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| | document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE | | | document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE |
| | page count = 5 | | | page count = 5 |
| | | project = TAC:M96803 |
| | | stage = Other |
| }} | | }} |
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| On January 28,1997, Toledo Edison (TE) provided by letter (Serial Number 2439) an interim response to GL 96-06. On February 28,1997, TE provided by letter (Serial Number 2442) a | | On January 28,1997, Toledo Edison (TE) provided by letter (Serial Number 2439) an interim response to GL 96-06. On February 28,1997, TE provided by letter (Serial Number 2442) a |
| ' summary report describing the actions taken to that date and the results of those actions. The summary report stated that TE would submit a letter to the NRC by July 30,1997,1) addressing the plans for final corrective actions for the piping penetrations, and 2) providing the final conclusion with respect to the water hammer effects on the CAC trains based on completion of , | | ' summary report describing the actions taken to that date and the results of those actions. The summary report stated that TE would submit a letter to the NRC by July 30,1997,1) addressing the plans for final corrective actions for the piping penetrations, and 2) providing the final conclusion with respect to the water hammer effects on the CAC trains based on completion of , |
| the detailed calculations. The final plan for corrective actions and completion of the detailed - l calculations have been delayed because of the forced outage that occurred due to a plant trip on May 4,1997. However, the following provides an update on the status of TE's progress in resolving these two issues. J Thennal Overoressurization of Pinine Penetrations .j During the forced outage, TE utilized the opportunity to install a modification to Containment Penetration Number 12, Component Cooling Water Supply to the Control Rod Drive Mechanisms. This modification was previously described to the NRC in TE's letter dated February 28,1997 as Modification Number 97-0009. The modification installed a bypass check valve that vents the portion of pipe between the containment isolation valves to the piping inside of the containment thus providing an inherent relief path for the isolated piping section. | | the detailed calculations. The final plan for corrective actions and completion of the detailed - l calculations have been delayed because of the forced outage that occurred due to a plant trip on May 4,1997. However, the following provides an update on the status of TE's progress in resolving these two issues. J Thennal Overoressurization of Pinine Penetrations .j During the forced outage, TE utilized the opportunity to install a modification to Containment Penetration Number 12, Component Cooling Water Supply to the Control Rod Drive Mechanisms. This modification was previously described to the NRC in TE's {{letter dated|date=February 28, 1997|text=letter dated February 28,1997}} as Modification Number 97-0009. The modification installed a bypass check valve that vents the portion of pipe between the containment isolation valves to the piping inside of the containment thus providing an inherent relief path for the isolated piping section. |
| Therefore, the overpressurization issue for Penetration Number 12 has been resolved. | | Therefore, the overpressurization issue for Penetration Number 12 has been resolved. |
| During this time, further analysis was also performed on Containment Penetration Number 32 for the Reactor Coolant Drain Tank pipe. Penetration Number 32 was previously reported to the NRC as partially drained to prevent pressure increases in the isolated portion of piping. Further analysis of this penetration determined that the air operated valves used to isolate this penetration I | | During this time, further analysis was also performed on Containment Penetration Number 32 for the Reactor Coolant Drain Tank pipe. Penetration Number 32 was previously reported to the NRC as partially drained to prevent pressure increases in the isolated portion of piping. Further analysis of this penetration determined that the air operated valves used to isolate this penetration I |
| provide inherent pressure relief. Therefore, Penetration Number 32 will no longer be maintained in a partially drained condition. | | provide inherent pressure relief. Therefore, Penetration Number 32 will no longer be maintained in a partially drained condition. |
| The following table provides the current status of the thi-tcen containment penetrations that TE had identified in its February 28,1997 letter as potentially adversely susceptible to post-LOCA thermal overpressurization. | | The following table provides the current status of the thi-tcen containment penetrations that TE had identified in its {{letter dated|date=February 28, 1997|text=February 28,1997 letter}} as potentially adversely susceptible to post-LOCA thermal overpressurization. |
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| Docket Number 50-346 License Number NPF-3 Serial Number 2473 Page 3 Penetration Name Status 1 Pressurizer Sample Line Meets ASME Code Faulted Stress Allowables 3 Component Cooling Water Meets ASME Code Faulted Stress Allowables to Containment 14 RCS Letdown Meets ASME Code Faulted Stress Allowables 56 Reactor Coolant Pump Seal Meets ASME Code Faulted Stress Allowables Return 13 Containment Normal Sump Meets D3NPS Interim Stress Allowables. | | Docket Number 50-346 License Number NPF-3 Serial Number 2473 Page 3 Penetration Name Status 1 Pressurizer Sample Line Meets ASME Code Faulted Stress Allowables 3 Component Cooling Water Meets ASME Code Faulted Stress Allowables to Containment 14 RCS Letdown Meets ASME Code Faulted Stress Allowables 56 Reactor Coolant Pump Seal Meets ASME Code Faulted Stress Allowables Return 13 Containment Normal Sump Meets D3NPS Interim Stress Allowables. |
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| License Number NPF-3 I Serial Number 2473 Page 4 ) | | License Number NPF-3 I Serial Number 2473 Page 4 ) |
| o! | | o! |
| Toledo Edison has determined that the penetrations and their associated components remain operable, as discussed in TE's February 28,1997 letter. | | Toledo Edison has determined that the penetrations and their associated components remain operable, as discussed in TE's {{letter dated|date=February 28, 1997|text=February 28,1997 letter}}. |
| Containment Air Cooler Water Hammer Effects , | | Containment Air Cooler Water Hammer Effects , |
| The status of the engineering evaluations of the water hanuner conditions in the Containment Air I Cooling System (CACS)is as follows: | | The status of the engineering evaluations of the water hanuner conditions in the Containment Air I Cooling System (CACS)is as follows: |
Letter Sequence Other |
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MONTHYEARML20151K0611997-07-28028 July 1997 Responds to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions. Listed Generic Issues Addressed Project stage: Other ML20211J0721997-09-30030 September 1997 Submits Response to NRC GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions Project stage: Other ML20199B1251997-11-0505 November 1997 Discusses Info Submitted Re 120-day Response to GL 96-06, Assurance of Equipment Operabiltiy & Containment Integrity During DBA Conditions, Per Implementation of Mods.If Commitments Revised,Revised Response Should Be Submitted Project stage: Other ML20216J0921998-03-18018 March 1998 Ack Receipt of 970128,0228,0728 & 0930 Submittals Re GL 96-06, Assurance of Equipment Operability & Ci During DBA Conditions. Addl Info Re Applicable Design Criteria for Piping & Valve & Drawing of Piping Between Valves Requested Project stage: Other ML20216G9451998-04-15015 April 1998 Requests Addl Info Pertaining to GL 96-06 Dtd 980930,which Included Request for Licensees to Evaluate Cooling Water Systems That Serve Containment Air Coolers to Assure Not Vulnerable to Waterhammer & two-phase Flow Conditions Project stage: Other ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event Project stage: Other ML20238F7971998-08-28028 August 1998 Submits Response to NRC Request for Addl Info Pertaining to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions Project stage: Request ML20205K5641999-04-0707 April 1999 Forwards Response to NRC 980415 RAI Re GL 96-06, Assurance of Equipment Operability & Ci During Design-Basis Accident Conditions. Rept FAI/98-126, Waterhammer Phenomena in Containment Air Cooler Swss, Encl Project stage: Other 1998-03-18
[Table View] |
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program IR 05000346/19980211999-08-0606 August 1999 Refers to NRC Insp Rept 50-346/98-21 Conducted on 980901- 990513 & Forwards Nov.Two Violations Identified Involving Failure to Maintain Design of Valve & Inadequate C/A for Degraded Condition Cited in Encl NOV 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207F4231999-06-0202 June 1999 Forwards Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504, IAW 10CFR50.4.NRC Evaluated Exercise Has Been Rescheduled for 991208,since NRC Did Not Evaluate 990504 Exercise ML20207E2521999-05-28028 May 1999 Forwards Rev 18,App A,Change 1 to Davis-Besse Nuclear Power Station,Unit 1,industrial Security Plan IAW Provisions of 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 ML20207E9561999-05-28028 May 1999 Forwards Update to NRC AL 98-03,re Estimated Info for Licensing Activities Through Sept 30,2000 ML20207E7801999-05-21021 May 1999 Forwards Application for Amend to License NPF-3,allowing Use of Expanded Spent Fuel Storage Capacity.Proprietary & non- Proprietary Version of Rev 2 to HI-981933 Re Cask Pit Rack Installation Project,Encl.Proprietary Info Withheld ML20206N0231999-05-0606 May 1999 Forwards License Renewal Applications for Davis-Besse Nuclear Power Station,Unit 1 for ML Klein,Cn Steenbergen & CS Strumsky.Without Encls ML20206D2421999-04-28028 April 1999 Forwards Combined Annual Radiological Environ Operating Rept & Radiological Effluent Release Rept for 1998. Rev 11, Change 1 to ODCM & 1998 Radiological Environ Monitoring Program Sample Analysis Results Also Encl PY-CEI-NRR-2382, Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl1999-04-21021 April 1999 Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl ML20206B8831999-04-17017 April 1999 Forwards 1634 Repts Re Results of Monitoring Provided to Individuals at Davis-Besse Nuclear Power Station During 1998,per 10CFR20.2206.Without Repts ML20205K3871999-04-0707 April 1999 Forwards Copy of Application of Ceic,Oec,Ppc & Teco to FERC, Proposing to Transfer Jurisdictional Transmission Facilities of Firstenergy Operating Companies to American Transmission Sys,Inc.With One Oversize Drawing ML20205K5641999-04-0707 April 1999 Forwards Response to NRC 980415 RAI Re GL 96-06, Assurance of Equipment Operability & Ci During Design-Basis Accident Conditions. Rept FAI/98-126, Waterhammer Phenomena in Containment Air Cooler Swss, Encl ML20205J1171999-03-29029 March 1999 Forwards Rev 1 to BAW-2325, Response to RAI Re RPV Integrity, Per GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rev Includes Corrected Values in Calculations PY-CEI-NRR-2377, Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1)1999-03-29029 March 1999 Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1) ML20205F5961999-03-27027 March 1999 Forwards Comments on Preliminary Accident Sequence Percursor (ASP) Analysis of 980624 Operational Event at Dbnps,Unit 1, as Transmitted by NRC Ltr ML20205D4791999-03-26026 March 1999 Forwards Rept Submitting Results of SG Tube ISI Conducted in Apr 1998.Rept Includes Description of Number & Extent of Tubes Inspected,Location & Percent wall-thickness Penetration for Each Indication of Imperfection ML20205L2031999-03-26026 March 1999 Submits Correction to Dose History of Tj Chambers.Dose Records During 1980-1997 Were Incorrectly Recorded Using Wrong Social Security Number.Nrc Form 5 Not Encl ML20205C7371999-03-25025 March 1999 Certifies That Dbnps,Unit 1,plant-referenced Simulator Continues to Meet Requirements of 10CFR55.45(b) for Simulator Facility Consisting Solely of plant-referenced Simulator.Acceptance Test Program & Test Schedule,Encl ML20205E3551999-03-19019 March 1999 Requests That Proposed Changes to TS 6.8.4.d.2 & TS 6.8.4.d.7 Be Withdrawn from LAR Previously Submitted to NRC ML20204J6361999-03-17017 March 1999 Forwards Firstenergy Corp Annual Rept for 1998 & 1999 Internal Cash Flow Projection as Evidence of Util Guarantee of Retrospective Premiums Which May Be Served Against Facilities PY-CEI-NRR-2375, Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage1999-03-15015 March 1999 Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage ML20204E6821999-03-12012 March 1999 Requests That Listed Changes Be Made to NRC Document Svc List for Davis-Besse Nuclear Power Station,Unit 1 1999-09-09
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GENTEREOR
. ENERGY 5501 N. State Route 2 419-249 2300 John K. Wood Oak Harbor. OH 43449 FAX: 419 321-8337 Vce Prescert . Nuclear I Davis Besse Docket Number 50-346 License Number NPF-3 Serial Number 2473 July 28, 1997 Un'ted States Nuclear Regulatory Commission Document Control Desk Washington, D. C. 20555-0001
Subject:
Response to NRC Generic Letter 96-06: Assurance of Equipment Operability and Containment Integrity During Design-Basis Accident Conditions (TAC No. M96803)
Ladies and Gentlemen:
On September 30,1996, the Nuclear Regulatory Commission (NRC) issued Generic Letter (GL) 96-06. That letter requested licensees, such as those for the Davis-Besse Nuclear Power Station (DBNPS) Unit Number 1, to address the following generic issues: i (1) Cooling water systems serving the containment air coolers (CACs) may be exposed to the hydrodynamic effects of water hammer during either a loss-of-coolant accident (LOCA) or a main steam line break (MSLB). These cooling water systems were not designed to withstand the hydrodynamic effects of water hammer and corrective actions may be needed to satisfy system design and operability requirements. Licensees are to determine if their plant's CACs cooling water systems are susceptible to water hammer during postulated accident conditions.
(2) Cooling water systems serving the containment air coolers may experience two-phase flow ;
conditions during postulated LOCA and MSLB scenarios. The heat removal assumptions for design-basis accident scenarios were based on single-phase flow conditions. Corrective actions may be needed to satisfy system design and operability requirements. Licensees are to determine if their plant's CACs are susceptible to two-phase flow conditions during l postulated accident conditions. i 9708050319 970728 8
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(3) Thermally-induced overpressurization ofisolated water-filled piping sections in containment i could: 1) jeopardize the ability of accident-mitigating systems to perform their safety functions, and 2) could also lead to a breach of containment integrity via bypass leakage.
Corrective actions may be needed to satisfy system operability requirements. Licensees are to determine if the piping systems which penetrate their plant's containment are susceptible to thermal expansion of fluid so that overpressurization could occur.
On January 28,1997, Toledo Edison (TE) provided by letter (Serial Number 2439) an interim response to GL 96-06. On February 28,1997, TE provided by letter (Serial Number 2442) a
' summary report describing the actions taken to that date and the results of those actions. The summary report stated that TE would submit a letter to the NRC by July 30,1997,1) addressing the plans for final corrective actions for the piping penetrations, and 2) providing the final conclusion with respect to the water hammer effects on the CAC trains based on completion of ,
the detailed calculations. The final plan for corrective actions and completion of the detailed - l calculations have been delayed because of the forced outage that occurred due to a plant trip on May 4,1997. However, the following provides an update on the status of TE's progress in resolving these two issues. J Thennal Overoressurization of Pinine Penetrations .j During the forced outage, TE utilized the opportunity to install a modification to Containment Penetration Number 12, Component Cooling Water Supply to the Control Rod Drive Mechanisms. This modification was previously described to the NRC in TE's letter dated February 28,1997 as Modification Number 97-0009. The modification installed a bypass check valve that vents the portion of pipe between the containment isolation valves to the piping inside of the containment thus providing an inherent relief path for the isolated piping section.
Therefore, the overpressurization issue for Penetration Number 12 has been resolved.
During this time, further analysis was also performed on Containment Penetration Number 32 for the Reactor Coolant Drain Tank pipe. Penetration Number 32 was previously reported to the NRC as partially drained to prevent pressure increases in the isolated portion of piping. Further analysis of this penetration determined that the air operated valves used to isolate this penetration I
provide inherent pressure relief. Therefore, Penetration Number 32 will no longer be maintained in a partially drained condition.
The following table provides the current status of the thi-tcen containment penetrations that TE had identified in its February 28,1997 letter as potentially adversely susceptible to post-LOCA thermal overpressurization.
Docket Number 50-346 License Number NPF-3 Serial Number 2473 Page 3 Penetration Name Status 1 Pressurizer Sample Line Meets ASME Code Faulted Stress Allowables 3 Component Cooling Water Meets ASME Code Faulted Stress Allowables to Containment 14 RCS Letdown Meets ASME Code Faulted Stress Allowables 56 Reactor Coolant Pump Seal Meets ASME Code Faulted Stress Allowables Return 13 Containment Normal Sump Meets D3NPS Interim Stress Allowables.
47a Core Flood Tank Sample Meets DBNPS Interim Stress Allowables.
Line 74C Pressurizer Auxiliary Spray Meets DBNPS Interim Stress Allowables. Partially drained to ensure availability post-accident.
4 Component Cooling Water Soft seat butterfly valve. LLRT documented leakage Retum from Containment will prevent overpressurization.
12 Component Cooling Water Action completed: Modification Number 97-0009 to the Control Rod Drive installed during the May 4,1997 outage to prevent Mech V ms overpressurization.
21 Demineralized Water to AOV Globe valve-Provides inherent relief to Containment prevent overpressurization.
32 Reactor Coolant Drain to AOV Diaphragm Valve-Provides inherent relief to Reactor Coolant Drain Tank prevent overpressurization.
48 Pressurizer Quench Tank AOV Globe valve-Provides inherent relief to Outlet prevent overpressurization.
49 Refueling Canal Fill Used only during refueling outages. Partially drhined to prevent overpressurization.
Four (1,3,14 and 56) of these thirteen piping penetrations have been determined to meet the American Society of Mechanical Engineers (ASME) Boiler & Pressure Vessel Code faulted allowable stress values and no further action would be required to reduce stress levels at these penetrations. Three penetrations (13,47a and 74c) have been determined to meet DBNPS interim stress allowables and will require changes in order to reduce the stress values during the next refueling outage. In order to comply with the ASME Code pressure limitations under faulted conditions for the components of these seven penetrations, further engineering action is planned under Modification Number 97-0009.
As discussed above, Penetration Numbers 12 and 32 have had their overpressurization issues resolved. Engineering reviews for final resolution of the potential overpressurization issues for the other four penetrations (4,21,48 and 49) are ongoing. The issues for all twelve penetrations will be resolved prior to start-up from the next refueling outage which is currently scheduled to commence in April,1998. Toledo Edison plans to provide a summary ofits plans for final corrective actions for these penetrations in a letter to the NRC by September 30,1997.
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Docket Number 50-346 ,
License Number NPF-3 I Serial Number 2473 Page 4 )
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Toledo Edison has determined that the penetrations and their associated components remain operable, as discussed in TE's February 28,1997 letter.
Containment Air Cooler Water Hammer Effects ,
The status of the engineering evaluations of the water hanuner conditions in the Containment Air I Cooling System (CACS)is as follows:
I A thermal-hydraulic evaluation was performed on each train of the CACS and also on l simultaneously operated CACS trains. The thermal-hydraulic evaluations have been completed,
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with the results being used to evaluate the acceptability of the system piping stresses and the !
support / restraint loads. A preliminary time history analysis on all piping has been completed, )
with the results showing that the piping stresses are relatively low. The structural review I revealed that the majority of the restraint loads are within the present design value, however, several exceed the conservative values used in the design basis calculations. The thermal- '
hydraulic evaluation has been revised to provide a more accurate model which will provide more representative loadings on the piping and, subsequently, the restraints. The revised data is currently being used to re-evaluate the piping restraint loads. The current review indicates that the CACS remains operable.
If modifications are required to restore the full qualification of any CACS components, Toledo Edison will establish a schedule for implementation based on operability considerations and the time required for modification design development. Toledo Edison plans to provide its final conclusions with respect to the water hammer effects and a description of any planned modifications in a letter to the NRC by September 30,1997.
Should you have any questions or require additional information, please contact Mr. James L.
Freels, Manager - Regulatory Affairs, at (419) 321-8466.
Very truly yours,
& s FWK/laj cc: A. B. Beach, Regional Administrator, NRC Region Ill A. G. Hansen, DB-1 NRC/NRR Project Manager S. Stasek, DB-1 NRC Senior Resident Inspector Utility Radiological Safety Board
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l Document Number 50-346 License Number NPF-3
- Sedal Number 2473 Attachment
RESPONSE
TO NRC GENERIC LETTER 96-06
.c FOR THE DAVIS-BESSE NUCLEAR POWER STATION UNIT NUMBER 1 This letter is submitted pursuant to 10 CFR 50.54(f) and contains information pursuant to NRC Generic Letter 96-06, " Assurance of Equipment Operability and Containment Integrity During !
Design - Basis Accident Conditions" for the Davis-Besse Nuclear Power Station, Unit Number 1.
By: .
John g Wood, Vice President - N'uclear Sworn to and subscribed before me this 28th day of July,- 1997.
M -4ns-~
Notary Public, Stite of Ohio Nora Lynn Flood ~
My commission expires September 3, 1997.