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{{#Wiki_filter:NRC Fo 36E O*U.S. NUCLEAR REGULATORY COMMISSION
{{#Wiki_filter:*
.(7 771 Ow c..BENSEE EVENT REPORT
NRC Fo             36E O                                                           .                                          U.S. NUCLEAR REGULATORY COMMISSION (7 771 Ow                   c               ..             BENSEE EVENT REPORT CONTROL BLOCK: l                 l    l    l      l  l      lh,               (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1                                   6 7
: CONTROL BLOCK: l llllllh, (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6l P l A l 3 l V l S l 1 l@l 0 l0 l- l 0 l 0 l 0 l 0 l 0
o    1 8 9 lPlA          l 3 l V l S l 141 l@l LICENSEE CODE                    15 0 l0 l- l 0 l uCENaE      l 0 l 0 -- l0 l025l@l4 0 l 0 NUMBER                              26 l1UCENSE l1 l1TYPE    l1 J0l@l57 CAT l SS l@
-- l0 l0 l@l4 l1 l1 l1 l1 l@l ll@o 1 7 8 9 LICENSEE CODE 14 15 uCENaE NUMBER 25 26 UCENSE TYPE J0 57 CAT SS CON'T"$RC l L l@l 0 l 5 l 0 l 0 l 0 l 3 l 3 l 4 @[1 l 0 l 1 l 3 l 7 l 9 @ ] 1l 1l 31 7l 9l@
CON'T "7
"7 o 1 7 8 60 61 DOCKET NUM8ER 68 69 EVENT OATE 74 75 REPORT DATE 80 EVENT OESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l At 1130 hours, RCS Loop A Feedwater Flow Channel 3 indication was observed I o 3 l periodically spiking downscale. At 1206 hours, the channel was declared inoperable I l and the channel bistables were placed in the tripped position. The health and I o 4 o s l safety of the general public was not jeopardized as the redundant instrument 1'0 6 l channel was operable throughout the incident.
o 7
l 0 7 llo a l I 80 7 8 9 E CODE S SC E COMPONENT CODE SUSCbOE SU El Il A @ lE l@ l El@ l Il Nl Sl Tl Rl Ul@ l Y l@ l 21@
1 8
O 9 7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION_ EVENT YEAR REPORT NO.
                        "$RC 60l L l@l           61 0 l 5 DOCKET l 0 l 0NUM8ERl 0 l 3 l 368l 469@[1EVENT        l 0 OATE l 1 l 3 l 774 l 9 @ ]REPORT 75          1l 1lDATE31 7l 9l@ 80 EVENT OESCRIPTION AND PROBABLE CONSEQUENCES h o   2 l At 1130 hours, RCS Loop A Feedwater Flow Channel 3 indication was observed                                                                                           I o   3 l periodically spiking downscale. At 1206 hours, the channel was declared inoperable I o  4      l and the channel bistables were placed in the tripped position. The health and                                                                                 I o   s l safety of the general public was not jeopardized as the redundant instrument                                                                                         1 0   6 l channel was operable throughout the incident.                                                                                                                         l 0   7 l                                                                                                                                                                    l o  a l                                                                                                                                                                     I 80 7         8 9 E             CODE         S SC E                 COMPONENT CODE                   SUSCbOE           SU       E 7
CODE TYPE N O.h g"LER/Ro 7l9l_ll 0l 4l 2]
O  9 8                        9 l Il A @ lE l@ l El@ l Il Nl Sl Tl Rl Ul@ l Y l@ l 21@
]/l0 l 3ll Ll[._]W uMg_ 21 22 23 24 26 27 28 29 30 31 32 T N AC ON ON PLANT MET HOURS S8 I FOR h 8.S P LIE MANUFACTURER lDl@lZl@WQl Z l@l 0l 0j 0l 0l lN l@Yl@lNl@l W l 1 l 2 l 0l@
10         11             12           13                             18         19                 20 SEQUENTIAL                         OCCURRENCE         REPORT                       REVISION
33 34 35 36 37 du 44 42 43 44 47 CAUSE DESCRIPTION AND CC3RECTIVE ACTIONS h i o l The incident resulted from a loose printed circuit cavi in the instrument loop.
_ EVENT YEAR                               REPORT NO.                             CODE             TYPE                           N O.
I~g l The card was strapped to hold it in position and the loon was satisfactorily Il returned to service.
h g"LER/Ro uMg
, 7 I Li Lu I-,_lli 4 7 8 9 So ST S% POWER OTHER STATUS Ots Y DISCOVERY DESCRIPTION y El@ l 0 l 4 l 9 l@l N/AllA l@lOperatorobservation lAfTIVITY CO TENT RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE ITl6l LZ_] @3 OF RELEASE l Zl@l N/AllN/Al7 8 9 to 11 44 45 80 PERSONNEL E)tPOSURES NUM8ER TYPE DESCRIPTION Tl l 0 l 0 l 0 l@l Z l@l N/Al1'''''* *PERSO~NE'L imu'4ES oESCRiPTiON@
_ 21 7l9l 22        23
~uM8tR 10l0j0l@lN/Al1 a 7 8 9 1t 12 80 LOSS of OR DAMAGE TO FACILITY
_l            l 0l 4l 2]
[Tlil l Z l@l N/A 13$3 3khlTYPE DESCRIPTION 7 8 9 10" '80"'*"'JESCRiPTiONO 7 911200 Q7
24          26
'" NRC uSE ONLY iSSuEf@l IN N/All1llllll1IIili 2 o 68 69 80 1;7 8 9 to 412-643-1258
                                                                                                    ]/
?8 PHONE:**NAME OF PREPARER}}
27 l0 l 3l 28      29 l Ll 30
[._]
31 W32 T     N AC ON                 ON PLANT           MET                     HOURS               S8 I           FOR h 8.         S P LIE               MANUFACTURER lDl@lZl@                       WQ                l36Z l@         l 0l 0j 0l 0l               lN   l@         Yl@             lNl@           l W l 1 l 2 l 47 0l@
33         34                 35                               37                   du     44             42                 43             44 CAUSE DESCRIPTION AND CC3RECTIVE ACTIONS h i   o l The incident resulted from a loose printed circuit cavi in the instrument loop.                                                                                     I
                                                                                                                                                              ~
g l The card was strapped to hold it in position and the loon was satisfactorily                                                                                                 I
        ,  7    l returned to service.
I Li Lu I 4     l                                                                                                                                                                l 7         8 9                                                                                                                                                                 So ST     S             % POWER                     OTHER STATUS               Ots         Y                         DISCOVERY DESCRIPTION y                 El@ l 0 l 4 l 9 l@l                           N/A                    l    lA l@lOperatorobservation                                                       l AfTIVITY CO TENT RELEASE                                     AMOUNT OF ACTIVITY                                                     LOCATION OF RELEASE N/A                                                                        N/A                                l ITl6l8 9LZ_] @3 OF RELEASE l Zl@l 7                            to           11                                         44 l          l 45                                                                       80 PERSONNEL E)tPOSURES NUM8ER             TYPE         DESCRIPTION 1
Tl l 0 l 0 l 0 l@l Z l@l                                 N/A                                                                                                            l PERSO~NE'L imu'4ES
                      ~uM8tR              oESCRiPTiON@
1  a      10l0j0l@l                                        N/A 80 l
7         8 9                 1t     12 LOSS of OR DAMAGE TO FACILITY TYPE        DESCRIPTION
[Tlil 8l 9Z l@l                                                 N/A                                                                       13$3 3kh l
7                         10                                                                                                                                                 80
                      "'*"'JESCRiPTiONO                                                       7 911200 Q7                                                     NRC uSE ONLY l1llllll1IIili 2  o      IN iSSuEf@l                                           N/A                                                                          l 7        8 9              to                                                                                                                68 69                           80 1;
                                                                        *
* 8                                       PHONE:
412-643-1258                     ?
NAME OF PREPARER}}

Latest revision as of 05:26, 2 February 2020

LER 79-042/03L-0:on 791013,RCS Loop a Feedwater Flow Channel 3 Indication Observed Spiking Downscale.Caused by Loose Printed Circuit Card in Instrument Loop.Card Strapped to Position & Loop Returned to Svc
ML19210D021
Person / Time
Site: Beaver Valley
Issue date: 11/13/1979
From: Werling J
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19210D017 List:
References
LER-79-042-03L, LER-79-42-3L, NUDOCS 7911200425
Download: ML19210D021 (1)


Text

NRC Fo 36E O . U.S. NUCLEAR REGULATORY COMMISSION (7 771 Ow c .. BENSEE EVENT REPORT CONTROL BLOCK: l l l l l l lh, (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 7

o 1 8 9 lPlA l 3 l V l S l 141 l@l LICENSEE CODE 15 0 l0 l- l 0 l uCENaE l 0 l 0 -- l0 l025l@l4 0 l 0 NUMBER 26 l1UCENSE l1 l1TYPE l1 J0l@l57 CAT l SS l@

CON'T "7

o 7

1 8

"$RC 60l L l@l 61 0 l 5 DOCKET l 0 l 0NUM8ERl 0 l 3 l 368l 469@[1EVENT l 0 OATE l 1 l 3 l 774 l 9 @ ]REPORT 75 1l 1lDATE31 7l 9l@ 80 EVENT OESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l At 1130 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.29965e-4 months <br />, RCS Loop A Feedwater Flow Channel 3 indication was observed I o 3 l periodically spiking downscale. At 1206 hours0.014 days <br />0.335 hours <br />0.00199 weeks <br />4.58883e-4 months <br />, the channel was declared inoperable I o 4 l and the channel bistables were placed in the tripped position. The health and I o s l safety of the general public was not jeopardized as the redundant instrument 1 0 6 l channel was operable throughout the incident. l 0 7 l l o a l I 80 7 8 9 E CODE S SC E COMPONENT CODE SUSCbOE SU E 7

O 9 8 9 l Il A @ lE l@ l El@ l Il Nl Sl Tl Rl Ul@ l Y l@ l 21@

10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION

_ EVENT YEAR REPORT NO. CODE TYPE N O.

h g"LER/Ro uMg

_ 21 7l9l 22 23

_l l 0l 4l 2]

24 26

]/

27 l0 l 3l 28 29 l Ll 30

[._]

31 W32 T N AC ON ON PLANT MET HOURS S8 I FOR h 8. S P LIE MANUFACTURER lDl@lZl@ WQ l36Z l@ l 0l 0j 0l 0l lN l@ Yl@ lNl@ l W l 1 l 2 l 47 0l@

33 34 35 37 du 44 42 43 44 CAUSE DESCRIPTION AND CC3RECTIVE ACTIONS h i o l The incident resulted from a loose printed circuit cavi in the instrument loop. I

~

g l The card was strapped to hold it in position and the loon was satisfactorily I

, 7 l returned to service.

I Li Lu I i 4 l l 7 8 9 So ST S  % POWER OTHER STATUS Ots Y DISCOVERY DESCRIPTION y El@ l 0 l 4 l 9 l@l N/A l lA l@lOperatorobservation l AfTIVITY CO TENT RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE N/A N/A l ITl6l8 9LZ_] @3 OF RELEASE l Zl@l 7 to 11 44 l l 45 80 PERSONNEL E)tPOSURES NUM8ER TYPE DESCRIPTION 1

Tl l 0 l 0 l 0 l@l Z l@l N/A l PERSO~NE'L imu'4ES

~uM8tR oESCRiPTiON@

1 a 10l0j0l@l N/A 80 l

7 8 9 1t 12 LOSS of OR DAMAGE TO FACILITY TYPE DESCRIPTION

[Tlil 8l 9Z l@l N/A 13$3 3kh l

7 10 80

"'*"'JESCRiPTiONO 7 911200 Q7 NRC uSE ONLY l1llllll1IIili 2 o IN iSSuEf@l N/A l 7 8 9 to 68 69 80 1;

  • 8 PHONE:

412-643-1258  ?

NAME OF PREPARER