determined that personnel at the site felt free to raise safety concerns to management and use the CAP to resolve those concerns.
REPORT DETAILS
OTHER ACTIVITIES
4OA2 Problem Identification and Resolution
.1 Assessment of the Corrective Action Program
a. Inspection Scope
The inspectors reviewed the licensee's CAP procedures which described the administrative process for initiating and resolving problems primarily through the use of the problem investigation program. To verify that problems were properly identified, appropriately characterized and entered into the CAP, the inspectors reviewed Nuclear Condition Reports (CRs) that were issued between June 2015 and June 2017, including a detailed review of selected CRs associated with the following risk-significant systems:
the Control Air System, the Heating Ventilation and Air Conditioning (HVAC) System, and the Emergency Diesel Generators. Where possible, the inspectors independently verified that the corrective actions were implemented. The inspectors also reviewed selected common causes and generic concerns associated with root cause evaluations to determine if they had been appropriately addressed. To help ensure that samples were reviewed across all cornerstones of safety identified in the NRC's Reactor Oversight Process (ROP), the inspectors selected a representative number of CRs that were identified and assigned to the major plant departments, including operations, maintenance, engineering, health physics, chemistry, emergency preparedness and security. These CRs were reviewed to assess each department's threshold for identifying and documenting plant problems, thoroughness of evaluations, and adequacy of corrective actions (CAs). The inspectors reviewed selected CRs, verified corrective actions were implemented, and attended meetings where CRs were screened for significance to determine whether the licensee was identifying, accurately characterizing, and entering problems into the CAP at an appropriate threshold.
The inspectors conducted plant walkdowns within the selected systems listed above and other plant areas to assess the material condition and to identify any deficiencies that had not been previously entered into the CAP. The inspectors reviewed CRs, maintenance history, CAs, completed work orders (WOs) for the systems, and reviewed associated system health reports. These reviews were performed to verify that problems were being properly identified, appropriately characterized, and entered into the CAP. Items reviewed generally covered a two-year period; however, in accordance with the inspection procedure, a five-year review was performed for selected systems for age-dependent issues. Control room walkdowns were also performed to assess the main control room (MCR)deficiency list and to ascertain if deficiencies were entered into the CAP and tracked to resolution. Operator workarounds and operator burden screenings were reviewed, and the inspectors verified compensatory measures for deficient equipment which were being implemented in the field.
The inspectors conducted a detailed review selected CRs to assess the adequacy of the root-cause and apparent-cause evaluations of the problems identified. The inspectors reviewed these evaluations against the descriptions of the problem described in the CRs and the guidance in licensee procedures NPG-SPP-22.306, "Level 1 Evaluation,"
Revision 0006 and NPG-SPP-22.305, "Level 2 Evaluation," Revision 0006. The inspectors assessed if the licensee had adequately determined the cause(s) of identified problems, and had adequately addressed operability, reportability, common cause, generic concerns, extent-of-condition, and extent-of-cause. The review also assessed if the licensee had appropriately identified and prioritized corrective actions to prevent recurrence for significant conditions adverse to quality.
The inspectors reviewed selected industry OE items, including NRC generic communications, to verify that they had been appropriately evaluated for applicability and that issues identified through these reviews had been entered into the CAP.
The inspectors reviewed site trend reports, to determine if the licensee effectively trended identified issues and initiated appropriate corrective actions when adverse trends were identified.
The inspectors reviewed licensee audits and self-assessments, including those which focused on problem identification and resolution programs and processes, to verify that findings were entered into the CAP and to verify that these audits and assessments were consistent with the NRC's assessment of the licensee's CAP.
The inspectors attended various plant meetings to observe management oversight functions of the corrective action process. These included Plant Screening Committee meetings and Management Review Committee (MRC) meetings.
Documents reviewed are listed in the Attachment.
b. Assessment Problem Identification The inspectors determined that the licensee was generally effective in identifying problems and entering them into the CAP and there was an appropriately low threshold for entering issues into the CAP. This conclusion was based on a review of the requirements for initiating CRs as described in licensee procedure NPG-SPP-300, "Corrective Action Program," Revision 0008, in addition to management's expectation that employees were encouraged to initiate CRs for any reason. Trending was generally effective in monitoring equipment performance. Site management was actively involved in the CAP and focused appropriate attention on significant plant issues.
Based on reviews and walkdowns of accessible portions of the selected systems, the inspectors determined that system deficiencies were being identified and placed in the CAP.
Problem Prioritization and Evaluation Based on the review of CRs sampled by the inspection team during the onsite period, the inspectors concluded that problems were generally prioritized and evaluated in accordance with the licensee's CAP procedures as described in the CR severity level determination guidance in NPG-SPP-300. Each CR was assigned a priority level at the MRC meeting and adequate consideration was given to system or component operability and associated plant risk.
The inspectors determined that plant personnel had conducted root cause and apparent cause analyses in compliance with the licensee's CAP procedures and assigned cause determinations were appropriate, considering the significance of the issues being evaluated. A variety of formal causal-analysis techniques were used depending on the type and complexity of the issue consistent with procedures.
Effectiveness of Corrective Actions Based on a review of corrective action documents, interviews with licensee staff, and verification of completed corrective actions, the inspectors determined that, overall, corrective actions were timely, commensurate with the safety significance of the issues, and effective, in that conditions adverse to quality were corrected and non-recurring. For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence, in that a review of performance indicators, CRs, and effectiveness reviews demonstrated that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence were sufficient to ensure corrective actions were properly implemented and were effective.
c. Findings
No findings were identified.
.2 Assessment of the Use of Operating Experience
a. Inspection Scope
The inspectors examined the licensee's use of industry OE to assess the effectiveness of the plant. In addition, the inspectors selected OE documents (e.g., NRC generic communications, 10 CFR Part 21 reports, licensee event reports, vendor notifications, and plant internal OE items, etc.) which had been issued since June 2015, to verify whether the licensee had appropriately evaluated each notification for applicability to the Sequoyah Nuclear Plant, and whether issues identified through these reviews were entered into the CAP. Documents reviewed are listed in the Attachment.
b. Assessment Based on a review of selected documentation related to operating experience issues, the inspectors determined that the licensee was generally effective in screening OE for applicability to the plant. Industry OE was evaluated at either the corporate or plant level depending on the source and type of the document. Relevant information was then forwarded to the applicable department for further action or informational purposes.
Operating experience issues requiring action were entered into the CAP for tracking and closure. In addition, OE was included in all root cause evaluations in accordance with licensee procedure NPG-SPP-22.306.
c. Findings
No findings were identified.
.3 Assessment of Self-Assessments and Audits
a. Inspection Scope
The inspectors reviewed audit reports and self-assessment reports, including those which focused on problem identification and resolution, to assess the thoroughness and self-criticism of the licensee's audits and self-assessments, and to verify that problems identified through those activities were appropriately prioritized and entered into the CAP for resolution in accordance with licensee procedure NPG-SPP-22.102, "NPG Self-Assessment and Benchmarking Programs," Rev. 0002.
b. Assessment The inspectors determined that the scopes of assessments and audits were adequate.
Self-assessments were generally detailed and critical, as evidenced by findings consistent with the inspector's independent reviews. The inspectors verified that CRs were created to document all areas for improvement and findings resulting from the self-assessments, and verified that actions had been completed consistent with those recommendations. Generally, the licensee performed evaluations that were technically accurate.
c. Findings
No findings were identified.
.4 Assessment of Safety-Conscious Work Environment
a. Inspection Scope
During the course of the inspection, the inspectors assessed the plant's safety-conscious work environment through review of the plants employee concerns program (ECP) and interviews with various departmental personnel. The inspectors reviewed a sample of ECP issues to verify that concerns were being properly reviewed and identified deficiencies were being resolved and entered into the CAP when appropriate.
b. Assessment Based on the interviews conducted and the CRs reviewed, the inspectors determined that licensee management emphasized the need for all employees to identify and report problems using the appropriate methods established within the administrative programs, including the CAP and ECP. These methods were readily accessible to all employees.
Based on discussions conducted with a sample of plant employees from various departments, the inspectors determined that employees felt free to raise issues, and that management encouraged employees to place issues into the CAP for resolution. The inspectors did not identify any reluctance on the part of the licensee staff to report safety concerns.
c. Findings
No findings were identified.
4OA6 Exit
Exit Meeting Summary
On June 22, 2017, the inspectors presented the inspection results to Mr. A. Williams and other members of the site staff. The inspectors confirmed that all proprietary information examined during the inspection had been returned to the licensee.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- A. Williams, Site Vice President
- B. Basham, Performance Improvement Manager
- M. McBrearty, Site Licensing Manager
- S. Bowman, Site Licensing Engineer
- P. Parashek, Operations Senior Reactor Operator
- M. Randolph, Performance Improvement
- L. Williams, Performance Improvement
LIST OF REPORT ITEMS
Opened and Closed
None
Closed
- None
Discussed
None
LIST OF DOCUMENTS REVIEWED
Procedures
- NPG-SPP-01.16, Condition Report Initiation, Rev. 0000
- NPG-SPP-03.4, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting -
- 10CFR50.65, Rev. 0003
- NPG-SPP-01.7.1, Employee Concerns Program, Rev. 0001
- NPG-SPP-06.2, Preventive Maintenance, Rev. 0011
- NPG-SPP-07.1.4, Work Management Prioritization - On Line, Rev. 0006
- NPG-SPP-09.3, Plant Modifications and Engineering Change Control, Rev. 0024
- NPG-SPP-09.20, Vendor Manual Control, Rev. 0005
- NPG-SPP-09.16.1, System, Component and Program Health, Rev. 0010
- NPG-SPP-22.102, NPG Self-Assessment and Benchmarking Programs, Rev. 0002
- NPG-SPP-22.300, Corrective Action Program, Rev. 0008
- NPG-SPP-22.302, Corrective Action Program Screening, Rev. 0010
- NPG-SPP-22.303, CR Actions, Closures and Approvals, Rev. 0008
- NPG-SPP-22.305, Level 2 Evaluation, Revision 0006
- NPG-SPP-22.306, Level 1 Evaluation, Rev. 0006
- NPG-SPP-22.500, Operating Experience Program, Rev. 0003
- NEDP-8.0, Evaluations for Procurement of Materials, Items, and Services, Rev. 0002
- NEDP-22, Operability Determinations and Functional Evaluations, Rev. 0017
- NEDP-27, Past Operability Evaluations, Rev. 0003
- OPDP-1, Conduct of Operations, Rev. 0038
- OPDP-8, Operability Determination Process and Limiting Conditions for Operation Tracking, Rev. 0023 17-SBE-026-023, Engineering Work Request: Evaluate Acceptability of Debris in the Fire
- Protection Piping, Rev. 1
- M&AI-7.1, Cable Terminations and Repairing Damaged Cables, Rev.33
- 0-PI-FPU-317-299.W, Fire Protection Miscellaneous Inspections, Revision 0044
- TI-4, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting -
- 10CFR50.65, Rev. 0029 OPL273C1626, Cycle 16-4 Plant Status Update (Licensed Operator Training), dated 6/13/16
- OPL273C1636, Cycle 16-5 Plant Status Update (Licensed Operator Training), dated 8/1/16
- OPL273C1707, Cycle 17-2 Plant Status Update (Licensed Operator Training), dated 2/27/17
- SO-16-008, Sequoyah Fire Operations Department Standing Order, Increased Walk-Downs for Fire Areas Potentially Impacted by Trend of Debris in HPFP Non-Draining Sections, dated
- 11/27/2016
- SO-16-103, Sequoyah Operations Department Standing Order, Compensatory Actions for D/G
- Bldg Tornado Vulnerabilities, dated 05/16/2016
Condition Reports
- 1040168
- 1044251
- 1044255
- 1062507
- 1117466
- 1119661
- 1119663
- 1143804
- 1144342
- 1148228
- 1148543
- 1151352
- 1155763
- 1163235
- 1164452
- 1164446
- 1166927
- 1174405
- 1117456
- 1175834
- 1177144
- 1180402
- 1183201
- 1183350
- 1186385
- 1188774
- 214460
- 27479
- 239449
- 1242395
- 1289543
- 29296
- 1034503
- 1034504
- 1036980
- 1039545
- 1041093
- 1044530
- 1052611
- 1053615
- 1058327
- 1058754
- 1064736
- 1084292
- 1084294
- 1086421
- 1089802
- 1093946
- 1105025
- 1107364
- 1108257
- 1108270
- 1109158
- 1109400
- 1111730
- 1112088
- 1114858
- 1117470
- 1149169
- 1150202
- 1157650
- 1159677
- 1162711
- 1170545
- 1170721
- 1171143
- 1171265
- 1171811
- 1172955
- 1178891
- 1179126
- 1181710
- 1182472
- 1183093
- 1198163
- 1198170
- 206136
- 206142
- 206145
- 1206148
- 1222814
- 26511
- 29204
- 29213
- 29221
- 1230505
- 1237160
- 239748
- 239849
- 240993
- 1245204
- 1248045
- 250669
- 251829
- 254414
- 262587
- 1265577
- 1266643
- 271866
- 282928
- 1284205
- 1289625
- 1292997
- 1295662
- 1039485
- 1039545
- 1040168
- 1040619
- 1041370
- 1041787
- 1042155
- 1042919
- 1043817
- 1044831
- 1046074
- 1050108
- 1056760
- 1056796
- 1059220
- 1063266
- 1063399
- 1067941
- 1068000
- 1074991
- 1075135
- 1087006
- 1091218
- 1091675
- 1104481
- 1127022
- 1134056
- 1151732
- 1155285
- 1171371
- 1171811
- 1178891
- 1198155
- 1202710
- 1204345
- 1210565
- 1210595
- 1230951
- 1232336
- 1253437
- 1254414
- 1255707
- 1255800
- 1260873
- 1262322
- 1262323
- 1263606
- 1271796
- 1284668
- 1289929
- 1254101
- 1045080
- 1060847
- 1232494
- 1146638
- 1275616
- 1144824
- 1031280
- 1059536
- 1096404
- 1111677
- 206882
- 212994
- 1143804
- 1167448
- 1181710
- 1076179
- 297498
- 276635
- 292256
- 1289349
- 1281609
- 291042
- 289328
- 1110460
- 1115030
- 1101732
- 1085879
- 1085848
- 20225
- 1116316
- 1115221
- 1093348
- 1100725
- 1102444
- 1098901
- 1174406
- 1135308
- 1103389
- 1016839
- 1070076
- 1117468
- 1085005
- 1082712
- 1103382
- 1083349
- 1149872
- 1155352
- 1074347
- 1063258
- 1095026
Condition Reports
- Generated
- 1305227, Develop and submit a licensing amendment request to NRC to remove kirk key interlock from 480 V ERCW MCC breakers
- 1306151, Evaluate need for more clear guidance for documenting Operations Management periodic review of operator workarounds, burdens, and challenges
- 1309730, SDBR chiller TCB adjustment PM performance was NA'd more than two times
- 1309574, Possible galvanic corrosion on drain nozzle of A-A MCR chiller condenser
- 1309286, Evaluate if a process for ensuring future changes to the diesel generators are evaluated for design bases tornado effects is necessary
- 1308624, Maximo auto populates the discovery date field when a CR is initiated and remains unless altered by the initiator
- 1305148, Evaluate if there is a potential vulnerability in the CR initiation process related to the timeliness of when Operations conducts their reviews
- 1305166, Evaluate software controls surrounding the ability to alter CR details once a CR is initiated
Work Orders
- 116906503
- 117015332
- 117088253
- 117124473
- 117176358
- 117406363
- 117431751
- 117434676
- 117440586
- 117459392
- 117470238
- 117554876
- 117581739
- 117823147
- 117823150
- 117823154
- 117990153
- 118024597
- 118279373
- 118284379
- 118296319
- 118388469
- 118497195
- 118703684
- 116705902
- 118101414
- 118101417
- 118101419
- 118101421
- 118551379
- 118753107
- Self-Assessments
- SQN-PI-FSA-15-002, 2015 INPO Mid-Cycle Focused Self Assessment
- SQN-PI-SSA-16-013, Follow-Up Assessment CAP Quality
- SQN-PI-SSA-17-003, Monthly SQN Corrective Action Program Audit - November
Other Documents
- AFW system health report
- HVAC system health report DCN D23085A, Corrective Action
- 1076179 revised 50.59 Auxiliary Building, Containment, and EDG Ventilation System Cooler Coil Replacement Project
- Control Air System Diagram, OPT200.CSA SB
- HO-2, Rev.5
- Maintenance Rule Expert Panel Meeting Minutes, May 26, March 24, and February 5, 2016
- SSCs in Alert Status- 5/21/17 Plant Screening Committee Meeting Agenda, June 7, 2017 Management Review Committee Meeting Agenda, July 28, 2016
- Management Review Committee Meeting Agenda, June 8, 2017
- MRC Meeting Minutes, July 28, 2016
- GAP Analysis for
- CRs 1103389 and
- 1016839 GAP Analysis for CR 1174406