ML20215A011

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Safety Insp Rept 50-271/86-22 on 860904-1103.No Violations Noted.Major Areas Inspected:Actions on Previous Insp Findings,Physical Security,Plant Operations,Licensee Actions in Response to NUREG-0737 Items & Surveillance Testing
ML20215A011
Person / Time
Site: Vermont Yankee Entergy icon.png
Issue date: 12/04/1986
From: Elsasser T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20215A002 List:
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-***, TASK-TM 50-271-86-22, GL-83-02, GL-83-05, GL-83-2, GL-83-5, GL-84-09, GL-84-23, GL-84-9, GL-85-06, GL-85-6, IEB-80-11, NUDOCS 8612110122
Download: ML20215A011 (27)


See also: IR 05000271/1986022

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U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Report No. 86-22

Docket No. 50-271 License No. DPR-28

Licensee: Vermont Yankee Nuclear Power Corporation l

RD 5, Box 169, Ferry Road

Brattleboro, Vermont 05301

Facility: Vermont Yankee Nuclear Power Station

Location: Vernon, Vermont

Inspection Dates: September 4 - November 3, 1986

Inspectors: William J. aymond, Senior Resident Inspector

Thomas B. J1ko, Resident spector Trainee

Plackee fC Eape Chie , Quality Assurance Section

Approved by: -

M / Y[8[

Thomas C. Elsasser p f, Reactor Projects Section 3C Date

Inspection Summary: Inspection on September 4 - November 3, 1986 (Report No.

50-271/86-22)

Areas Inspected: Routine, unannounced inspection on day time and backshifts by

the resident inspectors of: actions on previous inspection findings; physical

security; plant operations; licensee actions in response to NUREG-0737 items;

surveillance testing; maintenance activities; followup of previous inspection

issues; GE AKF-2-25 circuit breakers used in ATWS circuits; and, licensee actions

to correct block wall discrepancies. The inspection involved 291 hours0.00337 days <br />0.0808 hours <br />4.811508e-4 weeks <br />1.107255e-4 months <br />.

Results: No violations were identified. Operational status reviews identified

no conditions adverse to plant safety. Further licensee and NRC followup actions

are warranted to assure that AKF-2-25 circuit breakers used in ATWS circuits are

reliable, as assured by application of a quality assurance program per NRC Generic

Letter 85-06 (section 9.0).

8612110122 861205

PDR ADOCK 05000271

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DETAILS

1. Persons Contacted

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Interviews and discussions were conducted with members of the licensee staff

and management during the report period to obtain information pertinent to

the areas inspected. Inspection findings were discussed periodically with

the management and supervisory personnel listed below.

Mr. P. Donnelly, Maintenance Superintendent

Mr.- G. Johnson, Operations Supervisor

Mr. J. Pelletier, Plant Manager

Mr. D. Phillips, Senior Engineer, Electrical

Mr. D. Taylor, Maintenance Engineer

Mr. S. Wender, I&C Engineer

Messrs. T. Murley, W. Raymond, P. Lohaus, V. Rooney, and G. Lainas attended

a meeting of the Vermont State Nuclear Advisory Panel on October 8, 1986 in

Montpelier, Vermont to discuss the following issues: State of Vermont person-

nel attendance at NRC inspections of licensed activities; and, the status of

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NRC review of the Mark I Containment Safety Study completed by the licensee.

The inspector also notified the Vermont State Nuclear Engineer by telephone

on October 6 and 30, 1986 of pending routine inspections at the site by Region

I personnel, and of the results of Region I Inspection Report 86-17 concerning

actions to address masonry walls for IE Bulletin 80-11.

The inspector also met with Messrs. Di Palo Luigi and Golfieri Manfredo of

the Italian Comitato Nazionale Per L'Energia Nucleare on October 9,1986 to

tour the site and discuss plant procedures and experiences relative to plant

operations with a nitrogen inerted containment.

2. Summary of Facility Activities

The plant continued routine operation at full power during the period, except

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as noted below. Reactor power was reduced on October 3, 1986 and the plant

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maintained in a hot standby condition (Mode Switch in Startup) while actions

were completed to repair a leak in the turbine-to-condenser boot seal. While

maintaining the reactor critical with the MSIVs shut on October 4, 1986, the

reactor scrammed at 5:33 p.m. on high neutron flux as the HPCI system was

secured. The turbine seal failure and the reactor scram are discussed further

in Section 5.0 below. The plant was restarted on October 5, 1986 and routine

power operations continued.

3. 0 Status of Previous Inspection Findings

3.1 (Closed) Violation 84-11-09: Containment High Range Monitor. In an SER

dated March 25, 1986, NRC:NRR accepted the existing detector locations

for the containment high range monitors, based on additional information

provided by the licensee in a submittal dated November 22, 1985. The

licensee's followup actions for this violation are acceptable and no

further action is required. This item is closed.

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3.2 (Closed) Inspector Follow Item 85-36-07: Review of Revision 1 to LER

85-11. The licensee submitted Revision 1 to LER 85-11 which described

the events associated with the inadvertent PCIS Group III actuation that

occurred on October 9, 19 and 20, 1985 due to spurious signals from the

West Refuel Floor Zone radiation monitor. The inspector reviewed the

revised LER and determined that the report accurately described the facts

surrounding the event including the cause of the event. The corrective

actions taken were acceptable, and the pertinent codes for NRC Form 366

were properly included. The inspector noted that there were no addi-

tional spurious signals from any of the refuel floor ARMS since October

20, 1985. This item is closed.

3.3 (Closed) Violation 86-15-02: Standby Liquid Control Boron Concentration

Surveillance. A violation was issued for the failure to determine the

boron concentration of the standby liquid poison tank following the ad-

dition of water on July 8 and July 15, 1986. The licensee's corrective

actions, documented in letter FVY 86-96 dated October 16, 1986, were

reviewed and found acceptable. The inspector verified an operator aid

tag was placed on the demineralized water addition valve to the SLC

storage tank that instructs the operator to inform the Shift Supervisar

when the valve is opened. Additionally, the inspector reviewed the

changes proposed to procedures OP 4611, OP 4114 and OP 2114 to prevent

recurrence of the event. No inadequacies were identified. This item

is closed.

3.4 (Closed) Unresolved Item 86-15-04: Traversing In-Core Probe (TIP) Modi-

fications. The licensee completed corrective actions to prevent the

recurrence of an inadvertent retraction of the TIP detectors from the

shielded position back into the TIP drive housing.

The corrective actions included adding a mechanical stop that would iso-

late motor current to the TIP drive unit in the event that the drive unit

rotated backwards when the probe was already in the shielded position.

Software changes included redefining the home position (0000) to be a

constant rather than a variable, so that electrical line noise will not

change the inshield position. Additionally, a 20-inch stopping range

was provided behind the home position to prevent overshoot of 0000. The

probe can be driven forward from any position within this 20-inch range.

The final modification involved having the TIP control unit (TCU) deter-

mine where the TIP detector was located prior to initiating the " withdraw

TIP" command upon receiving a Group 2 isolation signal, to prevent with-

drawal of the TIP when the detector is already in the shielded position.

No inadequacies were identified. This item is closed.

During the above review, the inspector noted that the TIP ball valves

did not function in the same manner as originally intended by the licen-

see when the TIP system modification was initiated during the last outage.

This item was identified by the licensee and corrective actions were in

progress. The TIP ball valves are 120 VAC solenoid-operated valves fed

from non-Class 1E power panel PP-6A, that operate energize-to-open and

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spring-to-close. The 120 VAC supply to the solenoids is controlled

within the TCU in a 24 VDC logic circuit. The specific discrepancy was

that the licensee ordered the new TCU from GE with a logic design that

would require the valves to go closed upon loss of control power. How-

ever the TCUs were received with software and a 24 VDC control scheme

with the opposite logic (i.e., energize-to-close), which was not fail

safe for containment isolation purposes.

The new hardware was installed as received, but interim administrative

controls were established to keep the ball valves from opening inadver-

tently by opening the PP-6A supply breaker to both the ball valves and

the TCUs whenever the TIPS were not in use. This configuration left the

TIPS parked in the shields with the ball valves closed. Actions were

completed by the licensee during this inspection to further modify the

ball valve control logic to achieve the desired configuration. This

matter will be reviewed during a subsequent inspection, including review

of the original and modified circuit designs, and verification that the

as-left circuit configuration meets the design and FSAR (Table 7.3.1)

requirements for a primary containment isolation valve.

3.5 (0 pen) Unresolved Item 86-10-07: Adequacy of HCU ASCO Rebuild Kits. This

item is discussed further in Section 8.1 below. The licensee submitted

a report under 10 CFR Part 21 based on his determination that ASCO re-

build kits HVA-405-90-2A (GE Part FV 204-139) contain a defect that might

create a significant safety hazard for other users. This item was also

addressed by GE in RICSIL No. 008. The licensee's action relative to

this part of the outstanding item is considered complete. This item will

remain open pending completion of actions relative to review of post-

maintenance testing and the sequence of rod scram testing following out-

ages.

3.6 (0 pen) Unresolved Item 86-10-02: Condensate Storage Tank (CST) Leakage

Monitoring. The inspector reviewed the licensee's ongoing leakage moni-

toring results for the CST and noted that none of the data collected

through the month of October was indicative of additional tank leakage.

This item will remain open pending completion of the licensee's long term

corrective actions identified in reports 86-10 and 86-15.

4.0 Observations of Physical Security

Selected aspects of plant physical security were reviewed during regular and

backshift hours to verify that controls were in accordance with the security

plan and approved orocedures. This review included the following security

measures: guard staffing; verification of physical barrier integrity in the

protected and vital areas; verification that isolation zones were maintained;

and implementation of access controls, including identification, authorization,

badging, escorting, and personnel and vehicle searches.

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4.1 Security Event

On September 11, 1986, a moderate loss of physical security effectiveness

occurred due to hardware failures within the central alarm station. The

event was reported via the Emergency Notification System at 9:30 a.m.

on September 11, 1986, and a written report dated September 12, 1986 was

submitted as Physical Security Event Report 86-05. The inspector re-

viewed the circumstances involved in the event, the compensatory actions

taken, the corrective actions to prevent the hardware failures, and the

content of the physical security event report. No inadequacies were

identified.

4.2 Demonstration

The Green Mountain Alliance and other groups conducted a planned demon-

stration against the plant on Saturday, September 27, 1986. Following

a noon rally by about 250 people in Brattleboro, a group marched to the

plant in spite of the previous refusal by the Vernon Town Selectmen to

grant an open air permit for the assembly. Plant security declared a

precautionary alert at 4:20 p.m. when about 200 persons arrived at the

plant main gate to block access to the site. The demonstrators conducted

themselves in a peaceful and orderly manner, and most people left the

gate area when requested by local law enforcement officials.

Vermont State Police arrested 35 persons who refused to leave the gate

area, who were transported to Rockingham for arraignment on charges of

trespassing and violation of the town ordinance for assembly without a

permit. All were subsequently released on personal recognizance. One

woman was injured while being removed by State Police from the gate to

a State police bus. She was treated by a licensee medical technician

and transported to Brattleboro Memorial Hospital by the Rescue, Inc.

ambulance service, where she was treated and released. All charges were

subsequently dropped.

The licensee had prepared for the demonstration based on pre-event pub-

licity, and special precautionary security measures were implemented.

All demonstrators were gone from the site area by 6:00 p.m. on September

27, 1986, and the plant security force then returned to a normal status.

The inspector reviewed the licensee's cecurity plans and measures and

identified no inadequacies.

5.0 Inspection Tours and Operational Status Reviews

Plant tours were conducted routinely to observe operating activities in pro-

gress and to verify compliance with regulatory and administrative requirements.

Tours of accessible plant areas included the control room, reactor building,

cable spreading and switchgear rooms, diesel rooms, turbine building, intake

structure and grounds within the protected area. Radiation controls were

reviewed to verify access control barriers, postings, and posted radiation

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levels were appropriate. Work activities reviewed for conformance with RWP

requirements. Plant housekeeping conditions were verified to be in accordance

with the requirements of AP 0042.

Shift logs and records were reviewed to determine the status of plant condi-

tions and changes in operational status. Control room working conditions and

activities were observed to be maintained in a professional and orderly manner

throughout the inspection period. In response to an NRC initiative, a radio

that has been used in the control room was removed on October 17, 1986 fol-

lowing a verbal request by Region I management. Items that received further

review arc discussed below.

5.1 Turbine-Condenser Boot Seal Failure

Due to a significant increase in the offgas air inleakage from 18 SCFM

on September 27, 1986 to 30 SCFM on October 3, 1986, the licensee reduced

power to 50 percent to facilitate helium leak testing. The increased

inleakage was caused by a defect in the turbine to condenser boot seal.

Reactor power was reduced, the mode switch was placed in Startup, and

the MSIV's were closed to allow inspection and repairs of the damaged

boot.

The rubber boot had a crack approximately 1.5" long and .25" wide which

originated at the location of a patch applied to the boot by the manu-

facturer in an attempt to repair a manufacturing defect. Since the crack

was limited in size to that of the original defect, gross failure of the

boot was determined to be unlikely. The torn section of the boot was

repaired by valcanizing new belts and rubber into the existing boot.

The original cords on the boot were left intact to provide continuity.

The remaining portion of the boot was inspected by the licensee and was

found to be in an acceptable condition. Following repair of the boot,

condenser air inleakage returned to its nominal value of about 16 SCFM

during power operations which commenced on October 5, 1986.

During the period of operation when condenser inleakage was greater than

normal, the inspector verified that the operators were aware of the con-

sequences of a sudden failure cf the turbine boot and what action would

be required should the event occur. The inspector identified no inade-

quacies.

5.2 Single Loop Operation

Reactor power was reduced to 50 percent of rated power on October 3, 1986

to facilitate the search for the source of the offgas air inleakage as

discussed above. During the period of reduced power, the recirculation

system was placed in single loop operation. Single loop operation is

permitted, with restrictions, per Technical Specifications (TS) 3.6.G.

The inspectnr verified that the TS required actions were completed during

single loop operation.

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TS 3.6.G specifies that during single loop operation "the recirculation

system controls will be placed in the manual flow control mode". The

inspector noted that on October 3, 1986, the recirculation flow control

system (RFCS) was in master manual while in single loop operation, with

the the individual transfer station for the operable loop in the auto- '

matic mode. The inspector questioned whether placing the RFCS in master

manual met the intent of the specification to be in " manual flow control "'

mode". The Operations Supervisor presented GE Report NE00-30060, "Ver-

mont Yankee Single Loop Operation", dated February 1983 for inspector

review, which showed that the intent of the specification was met.-The

inspector noted that Vermont Yankee's naster flow controller is pinned

in the master manual position thus mechanically prohibiting control in

the master auto mode.

No inadequacies were identified.

5. 3 Feedwater Water Hammer and Scram on October 4, 1986 *-

Plant operators maintained the reactor critical on IRM Range 6 on October

4,1986, using the RCIC system (and HPCI as necessary) for pressure con-

trol, and with one condensate and one feedwater pump in operation for

level control. The MSIVs were closed for turbine condenser work. All

reactor systems were operating normally with the exception of IRM D, ,

which had been bypassed previously due to its lack of response.

Maintenance personnel requested additional condenser cooling to improve

environmental conditions in the B condenser. Plant cperators initiated

cooling at 1:05 p.m. by opening the feedwater long cycle recirculation

valve V63-22A to spray the tubes in the A condenser. A water nammer

occurred in the recirculation line due to steam in the line~and steam

in the A condenser. The 22A valve was closed immediately. Operators

subsaquently established additional cooling at 1:30 p.m. by first .

throttling manual valve V63-23A open one turn before opening the 22A

valve.

Plant operators and maintenance personnel inspected portions of the re-

circulation line and noted no damage. The inspector also walked down

portions of the recirculation line on October 4, 1986 and noted no damage

to the piping or pipe supports. Additional licensee corrective actions

in this area are discussed further below.

While continuing to maintain the reactor critical on Range 6 on October

4th, plant operators noted that reactor pressure had increased to about

1000 psig. The HPCI system was started at 5:21 p.m. in the CST recir-

culation mode to reduce pressure. Neutron flux levels decreased to IRM

Range 1 due to the negative reactivity effects of reducing pressure to

, about 700 psig. When the HPCI system was secured at 5:33 p.m., the sud-

l den pressure increase caused vessel level to shrink from about 158 inches

i to 150 inches above the top of the active fuel. The vessel level control

system over-responded to the decrease and injected relatively cold (200

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degree F) water into the core through the startup feedwater valve FCV6-13.

Vessel level increased to 159 inches. However,:the cold water addition

caused a rapid flux increase and the reactor scrammed automatically on

a high neutron flux on IRM Range 1 (about 16 kilowatts of thermal power

, level).

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The' reactor responded normally to the scram-and the operators stabilized

r the plant in the hot shutdown condition. The reactor was left-hot but

, subcritical'with the MSIVs closed for the remainder of the condenser work.

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.v.. The licensee's summary and evaluation of the scram was provided in a Post

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Trip Report (VYAPF 0154.01) dated October 4,1986, which was reviewed and-

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f found to accurately describe the event.'

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u The inspector reviewed the reactor response to the scram using strip

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(,*' charts of reactor parameters, plant logs and computer information. Data

from the computer " REC" logs was not obtained after the scram due to a
., s computer malfunction. This review confirmed that the. reactor scrammed

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as a result of the flux increase caused by the cold water injection,

, which resulted in a reactor period estimated by the inspector to be on

the order of five seconds. Thu reactor protection system responded

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promptly and properly to shut down the reactor,

i Subsequent licensee: review determined that the GEMAX 6-85 rack-mounted

controller for the startup feedwater valve ccn aibuted to the event be-

-t Cduse the valve did not respond properly to a flow demand signal. The

N . faulty controller was replaced on October 4, 1986 under maintenance re-

( i quest (MR) 86-2127. The licensee's review also identified procedural

3 d, and operator training deficiencies for both the scram and feedwater water

1 4 hammer events. For the scram, the licensee determined that, even Rough

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the mode of operating in hot standby with the MSIVs shut had been iione

successfully in the past for short periods, existing plant procedures

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do not provide adequate instructions to define the bounds for operational

. parameters. Additionally, the licensee identified the need to upgrade

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procedures that establish environmental control for work in the main

,- condenser, or other confined spaces. The water hammer and scram events

will be described in a plant information report (PIR) that is scheduled

for issuance in November, 1986. The PIR will contain recommendations

for procedure changes and operator training to cover the identified O s-

i crepancies. This item is unresolved pending completion of the proc wire

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changes and training, and subsequent review by the NRC (UNR 86-22-01,.

The licensee reported the scram per 10 CFR 50.72(b)(2)(ii) and notified

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the resident inspector at 6:00 p.m. on October 4, 1986. The licensee

submitted LER 86-15 for the scram by letter dated November 4, 1986, which

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< was reviewed by the inspector and found to accurately describe the event.

The plant was restarted at 7:54 p.m. on October 5, 1986 following the

, completion of the condenser work. The plant resumed full power operation

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without further incident.

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5.4 Transportation Violation

The licensee received a letter from the Barnwell, S.C. low level burial

site on October 9, 1986, imposing a $2,000 fine for a resin shipment

received at the burial site on September 24, 1986, that had about one-

half cup of resin beads on the outside of the liner. The burial site

measured loose surface contamination on the inside of the shipping cask

at 300,000 dpm/100 sq-cm. The burial site requires the licensee to pro-

vide prior notification for any shipment having greater than 50,000 dpm/

100 sq-cm loose contamination on the exteriors of the liner. The licen-

see has retained burial site privileges at Barnwell and is drafting a

response to the State of South Carolina to address what steps will be

taken to prevent recurrence. The licensee's actions and the adequacy

of the corrective measures will be reviewed by Region I health physics

personnel during the next transportation and process control program

inspection.

5.5 HPCI Vioration Testing

Vibration monitoring of the Vermont Yankee HPCI system was conducted on

October 20, 1986, to obtain supplemental information for a test conducted

in August of this year. The August test results indicated a possible

vibration problem associated with the HPCI pump pedestal which is be-

lieved to have a natural resonance frequency very close to the operating

frequency of the pump. The August test results were significant enough

to warrant additional vibration tests but were not indicative of an in-

operable system. It is noted that the required inservice inspection

vibration tests concluded on the HPCI system per ASME Section XI do not

indicate any degraded performance. The inspector noted that the highly

sensitive vibration testing conducted in August and October is an aid

used by the licensee in long term preventive maintenance testing. The

inspector verified that the testing on October 20, 1986 was conducted

without rendering the system inoperable.

The inspector observed the startup and running of the HPCI system during

the test conducted per operating procedure (0P) 2120 "High Pressure Cool-

ant Injection System". The HPCI test was successfully completed and the

system was returned to a standby condition. The inspector had no further

comments, except as discussed below.

OP 2120 has a precaution to instruct the operator to trip the system if

turbine vibration exceeds 2 mils. However, the procedure does not direct

the operators to activate the HPCI vibration monitor located on CRP 9-3

so that turbine vibrations can be monitored. The inspector discussed

these observations with the Senior Operations Engineer, who stated that

the procedure would be revised to incorporate the appropriate guidance.

The inspector had no further comments in this area. The vibration test

results of October 20, 1986, will be reviewed by the inspector during

a subsequent inspection.

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5.6 Offsite Train-Truck Accident

At approximately 9:11 a.m. on October 21, 1986, a train collided with

a propane tank truck at the intersection of the rail line with Route 142,

about one-half mile Southwest of the Vermont Yankee site. The accident

resulted in a minor propane leak from the tank truck which was stopped

at approximately 11:00 a.m.

The accident was reported to the Vermont Yankee control room at approxim-

ately 9:30 a.m. by plant security guards at gate 2 who heard a report

of the accident on a local radio station. The licensee dispatched the

fire brigade commander and other personnel to the accident site to per-

form a first hand evaluation of the event. The shift supervisor subse-

quently reviewed the site emergency plan and the emergency notification

procedure, and determined that no additional action was necessary. Ad-

ditionally, local authorities decided not to evacuate either the element-

ary school or the post office in the immediate vicinity of the collision

site.

The inspector reviewed the licensee's actions and no inadequacies were

identified.

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5.7 Seismic Event

An earthquake measuring 3.5 on the Richter scale and centered in Laconia,

New Hampshire occurred at 1:17 p.m. on October 25, 1986. Reactor opera-

tors at Vermont Yankee heard reports from offsite sources that tremors

were felt as near as Brattleboro, Vermont and Northfield, Massachusetts

(both within 5 miles from the site), but no tremors were felt onsite.

The onsite seismic accelerometer has a trigger level of 0.01 G and did

not register any ground motion. Plant operators noted the offsite re-

ports, but took no further action since no reporting or action levels

were reached at the site. The design of the site is such that a safe

shutdown can be made following a ground horizontal acceleration of .14

G. No inadequacies were identified.

5.8 Review of Inoperable Equipment

Actions taken by plant personnel during periods when equipment was in-

operable were reviewed to verify: (1) technical specifications limits

were met; (2) alternate surveillance testing was completed satisfactorily;

and, (3) equipment return to service upon completion of repairs was pro-

per. The above reviews were completed for the following items: (1) elec-

tric fire pump taken out of service for maintenance on October 21, 1986;

and (2) "B" standby liquid control pump taken out of service to facili-

tate the repair of the SLC squib continuity circuit. No inadequacies

were identified.

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5.9 Feed Water Leak Detection

The inspector reviewed the feed water sparger leakage detection system

and the monthly performance summary provided by the licensee in accord-

ance with letter FVY 82-105. The licensee reported that, based on the

leakage monitoring data reduced as of September 30, 1986, there were no

deviations in excess of 0.10 from the steady-state value of normalized

thermocouple readings, and no failures in the sixteen thermocouples

initially installed on the four feedwater nozzles. No unacceptable con-

ditions were identified.

5.10 Safety System Review

The residual heat removal, residual beat removal service water, high

pressure coolant injection, core spray, stanaby liquid control, standby

gas treatment and reactor core isolation cooling systems were reviewed

to verify the systems were properly aligned and fully operational in the

standby mode. The review included: (1) verification that accessible,

major flow path valves were correctly positioned; (2) verification that

power supplies were properly aligned; and, (3) visual inspection of major

components for leakage, proper lubrication, cooling water supply, and

general condition. No inadequacies were identified.

5.11 Control Rod 18-31

Plant operators experienced difficulty getting control rod 18-31 to move

out from position 00 initially during the reactor startup on October 5,

1986. However, the rod did move after the operator increased drive pres-

sure to 350 psid and then back to the normal pressure of about 250 psid

per ON 3143. Plant operators and reactor engineering personnel reviewed

the status of the rod and determined it to be operable. The rod subse-

quently moved out of the core upon demand with the rest of its group

without further problem. The licensee measured flux profiles in the

vicinity of the rod as it was withdrawn. The inspector reviewed TIP

traces for rod moves from position 00, 04, 08, 12, 16, 20, 24 and 28,

and noted that the control rod was moving with the drive mechanism.

No other problems were noted with the rod, except for the inability to

move it beyond position 46. This problem was reviewed on previous in-

spections (reference: Inspection Reports 86-10, page 13, and 86-15,'page

8). The performance of control rod 18-31 will be reviewed during subse-

quent routine inspections. No inadequacies were identified.

5.12 Contaminated TBED Sump

The inspector reviewed licensee followup actions on September 12, 1986

after routine surveys identified a low level of contamination in the

normally " clean" turbine building equipment drain (TBED) sump. A water

sample from the sump had a specific activity that measured a few counts

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above background at 1.16 +/- 3 X10-6 uCi/ml. The licensee took actions

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to secure, drain and clean the sump. The licensee determined that the

most likely source of the contamination was the buildup of very low

levels of activity from turbine building floor areas drained into the

sump over long periods of time. The sump was resurveyed and returned

to service at 5:30 p.m. on September 12, 1986.

The inspector reviewed the licensee's actions and sample results for the

sump. The inspector also verified the license's compensatory measures

were acceptable to meet Technical Specification 3.9.A.1 requirements for

the service water effluent monitor during the 8-hour period that the TBED

sump was out of service. The inspector reviewed plant drawings and

walked down plant lines connected with the sump to verify that no un-

intended source of contaminated water from fluid systems was added to

the sump. No inadequacies were identified.

5.13 SBGTS Review

The inspector reviewed the standby gas treatment system (SBGTS) per the

requirements of inspection temporary instruction TI R1-86-01 to determine

whether certain design deficiencies existed which could render both SBLIS

trains inoperable from a single failure. The potentially generic defi-

ciency was identified by Boston Edison Co. (BECo) engineering personnel

during a review of the SBGTS design at the Pilgrim plant. The units at

Vermont Yankee were found to not have the subject deficiency.

The problem at Pilgrim stemmed from a design using a normally open, air-

operated cross connect valve on the discharge side of the parallel SBGTS

trains that would fail open on loss of power. BECo found that a single

failure in the fire protection sprinkler system adjacent to the SBGTS

at Pilgrim could place both trains in a degraded condition. At Vermont

Yankee, no water-based fire suppression is used for the SBGTS. Addi-

tionally, the compar'able cross connect valve, SGT-5, is a normally closed,

normally de energized air-operated valve that will fail closed on loss

of power (power / air-to-open, spring-to-close). Based on the above, the

postulated failure mode could not occur at Vermont Yankee.

One print discrepancy was identified on drawing G191238, Revision 16,

which shows SGT-5 as a motor-operated valve instead of an air-operated

valve. The discrepancy was referred to the engineering support super-

visor for review and followup action to submit a corrective update to

the drawing.

5.14 Shelf Life of Scram Valve Air Operators

The inspector received information from Region I on September 24, 1986

regarding a problem identified at Nine Mile 1 with potentially generic

implications at Vermont Yankee. The item concerned the failure of the

diaphram on the air operator for the scram outlet valve (CV13-127) on

a control rod. The control rod inserted upon failure of the air operator

at the other facility, which was a failure in the conservative direction.

The probability of this outcome for the failure is highly certain.

-- -

-_. - . - _

,

-

.

.

13

However, if the same part (GEI 92807A) is postulated to fail on the scram

inlet valve (CV13-126), it is not certain that insertion of the rod would

occur. Information from the NSSS vendor suggests that the rod would in-

sert for the failure of the 126 valve because the common air supply

header from the scram pilot valves (50 13-117 & 118) would bleed down ,

the air pressure and cause the 127 valve to open. However, further study

of this mechanism is planned, and operating experiences at another plant

(Clinton) indicates that rod insertion may not always occur.

The seced item of significance received by the inspector was the infor-

mation purportedly from the NSSS vendor that the material used in the

air operator diaphrams had a shelf life of 10 years if stored in the

original shipping package, and 5 years otherwise. The unit that failed

at Nine Mile 1 had been in service since 1975. Based on a preliminary

review and discussions with plant staff members, the inspector determined

that the same GE parts are used at Vermont Yankee, they have been in

service since the plant started up in 1972, and they are not included

in a shelf / service life control program. Plant personnel interviewed

did not recall experiencing any problems involving failure of the air

operator diaphrams.

This item was discussed with the operations superintendent on September

24, 1986, who noted the inspector's findings for followup review to de-

termine what further action may be warranted to address shelf / service

life limitations on the installed scram valve air operators. The licen-

see stated that this item would be assigned to the plant staff for fol-

lowup and review with the NSSS vendor. This item is unresolved pending

completion of the licensee's actions and subsequent review by the NRC

(UNR 86-22-02).

6.0 Surveillance Testing

The inspector reviewed portions of the surveillance tests listed below to

verify that testing was performed in accordance with administrative require-

ments. The review included consideration of the following criteria: proce-

dures technically adequate; testing performed by qualified personnel; test

data demonstrated conformance with technical specifications requirements; test

data anomalies appropriately resolved; surveillance schedules met; test re-

sults reviewed and approved by supervisory personnel; and, proper restoration

of systems to service.

--

OPF 2428.01 R/CE Checklist to Support Extended Single Loop Operation

dated August 19, 1986 and October 3, 1986

--

OPF 2428.02 R/CE Checklist for Returning to Two Loop Operation dated

August 20, 1986

--

OPF 4379.01 Drywell/ Torus Differential Pressure Functional Test

No inadequacies were identified.

t

. .

.

14

7.0 Maintenance Activities

The maintenance request (MR) log was reviewed to determine the scope and

nature of work done on safety-related equipment. The review confirmed that:

the repair of safety related equipment received priority attention; technical

specifications limiting conditions for operation were met while components

were out of service; performance of alternate safety related systems was not

impaired; and, the maintenance activity did not create an unreviewed safety

question.

Maintenance activity associated with the following was reviewed to verify

(where applicable) procedure compliance and equipment return to service,

including operability testing.

,

--

MR 86-1947, Loss of Closed Indication on System I Torus-To-Drywell "D"

l Vacuum Breaker

--

MR 86-1952, Uninterruptible Power Supply B - Blown Inverter Leg Fuse

--

MR 86-2064, Repair Oil Leak on "B" Recirculation MG Set

--

MR 86-2120, IRM D - No Response to Neutron Flux

--

MR 86-2131, SRM C - Drive Problems

--

MR 86-2235, Loss of SLC Squib Vaive Continuity

--

MR 86-2101, High Containment Air Usage

--

MR 86-2262, Repair Leak on RWCU-68 Valve

No inadequacies were identified.

8.0 Followup of Previous Inspection Findings

8.1 Part 21 Report

A licensee representative informed the inspector on September 12, 1986

of the completed licensee evaluation of the control room rod scram anom-

aly on June 4, 1986 (Reference: Inspection Report 86-10, Section 6), the /

licensee's conclusion that the event was reportable under 10 CFR Part

21. **

Of the three discrepancies noted with the ACS0 HVA-90-405-SA rebuild kits,

the licensee concluded that the discrepancy involving the partially at-

tached core assembly spring could create a significant safety hazard if

the mis-assembled springs are not identified during oreservice inspec-

tions and testing. The improperly assembled springs may not be identi-

fied during the normal post maintenance testing following rebuild of the

HCU 126 and 127 valve solenoid operators, but could subsequently cause

scram valve failure (and loss of proper rod scram function) after several

. .

_ _ _ - - _

.

.

.

15

operations of the solenoid valve. The ASCO rebuild kits are custom made

for BWRs and supplied to the industry as GE spare part kit FV 204-137.

The corrective actions taken by Vermont Yankee for this problem have been

previously reviewed and found acceptable.

The licensee submitted a written report per Part 21 requirements on

September 16, 1986 to alert other users of the kits of the potential

defects. The inspector reviewed the report and found that it accurately

reflected the circumstances and actions taken at Vermont Yankee. The

report will be reviewed for further action by the NRC staff. No inade-

quacies were identified.

8.2 Worker Exposure Concern

This item was previously reviewed and closed as described in Inspection

Report 85-40, Paragraph 5.4. A former licensee contractor employee and

his attorney contacted the inspector by telephone on October 10, 1986

to provide comments on their review of the inspection documentation of

this matter, which involved a radiation exposure concern identified by

the worker when he was a contractor at the site. The worker has filed

a civil suit against the Morrison & Knudsen Company (M&K), the former

recirculation piping contractor for Vermont Yankee, and is seeking dam-

ages from M&K after being fired on December 5,1985 for refusing to fol-

low the directions of his foreman on that date to wait in a " radiation

area" in the reactor building while staging was constructed at his in-

tended work station inside the drywell. The inspector's followup of the

worker's concerns regarding radiation exposure control did not substanti-

ate supervisory directions that were contrary to good ALARA practices.

The worker stated that the purpose of the October 10, 1986 telephone call

was to point out two errors of fact in the NRC inspection report, as

follows:

(1) The report indicated that the worker signed out on RWP 4114 prior

to leaving the job site. The worker stated that while he did sign

in on the RWP, he left the site without signing out, and thus,

someone else must have completed the sign-out process. The sign out

process involved recording the exit time and the whole body dose

rate as read on a pocket dosimeter upon leaving the RWP work area.

(2) The report indicated that the foreman directed the worker to wait

in a holding area outside the drywell. The worker stated that his

foreman in fact directed him to wait inside the drywell where the

radiation exposures were much higher. The inspector noted on Octo-

ber 10, 1986 that had the worker been asked to spend 1.5 non working

hours in the drywell where dose rates were much higher than in the

reactor building holding area, then that would have been a matter

of concern to the NRC for not maintaining good health physics prac-

tices.

-

. .

9

16

The inspector accepted the worker's statements on October 10, 1986 as

accurate. However, the inspector noted that the account of the worker's

activities in Inspection Report 85-40 was based solely on the interview

with him, and that on December 5, 1985, he stated that he was asked to

wait in the reactor building holding area designated in the inspection

report and surveyed on that date.

The worker stated further on October 10, 1986, in regard to previous work

practices, that M&K tried to use RWP information to show progress made

on the pipe replacement effort. The inspector thanked the worker for

the additional information and stated that the NRC would perform a fol-

lowup review of the December 5, 1985 events with this new information.

The above information was submitted to NRC Region I for management review

to determine whether a followup review of the drywell work practices

should be performed in light of the new information to determine whether

regulatory concerns exist. The inspector identified no concerns wherein

a third party signs off on the RWP under the circumstances where the

worker is no longer present, so long as the correct information from the

pocket dosimeter was used. The inspector noted that the control of work

activities in the drywell so as to minimize worker idle time was reviewed

during the outage by the resident and regional inspectors and no concerns

were identified.

This item is unresolved pending further NRC review of the information

provided by the worker (UNR 86-22-03).

8.3 Block Wall Concerns

This item was previously reviewed as 86-18-02. The licensee provided

a summary of the licensee plans and assessments relative to block wall

deficiencies in a letter to NRC Region I, serial FVY 86-85, dated Sep-

tember 19, 1986. The deficiencies concerned unqualified and unrestrained

block walls in the turbine building ventilation corridor that could fail

during a seismic event and potentially adversely affect the following

plant electrical circuits and systems:

(a) Cables for all four main steam line radiation monitors that provide

trip inputs (main steam line radiation levels 3X normal background)

for the reactor protection system and the primary containment (Group

I) isolation system. There is no backup isolation initiator to

assure the main steam lines automatically close in the event of a

dropped rod accident. However, the licensee's assessment noted that

the probability of a rod drop accident is highly unlikely: (1) due

to the fact that any components that would need to fail as part of

the control rod drop scenario are of Seismic Class I design, and

(2) due to the control rod coupling checks that are performed at

the beginning of each operating cycle. The inspector noted that

.

, _ _ - - - . - . - . - - -

-

,,_

17

control rod 18-31 in particular passed a coupling check at least

once at the start of the operating cycle (see further discussions

in section 5.11 above).

(b) Control cables for tihe four reactor recirculation units, RRU 5, 6,

'7 & 8, in the ECCS corner rooms in the reactor building. The RRUs

are normally in standby and receive a start signal when equipment

in'the respective. rooms are in service. The RRUs are required to

be operable to control corner room environmental conditions and

thereby assure ECCS equipment long term operability.

Assuming the reactor building is accessible following a seismic

'

event, the licensee stated that actions could be taken to (1) open

the corner room doors and install portable ventilation equipment,

! and (2) write a jumper and-lifted lead procedure to rewire the RRUs

locally and restart the fan cooler units. The licensee has calcu-

l lations on file that were' performed for 10 CFR 50 Appendix R an-

alyses that show that the RHR corner rooms would heat up to 128

degrees F within two hours assuming no ventilation flow, and the

. core spray pumps are operated 50% of the time. With the doors open

!

and portable ventilation fans providing 10,000 cfm of forced venti -

i

lation-at two hours into the event, the room temperatures would

stabilize between 108 and 113 degrees F, with core spray and RHR

running 50% and 67% of the time, respectively. 0ther calculations

-

- show tut the above environmental conditions are within the ultimate

, equipment capabilities of the equipment following temperature ex-

cursions.

! The inspector requested and received for review a copy of the cal-

culations that demonstrate the equipment capabilities referenced

'

above. This review was.in progress at the end of the inspection.

The inspector noted that no temporary procedure had been written

i to show the conceptual design needed to rewire the RRUs locally,

or to translate the assumed ECCS equipment operating times into a

'

set of operational restrictions that would assure the bounding ,

assumptions used in the analyses would not be exceeded. The above

items will be reviewed further during a subsequent inspection, along

with the radiological conditions assumed to exist in the reactor

building following a DBA SSE/LOCA with with no degraded core condi-

'

tions, to verify areas would remain accessible to perform the ac-

tions needed to mitigate the degraded conditions.

(c) Control cables for the fans in the A and B diesel rooms. -The diesel

room fans are required to operate during diesel generator operation

! to maintain room environmental conditions acceptable. The licensee

i stated that actions could be taken following a seismic event to

start the fans locally and/or otherwise provide for room cooling.

A temporary design change was issued to the control room as Jumper

and Lifted Lead 86-146 on October 14, 1986, but not implemented.

l

l

l

t.

I , - _ . . ~ . . . _ . . _ - _ _ , . . _ - _ __ . _ . _ .- _ .-_,- _ --- _ .- _--_._-_ -. __

.

.

,

18

The inspector reviewed the proposed circuit modifications with the

. cognizant engineer and verified that the revised circuit would pro-

vide for diesel room fan operation independent from.the HVAC panel,

and provide circuit isolation from the panel. Aside from the above,

a design change initiated.as a result of Appendix R concerns is

presently scheduled for. implementation during the first quarter of

1987. No inadequacies were identified.

(d) Service building air conditionina (SAC) unit'1A and associated duct l

work. SAC 1A is part of the normal and emergency heating and ven-

. tlTation system for'the main control room. Failure of.a block wall

'

'

adjacent to SAC 1A could affect the unit control circuits and damage

a portion of the fresh air intake and closed circuit recirculation

ducting for the control room HVAC.

i The licensee stated that upon failure of the SAC 1A unit, actions

could be taken locally to provide for cooling in the control room

by opening doors and installing portable ventilation fans. The

inspector noted that this action would address room heating concerns,

I. but would not address concerns due to a potential radioactive source

i term that could be present, for example, from MSIV leakage.

The inspector noted that irrespective of the damage that a failed

4 block wall may cause to SAC 1A, the remainder of the control room

1

HVAC, even though it is safety class 3, it is not seismically quali-

fied, since the HVAC was installed as non nuclear safety during the

initial plant design and was administrative 1y upgraded to safety

i

-class 3 during the late 1970's to assure repair and modification

-

of the system would be subjected to the quality assurance program.

The licensee stated that protection of the control room environment .

for a concurrent seismic event, LOCA and degraded core (TMI type

>

source term) condition was beyond the design basis for the plant.

l The licensee's engineering evaluation addressed the above items and pro-

vided a justification for continued operation pending completion of ac-

'

' tions to correct the block wall deficiencies. The licensee evaluation

concluded that no immediate safety concerns exist, but the affected areas

! should be upgraded. The licensee submittal of September 19, 1986 stated -

, that modifications to either relocate control cables or to support block-

walls would be completed as necessary to address inadequacies in each

!

of the above four areas. The licensee's submittal also stated that a

schedule for completing the required modifications (for other than item

c c above) would be established by the end of 1985 after preliminary (con-

ceptual) design changes are established. The inspector noted that the

licensee's written commitment departed significantly from the verbal

commitment made previously, as documented on page 15 of NRC Inspection

Report 86-18.

This item remains unresolved pending completion of the licensee's actions

,

noted above to assess and correct the identified discrepancies, and pend-

}

ing NRC staff review of the licensee's actions.

.

,. , - - . . . , . , ,-.,e.n.-- -me. ., ,,,e.-.w-, .c .e,, .,- . .e.,--, e sm ,,mm, ,.- . - - - , %-, -.- rgm ,w me* s mew - -wr-e-e,---c= w-~ --

-

.

,

19

9.0 Review of GE AKF-2-25 Field Breakers

The inspector reviewed recirculation pump trip system design features and,

in particular, the maintenance and failure history of GE-AKF-2-25 field

breakers in accordance with NRC Region I temporary inspection instruction No.

RI-86-02. Details of the review are discussed below.

9.1 Design

The recirculation pump trip (RPT) system mitigates the consequences of

an anticipated transient without scram (ATWS) event and is accomplished

by opening the field breaker for the recirculation pump motor generator

(MG) set. This field breaker is a GE-AKF-2-25 unit. The field breaker

is designed to open upon completion of a two-out-of-two trip taken once

logic using any combination of two high reactor pressure or two low-low

reactor level trip input setpoints, arranged in two trip channel systems.

The technical specification required set point for high reactor pressure

is 1150 psig, and for low-low level is 82.5" above the top of the active

fuel, after a ten-second time delay.

The reactor high pressure signal is obtained from the slave trip units

of Rosemont 1152 DP level transmitters and the low-low level signal is

obtained from the slave trip units of Rosemont 1152 GP transmitters.

The master trip unit and other slave units are used to provide trips

required by the facility's emergency core cooling systems. Upon comple-

tion of the two-out-of-two taken once logic in a trip system, the neces-

sary contacts will be made and one of the two redundant shunt trip coils

will be energized to trip the AKF-2-25 field breakers for botn recircu-

lation MG sets. The entire trip system is safety grade except for the

breakers and the shunt trip coils. The instruments are powered from the

station instrument bus. The power to the logic is supplied by the sta-

tion batteries. The DC power to the trip units is supplied by dedicated

batteries. The RPT system interfaces with other safety systems that are

protected by fuses. Inadvertent actuation of the RPT system is minimized

by selecting set points such that this system would actuate only after

the set points for reactor scram are exceeded. The sensing instruments

and the trip logic are designed to be tested during power operation.

However, the breakers are not designed to be tested at power.

The licensee's design conforms with the Monticello design discussed in

BWR owner's group topical report NEDE-31096-P except for the trip sensor

arrangement. The Monticello design uses two-out-of-two logic for sepa-

rate reactor pressure or level trip channels. VY design uses both reactor

level or pressure trip input signals for each of the two trip channels.

9.2 Preventive Maintenance and Surveillance

Technical Specification Tables 3.2.1 and 4.2.1 specify the trip set

points and surveillance requirements, respectively, for the RPT actuation

instrumentation. These instruments are required to be checked daily,

. .. .

_ _________-_ _ . _ - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ . __ _____ _

. .

,

20

functional tested monthly and calibrated once per operating cycle. Plant

procedures OP 4342 and 4369 are specifically established to control func-

tional tests and calibrations of the RPT actuation instrumentation.

,

The MG set field breakers are tested once every operuting cycle. Plant

l- procedure OP 5221 is established to control the inspection, testing and

calibration of these breakers. Maintenance personnel are responsible

for the testing and calibration of the RPT MG set field breakers. The

history of those breakers is maintained on readily available "VISIrecord"

sheets.

9.3 Use of GE-AKF-2-25 Breakers

The licensee uses AKF-2-25 breakers for the recirculation pump MG set

field breakers and the main generator field breaker. During 1981 there

were four failures of recirculation pump MG set field breakers and in

1986 there was a failure of the main generator field breaker. As a re-

sult of the earlier failures, the licensee implemented a more thorough

preventive maintenance program for AKF-2-25 breakers in 1981. Since then,

no further failures were noted in the recirculation pump MG set field

breaker. The same preventive maintenance program is also applied to the

main generator field breaker. However, this did not prevent the recent

failure of the main generator field breaker.

9.4 Reliability of the RPT System

The system, except for the field breaker, is designed to be safety grade.

The redundancy and separation requirements inherent in the design adds

to the reliability of the instrumentation and trip logic. The licensee

also has a detailed preventive maintenance program and equipment history

files. As stated in the licensee's letter FVY 85-93 dated September 29,

1985 in response to NRC Generic Letter 65-06, the plant has the equipment

to trip the reactor coolant recirculating pumps automatically under the

conditions of an ATWS. However, the licensee has not established the

reliability of this system and in particular the MG set field breaker.

The inspectors discussed the 10 CFR 50.62 requirement, "This equipment

must be designed to perform its intended function in a reliable manner.",

and the use of the NRC guidance for non-safety related components

(Generic Letter 85-06) with the licensee's management.

The plant manager informed the inspectors that, other than an established

PM program and history files, there are no special reliability measures

for the MG set field breakers, and the breakers are not treated any dif-

ferently than other non-safety related equipment. The licensee has not

compared the existing controls for maintaining the field breakers to the

NRC guidance published in Generic Letter 85-06. The licensee management

stated that actions will be taken within six months to establish posi-

tions to (1) determine reliability of the RPT system during an ATWS and

(2) show that the licensee reliability measures for the RPT system are

_ _ _ _ _ _ _ _ _ _ _ - _ _

  • '

..

21

comparable to the NRC positions stated in Generic Letter 85-06. The

effectiveness of licensee's actions in this regard will be reviewed dur-

ing a future NRC inspection (UNR 86-22-04).

In the event that the recirculation pumps fail to trip automatically on

demand, the control room operators are required to run back and trip the

pump manually. If this is not possible, the breakers can be tripped

locally at the breaker. The inspectors noted that the operators and the

electricians were knowledgeable of the back-up actions in the event the

RPT is not accomplished automatically.

At the time of this inspection, the licensee had no plans to further

enhance the RPT system reliability through design change.

10.0 Status of Actions on NURfG 0737 - TMI Items

10.1 Item II.E.4.1.2, Dedicated Hydrogen Penetrations

This item was previously reviewed during Inspection 81-18 and was left

open pending development of the NRC staff position regarding the instal-

lation of hydrogen recombiners for post-accident hydrogen control in the

containment. Following amendment of 10 CFR 50.44 on December 2, 1981,

the NRC staff issued Generic Letter 84-09 on May 8, 1984, to clarify the

requirements for hydrogen control, including the use of hydrogen recom-

binars. The licensee rasponded to the amended regulation and the generic

letter by letters FVY 82-40 dated April 9, 1982, FVY 82-81 dated July

6, 1982, FVY 84-108 dated August 24, 1984, and FVY 84-128 dated October

31, 1984.

In FVY 84-104, the licensee committed to modify the existing air con-

tainment atmosphere dilution (CAD) system to make it a nitrogen purge

and repressurization system. The necessary modifications were completed

per plant design change request 85-04 prior to the startup from the re-

fueling outage that began in September, 1985. Completion of this action

eliminated the CAD system as a potential source of oxygen in the post-

accident drywell environment. NRC:NRR determined in a safety evaluation

,

dated September 10, 1985, that the three criteria of Generic Letter 84-09

! were satisfied and that recombiner capability per 10 CFR 50.44(C)(3)(II)

was not required.

l

'

Based on the above, the inspector determined that the licensee commit-

ments for this NUREG item were met and no further actions were required.

This item is closed.

10.2 Items I.C.1.2.8 and 3.B, Transient and Accident Procedures

l

,

The requirements of the original NUREG item were superseded by Supplement

l

'

1 issued on December 17, 1982. This item was last reviewed in Inspection

Reports 86-13 and 85-18, which verified implementation of new emergency

operating procedures (EOPs) following operator training.

!

l

l

.6 '

'22

The licensee implemented new emergency' operating procedures in accordance

with the Emergency Procedure Guidelines developed by the BWR Owner's

Group and approved by the NRC in Generic Letter ~83-05, Safety Evaluation

of Emergency Procedure Guidelines, NED0-24934. . NRC staff approval of

~this document constituted the pre-implementation review and approval of

the procedure technical guidelines, as required by section 7.2 of Sup-

plement 1 of the NUREG. Revision 3 of the guidelines were implemented

in the following E0Ps in November, 1985: OE 3100 - Reactor Scram; OE

<

,' 3101 - Reactivity Control; OE 3102 - RPV Level Control; OE 3103 - Drywell ,

'

Pressure and Temperature Control; and, OE 3104 - Torus _ Temperature and ,

.

Level Control. The guidelines for secondary containment control were

subsequently implemented by the licensee as OE 3105 Secondary Containmant

Control prior to startup from the refueling outage ending June, 1986.

The licensee also submitted an E0P Procedures Generation Package, inclu-

~

i

sive of a Writer's Guide, by letter FVY 84-75 on June 29, 1984, which

is presently under review by NRC:NRR. Implementation of the above pro-

.

cedures and completion of the above actions satisfied the licensee's

l commitments for this item.

1

The licensee is presently considering enhancements to the present E0Ps

'

i as part of the recent Containment Safety Study completed in August, 1985.

The procedure upgrade would consider incorporation of changes made_in

Revision 4 of the_E0Ps, and include instructions and/or enhancements for

combustible gas control, reactor level / power control and containment

venting. The inspector noted that_an in process, partial review of the

E0Ps has been completed by NRC inspection personnel during previous in-

[ spections of procedure validation activities and completion of operator

training on the procedures.(Reference: Inspections 84-21, 85-10, 85-18,

85-36, 86-10 and 86-13). Additionally, use of the procedures on the VY

plant-specific simulator were reviewed as part of the operator licensing

activities in July, 1986. However, the inspector noted that a systematic, '

comprehensive review of the E0Ps remains to be completed in accordance

i

with NRC:IE inspection instructions (TI 2515/79) pending approval of the

PGPs by NRC:NRR. This review will be completed to verify that the E0Ps

are prepared in accordance with the approved PGPs and are adequate to

control safety related functions following an accident. This item will

e be reviewed during a subsequent inspection and will be tracked under

i

NUREG Item I.C.1.3.B. Item I.C.1.2.B is considered closed administra-

tively.

+

10.3 Item II.E.4.2.7, Containment Vent and Purge Valves

'

This item was last reviewed during Inspection Report 81-18, which con-

tained an open staff item to review the ventilation system purge path

after plant operations began with the drywell inerted with nitrogen.

j NRC letter NVY 82-201 dated December 9, 1982 accepted the licensee's

'

design for this item, which relies on radiation monitors installed on

the reactor building ventilation ducting to detect elevated radiatien

levels in.the drywell and to initiate a containment isolation in the
event trip setpoints are exceeded. This approach is acceptable as long

l ,

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. . - - . - -

!

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23

as the method of drywell-to-torus differential pressure control maintains

a vent path from the torus through the standby gas system filter trains,

located below the radiation monitors. The inspector noted that the above

vent path was maintained subsequent to the start of plant operations with

an inerted drywell in May, 1982.

The licensee responded to the NRC staff's request for changes to the

technical specifications for this item by letter FVY 83-38 dated May 17,

1983. Based on the existing plant design and technical specifications,

the licensee concluded that no further actions were required for this

item. No inadequacies were identified. This item is closed.

10.4 Item II.K.3.18, ADS Actuation Logic

This item was last reviewed during Inspection 84-01, and was left open

pending NRC:NRR's approval of the licensee's position to not make any

modifications to the existing ADS logic. NRR rejected the licensee's

position by letter dated October 7, 1985, and requested that one of two

designs developed in conjunction with the BWROG and approved by the staff

be implemented.

In FVY 85-109 dated November 11, 1985, the licensee agreed to implement

one of the two modifications after completion of a limited probabilistic

risk assessment to aid in the selection of a design. The licensee's

initial preference would be to modify the existing ADS logic by adding

a manual inhibit switch in conjunction with a timer that would bypass

the high drywell pressure permissive after a sustained low vessel water

level. The FRA was scheduled for completion by November, 1986, so that

the final design details could be submitted for NRC staff review and

approval in time for implementation of the design change during the

refueling outage starting in June, 1987.

The licensee stated that scheduled completion of the PRA study has been

impacted by the containment safety study, but the engineering should be

completed carly in 1987. The licensee will proceed concurrently with

the development of EDCR 86-409 so that the modifications can be installed

during the 1987 outage as planned. The inspector stated that proposed

changes to the ADS technical specifications should be submitted early

in 1987 to allow sufficient time for NRR staff review of the amendment

request in time for startup from the outage. The licensee noted the

inspector's comments.

This item is open pending completion of the licensee's actions to modify

the ADS logic in a manner approved by the NRC staff, and subsequent re-

view during a future inspection.

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10.5 Item II.F.1.3, Containment High Range Monitor

This item was last reviewed during Inspection 84-11, and based on an NRR

safety evaluation (SE; dated July 16, 1985, the licensee was requested

to take actions to relocate the monitors within the drywell to better

meet the NUREG criteria for the radiation monitors. Following a Septem-

ber 4, 1985 meeting on the issue in NRC Region I, the licensee submitted

FVY 85-110 on November 22, 1985 to provide the basis for a technical

deviation from the requirements of the NUREG 0737 Table II.F.1-3 criteria

regarding location of the radiation detectors. In a subsequent SE dated

March 25, 1986, NRR accepted the existing installation based on addi-

tional information provided in the November 22, 1985 submittal, which

showed that the objectives of the NUREG criteria were met. No further

actions is required by the licensee on this item and this matter is

closed.

10.6 Item I.D.2.2&3, Safety Parameter Display System (SPDS)

The licensee provided commitments to this item in response to NUREG 0737

Supplement 1 by letter FVY 83-30 dated April 19, 1983. By letter FVY

85-10 dated February 1,1985, the licensee submitted a functional safety

analysis for the proposed SPDS, and committed to implement the modifica-

tions in conjunction with an upgrade to the plant computer. The computer

will be upgraded in two phases starting with the 1987 refueling outage,

and the SPDS will be completed during the Fall 1988 outage and thus be

operational for startup for operating cycle 14.

The licensee approach to this item was to finalize the SPDS design in

conjunction with the actions taken in response to other Supplement 1

items, which resulted in a schedule to fully implement the original NUREG

requirements upon initial installation of the necessary hardware. NRC:

NRR accepted the licensee's plans and schedule, as confirmed in an Order

dated August 29, 1985. Based on the above, NUREG Item I.D.2.2 is con-

sidered closed administrative 1y, and subsequent licensee actions for the

SPDS will be tracked under Item I.D.2.3. This item will be reviewed

further upon completion of the licensee's actions.

10.7 Item II.F.2, Inadequate Core Cooling Instrumentation

This item was last reviewed during Inspection 84-01. In response to this

NUREG item and Generic Letter 84-23, the licensee committed in letters

FVY 84-144 dated December 6, 1984 and FVY 85-29 dated March 28, 1985 to

change the reactor vessel level measurement system during the 1985-86

refueling outage. The plan was to replace the existing Yarway columns

and cold reference columns with a dual cold leg arrangement. The modi-

fications will be installed as safety class equipment and seismically

supported. The purpose of the change is to reduce Yarway level measure-

ment inaccuracies resulting from density variations caused by elevated

. . . -

-.

. . ~ . . - . . . . . _ . - - - - .

s

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. . .

.-

25 -

1

drywell temperatures, and to allow the reference _ legs to operate at a

lower temperature to reduce the possibility of boiling / flashing in the

legs.

In a letter dated May 24,_1985, NRR provided the results of the staff's

review of the licensee's proposal and approved the intended modifications

-

and schedule to complete:the NRR action for Item II.F.2. By letter dated

July 18,.1985,-the licensee _ proposed deferral of the modifications until

the 1987 outage to allow field verification of the exiting drywell con-

i figurations to finalize the new reference level support' design. NRR

accepted the revised schedule by letter dated September 6, 1985.

The' inspector had no further comment on this item. Completion of the

licensee actions to meet comnitments will be reviewed during a subsequent

inspection.

{

\ . 10.8 Item II.K.57, Manual Actuation of ADS

The licensee responded to this item by letter FVY 80-170 dated December

15, 1980 and stated that no actior would be tsken until the new symptom-

1 orientated emergency procedure guidelines were developed by the BWROG

i and approved by the NRC staff. The licensee implemented new emergency-

i operating procedures in accordance with Revision 3 of the guidelines,

- as discussed in section 10.2_above, which were approved by the NRC staff.

'

'

The inspector reviewed licensee procedure OE 3102, Reactor Pressure

Vessel Level Control, Revision 2. Step LC/D-10 cautions the operator

'

to assure low head pumps sufficient to maintain vessel water level are

running and available for injection prior to manually blowing down the

vessel with the ADS system.

l The licensee has satisfied the requirements for this item. This item

i

is closed.

!

10.9 Item III.A.1 & III.A.2, Emergency Response Capability (ERF Approval)

l By letter dated October 30, 1986, the licensee affirmed to NRC:NRR that

j. actions had been completed per Confirmatory Orders dated June 12, 1984,

r September 28, 1984, and August 29, 1986 to implement all emergency re-

sponse capability and meteorological data upgrade items required by Sup-

plement 1 of NUREG 0737, with the exception of the SPDS, which will be

[ completed prior to the startup from the 1988 refueling outage. NRR

acknowledged the licensee's commitments by letter dated April 28, 1986

and stated that an ERF Appraisal audit will be scheduled at a future time.

This item will be reviewed further during a subsequent inspection.

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26

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10.10 Technical Specifications for NUREG 0737 Items

The licensee responded to NUREG 0737 and Generic Letter 83-02 by letters

FVY 81-178 dated December 29, 1981, FVY 83-38 dated May 17, 1983, FVY

84-146 dated December 14, 1984 and FVY 85-117 dated November 26, 1985

to propose changes to the technical specifications (TSs) for various TMI

items, or otherwise provide justification why changes were not required.

Proposed Change No. 99 (FVY 81-178) covers the stack high range noble

gas monitor and is still outstanding. By letter dated August 11, 1986,

the NRC staff safety evaluation (SE) erroneously concluded that the TS

requirements for II.F.1.1 were addressed in the new RETS issued with

Amendment 83 on October 9, 1984. The new RETS address only the existing

(low range) stack noble gas monitors. This item will be followed with

NRC:NRR.

By letter dated August 11, 1986, NRR issued Amendment No. 96 to the

Technical Specifications to address modifications made per Items

III.D.3.4, II.F.1.3, II.F.1.4, II.F.1.'5, and II.F.1.6. The NRC staff

also concluded that no TSs or changes were required for Items II.B.1,

II.B.3 and II.F.1.2. In letters dated December 9,1982 and March 4, 1985,

the staff SEs concluded that no TSs were required for Items II.E.4.2.7

and II.K.3.28, respectively. The inspector noted that TS changes will

subsequently be required for Item II.K.3.18 upon installation of the ADS

design changes during the 1987 outage. No TS changes are required for

II.E.4.1, II.E.4.2.5, II.E.4.2.6, II.K.3.19 and II.K.3.45.

Technical specification changes have previously been issued for

I.A.1.1.3 - STA Training, II.K.3.15 - HPCI and RCIC Isolation, and

II.K.3.27 - Reactor Vessel Reference Level.

By letter FVY 83-38, the licensee provided reasons why TS changes are

not required for Items I.A.1.3, II.K.3.3, II.K.3.13 and II.K.3.22, and

no further actions are planned. The licensee's position on this item

has yet to be approved by NRR. This item will be followed during a sub-

sequent inspection.-

This item is unresolved pending completion of licensee and NRC actions

as listed above regarding NUREG 0737 technical specifications (UNR 86-

22-05).

11.0 Errata

The licensee informed the inspector of an error on page 26 of Inspection Re-

port 86-13, Section 10.0. The recirculation project team QA Supervisor was

Mr. R. L. Martin, and not Mr. A. Small.

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12.0 Management Meetings

Preliminary inspection findings were discussed with licensee management peri-

odically during the inspection. A summary of findings for the report period

was also discussed at the conclusion of the inspection and prior to report

issuance.

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