ML20154Q614

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Insp Rept 50-271/88-10 on 880701-0822.No Violations Noted. Major Areas Inspected:Actions on Previous Insp Findings, Operational Safety Security,Plant Operations,Maint & Surveillance,Lers & Licensee Response to NRC Initiatives
ML20154Q614
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 09/16/1988
From: Haverkamp D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20154Q612 List:
References
50-271-88-10, GL-84-11, IEB-80-11, IEB-82-03, IEB-82-3, IEB-83-02, IEB-83-2, IEB-88-007, IEB-88-7, NUDOCS 8810040019
Download: ML20154Q614 (17)


See also: IR 05000271/1988010

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U. S. "HCLEAR REGULATORY COMMISSION

REGION I

Report No.

_50-271/88-10

CJckt:t No.

50-271

License No. OPR-28

Licensee:

Vermont Yankee Nuclear Power Corporation

RD 5, Box 169

,

Brattleboro, Vermont

05301

Facility:

Vermont Yankee Nuclear Power Station

Inspection At: Vernon, Vermont

Inspection Conducted: July 1, 1988 - August 22, 1988

Inspectors:

Geoffrey E. Grant, Senior Resident Inspector

John 8. Macdonald, Resident Inspector

Joseph E. Carrasco, Reactor Engineer, Materials and Processes

Section (MPS), Engineering Branch (EB), Division of Reactor

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Safety (DRS)

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Robert A. McBrearty, Reactor Engineer, MPS, EB, DRS

Approved by:

o d / w*d M

4/dlif"

Donald R. Haverkamp, CWief

Date

Reactor Projects Section No. 3C

Inspection Sumn ary:

Inspection on July 1, 1988 - August 22, 1988

(Report No. 50-271/68-10)

Areas Inspceted:

Routine inspection on daytime and backshif ts by two resident

inspectors of:

actions on previous inspection findings;

operational safety;

security; plant operationc; maintenance and surveillance;

licensee event

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reports; licensee response to NRC initiatives; and, periodic reports.

Results:

1.

General Conclusions on Adequacy, Strength or Weakness in the Licensee's

Program

The licensee response to the reactor trip of July 3,1988 was a noteworthy

strength. The review process was much improved over recent performance in

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this area.

The review and PORC analysis were excellent and provided a

number of internal commitments for various corrective actions.

However,

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the evens itself highlighted a number of potential weaknesses including:

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lack of ade:quate training or understanding of reactor pressure regulator

operation and response, and indications that operators failed to utilize

all available plant parameter indications in their analysis of the press-

ure transient portion of the event (Section 6.1).

881004:.Ulv weuyte

PDR

ADOCK 05000271

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Inspection Summary (Continued)

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The licensee identified violation concerning failure to post a required

fire watch demonstrated several potential weaknesses including an inabil-

ity to adequately distinguish the difference between Technical Specifica-

tion .(TS) and non-TS 'related portions of fire protection system surveil-

lance and a failure to correctly determine the safety significance'of a

mali

ance action associated with the TS-related portion of the system

(Scr .an 6.4).

2.

Violations

The licensee identified a violation of a TS requirement to post a fire

watch when a portion of a fire protection system was inoperable.

No

Notice of Violation was issued (Section 6.4).

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TABLE OF CONTENTS

PAGE

1.

Persons Contacted. . . . . . . . . . . . . . . . . . . . . .

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2.

Summary of Facility Activities . . . . . . . . . . . . . . .

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3.

Status of Previous Findings (IP 92701) . . . . . . . . . . .

2

3.1 (Closed) Unresolved Item 88-08-07:

Licensee to Revise LER 88-05. . . . . . . . . . . . .

2

3.2 (Closed) Unresolved Item 88-08-01:

Establish a Fuel Oil Sampling Program in

Accordance with ASTM 0975-68 and TS . . . . . . . . .

2

3.3 (Closed) Unresolved Item 86-10-12-

Standby Liquid Control System (52) TS Submittal. . .

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3.4 (Closed) Unresolved Item 86-18-02:

Degraded Block Walls. . . . . . . . . . . . . . . . .

2

3.5 (Closed) Violation 86-17-01:

Lack of Procedure for Original 1980 Masonry Wall

Survey.

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3.6 (Closed) Violation 86-17-02:

QA Audit of 1980 Masonry Wall Activities Not

Documented for Evidence of Completion .

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3.7 (Closed) Deviation 86-17-03:

Masonry Wall Design Used Unverified, Non-Conservative

Mortar Strength. . . . . . . . . . . . . .

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3.8 (Closed) Unresolved Item 86-17-04:

YAEC Evaluation of Wall 22 Using Strain Criteria

Required Verfication Based on NRC-Approved Stress

Criteria. . . .

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3.9 (Closed) Unresolved Item 86-17-05:

Inadequate Data on Extent and Cause of Crack

Observed by the NRC in Three Unreinforced Walls

and Calculation Revised to Account for Cracks . . . .

3

4.

Operational Safety (IP 71707, 71710,). . . . . . .

. . . .

3

4.1 Plant Operations Review . . .

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4.2 Safety System Review.

4

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4.3 Feedwater leak Detection System . . .

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4.4 Inoperable Equipment.

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4.5 Review of Lifted Leads, Jumpers and Mechanical

Bypasses. . . . . . . . . . . . . . . . . . . . . . .

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4.6 Review of Switching and Tagging Operations. . . . . . .

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4.7 Operational Safety Findings .

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Table of Contents (Continued)

PAGE

5.

Security (IP 71707). . . . . . . . . . . . . . . . . . . . .

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5.1 Observations of Physical Security . . . . . . . . .

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5.2 Fitness for Duty Testing. . . . . . . . . . . . . . . .

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6.

Plant Operations (IP 71707, 93702, 82201, 94703) . . . . . .

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6.1 Reactor Trip: July 3, 1988 . . . . . . . . . . . . . .

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6.2 Loss of Wind Speed Indication . .

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6.3 Steam Leak from "2A" High Pressure Feedwater Heater . .

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6.4 Failure to Establish a TS-Required Fire Watch . . . . .

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7.

Maintenance / Surveillance (IP 71710, 61726, 62703, 61700) . .

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8.

Licensee Event Reporting (LER) (IP 90712, 92700) . . . . . .

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8.1 LER 88-06 . . . . . . . . . . . . . . . . . . . . . . .

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8.2 LER 88-07 . . . . . . . . . . . . . . . . . . . . . . .

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8.3 LER 88-08 . . . . . . . . . . . . . . . . . . . . . . .

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9.

Review of Licensee Response to NRC Initiatives:

(IP 92703) . . . . . . . . . . . . . . . . . . . . . . . .

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9.1 Generic Letter 84-11. . . . . . . . . . . . . . . . . .

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9.2 NRC Bulletin 88-07: Power Oscillations in Boiling

Water Reactors. . . . . . . . . . . . . . . . . . . .

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10.

Review of Periodic and Special Reports (IP 90713). . . . . .

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11. Management Meetings (IP 30703, 40700). . . . . . . . . . . .

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The NRC Inspection Manual inspection procedure (IP) or temporary instruc-

tion (TI) or the Region I temporary instruction (R1 TI) that was used as

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inspection guidance is listed for each applicable report section.

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DETAILS

1.

Persons Contacted

Interviews and discussions were conducted with members of the licensee

staff and management during the report period to obtain information per-

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tinent to the areas inspected.

Inspection findings were discussed per-

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iodically with the management and supervisory personnel listed below.

Mr. P. Donnelly, Maintenance Superintendent

  • Mr. R. Grippardi, Quality Assurance Supervisor

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Mr. S. Jefferson, Assistant to Plant Superintendent

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Mr. G. Johnson, Operations Supervisor

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Mr. R. Lopriore, Maintenance Supe-visor

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  • Mr. R. Pagodin, Technical Services Superintendent

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  • Mr. J. Pelletier, Plant Manager

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  • Mr. R. Wanczyk, Operations Superintendent

Mr. T. Watson, I & C Supervisor

  • Attendee at post-inspection exit meeting conducted on September 12, 1988.

2.

Summary of Facility Activities

Vermont Yankee Nuclear Power Station (VYNPS) was r(covering from a two-

week maintenance outage at the beginning of this inspection period.

The

reactor was taken critical on July 2,1988 and power ascension was com-

menced. On July 3, with plant power at 58% a reactor shutdown was initi-

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ated following the discovery of a through-wall leak in the "3B" low press-

ure feedwater heater steam extraction inlet piping. During the shutdown a

reactor scram occurred from approximately 5% power due to a malfunction in

the mechanical hydraulic control (MHC) system which was exacerbated by

procedural weakness and personnel error (Section 6.1). The heater repairs

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were completed and the reactor was taken critical on July 7.

On July 14

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power was reduced to facilitate the isolation of a leaking sight glass on

the "2A" high pressure feedwater heater (Section 6.3).

The licensee per-

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formed an emergency preparedness (EP) practice drill on August 5 in pre-

paration for the EP exercise later this month.

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NRC Region I specialists performed a confirmatory measurements inspection

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during the period August 7-12,1988 (Inspection Report 88-12). An emerg-

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ency preparedness inspection was performed by Region I specia?ists during

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the period August 16-19. 1988 (Inspection Report 88-11).

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3.

Status of Previous Inspection Findings

3.1 (Closed) Unresolved Item 88-08-07:

Licensee to Revise LER 88-05.

The licensee submitted LER 88-05 to report a potential loss of the

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standby gas treatment system.

Inspector review of the LER noted

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areas requiring correction or clarification.

The licensee subse-

quently revised LER 88-05.

This item is closed.

3.2 (Closed) Unresolved Item 88-08-01:

Establish a Fuel Oil Sampling

Program in Accordance with ASTM 0975-68 and Technical Specifications,

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The licensee fuel oil sampling program performed per TS 4.10.C.2 did

not fully conform to ASTM 0975-68 Table 1 requirements. The liceasee

has modified the sampling program to expand the analyses to include

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all of the ASTM 0975-68 Table 1 criteria. ^ Additionally, in order to

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increase the quality assurance of the John Deere and fire pump

diesels, the licensee has expanded the new analysis program to

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include these diesels as well.

This item is closed.

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3.3 (Closedl_ Unresolved Item 86-10-12:

Standby Liquid Control System

(SLC) TS Submittal.

This item remained open pending submittal of a

TS amend. Tent to clarify and upgrade SLC squib vrive trigger assembly

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surveillance testing. As noted in IR 50-271/87-02, Proposed Change-

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No. 136 was submitted by the licensee on January 16, 1987 and is

under review by NRC:NRR.

This item is closed.

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3.4 (Closed) Unresolved Item 86-18-02:

Degraded Block Walls.

Several

deficiencies were noted in safety related masonry block walls in IR

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50-271/86-17 and 86-18. Justificatinns for continued operations were

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reviewed and found acceptable in IR 50-271/86-22. Licensee plans to

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correct block wall deficiencies were reviewed and found acceptable in

IR 50-271/87-04. Work to correct the deficiencies was performed dur-

ing the 1987 refueling outage. The specialist inspection during this

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report period that reviewed and closed out IR 50-271/86-17 open items

related to block wall deficiencies also reviewed the effectiveness of

the physical repairs and found no deftetencies.

This item is closed.

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3.5 (Closed) Violation 86-17-01:

Lack of Procedure for Original 1980

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Masonry Wall Survey.

The inspector verified the existence of proced-

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ures to ensure the adequate scoping and implementation of bulletin

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IEB 80-11.

In addition, the four turbine building walls that had

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been omitted were modified to prevent any damage of adjacent safety

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related equipment during a postulated event.

This item is closed.

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3.6 (Closed) Violation 86-17-02:

QA Audit of 1980 Masonry Wall

Activities not Documented for Evidence c

.ompletion.

The inspector

determined that revised controi and imple,nenting procedu es provided

retrievable documentation of activities associated with-the IEB 80-11

program. This item is closed,

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3.7 (Closed) Deviation 86-17-05:

Masonry Wall Design Used Unverified,

Non-conservative Mortar Strength.

The inspector verified that mortar

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samples were obtained and independently tested. The samples exhibited

the following results:

the minimum mortar strength for any mortar

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sample tested was equal to 2000 pounds per square inch (psi).

Since

this exceeded the value which was used in the calculation (1800 psi),

the mortar used was appropriate and acceptable.

This item is closed.

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3.8 (Closed) Unresolved Item 86-17-04:

YAEC Evaluation of Wall 22 Using

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Strain Criteria Required Verification Based on NRC Approved Stress-

Criteria.

The inspector veri,fied that this wall was re-analyzed

using stress criteria consistent with the ACI 531-79 code.

The

analysis results showed that the subject masonry wall structural

integrity was adequate for all loading conditions.

This item is

closed.

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3.9 (Closed) Unresolved Item 86-17-05:

Inadequate Data on Extent and

Cause of Crack Observed by the NRC in Three Unreinforced Walls and

Calculation Revised to Account for Cracks.

The inspector determined

that the calculation was approached conservatively by assuming the

worst case (i.e. the effective shear area was taken as the width of

only one nominal block flange width).

Based on this assumption, the

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resulting shear stress was below the allowable.

The licensee agreed

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to maintain the structural integrity of this wall and to take the

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proper corrective and preventive actions required.

This item is

closed.

4.

Operational Safety

4.1 plant Operations Review

The inspector observed plant operations during regular and backshift

tours of the following areas:

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Control Room

Cable Vault

Reactor Building

Fence Line (Protected Area)

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Diesel Generator Rooms

Intake Structure

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Vital Switchgear Room

Turbine Building

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Control Room instruments were observed for correlation between chan-

nels, proper functioning, and conformance with Technical Specifica-

tions. Alarm conditions in effect and alarms received in the control

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room were reviewed and discussed with the operators. Operator aware-

ress and response to these conditions were reviewed. Operators were

found cognizant of board and plant conditions.

Control room and

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shift manning were compared with' Technical Specification require-

ments.

Posting and control of radiation, contaminated and high radt-

ation areas were inspected.

Use of and compliance with Radiation

Work Permits and use of required personnel monitoring devices were

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checked. Plant housekeeping controls were observed including control

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of flammable and other hazardous materials. During plant tours, logs

and records were reviewed to ensure compliance with station proced-

ures, to determine if entries were correctly made, and to verify cor-

rect communication of equipment status.

These records included var-

ious operating logs, turnover sheets, tagout and jumper logs, and

Potential Reportable Occurence Reports.

Inspections of the control

room were performed on weekends and backshifts including July 5-8,

18-22, 25, 26, and August 22, 1988. Operators and shift supervisors

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were alert, attentive and responded appropriately to annunciators and

plant conditions.

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4.2 Safety System Review

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The emergency diesel generators (EOG's), core spray, residual heat

removal, residual heat removal service water, and

high pressure

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coolant injection systems were reviewed to verify proper alignment

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and operational status in the standby mode.

The review included

verification that:

(i) accessible major flow path valves were cor-

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rectly positioned, (ii) power supplies were energized, (iii) lubri-

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cation and component cooling was proper, and (iv) components were

operable based on a visual inspection of equipment for leakage and

general

conditions.

No

violations

or

safety

concerns

were

identified.

4.3 Feedwater Leak Detection System Status

The inspector reviewed the feedwater leakage detection system and the

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monthly performance summary provided by the licensee in accordance

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with VYNPC letter FVY 82-105.

The licensee reported that, based on

the leakage monitoring data for July 1988, there were some deviations

in excess of 0.10 from the steady state value of normalized thermo-

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couple readings, and no failures in the sixteen thermocouples in-

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stalled on the four feedwater nozzles.

The deviations are related

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to the plant shutdowns and startups experienced in late June and

early July and do nut appear to be abnormalities. The inspector had

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no further questions in this area.

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4.4 Inoperable Equipment

Actions taken by plant personnel during periods when equipment was

inoperable were reviewed to verify that technical specification

limits were met, alternate surveillance testing was completed satis-

factorily, and equipment return to service upon completion of repairs

was proper.

This review was completed for the following items:

traversing incore probe drive ball valve,

"A"

EDG, Service Water

radiation monitor, stack air flow monitor, and fire deluge valve (see

Section 6.4).

4.5 Review of Lifted Leads, Jumpers and Mechanical Bypasses

Lif ted lead and jumper (LL/J) requests and mechanical bypasses were

reviewed to verify that controls established by AP 0020 were met, no

conflict with the technical specifications were created, the requests

were properly approved prior to installation, and a safety evaluation

in accordance with 10 CFR 50.59 was prepared if required. Imphmen-

tation of the requests was reviewed on a sampling basis.

4.6 Review of Switching & Tagging Operations

The switching and tagging log was reviewed and tagging activities

were inspected to verify plant equipment was controlled in accordance

with the requirements of AP 0140, Vermont Local Control Switching

Rules.

Implementation of the requests was reviewed on a sampling

basis.

4.7 Operational Safety Findings

Licensee administrative control of off-normal system configurations

by the use of LL/J, mechanical bypass, and switching and tagging pro-

cedures, as reviewed in Sections 4.4, 4.5, and 4.6 was in compliance

with procedural instructions and was consistent with plant safety

with the exception of a failure to station a fire watch for the

inoperable fire deluge valve. Licensee efforts to minimizo active

lif ted leads, jumpers and mechanical bypasses is noteworthy.

5.

Security

5.1 Observ,ap

af Physical Security

Selected

. acts of plant physical security were reviewed during

regular ant. backshif t hours to verify that controls were in accord-

ance with the security plan and approved procedures.

This review

included the following security measures:

guard staffing; vital and

protected area barrier integrity; maintenance of isolation zones-

and,

implementation of access controls, including authorizatic.,

badging, escorting, and searches.

No inadequacies were identif b .

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5.2 Fitness for Duty Testing

On August 12, 1988, the licensee received information from a local

law enforcement agency which implicated two site contractors in the

usage of illegal controlled substances.

The licensee immediately

escorted the individuals offsite, suspended their site access and

subjected them to drug testing in accordance with the VYNPC fitness

for duty program.

The individuals submitted to the testing.

On

August 15, 1988, test results for both individuals came back positive

and their site access was permanently suspended. The two contractors

are employed by TTI Engineering and had worked within the maintenance

department primarily in support of stores / procurement and work pack-

age preparation activities.

All projects in which the individuals

were involved received several levels of management review.

The

inspectors had no further questions.

6.

plant Operations

6.1 Reactor Trip: July 3, 1988

The plant experienced an automatic reactor trip on July 3,1988 due

to high flux rate on the intermediate range monitors.

The plant was

in the process of shutting down to repair a feedwater heater leak and

was at less than l's power at the time of the trip. Just prior to the

trip, operators had observed a decrease in reactor pressure from 930

to 872 psig.

In response to the pressure decrease, the operators

attempted to establish the mechanical pressure regulator (MPR) e.cds

of the mechanical hydraulic control (MHC) system to control reactor

pressure.

This effort continued for approximately five minutes with

little apparent MPR setpoint response.

During this period of time

reactor pressure had decreased to 850 psig.

The operators then at-

tempted to establish reactor pressuro control with the bypass valve

opening jack (BP0J). Because the BP0J regulator was not set for the

lowest demanded pressure, the BP0J could not assume pressure control

at the desired pressure. When the BP0J did assume pressure control,

the setpoint manipulations resulted in greater b, sass valve opening,

a further reduction in reactor pressure, and subsequent reactor

pressure and level oscillations. The single operating feedwater pump

tripped on a high reactor water level signal resulti.1g from a high

water level oscillation. Reactor water level then decreased until a

standby feedwater pump started and delivered relatively cold water to

the vessel, resulting in a rapid neutron flux and power increase

sufficient to cause the IRM high flux scram from less than 1% power.

All systems performed as required following the trip.

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Several concerns were identified in review of this event. During the

period when the operators were attempting to establish pressure con-

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trol with the MPR (and subsequently the BP0J), two IRM high flux half

scrams were received as a result of reactor pressure induced power

oscillations. The inspectors believe that, based on the uncertainty

as to the effectiveness of the actions the operators had taken to

control pressure as well as the pressure, level and flux oscillations

experienced at less than 5% power, a more prudent operator action

might have been to manually trip the reactor.

Existing plant pro-

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cedures did not address operator response to a low reactor pressure

condition with the reactor mode switch not in "RUN" as was the case

in this event.

Further, the operators on shift did not realize that

the use of any MHC pressure regulating mode during the decreasing

pressure trend would have further reduced reactor pressure. It also

appeared that the operators did not utilize all of the plant opera-

ting parameter indicators available when interpretting the impact of

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their actions with regard to pressure control.

The PORC reviews of the event and post trip report were thorough and

comprehensive.

The committee discussions of the event and causal

analysis were perceptive and probing.

Significant licensee internal

actions and commitments resulting from the PORC review included:

I&C replacement of the IRM recorders with more reliable units

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less prone to recorder pen hang ups.

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Operations assurance that operators were made aware of the above

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recorder problems.

Operations assurance that operators utilize all plant parameter

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indicators

available when diagnosing

transient conditions.

Operations implementation of appropriate precedure revisions to

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address this event.

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Operations to attempt to reproduce this event on the site

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specific simulator.

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Training to determine the fidelity of the site specific simula-

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tor with respect to this event and MHC pressure control in

general.

The content and completeness of the post trip report improved mark-

edly from recent similar reports.

The increased quality of the

report enabled FORC members to perform an exhaustive review of the

event and to propose comprehensive actions to improve operator and

equipment performance and response with respect to the transient

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experie-

'd in this event.

Inspectors previously documented concerns

about c...

iences in post trip reports. The unresolved item (50-271/

88-08-03) which addressed this issue remains open pending completion

of licensee corrective actions.

The inspectors had no further

questions.

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6.2 Loss of Wind Speed Indication

On July.21,1988, at 3:00 a.m., the shift supervisor determined that

an emergency assessment capability had been compromised when a loss

of all wind speed indication was discovered. All appropriate notifi-

cations were made at that time.

The primary meteorological (MET)

tower parameter printer was out of service since a lightning strike

on July 16.

Local indication of primary MET tower wind speed was

discovered out of service on July 21. The back-up wind speed indi-

c.ator was judged inoperable by the shif t supervisor because it had an

outstanding maintenance / inoperable equipment sticker on it.

Subse-

quent I&C investigation revealed that the back-up wind speed indi-

cator was previously repaired and the sticker was not yet authorized

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for removal. The back-up wind speed indicator was declared operable

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at 5:00 a.m. cn July 21, 1988.

The shif t supervisor properly reported this event based on the infor-

mation available to him.

Failure of I&C to remove the maintenance /

inoperable equipment sticker was an isolated instance of personnel

inattentiveness. It was not indicative of a programmatic deficiency.

The inspectors had no further questions.

6.3 Steam Leak from "2A" High pressure Feedwater Heater

On July 15, 1988, the licensee performed a power reduction in order

to isolate a steam leak that had been discovered on the "2A" high

pressure feedwater heater sight glass.

Once the heater was isolated

operators entered the heater bay area and closed the sight glass

isolation valves.

The sight glass will probably not be repaired

until the 1989 refueling outage.

Local heater level indication will

be lost during this period.

The inspectors had no further questions.

6.4 Failure to Establish a TS-Required Fire Watch

The VYNPS Technical Specification (TS) 3.13.F.2 requires that from

and after the date that one of the sprinkler systems specified in

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Table 3.13.F.1 is inoperable, a fire watch shall be established

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within one hour to inspect the location with the inoperable sprinkler

system at least once every hour.

Contrary to the above, from Jt

Aupust 2, 1988, the licensee

failed to establish a one-hour firs

a of the area served by the

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cable penetration area sprinkler sy sem after the system failed

surveillance testing on July 28.

On August 2, a management review

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of the surveillance identified this situation and a one-hour fire

watch was immediately established.

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During routine surveillance testing of the cable penetration area

sprinkler system, deluge valve DV-301 failed to open and the system

was therefore rendered inoperable.

A maintenance request (MR) was

issued to initiate repairs to the valve. However, the shift super-

visor review of the MR failed to identify the system as being

inoperable and thus did not establish a fire watch.

The immediate root cause of this event was personnel error, in that

the initial shift supervisor and Operations Supervisor review of the

MR failed to identify.the cable penetration area sprinkler system as

inoperable.

The inspectors addressed an additional concern to the

licensee that ?.he fire protection system surveillance procedure con-

trols testing of TS- and non-TS related portions of the system with-

out distinction.

Although not a contributor to this event, proced-

ures written in this style increase the probability of TS require-

ments not being properly implemented following a failed surveillance.

The licensee reviewed this event with'each operating shift. Emphasis

was placed on proper equipment operability determinations.

Because

the failure to establish a TS-required fire watch was identified by

the licensee, was of a low severity level, had prompt corrective

actions, was reported in LER 88-10, and was not related to corrective

actions for a previous violation, no notice of violation will be

issued in this instance.

However, long term review of licensee

actions to ensure proper operability determinations are made and

review of clarifications to the surveillance procedure remains an

open issue (50-271/88-10-01).

7.

Maintenance / Surveillance

On July 11,1988, the #3 traversing incore probe (TIp) drive machine ball

valve failed to close following withdrawal of the probe. The ball valve

failure occurred during the reactor startup from a two-week mini outage.

Because the TIp machines must be readily available to perform traces as

required by reactor engineering procedure and the probes must be in the

shields for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> prior to entry into the TIP room, the valve was not

replaced until the reactor attained a steady power level. On July 14, 1988,

I&C personnel removed the 3/8 inch ball valve and its actuator, and leak

rate tested and installed a replacement valve under the direction of '4R

88-1649. The maintenanca effort was well supervised and coordinated.

The

engineering support department (E50) provided technical guidance to the

I&C department for testing and installation requirements for the valve and

actuator. This was a routine example of typical support provided to the

maintenance department by ESD.

The inspectors had no further questions.

',;

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8.

Licensee Event Reporting (LER)

The inspector reviewed the below licensee event reports (LER's) to deter-

mine that with respect to the general aspects of the event:

(1) the re-

port was submitted in a timely manner; (2) description of the event was

accurate; (3) root cause analysis was performed; (4) safety implications

were considered; and (5) corrective actions implemented or planned were

sufficient to preclude recurrence of a similar event.

8.1 lj_R88-06

The LER 88-06, "Source Inventory and Leak Test" addressed a licensee

identified failure to adequately document a sealed source survey in

accordance with TS 6.5.F.

The details of the missed survey were

previously reviewed as documented in IR 50-271/88-06, Section 9.1.

The LER fulfilled the above criteria with the exception of timeli-

ness.

The licensee had originally intended on making a special re-

port to the NRC to describe this licensee identified violation.

On

that basis, a notice of violation was not issued and item 88-06-02

was considered closed.

The licensee subsequently determined that a

special report was not appropriate but a voluntary LER would be sub-

mitted.

This determination took an excessive amount of time and

resulted in an LER submittal four months af ter the event date. Expe-

dited submittal of the LER occurred after inspector inquiry of the

status.

8.2 LER 88-07

The LER 88-07, "Main Turbine Trip and Reactor Scram from Feedwater

Flow Controller Malfunction" addressed a plant trip f rom a high

reactor water level caused by a component failure in the feedwater

ficw controller.

The details of the scram were previously reviewed

as documented in IR 50-271/88-08, Section 6.1.

The LER fulfilled the

above criteria and no deficiencies were noted. Additionally, the LER

was a good example of detailed and thorough event analysis and

reporting.

8.3 LER 88-08

The LER 88-08, "Unanticipated Scram Due to Malfunction of Turbine

Vibration Probe" addressed a plant trip due to an end-of-life failure

of the #10 main turbine bearing vibration monitoring probe. The LER

fulfilled the above criteria and no deficiencies were noted.

Licen-

i

see event description, analysis, and corrective actions detailed in

the LER were comprehensive,

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9.

Review of Licensee Response to NRC Initiatives

9.1 Generic Letter 84-11

Inspections conducted at several boiling water reactors (BWR's) re-

vealed intergranular stress corrosion cracking (IGSCC) in large

-

diameter recirculation and residual heat removal piping.

Based on

the results of those inspections which were conducted pursuant to IE

Bulletins 82-03, Revision 1 and 83-02, and the NRC August 26, 1983

Orders, the Commission concluded that an ongoing program for similar

reinspections at all BWRs was needed.

Generir Letter (GL) 84-11 was

issued on April 19, 1984 to provide licensees with NRC recommended

actions to accomplish the a forementioned reinspections.

The GL

listed the following actions as an acceptable response to the IGSCC

concerns:

Inspections should include 20% of the welds in each pipe size

--

of IGSCC sensitive welds not inspected previously (but no less

than four welds) and reinspection of 20% of the welds in each

pipe size inspected previously (but not less than two welds) and

found not be cracked.

This sample should be selected primarily

from weld locations shown by experience to have the highest

propensity for cracking.

Inspection of all unrepaired cracked welds.

--

Inspection of all weld overlays on welds where circumferential

--

cracks longer than 10*.' of circumference were measured.

Inspection of any veld treated by induction heating stress

--

improvement which had not been post treatment UT acceptance

tested.

In the event that cracks or significant growth of old cracks are

--

identified, expand the inspection scope in accordan.:e with IEB 83-02.

All Level !! and Level IIT UT examiners should demonstrate com-

--

petence in accordance with IEB 83-02, and Level I examiners

should demonstrate fie*d performance capability.

Leak detection and

leakage

limits

should be sufficiently

--

restrictive to ensure timely investigation of unidentified

leakage.

The inspector reviewed licensee actions in response to IE Bulletin 83-02 and Generic Letter 84-11 to ascertain that regulatory require-

ments regarding IGSCC concerns were met.

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Bulletin 83-02 required that licensees of BWR facilities identified

in Table 1 of the Bulletin perform a demonstration of the effective-

ness of the ultrasonic testing (UT) methodology used to examine welds

in recirculation system piping.

The demonstrations were to be per-

formed at the EPRI NDE Center at Charlotte, North Carolina on service

induced cracked pipe samples made available for this purpose.

In response to the above mentioned requirement, on March 10-11, 1983,

the licensee sent a five member team of Magnaflux Quality Services

personnel, its inservice inspection ISI vendor, to the EPRI NDE cen-

ter to perform the required demonstration.

The team included one

level III examiner, three Level II examiners and one Level I trainee.

Scanning and data recording were performed by the Level II examiners

aided by the Level I trainee, and the Level III team member was

responsible for data evaluation and classification of the findings

into two Categories, "Crack" or "no Crack."

The team performance was found to be acceptable in that eighty per-

cent of the total number of cracks were detected within the six hour

time limit and the number of false calls was within the pre-estab-

lished limit.

The licensee's letter dated June 5,

1984 to the NRC compared the

licensee's Generic Letter 84-11 reinspection program to the staff's

recommendations listed in GL 84-11 and provided additional in fo rma-

tion requested by the NRC.

The licensee's reinspection program was

found, with two exceptions, to meet the Ceneric Letter.

The 11cen-

see's June 5,1984 letter identified the exceptions to the GL taken

by the licensee which involved the number of weld overlays to be

inspected on welds of identical joint geometry in the same system,

and the definition of "ef fective overlay thickness." The NRC Inspec-

tion Report No. 271/84-13 identified the exceptions as an unresolved

item.

The item was closed in NRC Inspection Report No. 271/85-32

based on licensee actions in 1985 regarding the replacement of recir-

culation and residual heat removal piping which eliminated the basis

l

'er the unresolved item.

I

Prior to the replacement of the recirculation and residual heat

removal system piping, the licensee initiated the use of moisture

sensitive tape as a leak detection method for the early detection of

leaking pipe joints. Since the completion of the replacement program

the tape is no longer used.

The licensee is bound by its Technical Specification 3.6.C requirements regarding leak rate limits and leak

detection methods.

The inspector determined that IGSCC inspections at Vermont Yankee

have met the requirements contained in IE Bulletin 83-02, and Generic

letter 84-11.

No violations were identified.

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9.2 NRC Bulletin 88-07:

Power Oscillations in Boiling Water Reactors

The inspectors reviewed the initial licensee actions in response to

NRC Bulletin 88-07, which documented the LaSalle dual recirculation

purrp trip and power ocsillation event.

Operations management placed

Bulletin 88-07, previously issued NRC Information Notice 88-39, and

INPO SER 14-86 in the control room night orders book for all licensed

individuals to read.

During shift turnovers, an assistant to the

operations supervisor held discussions and addressed questions relat-

ing to the event.

THe VYNPS TS requires that in the event of a dual recirculation pump

trip, power be immediately reduced to below TS limits and the plant

be in hot shutdown within the next twelve hours.

These requirements

are implemented in plant procedure OT-3118, "Recirculation Pump Trip

- Procedure."

Inspector discussions with several operators determined that they

were familiar with the LaSalle event and also that, if a similar

event were to have occurred at VYNPS, the operators would have pro-

perly executed the above requirements and avoided the power oscilla-

tions experienced at LaSalle. The inspector had no further questions

regarding immediate licensee actions in response to this bulletin.

10. Review of periodic and Special Reports

Upon receipt, the inspector reviewed periodic and special reports submit-

ted pursuant to Technical Specifications. This review verified, as appli-

cable: (1) that the reported information was valid and included the NRC-

required data; (2) that test results and supporting information were con-

sistent with design

predictions and

performance

specification;

and

'

(3) that planned corrective actions were adequate for resolution of the

problem. The inspector also ascertained whether any reported information

'

should be classified as an abnormal occurrence. The following report was

reviewed:

Monthly Statistical Report for plant operations for the month of

--

July 1988.

No violations or safety concerns were identified.

11. Management Meetings

At periodic intervals during this inspection, meetings were held with

senior plant management to discuss the findings.

A summary of findings

for the report period was also discussed at the conclusion of the inspec-

tion and prior to report issuance.

No proprietary information was

identified as being included in the report.

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