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 Issue dateTitleTopic
ML20042D84030 March 1990Supplement to 900105 Special Rept Re Inoperability of Diesel Fire Pump Due to Failure in Right Angle Gear Drive. Broken Studs Replaced W/Cap Screws Per Vendor Recommendations & Preventive Maint Activity Added
ML20012C68615 March 1990Ro:On 900204,daily Functional Test Not Done for Portable Fire Detection Sys.Caused by Shift Supervisor Failure to Ensure That Test Was Done.Requirements of Daily Functional Test Will Be Added to Operations Dept Monthly Activity Log
ML20005F4405 January 1990Special Rept:On 891129,diesel Fire Pump Failed While Providing Water to Support Cleaning Activity Unrelated to Fire Protection Sys.Caused by Broken Studs.Broken Studs Replaced W/Cap Screws Per Vendor Current Recommendation
ML20050A96522 March 1982RO NP-09-82-02:on 820222,free Chlorine Discharged in Excess of Ets,Section 2.3.1 Limit of 2-h Per Day.Caused by Equipment Deficiency.Feed Rate Will Be Verified During Chlorination Sys Lineup Changes
ML20040G1193 February 1982RO NP-09-82-01:on 820104,max Discharge Temp Above Ambient Lake Temp Limit Was Exceeded During Unusual Weather Change. Alarm T189 Setpoint Changed from 15 F to 17 F
ML20010G30731 August 1981Ro:Ie Bulletin 80-11 Analysis Determined That Listed Walls Would Be Overstressed During Seismic Event
ML20005B38325 June 1981RO NP-09-81-01:on 810526,max Discharge Temp Differential, Above Ambient Lake Temp,Was Slightly Exceeded.Caused by Difficulty in Maintaining Balance Between Operating to Prevent Exceeding Limit & to Prevent Cooling Tower Damage
ML19350C22617 March 1981Corrected Page 3 to Supplemental Info for LER 80-090
ML19341C23918 February 1981Forwards Revised Supplemental Info Sheets for LER 79-050 Re Unplanned Reactivity Insertion.Caused by Mechanical, Personnel & Procedural Error.Valve Mu 39 Disassembled & Gaskets InstalledShutdown Margin
ML19340C8281 December 1980Supplemental Info Re RO NP-32-80-12:on 800724,w/unit in Mode 5,loss of Decay Heat Flow Observed.No Indication for Valve Position of Decay Heat Isolation Valve DH12.Revision Replaces Supplemental Info for RO 80-058
ML19345A84618 November 1980Ro:On 801117 All Four Containment Pressure Transmitters Found to Be Inoperable Due to Surveillance Test Procedure Error.Emergency Tech Spec Relief Requested
ML19337B4289 September 1980RO NP-09-80-01:on 800116 & 0210,discharge Temp for Liquid Effluents Exceeded 20 F Above Lake Temp Due to Procedural Deficiencies.Cooling Tower Was Operated in Bypass Mode Causing Temp to Elevate Above Normal Temp During Startup
ML19331B9034 August 1980Ro:On 800803,heat Decay Flow Interrupted.Caused by Traveling Decay Heat Isolation Valve DH11 During Safety Features Actuation Sys Removal.Bistable Reinstalled & Pump Restarted within 3 Minutes
ML19331B90026 July 1980Ro:On 800724,decay Heat Flow Interrupted Twice.Caused by Inadvertently Shorted Decay Heat Isolation Valve DH12 Fuse Clip to Ground & by Tripped Output Bistable BA413 During Facility Change Request Work
ML19320B99227 June 1980Ro:On 800627,pipe Support HCB-40-41 on Component Cooling Water Supply to Control Rod Drive Mechanism Found Not Installed.Also,Lateral Restraint CCA-8-H15 on Pressurizer Relief Inlet Located 9 Inches from Analyzed LocationEarthquake
ML19312E16423 May 1980Ro:On 800430,chemistry & Health Physics Individual Received Dose of 4.7 Rems.Cause of Exposure Was Erroneously Low Reading on Meter or Misreading of Teletector.Individual Was Removed from Working in Radiation Controlled AreasLocked High Radiation Area
ML19309G73419 April 1980Ro:On 800418,discovered That Level of RCS Had Dropped Significantly.Control Room Operator Tripped Running Decay Heat Pump Because of Concern for Possible Loss of Suction. Caused by Vent Valve in Decay Heat Sys
ML19305C9652 April 1980NP-11-80-01,describing 791022 Beach Well Sample Which Indicated Tritium Concentration Three Times Beyond Normal. Procedure Changed to Require Monthly Rather than Quarterly Sampling
ML19294B51915 February 1980Ro:Reanalysis of RCS Pipe Restraints Revealed Less Conservative Design than Assumed on Two Reactor Coolant Hot Leg Whip Restraints Near Steam Generator Tops.Cause Unstated.Action During Refueling Outage in Eight Wks
ML19296A92612 February 1980RO-NP-09-80-01:on 800116,during Normal Plant Startup,Temp Differential Limit Between Station Liquid Effluent Discharge & Lake Temp Was Exceeded.Caused by Operation of Plant W/ Cooling Tower in Bypass Mode
ML19276H55113 November 1979Ro:On 791112,during Seismic Supports Analysis,Safety Factors on 11 Seismic Supports Found Lower than Expected.Unit Was in Cold Shutdown.Caused by Design Error in Initial Stress Calculations.Hangers Will Be Modified
ML19210D70312 November 1979Ro:On 791109,steam & Feedwater Rupture Control Sys Steam Generator Low Level Trip Setpoint Discovered Less Conservative than Tech Spec Requirements.Caused by Level Transmitter Setpoint Drift.Design Work Underway
ML19254F9262 November 1979RO-NP-09-79-06:on 791008,station Vent Recorder UJR5023 Was Inoperable.Caused by Recorder Not Advancing Paper Under Printer Due to Drive Shaft & Gear Mechanism Jam.All Ujr Recorders Will Be Replaced
ML19275A59127 September 1979RO NP-09-79-05:on 790831,during Review of Station Vent Data, Physicist Determined That Vent Recorder Was Inoperable. Caused by Inoperable Computer Point.Recorder Recalibr & Computer Input Card Changed
ML19253A09629 June 1979Notification of Violation of Tech Spec 3.4.1 on 790628. During Surveillance Testing on Reactor Protection Sys Channel 4,instrument & Control Technician Shorted Several Terminals W/Allegator Clip
ML19282B70528 February 1979Ro:On 790228,during Maint,Startup Transformer 01 Was de- Energized,But Addl Surveillance Required by Action Statement of Tech Spec 3.8.1.1 Was Not Performed.Caused by Personnel Oversight.Surveillance Testing Begun Approx 2-h Later
ML19282A86821 February 1979RO NP-09-79-04:on 790126,station Vent Monitor Re 2024 Generated Excessive Noise;Later Pump for Station Vent Monitor Re 2025 Seized.Caused by Normal Vane Wear & Low Flow During Testing.Pumps for Both Monitors ReplacedGrab sample
ML19269C5951 February 1979RO NP-09-79-02:on 790104,svc Water Sys Header Outflow Radiation Monitor Re 8432 Found Inoperable.Caused by Design Error Resulting in Component Deficiency.Flow Switch on Re 8432 Replaced & Facility Change Request PreparedGrab sample
ML19256A80112 January 1979Reportable Occurrence NP-09-78-01:on 781215,during Routine Review of Shift Foreman'S Log,Discovered Svc Water Sys Out Header Radiation Monitor RE8432 Had Been Inoperable.Caused Apparently by Design Error.Facility Change Request PreparedGrab sample
ML19289C3685 January 1979Reportable Occurrence NP-09-78-03 on 781209-10:discharge Temp for Station Liquid Effluents Exceeded 20 F Limit Above Lake Temp.Caused in Part by Design Deficiency in Sys Used to Determine Effluent Liquid Discharge Temp
ML19256A7862 January 1979to Suppl Info Sheet for LER NP-33-78-120 on 781005.Other Svc Water Valves Associated W/Component Cooling Water Heat Exchangers Were Inspected for Similar Inoperable Conditions.No Problems NotedStroke time
ML19261B2122 January 1979RO NP-09-79-01:on 790102,station Ventilation Radiation Monitors Re 2024 & Re 2025 Found Inoperable.Apparently Caused by Component Failure.Previous Occurrences on 770829 & 771214 Not Reported Due to Personnel Error.Units RepairedGrab sample
ML19263C17615 December 1978RO-NP-09-78-01 on 781215:svc Water Sys Out Header Radiation Monitor Was Inoperable.Caused by Component Failure Due to Design Error.Personnel Informed of Environ Tech SpecsGrab sample
ML20027A37522 September 1978RO NP-33-77-64 on 770827:reactor Coolant Pump 1-1-2 Tripped Removing One of Two Reactor Coolant Pumps of Loop from Operation.B&C Phase Surge Capacitors Were Discovered to Be Damaged Due to Design Deficiency
ML19329B03518 July 1978RO 78-072-04-T-0:on 780710,station Effluent Chlorine Concentration Exceeded Tech Spec Limits.Caused by Personnel Mistakenly Returning Intake Chlorinator to Automatic Return to Svc to Be Expedited
ML19317F53117 April 1978Ro:On 780414,taped Electrical Terminations on Containment Air Cooler Units Found Not to Have Required LOCA Qualification.Caused by Mfg Inadequacy.Terminations to Be Reworked W/Qualified Tubing
ML19317F56224 February 1978Ro:On 780221,control Rod Drive Sys Trip Circuit Breaker Cabinets Found to Have Inadequate Welds.Welds to Be Lengthened to Conform W/Shaker Table Test During Apr 1978 Outage
ML19317F53816 November 1977Ro:On 771110,defect Discovered in Auxiliary Feed Pump Turbine Installed at Facility.Involves Potential for Governing Valve to Close While Turbine Not in Svc.Closure Caused by Excessive Vibration of Adjacent Startup Feed Pump
ML19329A78212 October 1977RO NP-33-77-73:on 770917,makeup Pump 1-2 Removed from Svc to Allow Repair of Oil Leak on Outboard Bearing Plate. Caused by Design Deficiency in End Plate Seal.New O-ring Installed
ML19317F53511 October 1977Ro:On 770930,defect Discovered in Governor on Auxiliary Feed Pumps Installed at Facility.Potential Created for Failure of Both Auxiliary Feed Pumps to Come Up to Design Speed Upon Startup.Superceded Util 771005 Ltr
ML19329A8124 October 1977RO NP-33-77-76:on 770901,reactor Coolant Pump 1-2-1 Tripped.Caused by Low Seal Injection & Component Cooling Water Flow,Due to Personnel Error.Instrument Air Valves Relabeled
ML19329A7964 October 1977RO NP-33-77-74:on 770907,decay Heat Suction Valve DH-12 Closed During Switching from Normal to Alternate Power Supply for Valve.Caused by Design Deficiency in Interlock/Control Circuit.Wiring Change in Process
ML19329A80728 September 1977RO NP-33-77-75:on 770829,RCS Have Less than 525 F in Mode 2,startup.Caused by Procedure Error in Shutdown Procedure & Fact That Only Three Reactor Coolant Pumps Were in Operation.Reactor Shut DownShutdown Margin
ML19319B82227 September 1977RO NP-33-77-62:on 770825,auxiliary Feed Pump 1-1 Rendered Inoperable During Permanent Pressure Relief Valve Psv 4980 Installation.Relief Valve Installation Completed,Auxiliary Feed Pump Cooling Water Restored & Pump Declared Operable
ML19329B65226 September 1977RO NP-09-77-02:on 770830,during Surveillance Test,Personnel Discovered That Weekly Gaseous Grab Sample from Station Vent Monitor Was Not Obtained.Caused by Component Failure. Stack Radiation Monitor Returned to SvcGrab sample
ML19319B81522 September 1977RO NP-33-77-59:on 770826,intermediate Range Nuclear Instrument NI-3 Disconnected from Reactor Protection Sys & Connected to Reactimeter to Perform Reactivity Measurements. NI-4 Operable During Test.Power Level Maintained at 5%
ML19319B80922 September 1977RO NP-33-77-64:on 770827,reactor Coolant Pump Motor 1-1-2 Tripped W/Instantaneous Ground & Differential Current Relay Indicating Fault.Caused by Damaged B&C Phase Surge Capacitors.Capacitors Repaired & Setpoints Reset
ML19274D93922 September 1977LER NP-33-77-64 on 770827:reactor Coolant Pump 1-1-2 Tripped,Removing One of Two Reactor Coolant Pumps from Operation.Caused by Damage to Surge Capacitors Due to Insufficient Mounting Base
ML19289D51722 September 1977Updated RO NP-33-77-64 on 770827:reactor Coolant Pump 1-1-2 Tripped,Removing Reactor Coolant Pump from Operation.Caused by Damaged Surge Capacitors.Capacitors on All Four Reactor Coolant Pump Motors Replaced W/Units of New Design
ML19319B78619 September 1977RO NP-33-77-69:on 770823,hydraulic Snubber EBD-19-H 144 Discovered Upside Down.Caused by Loose Lock Nut on Snubber Extension Piece Allowing Rotation & Placing Fluid Reservoir Below Cylinder.Snubber Purged & Tested.Lock Nut Tightened