IR 05000220/2013004: Difference between revisions

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| issue date = 11/13/2013
| issue date = 11/13/2013
| title = IR 05000220-13-004, 05000410-13-004; 07/01/2013 - 09/30/2013; Nine Mile Point Nuclear Station (Nmpns), Units 1 and 2; Routine Integrated Inspection Report
| title = IR 05000220-13-004, 05000410-13-004; 07/01/2013 - 09/30/2013; Nine Mile Point Nuclear Station (Nmpns), Units 1 and 2; Routine Integrated Inspection Report
| author name = Schroeder D L
| author name = Schroeder D
| author affiliation = NRC/RGN-I/DRP/PB1
| author affiliation = NRC/RGN-I/DRP/PB1
| addressee name = Costanzo C
| addressee name = Costanzo C
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| docket = 05000220, 05000410
| docket = 05000220, 05000410
| license number = DPR-063, NPF-069
| license number = DPR-063, NPF-069
| contact person = Schroeder D L
| contact person = Schroeder D
| document report number = IR-13-004
| document report number = IR-13-004
| document type = Inspection Report, Letter
| document type = Inspection Report, Letter
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:UNITED STATES ber 13, 2013
[[Issue date::November 13, 2013]]


Mr. Christopher Costanzo Vice President Nine Mile Point Nuclear Station, LLC Constellation Energy Nuclear Group, LLC P.O. Box 63 Lycoming, NY 13093
==SUBJECT:==
 
NINE MILE POINT NUCLEAR STATION, LLC - NRC INTEGRATED INSPECTION REPORT 05000220/2013004 AND 05000410/2013004
SUBJECT: NINE MILE POINT NUCLEAR STATION, LLC - NRC INTEGRATED INSPECTION REPORT 05000220/2013004 AND 05000410/2013004


==Dear Mr. Costanzo:==
==Dear Mr. Costanzo:==
On September 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Nine Mile Point Nuclear Station, LLC (NMPNS) Units 1 and 2. The enclosed inspection report documents the inspection results, which were discussed on October 24, 2013, with you and other members of your staff.
On September 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Nine Mile Point Nuclear Station, LLC (NMPNS) Units 1 and 2. The enclosed inspection report documents the inspection results, which were discussed on October 24, 2013, with you and other members of your staff.


The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.


No findings were identified during this inspection.
No findings were identified during this inspection.


In accordance with Title 10 of the Code of Federal Regulations 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with Title 10 of the Code of Federal Regulations 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of the NRCs Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Sincerely,/RA/ Daniel L. Schroeder, Chief Reactor Projects Branch 1
 
Division of Reactor Projects


Docket Nos: 50-220 and 50-410 License Nos: DPR-63 and NPF-69  
Sincerely,
/RA/
Daniel L. Schroeder, Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos: 50-220 and 50-410 License Nos: DPR-63 and NPF-69


===Enclosure:===
===Enclosure:===
Inspection Report 05000220/2013004 and 05000410/2013004 w/  
Inspection Report 05000220/2013004 and 05000410/2013004 w/ Attachment: Supplementary Information
 
===Attachment:===
Supplementary Information  
 
cc w/encl: Distribution via ListServ
 
ML13317B750 SUNSI Review Non-Sensitive Sensitive Publicly Available Non-Publicly Available OFFICE klm RI/DRP RI/DRP RI/DRP NAME KKolaczyk/KK via telecon ARosebrook/AAR DSchroeder/DLS DATE 11/12/13 11/12/13 11/13/13 Enclosure 1U.S. NUCLEAR REGULATORY COMMISSION REGION I Docket Nos: 50-220 and 50-410
 
License Nos: DPR-63 and NPF-69
 
Report Nos: 05000220/2013004 and 05000410/2013004
 
Licensee: Constellation Energy Nuclear Group, LLC (CENG)


REGION I==
Docket Nos: 50-220 and 50-410 License Nos: DPR-63 and NPF-69 Report Nos: 05000220/2013004 and 05000410/2013004 Licensee: Constellation Energy Nuclear Group, LLC (CENG)
Facility: Nine Mile Point Nuclear Station, LLC (NMPNS)
Facility: Nine Mile Point Nuclear Station, LLC (NMPNS)
Units 1 and 2  
Units 1 and 2 Location: Oswego, NY Dates: July 1, 2013, through September 30, 2013 Inspectors: K. Kolaczyk, Senior Resident Inspector E. Miller, Resident Inspector J. Ambrosini, Senior Resident Inspector J. DeBoer, Project Engineer B. Dionne, Health Physicist S. Hammann, Senior Health Physicist P. Kaufman, Senior Reactor Inspector J. Krafty, Resident Inspector J. Laughlin, Emergency Preparedness Inspector Approved by: Daniel L. Schroeder, Chief Reactor Projects Branch 1 Division of Reactor Projects Enclosure


Location: Oswego, NY
=SUMMARY=
 
IR 05000220/2013004, 05000410/2013004; 07/01/2013 - 09/30/2013; Nine Mile Point Nuclear
Dates: July 1, 2013, through September 30, 2013  
 
Inspectors: K. Kolaczyk, Senior Resident Inspector E. Miller, Resident Inspector J. Ambrosini, Senior Resident Inspector J. DeBoer, Project Engineer B. Dionne, Health Physicist S. Hammann, Senior Health Physicist P. Kaufman, Senior Reactor Inspector J. Krafty, Resident Inspector J. Laughlin, Emergency Preparedness Inspector
 
Approved by: Daniel L. Schroeder, Chief Reactor Projects Branch 1
 
Division of Reactor Projects
 
Enclosure 2


=SUMMARY=
Station (NMPNS), Units 1 and 2; Routine Integrated Inspection Report.
IR 05000220/2013004, 05000410/2013004; 07/01/2013 - 09/30/2013; Nine Mile Point Nuclear Station (NMPNS), Units 1 and 2; Routine Integrated Inspection Report.


The report covered a 3-month period of inspection by resident inspectors and announced inspections performed by regional inspectors. The inspectors identified no findings during this period. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "R eactor Oversight Process," Revision 4.
The report covered a 3-month period of inspection by resident inspectors and announced inspections performed by regional inspectors. The inspectors identified no findings during this period. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4.


No findings were identified.
No findings were identified.
4


=REPORT DETAILS=
=REPORT DETAILS=
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Reactor power was returned to 100 percent later that day. Unit 1 remained at full power for the remainder for the inspection period.
Reactor power was returned to 100 percent later that day. Unit 1 remained at full power for the remainder for the inspection period.


Unit 2 began the inspection period at 100 percent power. On July 19, 2013, reactor power was decreased to 98 percent due to high condensate pump discharge header temperature. Power was returned to 100 percent later that day. On September 7, Unit 2 reduced power to 85  
Unit 2 began the inspection period at 100 percent power. On July 19, 2013, reactor power was decreased to 98 percent due to high condensate pump discharge header temperature. Power was returned to 100 percent later that day. On September 7, Unit 2 reduced power to 85 percent to conduct turbine stop valve testing, returning to full power that same day. On September 21, Unit 2 reduced power to 70 percent to perform a control rod pattern adjustment and scram time testing. Unit 2 returned to full power on September 22 and operated at full power for the remainder of the inspection period.
 
percent to conduct turbine stop valve testing, returning to full power that same day. On September 21, Unit 2 reduced power to 70 percent to perform a control rod pattern adjustment and scram time testing. Unit 2 returned to full power on September 22 and operated at full power for the remainder of the inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
 
{{a|1R01}}
{{a|1R01}}
==1R01 Adverse Weather Protection==
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01|count=1}}
{{IP sample|IP=IP 71111.01|count=1}}
Readiness for Seasonal Extreme Weather Conditions
Readiness for Seasonal Extreme Weather Conditions


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a review of the station's readiness for the onset of seasonal high temperatures. The review focused on Unit 1 batteries 11 and 12 and emergency diesel generators (EDGs) 102 and 103 on July 17, 2013. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), technical specifications (TSs), and the corrective action program (CAP) to determine what temperatures or other seasonal weather could challenge these systems, and to ensure CENG personnel had adequately prepared for these challenges. The inspectors reviewed station procedures including CENG's seasonal weather readiness procedure and applicable operating procedures. The inspectors performed walkdowns of the selected systems to ensure station personnel identified issues that could challenge the operability of the systems during hot weather conditions. Documents reviewed for each section of this inspection report are listed in the Attachment.
The inspectors performed a review of the stations readiness for the onset of seasonal high temperatures. The review focused on Unit 1 batteries 11 and 12 and emergency diesel generators (EDGs) 102 and 103 on July 17, 2013. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), technical specifications (TSs), and the corrective action program (CAP) to determine what temperatures or other seasonal weather could challenge these systems, and to ensure CENG personnel had adequately prepared for these challenges. The inspectors reviewed station procedures including CENGs seasonal weather readiness procedure and applicable operating procedures.
 
The inspectors performed walkdowns of the selected systems to ensure station personnel identified issues that could challenge the operability of the systems during hot weather conditions. Documents reviewed for each section of this inspection report are listed in the Attachment.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R04}}
{{a|1R04}}
==1R04 Equipment Alignment==
==1R04 Equipment Alignment==


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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed partial walkdowns of the following systems:  
The inspectors performed partial walkdowns of the following systems:
 
Unit 2 Division I standby gas treatment system (SGTS) following functional testing on July 18, 2013 Unit 1 uninterruptible power supply (UPS) system for the reactor protection system bus 11 following the trip of the alternating current (AC) breaker for UPS 162A and B on July 22, 2013 Unit 1 offsite power systems following testing on EDG 102 on July 25, 2013 Unit 2 high-pressure core spray (HPCS) system while the reactor core isolation cooling (RCIC) system was out of service (OOS) for planned maintenance on August 6, 2013 The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the UFSAR, TSs, work orders (WOs), condition reports (CRs), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether CENG staff had properly identified equipment issues and entered them into the CAP for resolution with the appropriate significance characterization.
Unit 2 Division I standby gas treatment system (SGTS) following functional testing on July 18, 2013 Unit 1 uninterruptible power supply (UPS) system for the reactor protection system bus 11 following the trip of the alternating current (AC) breaker for UPS 162A and B  
 
on July 22, 2013 Unit 1 offsite power systems following testing on EDG 102 on July 25, 2013 Unit 2 high-pressure core spray (HPCS) system while the reactor core isolation cooling (RCIC) system was out of service (OOS) for planned maintenance on August 6, 2013  
 
The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the UFSAR, TSs, work orders (WOs), condition reports (CRs), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions. The inspectors also performed field walkdowns of accessible portions of t he systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether CENG staff had properly identified equipment issues and entered them into the CAP for resolution with the appropriate significance characterization.


====b. Findings====
====b. Findings====
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====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R05}}
{{a|1R05}}
==1R05 Fire Protection==
==1R05 Fire Protection==


Line 150: Line 116:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed a fire brigade drill scenario conducted on August 27, 2013, that involved a fire on the first floor of the Unit 2 operations building. The inspectors evaluated the readiness of the plant fire brigade to fight fires. The inspectors verified that CENG personnel identified deficiencies, openly discussed them in a self-critical manner at the debrief, and took appropriate corrective actions as required. The inspectors evaluated specific attributes as follows:
The inspectors observed a fire brigade drill scenario conducted on August 27, 2013, that involved a fire on the first floor of the Unit 2 operations building. The inspectors evaluated the readiness of the plant fire brigade to fight fires. The inspectors verified that CENG personnel identified deficiencies, openly discussed them in a self-critical manner at the debrief, and took appropriate corrective actions as required. The inspectors evaluated specific attributes as follows:
 
Proper wearing of turnout gear and self-contained breathing apparatus Proper use and layout of fire hoses Employment of appropriate fire-fighting techniques Sufficient fire-fighting equipment brought to the scene Effectiveness of command and control Search for victims and propagation of the fire into other plant areas Smoke removal operations Utilization of pre-planned strategies Adherence to the pre-planned drill scenario Drill objectives met The inspectors also evaluated the fire brigades actions to determine whether these actions were in accordance with CENGs fire-fighting strategies.
Proper wearing of turnout gear and self-contained breathing apparatus Proper use and layout of fire hoses Employment of appropriate fire-fighting techniques Sufficient fire-fighting equipment brought to the scene Effectiveness of command and control Search for victims and propagation of the fire into other plant areas Smoke removal operations Utilization of pre-planned strategies Adherence to the pre-planned drill scenario Drill objectives met The inspectors also evaluated the fire brigade's actions to determine whether these actions were in accordance with CENG's fire-fighting strategies.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|1R06}}
{{a|1R06}}
==1R06 Flood Protection Measures==
==1R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06|count=2}}
{{IP sample|IP=IP 71111.06|count=2}}
Line 172: Line 137:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted an inspection of underground bunkers/manholes subject to flooding that contain cables whose failure could affect risk-significant equipment. The inspectors performed walkdowns of risk-significant areas, including Unit 2 manholes MH-1 and MH-3 which contain power cables for the high-pressure coolant spray system pump, to verify that the cables were not submerged in water, that cables and/or splices appeared intact, and to observe the condition of cable support structures. The inspectors reviewed CENG corrective actions initiated following a July 22, 2013, discovery that a dewatering system, which had been installed in 2012 to dewater manholes MH-1 and MH-3, had failed to properly operate, and as a result, several feet of water had accumulated in the cable vaults. The performance deficiency surrounding this issue is discussed in greater detail in NRC Inspection Report 05000410/2013007
The inspectors conducted an inspection of underground bunkers/manholes subject to flooding that contain cables whose failure could affect risk-significant equipment. The inspectors performed walkdowns of risk-significant areas, including Unit 2 manholes MH-1 and MH-3 which contain power cables for the high-pressure coolant spray system pump, to verify that the cables were not submerged in water, that cables and/or splices appeared intact, and to observe the condition of cable support structures. The inspectors reviewed CENG corrective actions initiated following a July 22, 2013, discovery that a dewatering system, which had been installed in 2012 to dewater manholes MH-1 and MH-3, had failed to properly operate, and as a result, several feet of water had accumulated in the cable vaults. The performance deficiency surrounding this issue is discussed in greater detail in NRC Inspection Report 05000410/2013007. For those cables found submerged in water, the inspectors verified that CENG staff had conducted an operability evaluation for the cables and were implementing appropriate corrective actions.
. For those cables found submerged in water, the inspectors verified that CENG staff had conducted an operability evaluation for the cables and were implementing appropriate corrective actions.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R11}}
{{a|1R11}}
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
 
{{IP sample|IP=IP 71111.11Q}}
(71111.11Q)
 
===.1 Quarterly Review of Licensed Operator Requalification Testing and Training (2 samples)===
===.1 Quarterly Review of Licensed Operator Requalification Testing and Training (2 samples)===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed:
The inspectors observed:
 
Unit 1 licensed operator training simulator scenario which included a control rod drive failure, failure of power board 11, and a leak in the reactor water cleanup system on September 3, 2013 Unit 2 licensed operator training simulator scenario which included a loss of instrument air, a loss of a control rod drive pump, a stuck open safety relief valve, and a stuck open turbine bypass valve on September 3, 2013 The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classifications made by the shift manager and the TS action statements entered by the shift technical advisor.
Unit 1 licensed operator training simulator scenario which included a control rod drive failure, failure of power board 11, and a leak in the reactor water cleanup system on September 3, 2013 Unit 2 licensed operator training simulator scenario which included a loss of instrument air, a loss of a control rod drive pump, a stuck open safety relief valve, and a stuck open turbine bypass valve on September 3, 2013
 
The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classifications made by the shift manager and the TS action statements entered by the shift technical advisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify


and document crew performance problems.
Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.


====b. Findings====
====b. Findings====
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===.2 Quarterly Review of Licensed Operator Performance in the Main Control Room===
===.2 Quarterly Review of Licensed Operator Performance in the Main Control Room===
  (2 samples)
 
      (2 samples)


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed:
The inspectors observed:
Unit 1 control room operations during a scheduled plant shutdown due to increased drywell leakage on July 8, 2013 Unit 2 control room operations during planned surveillance activities on the Division III EDG and an emergency preparedness drill on August 20, 2013  
Unit 1 control room operations during a scheduled plant shutdown due to increased drywell leakage on July 8, 2013 Unit 2 control room operations during planned surveillance activities on the Division III EDG and an emergency preparedness drill on August 20, 2013 The inspectors reviewed CNG-OP-1.01-1000, Conduct of Operations, Revision 01000, and verified that procedure use, crew communications, and coordination of plant activities among work groups similarly met established expectations and standards.
 
The inspectors reviewed CNG-OP-1.01-1000, "Conduct of Operations," Revision 01000, and verified that procedure use, crew communications, and coordination of plant  
 
activities among work groups similarly met established expectations and standards.


Additionally, the inspectors observed test performance to verify that procedure use, crew communications, and coordination of activities between work groups similarly met established expectations and standards.
Additionally, the inspectors observed test performance to verify that procedure use, crew communications, and coordination of activities between work groups similarly met established expectations and standards.
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No findings were identified.
No findings were identified.


{{a|1R12}}
{{a|1R12}}
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12Q|count=4}}
{{IP sample|IP=IP 71111.12Q|count=4}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on structure, system, and component (SSC) performance and reliability. The inspectors reviewed system health reports, CAP documents, maintenance WOs, and maintenance rule basis documents to ensure that CENG personnel were identifying and properly eval uating performance problems within the scope of the maintenance rule. For each sample selected, the inspectors verified that the SSC were properly scoped into the maintenance rule in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 50.65 and verified that the (a)(2) performance criteria established by CENG staff were reasonable. As applicable, for SSCs classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these SSCs to (a)(2) status. Additionally, the inspectors ensured that CENG staff were identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.
The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on structure, system, and component (SSC) performance and reliability. The inspectors reviewed system health reports, CAP documents, maintenance WOs, and maintenance rule basis documents to ensure that CENG personnel were identifying and properly evaluating performance problems within the scope of the maintenance rule. For each sample selected, the inspectors verified that the SSC were properly scoped into the maintenance rule in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 50.65 and verified that the (a)(2) performance criteria established by CENG staff were reasonable. As applicable, for SSCs classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these SSCs to (a)(2) status. Additionally, the inspectors ensured that CENG staff were identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.


Unit 1 AC electric power on August 19, 2013 Unit 2 control room heating, ventilation, and air conditioning (HVAC) and RB and EDG building ventilation on August 21, 2013 Unit 2 main station safety-related batteries on September 12, 2013 Unit 1 instrument air system on September 13, 2013
Unit 1 AC electric power on August 19, 2013 Unit 2 control room heating, ventilation, and air conditioning (HVAC) and RB and EDG building ventilation on August 21, 2013 Unit 2 main station safety-related batteries on September 12, 2013 Unit 1 instrument air system on September 13, 2013


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|1R13}}
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13|count=6}}
{{IP sample|IP=IP 71111.13|count=6}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed station evaluation and management of plant risk for the  
The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that CENG personnel performed the appropriate risk assessments prior to removing equipment from service.


maintenance and emergent work activities listed below to verify that CENG personnel performed the appropriate risk assessments prior to removing equipment from service. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that CENG personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When CENG personnel performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the station's probabilistic risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that CENG personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When CENG personnel performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the stations probabilistic risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.


Unit 2 Division I standby liquid control system during Division II surveillance testing on July 31, 2013 Unit 1 containment spray 122 during planned maintenance on containment spray loop 121 on August 8, 2013 Unit 1 high-pressure coolant injection system 11 during planned maintenance on the high-pressure coolant injection system 12 on August 13, 2013 Unit 2 Division II control room ventilation system during planned maintenance on the Division I control room ventilation system on August 27, 2013 Unit 1 EDG 102 and core spray 121 during the core spray 122 surveillance test on September 12, 2013 Unit 1 EDG 103 during EDG 102 surveillance testing on September 25, 2013
Unit 2 Division I standby liquid control system during Division II surveillance testing on July 31, 2013 Unit 1 containment spray 122 during planned maintenance on containment spray loop 121 on August 8, 2013 Unit 1 high-pressure coolant injection system 11 during planned maintenance on the high-pressure coolant injection system 12 on August 13, 2013 Unit 2 Division II control room ventilation system during planned maintenance on the Division I control room ventilation system on August 27, 2013 Unit 1 EDG 102 and core spray 121 during the core spray 122 surveillance test on September 12, 2013 Unit 1 EDG 103 during EDG 102 surveillance testing on September 25, 2013


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|1R15}}
{{a|1R15}}
==1R15 Operability Determinations and Functionality Assessments==
==1R15 Operability Determinations and Functionality Assessments==
{{IP sample|IP=IP 71111.15|count=8}}
{{IP sample|IP=IP 71111.15|count=8}}
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed operability determinations for the following degraded or non-conforming conditions:
The inspectors reviewed operability determinations for the following degraded or non-conforming conditions:
Unit 2 RCIC/HPCS initiation logic discrepancy on July 1, 2013 Unit 2 control rod 30-51 failed to settle at position 46 on July 2, 2013 Unit 2 Division II EDG volt amperes reactive and amperes over procedural limit on July 30, 2013 Unit 2 RCIC trip throttle valve did not reset from the control room on August 9, 2013   Unit 1 RB instrument air compensatory action for postulated fires in the turbine and control buildings on August 12, 2013   Unit 2 improper design of scram di scharge volume vent and drain valves 2RDS*AOV130 and 2RDS*AOV132 on August 26, 2013 Unit 1 elevated technical support center temperatures on September 10, 2013 Unit 1 control rod drive flange leakage on September 18, 2013 The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the operability determinations to assess whether TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to CENG staff's evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by CENG personnel. The inspectors determined, where appropriate, compliance with bounding limitations associated with these evaluations.
Unit 2 RCIC/HPCS initiation logic discrepancy on July 1, 2013 Unit 2 control rod 30-51 failed to settle at position 46 on July 2, 2013 Unit 2 Division II EDG volt amperes reactive and amperes over procedural limit on July 30, 2013 Unit 2 RCIC trip throttle valve did not reset from the control room on August 9, 2013 Unit 1 RB instrument air compensatory action for postulated fires in the turbine and control buildings on August 12, 2013 Unit 2 improper design of scram discharge volume vent and drain valves 2RDS*AOV130 and 2RDS*AOV132 on August 26, 2013 Unit 1 elevated technical support center temperatures on September 10, 2013 Unit 1 control rod drive flange leakage on September 18, 2013 The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the operability determinations to assess whether TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to CENG staffs evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by CENG personnel. The inspectors determined, where appropriate, compliance with bounding limitations associated with these evaluations.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R18}}
{{a|1R18}}
==1R18 Plant Modifications==
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18}}
{{IP sample|IP=IP 71111.18}}
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the temporary modifications listed below to determine whether the modifications affected the safety functions of systems that are important to safety. The inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results, and conducted field walkdowns of the modifications to verify that the temporary modifications did not degrade the design bases, licensing bases, and performance capability of the affected systems.
The inspectors reviewed the temporary modifications listed below to determine whether the modifications affected the safety functions of systems that are important to safety.
 
The inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results, and conducted field walkdowns of the modifications to verify that the temporary modifications did not degrade the design bases, licensing bases, and performance capability of the affected systems.
 
Engineering Change Package (ECP) 13-000436 - Long-time and instantaneous over-current settings for 600V breaker BKR-(16B/010A)52 for the emergency service water (ESW) pump 11 motor at Unit 1.


Engineering Change Package (ECP) 13-000436 - Long-time and instantaneous over-current settings for 600V breaker BKR-(16B/010A)52 for the emergency service water (ESW) pump 11 motor at Unit 1. ECP 13-000766 - Remove over-speed trip device from diesel fire pump at Unit 2.
ECP 13-000766 - Remove over-speed trip device from diesel fire pump at Unit 2.


====b. Findings====
====b. Findings====
Line 264: Line 222:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated a modification to remove the Unit 1 hottest spot indicator relay from the 4160V-600V transformers for sa fety-related power boards 16B and 17A implemented by ECP 12-000536, "Removal of the Hottest Spot Indicating-Relay from Transformers XF-(16B)4160-600V and XF-(17A)4160-600V Associated With Power Boards (PB)-16B and PB-17A.The inspectors verified that the design bases, licensing bases, and performance capability of the affected system was not degraded by the modification. In addition, the inspectors reviewed modification documents associated with the upgrade and design change including the post-maintenance testing and the 10 CFR 50.59 screening form. The inspectors also reviewed proposed revisions to the control room alarm response procedure to ensure the changes were appropriate.
The inspectors evaluated a modification to remove the Unit 1 hottest spot indicator relay from the 4160V-600V transformers for safety-related power boards 16B and 17A implemented by ECP 12-000536, Removal of the Hottest Spot Indicating-Relay from Transformers XF-(16B)4160-600V and XF-(17A)4160-600V Associated With Power Boards (PB)-16B and PB-17A. The inspectors verified that the design bases, licensing bases, and performance capability of the affected system was not degraded by the modification. In addition, the inspectors reviewed modification documents associated with the upgrade and design change including the post-maintenance testing and the 10 CFR 50.59 screening form. The inspectors also reviewed proposed revisions to the control room alarm response procedure to ensure the changes were appropriate.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|1R19}}
{{a|1R19}}
==1R19 Post-Maintenance Testing==
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=4}}
{{IP sample|IP=IP 71111.19|count=4}}
Line 276: Line 234:
The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test procedure to verify that the procedure adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure were consistent with the information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed test data to verify that the test results adequately demonstrated restoration of the affected safety functions.
The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test procedure to verify that the procedure adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure were consistent with the information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed test data to verify that the test results adequately demonstrated restoration of the affected safety functions.


Unit 2 Division II SGTS following preventive maintenance on August 1, 2013 Unit 1 ESW pump 11 following failure to start on August 2, 2013 Unit 2 RB truck bay inner door seal on August 21, 2013 Unit 1 liquid poison pump 12 following installation of a new flow meter on September 24, 2013
Unit 2 Division II SGTS following preventive maintenance on August 1, 2013 Unit 1 ESW pump 11 following failure to start on August 2, 2013 Unit 2 RB truck bay inner door seal on August 21, 2013 Unit 1 liquid poison pump 12 following installation of a new flow meter on September 24, 2013


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|1R20}}
{{a|1R20}}
==1R20 Refueling and Other Outage Activities==
==1R20 Refueling and Other Outage Activities==
{{IP sample|IP=IP 71111.20|count=1}}
{{IP sample|IP=IP 71111.20|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the station's work schedule and outage risk plan for the Unit 1 planned outage which was conducted July 8 through July 11, 2013. The inspectors reviewed CENG staff's development and implementation of outage plans and schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered. During the outage, the inspectors observed portions of the shutdown and cooldown processes and monitored controls associated with the following outage activities:
The inspectors reviewed the stations work schedule and outage risk plan for the Unit 1 planned outage which was conducted July 8 through July 11, 2013. The inspectors reviewed CENG staffs development and implementation of outage plans and schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered. During the outage, the inspectors observed portions of the shutdown and cooldown processes and monitored controls associated with the following outage activities:
Power reduction activities Drywell closeout activities Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable TSs when taking equipment OOS Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated work or testing Status and configuration of electrical systems and switchyard activities to ensure that TSs were met Monitoring of decay heat removal operations Activities that could affect reactivity Power ascension activities
Power reduction activities Drywell closeout activities Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable TSs when taking equipment OOS Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated work or testing Status and configuration of electrical systems and switchyard activities to ensure that TSs were met Monitoring of decay heat removal operations Activities that could affect reactivity Power ascension activities


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
{{a|1R22}}
==1R22 Surveillance Testing (71111.22==


- 5 samples)
{{a|1R22}}
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22|count=5}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR, and CENG procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:  
The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR, and CENG procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:
 
Unit 1, N1-ISP-201-501, Type B Containment Isolation Airlock Door Leak Rate Test on July 10, 2013 Unit 1, N1-ST-Q20, Reactor Building Heating, Cooling, and Ventilation System Test on July 31, 2013 Unit 1, N1-ST-M4B, Emergency Diesel Generator 103 and PB 103 Operability Test on August 5, 2013 Unit 1, N1-ST-M1B, Liquid Poison Pump 12 Operability Test on August 26, 2013 (inservice test)
Unit 1, N1-ISP-201-501, Type 'B' Containment Isolation Airlock Door Leak Rate Test on July 10, 2013   Unit 1, N1-ST-Q20, Reactor Building Heating, Cooling, and Ventilation System Test on July 31, 2013 Unit 1, N1-ST-M4B, Emergency Diesel Generator 103 and PB 103 Operability Test on August 5, 2013 Unit 1, N1-ST-M1B, Liquid Poison Pump 12 Operability Test on August 26, 2013 (inservice test) Unit 1, N1-ST-M6, Core Spray Keep Fill Verification Test on September 24, 2013
Unit 1, N1-ST-M6, Core Spray Keep Fill Verification Test on September 24, 2013


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===Cornerstone:===
===Cornerstone: Emergency Preparedness===
Emergency Preparedness 1EP4 Emergency Action Level and Emergency Plan Changes (71114.04  
 
- 1 sample)
{{a|1EP4}}
==1EP4 Emergency Action Level and Emergency Plan Changes==
{{IP sample|IP=IP 71114.04|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The Office of Nuclear Security and Incident Response headquarters staff performed an in-office review of the latest revisions of various emergency plan implementing procedures and the emergency plan located under ADAMS accession number ML13155A006.
The Office of Nuclear Security and Incident Response headquarters staff performed an in-office review of the latest revisions of various emergency plan implementing procedures and the emergency plan located under ADAMS accession number ML13155A006.


CENG staff determined that in accordance with 10 CFR 50.54(q), the changes made in the revisions resulted in no reduction in the effectiveness of the plan and that the revised plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50, "Emergency Planning and Preparedness of Production and Utilization Facilities.The NRC review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, this revision is subject to future inspection.
CENG staff determined that in accordance with 10 CFR 50.54(q), the changes made in the revisions resulted in no reduction in the effectiveness of the plan and that the revised plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50, Emergency Planning and Preparedness of Production and Utilization Facilities. The NRC review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, this revision is subject to future inspection.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


1EP6 Drill Evaluation (71114.06  
{{a|1EP6}}
- 1 sample)
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06|count=1}}
Training Observation
Training Observation


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed a simulator training evolution for Unit 1 licensed operators on September 3, 2013, which required emergency plan implementation by an operations crew. CENG staff planned for this evolution to be evaluated and included in performance indicator (PI) data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors' activities was to note any weaknesses and deficiencies in the crew's performance and ensure that CENG evaluators noted the same issues and entered them into the CAP.
The inspectors observed a simulator training evolution for Unit 1 licensed operators on September 3, 2013, which required emergency plan implementation by an operations crew. CENG staff planned for this evolution to be evaluated and included in performance indicator (PI) data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew.
 
The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the crews performance and ensure that CENG evaluators noted the same issues and entered them into the CAP.


====b. Findings====
====b. Findings====
Line 330: Line 293:
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
{{IP sample|IP=IP 71151}}
===.1 Safety System Functional Failures (2===
===.1 Safety System Functional Failures (2 samples)===
 
samples)


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled CENG's submittals for the Safety System Functional Failures PIs for Unit 1 and Unit 2 for the period of July 1, 2012, through June 30, 2013. To determine the accuracy of the PI data reported during those periods, inspectors used definitions and guidance contained in the Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, and NUREG-1022, "Event Reporting Guidelines 10 CFR 50.72 and 10 CFR 50.73." The inspectors reviewed CENG's operator narrative logs, operability assessments, maintenance rule records, CRs, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.
The inspectors sampled CENGs submittals for the Safety System Functional Failures PIs for Unit 1 and Unit 2 for the period of July 1, 2012, through June 30, 2013. To determine the accuracy of the PI data reported during those periods, inspectors used definitions and guidance contained in the Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 10 CFR 50.73." The inspectors reviewed CENGs operator narrative logs, operability assessments, maintenance rule records, CRs, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.


====b. Findings====
====b. Findings====
Line 343: Line 304:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed CENG's submittal of the Mitigating Systems Performance Index for the following systems for the period of July 1, 2012, through June 30, 2013
The inspectors reviewed CENGs submittal of the Mitigating Systems Performance Index for the following systems for the period of July 1, 2012, through June 30, 2013:
Unit 1 and Unit 2 Emergency AC Power System (MS06) High-Pressure Injection System (MS07) Heat Removal System (MS08) Residual Heat Removal System (MS09) Cooling Water System (MS10)
Unit 1 and Unit 2 Emergency AC Power System (MS06)
To determine the accuracy of the PI data reported during those periods, the inspectors used definitions and guidance contained in NEI 99-02. The inspectors also reviewed  
High-Pressure Injection System (MS07)
 
Heat Removal System (MS08)
CENG's operator narrative logs, CR, mi tigating systems performance index basis document, event reports, and NRC integrated ins pection reports to validate the accuracy of the submittals.
Residual Heat Removal System (MS09)
Cooling Water System (MS10)
To determine the accuracy of the PI data reported during those periods, the inspectors used definitions and guidance contained in NEI 99-02. The inspectors also reviewed CENGs operator narrative logs, CR, mitigating systems performance index basis document, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|4OA2}}
{{a|4OA2}}
==4OA2 Problem Identification and Resolution==
==4OA2 Problem Identification and Resolution==
{{IP sample|IP=IP 71152|count=2}}
{{IP sample|IP=IP 71152|count=2}}
Line 359: Line 322:


====a. Inspection Scope====
====a. Inspection Scope====
As required by Inspection Procedure 71152, "Problem Identification and Resolution," the  
As required by Inspection Procedure 71152, Problem Identification and Resolution, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that CENG personnel entered issues into the CAP at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the CAP.
 
inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that CENG personnel entered issues into the CAP at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the CAP.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.2 Annual Sample:===
===.2 Annual Sample: Maintenance Rule Implementation Assessment===
Maintenance Rule Implementation Assessment


====a. Inspection Scope====
====a. Inspection Scope====
The inspector's maintenance rule implementation review focused on CENG staff's screening of CRs for maintenance rule applicability, incorporation of operating experience (OE) into the maintenance rule, timing of maintenance rule evaluations once the threshold for (a)(1) was met, and balancing unavailability and unreliability. The inspectors reviewed CRs, system health reports, the (a)(1) database, and interviewed the maintenance rule coordinator and system engineers in order to assess if CENG was implementing the program in accordance with CNG-AM-1.01-1023, "Maintenance Rule Program," Revision 00201, and CNG-CA-1.01-1010, "Use of Operating Experience,"
The inspectors maintenance rule implementation review focused on CENG staffs screening of CRs for maintenance rule applicability, incorporation of operating experience (OE) into the maintenance rule, timing of maintenance rule evaluations once the threshold for (a)(1) was met, and balancing unavailability and unreliability. The inspectors reviewed CRs, system health reports, the (a)(1) database, and interviewed the maintenance rule coordinator and system engineers in order to assess if CENG was implementing the program in accordance with CNG-AM-1.01-1023, Maintenance Rule Program, Revision 00201, and CNG-CA-1.01-1010, Use of Operating Experience, Revision 01000.
 
Revision 01000.


====b. Findings and Observations====
====b. Findings and Observations====
No findings were identified.
No findings were identified.


The inspectors reviewed CRs that were screened for maintenance rule applicability for  
The inspectors reviewed CRs that were screened for maintenance rule applicability for three systems (AC electric power, control room HVAC, and EDG room ventilation). In general, the CRs were screened appropriately; however, there were two CRs in which the inspectors were unable to conclude that the CENG staffs determination that maintenance rule not applicable was correct until CENG staff provided additional information.


three systems (AC electric power, control room HVAC, and EDG room ventilation). In general, the CRs were screened appropriately; however, there were two CRs in which the inspectors were unable to conclude that the CENG staff's determination that maintenance rule not applicable was correct until CENG staff provided additional
The inspectors determined that OE was being incorporated into the maintenance rule through the system engineers health reports, maintenance rule manager software, and cause evaluations when required. The inspectors review of the OE sections of several systems in the maintenance rule manager software indicated that they were being maintained up-to-date with applicable OE.


information.
The inspectors reviewed 24 systems that were currently in (a)(1) status and determined that (a)(1) evaluations were typically done in a timely manner. The average time to make an (a)(1) determination was 35 days with a range of 0 to 78 days.
 
The inspectors determined that OE was being incorporated into the maintenance rule through the system engineers' health reports, maintenance rule manager software, and cause evaluations when required. The inspector's review of the OE sections of several systems in the maintenance rule manager software indicated that they were being maintained up-to-date with applicable OE.


The inspectors reviewed 24 systems that were currently in (a)(1) status and determined that (a)(1) evaluations were typically done in a timely manner. The average time to make an (a)(1) determination was 35 days with a range of 0 to 78 days.
===.3 Annual Sample: Corrective Actions to Address Repetitive Failures of the Radiation===


===.3 Annual Sample:===
Monitoring Equipment
Corrective Actions to Address Repetitive Failures of the Radiation  Monitoring Equipment


====a. Inspection Scope====
====a. Inspection Scope====
Units 1 and 2 have experienced repetitive failures of several radiation monitoring systems between August 2011 and August 2013. The four effluent monitors with the highest number of hours of unavailability were selected for a detailed sample review. The four effluent radiation monitors and associated number of CRs that were reviewed included:
Units 1 and 2 have experienced repetitive failures of several radiation monitoring systems between August 2011 and August 2013. The four effluent monitors with the highest number of hours of unavailability were selected for a detailed sample review.


The four effluent radiation monitors and associated number of CRs that were reviewed included:
Unit 1 off-gas effluent monitoring system (OGEMS) (6 CRs)
Unit 1 off-gas effluent monitoring system (OGEMS) (6 CRs)
Unit 1 service water (SW) radiation monitors PMP-72-461 and PMP-72-462 (20 CRs)
Unit 1 service water (SW) radiation monitors PMP-72-461 and PMP-72-462 (20 CRs)
Unit 2 SW radiation monitors 2SWP*CAB146A and 2SWP*CAB146B (52 CRs)
Unit 2 SW radiation monitors 2SWP*CAB146A and 2SWP*CAB146B (52 CRs)
Unit 2 radwaste/reactor building vent radiation monitor (20 CRs)
Unit 2 radwaste/reactor building vent radiation monitor (20 CRs)
From August 4 through 9, 2013, the inspectors performed an in-depth review of the events in these CRs to assess CENG staff's actions for initiating corrective and/or compensatory actions, timeliness, and addressing adverse trends. To perform this review, the inspectors conducted walkdowns of these radiation monitors, interviewed plant personnel, reviewed WOs, and associated apparent cause evaluations (ACEs). In addition, system health reports for the radiation monitoring system and associated maintenance rule reports were also reviewed.
From August 4 through 9, 2013, the inspectors performed an in-depth review of the events in these CRs to assess CENG staffs actions for initiating corrective and/or compensatory actions, timeliness, and addressing adverse trends. To perform this review, the inspectors conducted walkdowns of these radiation monitors, interviewed plant personnel, reviewed WOs, and associated apparent cause evaluations (ACEs). In addition, system health reports for the radiation monitoring system and associated maintenance rule reports were also reviewed.


====b. Findings and Observations====
====b. Findings and Observations====
Line 404: Line 360:
After identifying an adverse trend in radiation monitor availability and reliability, CENG personnel initiated its first generic CR on radiation monitors for Units 1 and 2 on January 16, 2013, and the second CR on February 27, 2013. These two CRs resulted in two ACEs. The first one was to investigate maintenance and engineering corrective actions for the effluent radiation monitors (CR-2013-000434), and the second was to investigate human performance impacts on equipment reliability of these instruments (CR-2013-001613). These two ACEs appeared to be thorough and included the extent of condition, common causes, and action plans to prevent recurrence. Based on these evaluations, CENG staff concluded that there were a number of system design improvements that could be made to improve reliability of the effluent monitoring systems. It was concluded that there had been errors assigning the appropriate priority (priority two or three instead of priority four) on the WOs resulting in untimely completion of some of the radiation monitoring equipment repairs. Briefings were conducted by CENG personnel with the appropriate staff to indicate the importance of the radiation monitoring instruments relative to event classification in the emergency plan. In addition, training was also provided on the steps that should be taken to expedite these instruments return to service.
After identifying an adverse trend in radiation monitor availability and reliability, CENG personnel initiated its first generic CR on radiation monitors for Units 1 and 2 on January 16, 2013, and the second CR on February 27, 2013. These two CRs resulted in two ACEs. The first one was to investigate maintenance and engineering corrective actions for the effluent radiation monitors (CR-2013-000434), and the second was to investigate human performance impacts on equipment reliability of these instruments (CR-2013-001613). These two ACEs appeared to be thorough and included the extent of condition, common causes, and action plans to prevent recurrence. Based on these evaluations, CENG staff concluded that there were a number of system design improvements that could be made to improve reliability of the effluent monitoring systems. It was concluded that there had been errors assigning the appropriate priority (priority two or three instead of priority four) on the WOs resulting in untimely completion of some of the radiation monitoring equipment repairs. Briefings were conducted by CENG personnel with the appropriate staff to indicate the importance of the radiation monitoring instruments relative to event classification in the emergency plan. In addition, training was also provided on the steps that should be taken to expedite these instruments return to service.


Listed below are summaries of the corrective actions CENG personnel developed to improve system availability and reliability for the four radiation monitors of concern:  
Listed below are summaries of the corrective actions CENG personnel developed to improve system availability and reliability for the four radiation monitors of concern:
 
Unit 1 Off-Gas Effluent Monitoring System Corrective action (CA)-2012-004479 was initiated to develop and execute a troubleshooting plan to isolate the cause for the noise intrusion on the Unit 1 stack radiation monitor. CENG is planning to implement the electrical troubleshooting plan via WO C92073592. No unplanned unavailability has occurred on the OGEMS radiation monitor since April 2013. CENG plans to monitor system performance until corrective actions are completed.
Unit 1 Off-Gas Effluent Monitoring System  
 
Corrective action (CA)-2012-004479 was initiated to develop and execute a troubleshooting plan to isolate the cause for the noise intrusion on the Unit 1 stack radiation monitor. CENG is planning to implement the electrical troubleshooting plan via WO C92073592. No unplanned unavailability has occurred on the OGEMS radiation monitor since April 2013. CENG plans to monitor system performance until corrective actions are completed.
 
Unit 1 Service Water Radiation Monitor
 
CR-2011-006930 was written to revise the procedures for biocide/chemical injections and sample line flushes to reduce the impact of both biofouling and zebra mussels on the SW system. In particular, chemistry procedure N1-CTP-V945, "Service Water Zebra Mussel Treatment," Revision 01600, was revised to notify the Unit 1 operations department of a requirement to perform N1-OP-18, "Service Water System," Revision 03000, sections 8 and 9, daily during biocide treatment and for 21 days following completion of the activity. Preventive maintenance surveillance N1149646 was established to track this operations activity in January 2012. The operations department has been performing these flushes daily following two biocide treatments conducted in


2013.
Unit 1 Service Water Radiation Monitor CR-2011-006930 was written to revise the procedures for biocide/chemical injections and sample line flushes to reduce the impact of both biofouling and zebra mussels on the SW system. In particular, chemistry procedure N1-CTP-V945, Service Water Zebra Mussel Treatment, Revision 01600, was revised to notify the Unit 1 operations department of a requirement to perform N1-OP-18, Service Water System, Revision 03000, sections 8 and 9, daily during biocide treatment and for 21 days following completion of the activity. Preventive maintenance surveillance N1149646 was established to track this operations activity in January 2012. The operations department has been performing these flushes daily following two biocide treatments conducted in 2013.


CA-2012-000076 was initiated to correct unexpected radiation monitor process annunciator H1-4-5 alarms of the SW radiation monitor. The system and central processing unit circuit cards were replaced in January 2013. No spurious annunciator alarms have occurred since completion of this maintenance activity.
CA-2012-000076 was initiated to correct unexpected radiation monitor process annunciator H1-4-5 alarms of the SW radiation monitor. The system and central processing unit circuit cards were replaced in January 2013. No spurious annunciator alarms have occurred since completion of this maintenance activity.
Line 420: Line 369:
CR-2012-008164 was initiated to perform a maintenance rule 10 CFR 50.65 (a)(1)evaluation for Unit 1 SW radiation monitor because the functional failure performance criteria was exceeded. On October 2, 2012, the plant health committee approved the system performance goals and action plan.
CR-2012-008164 was initiated to perform a maintenance rule 10 CFR 50.65 (a)(1)evaluation for Unit 1 SW radiation monitor because the functional failure performance criteria was exceeded. On October 2, 2012, the plant health committee approved the system performance goals and action plan.


CR-2012-002176 investigated the root cause for the repeated low flow alarms on the SW radiation monitor pump. It was determined that the installed pump, PMP-72-462, was being operated outside the manufacturer pump curve and was likely being operated near the pump's shutoff head. ECP 13-000167, "Unit 1 Service Water Radiation Monitor Sample Pumps are Over-Sized Resulting in Premature Failure,"
CR-2012-002176 investigated the root cause for the repeated low flow alarms on the SW radiation monitor pump. It was determined that the installed pump, PMP-72-462, was being operated outside the manufacturer pump curve and was likely being operated near the pumps shutoff head. ECP 13-000167, Unit 1 Service Water Radiation Monitor Sample Pumps are Over-Sized Resulting in Premature Failure, was processed and has resulted in the replacement of the PMP-72-462 pump with a smaller capacity centrifugal pump on June 28, 2013. No unplanned unavailability has occurred on the Unit 1 SW radiation monitor since June 2013. Corrective actions appear to be effective.
was processed and has resulted in the replacement of the PMP-72-462 pump with a smaller capacity centrifugal pump on June 28, 2013. No unplanned unavailability has occurred on the Unit 1 SW radiation monitor since June 2013. Corrective actions appear to be effective.


Unit 2 Service Water Radiation Monitor CR-2012-011225 was initiated to perform a maintenance rule 10 CFR 50.65 (a)(1)evaluation for Unit 2 SW radiation monitors, 2-RMS-F11. On January 29, 2013, the plant health committee approved the system performance goals and action plan. The following corrective actions from this plan are listed below along with their current status:
Unit 2 Service Water Radiation Monitor CR-2012-011225 was initiated to perform a maintenance rule 10 CFR 50.65 (a)(1)evaluation for Unit 2 SW radiation monitors, 2-RMS-F11. On January 29, 2013, the plant health committee approved the system performance goals and action plan. The following corrective actions from this plan are listed below along with their current status:
Replace the remaining piping in accordance with ECP 12-000565, "2SWP*CAB146B Replace Carbon Steel Pipe to Stainless Steel" and WO C91883844. This action was completed on April 1, 2013.
Replace the remaining piping in accordance with ECP 12-000565, 2SWP*CAB146B Replace Carbon Steel Pipe to Stainless Steel and WO C91883844. This action was completed on April 1, 2013.
 
Initiate temporary sodium bisulfate injection until repairs can be completed on the permanent chemical treatment equipment per WO C92156031 (CA-2013-000702).


Initiate temporary sodium bisulfate injection until repairs can be completed on the permanent chemical treatment equipment per WO C92156031 (CA-2013-000702). The temporary equipment for injecting the chemical to SW was completed in April 2013. Injection of chemicals into SW was reinitiated on April 22, 2013. Replace the current flow switch design with a design less susceptible to fouling and scaling. ECP 13-000140, "Replacement of the Existing Resistance-Type Flow Switch with a New Magnetic Flow Switch" is projected to be completed by December 31, 2013, as identified in CR-2013-001810.
The temporary equipment for injecting the chemical to SW was completed in April 2013. Injection of chemicals into SW was reinitiated on April 22, 2013.


The inspectors noted that one of the a(1) action plan items, chemical treatments, was
Replace the current flow switch design with a design less susceptible to fouling and scaling. ECP 13-000140, Replacement of the Existing Resistance-Type Flow Switch with a New Magnetic Flow Switch is projected to be completed by December 31, 2013, as identified in CR-2013-001810.


not performed on the SW system for over 7 months, from September 2012 to April 22, 2013, due to a leak in one of the chemical injection tanks. Unavailability problems continue as evidenced by a recent reactor operating event notification report number 49391. This notification indicated that the SW digital radiation monitor received a low sample flow alarm and was nonfunctional on September 28 and 29, 2013.
The inspectors noted that one of the a(1) action plan items, chemical treatments, was not performed on the SW system for over 7 months, from September 2012 to April 22, 2013, due to a leak in one of the chemical injection tanks. Unavailability problems continue as evidenced by a recent reactor operating event notification report number 49391. This notification indicated that the SW digital radiation monitor received a low sample flow alarm and was nonfunctional on September 28 and 29, 2013.


In accordance with the NRC Enforcement Manual , this does not constitute a violation of 10 CFR 50.65.(a)(1) since an action plan was developed and was being implemented and monitoring goals in accordance with the 50.65 (a)(1). CENG initiated CR-2013-005232 to address the need to create PIs for ke y system chemical parameters to assist in more optimal scheduling of chemical treatments and flushes on the SW system. Corrective actions are not yet completed.
In accordance with the NRC Enforcement Manual, this does not constitute a violation of 10 CFR 50.65.(a)(1) since an action plan was developed and was being implemented and monitoring goals in accordance with the 50.65 (a)(1). CENG initiated CR-2013-005232 to address the need to create PIs for key system chemical parameters to assist in more optimal scheduling of chemical treatments and flushes on the SW system.
 
Corrective actions are not yet completed.


Unit 2 Radwaste/Reactor Building Vent Radiation Monitor Several instrument calibrations failures have occurred on this instrument due to issues with the calibration equipment associated with this monitor. CA-2013-000226 was initiated to create a preventive maintenance surveillance to periodically inspect the check source insertion assembly for wear, re-orient steel roll pin in the check source assembly so that it does not contact the aluminum guide tube, and replace the aluminum guide tube with an equivalent sized steel guide tube. These inspections and modifications will be completed during the next monitor surveillance currently scheduled to be completed in November 2013.
Unit 2 Radwaste/Reactor Building Vent Radiation Monitor Several instrument calibrations failures have occurred on this instrument due to issues with the calibration equipment associated with this monitor. CA-2013-000226 was initiated to create a preventive maintenance surveillance to periodically inspect the check source insertion assembly for wear, re-orient steel roll pin in the check source assembly so that it does not contact the aluminum guide tube, and replace the aluminum guide tube with an equivalent sized steel guide tube. These inspections and modifications will be completed during the next monitor surveillance currently scheduled to be completed in November 2013.
Line 438: Line 390:
A design issue for this flow sensor was identified and documented on March 10, 2009.
A design issue for this flow sensor was identified and documented on March 10, 2009.


In 2011, ECP 11-000140, "Install a Separate Flow Sensor Array on the Radwaste Vent Ducting" was initiated. These flow sensors were designed to establish representative flow sample rates for the plant configuration when the RB ventilation flow is isolated or when the RB ventilation fans are not available.
In 2011, ECP 11-000140, Install a Separate Flow Sensor Array on the Radwaste Vent Ducting was initiated. These flow sensors were designed to establish representative flow sample rates for the plant configuration when the RB ventilation flow is isolated or when the RB ventilation fans are not available.


CR-2013-006249 identified the degraded flow sensing array modification was not being tracked properly and developed corrective actions which included long-term asset management. On August 26, 2013, this modification was approved for conceptual design work. CENG initiated CR-2013-006249 to track completion of this modification.
CR-2013-006249 identified the degraded flow sensing array modification was not being tracked properly and developed corrective actions which included long-term asset management. On August 26, 2013, this modification was approved for conceptual design work. CENG initiated CR-2013-006249 to track completion of this modification.


The inspectors noted that the Unit 2 radwaste/RB vent radiation monitor was nonfunctional for 2,731 hours between August 2011 and August 2013. A non safety related, low risk system is only required to monitor for reliability and not required to monitor for system unavailability; however, the high level of system unavailability has resulted in a reduction of EP staff's assessment capability. Although 10 CFR 50.65 a(2)performance criteria were met and no maintenance rule functional failures were identified by CENG staff, on two occasions CENG staff made reports to the NRC as required by 10 CFR 50.72 (b)(3)(xiii) due to unavailability of these instruments. This included reactor operating event notification reports 49127 and 49176 for loss of radwaste/RB vent gaseous effluent radiation monitor that occurred in June and July 2013. No findings were identified since compensatory sampling of the gaseous effluents occurred as required. CR-2013-008833 was written to address this observation.
The inspectors noted that the Unit 2 radwaste/RB vent radiation monitor was nonfunctional for 2,731 hours between August 2011 and August 2013. A non safety related, low risk system is only required to monitor for reliability and not required to monitor for system unavailability; however, the high level of system unavailability has resulted in a reduction of EP staffs assessment capability. Although 10 CFR 50.65 a(2)performance criteria were met and no maintenance rule functional failures were identified by CENG staff, on two occasions CENG staff made reports to the NRC as required by 10 CFR 50.72 (b)(3)(xiii) due to unavailability of these instruments. This included reactor operating event notification reports 49127 and 49176 for loss of radwaste/RB vent gaseous effluent radiation monitor that occurred in June and July 2013. No findings were identified since compensatory sampling of the gaseous effluents occurred as required. CR-2013-008833 was written to address this observation.


{{a|4OA3}}
{{a|4OA3}}
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
{{IP sample|IP=IP 71153|count=1}}
{{IP sample|IP=IP 71153|count=1}}
 
    (Closed) Licensee Event Report (LER) 05000220/2013-001-00: Emergency Condenser 11 High Steam Flow Isolation Instrumentation Loss During Plant Startup On May 14, 2013, at 11:45 a.m., while Unit 1 was in the startup mode of reactor plant operation with reactor power at 3 percent, channel 11 high steam flow instrumentation for emergency condenser loop 11 alarmed due to a gross failure trip. The gross failure trip is a design feature of the instrument loop that monitors the integrity of the emergency condenser piping system. The failure of the channel 11 high steam flow instrumentation concurrently with channel 12, which had failed earlier in the day at 8:40 a.m., resulted in the loss of emergency condenser system loop 11 isolation capability on high steam flow.
(Closed) Licensee Event Report (LER) 05000220/2013-001-00: Emergency Condenser 11 High Steam Flow Isolation Instrumentation Loss During Plant Startup  
 
On May 14, 2013, at 11:45 a.m., while Unit 1 was in the startup mode of reactor plant operation with reactor power at 3 percent, channel 11 high steam flow instrumentation for emergency condenser loop 11 alarmed due to a gross failure trip. The gross failure trip is a design feature of the instrument loop that monitors the integrity of the emergency condenser piping system. The failure of the channel 11 high steam flow instrumentation concurrently with channel 12, which had failed earlier in the day at 8:40 a.m., resulted in the loss of emergency condenser system loop 11 isolation capability on high steam flow.


In response to the instrument failure, operators declared emergency condenser system loop 11 inoperable, isolated the system, and entered plant TS 3.1.3.b, which required operators to return the system to service within 7 days when the reactor is critical and reactor coolant system temperature is greater than 212 degree Fahrenheit. Emergency condenser system loop 11 was declared operable on May 15 when the cause for the gross failure trip signal and inadequately filled sensing lines was resolved.
In response to the instrument failure, operators declared emergency condenser system loop 11 inoperable, isolated the system, and entered plant TS 3.1.3.b, which required operators to return the system to service within 7 days when the reactor is critical and reactor coolant system temperature is greater than 212 degree Fahrenheit. Emergency condenser system loop 11 was declared operable on May 15 when the cause for the gross failure trip signal and inadequately filled sensing lines was resolved.


A CENG investigation determined that the cause of the event was leakage from the shared high-pressure sensing line for transmitters DPT-36-06C and DPT-36-06D. The suspected leakage path was seat leakage from instrument blowdown valves VLV-36-374 and VLV-8-172. CENG staff's corrective actions include replacement of the suspect blowdown isolation valves during the next refueling outage and enhanced monitoring of the output signals on the high steam flow instruments to ensure the sensing lines remain full. The inspectors reviewed the LER and determined that no findings or violations of NRC requirements were identified. This LER is closed  
A CENG investigation determined that the cause of the event was leakage from the shared high-pressure sensing line for transmitters DPT-36-06C and DPT-36-06D. The suspected leakage path was seat leakage from instrument blowdown valves VLV-36-374 and VLV-8-172. CENG staffs corrective actions include replacement of the suspect blowdown isolation valves during the next refueling outage and enhanced monitoring of the output signals on the high steam flow instruments to ensure the sensing lines remain full. The inspectors reviewed the LER and determined that no findings or violations of NRC requirements were identified. This LER is closed
 
{{a|4OA5}}
{{a|4OA5}}
==4OA5 Other Activities==
==4OA5 Other Activities==
Line 466: Line 414:
The report primarily relied on observations made by INPO representatives during the weeks of October 5 and October 18, 2012.
The report primarily relied on observations made by INPO representatives during the weeks of October 5 and October 18, 2012.


The inspectors evaluated the report to ensure that NRC perspectives of CENG staff's performance were consistent with any issues identified during the assessment and to verify that the final report content was similar to the initial report provided in January.
The inspectors evaluated the report to ensure that NRC perspectives of CENG staffs performance were consistent with any issues identified during the assessment and to verify that the final report content was similar to the initial report provided in January.


The inspectors also reviewed the report to determine whether INPO identified any significant safety issues that required further NRC follow-up.
The inspectors also reviewed the report to determine whether INPO identified any significant safety issues that required further NRC follow-up.
Line 473: Line 421:
No findings were identified.
No findings were identified.


===.2 Temporary Instruction (TI) 2515/182, Review of the Implementation of the Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 2===
===.2 Temporary Instruction (TI) 2515/182, Review of the Implementation of the Industry===
 
Initiative to Control Degradation of Underground Piping and Tanks, Phase 2


====a. Inspection Scope====
====a. Inspection Scope====
In accordance with paragraph 03.02.a of TI 2515/182, the inspectors reviewed CENG's programs for buried piping and underground piping and tanks and confirmed that activities which correspond to the completion dates specified in the program which have passed since the Phase 1 inspection was conducted have been completed.
In accordance with paragraph 03.02.a of TI 2515/182, the inspectors reviewed CENGs programs for buried piping and underground piping and tanks and confirmed that activities which correspond to the completion dates specified in the program which have passed since the Phase 1 inspection was conducted have been completed.


CENG staff's buried piping and underground piping and tanks program were inspected in accordance with paragraph 03.02.b of TI 2515/182 and responses to specific questions found in www.nrc.gov/reactors/operating/ops-experience/buried-pipe-ti-phase-2-insp-req-2011-11-16.pdf were submitted to NRC headquarters staff.
CENG staffs buried piping and underground piping and tanks program were inspected in accordance with paragraph 03.02.b of TI 2515/182 and responses to specific questions found in www.nrc.gov/reactors/operating/ops-experience/buried-pipe-ti-phase-2-insp-req-2011-11-16.pdf were submitted to NRC headquarters staff.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.3 TI 2515/190, Inspection of the Proposed Interim Actions Associated with Near-Term Task Force Recommendation 2.1 Flooding Hazard Evaluations.===
===.3 TI 2515/190, Inspection of the Proposed Interim Actions Associated with Near-Term===
 
Task Force Recommendation 2.1 Flooding Hazard Evaluations.


====a. Inspection Scope====
====a. Inspection Scope====
Inspectors verified that CENG staff's interim actions will perform their intended function for flooding mitigation.
Inspectors verified that CENG staffs interim actions will perform their intended function for flooding mitigation.


The inspectors independently verified that CENG staff's proposed interim actions would perform their intended function for flooding mitigation.
The inspectors independently verified that CENG staffs proposed interim actions would perform their intended function for flooding mitigation.


Visual inspection of the flood protection feature was performed if the flood protection feature was relevant. External visual inspection for indications of degradation that would prevent its credited function from being performed was performed.
Visual inspection of the flood protection feature was performed if the flood protection feature was relevant. External visual inspection for indications of degradation that would prevent its credited function from being performed was performed.
Line 496: Line 448:
Flood protection feature functionality was determined using either visual observation or by review of other documents.
Flood protection feature functionality was determined using either visual observation or by review of other documents.


The inspectors verified that issues identified were entered into CENG's CAP.
The inspectors verified that issues identified were entered into CENGs CAP.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.4 Operation of an Independent Spent Fuel Storage Installation (ISFSI) at Operating Plants (IP 60855)===
===.4 Operation of an Independent Spent Fuel Storage Installation (ISFSI) at Operating Plants===
 
      (IP 60855)


====a. Inspection Scope====
====a. Inspection Scope====
(1 partial sample)
(1 partial sample)
Region I materials inspectors conducted a follow up inspection to review CENG staff's action following a hydrogen deflagration during ISFSI loading operations using NRC Inspection Procedure (IP) 60855.1, "Operation of an Independent Spent Fuel Storage Installation at Operating Plants."
Region I materials inspectors conducted a follow up inspection to review CENG staffs action following a hydrogen deflagration during ISFSI loading operations using NRC Inspection Procedure (IP) 60855.1, Operation of an Independent Spent Fuel Storage Installation at Operating Plants.


On August 14, 2013, Unit 2 experienced a hydrogen deflagration during ISFSI loading operations (CR-2013-006840). A dry shielded canister (DSC) filled with spent fuel assemblies was on the refuel floor and the DSC inner cover was in the process of being welded in place by an automated welding system. During the welding evolution, hydrogen concentration built up above the lower explosive limit and the deflagration occurred. CENG staff completed a technical evaluation and concluded that spent fuel within the cask was not impacted and that the cask remained within UFSAR specifications.
On August 14, 2013, Unit 2 experienced a hydrogen deflagration during ISFSI loading operations (CR-2013-006840). A dry shielded canister (DSC) filled with spent fuel assemblies was on the refuel floor and the DSC inner cover was in the process of being welded in place by an automated welding system. During the welding evolution, hydrogen concentration built up above the lower explosive limit and the deflagration occurred. CENG staff completed a technical evaluation and concluded that spent fuel within the cask was not impacted and that the cask remained within UFSAR specifications.


The ISFSI inspectors performed an on-site inspection August 26 through 28, 2013. The inspection consisted of interviews with CENG personnel and contractor personnel and observations of ISFSI equipment configuration on the refuel floor. The inspectors reviewed documentation to verify compliance with the conditions of the general license, certificate of compliance, TSs, and the UFSAR. The inspectors also reviewed CRs, WOs, and procedures. The inspectors reviewed CENG staff's evaluations and immediate follow-up actions to assure that CENG staff implemented appropriate compensatory and corrective actions prior to resuming ISFSI welding and loading operations.
The ISFSI inspectors performed an on-site inspection August 26 through 28, 2013. The inspection consisted of interviews with CENG personnel and contractor personnel and observations of ISFSI equipment configuration on the refuel floor. The inspectors reviewed documentation to verify compliance with the conditions of the general license, certificate of compliance, TSs, and the UFSAR. The inspectors also reviewed CRs, WOs, and procedures. The inspectors reviewed CENG staffs evaluations and immediate follow-up actions to assure that CENG staff implemented appropriate compensatory and corrective actions prior to resuming ISFSI welding and loading operations.


====b. Findings====
====b. Findings====
This inspection remains open at the end of this inspection period while CENG staff completes their ACE and the inspectors have the opportunity to review CENG staff's evaluation and long-term corrective actions to address the event.
This inspection remains open at the end of this inspection period while CENG staff completes their ACE and the inspectors have the opportunity to review CENG staffs evaluation and long-term corrective actions to address the event.


{{a|4OA6}}
{{a|4OA6}}
==4OA6 Meetings, Including Exit==
==4OA6 Meetings, Including Exit==


Exit Meeting  
Exit Meeting On October 24, 2013, the inspectors presented the inspection results to Mr. Christopher Costanzo, Site Vice President, and other members of the NMPNS staff. The inspectors verified that no propriety information was retained by the inspectors or documented in this report.
 
On October 24, 2013, the inspectors presented the inspection results to Mr. Christopher Costanzo, Site Vice President, and other members of the NMPNS staff. The inspectors verified that no propriety information was retained by the inspectors or documented in this report.


ATTACHMENT:
ATTACHMENT:  


=SUPPLEMENTARY INFORMATION=
=SUPPLEMENTARY INFORMATION=
Line 528: Line 480:


===Licensee Personnel===
===Licensee Personnel===
: [[contact::C. Costanzo]], Vice President  
: [[contact::C. Costanzo]], Vice President
: [[contact::J. Stanley]], Plant General Manager  
: [[contact::J. Stanley]], Plant General Manager
: [[contact::P. Bartolini]], Supervisor, Design Engineering  
: [[contact::P. Bartolini]], Supervisor, Design Engineering
: [[contact::J. Bouck]], Manager, Operations  
: [[contact::J. Bouck]], Manager, Operations
: [[contact::B. Busch]], Unit 1 General Supervisor, Operations
: [[contact::B. Busch]], Unit 1 General Supervisor, Operations
: [[contact::K. Clark]], Director, Security
: [[contact::K. Clark]], Director, Security
: [[contact::J. Dean]], Supervisor, Quality Assurance  
: [[contact::J. Dean]], Supervisor, Quality Assurance
: [[contact::S. Dhar]], Design Engineering  
: [[contact::S. Dhar]], Design Engineering
: [[contact::S. Eckhard]], Supervisor Design Engineering  
: [[contact::S. Eckhard]], Supervisor Design Engineering
: [[contact::W. Farnham]], System Engineer  
: [[contact::W. Farnham]], System Engineer
: [[contact::N. Fisher]], Quality Performance Assessor  
: [[contact::N. Fisher]], Quality Performance Assessor
: [[contact::J. Gerber]], Manager, Training  
: [[contact::J. Gerber]], Manager, Training
: [[contact::J. Gillard]], Emergency Preparedness Analyst  
: [[contact::J. Gillard]], Emergency Preparedness Analyst
: [[contact::J. Holton]], Supervisor, Systems Engineering  
: [[contact::J. Holton]], Supervisor, Systems Engineering
: [[contact::G. Inch]], Principle Engineer, EPU Project Manager  
: [[contact::G. Inch]], Principle Engineer, EPU Project Manager
: [[contact::M. Kunzwiler]], Security Supervisor
: [[contact::M. Kunzwiler]], Security Supervisor
: [[contact::M. Khan]], General Supervisor Design Engineering  
: [[contact::M. Khan]], General Supervisor Design Engineering
: [[contact::J. Leonard]], Supervisor Design Engineering  
: [[contact::J. Leonard]], Supervisor Design Engineering
: [[contact::J. Manly]], Unit 2 General Supervisor, Operations  
: [[contact::J. Manly]], Unit 2 General Supervisor, Operations
: [[contact::C. McClay]], Senior Engineer  
: [[contact::C. McClay]], Senior Engineer
: [[contact::E. Perkins]], Director, Licensing  
: [[contact::E. Perkins]], Director, Licensing
: [[contact::J. Reid]], Design Engineer  
: [[contact::J. Reid]], Design Engineer
: [[contact::T. Roche]], System Engineer  
: [[contact::T. Roche]], System Engineer
: [[contact::S. Segretto]], System Engineer  
: [[contact::S. Segretto]], System Engineer
: [[contact::M. Shanbhag]], Licensing Engineer  
: [[contact::M. Shanbhag]], Licensing Engineer
: [[contact::J. Snyder]], Maintenance Rule Coordinator  
: [[contact::J. Snyder]], Maintenance Rule Coordinator
: [[contact::S. Stone]], System Engineer  
: [[contact::S. Stone]], System Engineer
: [[contact::T. Syrell]], Manager, Nuclear Safety and Security  
: [[contact::T. Syrell]], Manager, Nuclear Safety and Security
: [[contact::J. Thompson]], General Supervisor, Mechanical Maintenance  
: [[contact::J. Thompson]], General Supervisor, Mechanical Maintenance
: [[contact::A. Verno]], Director, Emergency Preparedness  
: [[contact::A. Verno]], Director, Emergency Preparedness


==LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED==
==LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED==


===Closed===
===Closed===
: [[Closes LER::05000220/LER-2013-001]]-00 LER Emergency Condenser 11 High Steam Flow Isolation Instrumentation Loss During Plant Startup  
: 05000220/2013-001-00           LER           Emergency Condenser 11 High Steam Flow Isolation Instrumentation Loss During Plant Startup (Section 4OA3)
(Section 4OA3)  
 
: A-2
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
==Section 1R01: Adverse Weather Protection==
===Procedures===
: N1-OP-64, Meteorological Monitoring, Revision 00603 N2-OP-102, Meteorological Monitoring, Revision 01103
: N2-OP-102, Hot Weather Preparation Checklist, Attachment 3, Revision 01102
: NAI-PSH-11, Seasonal Readiness Program, Revision 00700 
===Condition Reports===
: CR-2012-008748
: CR-2013-007010 
===Miscellaneous===
: 1EQPBD, Unit 1 Environmental Qualification Program Basis Document, Revision 2.00
: UFSAR
==Section 1R04: Equipment Alignment==
===Procedures===
: N1-OP-40, Reactor Protection and ATWS Systems, Revision 02100
: N1-ST-Q5, Primary Containment Isolation Valves Operability Test, Revision 02901
: N1-ST-R10, Drywell to Torus Leak Rate Test, Revision 01701
: N2-OP-33, High-Pressure Core Spray System, Revision 01201
: N2-OP-61B, Standby Gas Treatment System, Revision 01000 N2-OSP-GTS-M001, Standby Gas Treatment System Functional Test, Revision 00201 
===Drawings===
: C19408C, AC Station Power Distribution One-Line Diagram, Revision 16
: PID-061-A, Primary Containment Purge and Standby Gas Treatment System, Revision 13 
===Condition Reports===
: CR-2013-003840
: CR-2013-005794
: CR-2013-007068 
===Work Orders===
: WO
: C91475487 WO
: C91948721 
===Miscellaneous===
: CNG-CA-1.01-1005, Apparent Cause Evaluation CR- 2013-004755, Revision 00603
==Section 1R05: Fire Protection==
===Procedures===
: N1-PFP-0101, Unit 1 Pre-Fire Plans, Revision 00200
: N2-FPI-PFP-0201, Unit 2 Pre-Fire Plans, Revision 001
: NMP-TR-1.01-107, Nuclear Fire Brigade Training Program, Revision 01101
===Miscellaneous===
: Fire Brigade Scenario,
: OS-FT-FIR-SCN-2-01, Operations Building Fire, Revision 0
: Unit 1 UFSAR, Appendix 10A, Fire Hazards Analysis, Revision 22
: Unit 2 UFSAR, Sections 9 and 9.5, Appendix A, Revision 20
==Section 1R06: Flood Protection Measures==
===Procedure===
: N2-CTP-GEN-@200, Floor and Equipment Drain Sump Inspections, Revision 00400 
===Condition Report===
: CR-2013-004527 
===Miscellaneous===
: Calculation A10.1-AA-014, Flood Heights in RB Elevation 175 feet 0 inches UFSAR Section 3C, Revision 8 UFSAR Section 3.4, Revision 10
==Section 1R11: ==
: Licensed Operator Requa lification Program and Licensed Operator Performance 
===Procedure===
: CNG-OP-1.01-1000, Conduct of Operations, Revision 01000
==Section 1R12: Maintenance Effectiveness==
===Procedures===
: CNG-AM-1.01-1023, Maintenance Rule Program, Revision 00201
: CNG-MN-4.01-1002, Work Order Initiation, Screening, and Prioritization, Revision 00500
: CNG-OP-1.01-1002, Conduct of Operability Determinations/Functionality Assessments, Revision 00201 
===Condition Reports===
: CR-2011-006003
: CR-2011-009843
: CR-2011-009980
: CR-2012-000052
: CR-2012-001296
: CR-2012-002146
: CR-2012-002367
: CR-2012-002710
: CR-2012-002808
: CR-2012-007727
: CR-2012-008435
: CR-2012-009630
: CR-2012-009631
: CR-2012-010556
: CR-2012-010657
: CR-2012-010840
: CR-2012-010851
: CR-2013-000862
: CR-2013-000864
: CR-2013-000951
: CR-2013-001851
: CR-2013-002154
: CR-2013-002293
: CR-2013-005784
: CR-2013-006152
: CR-2013-006755
: CR-2013-006756
: CR-2013-006787
: CR-2013-007526
: CR-2013-007529 
===Work Orders===
: WO
: C91700891
: WO
: C91968032 
===Miscellaneous===
: 2-BYS-F01- 125 DC Battery Maintenance Rule Scoping Document 
: AC Electric Power System Health Report, 2
nd Quarter 2013
: ACE for
: CR-2012-008435
: Control Room HVAC System Health Report, 2
nd Quarter 2013 Direct Current Electric Power and UPS System Health Report, 2
nd Quarter 2013 EDG System Health Report, 2
nd Quarter 2013 SGTS Health Report, 2
nd Quarter 2013
==Section 1R13: Maintenance Risk Assessments and Emergent Work Control==
===Procedure===
: S-ODP-OPS-0122, Posting and Control of Protected Equipment during Online and Outage
: Operations, Revision 00500
==Section 1R15: Operability Determinations and Functionality Assessments==
===Procedures===
: CNG-HU-1.01-1000, Human Performance, Revision 00801
: N1-SO-13-01, NFPA 805 Interim Actions, Revision 0
: N2-OSP-RDS-Q001, Scram Discharge Volume Vent and Drain Valve Operability Test on November 4, 2012, Revision 00201
: N2-OSP-RDS-Q001, Scram Discharge Volume Vent and Drain Valve Operability Test on February 5, 2013, Revision 00201
: N2-OSP-RDS-Q001, Scram Discharge Volume Vent and Drain Valve Operability Test on May 6, 2013, Revision 00201 N2-OSP-RMC-W@001, Control Rod Movement and Position Indicator Verification, Revision 00501 
===Drawings===
: 0007.243-001-007, Elementary Diagram High Pressure Core Spray System, Revision 3 0007.245-001-018, Elementary Diagram Reactor Core Isolation Cooling System, Revision 6
: PID-30C-13, Piping and Instrument Drawing (P&ID) Control Rod Drive Hydraulic System, Revision 11 TL2ISC0060, Test Loop Diagram Reactor Water Level - Wide Range 2ISC*LT9A, Sheets 1 and 2 
===Condition Reports===
: CR-2012-005954
: CR-2013-004044
: CR-2013-005419
: CR-2013-005569
: CR-2013-006412
: CR-2013-006738
: CR-2013-007119
: CR-2013-007443
: CR-2013-004958
: Work Order WO
: C91934617 
===Miscellaneous===
: NUREG-0696, Functional Criteria for Emergency Response Facilities, February 1981
==Section 1R18: Plant Modifications==
===Procedures===
: CNG-FES-015, Design Engineering and Configuration Management Forms, Revision 00006
: CNG-NL-1.01-1011, 10
: CFR 50.59/10
: CFR 72.48 Applicability Determinations, Screenings and Evaluations, Revision 00300 
: A-5N1-EPM-GEN-153, Inspection and Testing of
: AK-15/25 Breakers and Associated Motors, Revision 00600 N1-RCPM-GEN-155, Load Testing of AK and ITE Breaker Trip Devices, Revision 00200 
===Condition Reports===
: CR-2013-002926
: CR-2013-006479 
===Work Orders===
: WO
: C91736503 WO
: C92057979 WO
: C92263206 
===Miscellaneous===
: ECP 12-000536, Removal of the Hottest Spot Indicating-Relay from Transformers
: XF-(16B)4160-600V and XF-(17A)4160-600V Associated With Power Boards
: PB-16B and
: PB-17A
: ECP 13-000436, Long-Time and Instantaneous Over-Current Settings for 600V Breaker
: BKR-(16B/010A)52 for the 11 ESW pump motor, Revision 0
: ECP 13-000766, Remove Over-Speed Trip from Unit 2 from Unit 2 Diesel Fire Pump, Revision 0
: ESR-13-00425, Unit 2 Diesel Fire Pump Tripped on Over-Speed with No Over-Speed Condition
: SDBD-503, RB Closed Loop Cooling System Design Basis Document, Revision 07
==Section 1R19: Post-Maintenance Testing==
===Procedures===
: N1-ST-Q8B, Liquid Poison Pump 12 and Check Valve Operability Test, Revision 00700
: N2-OSP-CNT-M003, Reactor Building Integrity Verification Test, Revision 00201 
: N2-OSP-GTS-M001, Standby Gas Treatment System Functional Test, Revision 00201 N2-OSP-LOG-W@001, GTS and HVC Run Time Log, Revision 00900 S-MMP-SDM-001, Site Doors Maintenance, Revision 00500 
: Drawing
: C-18009-C, Reactor Cleanup System P&ID, Revision 60 
===Condition Report===
: CR-2013-005740 
===Work Orders===
: WO
: C92402995 WO
: C92181936
: WO C91214860
==Section 1R20: Refueling and Other Outage Activities==
===Procedures===
: N1-OP-43A, Plant Startup, Revision 03201
: N1-OP-43C, Plant Shutdown, Revision 01200
: Drawing
: C-18009-C, Reactor Water Clean-Up P&ID, Revision 60 
===Condition Report===
: CR-2013-005749
: Work Order
: C92338737
==Section 1R22: Surveillance Testing==
===Procedures===
: N1-ISP-201-501, Type 'B' Containment Isolation Airlock Doors Leak Rate Test, Revision 00401 N1-ST-M1B, Liquid Poison Pump 12 Operability Test, Revision 00501
: N1-ST-M4B, Emergency Diesel Generator 103 and
: PB 103 Operability Test, Revision 00802
: N1-ST-M6, Core Spray Keep Fill Verification Test, Revision 01300 N1-ST-Q20, Reactor Building Heating, Cooling, and Ventilation System Test, Revision 01300 N1-ST-V13, Drywell Access Doors Interlock Test, Revision 00301 
===Condition Reports===
: CR-2013-000829
: CR-2013-003266
: CR-2013-005604
: CR-2013-005840 
===Work Orders===
: WO
: C91979329 WO C91948380
==Section 1EP4: Emergency Action Level and Emergency Plan Changes==
===Procedure===
: Off-Site Dose Assessment and Protective Action Recommendations, Revision 27
==Section 1EP6: Drill Evaluation==
===Procedure===
: EPIP-EPP-20, Emergency Notifications, Revision 02900
==Section 4OA1: Performance Indicator Verification==
===Condition Reports===
: CR-2011-001172
: CR-2013-002461
: CR-2013-004199
: CR-2013-004333
: CR-2013-004347
: CR-2013-004408
: CR-2013-004555
: A-7Miscellaneous
: LER 05000220/2012-001, Automatic Reactor Scram due to Electronic Pressure Regulator Failure
: LER 05000220/2012-002, Automatic Reactor Scram due to Automatic Generator Protective Trip
: LER 05000220/2012-003, Loss of Isolation Function on Shutdown Cooling System Suction Line due to an Operating Procedure Deficiency
: LER 05000220/2012-004, Automatic Reactor Scram Due to a Generator Load Reject
: LER 05000220/2012-005, Feedwater Level Control Failure, HPCI Initiation and Reactor Scram
: LER 05000220/2012-006, Technical Specification Shutdown due to Containment Leakage
: LER 05000410/2012-002, Loss of Isolation Function on RHR Shutdown Cooling Suction Line due to Breaker Trip
: LER 05000410/2012-003, Suppression Pool Level Below Technical Specification Limit During
: Mode Change
: LER 05000410/2012-004, Manual Reactor Scram due to a Loss of Main Turbine Gland Sealing Steam Resulting in Lowering Condenser
: LER 05000410/2012-005, Automatic Diesel Actuation due to the Loss of a 115 kV Offsite Power Source
: LER 05000410/2013-001, Reactor Core Isolation Cooling System Isolation due to a Temperature Switch Unit Failure
: LER 05000410/2013-002, Failure of High-Pressure Core Spray System Pressure Pump due to Motor Winding Failure
: NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7 Unit 1 Mitigating System Performance Index Basis Document, Revision 9 Unit 2 Mitigating System Performance Index Basis Document, Revision 11
==Section 4OA2: Problem Identification and Resolution==
===Procedures===
: CNG-AM-1.01-1023, Maintenance Rule Program, Revision 00201
: CNG-CA-1.01-1000, Corrective Action Program, Revision 00902
: CNG-CA-1.01-1010, Use of Operating Experience, Revision 01000
: CNG-MN-4.01-1002, Work Order Initiation, Screening, and Prioritization, Revision 00500
: N1-CTP-V937, Operation of the Circulating Water Chemical Injection System, Revision 00100 N1-CTP-V938, Treatment of Screen and Pump House Raw Water with Biocide, Revision 01900 N1-CTP-V945, Service Water Zebra Mussel Treatment, Revision 01600, 
: N1-OP-18, Service Water System, Revision 03000
: N2-CTP-GEN-@643, EVAC Treatment of the Service Water System, Revision 5 N2-CTP-SCT-D201, SWP Chemical Treatment System, Revision 10
: N2-ISP-RMS-002, Reactor Building Vent Wide Range Gas Monitor System Calibration, Revision 8 N2-ISP-SWP-R112, Service Water Effluent Lines 'A' and 'B' Flow Instrument Channel Calibration,
: Revision 9
: N2-RSP-RMS-SA113, Channel Functional Test of the Service Water Effluent Line Liquid
: Process Radiation Monitor, Revision 7 N2-RSP-RMS-R100, Operating Cycle Channel Calibration of the Flow System on the DRMS
: Gaseous and Gaseous/Particulate Process Radiation Monitor, Revision 3
: N2-RTP-130, Manual Flush of the Service Water Process Radiation Monitors, Revision 9
: S-ODP-OPS-0124, Control of Operator Workarounds and Burdens, Revision 00100 
===Condition Reports===
: CR-2002-004577
: CR-2011-007830
: CR-2011-008817
: CR-2011-010179
: CR-2011-010817
: CR-2012-000013 
: A-8CR-2012-000017
: CR-2012-000622
: CR-2012-000977
: CR-2012-001210
: CR-2012-001605
: CR-2012-001638
: CR-2012-002146
: CR-2012-002176
: CR-2012-002198
: CR-2012-002249
: CR-2012-002616
: CR-2012-002711
: CR-2012-002713
: CR-2012-004475
: CR-2012-004609
: CR-2012-005012
: CR-2012-005017
: CR-2012-005119
: CR-2012-005270
: CR-2012-005315
: CR-2012-005422
: CR-2012-005465
: CR-2012-005525
: CR-2012-005752
: CR-2012-001586
: CR-2012-006075
: CR-2012-006141
: CR-2012-006277
: CR-2012-006432
: CR-2012-006437
: CR-2012-006473
: CR-2012-006587
: CR-2012-007193
: CR-2012-007303
: CR-2012-007977
: CR-2012-008126
: CR-2012-008164
: CR-2012-008548
: CR-2012-008831
: CR-2012-008912
: CR-2012-009055
: CR-2012-009080
: CR-2012-009274
: CR-2012-009400
: CR-2012-009583
: CR-2012-009594
: CR-2012-009830
: CR-2012-009968
: CR-2012-010220
: CR-2012-010313
: CR-2012-010343
: CR-2012-010442
: CR-2012-010467
: CR-2012-010479
: CR-2012-010515
: CR-2012-010677
: CR-2012-010700
: CR-2012-010718
: CR-2012-010730
: CR-2012-010817
: CR-2012-010885
: CR-2012-010900
: CR-2012-010933
: CR-2012-011481
: CR-2012-011483
: CR-2012-011501
: CR-2012-011517
: CR-2012-011574
: CR-2012-011620
: CR-2013-000007
: CR-2013-000012
: CR-2013-000136
: CR-2013-000141
: CR-2013-000243
: CR-2013-000563
: CR-2013-000868
: CR-2013-000917
: CR-2013-000978
: CR-2013-001234
: CR-2013-001286
: CR-2013-001491
: CR-2013-001810
: CR-2013-002562
: CR-2013-002615
: CR-2013-004689
: CR-2013-004986
: CR-2013-005171
: CR-2013-005206
: CR-2013-005591
: CR-2013-005684 CR-2013-005854
: CR-2013-006244
: CR-2013-006249
: Work Order WO
: C92073592 
===Miscellaneous===
: ECP 11-000140, Install a Separate Flow Sensor Array on the Radwaste Vent Ducting
: ECP 12-000565, 2SWP*CAB146B Replace Carbon Steel Pipe to Stainless Steel
: ECP 13-000140, Replacement of the Existing Resistance-Type Flow Switch with a New Magnetic Flow Switch
: ECP 13-000167, Unit 1 Service Water Radiation Monitor Sample Pumps are Over-Sized Resulting in Premature Failure Nine Mile Point (a)(1) Database
: OE Section of Maintenance Rule Manager Database Unit 2 Offsite Dose Calculation Manual, Revision 34
==Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion==
: Drawing C18017C, Emergency Cooling System P&ID, Revision 55
==Section 4OA5: Other Activities==


===Procedures===
: CNG-AM-9.01-1000, Underground Pipe and Tank Management, Revision 00300
: CNG-FES-047, Performance of Underground Pipe and Tank Management Program Activities
: Revision 00001
: CNG-OP-1.01-1001, Rev. 00701, Operational Decision Making
: CNG-OP-1.01-1009, Rev. 00100, Monitoring and Contingency Planning For Abnormal Conditions
: CNG-OP-4.01-1000, Integrated Risk Management, Revision 01300
: CNG-PR-1.01-1009, Procedure and Work Order Use and Adherence Requirements, Revision 00004
: EPIP-EPP-26, Natural Hazard Preparation and Recovery, Revision 00400
: GAP-MTE-01, Control and Use of Measuring and Test Equipment, Revision 01501
: N1-OP-64, Meteorological Monitoring, Revision 00700 N2-OP-102, Meteorological Monitoring, Revision 01103 N2-SOP-90, Natural Events, Revision 00302
: S-MAP-SPC-0101, NMP Welding Procedure
: S-MMP-ISFSI-004, DSC Sealing Operation, Revision 00201
: S-MMP-ISFSI-004, DSC Sealing Operation, Revision 00300 S-MMP-ISFSI-011, ISFSI Abnormal Events, Revision 0001 
===Condition Reports===
: CR-2013-001952
: CR-2013-004298
: CR-2013-006461
: CR-2013-006940 
===Miscellaneous===
: CENG Flood Hazard Reevaluation Report for NMPNS (ML130740943), November 20, 2012
: Interim Staff Guidance, November 30, 2012, Revision 0
: NEI 09-14, Guidelines for the Management of Underground Piping and Tank Integrity,
: Revision 3, April 2013
: NEI 12-07, Guidelines for Performing Verification Walkdowns of Plant Flood Protection Features,
: May 2012 NMPNS Flood Stop Test Fit Report, July 16 and 17, 2013
: Self-Assessment Report,
: SA-2012-000241, Underground Pipe and Tanks Underground Piping and Tanks Management Condition Assessment Plan, August 7, 2013 Units 1 and 2 Program Health Reports, Underground Pipe and Tank for April 1 to June 30, 2013
: USAR, Section 2.4.2, Revision 20 
: A-10
==LIST OF ACRONYMS==
: [[CFR]] [[Title 10 of the Code of Federal Regulations]]
: [[AC]] [[alternating current]]
: [[ACE]] [[apparent cause evaluation]]
: [[ADAMS]] [[Agencywide Documents Access and Management System]]
: [[CAP]] [[corrective action program]]
: [[CENG]] [[Constellation Energy Nuclear Group,]]
: [[LLC]] [[]]
: [[CR]] [[condition report]]
: [[DSC]] [[dry shielded canister]]
: [[ECP]] [[engineering change package]]
: [[EDG]] [[emergency diesel generator]]
: [[ESW]] [[emergency service water]]
: [[FA]] [[fire area]]
: [[HPCS]] [[high-pressure core spray]]
: [[HVAC]] [[heating, ventilation, and air conditioning]]
: [[INPO]] [[Institute of Nuclear Power Operations]]
: [[IMC]] [[Inspection Manual Chapter]]
: [[ISFSI]] [[independent spent fuel storage installation]]
: [[LER]] [[licensee event report]]
: [[NEI]] [[Nuclear Energy Institute]]
: [[NMPNS]] [[Nine Mile Point Nuclear Station,]]
: [[LLC]] [[]]
: [[NRC]] [[Nuclear Regulatory Commission]]
: [[OE]] [[operating experience]]
: [[OGEMS]] [[off-gas effluent monitoring system]]
: [[OOS]] [[out of service]]
: [[PI]] [[performance indicator]]
: [[RB]] [[reactor building]]
: [[RCIC]] [[reactor core isolation cooling]]
: [[SGTS]] [[standby gas treatment system]]
: [[SSC]] [[structure, system, and component]]
: [[SW]] [[service water]]
: [[TI]] [[temporary instruction]]
: [[TS]] [[technical specification]]
: [[UFSAR]] [[Updated Final Safety Analysis Report]]
: [[UPS]] [[uninterruptible power supply WO  work order]]
}}
}}

Latest revision as of 14:02, 20 December 2019

IR 05000220-13-004, 05000410-13-004; 07/01/2013 - 09/30/2013; Nine Mile Point Nuclear Station (Nmpns), Units 1 and 2; Routine Integrated Inspection Report
ML13317B750
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 11/13/2013
From: Daniel Schroeder
Reactor Projects Branch 1
To: Costanzo C
Constellation Energy Nuclear Group
Schroeder D
References
IR-13-004
Download: ML13317B750 (35)


Text

UNITED STATES ber 13, 2013

SUBJECT:

NINE MILE POINT NUCLEAR STATION, LLC - NRC INTEGRATED INSPECTION REPORT 05000220/2013004 AND 05000410/2013004

Dear Mr. Costanzo:

On September 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Nine Mile Point Nuclear Station, LLC (NMPNS) Units 1 and 2. The enclosed inspection report documents the inspection results, which were discussed on October 24, 2013, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

No findings were identified during this inspection.

In accordance with Title 10 of the Code of Federal Regulations 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of the NRCs Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Daniel L. Schroeder, Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos: 50-220 and 50-410 License Nos: DPR-63 and NPF-69

Enclosure:

Inspection Report 05000220/2013004 and 05000410/2013004 w/ Attachment: Supplementary Information

REGION I==

Docket Nos: 50-220 and 50-410 License Nos: DPR-63 and NPF-69 Report Nos: 05000220/2013004 and 05000410/2013004 Licensee: Constellation Energy Nuclear Group, LLC (CENG)

Facility: Nine Mile Point Nuclear Station, LLC (NMPNS)

Units 1 and 2 Location: Oswego, NY Dates: July 1, 2013, through September 30, 2013 Inspectors: K. Kolaczyk, Senior Resident Inspector E. Miller, Resident Inspector J. Ambrosini, Senior Resident Inspector J. DeBoer, Project Engineer B. Dionne, Health Physicist S. Hammann, Senior Health Physicist P. Kaufman, Senior Reactor Inspector J. Krafty, Resident Inspector J. Laughlin, Emergency Preparedness Inspector Approved by: Daniel L. Schroeder, Chief Reactor Projects Branch 1 Division of Reactor Projects Enclosure

SUMMARY

IR 05000220/2013004, 05000410/2013004; 07/01/2013 - 09/30/2013; Nine Mile Point Nuclear

Station (NMPNS), Units 1 and 2; Routine Integrated Inspection Report.

The report covered a 3-month period of inspection by resident inspectors and announced inspections performed by regional inspectors. The inspectors identified no findings during this period. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4.

No findings were identified.

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent power. On July 3, 2013, power was decreased to 90 percent to start recirculation pump 15. Power was returned to 100 percent later that day. On July 8, Unit 1 was shut down due to elevated unidentified leakage in the primary containment. Following identification of the source of the leakage and the completion of repairs to the reactor water cleanup vent valve 33-61, Unit 1 returned to 100 percent power on July 12. On July 13, power was reduced to 75 percent for a rod pattern adjustment and later that day returned to 100 percent power. On September 9, Unit 1 decreased power to 90 percent to perform turbine stop valve testing and remove recirculation pump 13 from service.

Reactor power was returned to 100 percent later that day. Unit 1 remained at full power for the remainder for the inspection period.

Unit 2 began the inspection period at 100 percent power. On July 19, 2013, reactor power was decreased to 98 percent due to high condensate pump discharge header temperature. Power was returned to 100 percent later that day. On September 7, Unit 2 reduced power to 85 percent to conduct turbine stop valve testing, returning to full power that same day. On September 21, Unit 2 reduced power to 70 percent to perform a control rod pattern adjustment and scram time testing. Unit 2 returned to full power on September 22 and operated at full power for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

The inspectors performed a review of the stations readiness for the onset of seasonal high temperatures. The review focused on Unit 1 batteries 11 and 12 and emergency diesel generators (EDGs) 102 and 103 on July 17, 2013. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), technical specifications (TSs), and the corrective action program (CAP) to determine what temperatures or other seasonal weather could challenge these systems, and to ensure CENG personnel had adequately prepared for these challenges. The inspectors reviewed station procedures including CENGs seasonal weather readiness procedure and applicable operating procedures.

The inspectors performed walkdowns of the selected systems to ensure station personnel identified issues that could challenge the operability of the systems during hot weather conditions. Documents reviewed for each section of this inspection report are listed in the Attachment.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems:

Unit 2 Division I standby gas treatment system (SGTS) following functional testing on July 18, 2013 Unit 1 uninterruptible power supply (UPS) system for the reactor protection system bus 11 following the trip of the alternating current (AC) breaker for UPS 162A and B on July 22, 2013 Unit 1 offsite power systems following testing on EDG 102 on July 25, 2013 Unit 2 high-pressure core spray (HPCS) system while the reactor core isolation cooling (RCIC) system was out of service (OOS) for planned maintenance on August 6, 2013 The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the UFSAR, TSs, work orders (WOs), condition reports (CRs), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether CENG staff had properly identified equipment issues and entered them into the CAP for resolution with the appropriate significance characterization.

b. Findings

No findings were identified.

.2 Full System Walkdown

a. Inspection Scope

On September 17, 2013, the inspectors performed a complete system walkdown of accessible portions of the Unit 1 primary containment isolation valves to verify the existing equipment lineup was correct. The inspectors reviewed operating procedures, drawings, completed surveillances, and the UFSAR to verify the system was aligned to perform its required safety functions. The inspectors performed field walkdowns of accessible portions of the system to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of components and observed operating parameters of equipment to verify that there were no deficiencies. Additionally, the inspectors reviewed a sample of related CRs and WOs to ensure CENG personnel appropriately evaluated and resolved any deficiencies.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Resident Inspector Quarterly Walkdowns

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that CENG personnel controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression equipment were available for use, as specified in the area pre-fire plan, and that passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for OOS, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.

Unit 1 control room (fire area (FA)-11) on July 3, 2013 Unit 2 control room (FA-26) on July 3, 2013 Unit 1 EDG 102 (FA-22) on July 9, 2013 Unit 1 EDG 103 (FA-19) on July 9, 2013 Unit 2 Division I EDG (FA-28) on July 9, 2013 Unit 2 Division II EDG (FA-29) on July 9, 2013 Unit 2 Division III EDG (FA-30) on July 9, 2013

b. Findings

No findings were identified.

.2 Fire Protection - Drill Observation

a. Inspection Scope

The inspectors observed a fire brigade drill scenario conducted on August 27, 2013, that involved a fire on the first floor of the Unit 2 operations building. The inspectors evaluated the readiness of the plant fire brigade to fight fires. The inspectors verified that CENG personnel identified deficiencies, openly discussed them in a self-critical manner at the debrief, and took appropriate corrective actions as required. The inspectors evaluated specific attributes as follows:

Proper wearing of turnout gear and self-contained breathing apparatus Proper use and layout of fire hoses Employment of appropriate fire-fighting techniques Sufficient fire-fighting equipment brought to the scene Effectiveness of command and control Search for victims and propagation of the fire into other plant areas Smoke removal operations Utilization of pre-planned strategies Adherence to the pre-planned drill scenario Drill objectives met The inspectors also evaluated the fire brigades actions to determine whether these actions were in accordance with CENGs fire-fighting strategies.

b. Findings

No findings were identified.

1R06 Flood Protection Measures

.1 Internal Flooding Review

a. Inspection Scope

The inspectors reviewed the UFSAR, flooding calculations, and plant procedures to assess susceptibilities involving internal flooding. The inspectors also reviewed the CAP to determine if CENG personnel identified and corrected flooding problems and whether operator actions for coping with flooding were adequate. The inspectors also focused on the Unit 2 reactor building (RB) elevation 175 feet to verify the adequacy of equipment seals located below the flood line, floor and water penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, control circuits, and temporary or removable flood barriers.

b. Findings

No findings were identified.

.2 Annual Review of Cables Located in Underground Bunkers/Manholes

a. Inspection Scope

The inspectors conducted an inspection of underground bunkers/manholes subject to flooding that contain cables whose failure could affect risk-significant equipment. The inspectors performed walkdowns of risk-significant areas, including Unit 2 manholes MH-1 and MH-3 which contain power cables for the high-pressure coolant spray system pump, to verify that the cables were not submerged in water, that cables and/or splices appeared intact, and to observe the condition of cable support structures. The inspectors reviewed CENG corrective actions initiated following a July 22, 2013, discovery that a dewatering system, which had been installed in 2012 to dewater manholes MH-1 and MH-3, had failed to properly operate, and as a result, several feet of water had accumulated in the cable vaults. The performance deficiency surrounding this issue is discussed in greater detail in NRC Inspection Report 05000410/2013007. For those cables found submerged in water, the inspectors verified that CENG staff had conducted an operability evaluation for the cables and were implementing appropriate corrective actions.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Quarterly Review of Licensed Operator Requalification Testing and Training (2 samples)

a. Inspection Scope

The inspectors observed:

Unit 1 licensed operator training simulator scenario which included a control rod drive failure, failure of power board 11, and a leak in the reactor water cleanup system on September 3, 2013 Unit 2 licensed operator training simulator scenario which included a loss of instrument air, a loss of a control rod drive pump, a stuck open safety relief valve, and a stuck open turbine bypass valve on September 3, 2013 The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classifications made by the shift manager and the TS action statements entered by the shift technical advisor.

Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.

b. Findings

No findings were identified.

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

(2 samples)

a. Inspection Scope

The inspectors observed:

Unit 1 control room operations during a scheduled plant shutdown due to increased drywell leakage on July 8, 2013 Unit 2 control room operations during planned surveillance activities on the Division III EDG and an emergency preparedness drill on August 20, 2013 The inspectors reviewed CNG-OP-1.01-1000, Conduct of Operations, Revision 01000, and verified that procedure use, crew communications, and coordination of plant activities among work groups similarly met established expectations and standards.

Additionally, the inspectors observed test performance to verify that procedure use, crew communications, and coordination of activities between work groups similarly met established expectations and standards.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on structure, system, and component (SSC) performance and reliability. The inspectors reviewed system health reports, CAP documents, maintenance WOs, and maintenance rule basis documents to ensure that CENG personnel were identifying and properly evaluating performance problems within the scope of the maintenance rule. For each sample selected, the inspectors verified that the SSC were properly scoped into the maintenance rule in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 50.65 and verified that the (a)(2) performance criteria established by CENG staff were reasonable. As applicable, for SSCs classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these SSCs to (a)(2) status. Additionally, the inspectors ensured that CENG staff were identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.

Unit 1 AC electric power on August 19, 2013 Unit 2 control room heating, ventilation, and air conditioning (HVAC) and RB and EDG building ventilation on August 21, 2013 Unit 2 main station safety-related batteries on September 12, 2013 Unit 1 instrument air system on September 13, 2013

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that CENG personnel performed the appropriate risk assessments prior to removing equipment from service.

The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that CENG personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When CENG personnel performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the stations probabilistic risk analyst to verify plant conditions were consistent with the risk assessment. The inspectors also reviewed the TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.

Unit 2 Division I standby liquid control system during Division II surveillance testing on July 31, 2013 Unit 1 containment spray 122 during planned maintenance on containment spray loop 121 on August 8, 2013 Unit 1 high-pressure coolant injection system 11 during planned maintenance on the high-pressure coolant injection system 12 on August 13, 2013 Unit 2 Division II control room ventilation system during planned maintenance on the Division I control room ventilation system on August 27, 2013 Unit 1 EDG 102 and core spray 121 during the core spray 122 surveillance test on September 12, 2013 Unit 1 EDG 103 during EDG 102 surveillance testing on September 25, 2013

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or non-conforming conditions:

Unit 2 RCIC/HPCS initiation logic discrepancy on July 1, 2013 Unit 2 control rod 30-51 failed to settle at position 46 on July 2, 2013 Unit 2 Division II EDG volt amperes reactive and amperes over procedural limit on July 30, 2013 Unit 2 RCIC trip throttle valve did not reset from the control room on August 9, 2013 Unit 1 RB instrument air compensatory action for postulated fires in the turbine and control buildings on August 12, 2013 Unit 2 improper design of scram discharge volume vent and drain valves 2RDS*AOV130 and 2RDS*AOV132 on August 26, 2013 Unit 1 elevated technical support center temperatures on September 10, 2013 Unit 1 control rod drive flange leakage on September 18, 2013 The inspectors selected these issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the operability determinations to assess whether TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to CENG staffs evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled by CENG personnel. The inspectors determined, where appropriate, compliance with bounding limitations associated with these evaluations.

b. Findings

No findings were identified.

1R18 Plant Modifications

.1 Temporary Modifications (2 samples)

a. Inspection Scope

The inspectors reviewed the temporary modifications listed below to determine whether the modifications affected the safety functions of systems that are important to safety.

The inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results, and conducted field walkdowns of the modifications to verify that the temporary modifications did not degrade the design bases, licensing bases, and performance capability of the affected systems.

Engineering Change Package (ECP) 13-000436 - Long-time and instantaneous over-current settings for 600V breaker BKR-(16B/010A)52 for the emergency service water (ESW) pump 11 motor at Unit 1.

ECP 13-000766 - Remove over-speed trip device from diesel fire pump at Unit 2.

b. Findings

No findings were identified.

.2 Permanent Modification (1 sample)

a. Inspection Scope

The inspectors evaluated a modification to remove the Unit 1 hottest spot indicator relay from the 4160V-600V transformers for safety-related power boards 16B and 17A implemented by ECP 12-000536, Removal of the Hottest Spot Indicating-Relay from Transformers XF-(16B)4160-600V and XF-(17A)4160-600V Associated With Power Boards (PB)-16B and PB-17A. The inspectors verified that the design bases, licensing bases, and performance capability of the affected system was not degraded by the modification. In addition, the inspectors reviewed modification documents associated with the upgrade and design change including the post-maintenance testing and the 10 CFR 50.59 screening form. The inspectors also reviewed proposed revisions to the control room alarm response procedure to ensure the changes were appropriate.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test procedure to verify that the procedure adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure were consistent with the information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed test data to verify that the test results adequately demonstrated restoration of the affected safety functions.

Unit 2 Division II SGTS following preventive maintenance on August 1, 2013 Unit 1 ESW pump 11 following failure to start on August 2, 2013 Unit 2 RB truck bay inner door seal on August 21, 2013 Unit 1 liquid poison pump 12 following installation of a new flow meter on September 24, 2013

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

The inspectors reviewed the stations work schedule and outage risk plan for the Unit 1 planned outage which was conducted July 8 through July 11, 2013. The inspectors reviewed CENG staffs development and implementation of outage plans and schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered. During the outage, the inspectors observed portions of the shutdown and cooldown processes and monitored controls associated with the following outage activities:

Power reduction activities Drywell closeout activities Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable TSs when taking equipment OOS Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated work or testing Status and configuration of electrical systems and switchyard activities to ensure that TSs were met Monitoring of decay heat removal operations Activities that could affect reactivity Power ascension activities

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR, and CENG procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests:

Unit 1, N1-ISP-201-501, Type B Containment Isolation Airlock Door Leak Rate Test on July 10, 2013 Unit 1, N1-ST-Q20, Reactor Building Heating, Cooling, and Ventilation System Test on July 31, 2013 Unit 1, N1-ST-M4B, Emergency Diesel Generator 103 and PB 103 Operability Test on August 5, 2013 Unit 1, N1-ST-M1B, Liquid Poison Pump 12 Operability Test on August 26, 2013 (inservice test)

Unit 1, N1-ST-M6, Core Spray Keep Fill Verification Test on September 24, 2013

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

The Office of Nuclear Security and Incident Response headquarters staff performed an in-office review of the latest revisions of various emergency plan implementing procedures and the emergency plan located under ADAMS accession number ML13155A006.

CENG staff determined that in accordance with 10 CFR 50.54(q), the changes made in the revisions resulted in no reduction in the effectiveness of the plan and that the revised plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50, Emergency Planning and Preparedness of Production and Utilization Facilities. The NRC review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, this revision is subject to future inspection.

b. Findings

No findings were identified.

1EP6 Drill Evaluation

Training Observation

a. Inspection Scope

The inspectors observed a simulator training evolution for Unit 1 licensed operators on September 3, 2013, which required emergency plan implementation by an operations crew. CENG staff planned for this evolution to be evaluated and included in performance indicator (PI) data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew.

The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the crews performance and ensure that CENG evaluators noted the same issues and entered them into the CAP.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Safety System Functional Failures (2 samples)

a. Inspection Scope

The inspectors sampled CENGs submittals for the Safety System Functional Failures PIs for Unit 1 and Unit 2 for the period of July 1, 2012, through June 30, 2013. To determine the accuracy of the PI data reported during those periods, inspectors used definitions and guidance contained in the Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 10 CFR 50.73." The inspectors reviewed CENGs operator narrative logs, operability assessments, maintenance rule records, CRs, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index (10 samples)

a. Inspection Scope

The inspectors reviewed CENGs submittal of the Mitigating Systems Performance Index for the following systems for the period of July 1, 2012, through June 30, 2013:

Unit 1 and Unit 2 Emergency AC Power System (MS06)

High-Pressure Injection System (MS07)

Heat Removal System (MS08)

Residual Heat Removal System (MS09)

Cooling Water System (MS10)

To determine the accuracy of the PI data reported during those periods, the inspectors used definitions and guidance contained in NEI 99-02. The inspectors also reviewed CENGs operator narrative logs, CR, mitigating systems performance index basis document, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure 71152, Problem Identification and Resolution, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that CENG personnel entered issues into the CAP at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the CAP.

b. Findings

No findings were identified.

.2 Annual Sample: Maintenance Rule Implementation Assessment

a. Inspection Scope

The inspectors maintenance rule implementation review focused on CENG staffs screening of CRs for maintenance rule applicability, incorporation of operating experience (OE) into the maintenance rule, timing of maintenance rule evaluations once the threshold for (a)(1) was met, and balancing unavailability and unreliability. The inspectors reviewed CRs, system health reports, the (a)(1) database, and interviewed the maintenance rule coordinator and system engineers in order to assess if CENG was implementing the program in accordance with CNG-AM-1.01-1023, Maintenance Rule Program, Revision 00201, and CNG-CA-1.01-1010, Use of Operating Experience, Revision 01000.

b. Findings and Observations

No findings were identified.

The inspectors reviewed CRs that were screened for maintenance rule applicability for three systems (AC electric power, control room HVAC, and EDG room ventilation). In general, the CRs were screened appropriately; however, there were two CRs in which the inspectors were unable to conclude that the CENG staffs determination that maintenance rule not applicable was correct until CENG staff provided additional information.

The inspectors determined that OE was being incorporated into the maintenance rule through the system engineers health reports, maintenance rule manager software, and cause evaluations when required. The inspectors review of the OE sections of several systems in the maintenance rule manager software indicated that they were being maintained up-to-date with applicable OE.

The inspectors reviewed 24 systems that were currently in (a)(1) status and determined that (a)(1) evaluations were typically done in a timely manner. The average time to make an (a)(1) determination was 35 days with a range of 0 to 78 days.

.3 Annual Sample: Corrective Actions to Address Repetitive Failures of the Radiation

Monitoring Equipment

a. Inspection Scope

Units 1 and 2 have experienced repetitive failures of several radiation monitoring systems between August 2011 and August 2013. The four effluent monitors with the highest number of hours of unavailability were selected for a detailed sample review.

The four effluent radiation monitors and associated number of CRs that were reviewed included:

Unit 1 off-gas effluent monitoring system (OGEMS) (6 CRs)

Unit 1 service water (SW) radiation monitors PMP-72-461 and PMP-72-462 (20 CRs)

Unit 2 SW radiation monitors 2SWP*CAB146A and 2SWP*CAB146B (52 CRs)

Unit 2 radwaste/reactor building vent radiation monitor (20 CRs)

From August 4 through 9, 2013, the inspectors performed an in-depth review of the events in these CRs to assess CENG staffs actions for initiating corrective and/or compensatory actions, timeliness, and addressing adverse trends. To perform this review, the inspectors conducted walkdowns of these radiation monitors, interviewed plant personnel, reviewed WOs, and associated apparent cause evaluations (ACEs). In addition, system health reports for the radiation monitoring system and associated maintenance rule reports were also reviewed.

b. Findings and Observations

No findings were identified.

After identifying an adverse trend in radiation monitor availability and reliability, CENG personnel initiated its first generic CR on radiation monitors for Units 1 and 2 on January 16, 2013, and the second CR on February 27, 2013. These two CRs resulted in two ACEs. The first one was to investigate maintenance and engineering corrective actions for the effluent radiation monitors (CR-2013-000434), and the second was to investigate human performance impacts on equipment reliability of these instruments (CR-2013-001613). These two ACEs appeared to be thorough and included the extent of condition, common causes, and action plans to prevent recurrence. Based on these evaluations, CENG staff concluded that there were a number of system design improvements that could be made to improve reliability of the effluent monitoring systems. It was concluded that there had been errors assigning the appropriate priority (priority two or three instead of priority four) on the WOs resulting in untimely completion of some of the radiation monitoring equipment repairs. Briefings were conducted by CENG personnel with the appropriate staff to indicate the importance of the radiation monitoring instruments relative to event classification in the emergency plan. In addition, training was also provided on the steps that should be taken to expedite these instruments return to service.

Listed below are summaries of the corrective actions CENG personnel developed to improve system availability and reliability for the four radiation monitors of concern:

Unit 1 Off-Gas Effluent Monitoring System Corrective action (CA)-2012-004479 was initiated to develop and execute a troubleshooting plan to isolate the cause for the noise intrusion on the Unit 1 stack radiation monitor. CENG is planning to implement the electrical troubleshooting plan via WO C92073592. No unplanned unavailability has occurred on the OGEMS radiation monitor since April 2013. CENG plans to monitor system performance until corrective actions are completed.

Unit 1 Service Water Radiation Monitor CR-2011-006930 was written to revise the procedures for biocide/chemical injections and sample line flushes to reduce the impact of both biofouling and zebra mussels on the SW system. In particular, chemistry procedure N1-CTP-V945, Service Water Zebra Mussel Treatment, Revision 01600, was revised to notify the Unit 1 operations department of a requirement to perform N1-OP-18, Service Water System, Revision 03000, sections 8 and 9, daily during biocide treatment and for 21 days following completion of the activity. Preventive maintenance surveillance N1149646 was established to track this operations activity in January 2012. The operations department has been performing these flushes daily following two biocide treatments conducted in 2013.

CA-2012-000076 was initiated to correct unexpected radiation monitor process annunciator H1-4-5 alarms of the SW radiation monitor. The system and central processing unit circuit cards were replaced in January 2013. No spurious annunciator alarms have occurred since completion of this maintenance activity.

CR-2012-008164 was initiated to perform a maintenance rule 10 CFR 50.65 (a)(1)evaluation for Unit 1 SW radiation monitor because the functional failure performance criteria was exceeded. On October 2, 2012, the plant health committee approved the system performance goals and action plan.

CR-2012-002176 investigated the root cause for the repeated low flow alarms on the SW radiation monitor pump. It was determined that the installed pump, PMP-72-462, was being operated outside the manufacturer pump curve and was likely being operated near the pumps shutoff head. ECP 13-000167, Unit 1 Service Water Radiation Monitor Sample Pumps are Over-Sized Resulting in Premature Failure, was processed and has resulted in the replacement of the PMP-72-462 pump with a smaller capacity centrifugal pump on June 28, 2013. No unplanned unavailability has occurred on the Unit 1 SW radiation monitor since June 2013. Corrective actions appear to be effective.

Unit 2 Service Water Radiation Monitor CR-2012-011225 was initiated to perform a maintenance rule 10 CFR 50.65 (a)(1)evaluation for Unit 2 SW radiation monitors, 2-RMS-F11. On January 29, 2013, the plant health committee approved the system performance goals and action plan. The following corrective actions from this plan are listed below along with their current status:

Replace the remaining piping in accordance with ECP 12-000565, 2SWP*CAB146B Replace Carbon Steel Pipe to Stainless Steel and WO C91883844. This action was completed on April 1, 2013.

Initiate temporary sodium bisulfate injection until repairs can be completed on the permanent chemical treatment equipment per WO C92156031 (CA-2013-000702).

The temporary equipment for injecting the chemical to SW was completed in April 2013. Injection of chemicals into SW was reinitiated on April 22, 2013.

Replace the current flow switch design with a design less susceptible to fouling and scaling. ECP 13-000140, Replacement of the Existing Resistance-Type Flow Switch with a New Magnetic Flow Switch is projected to be completed by December 31, 2013, as identified in CR-2013-001810.

The inspectors noted that one of the a(1) action plan items, chemical treatments, was not performed on the SW system for over 7 months, from September 2012 to April 22, 2013, due to a leak in one of the chemical injection tanks. Unavailability problems continue as evidenced by a recent reactor operating event notification report number 49391. This notification indicated that the SW digital radiation monitor received a low sample flow alarm and was nonfunctional on September 28 and 29, 2013.

In accordance with the NRC Enforcement Manual, this does not constitute a violation of 10 CFR 50.65.(a)(1) since an action plan was developed and was being implemented and monitoring goals in accordance with the 50.65 (a)(1). CENG initiated CR-2013-005232 to address the need to create PIs for key system chemical parameters to assist in more optimal scheduling of chemical treatments and flushes on the SW system.

Corrective actions are not yet completed.

Unit 2 Radwaste/Reactor Building Vent Radiation Monitor Several instrument calibrations failures have occurred on this instrument due to issues with the calibration equipment associated with this monitor. CA-2013-000226 was initiated to create a preventive maintenance surveillance to periodically inspect the check source insertion assembly for wear, re-orient steel roll pin in the check source assembly so that it does not contact the aluminum guide tube, and replace the aluminum guide tube with an equivalent sized steel guide tube. These inspections and modifications will be completed during the next monitor surveillance currently scheduled to be completed in November 2013.

A design issue for this flow sensor was identified and documented on March 10, 2009.

In 2011, ECP 11-000140, Install a Separate Flow Sensor Array on the Radwaste Vent Ducting was initiated. These flow sensors were designed to establish representative flow sample rates for the plant configuration when the RB ventilation flow is isolated or when the RB ventilation fans are not available.

CR-2013-006249 identified the degraded flow sensing array modification was not being tracked properly and developed corrective actions which included long-term asset management. On August 26, 2013, this modification was approved for conceptual design work. CENG initiated CR-2013-006249 to track completion of this modification.

The inspectors noted that the Unit 2 radwaste/RB vent radiation monitor was nonfunctional for 2,731 hours0.00846 days <br />0.203 hours <br />0.00121 weeks <br />2.781455e-4 months <br /> between August 2011 and August 2013. A non safety related, low risk system is only required to monitor for reliability and not required to monitor for system unavailability; however, the high level of system unavailability has resulted in a reduction of EP staffs assessment capability. Although 10 CFR 50.65 a(2)performance criteria were met and no maintenance rule functional failures were identified by CENG staff, on two occasions CENG staff made reports to the NRC as required by 10 CFR 50.72 (b)(3)(xiii) due to unavailability of these instruments. This included reactor operating event notification reports 49127 and 49176 for loss of radwaste/RB vent gaseous effluent radiation monitor that occurred in June and July 2013. No findings were identified since compensatory sampling of the gaseous effluents occurred as required. CR-2013-008833 was written to address this observation.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

(Closed) Licensee Event Report (LER) 05000220/2013-001-00: Emergency Condenser 11 High Steam Flow Isolation Instrumentation Loss During Plant Startup On May 14, 2013, at 11:45 a.m., while Unit 1 was in the startup mode of reactor plant operation with reactor power at 3 percent, channel 11 high steam flow instrumentation for emergency condenser loop 11 alarmed due to a gross failure trip. The gross failure trip is a design feature of the instrument loop that monitors the integrity of the emergency condenser piping system. The failure of the channel 11 high steam flow instrumentation concurrently with channel 12, which had failed earlier in the day at 8:40 a.m., resulted in the loss of emergency condenser system loop 11 isolation capability on high steam flow.

In response to the instrument failure, operators declared emergency condenser system loop 11 inoperable, isolated the system, and entered plant TS 3.1.3.b, which required operators to return the system to service within 7 days when the reactor is critical and reactor coolant system temperature is greater than 212 degree Fahrenheit. Emergency condenser system loop 11 was declared operable on May 15 when the cause for the gross failure trip signal and inadequately filled sensing lines was resolved.

A CENG investigation determined that the cause of the event was leakage from the shared high-pressure sensing line for transmitters DPT-36-06C and DPT-36-06D. The suspected leakage path was seat leakage from instrument blowdown valves VLV-36-374 and VLV-8-172. CENG staffs corrective actions include replacement of the suspect blowdown isolation valves during the next refueling outage and enhanced monitoring of the output signals on the high steam flow instruments to ensure the sensing lines remain full. The inspectors reviewed the LER and determined that no findings or violations of NRC requirements were identified. This LER is closed

4OA5 Other Activities

.1 Institute of Nuclear Power Operations (INPO) Report Review

a. Inspection Scope

The inspectors reviewed the January 30, 2013, final report for the INPO plant assessment of NMPNS conducted for the period of September 2010 to December 2012.

The report primarily relied on observations made by INPO representatives during the weeks of October 5 and October 18, 2012.

The inspectors evaluated the report to ensure that NRC perspectives of CENG staffs performance were consistent with any issues identified during the assessment and to verify that the final report content was similar to the initial report provided in January.

The inspectors also reviewed the report to determine whether INPO identified any significant safety issues that required further NRC follow-up.

b. Findings

No findings were identified.

.2 Temporary Instruction (TI) 2515/182, Review of the Implementation of the Industry

Initiative to Control Degradation of Underground Piping and Tanks, Phase 2

a. Inspection Scope

In accordance with paragraph 03.02.a of TI 2515/182, the inspectors reviewed CENGs programs for buried piping and underground piping and tanks and confirmed that activities which correspond to the completion dates specified in the program which have passed since the Phase 1 inspection was conducted have been completed.

CENG staffs buried piping and underground piping and tanks program were inspected in accordance with paragraph 03.02.b of TI 2515/182 and responses to specific questions found in www.nrc.gov/reactors/operating/ops-experience/buried-pipe-ti-phase-2-insp-req-2011-11-16.pdf were submitted to NRC headquarters staff.

b. Findings

No findings were identified.

.3 TI 2515/190, Inspection of the Proposed Interim Actions Associated with Near-Term

Task Force Recommendation 2.1 Flooding Hazard Evaluations.

a. Inspection Scope

Inspectors verified that CENG staffs interim actions will perform their intended function for flooding mitigation.

The inspectors independently verified that CENG staffs proposed interim actions would perform their intended function for flooding mitigation.

Visual inspection of the flood protection feature was performed if the flood protection feature was relevant. External visual inspection for indications of degradation that would prevent its credited function from being performed was performed.

Reasonable simulation, if applicable, to the site.

Flood protection feature functionality was determined using either visual observation or by review of other documents.

The inspectors verified that issues identified were entered into CENGs CAP.

b. Findings

No findings were identified.

.4 Operation of an Independent Spent Fuel Storage Installation (ISFSI) at Operating Plants

(IP 60855)

a. Inspection Scope

(1 partial sample)

Region I materials inspectors conducted a follow up inspection to review CENG staffs action following a hydrogen deflagration during ISFSI loading operations using NRC Inspection Procedure (IP) 60855.1, Operation of an Independent Spent Fuel Storage Installation at Operating Plants.

On August 14, 2013, Unit 2 experienced a hydrogen deflagration during ISFSI loading operations (CR-2013-006840). A dry shielded canister (DSC) filled with spent fuel assemblies was on the refuel floor and the DSC inner cover was in the process of being welded in place by an automated welding system. During the welding evolution, hydrogen concentration built up above the lower explosive limit and the deflagration occurred. CENG staff completed a technical evaluation and concluded that spent fuel within the cask was not impacted and that the cask remained within UFSAR specifications.

The ISFSI inspectors performed an on-site inspection August 26 through 28, 2013. The inspection consisted of interviews with CENG personnel and contractor personnel and observations of ISFSI equipment configuration on the refuel floor. The inspectors reviewed documentation to verify compliance with the conditions of the general license, certificate of compliance, TSs, and the UFSAR. The inspectors also reviewed CRs, WOs, and procedures. The inspectors reviewed CENG staffs evaluations and immediate follow-up actions to assure that CENG staff implemented appropriate compensatory and corrective actions prior to resuming ISFSI welding and loading operations.

b. Findings

This inspection remains open at the end of this inspection period while CENG staff completes their ACE and the inspectors have the opportunity to review CENG staffs evaluation and long-term corrective actions to address the event.

4OA6 Meetings, Including Exit

Exit Meeting On October 24, 2013, the inspectors presented the inspection results to Mr. Christopher Costanzo, Site Vice President, and other members of the NMPNS staff. The inspectors verified that no propriety information was retained by the inspectors or documented in this report.

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

C. Costanzo, Vice President
J. Stanley, Plant General Manager
P. Bartolini, Supervisor, Design Engineering
J. Bouck, Manager, Operations
B. Busch, Unit 1 General Supervisor, Operations
K. Clark, Director, Security
J. Dean, Supervisor, Quality Assurance
S. Dhar, Design Engineering
S. Eckhard, Supervisor Design Engineering
W. Farnham, System Engineer
N. Fisher, Quality Performance Assessor
J. Gerber, Manager, Training
J. Gillard, Emergency Preparedness Analyst
J. Holton, Supervisor, Systems Engineering
G. Inch, Principle Engineer, EPU Project Manager
M. Kunzwiler, Security Supervisor
M. Khan, General Supervisor Design Engineering
J. Leonard, Supervisor Design Engineering
J. Manly, Unit 2 General Supervisor, Operations
C. McClay, Senior Engineer
E. Perkins, Director, Licensing
J. Reid, Design Engineer
T. Roche, System Engineer
S. Segretto, System Engineer
M. Shanbhag, Licensing Engineer
J. Snyder, Maintenance Rule Coordinator
S. Stone, System Engineer
T. Syrell, Manager, Nuclear Safety and Security
J. Thompson, General Supervisor, Mechanical Maintenance
A. Verno, Director, Emergency Preparedness

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

Closed

05000220/2013-001-00 LER Emergency Condenser 11 High Steam Flow Isolation Instrumentation Loss During Plant Startup (Section 4OA3)

LIST OF DOCUMENTS REVIEWED