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| issue date = 11/22/1989
| issue date = 11/22/1989
| title = Responds to Violations Noted in Insp Repts 50-250/89-43 & 50-251/89-43.Corrective Actions:Supervisors & Chiefs in Electrical Dept Instructed to Clearly Communicate Job Scope & Clearance Requirements to Control Room Personnel
| title = Responds to Violations Noted in Insp Repts 50-250/89-43 & 50-251/89-43.Corrective Actions:Supervisors & Chiefs in Electrical Dept Instructed to Clearly Communicate Job Scope & Clearance Requirements to Control Room Personnel
| author name = GOLDBERG J H
| author name = Goldberg J
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
Line 14: Line 14:
| page count = 9
| page count = 9
}}
}}
See also: [[followed by::IR 05000250/1989043]]


=Text=
=Text=
{{#Wiki_filter:ACCELERATED
{{#Wiki_filter:ACCELERATED DISTBXBUTION DEMONSTPJ!!,TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
DISTBXBUTION
CESSION NBR:8912050052             DOC.DATE:   89/11/22     NOTARIZED: NO       DOCKET g FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C               05000250 50-251 Turkey Point Plant, Unit 4, Florida Power and Light C               05000251 AUTH. NAME           AUTHOR AFFILIATION GOLDBERG,J.H.       Florida Power & Light Co.
DEMONSTPJ!!,TION
RECIP.NAME           RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SYSTEM REGULATORY
 
INFORMATION
==SUBJECT:==
DISTRIBUTION
Responds to violations noted in Insp Repts 50-250/89-43 &
SYSTEM (RIDS)CESSION NBR:8912050052
50-251/89-43.
DOC.DATE: 89/11/22 NOTARIZED:
DISTRIBUTION CODE: IE01D COPIES RECEIVED:LTR               1   ENCL 1 SIZE:
NO DOCKET g FACIL:50-250
TITLE: General     (50 Dkt)-Insp Rept/Notice of Violation Response NOTES RECIPIENT             COPIES            RECIPIENT          COPIES ID CODE/NAME            LTTR ENCL        ID CODE/NAME     LTTR ENCL PD2-2 PD                     1    1    EDISON,G                1    1 INTERNAL: AEOD                                     AEOD/DEIIB              1    1 AEOD/TPAD                                DEDRO                  1    1 NRR SHANKMAN,S                           NRR/DEST DIR            1    1 NRR/DLPQ/PEB                             NRR/DOEA DIR 11        1    1 NRR/DREP/EPB 10                         NRR/DREP/RPB 10        2    2 NRR/DRIS/DIR                                        I NRR/PMAS/ LRB1 2        1    1 NUDOCS-ABSTRACT                         0      B    N,J      1    1 OGC/HDS2                                   EG FILE      02      1    1 RES MORISSEAUiD                          RGN2      FILE 01      1     1 EXTERNAL: LPDR                                      NRC PDR                1    1 NSIC NOTE TO ALL "RIDS" RECIPIENTS:
Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 50-251 Turkey Point Plant, Unit 4, Florida Power and Light C 05000251 AUTH.NAME AUTHOR AFFILIATION
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEED!
GOLDBERG,J.H.
TAL NUMBER OF COPIES REQUIRED: LTTR               24  ENCL   24
Florida Power&Light Co.RECIP.NAME
 
RECIPIENT AFFILIATION
II P.O. Box 14000, Juno Beach, FL 33408-0420 I=PL                                  NOVEMBER      2 2 1989 L-89-423 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:
Document Control Branch (Document Control Desk)SUBJECT: Responds to violations
Re:   Turkey Point Units 3 and 4 Docket Nos. 50-250 and 50-251 Reply to Notice of Violation Ins ection Re ort 89-43 Florida Power 6 Light Company (FPL)    has  reviewed the subject e inspection report and pursuant to 10 attached.
noted in Insp Repts 50-250/89-43
CFR 2.201 the response is Very  truly yours, t
&50-251/89-43.
r
DISTRIBUTION
    ~i  -l~(4j.'.g J. H. Goldberg Executive Vice President JGH/JRH/rh Attachment cc:   Stewart D. Ebneter, Regional Administrator, Region II,                 USNRC Senior Resident Inspector, USNRC, Turkey Point Plant
CODE: IE01D COPIES RECEIVED:LTR
                                                                                        ~go f
1 ENCL 1 SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice
 
of Violation Response NOTES INTERNAL: RECIPIENT ID CODE/NAME PD2-2 PD AEOD AEOD/T PAD NRR SHANKMAN,S
0                                       ATTACHMENT RE:     Turkey Point Units 3 and 4 Docket Numbers 50-250 and 50-251 NRC Inspection Report 89-43 FINDING TS 6.8.1 requires. that written procedures and administrative. policies shall be established, implemented and maintained that meet or exceed the requirements and recommendations of Appendix A of USNRC Regulatory Guide 1.33 and Sections 5.1 and 5.3 of ANSI N18.7-1972.
NRR/DLPQ/PEB
NRC Regulatory Guide 1.33, Appendix A, item 1, specifies that procedures should be written for   equipment c'ontrol .
NRR/DREP/EPB
Section 5.1.2 of ANSI N18.7-1972 requires that procedures be followed.
10 NRR/DRIS/DIR
Administrative Procedure 0103.4, In-Plant Equipment Clearance Orders, dated July 27, 1989, specified that In-Plant Equipment Clearance Orders shall be re-quired for the safety and protection of plant personnel and equipment.
NUDOCS-ABSTRACT
Contrary to the above, clearance number 4-89-09-069 was inadequate on September 20, 1989, in that MOV-4-1420 was not fully isolated. This allowed the line to remain pressurized which caused the valve stem to be ejected resulting in ser-ious injury to a plant electrician.
OGC/HDS2 RES MORISSEAUiD
 
COPIES LTTR ENCL 1 1 RECIPIENT ID CODE/NAME EDISON,G AEOD/DEIIB
===RESPONSE===
DEDRO NRR/DEST DIR NRR/DOEA DIR 11 NRR/DREP/RPB
: 1. FPL concurs   with the finding.
10 NRR/PMAS/I LRB 1 2 0 B N,J EG FILE 02 RGN2 FILE 01 COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 EXTERNAL: LPDR NSIC NRC PDR 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
: 2. The reason   for the violation was inadequate training for the task at hand .
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION
When the job scope on Motor Operated Valve (MOV)-4-1420 expanded from re-placing the motor operator to replacing the actuator stem drive sleeve lock-nut., clearance requirements were not re-evaluated by Electrical Department personnel. It was assumed that because the initial clearance identified the sub)ect valve as being "isolated" the system pressure had been relieved .
LISIS FOR DOCUMENTS YOU DON'T NEED!TAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24
The Electrical Maintenance Department had received valve actuator training approximately 18 months prior to the accident. The Chief Electricians had the mechanical section of the training but remembered precautions concern-ing system pressure only after the accident occurred. In addition, the Chief Electrician and electrical crew had no practical experience in work-ing with piping systems.
II
: 3. Corrective steps which have been taken     and the results achieved include:
P.O.Box 14000, Juno Beach, FL 33408-0420
: a. The accounts of this event were described in Plant Safety Meetings.
I=PL NOVEMBER 2 2 1989 L-89-423 U.S.Nuclear Regulatory
The root cause and contributing causes for the accident were discuss-ed in detail.
Commission
: b. Supervisors and Chiefs within the Electrical Department have been in-structed to clearly communicate their job scope and clearance require-ments to Control Room personnel.       Additionally, the need to re-evalu-ate clearance requirements     each time a job scope changes and the need for strict adherence to the requirement for a clearance walkdown prior to the commencement of maintenance activities has been re-emphasized.
Attn: Document Control Desk Washington, D.C.20555 Gentlemen:
This was achieved through discussions at shop meetings and by memoran-dum to Electrical Department personnel.
Re: Turkey Point Units 3 and 4 Docket Nos.50-250 and 50-251 Reply to Notice of Violation Ins ection Re ort 89-43 Florida Power 6 Light Company (FPL)has reviewed the subject e inspection
C ~  General Maintenance Elect'rical (GME) procedures O-GME-0102.9, "Motor Operated Valve Operator, Inspection and Overhaul (SMB-OOO)," and 0-GME-0102.10, "Motor Operated Valve Operator, Inspection and Overhaul (SMB-00 and SMB-500)" have been converted from General Maintenance Mechani-cal (GMM) procedures and approved by the Plant Manager-Nuclear. A Pre-caution has been added to these procedures which states, "Do not remove stem nut locknut or upper bearing housing       if a thrust load is on the actuator or   if the valve is under pressure and not fully open, as per-sonnel injury may result. Once the stem nut locknut is removed, stem movement can occur. Stem blocking should be used when removing stem nut locknut and shall be used when     it cannot be verified that the pipe is drained and vented ." In addition, a Caution has been added which states, "Do not remove locking nut with unit under load or with valve under pressure.     Stem blocking should be used and shall be used when i
report and pursuant to 10 CFR 2.201 the response is attached.Very truly yours, t r~i-l~(4j.'.g
it c annot b e v erified that t he p p e is drained and vented.
J.H.Goldberg Executive Vice President JGH/JRH/rh
e 4. Corrective steps which a ~
Attachment
will be taken to avoid   further violations include:
cc: Stewart D.Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant~go f  
Procedure O-GMM-0102.8, "Motor Operated Valve Operator, Inspection and Overhaul (SMB-0 through SMB-4)," will be converted to a GME procedure after it has been revised to include Precaution and Caution statements similar to those added to procedures O-GME-0102.9 and O-GME-0102.10.
: b. Electrical   Department personnel assigned to work on valve actuators will receive training that,     as a minimum, will include the following:
0 ATTACHMENT
Methods to render a pressurized     valve actuator safe for disassem-bly.
RE: Turkey Point Units 3 and 4 Docket Numbers 50-250 and 50-251 NRC Inspection
Methods   for testing to verify that   a valve actuator has been made safe to work.
Report 89-43 FINDING TS 6.8.1 requires.that written procedures
Examples of a generic clearance needed to repair a valve under both pressurized and depressurized conditions.
and administrative.
Detailed discussion of Safe Work Practice Rules regarding clear-ance testing to verify and ensure a proper clearance'ntil this training is completed, Mechanical Maintenance personnel will support Electrical     Maintenance personnel during valve actuator
policies shall be established, implemented
 
and maintained
maintenance, as necessary.
that meet or exceed the requirements
: 5. The date when full compliance will be achieved:
and recommendations
a ~  Item 3.a was completed on November 1, 1989.
of Appendix A of USNRC Regulatory
: b. Item 3.b was completed on October 5, 1989.
Guide 1.33 and Sections 5.1 and 5.3 of ANSI N18.7-1972.
c~  Item 3.c was completed on November 9, 1989.
NRC Regulatory
d ~  Item 4.a  will be complete by February 15, 1990.
Guide 1.33, Appendix A, item 1, specifies that procedures
: e. Item 4.b will be  complete by February 15, 1990.
should be written for equipment c'ontrol.Section 5.1.2 of ANSI N18.7-1972
 
requires that procedures
~}}
be followed.Administrative
Procedure 0103.4, In-Plant Equipment Clearance Orders, dated July 27, 1989, specified that In-Plant Equipment Clearance Orders shall be re-quired for the safety and protection
of plant personnel and equipment.
Contrary to the above, clearance number 4-89-09-069
was inadequate
on September 20, 1989, in that MOV-4-1420
was not fully isolated.This allowed the line to remain pressurized
which caused the valve stem to be ejected resulting in ser-ious injury to a plant electrician.
RESPONSE 1.FPL concurs with the finding.2.The reason for the violation was inadequate
training for the task at hand.When the job scope on Motor Operated Valve (MOV)-4-1420
expanded from re-placing the motor operator to replacing the actuator stem drive sleeve lock-nut., clearance requirements
were not re-evaluated
by Electrical
Department
personnel.
It was assumed that because the initial clearance identified
the sub)ect valve as being"isolated" the system pressure had been relieved.The Electrical
Maintenance
Department
had received valve actuator training approximately
18 months prior to the accident.The Chief Electricians
had the mechanical
section of the training but remembered
precautions
concern-ing system pressure only after the accident occurred.In addition, the Chief Electrician
and electrical
crew had no practical experience
in work-ing with piping systems.3.Corrective
steps which have been taken and the results achieved include:  
a.The accounts of this event were described in Plant Safety Meetings.The root cause and contributing
causes for the accident were discuss-ed in detail.b.Supervisors
and Chiefs within the Electrical
Department
have been in-structed to clearly communicate
their job scope and clearance require-ments to Control Room personnel.
Additionally, the need to re-evalu-ate clearance requirements
each time a job scope changes and the need for strict adherence to the requirement
for a clearance walkdown prior to the commencement
of maintenance
activities
has been re-emphasized.
This was achieved through discussions
at shop meetings and by memoran-dum to Electrical
Department
personnel.
General Maintenance
Elect'rical (GME)procedures
O-GME-0102.9,"Motor Operated Valve Operator, Inspection
and Overhaul (SMB-OOO)," and 0-GME-0102.10,"Motor Operated Valve Operator, Inspection
and Overhaul (SMB-00 and SMB-500)" have been converted from General Maintenance
Mechani-cal (GMM)procedures
and approved by the Plant Manager-Nuclear.
A Pre-caution has been added to these procedures
which states,"Do not remove stem nut locknut or upper bearing housing if a thrust load is on the actuator or if the valve is under pressure and not fully open, as per-sonnel injury may result.Once the stem nut locknut is removed, stem movement can occur.Stem blocking should be used when removing stem nut locknut and shall be used when it cannot be verified that the pipe is drained and vented." In addition, a Caution has been added which states,"Do not remove locking nut with unit under load or with valve under pressure.Stem blocking should be used and shall be used when it annot e erified that he i e C~e c b v t p p is drained and vented.4.Corrective
steps which will be taken to avoid further violations
include: a~Procedure O-GMM-0102.8,"Motor Operated Valve Operator, Inspection
and Overhaul (SMB-0 through SMB-4)," will be converted to a GME procedure after it has been revised to include Precaution
and Caution statements
similar to those added to procedures
O-GME-0102.9
and O-GME-0102.10.
b.Electrical
Department
personnel assigned to work on valve actuators will receive training that, as a minimum, will include the following:
Methods to render a pressurized
valve actuator safe for disassem-bly.Methods for testing to verify that a valve actuator has been made safe to work.Examples of a generic clearance needed to repair a valve under both pressurized
and depressurized
conditions.
Detailed discussion
of Safe Work Practice Rules regarding clear-ance testing to verify and ensure a proper clearance'ntil
this training is completed, Mechanical
Maintenance
personnel will support Electrical
Maintenance
personnel during valve actuator  
5.The a~maintenance, as necessary.
date when full compliance
will be achieved: Item 3.a was completed on November 1, 1989.b.c~d~e.Item 3.b was completed on October 5, 1989.Item 3.c was completed on November 9, 1989.Item 4.a will be complete by February 15, 1990.Item 4.b will be complete by February 15, 1990.
~
}}

Latest revision as of 09:15, 22 October 2019

Responds to Violations Noted in Insp Repts 50-250/89-43 & 50-251/89-43.Corrective Actions:Supervisors & Chiefs in Electrical Dept Instructed to Clearly Communicate Job Scope & Clearance Requirements to Control Room Personnel
ML17347B436
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 11/22/1989
From: Goldberg J
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-89-423, NUDOCS 8912050052
Download: ML17347B436 (9)


Text

ACCELERATED DISTBXBUTION DEMONSTPJ!!,TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

CESSION NBR:8912050052 DOC.DATE: 89/11/22 NOTARIZED: NO DOCKET g FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 50-251 Turkey Point Plant, Unit 4, Florida Power and Light C 05000251 AUTH. NAME AUTHOR AFFILIATION GOLDBERG,J.H. Florida Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Responds to violations noted in Insp Repts 50-250/89-43 &

50-251/89-43.

DISTRIBUTION CODE: IE01D COPIES RECEIVED:LTR 1 ENCL 1 SIZE:

TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 PD 1 1 EDISON,G 1 1 INTERNAL: AEOD AEOD/DEIIB 1 1 AEOD/TPAD DEDRO 1 1 NRR SHANKMAN,S NRR/DEST DIR 1 1 NRR/DLPQ/PEB NRR/DOEA DIR 11 1 1 NRR/DREP/EPB 10 NRR/DREP/RPB 10 2 2 NRR/DRIS/DIR I NRR/PMAS/ LRB1 2 1 1 NUDOCS-ABSTRACT 0 B N,J 1 1 OGC/HDS2 EG FILE 02 1 1 RES MORISSEAUiD RGN2 FILE 01 1 1 EXTERNAL: LPDR NRC PDR 1 1 NSIC NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEED!

TAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24

II P.O. Box 14000, Juno Beach, FL 33408-0420 I=PL NOVEMBER 2 2 1989 L-89-423 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:

Re: Turkey Point Units 3 and 4 Docket Nos. 50-250 and 50-251 Reply to Notice of Violation Ins ection Re ort 89-43 Florida Power 6 Light Company (FPL) has reviewed the subject e inspection report and pursuant to 10 attached.

CFR 2.201 the response is Very truly yours, t

r

~i -l~(4j.'.g J. H. Goldberg Executive Vice President JGH/JRH/rh Attachment cc: Stewart D. Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant

~go f

0 ATTACHMENT RE: Turkey Point Units 3 and 4 Docket Numbers 50-250 and 50-251 NRC Inspection Report 89-43 FINDING TS 6.8.1 requires. that written procedures and administrative. policies shall be established, implemented and maintained that meet or exceed the requirements and recommendations of Appendix A of USNRC Regulatory Guide 1.33 and Sections 5.1 and 5.3 of ANSI N18.7-1972.

NRC Regulatory Guide 1.33, Appendix A, item 1, specifies that procedures should be written for equipment c'ontrol .

Section 5.1.2 of ANSI N18.7-1972 requires that procedures be followed.

Administrative Procedure 0103.4, In-Plant Equipment Clearance Orders, dated July 27, 1989, specified that In-Plant Equipment Clearance Orders shall be re-quired for the safety and protection of plant personnel and equipment.

Contrary to the above, clearance number 4-89-09-069 was inadequate on September 20, 1989, in that MOV-4-1420 was not fully isolated. This allowed the line to remain pressurized which caused the valve stem to be ejected resulting in ser-ious injury to a plant electrician.

RESPONSE

1. FPL concurs with the finding.
2. The reason for the violation was inadequate training for the task at hand .

When the job scope on Motor Operated Valve (MOV)-4-1420 expanded from re-placing the motor operator to replacing the actuator stem drive sleeve lock-nut., clearance requirements were not re-evaluated by Electrical Department personnel. It was assumed that because the initial clearance identified the sub)ect valve as being "isolated" the system pressure had been relieved .

The Electrical Maintenance Department had received valve actuator training approximately 18 months prior to the accident. The Chief Electricians had the mechanical section of the training but remembered precautions concern-ing system pressure only after the accident occurred. In addition, the Chief Electrician and electrical crew had no practical experience in work-ing with piping systems.

3. Corrective steps which have been taken and the results achieved include:
a. The accounts of this event were described in Plant Safety Meetings.

The root cause and contributing causes for the accident were discuss-ed in detail.

b. Supervisors and Chiefs within the Electrical Department have been in-structed to clearly communicate their job scope and clearance require-ments to Control Room personnel. Additionally, the need to re-evalu-ate clearance requirements each time a job scope changes and the need for strict adherence to the requirement for a clearance walkdown prior to the commencement of maintenance activities has been re-emphasized.

This was achieved through discussions at shop meetings and by memoran-dum to Electrical Department personnel.

C ~ General Maintenance Elect'rical (GME) procedures O-GME-0102.9, "Motor Operated Valve Operator, Inspection and Overhaul (SMB-OOO)," and 0-GME-0102.10, "Motor Operated Valve Operator, Inspection and Overhaul (SMB-00 and SMB-500)" have been converted from General Maintenance Mechani-cal (GMM) procedures and approved by the Plant Manager-Nuclear. A Pre-caution has been added to these procedures which states, "Do not remove stem nut locknut or upper bearing housing if a thrust load is on the actuator or if the valve is under pressure and not fully open, as per-sonnel injury may result. Once the stem nut locknut is removed, stem movement can occur. Stem blocking should be used when removing stem nut locknut and shall be used when it cannot be verified that the pipe is drained and vented ." In addition, a Caution has been added which states, "Do not remove locking nut with unit under load or with valve under pressure. Stem blocking should be used and shall be used when i

it c annot b e v erified that t he p p e is drained and vented.

e 4. Corrective steps which a ~

will be taken to avoid further violations include:

Procedure O-GMM-0102.8, "Motor Operated Valve Operator, Inspection and Overhaul (SMB-0 through SMB-4)," will be converted to a GME procedure after it has been revised to include Precaution and Caution statements similar to those added to procedures O-GME-0102.9 and O-GME-0102.10.

b. Electrical Department personnel assigned to work on valve actuators will receive training that, as a minimum, will include the following:

Methods to render a pressurized valve actuator safe for disassem-bly.

Methods for testing to verify that a valve actuator has been made safe to work.

Examples of a generic clearance needed to repair a valve under both pressurized and depressurized conditions.

Detailed discussion of Safe Work Practice Rules regarding clear-ance testing to verify and ensure a proper clearance'ntil this training is completed, Mechanical Maintenance personnel will support Electrical Maintenance personnel during valve actuator

maintenance, as necessary.

5. The date when full compliance will be achieved:

a ~ Item 3.a was completed on November 1, 1989.

b. Item 3.b was completed on October 5, 1989.

c~ Item 3.c was completed on November 9, 1989.

d ~ Item 4.a will be complete by February 15, 1990.

e. Item 4.b will be complete by February 15, 1990.

~