ML19276H674: Difference between revisions
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{{#Wiki_filter:. | {{#Wiki_filter:. | ||
.ys,, , | .ys,, , | ||
.-, - 3. . :. . . | .-, - 3. . :. . . | ||
,,,.1 | ,,,.1 | ||
. . - . -,,. .. .r. . g.g | . . - . -,,. .. .r. . g.g | ||
Line 32: | Line 28: | ||
r--c e rg :-?ce.'. r,' | r--c e rg :-?ce.'. r,' | ||
o | o | ||
"''':+ n NOVEMBER 1979 e | "''':+ n NOVEMBER 1979 e | ||
The unit tripped at 1347 on November 5th due to undervoltage on Bus 11 i caused by a ground fault in No.11 Feedwater Pump motor. tie unit was | The unit tripped at 1347 on November 5th due to undervoltage on Bus 11 i caused by a ground fault in No.11 Feedwater Pump motor. tie unit was | ||
;i returned to service at 0631 the following day and power was limited to | ;i returned to service at 0631 the following day and power was limited to about 65%. At 0942 on November 15th, a ground fault in No. 12 Feedwater Pump motor caused another trip. No.11 Feedwater Pump motor was re-paired and the unit restarted at 1714 on November 25th and limited to about 65% power. On November 30th, No.12 Feedwater Pump was returned to service and the unit was escals. ting to full power. | ||
about 65%. At 0942 on November 15th, a ground fault in No. 12 Feedwater Pump motor caused another trip. No.11 Feedwater Pump motor was re-paired and the unit restarted at 1714 on November 25th and limited to about 65% power. On November 30th, No.12 Feedwater Pump was returned to service and the unit was escals. ting to full power | |||
O D | O D | ||
eg9121B | eg9121B | ||
Line 44: | Line 36: | ||
4 DAII.Y UNIT POWER OUTPUT DOCKET NO. 50-282 ~ | 4 DAII.Y UNIT POWER OUTPUT DOCKET NO. 50-282 ~ | ||
UNIT Prairie Island No. 1 - | UNIT Prairie Island No. 1 - | ||
DATE 791201 COMPLETED BY A. A. HunsTa~d TELEPHONE 612-388-4767 MONT11 NOVEMBER 1979 DAY AVERACE LOAD MWe-Net DAY AVERACE LOAD MWe-Net t 480 17 -3 | DATE 791201 COMPLETED BY A. A. HunsTa~d TELEPHONE 612-388-4767 MONT11 NOVEMBER 1979 DAY AVERACE LOAD MWe-Net DAY AVERACE LOAD MWe-Net t 480 17 -3 486 18 -3 1 _ | ||
486 18 -3 1 _ | |||
483 19 -3 | 483 19 -3 | ||
: c. 492 20 -7 | : c. 492 20 -7 | ||
, 276 21 -9 6 182 22 -7 7 293 23 -8 | , 276 21 -9 6 182 22 -7 7 293 23 -8 g 297 ;;, -8 o 299 2s 2 10 284 26 239 | ||
. t1 300 27 275 17 299 28 276 13 296 29 275 14 294 30 269 15 111 31 16 -8 Average loads above 503 MWc-Net are due to cooler condenser circulating water, | |||
g 297 ;;, -8 o 299 2s 2 10 284 26 239 | |||
. t1 300 27 275 17 299 28 276 13 296 29 275 14 294 30 269 15 111 31 | |||
16 -8 Average loads above 503 MWc-Net are due to cooler condenser circulating water, | |||
OffRAMNG,,DAT". PEP,0RT . | OffRAMNG,,DAT". PEP,0RT . | ||
DOCKET NO 50-282 DATE 791201 CO iPLETED BY A. A. Hunstad OPERATING STATUS 7/1EPHONE-612-388-4767 | DOCKET NO 50-282 DATE 791201 CO iPLETED BY A. A. Hunstad OPERATING STATUS 7/1EPHONE-612-388-4767 | ||
Line 67: | Line 50: | ||
L l | L l | ||
: 5. Design Electrical Rating (Ncc MWe): 510 I | : 5. Design Electrical Rating (Ncc MWe): 510 I | ||
: 6. Maximum Dependable Capacity (Cross MWe): 534 | : 6. Maximum Dependable Capacity (Cross MWe): 534 L , | ||
L , | |||
C 7. Maximum Dependable Capacity (Net MWe': 503 g 8. If Changes Occter in Capacity Rar inne (Irems Numbe'- 3 Through 7) Sfoce Lart 3epart - | C 7. Maximum Dependable Capacity (Net MWe': 503 g 8. If Changes Occter in Capacity Rar inne (Irems Numbe'- 3 Through 7) Sfoce Lart 3epart - | ||
o z Cive Reason: _ . _ _ . - . . _ _ . . . _. | o z Cive Reason: _ . _ _ . - . . _ _ . . . _. | ||
, 9. Power Level To Which Restricted. ff Anv O'e t tr,c) : , , _ _ , , , , , , _ _ , , , , , _ , , , , . , , _, | , 9. Power Level To Which Restricted. ff Anv O'e t tr,c) : , , _ _ , , , , , , _ _ , , , , , _ , , , , . , , _, | ||
O Reasons for Restrictions, i f An _, , | O Reasons for Restrictions, i f An _, , | ||
: 10. _ _ , , , , _ _ , _ , _ _ , , , , , _ _ , | : 10. _ _ , , , , _ _ , _ , _ _ , , , , , _ _ , | ||
This Minch Yr-ro-D:.? c Co .ilative lls Hours In Reporting Period 720 8016 52224 | This Minch Yr-ro-D:.? c Co .ilative lls Hours In Reporting Period 720 8016 52224 | ||
: 12. Number Of Hours Reactor Was Crirical 467.3 5775.3 40464.4 | : 12. Number Of Hours Reactor Was Crirical 467.3 5775.3 40464.4 | ||
Line 94: | Line 70: | ||
: 23. Unit Forced Outage Rate 36.7 21.1 13.9 | : 23. Unit Forced Outage Rate 36.7 21.1 13.9 | ||
'4. Shutdowns Scheduled Over Next 12 Months (Type, Date and Duration of Ec.:h): | '4. Shutdowns Scheduled Over Next 12 Months (Type, Date and Duration of Ec.:h): | ||
Refueling, Summer 1980, 5 Weeks | Refueling, Summer 1980, 5 Weeks | ||
: 25. If Shut Down at End Of Report Pccied, Estimated Date of Startup - | : 25. If Shut Down at End Of Report Pccied, Estimated Date of Startup - | ||
m. | m. | ||
v M T .'> ' Pa''-). ,'s .3' P;D '. Di.'?"a "''T.'_'."..s"..N_ | v M T .'> ' Pa''-). ,'s .3' P;D '. Di.'?"a "''T.'_'."..s"..N_ | ||
JJ .,.a J 3. | JJ .,.a J 3. | ||
. . _2 0__ _- 2_ _8 2 | . . _2 0__ _- 2_ _8 2 R''?2'tT ?!3Tl11 _N.O_V_ E.M_BER 1_9 79 . . . _ _. | ||
R''?2'tT ?!3Tl11 _N.O_V_ E.M_BER 1_9 79 . . . _ _. | |||
' 'UN- I' ' '' ! - I J '. : 791201 ~~ | ' 'UN- I' ' '' ! - I J '. : 791201 ~~ | ||
L ',dF_ _ .. .) | L ',dF_ _ .. .) | ||
.1 ( A. A. Ilun'stad m.._... . . . . . .. | .1 ( A. A. Ilun'stad m.._... . . . . . .. | ||
t ' . i.? . .J . ' Q .,33 * ~.] _ | t ' . i.? . .J . ' Q .,33 * ~.] _ | ||
I .. | I .. | ||
4 .: .- / \. *; 1.12. ma a , | 4 .: .- / \. *; 1.12. ma a , | ||
ime 5 - % : :C i' e | ime 5 - % : :C i' e | ||
') ate .$ t .l 2 5 3.i 8' 2. ant j. - $ i .4 m A2' u3 h) | ') ate .$ t .l 2 5 3.i 8' 2. ant j. - $ i .4 m A2' u3 h) | ||
N ' j Il 'j i 'i d l$ ; | N ' j Il 'j i 'i d l$ ; | ||
l 1. | |||
:3 - | :3 - | ||
o s | o s | ||
3 .- a o u : : - | 3 .- a o u : : - | ||
.b p r t 4 | .b p r t 4 a .3fis 5 i | ||
a .3fis 5 i | |||
3 o3 | 3 o3 | ||
= > | = > | ||
1 | 1 e | ||
h>M - J A Nd-* ; J 1 | |||
j 1 fd m , | j 1 fd m , | ||
'# .4 - | '# .4 - | ||
.') | .') | ||
. l 4 l *$ : i i ; | . l 4 l *$ : i i ; | ||
; , | ; , | ||
O | O | ||
# b. | # b. | ||
0 | 0 s .al ; | ||
s .al ; | |||
l p | l p | ||
C. 3 f | C. 3 f | ||
* I... _ | * I... _ | ||
Line 155: | Line 110: | ||
a | a | ||
-e 791105 lF ! | -e 791105 lF ! | ||
6 | 6 | ||
* 16.4 A ! | |||
16.4 A ! | 3 ! N/A Cll MOTORX ' TripduetoundervoltageonBuslik t | ||
caused by ground fault on No. 11 A | |||
3 ! N/A | |||
Cll MOTORX ' TripduetoundervoltageonBuslik | |||
o | o | ||
- . Feedwater Pump motor. t e | |||
h | |||
- . Feedwater Pump motor. t | |||
' 3 | ' 3 | ||
~ 191115 . F I247.5 | ~ 191115 . F I247.5 | ||
' A 3 N/A | ' A 3 N/A CH MOTORX | ||
* Trip due to undervoltage on Bus 12 caused by ground fault on No. 12 | |||
* Trip due to undervoltage on Bus 12 | |||
caused by ground fault on No. 12 | |||
; | ; | ||
a , | a , | ||
Feedwater Pump motor. | Feedwater Pump motor. | ||
Line 187: | Line 127: | ||
. i Q i > | . i Q i > | ||
l Q l I i | l Q l I i | ||
l | l | ||
: W | : W | ||
- SEE a | - SEE a | ||
bc=-0 | bc=-0 F: Forced Reason Math'd: ; Exhibit C-In- ' | ||
S: Schedul*d A-E<1uipman t Failure (r cc pl.ain) 1 *f an.nl structions for B ' taint 2r.ance <:r Tect 2 .M.cnual Trip Preparat ion of C-R2f a211n ; 3 -A'2 tona:Le Trip Data Eatry Cheeta b, 3 | S: Schedul*d A-E<1uipman t Failure (r cc pl.ain) 1 *f an.nl structions for B ' taint 2r.ance <:r Tect 2 .M.cnual Trip Preparat ion of C-R2f a211n ; 3 -A'2 tona:Le Trip Data Eatry Cheeta b, 3 | ||
. -R23ula:.:ry Ra.stric tion '*- Other (P.::phin) f or 1.in u.'.s a + '*:ve.it F -Opar . ,r Train 'n3 5 L I: 'an L ' utin.ition | . -R23ula:.:ry Ra.stric tion '*- Other (P.::phin) f or 1.in u.'.s a + '*:ve.it F -Opar . ,r Train 'n3 5 L I: 'an L ' utin.ition | ||
Line 207: | Line 138: | ||
*!- ? t'! 'r *.- U li i M. I.') '. . I - . - ' | *!- ? t'! 'r *.- U li i M. I.') '. . I - . - ' | ||
.spv- . y. . n , , ,,. .- | .spv- . y. . n , , ,,. .- | ||
. r. , n,, g.,3, nn-r .T t'n. Sf'-306 _ma | . r. , n,, g.,3, nn-r .T t'n. Sf'-306 _ma | ||
":it.T I'es i -i r- } =.1 c a.1 'v . 2 t'.i-'' ' 791201 | ":it.T I'es i -i r- } =.1 c a.1 'v . 2 t'.i-'' ' 791201 | ||
Line 216: | Line 144: | ||
- -- r - - ~ -n (,3 3 c e ... | - -- r - - ~ -n (,3 3 c e ... | ||
e | e | ||
~ | ~ | ||
'*'" '! _ _ NOVI2GER,,19 7 9_ ..,, ____ | '*'" '! _ _ NOVI2GER,,19 7 9_ ..,, ____ | ||
The unit tripped at 2333 on November 1st on high steam generator level i when a feedwater regula*.ing valve alfunctioned. The unit was returned | The unit tripped at 2333 on November 1st on high steam generator level i when a feedwater regula*.ing valve alfunctioned. The unit was returned | ||
.' ; | .' ; | ||
to service at 0122 on November 3rd. Another trip occurred at 1044 on November 14th when a pressurizer level transmitter was valved out with another in trip. The unit was restarted at 1320 the same day but flux distribution problems caused power to be limited to 50% for a day. The unit is base loaded at 100%. | |||
to service at 0122 on November 3rd. Another trip occurred at 1044 on | |||
November 14th when a pressurizer level transmitter was valved out with another in trip. The unit was restarted at 1320 the same day but flux distribution problems caused power to be limited to 50% for a day. The unit is base loaded at 100% | |||
DAILY UNIT POWER OUTPUT DOCKET NO. 50-306 UNIT Prairie Island No. 2 DATE 791201 , | DAILY UNIT POWER OUTPUT DOCKET NO. 50-306 UNIT Prairie Island No. 2 DATE 791201 , | ||
COMPLETED BY A. A. Hunstad TI LEPHONE 612-388-4767 510NTil NOVEMBER 1979 | COMPLETED BY A. A. Hunstad TI LEPHONE 612-388-4767 510NTil NOVEMBER 1979 | ||
!).\Y AVERAGE LOAD MWe-Net DAY AVERACE LOAD MWe-N.'t | !).\Y AVERAGE LOAD MWe-Net DAY AVERACE LOAD MWe-N.'t | ||
: t. 495 17 523 | : t. 495 17 523 | ||
-21 18 522 3 401 19 528 | -21 18 522 3 401 19 528 | ||
: c. 517 20 522 | : c. 517 20 522 | ||
', 521 21 514 6 524 22 520 - | ', 521 21 514 6 524 22 520 - | ||
7 523 23 519 9 523 24 521 9 | 7 523 23 519 9 523 24 521 9 | ||
525 25 518 to 525 2 t> 518 | 525 25 518 to 525 2 t> 518 | ||
;1 527 27 520 t, 524 28 518 | ;1 527 27 520 t, 524 28 518 13 526 29 520 14 315 30 519 15 223 31 - | ||
13 526 29 520 14 315 30 519 15 223 31 - | |||
16 477 Average loads above 500 MNc-Net are due to cooler condenser circulating teater | 16 477 Average loads above 500 MNc-Net are due to cooler condenser circulating teater | ||
OJf p?TNG DAT3 PT-PORT pg 80 > | OJf p?TNG DAT3 PT-PORT pg 80 > | ||
DOCKET NO 50-306 DATE 791201 COMPLETED BY A. A. Hunstad OPERATING STATUS TELEPHONE 612-388-4767 | DOCKET NO 50-306 DATE 791201 COMPLETED BY A. A. Hunstad OPERATING STATUS TELEPHONE 612-388-4767 | ||
Line 253: | Line 167: | ||
: 2. Reporting Period: November 1979 Notes | : 2. Reporting Period: November 1979 Notes | ||
: 3. Licensed Thermal Power (MWt): 1650 4 Nameplate Rating (Gross MWe): 593 _,, | : 3. Licensed Thermal Power (MWt): 1650 4 Nameplate Rating (Gross MWe): 593 _,, | ||
t | t | ||
: 5. Design Electrical Rating (Net MWe): MO l | : 5. Design Electrical Rating (Net MWe): MO l | ||
Line 259: | Line 172: | ||
C 7. Maximum Dependable Capacity (Ne* We': 500 g 8. If Changes Occur in Capacity Rar im.r (f rems Numbe- 3 Through 7) Since- I.a n t h po r t - | C 7. Maximum Dependable Capacity (Ne* We': 500 g 8. If Changes Occur in Capacity Rar im.r (f rems Numbe- 3 Through 7) Since- I.a n t h po r t - | ||
v a: Cive Reason: . _ _ _ _ . _ _ . _ . .. _ _.._.. . | v a: Cive Reason: . _ _ _ _ . _ _ . _ . .. _ _.._.. . | ||
cn | cn | ||
[ 9. Power Level To Which Restricted. I f Mw O'. t f rge) . | [ 9. Power Level To Which Restricted. I f Mw O'. t f rge) . | ||
e F 10. Reasons for Restrictions, i f A r. - , , , , ,, , , , , , , _ _ _ _ _ _ _ , , , , , , , ,, _ | e F 10. Reasons for Restrictions, i f A r. - , , , , ,, , , , , , , _ _ _ _ _ _ _ , , , , , , , ,, _ | ||
Th in ." nth Yr-To-Date ai olative | Th in ." nth Yr-To-Date ai olative | ||
: 11. Ho'ars In Reporting Period 720 8016 43342 | : 11. Ho'ars In Reporting Period 720 8016 43342 | ||
Line 282: | Line 192: | ||
Refueling, January 1980, 5 Weeks | Refueling, January 1980, 5 Weeks | ||
: 25. If Shut Down at End Of Report Pcciod. Estimated Date of Starrup: | : 25. If Shut Down at End Of Report Pcciod. Estimated Date of Starrup: | ||
10iIT .:t'J-'+.. 3 i i'.a 'O m 't~c. F.' ' :M AL., o' :* 21.. .- 3. 0. 6 | 10iIT .:t'J-'+.. 3 i i'.a 'O m 't~c. F.' ' :M AL., o' :* 21.. .- 3. 0. 6 | ||
. ? iiri2 .s 8 eit !. . . .-*2 | . ? iiri2 .s 8 eit !. . . .-*2 d.h f .l.~. 2 | ||
d.h f .l.~. 2 | |||
:t';?T1E MG':111 --NOVD!BER 1979 - - - ,. | :t';?T1E MG':111 --NOVD!BER 1979 - - - ,. | ||
791201' ' | 791201' ' | ||
i | i | ||
: t. . .'__- J if A. A luits' tad 7 . .., | : t. . .'__- J if A. A luits' tad 7 . .., | ||
i '. .c .J . _y'- .. '_: .] | i '. .c .J . _y'- .. '_: .] | ||
., e 1 | ., e 1 | ||
4 ; 3 *4 | 4 ; 3 *4 | ||
. *; - | . *; - | ||
3.12 .'P. 3 2. j s- - AJ sJ u *. J.'C1.J | 3.12 .'P. 3 2. j s- - AJ sJ u *. J.'C1.J Date J 4s ''. 3 .: > > -2* -.. | ||
.6 ... | .6 ... | ||
: a. 3 . .D. . ant u ,, .s .., u. | : a. 3 . .D. . ant u ,, .s .., u. | ||
:s . i. a 'a a . .: .o-) a . , , , e. 3 .: ; | |||
:s . i. a 'a | |||
a . .: .o-) a . , , , e. 3 .: ; | |||
c4 ) ;J ..;)JrL 3~ | c4 ) ;J ..;)JrL 3~ | ||
1 -< o i j | 1 -< o i j | ||
> :: a p t] . | > :: a p t] . | ||
c> | c> | ||
.I s .) l 3 .3 | .I s .) l 3 .3 l | ||
l | |||
& & J 4 4.. L ? - a t' *.* l-a . J t | & & J 4 4.. L ? - a t' *.* l-a . J t | ||
> 4 i>> ;.: ; , .3 . . | > 4 i>> ;.: ; , .3 . . | ||
l :'1iv | l :'1iv | ||
. : ; lan | . : ; lan | ||
. s | . s | ||
. 3 2 .a e j | . 3 2 .a e j | ||
. i | . i j.j l '' , | ||
j.j l '' , | |||
+ 3 | + 3 | ||
, , g I | , , g I | ||
., -- .- ..-..L | ., -- .- ..-..L | ||
.e. | .e. | ||
I i | |||
I | 31 i | ||
-, i-- ! | -, i-- ! | ||
g | g | ||
. I j I | . I j I | ||
,} | ,} | ||
~ | ~ | ||
791101 l I' 25.8 A 3 N/A } | |||
Cli . VA' VEX | Cli . VA' VEX l : i ' Trip due to steam generator high | ||
l : i ' Trip due to steam generator high | |||
* i level caused by malfunction of its | * i level caused by malfunction of its | ||
:) | :) | ||
-- I' | -- I' | ||
; ,! feedwater regulating valve. | ; ,! feedwater regulating valve. | ||
re | re i . | ||
l 791114 i F 1 2.6 G 3 N/A IA INSTRU Trip due to personnel error in g | |||
i . | j . | ||
valving out a pressurizer level t ransmit te r. | |||
l 791114 i F 1 2.6 G 3 N/A IA INSTRU Trip due to personnel error in | |||
valving out a pressurizer level | |||
t ransmit te r. | |||
i e | i e | ||
i . | i . | ||
Line 387: | Line 248: | ||
! l | ! l | ||
$a ' | $a ' | ||
l | l | ||
{A D . - | {A D . - | ||
3 1 ')- 3 4 F: Fo rced Reason Method: Exhibit G-In-g S: 'ichedu led A -E<;uipx?a t Fai l"r a ( 5' :,,'.ain) 3 '!a !".: : nan c.e ir "e c. t 1 -!hn'o1 2 -Man.ml Trip trincti,ns for b | 3 1 ')- 3 4 F: Fo rced Reason Method: Exhibit G-In-g S: 'ichedu led A -E<;uipx?a t Fai l"r a ( 5' :,,'.ain) 3 '!a !".: : nan c.e ir "e c. t 1 -!hn'o1 2 -Man.ml Trip trincti,ns for b | ||
D C-tafu lin,; 3 -htonatic Trip Prepara:'_on .~ | D C-tafu lin,; 3 -htonatic Trip Prepara:'_on .~ | ||
Line 398: | Line 255: | ||
7 . . .'i 4 ., - ...g p:vi' .qi '-1 ) | 7 . . .'i 4 ., - ...g p:vi' .qi '-1 ) | ||
, t.l ' . J O ',3 | , t.l ' . J O ',3 | ||
: ,; 3 rn) . | : ,; 3 rn) . | ||
: u. w. 1 - - | : u. w. 1 - - | ||
N}} | N}} |
Revision as of 16:52, 1 February 2020
ML19276H674 | |
Person / Time | |
---|---|
Site: | Prairie Island |
Issue date: | 12/01/1979 |
From: | Hunstad A NORTHERN STATES POWER CO. |
To: | |
Shared Package | |
ML19276H673 | List: |
References | |
NUDOCS 7912180628 | |
Download: ML19276H674 (8) | |
Text
.
.ys,, ,
.-, - 3. . :. . .
,,,.1
. . - . -,,. .. .r. . g.g
" T U "". 50-282 qir.T p pi jc Tsin,a r. . 1 DN"" 791201
(** " F IP */1.
~
A . liuns tA4,__ _ .",~ ~
r--c e rg :-?ce.'. r,'
o
":+ n NOVEMBER 1979 e
The unit tripped at 1347 on November 5th due to undervoltage on Bus 11 i caused by a ground fault in No.11 Feedwater Pump motor. tie unit was
- i returned to service at 0631 the following day and power was limited to about 65%. At 0942 on November 15th, a ground fault in No. 12 Feedwater Pump motor caused another trip. No.11 Feedwater Pump motor was re-paired and the unit restarted at 1714 on November 25th and limited to about 65% power. On November 30th, No.12 Feedwater Pump was returned to service and the unit was escals. ting to full power.
O D
eg9121B
4 DAII.Y UNIT POWER OUTPUT DOCKET NO. 50-282 ~
UNIT Prairie Island No. 1 -
DATE 791201 COMPLETED BY A. A. HunsTa~d TELEPHONE 612-388-4767 MONT11 NOVEMBER 1979 DAY AVERACE LOAD MWe-Net DAY AVERACE LOAD MWe-Net t 480 17 -3 486 18 -3 1 _
483 19 -3
- c. 492 20 -7
, 276 21 -9 6 182 22 -7 7 293 23 -8 g 297 ;;, -8 o 299 2s 2 10 284 26 239
. t1 300 27 275 17 299 28 276 13 296 29 275 14 294 30 269 15 111 31 16 -8 Average loads above 503 MWc-Net are due to cooler condenser circulating water,
OffRAMNG,,DAT". PEP,0RT .
DOCKET NO 50-282 DATE 791201 CO iPLETED BY A. A. Hunstad OPERATING STATUS 7/1EPHONE-612-388-4767
- 1. Unit Name: Prairie Island No. 1
- 2. Reporting Period: November 1979 es
- 3. Licensed Thermal Power (MWt): 1650 1
4 Nameplate Rating (Gross MWe): M3 _,
L l
- 5. Design Electrical Rating (Ncc MWe): 510 I
- 6. Maximum Dependable Capacity (Cross MWe): 534 L ,
C 7. Maximum Dependable Capacity (Net MWe': 503 g 8. If Changes Occter in Capacity Rar inne (Irems Numbe'- 3 Through 7) Sfoce Lart 3epart -
o z Cive Reason: _ . _ _ . - . . _ _ . . . _.
, 9. Power Level To Which Restricted. ff Anv O'e t tr,c) : , , _ _ , , , , , , _ _ , , , , , _ , , , , . , , _,
O Reasons for Restrictions, i f An _, ,
- 10. _ _ , , , , _ _ , _ , _ _ , , , , , _ _ ,
This Minch Yr-ro-D:.? c Co .ilative lls Hours In Reporting Period 720 8016 52224
- 12. Number Of Hours Reactor Was Crirical 467.3 5775.3 40464.4
- 13. Reactor Reserve Shutdown Hours 252.7 1076.8 5531.9
- 14. Hours Generator on Line 456.1 5672.2 39389.4
- 15. Unit Reserve Shutdown Hourr, 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (M'.'ll) 533052 8627295 60907877
- 17. Gross Electrical Ener;;y Generatc] (Wl:' 162740 2753720 19784610
- 18. Net Electrical Energy Generat.m U S'U) 147998 2564831 18493253
- 19. Unit Service Factor 63.3 70.8 75.4
- 20. Unit Availability Factor 63.3 70.8 75.4
- 21. Unit Capacity Factor (lising MDC t:ct.) 40.9 63.6 70.4
- 22. Unit Capacity Factor (Using DER Net) 38.8 60.4 66.8
- 23. Unit Forced Outage Rate 36.7 21.1 13.9
'4. Shutdowns Scheduled Over Next 12 Months (Type, Date and Duration of Ec.:h):
Refueling, Summer 1980, 5 Weeks
- 25. If Shut Down at End Of Report Pccied, Estimated Date of Startup -
m.
v M T .'> ' Pa-). ,'s .3' P;D '. Di.'?"a "T.'_'."..s"..N_
JJ .,.a J 3.
. . _2 0__ _- 2_ _8 2 R?2'tT ?!3Tl11 _N.O_V_ E.M_BER 1_9 79 . . . _ _.
' 'UN- I' ' ! - I J '. : 791201 ~~
L ',dF_ _ .. .)
.1 ( A. A. Ilun'stad m.._... . . . . . ..
t ' . i.? . .J . ' Q .,33 * ~.] _
I ..
4 .: .- / \. *; 1.12. ma a ,
ime 5 - % : :C i' e
') ate .$ t .l 2 5 3.i 8' 2. ant j. - $ i .4 m A2' u3 h)
N ' j Il 'j i 'i d l$ ;
l 1.
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The unit tripped at 2333 on November 1st on high steam generator level i when a feedwater regula*.ing valve alfunctioned. The unit was returned
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to service at 0122 on November 3rd. Another trip occurred at 1044 on November 14th when a pressurizer level transmitter was valved out with another in trip. The unit was restarted at 1320 the same day but flux distribution problems caused power to be limited to 50% for a day. The unit is base loaded at 100%.
DAILY UNIT POWER OUTPUT DOCKET NO. 50-306 UNIT Prairie Island No. 2 DATE 791201 ,
COMPLETED BY A. A. Hunstad TI LEPHONE 612-388-4767 510NTil NOVEMBER 1979
!).\Y AVERAGE LOAD MWe-Net DAY AVERACE LOAD MWe-N.'t
- t. 495 17 523
-21 18 522 3 401 19 528
- c. 517 20 522
', 521 21 514 6 524 22 520 -
7 523 23 519 9 523 24 521 9
525 25 518 to 525 2 t> 518
- 1 527 27 520 t, 524 28 518 13 526 29 520 14 315 30 519 15 223 31 -
16 477 Average loads above 500 MNc-Net are due to cooler condenser circulating teater
OJf p?TNG DAT3 PT-PORT pg 80 >
DOCKET NO 50-306 DATE 791201 COMPLETED BY A. A. Hunstad OPERATING STATUS TELEPHONE 612-388-4767
- 1. Unit Name: Prairie Island No. 2
- 2. Reporting Period: November 1979 Notes
- 3. Licensed Thermal Power (MWt): 1650 4 Nameplate Rating (Gross MWe): 593 _,,
t
- 5. Design Electrical Rating (Net MWe): MO l
- 6. Maximum Dependable Capacity (Cross MWo): 531 [
C 7. Maximum Dependable Capacity (Ne* We': 500 g 8. If Changes Occur in Capacity Rar im.r (f rems Numbe- 3 Through 7) Since- I.a n t h po r t -
v a: Cive Reason: . _ _ _ _ . _ _ . _ . .. _ _.._.. .
cn
[ 9. Power Level To Which Restricted. I f Mw O'. t f rge) .
e F 10. Reasons for Restrictions, i f A r. - , , , , ,, , , , , , , _ _ _ _ _ _ _ , , , , , , , ,, _
Th in ." nth Yr-To-Date ai olative
- 11. Ho'ars In Reporting Period 720 8016 43342
- 12. Number Of Hours Reactor Was Criric;>l 699.2 7941.4 38385.0
- 13. Reactor Reserve Shutdown Hours 20.8 27.3 1406.0
- 14. Hours Cencrator On Line 691.6 7921.4 37657.0
- 15. Unit Rcserve Shutdown liours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated Of'..'!!) 1096602 12423406 58442691
- 17. Gross Electrical Energy Generate 3 ON!:' 367390 4085210 18672950
- 18. Net Electrical Energy Generat~ i!M:) 345703 3835162 17430750
- 19. Unit Service Factor 96.1 98.8 86.9
- 20. Unit Availability F.etor 96.1 98.8 86.9
- 21. Unit Capacity Facto - (Itsing EC Ne t.) 96.0 95.7 80.7
- 22. Unit Capacity Factor (Using DF.R Net) 90.6 90.3 76.1
- 23. Unit Forced Outage Rate 3.9 0.6 5.0
%. Shutdowns Scheduled Over Next 12 Months (Ty,c, Date and Duration of E ;h):
Refueling, January 1980, 5 Weeks
- 25. If Shut Down at End Of Report Pcciod. Estimated Date of Starrup:
10iIT .:t'J-'+.. 3 i i'.a 'O m 't~c. F.' ' :M AL., o' :* 21.. .- 3. 0. 6
. ? iiri2 .s 8 eit !. . . .-*2 d.h f .l.~. 2
- t';?T1E MG':111 --NOVD!BER 1979 - - - ,.
791201' '
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Cli . VA' VEX l : i ' Trip due to steam generator high
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l 791114 i F 1 2.6 G 3 N/A IA INSTRU Trip due to personnel error in g
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