IR 05000266/2005018: Difference between revisions

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{{IR-Nav| site = 05000266 | year = 2005 | report number = 018 | url = https://www.nrc.gov/reactors/operating/oversight/reports/poin_2005018.pdf }}
{{Adams
| number = ML060240610
| issue date = 01/18/2006
| title = IR 05000266-05-018; 05000301-05-018 (Drs); 12/12/2005 - 12/16/2005; Point Beach Nuclear Power Station, Units 1 and 2; Evaluation of Changes, Tests, or Experiments (10 CFR 50.59) and Permanent Plant Modifications
| author name = Hills D E
| author affiliation = NRC/RGN-III/DRS/EB1
| addressee name = Koehl D L
| addressee affiliation = Nuclear Management Co, LLC
| docket = 05000266, 05000301
| license number = DPR-024, DPR-027
| contact person =
| document report number = IR-05-018
| document type = Inspection Report, Letter
| page count = 26
}}
 
{{IR-Nav| site = 05000266 | year = 2005 | report number = 018 }}
 
=Text=
{{#Wiki_filter:
[[Issue date::January 18, 2006]]
 
Mr. Dennis Site Vice President
 
Point Beach Nuclear Plant
 
Nuclear Management Company, LLC
 
6590 Nuclear Road
 
Two Rivers, WI 54241-9516
 
SUBJECT: POINT BEACH NUCLEAR POWER PLANT, UNITS 1 AND 2 , NRCEVALUATION OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT
 
PLANT MODIFICATIONS BASELINE INSPECTION REPORT
 
05000266/2005018; 05000301/2005018 (DRS)
 
==Dear Mr. Koehl:==
On December 16, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed a combined baseline inspection of the Evaluation of Changes, Tests, or Experiments and
 
Permanent Plant Modifications at the Point Beach Nuclear Power Station. The enclosed report
 
documents the results of the inspection, which were discussed with Mr. and others of
 
your staff at the completion of the inspection on December 16, 2005.
 
The inspectors examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed
 
personnel. Based on the results of the inspection, two NRC-identified findings and one self-
 
revealing finding of very low safety significance were identified which involved violations of NRC requirements. However, because these violati ons were of very low safety significance and because they were entered into your corrective action program, the NRC is treating the issues
 
as Non-Cited Violations in accordance with Section VI.A.1 of the NRC's Enforcement Policy.
 
If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.
 
Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-
 
0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region
 
III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
 
Office at the Prairie Island Nuclear Generating Plant facility.
 
D. Koehl-2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public
 
Document Room or from the Publicly Av ailable Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Sincerely,/RA/ David E. Hills, Chief Engineering Branch 1
 
Division of Reactor Safety Docket Nos. 50-266; 50-301 License Nos. DPR-24; DPR-27
 
===Enclosure:===
Inspection Report 05000266/2005018; 05000301/2005018 (DRS)
cc w/encl:F. Kuester, President and Chief Executive Officer, We Generation
 
J. Cowan, Executive Vice President
 
Chief Nuclear Officer
 
D. Cooper, Senior Vice President, Group Operations
 
J. McCarthy, Site Director of Operations
 
D. Weaver, Nuclear Asset Manager
 
Plant Manager
 
Regulatory Affairs Manager
 
Training Manager
 
Site Assessment Manager
 
Site Engineering Director
 
Emergency Planning Manager
 
J. Rogoff, Vice President, Counsel & Secretary
 
K. Duveneck, Town Chairman
 
Town of Two Creeks
 
Chairperson
 
Public Service Commission of Wisconsin
 
J. Kitsembel, Electric Division
 
Public Service Commission of Wisconsin
 
State Liaison Officer
 
=SUMMARY OF FINDINGS=
IR 05000266/2005018; 05000301/2005018 (DRS); 12/12/2005 - 12/16/2005; Point Beach
 
Nuclear Power Station, Units 1 and 2;  Evaluation of Changes, Tests, or Experiments (10 CFR 50.59) and Permanent Plant Modifications.
 
The inspection covered a one-week announced baseline inspection on evaluations of changes, tests, or experiments and permanent plant modifi cations. The inspection was conducted by four regional based engineering inspectors. Three Green Non-Cited Violations (NCV) were identified. The significance of most findings is indicated by their color (Green, White, Yellow,
Red), using Inspection Manual Chapter 0609, "Significance Determination Process (SDP.)"
 
Findings for which the SDP does not apply, may be Green, or be assigned a severity level after
 
NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.Inspector-Identified and Self-Revealed Findings
 
===Cornerstone: Mitigating Systems===
: '''Green.'''
The inspectors identified a Severity Level IV Non-Cited Violation of 10 CFR 50.59(d)(1) for the licensee's failure to perform a safety evaluation for compensatory actions taken for an activity associated with a degraded plant condition.
 
Specifically, the licensee "screened out" an activity which replaced an automatic action for Chemical and Volume Control System (C VCS) letdown isolation on low pressurizer level with a manual action to isolate letdown on low pressurizer level, while replacing the
 
Unit 2 pressurizer low level bistables with Unit 2 online at power. At the end of the inspection period, the licensee planned to perform a safety evaluation in accordance with 10 CFR 50.59 for the compensatory actions taken for the activity associated with the degraded plant condition.
 
Because the issue affected the NRC's ability to perform its regulatory function, this finding was evaluated using the traditional enforcement process. The finding was determined to be more than minor because the inspectors, at the time of the inspection, could not reasonably determine that the UFSAR change, which adversely affected equipment important to safety, would not have ultimately required NRC approval. The inspectors evaluated the finding using IMC 0609, Appendix A, Phase 1 screening for the mitigating systems cornerstone and determined that the finding was of very low safety significance because the finding was not a design or qualification deficiency that was confirmed to result in a loss of operability or functionality per "Part 9900, Technical
 
Guidance, Operability Determination Process for Operability and Functional
 
Assessment."  (Section 1R02.1.b.2)
: '''Green.'''
A self-revealed finding of very low safety significance was associated with a violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control."  During replacement of the Service Water outlet valves for the Component Cooling Water (CCW)
 
heat exchangers, the licensee failed to evaluate design differences between the original valves and the replacement valves. These differences led to the eventual failure of the stems in both valves. This issue was entered into the licensee's corrective action system.
 
4 The issue was more than minor because it affected the mitigating system cornerstone attribute of "Design Control" and affected the cornerstone objective of ensuring reliability of systems that respond to initialing events to prevent undesirable consequences. Specifically, failure of these valves could prevent proper c ooling of safety related systems. The finding screened as having very low significance (Green) using IMC 0609, Appendix A,
"Significance Determination of Reactor Inspection Findings for the At-Power Situations,"
 
because the inspectors answered "no" to all five questions under the Mitigating Systems
 
Cornerstone column of the Phase 1 worksheet. While the design deficiency led to failure of the valves, the failures occurred during a plant shutdown; therefore, the valves would not have been required to function as designed.  (Section 1R17.1.b.1)
 
===Cornerstone: Barrier Integrity===
: '''Green.'''
The inspectors identified a Severity Level IV Non-Cited Violation associated with the failure to perform an adequate safety evaluation review as required by 10 CFR 50.59 for changes made to the facility as described in the UFSAR. In safety evaluation, EVAL 2004-
 
003, the licensee failed to provide a basis for the determination that on-line repairs to the excess letdown line with a freeze seal in place as a boundary for Reactor Coolant System (RCS) effluent from the Reactor Coolant Pumps (RCPs) was acceptable without a license amendment. Specifically, for this freeze seal evolution, the licensee would have replaced the American Society of Mechanical Engineers (ASME) Class II, Seismic Class I piping in the excess letdown line with a freeze plug while the plant was still on-line. Within the 10 CFR 50.59 evaluation, the licensee failed to provide a basis for why this freeze seal evolution did not present more than a minimal increase in the likelihood of occurrence of a malfunction of a Structure, System and Component (SSC) important to safety. As a result of this issue, the licensee performed a revision to the original safety evaluation to withdraw the facility change that allowed the freeze seal with the plant online.
 
Because the issue affected the NRC's ability to perform its regulatory function, this finding was evaluated using the traditional enforcement process. The finding was determined to be more than minor because the inspectors could not reasonably determine that the UFSAR change, which adversely affected equipment impor tant to safety, would not have ultimately required NRC approval. The finding was determined to be of very low safety significance (Green), because the inspectors answered "no" to all three questions under the
 
Containment Barriers Cornerstone column of the Phase 1 worksheet. Specifically, the licencee had not actually performed this evolution when the pressure boundary was required to be intact.  (Section 1R02.1.b.1).
 
===B.Licensee-Identified Violations===
 
No findings of significance were identified.
 
5
 
=REPORT DETAILS=
1.REACTOR SAFETYCornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity1R02Evaluations of Changes, Tests, or Experiments (71111.02).1Review of 10 CFR 50.59 Evaluations and Screenings
 
====a. Inspection Scope====
From December 12 through 16, 2005, the inspectors reviewed six evaluations performed pursuant to 10 CFR 50.59. The inspectors confirmed that the evaluations were thorough
 
and that prior NRC approval was obtained as appropriate. The inspectors also reviewed
 
14 screenings where licensee personnel had determined that a 10 CFR 50.59 evaluation
 
was not necessary. In regard to the changes reviewed where no 10 CFR 50.59 evaluation
 
was performed, the inspectors verified that the changes did not meet the threshold to
 
require a 10 CFR 50.59 evaluation. The evaluations and screenings were chosen based on
 
risk significance, safety significance, and complexity. The list of documents reviewed by the
 
inspectors is included as an attachment to this report.
 
The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, "Guidelines for 10 CFR 50.59 Implementation," Revision 1, to determine acceptability of the completed
 
evaluations and screenings. The NEI document was endorsed by the NRC in Regulatory
 
Guide 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and
 
Experiments," dated November 2000. The inspectors also consulted
 
Part 9900 of the NRC Inspection Manual, "10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments."
 
====b. Findings====
b.1Updated Final Safety Analysis Report Change to Replace ASME Class II, Seismic Class I, Piping with a Freeze Seal
 
=====Introduction:=====
The inspectors identified a Severity Level IV Non-cited Violation (NCV) of very low safety significance for failing to perform an adequate safety evaluation in accordance
 
with 10 CFR 50.59. The safety evaluation, EVAL 2004-003, involved an updated Final
 
Safety Analysis Report (UFSAR) change that a llowed on-line repairs to the excess letdown line with a freeze seal in place as a boundary for RCS effluent from the RCPs. Within the
 
safety evaluation, the licensee failed to provide a basis for why this freeze seal evolution did
 
not present more than a minimal increase in the likelihood of occurrence of a malfunction of
 
an SSC important to safety.
 
=====Description:=====
The licensee initiated 10 CFR 50.59 Evaluation 2004-003 to help facilitate repairs to valve 2CV-285, "Excess Letdown Outlet Valve."  To perform this work with the
 
plant on-line, the licensee proposed to install a freeze seal upstream of 2CV-285 to establish
 
isolation of the valve from the RCP seal return line. The line that the freeze seal would be
 
placed on was qualified as ASME Class II, Seismic Category I, pressure boundary piping.
 
During the work, the bonnet for 2CV-285 would be removed; however, if the freeze seal 6 were to fail, a contingency action was put in place for operators to manually realign 3-way valve 2CV-312, located upstream of the freeze seal, so that water could be diverted to the
 
Reactor Coolant Drain Tank (RCDT), and thus minimize leakage.
 
The inspectors noted that the 10 CFR 50.59 evaluation did not address the freeze seal evolution properly in its response to the question that asked if the activity resulted in a more
 
than minimal increase in the likelihood of occurrence of a malfunction of a Structure System
 
or Component (SSC) important to safety prev iously evaluated in the current license basis.
 
The 10 CFR 50.59 evaluation contained little justification for the downgrading of the ASME
 
Class II pressure boundary and no justification for the downgrading of the Seismic Class I
 
qualification. The freeze plug did not provide the same degree of barrier integrity as an
 
ASME Class II, Seismic Class I, pipe. The inspectors were concerned, because the
 
licensee would be substituting an ASME Class II, Seismic Category I, boundary with a non-
 
Code recognized pressure boundary material (e.g., ice plug). This was not a permissible repair under Section XI, Article IWA-4000, of the ASME Code, which only recognizes
 
pressure boundary repair by welding, brazing, or metal removal. The safety function of the
 
line was to serve as a pressure boundary for reactor coolant from the RCP seal return line, while the malfunction would be a line break. In response to this question in the 10 CFR
 
50.59 evaluation, the licensee justified the ev olution primarily by stating that strong procedural controls were in place to prevent any anticipated problems. This approach was
 
insufficient to show that downgrading of the boundaries would not have result in more than a
 
minimal increase in the likelihood of occurrence of a malfunction of the pressure boundary
 
line.Although the facility change described in the UFSAR and allowed by the 10 CFR 50.59 evaluation allowed this evolution to occur on-line, the licensee had instead performed the
 
evolution during an outage. While this was fortuitous, the licensee had still changed the
 
facility as described in the UFSAR to allow this type of evolution.
 
The inspectors determined that the 10 CFR 50.59 evaluation that was performed to allow this freeze seal evolution with the plant on-line was not in accordance with the requirements
 
in 10 CFR 50.59, because the evaluation did not adequately address the downgrading of the
 
pressure boundary from ASME Class II to a freeze plug, and because it did not address the
 
deletion of the Seismic Class I qualification for the line. The inspectors noted that this
 
change to the UFSAR may have resulted in more than a minimal increase in the likelihood
 
of occurrence of a malfunction of an SSC important to safety, since the freeze plug would
 
not have provided the same degree of barrier integrity for the RCS effluent from the RCP
 
seals as the actual ASME Class II, Seismic Class I, piping would have. The licensee
 
entered this condition into their corrective action program as CAP069372. As a result, the
 
licensee performed a revision to the original 10 CFR 50.59 evaluation to withdraw the
 
original facility change that allowed this freeze seal evolution with the plant on-line.
 
=====Analysis:=====
The inspectors determined that this issue was a performance deficiency, since the licensee permanently changed the facility as described in the UFSAR without providing the
 
necessary justification under 10 CFR 50.59 for the reduction of the pressure boundary of the
 
excess letdown line from an ASME Class II, Seismic Class I, pipe to a freeze seal. The
 
finding was determined to be more than minor, because the inspectors could not reasonably
 
determine that the UFSAR change, which adverse ly affected equipment important to safety, would not ultimately have required NRC approval.
 
7 Because violations of 10 CFR 50.59 are considered to be violations that potentially impede or impact the regulatory process, they are dispositioned using the traditional enforcement
 
process instead of the Significance Determination Process (SDP). However, if possible, the
 
underlying technical issue is evaluated under the SDP to determine the severity of the
 
violation. In this case, the finding screened as having very low significance (Green) using
 
IMC 0609, Appendix A, "Significance Determinat ion of Reactor Inspection Findings for the At-Power Situations," because the inspectors answered "no" to all three questions under the
 
Containment Barriers Cornerstone column of the Phase 1 worksheet. Specifically, the
 
licensee had not actually performed this evolution when the pressure boundary was required
 
to be intact. Based upon this Phase 1 screening, the inspectors concluded that the issue
 
was of very low safety significance (Green). In accordance with the Enforcement Policy, the
 
violation was therefore classified as a Severity Level IV violation.
 
Enforcement
:  Title 10 CFR 50.59(d)(1) states, in part, that the licensee shall maintain records of changes in the facility, of changes in procedures, and of tests and experiments.
 
These records must include a written evaluation which provides a basis for the
 
determination that the change, test, or experiment does not require a license amendment.
 
Contrary to the above, in  safety evaluat ion, EVAL 2004-003, the licensee failed to provide an adequate basis for the determination that on-line repairs to the excess letdown line with a
 
freeze seal in place as a boundary for RCS effluent from the RCPs was acceptable without
 
a license amendment. Specifically, for this freeze seal evolution, the change in the UFSAR, dated March 29, 2004, allowed replacement of the ASME Class II, Seismic Class I, piping in
 
the excess letdown line with a freeze plug while the plant was still on-line. Within the 10
 
CFR 50.59 evaluation, the licensee failed to provide a basis for why this freeze seal
 
evolution did not present more than a minimal increase in the likelihood of occurrence of a
 
malfunction of an SSC important to safety. In accordance with the Enforcement Policy, this
 
violation of the requirements of 10 CFR 50.59 was classified as a Severity Level IV Violation
 
because the underlying technical issue was of very low safety significance. Because this
 
non-willful violation was non-repetitive, and was captured in the licensee's corrective action
 
program (CAP069372), it is considered a Non-Cited Violation consistent with VI.A.1 of the
 
NRC Enforcement Policy (NCV).  (NCV 05000266/ 2005018-01; 05000301/2005018-01 (DRS)) b.2Failure to Perform a 10 CFR 50.59 Evaluation for Compensatory Actions Associated with Letdown Line Automatic Isolation Introduction
:  The inspectors identified a Severity Level IV Non-Cited Violation of very low safety significance for failing to perform a safety evaluation in accordance with 10 CFR
 
50.59(d)(1) for the compensatory actions taken for an activity associated with a degraded
 
plant condition. Specifically, the licensee "screened out" an activity which replaced an
 
automatic action for Chemical and Volume Cont rol System (CVCS) letdown isolation on low pressurizer level of 12 percent with a manual action to isolate letdown if pressurizer level
 
decreased to 20 percent, while replacing the Unit 2 pressurizer low level bistables with Unit
 
2 online at power.
 
Description
:  On February 5, 2004, a 10 CFR 50.59 screening (SCR 2004-0031) was completed to evaluate an activity to replace the Unit 2 pressurizer level low bistables online
 
while preventing CVCS letdown isolation from occurring and maintaining the pressurizer
 
backup heaters in service. The licensee planned to replace the pressurizer low level 8 bistables due to an inadvertent loss of Unit 2 letdown that occurred on February 4, 2005.
 
The licensee attributed the probable cause of the inadvertent loss of letdown to a spurious
 
failure of a pressurizer low level bistable. The licensee's 10 CFR 50.59 screening for the
 
activity concluded that a 10 CFR 50.59 evaluation was not required because, in part, the
 
activity did not adversely affect a design function. The 10 CFR 50.59 screening stated that a
 
designated operator would be stationed to monitor pressurizer level and would manually
 
initiate letdown isolation and deenergize the pressurizer backup heaters if pressurizer level
 
dropped below 20 percent. The activity to replace the Unit 2 pressurizer low level bistables
 
was completed on February 6, 2005.
 
The functions of the pressurizer low level bistables that were replaced were to isolate CVCS letdown and deenergize the pressurizer backup heaters on a low pressurizer level of 12
 
percent. The design function to isolate CVCS letdown on low pressurizer level was
 
addressed in the Point Beach Nuclear Plant (PBNP) UFSAR Table 9.3-7, "Malfunction
 
Analysis of Chemical and Volume Control System."  As stated in FSAR Table 9.3-7, the
 
letdown isolation function prevented supplementary loss of coolant during a letdown line
 
rupture event inside the reactor containment.
 
The inspectors noted that guidance contained in Section 4.4 of Nuclear Energy Institute Standard NEI 96-07, "Guidelines for 10 CFR 50.59 Evaluations," Revision 1, which the NRC
 
endorsed in Regulatory Guide 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments," stated, in part, that if interim compensatory actions are
 
taken to address a degraded condition, 10 CFR 50.59 should be applied to determine
 
whether the compensatory actions impact aspects of the facility described in the UFSAR. In
 
this case, the substitution of manual actions for the letdown isolation function was an
 
adverse change that warranted a full 10 CFR 50.59 evaluation.
 
The inspectors concluded and the licensee subsequently concurred that the activity to replace the pressurizer low level bistables required a safety evaluation. At the end of the
 
inspection period, the licensee planned to perform a safety evaluation in accordance with 10
 
CFR Part 50.59 for the compensatory actions taken for the activity associated with the
 
degraded plant condition.
 
=====Analysis:=====
The inspectors determined that the licensee's failure to perform a 10 CFR 50.59 evaluation for this substitution of manual actions for automatic actions was a licensee
 
performance deficiency warranting a significance evaluation. This finding was determined to
 
be more than minor because the inspectors could not reasonably determine that the change
 
would not ultimately have required NRC approval.
 
Because violations of 10 CFR 50.59 are considered to be violations that potentially impede or impact the regulatory process, these violations are dispositioned using the traditional
 
enforcement process instead of the SDP. However, if possible, the underlying technical
 
issue is evaluated under the SDP to determine the severity of the violation. In this case, the
 
inspectors determined that even though the change was not adequately evaluated in
 
accordance with 10 CFR 50.59, this violation was of very low safety significance, because
 
the design function of mitigating systems to respond to this initiating event scenario were not
 
adversely affected. The inspectors evaluated the finding using IMC 0609, Appendix A, Phase 1 screening for the mitigating systems cornerstone and determined that the finding
 
was of very low safety significance because the finding was not a design or qualification
 
deficiency that was confirmed to result in a loss of operability or functionality per "Part 9900, 9 Technical Guidance, Operability Determination Process for Operability and FunctionalAssessment."
 
Enforcement
:  Title 10 CFR 50.59(d)(1) states, in part, that the licensee shall maintain records of changes in the facility, of changes in procedures, and of tests and experiments.
 
These records must include a written evaluation which provides the bases for the
 
determination that the change, test, or experiment does not require a license amendment.
 
Contrary to the above, the licensee failed to per form a written safety evaluation to address compensatory actions associated with an activity which replaced an automatic action for
 
CVCS letdown isolation on low pressurizer level with a manual action to isolate letdown on
 
low pressurizer level, while replacing the Unit 2 pressurizer low level bistables with Unit 2
 
online at power. The results of this violation were determined to be of very low safety
 
significance; therefore, this violation was classified as a Severity Level IV Violation of 10
 
CFR 50.59. Because this violation was of very low significance, non-willful, non-repetitive, and documented in the licensee's corrective action program as CAP069337, this finding is
 
being treated as a Non-Cited Violation (NCV), consistent with Section VI.A. of the NRC
 
Enforcement Policy.  (NCV 05000266/2005018-02; 05000301/2005018-02 (DRS))1R17Permanent Plant Modifications (71111.17B).1Review of Permanent Plant Modifications
 
====a. Inspection Scope====
From December 12 through 16, 2005, the inspectors reviewed nine permanent plant modifications that had been installed in the plant during the last two years. The
 
modifications were chosen based upon risk significance, safety significance, and complexity.
 
As per inspection procedure 71111.17B, one modification was chosen that affected the
 
barrier integrity cornerstone. The inspectors reviewed the modifications to verify that the
 
completed design changes were in accordance with the specified design requirements and
 
the licensing bases and to confirm that the c hanges did not adversely affect any systems' safety function. Design and post-modification testing aspects were verified to ensure the
 
functionality of the modification, its asso ciated system, and any support systems. The inspectors also verified that the modifications performed did not place the plant in an
 
increased risk configuration.
 
The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is
 
included as an attachment to this report.
 
====b. Findings====
10  b.1Failure to  Apply Adequate Design Controls During Replacement of Service Water (SW)
Valves SW-360 and SW-322 Introduction
:  During replacement of the SW outlet valves for the CCW heat exchangers, the licensee did not implement adequate design controls in accordance with 10 CFR 50, Appendix B, Criterion III. Specifically, the licensee failed to evaluate design differences
 
between the original valves and the replacement valves. These differences led to the
 
eventual failure of the stems in both valves. This self-revealing finding was considered to be
 
of very low safety significance and was dispositioned as a Green NCV.
 
Description
:  Spare Parts Equivalency Evaluation Documents (SPEED) 2005-079 and 2005-080 were written to replace SW valves SW-360 and SW-322, respectively. These two
 
valves served as the CCW heat exchanger outlet valves for the service water cooling.
 
The SPEEDs were written to evaluate the change, since a new type valve was being put in to replace the older valves. Under the Point Beach SPEED process, this change was
 
considered an alternate replacement. As a part of the process for this type of replacement, the licensee was required to justify the differences between the old valves and the new
 
valves. In this justification, the licensee compared the plug and seat design of the valves
 
noting that the old valve contained a web and bridge design as well as a valve plug with a
 
spindle at the end of it. The spindle was designed to slide through the bridge, ensuring
 
proper alignment and uniform seating in all directions. The new design did not have these
 
features. This was a very important parameter, because the flow of water through the valve
 
could be excessive in this system. The desi gn of the old valve helped reduce the amount of vibration that the valve parts experienced during valve operation. While the SPEED
 
evaluations mentioned this design difference, it did not provide a justification for the absence
 
of these design features in the new valve.
 
As documented in the licensee's corrective action document (CE016479), because of these design differences, the new valves were not well suited for throttling at the flow rate seen in
 
the application. Consequently, the valve stem s for both valves broke approximately a week after installation, after being placed back inservice, but before returning the plant to
 
operation.
 
=====Analysis:=====
The inspectors determined that this self-revealed failure to assure design controls commensurate with the valves' original design was a performance deficiency warranting a
 
significance determination. Specifically, the licensee changed valve designs for the Service
 
Water outlet valves from the CCW heat exchangers and did not evaluate the effects of those
 
design changes. This failure to fully evaluate these effects resulted in the installation of an
 
inadequate design that could not withstand the flow of the system resulting in the breaking
 
of the valve stem for both valves.
 
The issue was more than minor because it was associated with the Mitigating System cornerstone attribute of "Design Control," and affected the cornerstone objective of ensuring
 
reliability of systems that respond to initiating events to prevent endesirable consequences.
 
Specifically, failure of these valves could prev ent proper cooling of safety related systems.
 
The finding screened as having very low significance (Green) using IMC 0609, Appendix A, "Significance Determination of Reactor Inspection Findings for the At-Power Situations,"
 
because the inspectors answered "no" to all five questions under the Mitigating Systems
 
Cornerstone column of the Phase 1 worksheet. While the design deficiency led to failures of 11 the valves, the failures occurred during a plant shut-down, therefore, the valves would not have been required to function as designed.
 
Enforcement
:  10 CFR Part 50, Appendix B, Criterion III, "Design Control" states, in part, that design changes, including field changes, shall be subject to design control measures
 
commensurate with those applied to the original design. Contrary to the above, during the
 
replacement of Service Water valves SW-360 and SW-322, the licensee did not evaluate
 
the design differences between the original valves and the new valves for this field change
 
as their design process required. This resulted in the eventual stem breakage of these valves. Because this failure to apply appropriate design control measures was determined to be of very low safety significance and because it was entered in the licensee's corrective action
 
program as CAP068445, this violation is being treated as an NCV, consistent with Section
 
VI.A of the NRC Enforcement Policy.  (NCV 05000266/2005018-03; 05000301/2005018-03 (DRS))4.OTHER ACTIVITIES (OA)4OA2Identification and Resolution of Problems.1Routine Review of Condition Reports
 
====a. Inspection Scope====
From December 12 through 16, 2005, the inspectors reviewed twelve Corrective Action Process documents that identified or were related to 10 CFR 50.59 evaluations and
 
permanent plant modifications. The inspectors reviewed these documents to evaluate the
 
effectiveness of corrective actions related to permanent plant modifications and evaluations for changes, tests, or experiments issues. In addition, corrective action documents written
 
on issues identified during the inspection were reviewed to verify adequate problem
 
identification and incorporation of the probl ems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the team are listed
 
in the attachment to this report.
 
====b. Findings====
No findings of significance were identified.
 
==OTHER ACTIVITIES==
4OA6Meetings.1Exit Meeting The inspectors presented the inspection results to Mr. D. Koehl and others of the licensee's staff, on December 16, 2005. Licensee personnel acknowledged the inspection results
 
presented. Licensee personnel were asked to identify any documents, materials, or
 
information provided during the inspection that were considered proprietary. No proprietary
 
information was identified.
 
12 ATTACHMENT: 
 
=SUPPLEMENTAL INFORMATION=
 
==KEY POINTS OF CONTACT==
 
Licensee
: [[contact::C. Butcher]], Engineering Director
: [[contact::K. Dittman]], Supervisor - Electrical Engineering
: [[contact::R. Grazio]], Regulatory Affairs Manager
: [[contact::D. Koehl]], Site Vice President
: [[contact::J. McNamara]], Supervisor - Mechanical Design
: [[contact::L. Peterson]], Engineering Design Manager
: [[contact::L. Schofield]], Senior Engineer - Regulatory Affairs
: [[contact::S. Scott]], Senior Engineer - Design Engineering
Nuclear Regulatory Commission
: [[contact::B. Burgess]], Reactor Projects Branch 2
: [[contact::H. Chernoff]], NRR
: [[contact::D. Hills]], Chief, Engineering Branch 1
: [[contact::R. Krsek]], Senior Resident Inspector
 
==ITEMS OPENED, CLOSED, AND DISCUSSED==
 
===Opened===
None.Opened and
===Closed===
: 05000266/2005018-01;
: [[Closes finding::05000301/FIN-2005018-01]] NCVUpdated Final Safety Analysis Report Change to
: Replace ASME Class II, Seismic Class I, Piping with a
: Freeze Seal
: 05000266/2005018-02;
: [[Closes finding::05000301/FIN-2005018-02]]NCVFailure to Perform a 10 CFR 50.59 Evaluation for
: Compensatory Actions Associated with Letdown Line
: Automatic Isolation
: 05000266/2005018-03;
: [[Closes finding::05000301/FIN-2005018-03]]NCVFailure to Apply Adequate Design Controls During
: Replacement of Service Water (SW) Valves SW-360
 
and SW-322
 
===Discussed===
None.
 
==LIST OF DOCUMENTS REVIEWED==
The following is a list of licensee documents reviewed during the inspection, including documents prepared by others for the licensee.
: Inclusion on this list does not imply that NRC inspectors
 
reviewed the documents in their entirety, but rather, that selected sections or portions of the
 
documents were evaluated as part of the overall inspection effort.
: Inclusion of a document in this
 
list does not imply NRC acceptance of the document, unless specifically stated in the inspection
 
report.IR02 Evaluation of Changes, Tests, or Experiments (71111.02)
: CFR 50.59 Screenings
: SCR-2002-0384-01; Auxiliary Feedwater Pump Room Fire Wall Addition; dated February
: 13, 2004
: SCR 2004-0031; Defeating PZR Low Level Letdown and Heater Cutoff to Replace Bistables Online; dated February 5, 2004
: SCR 2004-0091; OP 4F; Revision 0; Reactor Coolant system Reduced Inventory Requirements and Nozzle Dam Operational Requirements - Unit 1 and Unit 2; dated
: April 21, 2004
: SCR 2004-0093; Temporary Change to Become Permanent to HPIP 7.51.6; Isolation of the Containment Ventilation System Using the RMS High Alarm Automatic Trip Functions;
: Revision 14;
: TCN 2004-0339; Revision 00
: SCR 2004-0093-01; Temporary Change to Become Permanent to HPIP 7.51.6, Isolation of the Containment Ventilation System Using the RMS High Alarm Automatic Trip Functions;
: Revision 14;
: TCN 2004-0339; Revision 01
: SCR 2004-0138; Unit 1 RHR Cross Connect Valves Procedural Closing Requirements;
dated May 31, 2004
: SCR-2004-0195; Revision to
: IT-72; Service Water Valves; Attachment B (oSW-02817);
dated January 15, 2004
: SCR 2004-0261; Units 1 and 2
: EOP-3; Steam Generator Tube Rupture; Revision 36; dated October 14, 2004
: SCR 2005-0081; Change Battery Restoration Times in DC SOPs; dated July 27, 2005
: SCR 2005-0101; EDG Fuel Oil Duplex Filter Operations; dated April 16, 2005
: SCR 2005-0175-01; Revise 1P-15B, 2P-15A, and 2P-15B Safety Injection Pump Motor Over Current Relay Setpoints; dated August 2, 2005
: SCR 2005-0189; New Procedure 1-sop-y06 to Provide Operational Guidance for Removing from and Restoring to Service Instrument Panel 1-Y06; dated August 9, 2005
: SCR 2005-0192; Revision to FSAR 6.4 to Correct an Error and Remove Specific Procedural Details; dated September 6, 2005
: SCR 2005-0194; Revision 26 to Procedure
: AOP-0.0; "Vital Dc System Malfunction";
dated August 31, 2005
: SCR 2005-0200; New Procedure 1-SOP-4KV-001 for Islanding 1A05 & 1A06 Buses to Their Respective Emergency Diesels; dated August 30, 2005
: CFR 50.59 Evaluations
: SE 2004-001; Revise Time to Reach RHR Cut In Conditions in Various FSAR Radiological Consequences Evaluations; dated August 22, 2005
: EVAL 2004-003; Evaluation to Support
: TM 04-006 for Repairs to 2CV-285, "Excess Letdown Outlet Valve"; dated March 29, 2004
: EVAL 2004-004;
: MR 03-041; Repair of Unit 1 Reactor Vessel Head CRD Penetrations;
dated May 13, 2004
: EVAL 2004-004-01;
: MR 03-041 - Repair of Unit 1 Reactor Vessel Head CRDM
: Penetrations; dated May 26, 2004
: SE 2005-003;
: MR 99-035*A/B,
: MR 99-036*A/B - Containment Hatch Airlock Equalizing Valve Replacement; dated October 13, 2005
: EVAL 2005-007; Revision to
: PC 29; "Monthly Gas Turbine and Auxiliary Diesel Load Test," Oi 110; "Gas Turbine Operation and Np-2.1.5, "Electrical Communications Switchyard
: Access and Work Planning"; dated August 26, 2005
: IR17 Permanent Plant Modifications (71111.17B)
: Modifications
: MR 99-036*A; Upgrade Unit 2 Containment Airlock Operating Mechanism (C-2); dated April 6, 2004
: MR 99-036*B; Upgrade Unit 2 Containment Airlock Operating Mechanism (C-1); dated April 6, 2004
: MR 00-037; Replacement of DC Breakers in Main Control Boards; dated March 22, 2004
: MR 01-063; Replace Service Water Pump Motor On P-32B to Improve Reliability; dated April 10, 2003
: MR 01-074; Add Time Delays to Battery Charger and Dc Bus Voltage Alarm Circuits; dated June 21, 2002
: MR 02-011*B; Extend Unit 1 SI and RH High Point Vent Lines; dated March 27, 2004
: MR 01-144; AFW Motor Driven Pump Mini Recirc Control Valve Modification; dated December 11, 2001
: SPEED 2005-079; Replacement of 12 inch Powell Globe Valve (SW-360); dated September
: 27, 2005 SPEED 2005-080; Replacement of 12 inch Powell Globe Valve (SW-322); dated September
: 27, 2005 Other Documents Reviewed During Inspection Corrective Action Program Documents Generated As a Result of Inspection
: CAP069337;
: SCR 2004-0031 Should Have Resulted in a 50.59 Evaluation; dated December 13, 2005
: CAP069343; Appropriateness of Change to EOP 3.0 in Question; dated December 13, 2005
: CAP069365; Background and Deviation Documents are Not Current with
: EOP-3 Revision
: 37; dated December 14, 2005
: CAP069385; Calculation Documentation Deficiency; dated December 15, 2005
: CAP069391; ISI Classification Error for SI High Point Vent Tubing; dated December 15, 2005
: CAP 069398; Calculation Project HVAC - Explicitly Address Uncertainty and Heat Sink Info;
dated December 15, 2005
: PCR027728; Revise
: RMP 9225-2 to Reference Tech Spec Surveillance SR 3.6.2.2; dated December 13, 2005
: Corrective Action Program Documents Reviewed During the Inspection
: CAP 001618; All A-Train Diesel Fuel Oil Pump Power Lost During Postulated Fire; dated April 23, 1999
: CAP053555; Unit 2 Inadvertent Letdown Isolation; dated February 4, 2004
: CAP055833; Conflict in TS SRs for LCO 3.9.3; dated April 17, 2004
: CAP056416; 1RH-713B RHR Pump Discharge Cross Connect Does Not Isolate Per Design;
dated May 5, 2004
: CAP 057089; Modification to Unit 1 Feedwater Piping Not Done as Required; dated May 28, 2004
: CAP061764; Interim Condition Existing for Greater Than 90 Days Without 50.59
: Screening/Evaluation; dated January 28, 2005
: CAP063023; Inadequate 10CFR50.59 Screening for AOP 0.0 Temporary Change 2005-
: 0012; dated March 24, 2005
: CAP 066419; Conclusion of 50.59 screening
: SCR 2002-0377 questioned by NRC; dated August 16, 2005CAP068445; A/B CCW HX SW Outlet Vibration; dated October 30, 2005
: CAP068529; 1SW-322 Difficult to Operate; dated November 2, 2005
: CAP068622; Replacement for 1SW-322 and 1SW-360 Mechanically Failed after Installation;
dated November 4, 2005CAP068674; 1HX-12A Component Cooling Water Heat Exchanger Needs to Be Returned to Service; dated November 7, 2005
===Calculations===
: Calculation 692301-2.2-004-00-A; AFW Pump Room Loss of HVAC Analysis; dated January
: 29, 1990 Addendum to Calculation 692301-2.2-004-00-A; AFW Pump Room Loss of HVAC Analysis;
dated August 28, 2003
: Calculation 2002-0002; Nitrogen Backup System for MDAFP Discharge Valves (AF-4012/4019) and Minimum Flow Recirculation Valves (AF 4007/4014); Revision 3
===Drawings===
: Drawing
: 290585; Fire Protection for Turbine Building, Aux Building and Containment Elevation 8' 00''; Revision 16
===Procedures===
: AOP-5B; Loss of Instrument Air; Revision 27
: BG-EOP-3; Steam Generator Tube Rupture; Revision 31
: CL 7A; Safety Injection Checklist Unit 1; Revision 23
: CL 7B;
: Safety Injection Checklist Unit 1; Revision 21
: EOP-3 Unit 1; Steam Generator Tube Rupture; Revision 37
: IT 03E; Manual Stroke of Low Head Safety Injection Valves (Quarterly) Unit 1;
: Revision 7
: NMC 50.59 Resource Manual; Section 5.0; The 10
: CFR 50.59 Screening; Revision 2
: NMC 50.59 Resource Manual; Section 6.0; 10
: CFR 50.59 Evaluation; Revision 2
: NP 2.1.4; Operator Burdens; Revision 5
: NP 5.1.8; 10
: CFR 50.59/72.48 Applicability, Screening, and Evaluation; Revision 6
: NP 7.2.15; Fleet Modification Process; Revision 6
: NP 7.2.25; Modification Turnover and Closeout; Revision 0
: OI 128; SI System Fill and Vent Unit 1; Revision 11
: OI 135A; Fill and Vent Train A RHR System Unit 1; Revision 8
: OI 135B; Fill and Vent Train B RHR System Unit 1; Revision 10
: OM 3.26; Use of Dedicated Operators; Revision 9
: OP 4G; Steam Generator Nozzle Dam Operational Requirements Unit 1; Revision 0
: OP 7B; Removing Residual Heat Removal System from Operation; Revision 37
: PBF-2032; Daily Log Sheet; Revision 80
: RMP 9225-2; Defeating/Restoring Containment Personnel and Escape Hatch DoorInterlocks; Revision 7
: 1TS-ECCS-002; Safeguards System Venting (Monthly) Unit 1; Revision 6
===Miscellaneous Documents===
: Calculation 2001-0024; Containment Airlock and Door Seal Pressure Testing Acceptance Criteria; Revision 3
: EOPSTPT
: T.1; RCP Trip; Revision 0
: Engineering Evaluation 2004-0006; Effect of AFW Appendix R Firewall on Room Heatup Due to Loss of HVAC Calculations; dated February 19, 2004
: Modification 02-029; Aux Feed Mini Recirc Safety Upgrade/Remove
: AF-117 Internals; dated August 20, 2002
: Completed
: OI 92A; Fuel Oil Ordering, Receipt Sampling and Offloading; dated April 4, 2005
: Completed
: OI 92A; Fuel Oil Ordering, Receipt Sampling and Offloading; dated December 7, 2005 Operations Work Plan 2004-033; 1RH-713A and B Torque Determination; dated May 31, 2004
: NRC SER dated July 9, 1997; Safety Evaluation Related to Amendment Nos. 174 and 178
to Facility Operating License Nos
: DPR-24 and
: DPR-27; dated July 9, 1997
: Completed
: PBF 3005; Blended #1 and #2 Fuel Oil Acceptance Criteria; dated April 5, 2002
: Completed
: PBF 3005; Blended #1 and #2 Fuel Oil Acceptance Criteria; dated December 28, 2004 Completed
: PBF 3005a; Quarterly Sampling of Emergency Fuel Oil Tanks - T-30
dated September 29, 2005
: Completed
: PBF 3005a; Quarterly Sampling of Emergency Fuel Oil Tanks - T-32A; dated September 29, 2005
: Completed
: PBF 3005a; Quarterly Sampling of Emergency Fuel Oil Tanks - T-32B; dated September 29, 2005
: Completed
: RMP 9225-2; Defeating/Restoring Containment Personnel and Escape Hatch Door Interlocks; various from 2002 through 2005
: Station Log; dated February 4, 2004
: Station Log; dated February 6, 2004
: TCN 2004-0339; Temporary Change - Isolation of the Containment Ventilation System Using the RMS High Alarm Automatic Trip Functions; dated May 21, 2004
: Completed
: TS 10; Local Leak Test of Containment Airlock Bulkheads and Penetrations;
dated March 27, 2005
: Completed
: TS 10A; Containment Airlock Door Seal Testing Unit 2; dated March 31, 2005
: Completed
: TS 80; Sampling of Emergency Fuel Oil Tanks (Quarterly); dated March 29, 2005
: VPNPD 90-148; Supplement to 10
: CFR 50.63, TAC. NOS. 68583 and 68587 Loss of All Alternating Current Power Point Beach Nuclear Plant, Unit 1 and 2; dated
: March 30, 1990
: WEP-89-143; Letter from Westinghouse to Point Beach; Transmittal of Midloop Calculations; dated June 30, 1989
: WO 9950688; P-38A AFP Mini Recirc Control; dated January 25, 2002
: WO 9950689; P-38B AFP Mini Recirc Control; dated January 25, 2002
: WO 9926779; Replace Equalizing Device in Accordance with
: MR 99-036*A; dated February 21, 2004
: WO 9926780; Replace Equalizing Device in Accordance with
: MR 99-036*B; dated February 21, 2004
: WO 0203762001; MOV Actuator Checkout; dated April 14, 2003
: WO 0309001; Extend RH and SI Vent Lines per
: MR 02-011*B; dated October 7, 2005
: WO 0403678; Inadvertent Letdown Isolation and Loss of Heaters (All Heaters Tripped Off) Control; June 17, 2004
==LIST OF ACRONYMS==
USEDADAMSAgency-Wide Document Access and Management SystemASMEAmerican Society of Mechanical Engineers
CCWComponent Cooling Water
CFRCode of Federal Regulations
CVCSChemical and Volume Control System
DRPDivision of Reactor Projects
DRSDivision of Reactor Safety
EMAEngineered Maintenance Action
IMCInspection Manual Chapter
IRInspection Report
NCVNon-Cited Violation
NEINuclear Energy Institute
NRCNuclear Regulatory Commission
PBNPPoint Beach Nuclear Plant
PRAProbabilistic Risk Assessment
RCDTReactor Coolant Drain Tank
RCSReactor Coolant System
RCPReactor Coolant Pump
SBLCStandby Liquid Control
SDPSignificance Determination Process
SPEEDSpare Parts Equivalency Evaluation Document
SSCStructure, System, or Component
SWService Water
UFSARUpdated Final Safety Analysis Report
: [[URIU]] [[nresolved Item]]
}}

Revision as of 06:33, 29 October 2018

IR 05000266-05-018; 05000301-05-018 (Drs); 12/12/2005 - 12/16/2005; Point Beach Nuclear Power Station, Units 1 and 2; Evaluation of Changes, Tests, or Experiments (10 CFR 50.59) and Permanent Plant Modifications
ML060240610
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 01/18/2006
From: Hills D E
NRC/RGN-III/DRS/EB1
To: Koehl D L
Nuclear Management Co
References
IR-05-018
Download: ML060240610 (26)


Text

January 18, 2006

Mr. Dennis Site Vice President

Point Beach Nuclear Plant

Nuclear Management Company, LLC

6590 Nuclear Road

Two Rivers, WI 54241-9516

SUBJECT: POINT BEACH NUCLEAR POWER PLANT, UNITS 1 AND 2 , NRCEVALUATION OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT

PLANT MODIFICATIONS BASELINE INSPECTION REPORT

05000266/2005018; 05000301/2005018 (DRS)

Dear Mr. Koehl:

On December 16, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed a combined baseline inspection of the Evaluation of Changes, Tests, or Experiments and

Permanent Plant Modifications at the Point Beach Nuclear Power Station. The enclosed report

documents the results of the inspection, which were discussed with Mr. and others of

your staff at the completion of the inspection on December 16, 2005.

The inspectors examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel. Based on the results of the inspection, two NRC-identified findings and one self-

revealing finding of very low safety significance were identified which involved violations of NRC requirements. However, because these violati ons were of very low safety significance and because they were entered into your corrective action program, the NRC is treating the issues

as Non-Cited Violations in accordance with Section VI.A.1 of the NRC's Enforcement Policy.

If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.

Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-

0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region

III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Prairie Island Nuclear Generating Plant facility.

D. Koehl-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Av ailable Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/ David E. Hills, Chief Engineering Branch 1

Division of Reactor Safety Docket Nos. 50-266; 50-301 License Nos. DPR-24; DPR-27

Enclosure:

Inspection Report 05000266/2005018; 05000301/2005018 (DRS)

cc w/encl:F. Kuester, President and Chief Executive Officer, We Generation

J. Cowan, Executive Vice President

Chief Nuclear Officer

D. Cooper, Senior Vice President, Group Operations

J. McCarthy, Site Director of Operations

D. Weaver, Nuclear Asset Manager

Plant Manager

Regulatory Affairs Manager

Training Manager

Site Assessment Manager

Site Engineering Director

Emergency Planning Manager

J. Rogoff, Vice President, Counsel & Secretary

K. Duveneck, Town Chairman

Town of Two Creeks

Chairperson

Public Service Commission of Wisconsin

J. Kitsembel, Electric Division

Public Service Commission of Wisconsin

State Liaison Officer

SUMMARY OF FINDINGS

IR 05000266/2005018; 05000301/2005018 (DRS); 12/12/2005 - 12/16/2005; Point Beach

Nuclear Power Station, Units 1 and 2; Evaluation of Changes, Tests, or Experiments (10 CFR 50.59) and Permanent Plant Modifications.

The inspection covered a one-week announced baseline inspection on evaluations of changes, tests, or experiments and permanent plant modifi cations. The inspection was conducted by four regional based engineering inspectors. Three Green Non-Cited Violations (NCV) were identified. The significance of most findings is indicated by their color (Green, White, Yellow,

Red), using Inspection Manual Chapter 0609, "Significance Determination Process (SDP.)"

Findings for which the SDP does not apply, may be Green, or be assigned a severity level after

NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.Inspector-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a Severity Level IV Non-Cited Violation of 10 CFR 50.59(d)(1) for the licensee's failure to perform a safety evaluation for compensatory actions taken for an activity associated with a degraded plant condition.

Specifically, the licensee "screened out" an activity which replaced an automatic action for Chemical and Volume Control System (C VCS) letdown isolation on low pressurizer level with a manual action to isolate letdown on low pressurizer level, while replacing the

Unit 2 pressurizer low level bistables with Unit 2 online at power. At the end of the inspection period, the licensee planned to perform a safety evaluation in accordance with 10 CFR 50.59 for the compensatory actions taken for the activity associated with the degraded plant condition.

Because the issue affected the NRC's ability to perform its regulatory function, this finding was evaluated using the traditional enforcement process. The finding was determined to be more than minor because the inspectors, at the time of the inspection, could not reasonably determine that the UFSAR change, which adversely affected equipment important to safety, would not have ultimately required NRC approval. The inspectors evaluated the finding using IMC 0609, Appendix A, Phase 1 screening for the mitigating systems cornerstone and determined that the finding was of very low safety significance because the finding was not a design or qualification deficiency that was confirmed to result in a loss of operability or functionality per "Part 9900, Technical

Guidance, Operability Determination Process for Operability and Functional

Assessment." (Section 1R02.1.b.2)

Green.

A self-revealed finding of very low safety significance was associated with a violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control." During replacement of the Service Water outlet valves for the Component Cooling Water (CCW)

heat exchangers, the licensee failed to evaluate design differences between the original valves and the replacement valves. These differences led to the eventual failure of the stems in both valves. This issue was entered into the licensee's corrective action system.

4 The issue was more than minor because it affected the mitigating system cornerstone attribute of "Design Control" and affected the cornerstone objective of ensuring reliability of systems that respond to initialing events to prevent undesirable consequences. Specifically, failure of these valves could prevent proper c ooling of safety related systems. The finding screened as having very low significance (Green) using IMC 0609, Appendix A,

"Significance Determination of Reactor Inspection Findings for the At-Power Situations,"

because the inspectors answered "no" to all five questions under the Mitigating Systems

Cornerstone column of the Phase 1 worksheet. While the design deficiency led to failure of the valves, the failures occurred during a plant shutdown; therefore, the valves would not have been required to function as designed. (Section 1R17.1.b.1)

Cornerstone: Barrier Integrity

Green.

The inspectors identified a Severity Level IV Non-Cited Violation associated with the failure to perform an adequate safety evaluation review as required by 10 CFR 50.59 for changes made to the facility as described in the UFSAR. In safety evaluation, EVAL 2004-

003, the licensee failed to provide a basis for the determination that on-line repairs to the excess letdown line with a freeze seal in place as a boundary for Reactor Coolant System (RCS) effluent from the Reactor Coolant Pumps (RCPs) was acceptable without a license amendment. Specifically, for this freeze seal evolution, the licensee would have replaced the American Society of Mechanical Engineers (ASME) Class II, Seismic Class I piping in the excess letdown line with a freeze plug while the plant was still on-line. Within the 10 CFR 50.59 evaluation, the licensee failed to provide a basis for why this freeze seal evolution did not present more than a minimal increase in the likelihood of occurrence of a malfunction of a Structure, System and Component (SSC) important to safety. As a result of this issue, the licensee performed a revision to the original safety evaluation to withdraw the facility change that allowed the freeze seal with the plant online.

Because the issue affected the NRC's ability to perform its regulatory function, this finding was evaluated using the traditional enforcement process. The finding was determined to be more than minor because the inspectors could not reasonably determine that the UFSAR change, which adversely affected equipment impor tant to safety, would not have ultimately required NRC approval. The finding was determined to be of very low safety significance (Green), because the inspectors answered "no" to all three questions under the

Containment Barriers Cornerstone column of the Phase 1 worksheet. Specifically, the licencee had not actually performed this evolution when the pressure boundary was required to be intact. (Section 1R02.1.b.1).

B.Licensee-Identified Violations

No findings of significance were identified.

5

REPORT DETAILS

1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R02Evaluations of Changes, Tests, or Experiments (71111.02).1Review of 10 CFR 50.59 Evaluations and Screenings

a. Inspection Scope

From December 12 through 16, 2005, the inspectors reviewed six evaluations performed pursuant to 10 CFR 50.59. The inspectors confirmed that the evaluations were thorough

and that prior NRC approval was obtained as appropriate. The inspectors also reviewed

14 screenings where licensee personnel had determined that a 10 CFR 50.59 evaluation

was not necessary. In regard to the changes reviewed where no 10 CFR 50.59 evaluation

was performed, the inspectors verified that the changes did not meet the threshold to

require a 10 CFR 50.59 evaluation. The evaluations and screenings were chosen based on

risk significance, safety significance, and complexity. The list of documents reviewed by the

inspectors is included as an attachment to this report.

The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, "Guidelines for 10 CFR 50.59 Implementation," Revision 1, to determine acceptability of the completed

evaluations and screenings. The NEI document was endorsed by the NRC in Regulatory

Guide 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and

Experiments," dated November 2000. The inspectors also consulted

Part 9900 of the NRC Inspection Manual, "10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments."

b. Findings

b.1Updated Final Safety Analysis Report Change to Replace ASME Class II, Seismic Class I, Piping with a Freeze Seal

Introduction:

The inspectors identified a Severity Level IV Non-cited Violation (NCV) of very low safety significance for failing to perform an adequate safety evaluation in accordance

with 10 CFR 50.59. The safety evaluation, EVAL 2004-003, involved an updated Final

Safety Analysis Report (UFSAR) change that a llowed on-line repairs to the excess letdown line with a freeze seal in place as a boundary for RCS effluent from the RCPs. Within the

safety evaluation, the licensee failed to provide a basis for why this freeze seal evolution did

not present more than a minimal increase in the likelihood of occurrence of a malfunction of

an SSC important to safety.

Description:

The licensee initiated 10 CFR 50.59 Evaluation 2004-003 to help facilitate repairs to valve 2CV-285, "Excess Letdown Outlet Valve." To perform this work with the

plant on-line, the licensee proposed to install a freeze seal upstream of 2CV-285 to establish

isolation of the valve from the RCP seal return line. The line that the freeze seal would be

placed on was qualified as ASME Class II, Seismic Category I, pressure boundary piping.

During the work, the bonnet for 2CV-285 would be removed; however, if the freeze seal 6 were to fail, a contingency action was put in place for operators to manually realign 3-way valve 2CV-312, located upstream of the freeze seal, so that water could be diverted to the

Reactor Coolant Drain Tank (RCDT), and thus minimize leakage.

The inspectors noted that the 10 CFR 50.59 evaluation did not address the freeze seal evolution properly in its response to the question that asked if the activity resulted in a more

than minimal increase in the likelihood of occurrence of a malfunction of a Structure System

or Component (SSC) important to safety prev iously evaluated in the current license basis.

The 10 CFR 50.59 evaluation contained little justification for the downgrading of the ASME

Class II pressure boundary and no justification for the downgrading of the Seismic Class I

qualification. The freeze plug did not provide the same degree of barrier integrity as an

ASME Class II, Seismic Class I, pipe. The inspectors were concerned, because the

licensee would be substituting an ASME Class II, Seismic Category I, boundary with a non-

Code recognized pressure boundary material (e.g., ice plug). This was not a permissible repair under Section XI, Article IWA-4000, of the ASME Code, which only recognizes

pressure boundary repair by welding, brazing, or metal removal. The safety function of the

line was to serve as a pressure boundary for reactor coolant from the RCP seal return line, while the malfunction would be a line break. In response to this question in the 10 CFR

50.59 evaluation, the licensee justified the ev olution primarily by stating that strong procedural controls were in place to prevent any anticipated problems. This approach was

insufficient to show that downgrading of the boundaries would not have result in more than a

minimal increase in the likelihood of occurrence of a malfunction of the pressure boundary

line.Although the facility change described in the UFSAR and allowed by the 10 CFR 50.59 evaluation allowed this evolution to occur on-line, the licensee had instead performed the

evolution during an outage. While this was fortuitous, the licensee had still changed the

facility as described in the UFSAR to allow this type of evolution.

The inspectors determined that the 10 CFR 50.59 evaluation that was performed to allow this freeze seal evolution with the plant on-line was not in accordance with the requirements

in 10 CFR 50.59, because the evaluation did not adequately address the downgrading of the

pressure boundary from ASME Class II to a freeze plug, and because it did not address the

deletion of the Seismic Class I qualification for the line. The inspectors noted that this

change to the UFSAR may have resulted in more than a minimal increase in the likelihood

of occurrence of a malfunction of an SSC important to safety, since the freeze plug would

not have provided the same degree of barrier integrity for the RCS effluent from the RCP

seals as the actual ASME Class II, Seismic Class I, piping would have. The licensee

entered this condition into their corrective action program as CAP069372. As a result, the

licensee performed a revision to the original 10 CFR 50.59 evaluation to withdraw the

original facility change that allowed this freeze seal evolution with the plant on-line.

Analysis:

The inspectors determined that this issue was a performance deficiency, since the licensee permanently changed the facility as described in the UFSAR without providing the

necessary justification under 10 CFR 50.59 for the reduction of the pressure boundary of the

excess letdown line from an ASME Class II, Seismic Class I, pipe to a freeze seal. The

finding was determined to be more than minor, because the inspectors could not reasonably

determine that the UFSAR change, which adverse ly affected equipment important to safety, would not ultimately have required NRC approval.

7 Because violations of 10 CFR 50.59 are considered to be violations that potentially impede or impact the regulatory process, they are dispositioned using the traditional enforcement

process instead of the Significance Determination Process (SDP). However, if possible, the

underlying technical issue is evaluated under the SDP to determine the severity of the

violation. In this case, the finding screened as having very low significance (Green) using

IMC 0609, Appendix A, "Significance Determinat ion of Reactor Inspection Findings for the At-Power Situations," because the inspectors answered "no" to all three questions under the

Containment Barriers Cornerstone column of the Phase 1 worksheet. Specifically, the

licensee had not actually performed this evolution when the pressure boundary was required

to be intact. Based upon this Phase 1 screening, the inspectors concluded that the issue

was of very low safety significance (Green). In accordance with the Enforcement Policy, the

violation was therefore classified as a Severity Level IV violation.

Enforcement

Title 10 CFR 50.59(d)(1) states, in part, that the licensee shall maintain records of changes in the facility, of changes in procedures, and of tests and experiments.

These records must include a written evaluation which provides a basis for the

determination that the change, test, or experiment does not require a license amendment.

Contrary to the above, in safety evaluat ion, EVAL 2004-003, the licensee failed to provide an adequate basis for the determination that on-line repairs to the excess letdown line with a

freeze seal in place as a boundary for RCS effluent from the RCPs was acceptable without

a license amendment. Specifically, for this freeze seal evolution, the change in the UFSAR, dated March 29, 2004, allowed replacement of the ASME Class II, Seismic Class I, piping in

the excess letdown line with a freeze plug while the plant was still on-line. Within the 10

CFR 50.59 evaluation, the licensee failed to provide a basis for why this freeze seal

evolution did not present more than a minimal increase in the likelihood of occurrence of a

malfunction of an SSC important to safety. In accordance with the Enforcement Policy, this

violation of the requirements of 10 CFR 50.59 was classified as a Severity Level IV Violation

because the underlying technical issue was of very low safety significance. Because this

non-willful violation was non-repetitive, and was captured in the licensee's corrective action

program (CAP069372), it is considered a Non-Cited Violation consistent with VI.A.1 of the

NRC Enforcement Policy (NCV). (NCV 05000266/ 2005018-01;05000301/2005018-01 (DRS)) b.2Failure to Perform a 10 CFR 50.59 Evaluation for Compensatory Actions Associated with Letdown Line Automatic Isolation Introduction

The inspectors identified a Severity Level IV Non-Cited Violation of very low safety significance for failing to perform a safety evaluation in accordance with 10 CFR

50.59(d)(1) for the compensatory actions taken for an activity associated with a degraded

plant condition. Specifically, the licensee "screened out" an activity which replaced an

automatic action for Chemical and Volume Cont rol System (CVCS) letdown isolation on low pressurizer level of 12 percent with a manual action to isolate letdown if pressurizer level

decreased to 20 percent, while replacing the Unit 2 pressurizer low level bistables with Unit

2 online at power.

Description

On February 5, 2004, a 10 CFR 50.59 screening (SCR 2004-0031) was completed to evaluate an activity to replace the Unit 2 pressurizer level low bistables online

while preventing CVCS letdown isolation from occurring and maintaining the pressurizer

backup heaters in service. The licensee planned to replace the pressurizer low level 8 bistables due to an inadvertent loss of Unit 2 letdown that occurred on February 4, 2005.

The licensee attributed the probable cause of the inadvertent loss of letdown to a spurious

failure of a pressurizer low level bistable. The licensee's 10 CFR 50.59 screening for the

activity concluded that a 10 CFR 50.59 evaluation was not required because, in part, the

activity did not adversely affect a design function. The 10 CFR 50.59 screening stated that a

designated operator would be stationed to monitor pressurizer level and would manually

initiate letdown isolation and deenergize the pressurizer backup heaters if pressurizer level

dropped below 20 percent. The activity to replace the Unit 2 pressurizer low level bistables

was completed on February 6, 2005.

The functions of the pressurizer low level bistables that were replaced were to isolate CVCS letdown and deenergize the pressurizer backup heaters on a low pressurizer level of 12

percent. The design function to isolate CVCS letdown on low pressurizer level was

addressed in the Point Beach Nuclear Plant (PBNP) UFSAR Table 9.3-7, "Malfunction

Analysis of Chemical and Volume Control System." As stated in FSAR Table 9.3-7, the

letdown isolation function prevented supplementary loss of coolant during a letdown line

rupture event inside the reactor containment.

The inspectors noted that guidance contained in Section 4.4 of Nuclear Energy Institute Standard NEI 96-07, "Guidelines for 10 CFR 50.59 Evaluations," Revision 1, which the NRC

endorsed in Regulatory Guide 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments," stated, in part, that if interim compensatory actions are

taken to address a degraded condition, 10 CFR 50.59 should be applied to determine

whether the compensatory actions impact aspects of the facility described in the UFSAR. In

this case, the substitution of manual actions for the letdown isolation function was an

adverse change that warranted a full 10 CFR 50.59 evaluation.

The inspectors concluded and the licensee subsequently concurred that the activity to replace the pressurizer low level bistables required a safety evaluation. At the end of the

inspection period, the licensee planned to perform a safety evaluation in accordance with 10

CFR Part 50.59 for the compensatory actions taken for the activity associated with the

degraded plant condition.

Analysis:

The inspectors determined that the licensee's failure to perform a 10 CFR 50.59 evaluation for this substitution of manual actions for automatic actions was a licensee

performance deficiency warranting a significance evaluation. This finding was determined to

be more than minor because the inspectors could not reasonably determine that the change

would not ultimately have required NRC approval.

Because violations of 10 CFR 50.59 are considered to be violations that potentially impede or impact the regulatory process, these violations are dispositioned using the traditional

enforcement process instead of the SDP. However, if possible, the underlying technical

issue is evaluated under the SDP to determine the severity of the violation. In this case, the

inspectors determined that even though the change was not adequately evaluated in

accordance with 10 CFR 50.59, this violation was of very low safety significance, because

the design function of mitigating systems to respond to this initiating event scenario were not

adversely affected. The inspectors evaluated the finding using IMC 0609, Appendix A, Phase 1 screening for the mitigating systems cornerstone and determined that the finding

was of very low safety significance because the finding was not a design or qualification

deficiency that was confirmed to result in a loss of operability or functionality per "Part 9900, 9 Technical Guidance, Operability Determination Process for Operability and FunctionalAssessment."

Enforcement

Title 10 CFR 50.59(d)(1) states, in part, that the licensee shall maintain records of changes in the facility, of changes in procedures, and of tests and experiments.

These records must include a written evaluation which provides the bases for the

determination that the change, test, or experiment does not require a license amendment.

Contrary to the above, the licensee failed to per form a written safety evaluation to address compensatory actions associated with an activity which replaced an automatic action for

CVCS letdown isolation on low pressurizer level with a manual action to isolate letdown on

low pressurizer level, while replacing the Unit 2 pressurizer low level bistables with Unit 2

online at power. The results of this violation were determined to be of very low safety

significance; therefore, this violation was classified as a Severity Level IV Violation of 10

CFR 50.59. Because this violation was of very low significance, non-willful, non-repetitive, and documented in the licensee's corrective action program as CAP069337, this finding is

being treated as a Non-Cited Violation (NCV), consistent with Section VI.A. of the NRC

Enforcement Policy. (NCV 05000266/2005018-02; 05000301/2005018-02 (DRS))1R17Permanent Plant Modifications (71111.17B).1Review of Permanent Plant Modifications

a. Inspection Scope

From December 12 through 16, 2005, the inspectors reviewed nine permanent plant modifications that had been installed in the plant during the last two years. The

modifications were chosen based upon risk significance, safety significance, and complexity.

As per inspection procedure 71111.17B, one modification was chosen that affected the

barrier integrity cornerstone. The inspectors reviewed the modifications to verify that the

completed design changes were in accordance with the specified design requirements and

the licensing bases and to confirm that the c hanges did not adversely affect any systems' safety function. Design and post-modification testing aspects were verified to ensure the

functionality of the modification, its asso ciated system, and any support systems. The inspectors also verified that the modifications performed did not place the plant in an

increased risk configuration.

The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is

included as an attachment to this report.

b. Findings

10 b.1Failure to Apply Adequate Design Controls During Replacement of Service Water (SW)

Valves SW-360 and SW-322 Introduction

During replacement of the SW outlet valves for the CCW heat exchangers, the licensee did not implement adequate design controls in accordance with 10 CFR 50, Appendix B, Criterion III. Specifically, the licensee failed to evaluate design differences

between the original valves and the replacement valves. These differences led to the

eventual failure of the stems in both valves. This self-revealing finding was considered to be

of very low safety significance and was dispositioned as a Green NCV.

Description

Spare Parts Equivalency Evaluation Documents (SPEED) 2005-079 and 2005-080 were written to replace SW valves SW-360 and SW-322, respectively. These two

valves served as the CCW heat exchanger outlet valves for the service water cooling.

The SPEEDs were written to evaluate the change, since a new type valve was being put in to replace the older valves. Under the Point Beach SPEED process, this change was

considered an alternate replacement. As a part of the process for this type of replacement, the licensee was required to justify the differences between the old valves and the new

valves. In this justification, the licensee compared the plug and seat design of the valves

noting that the old valve contained a web and bridge design as well as a valve plug with a

spindle at the end of it. The spindle was designed to slide through the bridge, ensuring

proper alignment and uniform seating in all directions. The new design did not have these

features. This was a very important parameter, because the flow of water through the valve

could be excessive in this system. The desi gn of the old valve helped reduce the amount of vibration that the valve parts experienced during valve operation. While the SPEED

evaluations mentioned this design difference, it did not provide a justification for the absence

of these design features in the new valve.

As documented in the licensee's corrective action document (CE016479), because of these design differences, the new valves were not well suited for throttling at the flow rate seen in

the application. Consequently, the valve stem s for both valves broke approximately a week after installation, after being placed back inservice, but before returning the plant to

operation.

Analysis:

The inspectors determined that this self-revealed failure to assure design controls commensurate with the valves' original design was a performance deficiency warranting a

significance determination. Specifically, the licensee changed valve designs for the Service

Water outlet valves from the CCW heat exchangers and did not evaluate the effects of those

design changes. This failure to fully evaluate these effects resulted in the installation of an

inadequate design that could not withstand the flow of the system resulting in the breaking

of the valve stem for both valves.

The issue was more than minor because it was associated with the Mitigating System cornerstone attribute of "Design Control," and affected the cornerstone objective of ensuring

reliability of systems that respond to initiating events to prevent endesirable consequences.

Specifically, failure of these valves could prev ent proper cooling of safety related systems.

The finding screened as having very low significance (Green) using IMC 0609, Appendix A, "Significance Determination of Reactor Inspection Findings for the At-Power Situations,"

because the inspectors answered "no" to all five questions under the Mitigating Systems

Cornerstone column of the Phase 1 worksheet. While the design deficiency led to failures of 11 the valves, the failures occurred during a plant shut-down, therefore, the valves would not have been required to function as designed.

Enforcement

10 CFR Part 50, Appendix B, Criterion III, "Design Control" states, in part, that design changes, including field changes, shall be subject to design control measures

commensurate with those applied to the original design. Contrary to the above, during the

replacement of Service Water valves SW-360 and SW-322, the licensee did not evaluate

the design differences between the original valves and the new valves for this field change

as their design process required. This resulted in the eventual stem breakage of these valves. Because this failure to apply appropriate design control measures was determined to be of very low safety significance and because it was entered in the licensee's corrective action

program as CAP068445, this violation is being treated as an NCV, consistent with Section

VI.A of the NRC Enforcement Policy. (NCV 05000266/2005018-03; 05000301/2005018-03 (DRS))4.OTHER ACTIVITIES (OA)4OA2Identification and Resolution of Problems.1Routine Review of Condition Reports

a. Inspection Scope

From December 12 through 16, 2005, the inspectors reviewed twelve Corrective Action Process documents that identified or were related to 10 CFR 50.59 evaluations and

permanent plant modifications. The inspectors reviewed these documents to evaluate the

effectiveness of corrective actions related to permanent plant modifications and evaluations for changes, tests, or experiments issues. In addition, corrective action documents written

on issues identified during the inspection were reviewed to verify adequate problem

identification and incorporation of the probl ems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the team are listed

in the attachment to this report.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA6Meetings.1Exit Meeting The inspectors presented the inspection results to Mr. D. Koehl and others of the licensee's staff, on December 16, 2005. Licensee personnel acknowledged the inspection results

presented. Licensee personnel were asked to identify any documents, materials, or

information provided during the inspection that were considered proprietary. No proprietary

information was identified.

12 ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

C. Butcher, Engineering Director
K. Dittman, Supervisor - Electrical Engineering
R. Grazio, Regulatory Affairs Manager
D. Koehl, Site Vice President
J. McNamara, Supervisor - Mechanical Design
L. Peterson, Engineering Design Manager
L. Schofield, Senior Engineer - Regulatory Affairs
S. Scott, Senior Engineer - Design Engineering

Nuclear Regulatory Commission

B. Burgess, Reactor Projects Branch 2
H. Chernoff, NRR
D. Hills, Chief, Engineering Branch 1
R. Krsek, Senior Resident Inspector

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None.Opened and

Closed

05000266/2005018-01;
05000301/FIN-2005018-01 NCVUpdated Final Safety Analysis Report Change to
Replace ASME Class II, Seismic Class I, Piping with a
Freeze Seal
05000266/2005018-02;
05000301/FIN-2005018-02NCVFailure to Perform a 10 CFR 50.59 Evaluation for
Compensatory Actions Associated with Letdown Line
Automatic Isolation
05000266/2005018-03;
05000301/FIN-2005018-03NCVFailure to Apply Adequate Design Controls During
Replacement of Service Water (SW) Valves SW-360

and SW-322

Discussed

None.

LIST OF DOCUMENTS REVIEWED

The following is a list of licensee documents reviewed during the inspection, including documents prepared by others for the licensee.

Inclusion on this list does not imply that NRC inspectors

reviewed the documents in their entirety, but rather, that selected sections or portions of the

documents were evaluated as part of the overall inspection effort.

Inclusion of a document in this

list does not imply NRC acceptance of the document, unless specifically stated in the inspection

report.IR02 Evaluation of Changes, Tests, or Experiments (71111.02)

CFR 50.59 Screenings
SCR-2002-0384-01; Auxiliary Feedwater Pump Room Fire Wall Addition; dated February
13, 2004
SCR 2004-0031; Defeating PZR Low Level Letdown and Heater Cutoff to Replace Bistables Online; dated February 5, 2004
SCR 2004-0091; OP 4F; Revision 0; Reactor Coolant system Reduced Inventory Requirements and Nozzle Dam Operational Requirements - Unit 1 and Unit 2; dated
April 21, 2004
SCR 2004-0093; Temporary Change to Become Permanent to HPIP 7.51.6; Isolation of the Containment Ventilation System Using the RMS High Alarm Automatic Trip Functions;
Revision 14;
TCN 2004-0339; Revision 00
SCR 2004-0093-01; Temporary Change to Become Permanent to HPIP 7.51.6, Isolation of the Containment Ventilation System Using the RMS High Alarm Automatic Trip Functions;
Revision 14;
TCN 2004-0339; Revision 01
SCR 2004-0138; Unit 1 RHR Cross Connect Valves Procedural Closing Requirements;

dated May 31, 2004

SCR-2004-0195; Revision to
IT-72; Service Water Valves; Attachment B (oSW-02817);

dated January 15, 2004

SCR 2004-0261; Units 1 and 2
EOP-3; Steam Generator Tube Rupture; Revision 36; dated October 14, 2004
SCR 2005-0081; Change Battery Restoration Times in DC SOPs; dated July 27, 2005
SCR 2005-0101; EDG Fuel Oil Duplex Filter Operations; dated April 16, 2005
SCR 2005-0175-01; Revise 1P-15B, 2P-15A, and 2P-15B Safety Injection Pump Motor Over Current Relay Setpoints; dated August 2, 2005
SCR 2005-0189; New Procedure 1-sop-y06 to Provide Operational Guidance for Removing from and Restoring to Service Instrument Panel 1-Y06; dated August 9, 2005
SCR 2005-0192; Revision to FSAR 6.4 to Correct an Error and Remove Specific Procedural Details; dated September 6, 2005
SCR 2005-0194; Revision 26 to Procedure
AOP-0.0; "Vital Dc System Malfunction";

dated August 31, 2005

SCR 2005-0200; New Procedure 1-SOP-4KV-001 for Islanding 1A05 & 1A06 Buses to Their Respective Emergency Diesels; dated August 30, 2005
CFR 50.59 Evaluations
SE 2004-001; Revise Time to Reach RHR Cut In Conditions in Various FSAR Radiological Consequences Evaluations; dated August 22, 2005
EVAL 2004-003; Evaluation to Support
TM 04-006 for Repairs to 2CV-285, "Excess Letdown Outlet Valve"; dated March 29, 2004
EVAL 2004-004;
MR 03-041; Repair of Unit 1 Reactor Vessel Head CRD Penetrations;

dated May 13, 2004

EVAL 2004-004-01;
MR 03-041 - Repair of Unit 1 Reactor Vessel Head CRDM
Penetrations; dated May 26, 2004
SE 2005-003;
MR 99-035*A/B,
MR 99-036*A/B - Containment Hatch Airlock Equalizing Valve Replacement; dated October 13, 2005
EVAL 2005-007; Revision to
PC 29; "Monthly Gas Turbine and Auxiliary Diesel Load Test," Oi 110; "Gas Turbine Operation and Np-2.1.5, "Electrical Communications Switchyard
Access and Work Planning"; dated August 26, 2005
IR17 Permanent Plant Modifications (71111.17B)
Modifications
MR 99-036*A; Upgrade Unit 2 Containment Airlock Operating Mechanism (C-2); dated April 6, 2004
MR 99-036*B; Upgrade Unit 2 Containment Airlock Operating Mechanism (C-1); dated April 6, 2004
MR 00-037; Replacement of DC Breakers in Main Control Boards; dated March 22, 2004
MR 01-063; Replace Service Water Pump Motor On P-32B to Improve Reliability; dated April 10, 2003
MR 01-074; Add Time Delays to Battery Charger and Dc Bus Voltage Alarm Circuits; dated June 21, 2002
MR 02-011*B; Extend Unit 1 SI and RH High Point Vent Lines; dated March 27, 2004
MR 01-144; AFW Motor Driven Pump Mini Recirc Control Valve Modification; dated December 11, 2001
SPEED 2005-079; Replacement of 12 inch Powell Globe Valve (SW-360); dated September
27, 2005 SPEED 2005-080; Replacement of 12 inch Powell Globe Valve (SW-322); dated September
27, 2005 Other Documents Reviewed During Inspection Corrective Action Program Documents Generated As a Result of Inspection
CAP069337;
SCR 2004-0031 Should Have Resulted in a 50.59 Evaluation; dated December 13, 2005
CAP069343; Appropriateness of Change to EOP 3.0 in Question; dated December 13, 2005
CAP069365; Background and Deviation Documents are Not Current with
EOP-3 Revision
37; dated December 14, 2005
CAP069385; Calculation Documentation Deficiency; dated December 15, 2005
CAP069391; ISI Classification Error for SI High Point Vent Tubing; dated December 15, 2005
CAP 069398; Calculation Project HVAC - Explicitly Address Uncertainty and Heat Sink Info;

dated December 15, 2005

PCR027728; Revise
RMP 9225-2 to Reference Tech Spec Surveillance SR 3.6.2.2; dated December 13, 2005
Corrective Action Program Documents Reviewed During the Inspection
CAP 001618; All A-Train Diesel Fuel Oil Pump Power Lost During Postulated Fire; dated April 23, 1999
CAP053555; Unit 2 Inadvertent Letdown Isolation; dated February 4, 2004
CAP055833; Conflict in TS SRs for LCO 3.9.3; dated April 17, 2004
CAP056416; 1RH-713B RHR Pump Discharge Cross Connect Does Not Isolate Per Design;

dated May 5, 2004

CAP 057089; Modification to Unit 1 Feedwater Piping Not Done as Required; dated May 28, 2004
CAP061764; Interim Condition Existing for Greater Than 90 Days Without 50.59
Screening/Evaluation; dated January 28, 2005
CAP063023; Inadequate 10CFR50.59 Screening for AOP 0.0 Temporary Change 2005-
0012; dated March 24, 2005
CAP 066419; Conclusion of 50.59 screening
SCR 2002-0377 questioned by NRC; dated August 16, 2005CAP068445; A/B CCW HX SW Outlet Vibration; dated October 30, 2005
CAP068529; 1SW-322 Difficult to Operate; dated November 2, 2005
CAP068622; Replacement for 1SW-322 and 1SW-360 Mechanically Failed after Installation;

dated November 4, 2005CAP068674; 1HX-12A Component Cooling Water Heat Exchanger Needs to Be Returned to Service; dated November 7, 2005

Calculations

Calculation 692301-2.2-004-00-A; AFW Pump Room Loss of HVAC Analysis; dated January
29, 1990 Addendum to Calculation 692301-2.2-004-00-A; AFW Pump Room Loss of HVAC Analysis;

dated August 28, 2003

Calculation 2002-0002; Nitrogen Backup System for MDAFP Discharge Valves (AF-4012/4019) and Minimum Flow Recirculation Valves (AF 4007/4014); Revision 3

Drawings

Drawing
290585; Fire Protection for Turbine Building, Aux Building and Containment Elevation 8' 00; Revision 16

Procedures

AOP-5B; Loss of Instrument Air; Revision 27
BG-EOP-3; Steam Generator Tube Rupture; Revision 31
CL 7A; Safety Injection Checklist Unit 1; Revision 23
CL 7B;
Safety Injection Checklist Unit 1; Revision 21
EOP-3 Unit 1; Steam Generator Tube Rupture; Revision 37
IT 03E; Manual Stroke of Low Head Safety Injection Valves (Quarterly) Unit 1;
Revision 7
NMC 50.59 Resource Manual; Section 5.0; The 10
CFR 50.59 Screening; Revision 2
NMC 50.59 Resource Manual; Section 6.0; 10
CFR 50.59 Evaluation; Revision 2
NP 2.1.4; Operator Burdens; Revision 5
NP 5.1.8; 10
CFR 50.59/72.48 Applicability, Screening, and Evaluation; Revision 6
NP 7.2.15; Fleet Modification Process; Revision 6
NP 7.2.25; Modification Turnover and Closeout; Revision 0
OI 128; SI System Fill and Vent Unit 1; Revision 11
OI 135A; Fill and Vent Train A RHR System Unit 1; Revision 8
OI 135B; Fill and Vent Train B RHR System Unit 1; Revision 10
OM 3.26; Use of Dedicated Operators; Revision 9
OP 4G; Steam Generator Nozzle Dam Operational Requirements Unit 1; Revision 0
OP 7B; Removing Residual Heat Removal System from Operation; Revision 37
PBF-2032; Daily Log Sheet; Revision 80
RMP 9225-2; Defeating/Restoring Containment Personnel and Escape Hatch DoorInterlocks; Revision 7
1TS-ECCS-002; Safeguards System Venting (Monthly) Unit 1; Revision 6

Miscellaneous Documents

Calculation 2001-0024; Containment Airlock and Door Seal Pressure Testing Acceptance Criteria; Revision 3
EOPSTPT
T.1; RCP Trip; Revision 0
Engineering Evaluation 2004-0006; Effect of AFW Appendix R Firewall on Room Heatup Due to Loss of HVAC Calculations; dated February 19, 2004
Modification 02-029; Aux Feed Mini Recirc Safety Upgrade/Remove
AF-117 Internals; dated August 20, 2002
Completed
OI 92A; Fuel Oil Ordering, Receipt Sampling and Offloading; dated April 4, 2005
Completed
OI 92A; Fuel Oil Ordering, Receipt Sampling and Offloading; dated December 7, 2005 Operations Work Plan 2004-033; 1RH-713A and B Torque Determination; dated May 31, 2004
NRC SER dated July 9, 1997; Safety Evaluation Related to Amendment Nos. 174 and 178

to Facility Operating License Nos

DPR-24 and
DPR-27; dated July 9, 1997
Completed
PBF 3005; Blended #1 and #2 Fuel Oil Acceptance Criteria; dated April 5, 2002
Completed
PBF 3005; Blended #1 and #2 Fuel Oil Acceptance Criteria; dated December 28, 2004 Completed
PBF 3005a; Quarterly Sampling of Emergency Fuel Oil Tanks - T-30

dated September 29, 2005

Completed
PBF 3005a; Quarterly Sampling of Emergency Fuel Oil Tanks - T-32A; dated September 29, 2005
Completed
PBF 3005a; Quarterly Sampling of Emergency Fuel Oil Tanks - T-32B; dated September 29, 2005
Completed
RMP 9225-2; Defeating/Restoring Containment Personnel and Escape Hatch Door Interlocks; various from 2002 through 2005
Station Log; dated February 4, 2004
Station Log; dated February 6, 2004
TCN 2004-0339; Temporary Change - Isolation of the Containment Ventilation System Using the RMS High Alarm Automatic Trip Functions; dated May 21, 2004
Completed
TS 10; Local Leak Test of Containment Airlock Bulkheads and Penetrations;

dated March 27, 2005

Completed
TS 10A; Containment Airlock Door Seal Testing Unit 2; dated March 31, 2005
Completed
TS 80; Sampling of Emergency Fuel Oil Tanks (Quarterly); dated March 29, 2005
VPNPD 90-148; Supplement to 10
CFR 50.63, TAC. NOS. 68583 and 68587 Loss of All Alternating Current Power Point Beach Nuclear Plant, Unit 1 and 2; dated
March 30, 1990
WEP-89-143; Letter from Westinghouse to Point Beach; Transmittal of Midloop Calculations; dated June 30, 1989
WO 9950688; P-38A AFP Mini Recirc Control; dated January 25, 2002
WO 9950689; P-38B AFP Mini Recirc Control; dated January 25, 2002
WO 9926779; Replace Equalizing Device in Accordance with
MR 99-036*A; dated February 21, 2004
WO 9926780; Replace Equalizing Device in Accordance with
MR 99-036*B; dated February 21, 2004
WO 0203762001; MOV Actuator Checkout; dated April 14, 2003
WO 0309001; Extend RH and SI Vent Lines per
MR 02-011*B; dated October 7, 2005
WO 0403678; Inadvertent Letdown Isolation and Loss of Heaters (All Heaters Tripped Off) Control; June 17, 2004

LIST OF ACRONYMS

USEDADAMSAgency-Wide Document Access and Management SystemASMEAmerican Society of Mechanical Engineers

CCWComponent Cooling Water

CFRCode of Federal Regulations

CVCSChemical and Volume Control System

DRPDivision of Reactor Projects

DRSDivision of Reactor Safety

EMAEngineered Maintenance Action

IMCInspection Manual Chapter

IRInspection Report

NCVNon-Cited Violation

NEINuclear Energy Institute

NRCNuclear Regulatory Commission

PBNPPoint Beach Nuclear Plant

PRAProbabilistic Risk Assessment

RCDTReactor Coolant Drain Tank

RCSReactor Coolant System

RCPReactor Coolant Pump

SBLCStandby Liquid Control

SDPSignificance Determination Process

SPEEDSpare Parts Equivalency Evaluation Document

SSCStructure, System, or Component

SWService Water

UFSARUpdated Final Safety Analysis Report

URIU nresolved Item