ML19329A807: Difference between revisions
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{{#Wiki_filter:. . . . - - | {{#Wiki_filter:. . . . - - | ||
LICENSEE EVENT REPORT | LICENSEE EVENT REPORT | ||
)h ~ | )h ~ | ||
Co= raat stoCs LLJ l l l _sl i | |||
Co= raat stoCs LLJ l l l _sl | |||
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E .lolH IDlB1S11ji.- i,lt6 l Ol -l Gl 01 Ni P]F l-l0 ln3;a }4 1J1 11 1]I aol N. 3I$ | |||
.a,,co..::sr ceeen ~ | .a,,co..::sr ceeen ~ | ||
,,o.....v... ...e.,,a., ...o.,om.. . | ,,o.....v... ...e.,,a., ...o.,om.. . | ||
6 Coa'i p y G p 1 61 5 1 61..i 6l 3 4 I}t Or 8,2 ,9 7,7 1 161912181717 1 3 avawr ce sCaiPrio= | 6 Coa'i p y G p 1 61 5 1 61..i 6l 3 4 I}t Or 8,2 ,9 7,7 1 161912181717 1 3 avawr ce sCaiPrio= | ||
g , Reactor Coolant System Tave was less than 525 F in Mode 2, Startup. This; | g , Reactor Coolant System Tave was less than 525 F in Mode 2, Startup. This; g' placed the unit in the Action Statement of Technical Specification ; | ||
g' placed the unit in the Action Statement of Technical Specification ; | |||
m | m | ||
@l.s | @l.s 3.1.1.4. The reactor was shutdown within twelve miautes as required by 'I u | ||
3.1.1.4. The reactor was shutdown within twelve miautes as required by 'I u | |||
E [_the Action Statement. (NP-33-77-73) ] | E [_the Action Statement. (NP-33-77-73) ] | ||
3 :s = | 3 :s = | ||
0 l_ l | 0 l_ l ca amme at coor "su . a" naaTu"e7c"v'eIn't a veos a e som o>i E''i h c'nYt (DJ i 62z i zi z i zr z i 47zi - t_zJ i..zizi ziz.3l (NJ 7 89 so at 3 as l | ||
ca amme at coor "su . a" naaTu"e7c"v'eIn't a veos a e som o>i E''i h c'nYt (DJ i 62z i zi z i zr z i 47zi - t_zJ i..zizi ziz.3l (NJ 7 89 so at 3 as l | |||
CAUST oESCm8 piton | CAUST oESCm8 piton | ||
@l The cause is due_t,o.both procedure error in the shutdown procedure. I | @l The cause is due_t,o.both procedure error in the shutdown procedure. I | ||
Line 56: | Line 37: | ||
@' l PP 1102.10.1 and the fact that only three Reactor Coolant Pumps were in I as a | @' l PP 1102.10.1 and the fact that only three Reactor Coolant Pumps were in I as a | ||
@l operation. I a se ao | @l operation. I a se ao | ||
'% s EUS' ose.e a status ceWo av otSCovteev D.SCnertoom ii p_j i106EilII"6l gl NA l (Aj NA j 7 0 9 42 ** dl [%~ | '% s EUS' ose.e a status ceWo av otSCovteev D.SCnertoom ii p_j i106EilII"6l gl NA l (Aj NA j 7 0 9 42 ** dl [%~ | ||
me ' oe S"e'i"b a auovees or aCisvety toCatsoes er attEast i | me ' oe S"e'i"b a auovees or aCisvety toCatsoes er attEast i | ||
(_z_) ,[Y,z 1 NA - l l NA I | (_z_) ,[Y,z 1 NA - l l NA I | ||
, . , .. .o PER$oNNEL EMPoSURES mveeme n t vec ca.sceseveon is I NA | , . , .. .o PER$oNNEL EMPoSURES mveeme n t vec ca.sceseveon is I NA Q7,' l9 61 61 61 LE si s2 13 50 l | ||
Q7,' l9 61 61 61 LE si s2 13 50 l | |||
Pf ftsoNM(t INJusetts neuwet o. se mes tioes l | Pf ftsoNM(t INJusetts neuwet o. se mes tioes l | ||
QiaL61Ofbl 3 5 in [ NA tJ ao o0 9st1t CorestOutNCES 8 5 l NA I e u LOSS on oaheAGE To 0 ACILif v | QiaL61Ofbl 3 5 in [ NA tJ ao o0 9st1t CorestOutNCES 8 5 l NA I e u LOSS on oaheAGE To 0 ACILif v | ||
Line 74: | Line 50: | ||
l l s es n 1 aoottloseAt s ACTORS I' Ql | l l s es n 1 aoottloseAt s ACTORS I' Ql | ||
> es NA ''d | > es NA ''d | ||
% 1 y' f.d91 . | |||
% 1 | (419} 259-5000, Ext. 274 Dale Miller . | ||
y' f.d91 . | |||
(419} 259-5000, Ext. 274 | |||
Dale Miller | |||
. | |||
DVR #119-1 8001150 703 | DVR #119-1 8001150 703 | ||
* T . | * T . | ||
I TOLEDO EDISON COMPANY ' | |||
I | |||
TOLEDO EDISON COMPANY ' | |||
kj ' | kj ' | ||
DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-33-77-75 DATE OF EVENT: August 29, 1977 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Reactor Coolant System Tave less than 525 F. | DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-33-77-75 DATE OF EVENT: August 29, 1977 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Reactor Coolant System Tave less than 525 F. | ||
.:onditions Prior to Occurrence: The plant was in Mode 2, with Power (MWI) = 0 and Load (MWE) = 0. Reactor Coolant System pressure was 2155 psig and tempera-' | .:onditions Prior to Occurrence: The plant was in Mode 2, with Power (MWI) = 0 and Load (MWE) = 0. Reactor Coolant System pressure was 2155 psig and tempera-' | ||
ture was 5320F. Reactor power was being decreased from approximately 10-6 amps to approximately 10-8 amps. Preparations were being made to allow maintenance to inspect the Reactor Coolant Pump 1-1-2 Surge Capacitors. | ture was 5320F. Reactor power was being decreased from approximately 10-6 amps to approximately 10-8 amps. Preparations were being made to allow maintenance to inspect the Reactor Coolant Pump 1-1-2 Surge Capacitors. | ||
Description of Occurrence: At 0117 hours on August 29, 1977, the Main Feed Pump was removed from service. The Startup Feed Pump was on to provide minimum feed- ! | Description of Occurrence: At 0117 hours on August 29, 1977, the Main Feed Pump was removed from service. The Startup Feed Pump was on to provide minimum feed- ! | ||
water flow to the steam generators. At 0120 hours, average Reactor Coolant Sys-tem temperature decreased to 5250F, and continued to decrease. This placed the station into the Action Statement of Technical Specification 3,1.4. The Techni- | water flow to the steam generators. At 0120 hours, average Reactor Coolant Sys-tem temperature decreased to 5250F, and continued to decrease. This placed the station into the Action Statement of Technical Specification 3,1.4. The Techni- | ||
! j cal Specification requires average reactor coolant temperature (Tavg) to be main- | ! j cal Specification requires average reactor coolant temperature (Tavg) to be main- | ||
~ | ~ | ||
' tained at / 52507 while the reactor is critical. If Tavg decreases to less than i 5250F, the station must be in Hot Standby within 15 minutes. l When Tavg decreased to 5250F, the turbine bypass valves were shut momentarily to ) | ' tained at / 52507 while the reactor is critical. If Tavg decreases to less than i 5250F, the station must be in Hot Standby within 15 minutes. l When Tavg decreased to 5250F, the turbine bypass valves were shut momentarily to ) | ||
Line 110: | Line 68: | ||
The Shift Foreman ordered the ree.ctor shutdown. At 0129 hours, the reactor re- ) | The Shift Foreman ordered the ree.ctor shutdown. At 0129 hours, the reactor re- ) | ||
gulating rods were fully inserted. A shutdown margin calculation was performed and the reactor was verified to have a shutdown margin of 4.73% delta K/K. The | gulating rods were fully inserted. A shutdown margin calculation was performed and the reactor was verified to have a shutdown margin of 4.73% delta K/K. The | ||
~minimum Tavg temperature reached was 5120 F. The Operations Enginaar was informed of the occurrence. | ~minimum Tavg temperature reached was 5120 F. The Operations Enginaar was informed of the occurrence. | ||
Designation of Apparent Cause of Occurrence: A procedural error was one cause of this incident. The Shutdown and Cooldown Procedure, PP 1102.10.1, did not address i putting the Auxiliary Boiler on and switching steam loads to the Auxiliary Boiler until after reactnr power had been decreased to 10-8 amps. | Designation of Apparent Cause of Occurrence: A procedural error was one cause of this incident. The Shutdown and Cooldown Procedure, PP 1102.10.1, did not address i putting the Auxiliary Boiler on and switching steam loads to the Auxiliary Boiler until after reactnr power had been decreased to 10-8 amps. | ||
1 | 1 I | ||
j Contributing factors include the decay heat production of the new core was minimmi | |||
Contributing factors include the decay heat production of the new core was minimmi | |||
. and only three Reactor Coolant Pumps (RCP) were runnf*1g at the time. RCP l-1-2 l was out of service due to the failure of the surge capacitor at 1740 hours on | . and only three Reactor Coolant Pumps (RCP) were runnf*1g at the time. RCP l-1-2 l was out of service due to the failure of the surge capacitor at 1740 hours on | ||
! August 27, 1977. | ! August 27, 1977. | ||
l l O o | l l O o | ||
l i' . - . ._ - - - - - . - , .. - | |||
l | |||
i' . - . ._ - - - - - . - , .. | |||
. m r | |||
. m | |||
r | |||
. TOLEDO EDISON COMPANY DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION i | . TOLEDO EDISON COMPANY DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION i | ||
SUPPLEMENTAL INFORMATION FOR LER NP-33-77-75 PAGE 2 i | SUPPLEMENTAL INFORMATION FOR LER NP-33-77-75 PAGE 2 i | ||
Line 139: | Line 85: | ||
was not endangered. As a result of this occurrence, no abnormal instrumentation | was not endangered. As a result of this occurrence, no abnormal instrumentation | ||
? upsets were observed. Pressure was maintained in the Reactor Coolant System. No ether abnormal incidents occurred. | ? upsets were observed. Pressure was maintained in the Reactor Coolant System. No ether abnormal incidents occurred. | ||
I Corrective Action: As stated in the Description of Occurrence, the reactor was i==adiately shutdown to remove the station from the Action Statement. | I Corrective Action: As stated in the Description of Occurrence, the reactor was i==adiately shutdown to remove the station from the Action Statement. | ||
x | x | ||
! To prevent further recurrences, the Plant Shutdown and Cooldown Procedure, j PP 1102.10.1, is being revised. Revision is being made to have the Auxiliary i Boiler in service and the major steam loads transferred to the Auxiliary Boiler | ! To prevent further recurrences, the Plant Shutdown and Cooldown Procedure, j PP 1102.10.1, is being revised. Revision is being made to have the Auxiliary i Boiler in service and the major steam loads transferred to the Auxiliary Boiler | ||
! prior to decreasing reactor power to 10-8 amps. | ! prior to decreasing reactor power to 10-8 amps. | ||
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Failure Data: No previous similar events have occurred. | Failure Data: No previous similar events have occurred. | ||
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_}} | _}} |
Latest revision as of 21:50, 31 January 2020
ML19329A807 | |
Person / Time | |
---|---|
Site: | Davis Besse |
Issue date: | 09/28/1977 |
From: | Miller D TOLEDO EDISON CO. |
To: | |
Shared Package | |
ML19329A801 | List: |
References | |
NUDOCS 8001150703 | |
Download: ML19329A807 (3) | |
Text
. . . . - -
LICENSEE EVENT REPORT
)h ~
Co= raat stoCs LLJ l l l _sl i
f.*au' ' s oc ~,. ~em. . ",9ti ' <,vJ.~ '
6 E .lolH IDlB1S11ji.- i,lt6 l Ol -l Gl 01 Ni P]F l-l0 ln3;a }4 1J1 11 1]I aol N. 3I$
.a,,co..::sr ceeen ~
,,o.....v... ...e.,,a., ...o.,om.. .
6 Coa'i p y G p 1 61 5 1 61..i 6l 3 4 I}t Or 8,2 ,9 7,7 1 161912181717 1 3 avawr ce sCaiPrio=
g , Reactor Coolant System Tave was less than 525 F in Mode 2, Startup. This; g' placed the unit in the Action Statement of Technical Specification ;
m
@l.s 3.1.1.4. The reactor was shutdown within twelve miautes as required by 'I u
E [_the Action Statement. (NP-33-77-73) ]
3 :s =
0 l_ l ca amme at coor "su . a" naaTu"e7c"v'eIn't a veos a e som o>i Ei h c'nYt (DJ i 62z i zi z i zr z i 47zi - t_zJ i..zizi ziz.3l (NJ 7 89 so at 3 as l
CAUST oESCm8 piton
@l The cause is due_t,o.both procedure error in the shutdown procedure. I
=o w
@' l PP 1102.10.1 and the fact that only three Reactor Coolant Pumps were in I as a
@l operation. I a se ao
'% s EUS' ose.e a status ceWo av otSCovteev D.SCnertoom ii p_j i106EilII"6l gl NA l (Aj NA j 7 0 9 42 ** dl [%~
me ' oe S"e'i"b a auovees or aCisvety toCatsoes er attEast i
(_z_) ,[Y,z 1 NA - l l NA I
, . , .. .o PER$oNNEL EMPoSURES mveeme n t vec ca.sceseveon is I NA Q7,' l9 61 61 61 LE si s2 13 50 l
Pf ftsoNM(t INJusetts neuwet o. se mes tioes l
QiaL61Ofbl 3 5 in [ NA tJ ao o0 9st1t CorestOutNCES 8 5 l NA I e u LOSS on oaheAGE To 0 ACILif v
- otsC a ses soas
(
@,tver z 1 NA i
, a o . To w l
i PUst:Civv - I mr l NA ~
l l s es n 1 aoottloseAt s ACTORS I' Ql
> es NA d
% 1 y' f.d91 .
(419} 259-5000, Ext. 274 Dale Miller .
DVR #119-1 8001150 703
- T .
I TOLEDO EDISON COMPANY '
kj '
DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-33-77-75 DATE OF EVENT: August 29, 1977 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Reactor Coolant System Tave less than 525 F.
.:onditions Prior to Occurrence: The plant was in Mode 2, with Power (MWI) = 0 and Load (MWE) = 0. Reactor Coolant System pressure was 2155 psig and tempera-'
ture was 5320F. Reactor power was being decreased from approximately 10-6 amps to approximately 10-8 amps. Preparations were being made to allow maintenance to inspect the Reactor Coolant Pump 1-1-2 Surge Capacitors.
Description of Occurrence: At 0117 hours0.00135 days <br />0.0325 hours <br />1.934524e-4 weeks <br />4.45185e-5 months <br /> on August 29, 1977, the Main Feed Pump was removed from service. The Startup Feed Pump was on to provide minimum feed- !
water flow to the steam generators. At 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />, average Reactor Coolant Sys-tem temperature decreased to 5250F, and continued to decrease. This placed the station into the Action Statement of Technical Specification 3,1.4. The Techni-
! j cal Specification requires average reactor coolant temperature (Tavg) to be main-
~
' tained at / 52507 while the reactor is critical. If Tavg decreases to less than i 5250F, the station must be in Hot Standby within 15 minutes. l When Tavg decreased to 5250F, the turbine bypass valves were shut momentarily to )
maintain system pressure. Gland Steam was transferred to the Auxiliary Boiler !
and the Main Steam Line Warm-up Valves MS 1299A and MS 1299B were closed, to reduce stesa consumption.
The Shift Foreman ordered the ree.ctor shutdown. At 0129 hours0.00149 days <br />0.0358 hours <br />2.132936e-4 weeks <br />4.90845e-5 months <br />, the reactor re- )
gulating rods were fully inserted. A shutdown margin calculation was performed and the reactor was verified to have a shutdown margin of 4.73% delta K/K. The
~minimum Tavg temperature reached was 5120 F. The Operations Enginaar was informed of the occurrence.
Designation of Apparent Cause of Occurrence: A procedural error was one cause of this incident. The Shutdown and Cooldown Procedure, PP 1102.10.1, did not address i putting the Auxiliary Boiler on and switching steam loads to the Auxiliary Boiler until after reactnr power had been decreased to 10-8 amps.
1 I
j Contributing factors include the decay heat production of the new core was minimmi
. and only three Reactor Coolant Pumps (RCP) were runnf*1g at the time. RCP l-1-2 l was out of service due to the failure of the surge capacitor at 1740 hours0.0201 days <br />0.483 hours <br />0.00288 weeks <br />6.6207e-4 months <br /> on
! August 27, 1977.
l l O o
l i' . - . ._ - - - - - . - , .. -
. m r
. TOLEDO EDISON COMPANY DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION i
SUPPLEMENTAL INFORMATION FOR LER NP-33-77-75 PAGE 2 i
f
)
Analysis of Occurrence: The health'and safety of the public and station employees 3
was not endangered. As a result of this occurrence, no abnormal instrumentation
? upsets were observed. Pressure was maintained in the Reactor Coolant System. No ether abnormal incidents occurred.
I Corrective Action: As stated in the Description of Occurrence, the reactor was i==adiately shutdown to remove the station from the Action Statement.
x
! To prevent further recurrences, the Plant Shutdown and Cooldown Procedure, j PP 1102.10.1, is being revised. Revision is being made to have the Auxiliary i Boiler in service and the major steam loads transferred to the Auxiliary Boiler
! prior to decreasing reactor power to 10-8 amps.
4 i -
Failure Data: No previous similar events have occurred.
i i
I 4
l i
l i
6 a
5
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