ML20202G278
| ML20202G278 | |
| Person / Time | |
|---|---|
| Site: | Vermont Yankee File:NorthStar Vermont Yankee icon.png |
| Issue date: | 01/28/1999 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20202G265 | List: |
| References | |
| 50-271-98-14, NUDOCS 9902050078 | |
| Download: ML20202G278 (31) | |
See also: IR 05000271/1998014
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U.S. NUCLEAR REGULATORY COMMISSION
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REGION I
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Docket No.
50-271
Licensee No.
Report No.
98-14
. Licensee:
Vermont Yankee Nuclear Power Corporation
Facility:
Vermont Yankee Nuclear Power Station
. Location:
Vernon, Vermont
Dates:
November 22,1998 - January 4,1999
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Inspectors:
Brian J. McDermott, Senior Resident inspector
Edward C. Knutson, Resident inspector
William A. Maier, Emergency Preparedness Specialist
Richard P. Croteau, Project Manager, NR3
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Douglas A. Dempsey, Reactor Engineer
Thomas G. Scarbrough, Senior Mechanical Engineer, NRR
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Approved by:
Clifford J. Anderson, Chief, Projects Branch 5
Division of Reactor Projects
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2050078 990128
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ADOCK 05000271
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EXECUTIVE SUMMARY
Vermont Yankee Nuclear Power Station
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NRC Inspection Report 50-271/98-14
This inspection included aspects of licensee operations, engineering, maintenance, and plant
support. The report covers a six week period of routine resident inspector activities, and
includes the results of in-office procedure review by an emergency preparedness specialist. This
report also provides the results of a motor-operated valve inspection conductad the week of
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November 16,1998.
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Operations
VY was slow to pursue corrective action after the NRC identified a degraded high voltage
power supply with the potential to affected the operability of a TS-required instrument in
the reactor building ventilation isolation system. Once initiated, VY's corrective action was
prompt and adequately resolved the degraded condition. (Section 01.1)
VY failed to recognize that a long standing practice of allowing manual containment
isolation valves to be opened under administrative controls was in conflict with the
Technical Specifications. A November 1998 procedure change review was weak be ;ause
it invoked this practice for draining the torus and was a missed opportunity to identify the
problem. VY's practice did not compromise plant safety and the licensee promptly
submitted a TS change to correct the problem. (Section O3.1)
Maintenance
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The maintenance activities observed during this period were performed well. Workers
demonstrated appropriate radiological control and foreign material exclusion control
techniques. Good supervisory oversight, system engineering involvement, and
radiological protection support were observed. (Section M1.1)
The surveillance activities observed during the period were correctly performed. However,
in one case the multiple procedures which control the standby gas treatment system
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charcoal sample removal had the potential to cause errors. Activities were well controlled
and coordinated by the control room operators. (Section M1.2)
Maintenance personnel initiated work on the wrong standby gas treatment system filter
train and caused the entire system to be declared inoperable for a short period of time.
The error was identified by the licensee and appropriate corrective actions were initiated,
including a Maintenance department work stand down. The workers' failure to follow the
maintenance procedure is a violation of TS 6.5 and this issue was treated as a non-cited
violation. (Section M1.3)
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Executive Summary (cont'd)
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W identified that a pressure switch for the HPCI steam supply isolation logic had been
isolated during corrective maintenance and had not been properly returned to sewice.
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Because the switch had been depressurized, the low steam line pressure isolation would
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have functioned, if required. The failure to follow maintenance procedures was
determined to be a Non-cited Violation based on an assessment of the safety significance
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of the condition and W's corrective actions. (Section M1.4)
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The "C" residual heat removal service water pump failed inservice test acceptance criteria
for differential pressure on two occasions. Although immediate corrective actions restored
acceptable performance, W developed an operability justification to address the
degradation that was obsewed. The operability justification was adequate and W
management placed priority on the resolution of this degradad condition. (Section M2.1)
Primary containment isolation valve HPCI-16 failed to stroke closed during an inservice
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test due to the failure of the torque switch in its motor actuator. Appropriate immediate
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actions were taken in response to the test failure, a good evaluation was made to assess
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the generic implications of the problem and the failed torque switch was replaced.
Although the failure could have prevented full seating of the valve, the valve would have
closed enough to mitigate a high energy line break event. An inspector follow-up item was
initiated to track NRC review of W's final disposition of this issue. (Section M2.2)
W's approach to the Maintenance Rule requirements for assessing the effects of out-of-
service equipment on overall safety functions is consistent with NRC-accepted guidance.
However, implementing procedures lacked positive confirmation that alternatives to the
pre-analyzed work had been evaluated in accordance with the program expectations.
(Section M3.1)
W's methods for acquiring Maintenance Rule performance monitoring data are generally
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effective. However, the recording of unplanned equipment outages and the screening of
Maintenance Rule-related Event Reports are two areas where the accurate collection of
data may be challenged. (Section M3.1)
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Enaineerina
Positive aspects of the Generic Letter 96-05 periodic verification program for motor-
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operated valves (MOVs) were observed, including: (1) development of more efficient test
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techniques, (2) implementation of a motor test program, and (3) an aggressive motor-
actuator lubrication and refurbishment schedule. However, several aspects of the periodic
verification program, such as program documentation and MOV performance degradation
rates were as yet undeveloped. (Section E1.1)
Design-basis thrust calculations for two MOVs were not revised to reflect dynamic test
information, resu! ting in the calculations not reflecting the actual plant configuration. This
condition was an example of poor configuration management. (Section E1.1)
The inservice test failures of two scram discharge volume drain valves led to the
identification of problems with the new valve / actuator design installed during the 1998
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- Executive Summary (cont'd)
refueling outage. Errors were identified in the safety evaluation and there is a lack of
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design information from the vendor. In accordance with NRC guidance, this issue, which
may represent a violation of NRC requirements will remain open for a reasonable time to
allow the licensea to develop its corrective actions. (Section E2.1)
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TABLE OF CONTENTS
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EXECUTIVE SU MMARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11
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TABLE O F CONTE NTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . v
- Summary of Plant Status . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
1. Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
01
Conduct of 0pe rations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
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O1.1 Area Radiation Monitor Power Supply Failure . . . . . . . . . . . . . . . . . . . 1
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Operations Procedures and Documentation . . . . . . . . . . . . . . . . . . . . . . . . , . 2
03.1 Administrative Control of Manual Containment Isolation Valves . . . . . . 2
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Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
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08.1 In-Office Review of LERs Related to Operations . . . . . . . . . . . . . . . . . 3
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l l . Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4
M1
' Conduct of Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4
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M1.1 Maintenance Observations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4
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M1.2 Surveillance Observations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5
M1.3 Standby Gas Treatment System Maintenance . . . . . . . . . . . . . . . . . . . 6
M1.4. HPCI Low Steam Pressure Isolation Switch Not Returned To Service . 7
M2.
Maintenance and Material Condition of Facilities and Equipment . . . . . . . . . . . 9
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M2.1 ' Residual Heat Removal Service Water Pump "C" Low Differential
Pressu re . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
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M2.2 Motor-Operated Valve Torque Switch Failure . . . . . . . . . . . . . . . . . . . 10
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M3
Maintenance Procedures and Documentation . . . . . . . . . . . . . . . . . . . . . . . . 11
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M3.1 Maintenance Rule implementation Review . . . . . . . . . . . . . . . . . . . . . 11
M8
Miscellaneous Maintenance lssues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14
M8.1 In-Office Review of LERs Related to Maintenance . . . . . . . . . . . . . . . 14
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< l l i . E n gi nee rin g . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15
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E1
Conduct of Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15
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E1.1
Implementation of Generic Letter (GL) 96-05, " Periodic Verification of
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Design-Basis Capability of Safety-Related Motor-Operated Valves" . . 15
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E2
Engineering Support of Facilities and Equipment . . . . . . . . . . . . . . . . . . . . . . 20
E2.1
Scram Discharge Volume Drain Valve Failures . . . . . . . . . . . . . . . . . 20
E8
Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22
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E8.1
Review of Open items . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22
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E8.2 Review of VY Cycle 19 Operating Report . . . . . . . . . . . . . . . . . . . . . . 22
IV. Plant Support . . . . . . . . . . . . . . . . . . . . .................................... 23
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P3
EP Procedures and Documentation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
P3.1
In-Office Review of Emergency Plan Implementing Procedes . . . . . 23
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Table of Contents (cont'd)-
V. Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
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Exit Meeting Sum mary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
ATTACHMENTS
Attachment 1 - List of Acronyms Used
Attachment 2 - ltems Opened, Closed, or Discussed
Atthchment 3 - Emergency Response Plan and Implementing Procedures Reviewed
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Report Details
Summarv of Plant Status
Throughout the inspection period, Vermont Yankee (VY) was operating at 100 percent power,
with few exceptions. Minor power reductions were made in support of surveillance testing and a
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l. Operations
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. Conduct of Operations'
01.1 Area Radiation Monitor Power Suoolv Failure
a.
Inspection Scooe (71707)
' Area radiation monitor (ARMS) for the reactor building ventilation and refuel floor provide
input to the reactor building ventilation isolation. The detectors are powered by a safety
class high voltage power supply, ES-17-451B. During a routine control room tour, the
inspector noted that the output voltage of ES-17-451B was significantly lower than
expected and informed the licensee. The inspector assessed VY's response to the
degraded condition.
b.
Observations and Findinos
- On November 23, the inspector observed that the voltage meter on high voltage supply
ES-17-451B indicated 440 VDC, whereas the normal voltage for such a power supply was
approximately 600 VDC. The inspector related this observation to an on-shift licensed
operator, and again to the Operations Planning Group.
On November 24, the inspector observed that the power supply voltage had decreased to
420 VDC, confirming that the unit was degrading. Although a work order request had
been initiated the previous day, the voltage indication had not yet been verified and the
potential effect of low voltage on the operability of the associated ARMS had not been
thoroughly evaluated. After the inspector questioned the equipment operability, system
' engineering determined that the affected ARMS should not be considered operable
because the lower detector voltage could have a negative impact on detector sensitivity.
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The two ARMS were declared inoperable at 7:30 a.m. on November 24. Technical Specification 3.2, " Protective Instrument Systems," Table 3.2.3, requires that the reactor
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building ventilation system be isolated and the standby gas treatment system operated if
the subject ARMS are not available for more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
In response to this problem, VY performed as-found calibration checks on the affected
ARMS and determined that they were operating satisfactorily. ES-17-451B was replaced
later that day, and the ARMS were declared operable at 4:00 p.m.
' Topical headings such as O1, M8, etc., are used in accordance with the NRC standardized reactor
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inspection report outline. Individual reports are not expected to address all outline topics.
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Since the as-found calibrations of the affected ARMS were satisfactory, a condition
requiring entry into the action statement never actually existed; therefore, no violation of
TS occurred. Nonetheless, VY's actions in response to the identification of this problem
were slow. NRC inspection manual part 9900, " Operable / Operability: Ensuring the
Functional Capability of a System or Component," states that the timeliness of operability
determinations should be commensurate with the safety significance of the issue, and that
the allowed outage times ' contained in TS generally provide reasonable guidelines for
safety significance. In this case, VY did not perform a thorough investigation of the
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condition or evaluate the potential consequences of the condition for more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />
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after the problem was identified.
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Conclusions
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VY was slow to pursue corrective action after the NRC identified a degraded high voltage
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power supply with the potential to affected the operability of a TS-required instrument in
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the reactor building ventilation isolation system. Once initiated, VY's corrective action was
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prompt and adequately resolved the degraded condition.
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Operations Procedures and Documentation
O3.1 Administrative Control of Manual Containment Isolation Valves
a.
Inspection Scooe (71707)
On November 23,1998, the inspectors noted that VY revised procedure OP-2123 to allow
torus water level control using manual valves, including a normally locked closed
containment isolation valve (CIV). The inspector reviewed this procedure against the
FSAR description and TS requirements for primary containment.
b.
Observations and Findinas
A partial revision of OP-2123, " Core Spray," was approved on November 20,1998, to
allowed the use of a draln line on the core spray (CS) suction pipe, and temporary hose, to
drain water from the suppression pool to an equipment drain sump. The drain line has two
manual valves in series and is normally capped. The procedure change allowed a local
operator to uncap the line, unlock and open the manual CIV, and open a second
downstream manual valve to establish the drain flow path. OP-2123 also requires the
auxiliary operator to remain at the valves and to have direct communication with the
control room. This activity was first performed on November 20,1998, with the
requirements for primary containment integrity in effect.
TS 3.7.2 requires primary containment to be maintained at all time when the reactor is
critical. TS 1.N defines Primary Containment Integrity and, in part, states, all manual
containment isolation valves on lines connecting to the containment which are not required
to be open during accident conditions are closed. The inspector discussed the apparent
conflict between the revision to OP-2123 and TS with VY management.
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VY management initiated ER 98-2092 to determine the cause of this event and to develop
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corrective actions. VY subsequently identified several other activities where manual CIVs
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are opencd under administrative controls, including TS required surveillance testing. As
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an immediate corrective action, Operations management required Operators to document
entry into the TS 3.7.2,24-hour action statement for loss of primary containment integrity
when manual CIVs were opened. On December 11,1998, VY submitted a TS change
request to allow administrative control of manual containment isolation valves and
eliminate the need to enter the TS action statement for loss of primary containment
integrity.
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The inspector noted that VY's practice of using administratie controls for these valves
was consistent with standard Technical Specifications and did not compromise plant
safety. However, VY's practice was in conflict with their TS and should have been
recognized. The inspector concluded that VY's failure to recognize the conflict between
the TS wording and the procedure revision as a weakness in the procedure review and
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approval.
VY procedure AP-0152 requires the preparation of the Control Room Shift Turnover
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Checklist, which includes a log (VYAPF 0152.02) for inoperable Technical Specifications
systems or components. Step 4.a.1. of this procedure requires the use of this log when a
system or component is inoperable. VY's past failure to document entry into the TS action
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statement during use of the manual CIVs is a violation of VY procedures. This failure
constitutes a violation of minor significance and is not subject to formal enforcement
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action.
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c.
Conclusions
VY failed to recognize that their long standing practice of allowing manual containment
isolation valves to be opened under administrative controls was in conflict with the
Technical Specifications. A November 1998 procedure change review was weak because
it invoked this practice for draining the torus and was a missed opportunity to identify the
problem. VY's practice did not compromise plant safety and the licensee promptly
submitted a TS change to correct the problem.
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Miscellaneous Operations issues
08.1
In-Office Review of LERs Related to Ooerations (90712)
An in-office review of LERs was performed to assess whether further NRC actions were
required. The adequacy of the overall event description, immediate actions taken, cause
determination, and corrective actions were considered during this review. The following
issues were closed-out based on the in-office review.
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(Closed) LER 98-020-01: Inadequate Equipment Control Practices Result in Two
Mispositioned isolation Valves Allowing Degradation of Primary Containment Integrity
Supplemental LER 98-020-01 provided VY's conclusion regarding the root cause of the
mispositioned valves and a description of the long term corrective actions. VY's
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investigation determined that inadequate equipment control practices led to the problem.
Corrective actions planned for the event included a review of independent verification
practices, briefings of Operations crews, and changes to improve the clarity of valve
restoration documentation. The licensee's corrective actions described in the
supplemental report appeared adequate. The event was evaluated in NRC Inspection
Report 50-271/98-10, the original LER tvas reviewed, and the problem was dispositioned
as a non-cited violation. The inspector concluded that no additional action is required and
this LER is closed.
(Closed) LER 98-019-00: Off-Normal System Alignment Following a Plant Trip Which
involved the Loss of a Reactor Water Recirculation System Pump and Reactor Water
Thermal Stratification Results in a Spurious Shutdown Cooling Isolation
This event occurred on June 10,1998, during transition to the residual heat removal
(RHR) system shutdown cooling (SDC) modo of operation. Initiation of RHR flow caused
a transient pressure increase that exceeded the high pressure isolation setpoint and
resulted in automatic closure of the SDC suction isolation valves. Similar events had
occurred several times in the past, and had been addressed through operating procedure
changes and operator practices to gradually initiate flow. The precise cause of this event
was still being investigated at the time that the LER was issued, with the results to be
submitted in a supplemental report; however, as indicated by the LER title, the off-normal
plant alignment leading up to the event and resultant thermal stratification are likely
contributors. No water hammer occurred due to this event, and actual reactor pressure
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did not exceed the automatic isolation setpoint. Therefore, this LER is closed.
11. Maintenance
M1
Conduct of Maintenance
M1.1 Maintenance Observations
a.
Insoection Scope (62707)
The inspector observed portions of plant maintenance activities to verify that the correct
parts and tools were utilized, the applicable industry code and technical specification
requirements were satisfied, adequate measures were in place to ensure personnel safety
and prevent damage to plant structures, systems, and components, and to ensure that
equipment operability was verified upon completion of post maintenance testing,
implementation of the Maintenance Rule Program was also reviewed when applicable to
these activities.
b.
Observations and Findinas
The inspector observed portions of the following activities and reviewed a sample of the
administrative controls for the maintenance.
Control rod drive pump "B" rotating assembly replacement per work order 97-
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11585, observed on December 8 and 12.
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-- Observed preliminary disassembly to support the pump casing lift the following day,
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Work was being pc rformed in a contaminated area with dedicated RP support and full
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time foreman supavision. No deficiencies were noted.
-- On December 12, observed preparations to land the pump casing. Level 3 FME
controls were in effect and the material accountability log was being properly maintained.
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No deficiencies were noted.
Valve CRD-33B repair, observed on December 12.
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-- Attended the pre-job brief for CRD-33B disassembly and noted that the appropriate
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personnel were in attendance. Emphasis was placed on the time that would be allotted for
the work (4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, based on 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> between draining the scram discharge volume). In
addition, operations personnel were to have a separate brief prior to valve disassembly to
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discuss contingencies for draining during the maintenance.
-- Observed valve removal, disassembly, and reassembly. There were no obvious
problems with the valve internals. A vendor representative and engineering were at the
work site, and the job received full time RP coverage. No deficiencies were noted.
Safety related fuse replacements in the control room performed on December 18,
1998, under multiple work orders.
-- Observed the pre-evolution brief and noted a good emphasis was placed on confirming
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the accuracy of work documents and concurrent verification of the maintenance activities.
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-- System engineering support was present and actively involved in the oversight of the
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activities.
c.
Conclusions
The maintenance activities observed during this period were performed well. Workers
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demonstrated appropriate radiological control and foreign material exclusion control
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techniques. Good supervisory oversight, system engineering involvement, and
radiological protection support were observed.
M1.2 Surveillance Observations
a.
Inspection Scope (61726)
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The inspector observed portions of a surveillance test to verify proper calibration of test
instrumentation, use of approved procedures, performance of work by qualified personnel,
conformance to Limiting Conditions for Operations (LCOs), and correct post-test system
restoration.
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b.
Observations and Findinas
Portions of the following surveillance activities were observed:
"A" and "B" emergency diesel generator monthly surveillances, observed on
November 24-25. No deficiencies were noted.
High pressure coolant injection (HPCI) quarterly flow sunteillance, observed on
November 30.
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-- The HPCI steam supply isolation valve, V23-16, failed during this test. Refer to
section M2.2 of this report.
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"B" star'dby gas treatment system charcoal filter test cell change-out per OP-4501,
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" Filter Tosting," observed on December 9.
-- OP-4501was implemented by the radiation protection department, with
assistance at various points from the mechanical maintenance department. The
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inspector noted that the work order steps and the procedure steps were not well
integrated, and in some cases were duplicated. Although the individuals involved
understood their respective roles, the lack of integration of the two work
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documents could result in an inadequate charcoal sample. This issue was
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discussed with the VY maintenance superintendent. Procedure quality and
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content have been identified as areas for improvement by VY's Functional Area
Assessment and a corrective actions are planned.
increased frequency testing of the scram discharge volume vent and drain valves,
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see section E2.1.
c.
Conclusions
The surveillance activities eboarved during the period were correctly performed. However,
in one case the multiple procedures which control the standby gas treatment system
charcoal sample removal had the potential to cause errors. Activities were well controlled
and coordinated by the control room operators.
M1.3 Standbv Gas Treatment System Maintenance
a.
Insoection Scoce (62707)
The inspector observed portions of planned maintenance activities on the "B" train
standby gas treatment system (SGTS).
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b.
Observations and Findinas
On December 8, work order 98-10273 was approved for replacement of the "B" SGTS
charcoal filter test cell. In preparation for this activity, Operators tagged the "B" SGTS out
of service and placed the SGTS fan in " pull to lock." However, maintenance personnel
commenced work on the "A" SGTS train, which resulted in both trains being inoperab!e at
the sarne tirne. This problem was identified by an RP technician and was promptly
reported to the control roorn. Because the error was identified quickly, the maintenance
personnel had only begun to remove the filter train's exterior panel. Based on progression
of the work at the time of discovery, VY determined the unit would likely have performed
its safety function if required, and that there were no personnel safety issues.
VY restored the "B" SGTS to service within the TS 3.7 allowed outage time for two
inoperable SGTS subsystems (24 hrs). VY then restored frorn the inadvertent
>
maintenance on the "A" SGTS. Maintenance management conducted a work stand down
for tne department to review the incident and an Event Report was initiated.
'
The inspector determined this problem was the result of human error and that no
significant contributing causes were apparent. VY's management took immediate
corrective actions to reinforce expectations during a work stand down. A failure to follow
procedures for the conduct of maintenance is a violation of TS 6.5, Plant Operating
Procedures. This non-repetitive, licensee-identified and corrected violation is being
treated as a non-cited violation, consistent with Section Vlf.B.1 of the NRC Enforcement
Policy. (NCV 98-14-01: SGTS Maintenance Procedure implementation)
c.
Conclusions
Maintenance personnelinitiated work on the wrong standby gas treatment system filter
train and caused the entire system to be declared inoperable for a short period of time.
The error was identified by the licensee and appropriate corrective actions were initiated,
including a Maintenance department work stand down. The workers' failure to follow the
maintenance procedure is a violation of TS 6.5 and this issue was treated as a non-cited
violation.
M1.4 HPCI Low Steam Pressure Isolation Switch Not Returned To Service
a.
Inspection Scope (62707)
While per'orming a routine surveillance on the high pressure coolant injection (HPCI)
system on November 24, technicians discovered that one of four detectors for the low
steam pressure isolation function was isolated. The inspector reviewed the circumstances
surrounding this event.
b.
Observations and Findinas
While performing surveillance procedure OP-4357, HPCI Steam Line Low Pressure
Functional / Calibration, technicians identified that the instrument line valve for pressure
- .- -.
-.
-
. - - . -
_ - - .
_--. - - .-.
. ~- . - --...
-
.
.
8
switch PS-23-68D was closed and that the switch was in a tripped condition. The
pressure switch is designed to trip on low steam pressure, and inputs to a logic (one out of
two taken twice) that controls closure of the HPCI steam supply isolation valves. As such,
one half of the isolation logic was satisfied by the as-found condition. After consultation
with Operations shift supervision, the pressure detector was returned to service, the
surveillance was completed satisfactorily, and an event report was initiated.
,
The subject detector had been replaced on October 24,1998, as corrective maintenance.
W determined the detector had been inadvertently left isolated following its replacement
,
and post-maintenance testing. A root cause evaluation was in progress at the close of the
,
inspection period.
TS Table 3.2.2 requires 4 operable instrument channels for the Low HPCI Steam Supply
Pressure trip system. The TS definition of operable states, "a... component...shall be
operable or have operability when it is capable of performing its specified function (s)."
Since the pressure switch had been in a condition to initiate an isolation signal, VY
determined that it had been operable, even though its sensing line was isolated.
The inspector concluded that, although the Low HPCI Steam Supply Pressure trip system
remained capable of performing its intended safety function, the affected channel was
inoperable. The pressure switch is designed, tested, and maintained to provide an
isolation signal if steam pressure decreases to the trip setpoint. Based on the as-found
condition, the switch was not capable of its required function because the sensing line was
isolated from the HPCI steam supply. However, the inspector also concluded that, in this
case, the safety and risk significance of the isolated pressure switch was negligible.
Because the switch had been depressurized, the low steam line pressure isolation would
have functioned, if required. Also, a risk assessment by a Region I Senior Reactor
j
Analyst concluded there was an insignificant reduction in HPCI reliability as a result of the
as-found condition. Based on these findings, this failure constitutes a violation of minor
+
significance and is not subject to formal enforcement action. The inspector also noted the
W plant manager stated that a voluntary Licensee Event Report will be submitted on this
event.
l
,
in response to the technicians' finding, W initiated actions to restore the switch,
i
documented the problem in a Level 1 Event Report (98-2102), and performed an initial
review for programmatic proceduralissues that could have caused this event. Although
long term corrective actions were under evaluation by W at the close of this report period,
the inspector considered W's general response to this event reasonable.
The inspector reviewed the tagging order and procedure associated with replacement of
the pressure switch. The inspector concluded that if the administrative controls were
implemented, as written, the pressure switch would have been properly retumed to
service. The failure to follow procedures for corrective maintenance is a violation of TS , 6.5, Plant Operating Procedures. This non-repetitive, licensee-identified and corrected
violation is being treated as a Non-cited Violation, consistent with Section Vll.B.1 of the
NRC Enforcement Policy. (NCV 98-14-02: HPCI Steam Line Low Pressure isolation
Instrument isolated)
-_
-
-
,
,,
-.-
,-
-
. _ _ _ _ _ _ . _. _ _ _ _ _ _ _ _ , _ _ . - _ _ _ _ _ _ _ _ _ _ _ . . _ _ _ _ . . _ . .
.
-
9
c.
Conclusions
- W identified that a pressure switch for the HPCI steam supply isolation logic had been
isolated during corrective maintenance and had not been properly returned to service.
Because the switch had been depressurized, the low steam line pressure isolation would
have functioned, if required. The failure to follow maintenance procedures was
determined to be a Non-cited Violation based on an assessment of the safety significance
of the condition and W's corrective actions.
M2
Maintenance and Material Condition of Facilities and Equipment
M2.1 Residual Heat Removal Service Water Pumo "C" Low Differential Pressure
a.
Inspection Scope (62707)
Inspection Report 50-271/98-13 discussed the November 3,1998, surveillance test failure
of the "C" RHRSW pump. After replacement of the "C" pump, W had initiated plans to
refurbish the remaining three pumps on an expedited basis. Hcwever, while performing
alternate pump testing in preparation for maintenance on the "D" RHRSW pump, the new
,
"C" RHRSW pump failed the surveillance test. The inspector reviewed W's response to
J
this problem and revised corrective action plans.
,
b.
Observations and Findinas
'
On December 3,1998, the "C" RHRSW pump failed its surveillance test acceptance
criteria for differential pressure. This pump had been replaced on November 6 and post
maintenance testing had demonstrated a 15% margin above the minimum required
differential pressure. At the time of the second failure, VY's investigation of the first failure
was not completed. On December 5, W installed a refurbished pump, completed post
maintenance testing and surveillances, and declared the "C" RHRSW pump operable. W
continued to investigate the root cause and sent the pump which failed after only a month -
in service back to the vendor for testing.
Increased frequency testing of the RHRSW pumps had been initiated after the first
surveillance test failure and the frequency was increased after the second failure. On
December 28, the "D" RHRSW pump failed the acceptance criteria for minimum
differential pressure. However, a second set of test parameters collected later that same
day indicated the pump was performing acceptably and would meet all of the inservice test
criteria. Event Report 98-2223 was initiated to capture this event in the corrective action
program. On December 31, W management approved BMO 98-44 to justify the
operability of the RHRSW pumps. The BMO addressed the limiting RHRSW pump
configuration used for the Alternate Cooling System (ACS) and concluded that with
cooling tower basin temperature of s73* F, the ACS was operable, even if the RHRSW
pump performance was degraded.
The inspector reviewed BMO 98-44 and concluded W provided an adequate basis for
i
operability of the RHRSW pumps given the heat removal capability of the system during
the winter months. The BMO evaluated both the ACS function and the post-LOCA
1
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function of the RHRSW pumps. Because of the reduced deep basin temperature
assumed in the BMO (s73 F), VY performed a safety evaluation to address this change
from the system's FSAR described design condition (s105'F). The inspector verified a
sample of the procedure changes required to implement the BMO had been completed.
VY's root cause investigation was still under way at the conclusion of this inspection report
period. Several corrective actions were being pursued in parallel and the inspector
!
concluded that VY was placing priority on the long term resolution of this degraded
condition.
c.
Conclusions
The "C" residual heat removal service water pump failed inservice test acceptance criteria
I
for differential pressure on two occasions. Although immediate corrective actions restored
acceptable performance, VY developed an operability justification to address the
degradation that was observed. The operability justification was adequate and VY
management placed priority on the resolution of this degraded condition.
M2.2 Motor-Operated Valve Teraue Switch Failure
a.
Inspection Scope (62707)
On November 30,1998, the HPCI steam supply outboard isolation valve, HPCI-16, failed
to travel closed during a quarterly inservice test. The inspector observed the immediate
actions of the Operations crew and reviewed the subsequent investigation and corrective
actions by VY.
b.
Observations and Findinas
The control room operators took the actions required by TS in response to the valve's
failure by closing the redundant containment isolation valve in the penetration and
declaring the HPCI system inoperable. A conservative determination was made to report
the event as a failure of a single train safety system (reference Event Notification 35092).
This notification was later retracted after the licensee's investigation determined HPCI was
capable of performing its intended safety function, prior to being removed from service
when the penetration was isolated.
VY's investigation of the as-found condition identified that one set of contacts on the
valve's motor-operator did not have continuity. The control logic for HPCI-16 uses leaf-
style torque switch in series with the " seal-in" portion of close circuit for remote manual
operation. In (
"ast, the torque switch is bypassed in the closed direction by the circuits
for automatic isolation until the valve is 197% closed (i.e., the valve port is covered).
Based on the valve's control logic and valve being essentially open when travel stopped,
the inspector concluded the valve traveled closed while the operator held the hand switch.
After the closed limit switch provided dual control board indication, the operator released
the hand switch and the valve stopped because the seal-in circuit was not made up.
VY maintenance personnel reported that while checking continuity of the torque switch
contacts, the circuit was initially open but then made up. Close observation of the torque
.. . - -_ . . _ _ _ , _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ . _
__.
.
11
.
switch revealed that the second block of contacts, used for the logic of HPCI-16, was
slightly rotated in relation to the neutral position of the torque switch shaft. As a result, the
spring loaded contact fingers on one side of the contact block did not appear to have the
same contact pressure. At the end of the inspection report period, VY planned to ship the
torque switch to the vendor for evaluation.
'
The inspector reviewed VY's operability evaluation that addressed the generic implications
of the torque switch lailure. This condition was viewed as appkcable to direct current (DC)
operators since the second contact blocks were originally required on their torque
switches to minimize arcing. The inspector concluded this evaluation, coupled with an
absence of previous failures of this type, provided a good basis for VY's conclusion that no
generic operability concern exists. The inspector also noted that VY's assessment of 10
CFR 50.72 and 50.73 reporting requirements was appropriate. The isolated failure of a
containment isolation valve is not, by itself, reportable. In addition, the valve's capability to
. mitigate the consequences of a high energy line break were not impacted by the torque
j
switch failure.
'
Pending the inspectors review of the licensee's final root cause determination, evaluation
of 10 CFR 21 reportability, and maintenance rule functional failure review, this issue will
be tracked as an inspector follow-up item. (IFl 98-14-03: MOV Torque Switch Failure -
Final Resolution)
c.
Conclusions
Primary containment isolation valve HPCI-16 failed to stroke closed during an inservice
test due to the failure of the torque switch in its motor actuator. Appropriate immediate
,
actions were taken in response to the test failure, a good evaluation was made to assess
!
the generic implications of the problem and the failed torque switch was replaced.
'
Although the failure could have prevented full seating of the valve, the valve would have
closed enough to mitigate a high energy line break event. An inspector follow-up item was
- t
initiated to track NRC review of VY's final disposition of this issue.
M3
Maintenance Procedures and Documentation
M3.1 Maintenance Rule lmolementation Review
a.
Insoection Scope (62706)
10 CFR 50.65, " Requirements for Monitoring the Effectiveness of Maintenance at Nuclear
Power Plants," (the Maintenance Rule") states in part that, in performing monitoring and
preventive maintenance activities, an assessment of the total plant equipment that is out
of service should be taken into account to determine the overall effect on performance of
safety functions. The inspector reviewed VY's process for implementing this portion of the
maintenance rule. In addition, the inspector reviewed VY's process for acquiring
performance monitoring data.
.
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12
b.
Observations and Findinas
,
l
Measures to Assess the impact of Removina Eauipment from Service
Regulatory Guide 1.160, " Monitoring the Effectiveness of Maintenance at Nuclear Power
Plants," states that NUMARC 93-01, " Industry Guideline for Monitoring the Effectiveness
of Maintenance at Nuclear Power Plants," provides methods acceptable to the NRC staff
l
for complying with the provisions of the maintenance rule. As indicated in W procedure
PP-7009, "10 CFR 50.65 Maintenance Rule Program," W utilized this guidance in
developing maintenance rule implementation plan. To assess the equipment out of
service fcr overall effect on safety functions, NUMARC 93-01 indicates that a quantitative
assessment of probabilistic risk is not required. This guidance also states that guidelines
for removing structures, systems, and components (SSCs) from service could take the
form of a matrix, a check list, a list of pre-analyzed configurations or some other utility
specific approach. It goes on to indicate that each planned maintenance activity that will
result in the removal of an SSC from service should be assessed for its impact on key
plant safety functions both during the planning and scheduling phase and prior to
authorizing removal of the SSC from service.
VY uses 1) an integrated work schedule which provides a pre-analyzed assessment of
equipment out of service and safety impact, and 2) a matrix approach for when the pre-
analyzed schedule does not address the configuration the plant would be in to support a
maintenance activity due to schedule changes and/or emergent work. The integrated
work schedule consists of a 12-week fixed schedule that was evaluated by the Safety
Assessment Group from the approach of probabilistic risk assessment (PRA).
The inspector reviewed the Safety Assessment Group's evaluation of the 12-week
schedule. Many of the systems that are managed under the 12-week schedule were not
modeled in the PRA, and therefore cannot be assessed in that context. For systems that
were modeled in the PRA, the inspector noted that the assessment of impact was based
on scheduled maintenance, rather than removal of the system from service. This was
significant in that conclusions of " insignificant impact" were often based on the fact that the
scheduled preventive maintenance activities were non-intrusive and therefore the system
was assumed to be available.
'
The inspector determined there is a potential weakness in how VY's program addresses
the inclusion of corrective maintenance during the planning phase. The implementing
procedure requires that the weekly schedule be re-assessed if the work involves a system
that was not scheduled for the particular week. However, if the corrective maintenance
involves a system scheduled for the particular week, it does not have to be reassessed,
even if the scope of work changes the equipment availability assumed in the initial PRA
based assessment. While W's overall approach is consistent with the guidance of
NUMARC 93-01, it should be recognized that inclusion of corrective maintenance in the
12-week schedule may alter the basis of the pre-analysis and may render the prior
assessment invalid. System Engineering management stated that this issue will be
reviewed for possible procedure enhancements and will be tracked under W's internal
i
'
commitment system.
_ _ .__._..._ _ _ _ . . _ _ _ _ _ . _ _ _ _ _ _ _ _
.
l
.
.
13
The inspector reviewed VY's process for assessing the impact of maintenance prior to
authorizing removal of an SSC from service. VY procedure AP-0125," Plant Equipment
Control," govems this process, and reiterates the approach of using pre-analyzed
configurations and a matrix for this purpose. However, the procedural steps that discuss
use of the SSC redundancy matrix contain no binding requirements, stating only that it
provides additional guidance and identifies configurations that should be avoided.
Acauirina Performance Monitorina Data -
The two primary means of acquHng performance monitoring data are the Maintenance
Rule Out of Service Log and the Event Report process. The inspector noted that these
processes are generally effective at capturing equipment out-of-service times and
potential maintenance rule functional failures. However, an area for improvement is
capturing periods of unintended equipment unavailability. For example, a tagging error
resulted in the wrong service air compressor being removed from service; however, the
resultant unavailability was not captured in the Maintenance Rule Out of Service Log and
the Event Report was not flagged (that is, marked for routing through the Maintenance
Rule Coordinator) as a maintenance rule issue. in another example, reactor building
.
ventilation unexpectedly shut down on two occasions during this inspection period, due to
I
cold outside temperature. Event Reports were generated for both instances, but neither
was flagged as a maintenance rule issue until after the inspector discussed them with the
Maintenance Rule Coordinator.
From discussions with the work control center personnel who maintain the Maintenance
Rule Out of Service log, recording instances of unintended equipment unavailability is a
function of whether or not they are informed of it. From observations at Event Report
screening meetings, maintenance rule screening appears to concentrate on whether or
not the event constituted a maintenance rule functional failure; events relating only to
,
system reliability may not be flagged as containing maintenance rule information.
c.
Conclusions
I
'
VY's approach to the Maintenance Rule requirements for assessing the effects of out-of-
service equipment on overall safety functions is consistent with NRC-accepted guidance.
However, implementing procedures lacked positive confirmation that alternatives to the
!
pre-analyzed work had been evaluated in accordance with the program expectations.
i
VY's methods for acquiring Maintenance Rule performance monitoring data are generally
effective. However, the recording of unplanned equipment outages and the screening of
Maintenance Rule-related Event Reports are two areas where the accurate collection of
data may be challenged.
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.
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'
.
14
,
M8
Miscellaneous Maintenance issues
M8.1 In-Office Review of LERs Related to Maintenance (90712)
An in-office review of the following LERs was performed to assess whether further NRC
actions were required. The adequacy of the overall event description, immediate actions
taken, cause determination, and corrective actions were considered during this review.
l
The following issues were closed-out based on the in-office review.
. (Closed) LER 98-017-00.01: Inadequate Design Package and Implementing Procedure
Results in Redundant Trains of the Standby Gas Treatment System with Fan Supply
Breaker Trip Setpoints Potentially Attainable with Normal Start In-Rush Current
,
!
.
l
On June 1,1998, "B" standby gas treatment (SGTS) system train failed to start on
demand. Investigation revealed that the cause was that the fan supply breaker over-
'
l
current trip setpoint was set lower than the required value. Subsequently, the "A" SGTS
l
fan supply breaker was checked and found also to have a low over-current trip setpoint.
'
Both SGTS fan supply breakers had been replaced as part of a design change that had
been installed in 1992.- VY determined that the cause of the incorrect over-current trip
setpoints was that the design change package and installation procedure had not
established the setpoint during installation. This issue was discussed in inspection report
50-271/98-08, and resulted in the issuance of two violations.
In response to this event, VY performed a safety evaluation of other safety class breakers
to ensure that over-correct setpoint control was not a generic problem. Two other
i
breakers were identified as having the wrong over-current setpoint; one of these was in a
safety class application (a standby fuel pool cooling pump) and was reported in revision 1
i
!
to the LER. In addition, procedure AP-6001, " Installation and Test and Special Test
Procedures," has been revised to strengthen the procedure pertinent to establishing
protective device settings, and procedure OP-5210, "MCC Inspection," is being revised to
reference the motor data sheet as the governing document for breaker settings. The
inspector verified that the outstanding revision is being tracked under VY's commitment
tracking system. The inspector assessed that these actions, along with the immediate
actions as discussed in inspection report 50-271/98-08, adequately addressed the
,
l
problem. Accordingly, LERs 98-017-00 and 01, and VIO 98-08-02: Design Settings Not
Translated into Installation Procedures for SGTS Breakers, are closed.
-
(Closed) LER 98-021-00: Inadequate Licensing Basis Documentation Retrievabili y
l
Results in the Failure to Meet IST Requirements for Diesel Fuel Oil Day Tank Level
Control Valves
This event occurred on August 3,1998, when it was recognized that manual ope ation of
,
l
the emergency aiesel generator (EDG) fuel oil day tank level control valves had rat been
included in the inservice testing (IST) program. Manual opeiation of these valves L,
required for continued EDG operation in the event of a loss of station / instrument air
pressure; therefore, this function is required to be verified within the IST program. In
response to this event, VY verified that the valves could be operated manually and
entered them into the IST program. This event was of minimal safety significance,
,
.-
-
.
.
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-
l
l
l
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15
l
because subsequent testing indicated that the valves were (and therefore, always had
been) capable of being manually operated. Failure to include manual operation of the
l
valves in the VY IST program was a violation of minor significance and is not subject to
formal enforcement action. Therefore, this LER is closed.
.
M8.2 Review of Open items (92902)
The following open item was reviewed for closure based on a review of additional
l
info!mation from VY and a sampling of the licensee's corrective actions.
(Closed) VIO 98-08-02: Design Settings Not Translated into Installation Procedures for
SGTS Breakers
The open item was reviewed and closed with the associated LER 98-017-00 discussed in
Section M8.1 of this inspection report.
'
111. Engineering
E1
Conduct of Engineering
E1.1
Imolementation of Generic Letter (GL) 96-05. " Periodic Verification of Desian-Basis
Capability of Safetv-Related Motor-Operated Valves"
a.
Insoection Scoce (Temporarv Instruction 2515/140)
Generic Letter (GL) 96-05 requested licensees to establish programs to verify
through periodic testing that safety-related motor-operated valves (MOVs) are
capable of performing their safety functions within the current licensing basis. Prior to
'
the inspection, VY responded to the recommendations of GL 96-05 in letters to the
NRC dated November 15,1996, March 13,1997, and November 3,1997.
A three-phase MOV periodic verification program developed by the Joint Owners
Group (JOG) was reviewed by the NRC staff and determined to be acceptable with
certain conditions and limitations documented in a safety evaluation report issued on
October 30,1997. In its March 13,1997 letter, VY described an alternative program
plan. This inspection evaluated VY's alternative plan to determine whether it was
l
consistent with the licensee's commitments and with the recommendations of GL 96-
l
05. The inspection was conducted through reviews of documentation and interviews
with licensee personnel. The incpectors selected a sample of MOVs considering
dynamic test availability, valve type, and risk significance to evaluate program
(
implementation. The following valves were included:
V23-15
High piessure coolant injection (HPCI) inboard containment
.
isolation (10-inch Walworth flexible wedge gate valve)
V23-16
HPCI outboard containment isolation (10-inch Walworth flexible
'
.
wedge gate valve)
1
V13-15
Reactor core isolation cooling inboard containment isolation
.
valve (3-inch Walworth solid disk gate valve)
,
f'
. . . - . - . - --.- - - - _ . - -
-- - .
- -
- . - . - . -
. -
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!
i
-
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16
- V70-19A
Service water (SW) supply header cross-connect (24-inch
.
+
l
Walworth solid disk gate valve)
!
V70-20
SW turbine building supply isolation (20-inch Walworth solid
-
l
disk gate valve)
b.
. Opservations and Findinas
!
Commitments to GL 96-05 (Tl 2515/140. Paraaraoh 03.01)
VY indicated that it had not committed to the JOG program because of differences
between the interim MOV static diagnostic test program being implemented at
Vermont Yankee and the interim program recommended by the JOG. The licensee
did not specify any significant objections to the other two phases of the JOG program;
i.e. the five-year dynamic test program or final periodic test program. The licensee is
suppoding the JOG program by conducting periodic dynamic tests of two service
water system valves. VY also committed to review the JOG recommendations and, if
l
necessary, the test results on which they were based, and to incorporate the results
l
of the review into its own program.
VY's attemative periodic verification plan consists of a combination of static and
dynamic diagnostic testing and periodic maintenance activities. The periodicity of
these activities is based on MOV risk significance, reliability and margin, operating
.
conditions, and the results of the performance tracking and trending program. VY
l-
intends to implement its program using the methodology described in American
Society of Mechanical Engineers (ASME) Code Case OMN-1, " Alternate Rules for
,
L
Preservice and Inservice Testing of Certain Electric Motor Operated Valve
,
Assemblies In LWR Power Plants," OM-Code-1995 Edition; Subsection ISTC.
1
GL 89-10 Lona-Term Actions (Tl 2515/140. Paraaraoh 03.02)
In Inspection Report (IR) 50-271/97-08, the NRC closed its review of the program
implemented by VY Jn response to GL 89-10, " Safety-Related Motor Operated Valve
Testing and Surveillance," based on the licensee's actions to verify the design-basis
capability of its safety-related MOVs. The IR enumerated four long-term actions in
'
support of GL 89-10 program closure, including: (1) update the current MOV program
plan to ensure that a process is in place to incorporate future test results into design
calculations; (2) reviss existing design calculations to reflect statistically derived data
from dynamically tested valves; (3) apply bounding rate of loading data from
'
previously tested globe valves to non-testable globe valves; and (4) complete the
l
Electric Power Research Institute's Performance Prediction Methodology on all
!
applicable non-tested valves and apply the resulting differential pressure thrust
values, if higher than previously calculated, in the determination of design-basis
torque switch settings.
E
in letters, dated March 2,1998 and March 30,1998, VY notified the NRC that the
'
actions had been completed. The inspectors verified through review of selected
calculations and procedures that the commitments had been met, with one exception.
Design calculation VY 98-006, " Component Level Review of Service Water (SW)
MOVs for Generic Letter 89-10," was not updated following dynamic testing of valves
..
-, . - _
-
- - . -
-
-
.-. -
--
. _ _ _ . _ _ _ . _ - _..
_ _ . . _
_ _ _ _ _ _ _ _ _
.
_
. _ _ _ . . _
,
4 .
I
.
4
'
17
l
V70-19A and V70-20 in April 1998. In both cases, the new valve factors were
-
higher than those assumed in the design calculation of record. At the time of the
.
tests, the licensee informally evaluated the operabiliiy of the valves prior to returning
them to service. However, no formal operability determination, such as an
,
engineering evaluation conducted under Quality Assurance program controls, was
i
'
documented for the valves, and the need to revise the design calculations was not
'
captured in an established (e.g. engineering work or corrective action) tracking
system. Rather, the licensee informally prioritized the need to update the design
l
calculations on the basis of other work priorities and available resources.
l
The new valve factors render the current torque switch setup windows non-
'
conservative, which could result in setting the torque switches incorrectly in the
future. While W's practice of setting torque switches high in the allowable band and
l
bypassing the torque switches to the 99% closed position ameliorate the condition,
l
the current calculation of record for the valves does not reflect the actual plant
'
]
configuration. The inspectors considered the licensee's informal approach to revising
the valve design calculation to be a weakness in design control and configuration
l
management.
.
5
GL 96-05 Proaram (Tl 2515/140. Paraoraoh 03.03)
i
j.
In a November 15,1996 letter to the NRC, W stated that its GL 96-05 program,
'
. including implementing procedures and guidelines, would be established by
December 31,1997. In its November 3,1997 letter, the licensee stated the intention
to have the periodic verification program documentation completed by July 30,1998.
'
While progress had been made in developing procedures and schedules, W's
program documentation was not fully developed. The licensee attributed the
condition to resource constraints and did not offer a date by which the entire program
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as described in its March 13,1997 letter to the NRC would be in place. The
inspectors' findings for specific aspects of W's GL 96-05 program were as follows:
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Scooe of MOVs included in the Prooram
The MOVs included in the periodic verification program were the same 85 valves as
those selected for the GL 89-10 program. This scope is consistent with the
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recommendations of GL 96-05.
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MOV Desian Basis
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Procedure AP 6041, " Vermont Yankee Engineering Evaluations of MOV Dynamic
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Testing and Feedback of Results into MOV Component Calculations," states that
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inputs to MOV component calculations are revised after test data has been obtained
from dynamic testing. However, there were no administrative guidelines governing
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how soon after testing the revisions are to be performed, or formal mechanisms to
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track the need to revise the calculations.
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Dearadation Rate for Potential increase in Thrust or Toraue Ooeratina Reauirements
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Dynamic test information on the potential effects of aging is needed to establish the
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rate at which the thrust required to operate gate and globe valves and the torque
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required to operate butterfly valves might increase with time. The licensee conducted
repetitive dynamic tests of service water system valves V70-19A and V70-20 in April
1998 as part of its participation in the JOG test program. However, the licensee has
not established a process to obtain information regarding degradation of the thrust
and torque operating requirements for other MOVs in its GL 96-05 program based on
appropriate periodic dynamic tests. Thus, site-specific degradation rates must be
developed and justified. The licensee indicated that its basis for establishing
degradation rates for MOV operating requirements will be evaluated and addressed
' in future program documentation.
Dearadation Rate for Potential Decrease in MOV Motor Actuator Outout
VY uses procedures OP 5219, " Diagnostic Testing of Motor Operated Valves," and
AP 6041," Vermont Yankee Engineering Evaluations of MOV Dynamic Testing and
Feedback of Results into MOV Component Calculations," to monitor potential
degradation of motor-actuator performance. Parameters affecting motor-actuator
output under static and dynamic conditions in both the opening and closing
directions, such as stem friction coefficient, motor current, load sensitive behavior,
and dynamic margin are trended. In accordance with Vermont Yankee Tracking item
. # Vendor-98013, VY is addressing new information on alternating current (AC)
powered motor actuator output provided in Limitorque Corporation Technical Update
98-01. Limitorque also noted in Supplement 1 of the technical update that new
guidance is being considered for predicting direct current (DC) powered motor
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actuator output. The licensee was proactive in incorporating industry information on
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motor actuator output by specifying the use of pullout efficiency in MOV sizing
calculations, as described in procedure AP 6038," Component Level Review of
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Vermont Yankee Motor-Operated Valves." in a sample review, the inspectors
confirmed that the licensee used pullout efficiency in its MOV calculations. VY's
review of other information contained in the Limitorque update, such as the use of
application factor and evaluation of specific MOV configurations, was ongoing, with
an assigned completion date of December 20,1998. Based on the available MOV
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capability margins, the inspectors did not identify any immediate operability concerns
resulting from the Limitorque update.
VY was developing a means to monitor motor-actuator performance degradation and
evaluating Limitorque information on motor actuator output capability. However, the
precise process for determining motor-actuator output and rates of degradation in
static and dynamic performance was not fully developed.
Periodic Test Method
VY's proposed program relies heavily on testing its MOVs under static conditions
using diagnostic equipment installed at the motor control centers (MCCs) at intervals
based primarily on risk significance. The licensee has implemented an actuator
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motor test program and undertaken a project in cooperation with CRANE MOVATS,
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incorporated to develop the equipment and software for an MCC-based diagnostic
system for DC-powered MOVs. MCC data will be verified at much longer intervals by
direct thrust / torque measurements at the valves. Current plans call for obtaining
static MCC data from high-risk MOVs every refueling outage and from medium and
low-risk MOVs every other outage. Static diagnostic testing data directly at the MOV
tentatively is scheduled for up to once every eight outages (i.e.12 years).
The inspectors compared VY's method of ranking MOVs with respect to risk
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significance with the methodology described by ti.e Boiling Water Reactor Owners
Group (BWROG) in Topical Report NEDC 32264, " Application of Probabilistic Safety
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Assessment to Generic I etter 89-10 Implementation," and the NRC safety evaluation
dated February 27,1996, accepting the BWROG methodology with certain conditions
and limitations. For example, the inspectors reviewed the licensee's use of
importance measures, consideration of common cause failure, and expert panel
oversight. The inspectors also compared the MOVs identified at Vermont Yankee as
risk significant to the composite list developed by the BWROG, and reviewed the
basis for the limited differences in those lists. The inspectors found the licensee's
risk rankings to be reasonable.
In summary, VY's methods of identifying age-related degradation affecting operating
thrust / torque requirements and motor-actuator output were still being developed at
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the time of the inspection. Development of new diagnostic equipment for remote
testing of DC-powered MOVs is a noteworthy initiative. Several aspects of the GL 96-05 program were not dully developed, such as: (1) validation of MCC-based
diagnostic equipment, particular!y for de-powered MOVs, (2) validation that the
proposed long-term test method will detect degradation under dynamic conditions, (3)
justification of test intervals that exceed ten years, and (4) finalization of test
schedules. These aspects of the licensee's periodic verification program will be
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revisited during the final review of the Vermont Yankee GL 96-05 program by the
NRC Office of Nuclear Reactor Regulation (NRR).
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MOV Performance Evaluation
As noted earlier, procedure AP 6041 provides for the evaluation of dynamic test data
and its feedback into design calculations. Procedures PP 7004, " Vermont Yankee
Nuclear Power Station Motor Operated Valve Program," and DP 0210, " Tracking and
Trending Program," provide guidance for the review and trending of MOV failures
and static and dynamic diagnostic test results every two years . Valve deficiencies
and failures also are included. The primary performance parameters that are trended
are unseating thrust, thrust of close control switch trip (CST), total close thrust,
average running thrust and motor current, stem friction at close CST and backseating
thrust (if any). Significant differences from previous tests are noted and additional
parameters may be chosen for review as necessary. For the selected valves, the
inspectors reviewed the most current (1996) diagnostic testing trend report. The
report was comprehensive and contained a considerable amount of test data for each
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valve. No performance anomalies or adverse trends over the previous two years
were noted, and causes of significant performance differences were evaluated and
discussed.
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MOV Test interval
VY is considering a static diagnostic test program that combines frequent data
acquisition from the MCCs supplemented periodically by comparison with data taken
directly at the MOVs to assure design-basis capability between scheduled tests. As
an alternative to committing to the JOG program, the licensee must establish its own
long-term periodic test methods and intervals for establishing thrust / torque
degradation rates for each MOV in order to satisfy GL 96-05. The licensee plans to
monitor potential degradation of motor-actuator output through static and dynamic
testing. VY's technical justifications for its long-term MOV periodic test methods and
intervals were still under development. When the GL 96-05 program documentation
is prepared, NRR will review the licensee's methods for monitoring parameters to
ensure adequate capability between normally scheduled tests.
c.
Conclusions
Within the scope of the review performed on site, the inspectors concluded that the
actions to date by VY concerning periodic verification of long term MOV capability
were acceptable. The NRC Office of Nuclear Reactor Regulation will use this
information in preparing a safety evaluation on VY's response to GL 96-05. Positive
aspects of the periodic verification program were observed, including: (1)
development of more efficient test techniques,(2) implementation of a motor test
program, and (3) an aggressive motor-actuator lubrication and refurbishment
schedule. However, several aspects of the periodic verification program, such as
program documentation and MOV performance degradation rates, as yet were
incomplete. Design-basis thrust calculations for two MOVs were not revised to reflect
dynamic test information, resulting in the calculations not reflecting the actual plant
configuration. This condition was an example of poor configuration management.
E2
Engineering Support of Facilities and Equipment
E2.1
Scram Discharae Volume Drain Valve Failures
a.
Insoection Scope (62707,37551)
On December 6, containment isolatici vdve CRD-33D, the outboard drain isolation valve
for the south scram discharge volume 60V), failed to shut during a quarterly inservice
test. Following the repair of CRD-33D, VY initiated increased frequency testing for all four
SDV drain valves, pending a final root cause determination. On December 11, a second
SDV drain valve, CRD-33B, failed to shut within the required time and was declared
inoperable. The inspector examined VY's corrective actions and cause determination for
these failures.
b.
Observations and Findinas
The SDV is considered an extension of the primary containment and TS 3.7.2 requires the
SDV drain line to bc isolated if one of its automatic isolation valves is inoperable.
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However, because of minor HCU valve leakage, water accumulated in the south SDV and
required compensatory operator actions to keep the SDV drained.
The inspector reviewed VY's immediate actions to address the individual valve failures.
Compensatory actions were initially adequate and later were enhanced after W was self-
critical of the process used to implement the compensatory actions. There are three main
control panel indications that allow operators to monitor the SDV level when the drains are
isolated. This was the situation while the corrective actions were being planned and
implemented. The inspector concluded that the operators were provided with adequate
guidance and information to implement the compensatory measures.
The vent and drain valves for the north and south SDVs were modified during the 1998
refueling outage to resolve a long standing problem of corrosion products impacting the
valves' ability to meet pressure test acceptance criteria. VY selected new ball valve and
air operator pairs from BW/IP International based on the performance of similar ball valve
configurations in other plant applications. The new valves and actuators were installed
under an engineering design change, EDCR 97-410 with a 50.59 safety evaluation.
The inspector reviewed EDCR 97-410 and made the following observations:
The procurement specification provides no details regarding the cundition of the
process flow (i.e., intermittent water and air with corrosion products).
The safety evaluation states the new drain valves require a maximum torque of s
360 in-lbs (30 ft-lbs) to actuate and the vendor supplied valve data sheet shows a
required stem torque of 110 ft-Ibs.
W did not independently evaluate design aspects of matching the valve torque
requirements to the actuator capability and did not require documentation of this
activity in the purchase specification. Calculations and certification for other critical
design information such as closure time, seismic capability and material
traceability were required from the vendor.
The inspector concluded that the design change process failed to identify the
inadequate valve to actuator sizing for this application, pricr to installation of the
modification and subsequent failures while in service. Additionalinformation from
W is necessary to assess whether the process or its implementation was the
cause of this failure. Also, additional information is necessary for the inspector to
assess W's review of 10 CFR 21, Reporting of Defects and Noncompliance,
applicability.
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On December 14, W reported the problems observed with the SDV drain line
isolation valves based on the common mode failure mechanism and the reporting
requirements of 10 CFR 50.72. As such, a Licensee Event Report is expected
based on the parallel reporting requirements of 10 CFR 50.73.
10 CFR 50 Appendix B, Criterion Ill, " Design Control," requires, in part that
measures be established for the selection and review for suitability of application of
equipment that are essential to the safety related functions of systems and
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components. In accordance with the guidancc provided in NRC Enforcement
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Guidance Memorandum 98-006, this issue, which may represent a violation of
NRC requirements will remain open for a reasonable time to all the licensee to
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develop its corrective actions. (eel 98-14-04: Design Control For SDV Valve
Modification)
c.
Conclusions
The inservice test failures of two scram discharge volume drain valves led to the
identification of problems with the new valve / actuator design installed during the 1998
refueling outage. Errors were identified in the safety evaluation and there is a lack of
design information from the vendor. in accordance with NRC guidance, this issue, which
may represent a violation of NRC requirements will remain open for a reasonable time to
allow the licensee to develop its corrective actions.
E8
Miscellaneous Engineering issues
E8.1
Review of Open items (92903)
The following open items were reviewed for closure based on a review of additional
information from VY and a sampling of the licensee's corrective actions.
iClosed) URI 98-80-08: Complete Review of February 25,1998, Submittal
This item was opened because a VY submittal dated February 25,1998, (BVY 98-22)
incorrectly identified a dose criteria associated with the designation of structures, systems,
or components as Safety Class 3. A VY contractor study, dated February 6, identified the
dose criteria in the VY Safety Class Manual (reflected in the February 25 VY letter)
conflicted with the ANS 22 dose criteria required by the NRC-approved Operational
Quality Assurance Program.
Based on a review of VY's February 25,1998, letter, the inspector determined that the
ANS 22 dose criteria for classification of equipment was confused with the licensing basis
dose limit for abnormal operational occurrences listed in FSAR Chapter 14.2. In a letter
dated April 10,1998, VY retracted its February 25,1998, submittal to the NRC regarding
Revision 28 of the Operational Quality Assurance Program. VY initiated an Event Report
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to evaluate the impact of the dose criteria misunderstanding and appropriate initial actions
were taken. Violation 50-271/98-80-07 was previously issued for the licensee's reduction
in Quality Assurance commitments without prior NRC approval. The incorrect information
was retracted by VY and therefore, the inspector concluded that no violation of NRC
requirements existed. This item is closed.
E8.2
Review of VY Cycle 19 Ooere*jna Report
By letter dated December 1,1998, the licensee submitted the Vermont Yankee Cycle 19
Operating Report in accordance with 10CFR50.59(b)(2) and 10 CFR50.4. This report
contains a brief description of the changes, tests, and experiments, including a summary
of the safety evaluation of each, which were conducted between November 2,1996 and
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June 1,1998. An in-house review of this report was conducted by the NRR Project
Manager. The report described the changes, tests, and experiments in sufficient detail to
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support the licensee's conclusion that the changes did not involve unreviewed safety
questions. No concerns were identified during the review.
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IV. Plant Support
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P3
EP Procedures and Documentation
P3.1
in-Office Review of Emeraency Plan Imolementina Procedures (82701)
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The inspector reviewed recent changes the licensee made to its Emergency Plan
Implementing Procedures in the NRC Region I office.
Based on the licensee's determination that the changes do not decrease the overall
effectiveness of its emergency plan, no prior NRC approval is required in accordance with
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10 CFR 50.54(q). After a limited, in-office review of the changes, the inspector concluded
that these changes were made in accordance with the provisions of 50.54(q).
Implementation of these changes will be subject to future on-site inspection effort to
confirm that the changes have not decreased the effectiveness of the licensee's
emergency plan. A list of the changes reviewed are included as an attachment to this
report.
V. Management Meetings
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Exit Meeting Summary
The resident inspectors met with licensee representatives periodically throughout the
inspection and following the conclusion of the inspection on January 26,1998. At that
time, the purpose and scope of the inspection were reviewed, and the preliminary findings
were presented, in addition, visiting inspector debriefed with the licensee prior to leaving
the cite. The licensee acknowledged the preliminary inspection findings.
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The Inspector asked the licensee whether any material examined during the inspection
should be considered proprietary. No proprietary information was identified.
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ATTACHMENT 1
List of Acronyms Used
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ACS
Alternate Cooling System
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American National Standard
Area Radiation Monitor -
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.BMO
Basis for Maintaining Operation
Boiling Water Reactor Owners Group
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CFR
Code of Federal Regulations
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. CIV
Containment isolation Valve'
CRD ~
, Control Rod Drive
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EDCR
Engineering Design Change Request
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ER
' Event Report
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FME-
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- Final Safety Analysis Report
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GL~
Generic Letter
.HCU
Hydraulic Control Unit
High pressure coci
.Mjection
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'IFl
inspector Follow-up R,m .
IR(s)
Inspection reports (s)
IST -
Inservice Test
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LCO
Limiting Condition for Operation
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LER
Licensee Event Report
Loss of Coolant Accident
Motor Control Center
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MOV-
Motor Operated Valve
NRC
Nuclear Regulatory Commission
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NRC Office of Nuclear Reactor Regulation
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NUMARC Nuclear Management and Resources Council
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QA .
Quality Assurance
QC -
Quality Control
Reactor core isolation cooling
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Residual Heat Removal Service Water
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.RP
Radiation Protection
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SDC'
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SOV(s) -
Solenoid-operated valve (s)
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- Attachment 1 (continued) '
List of Acronyms Used
!SSC
Structure, System, or Component
TS
Technical Specifications
Unresolved item
VDC'
Volts Direct Current
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Violation
Vermont Yankee
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ATTACHMENT 2
Items Opened, Closed, or Discussed
Opened
IFl 98-14-03: MOV Torque Switch Failure - Final Resolution (page 11)
eel 98-14-04: Design Control For SDV Valve Modification (page 22)
Closed
LER 98-020-01: Inadequate Equipment Control Practices Result in Two Mispositioned Isolation
Valves Allowing Degradation of Primary Containment integrity (page 3)
LER 98-019-00: Off-Normal System Alignment Following a Plant Trip Which involved the Loss of
a Reactor Water Recirculation System Pump and Reactor Water Thermal Stratification
Results in a Spurious Shutdown Cooling isolation (page 4)
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LER 98-017-00,01: Inadequate Design Package and implementing Procedure Results in
Redundant Trains of the Standby Gas Treatment System with Fan Supply Breaker Trip
Setpoints Potentially Attainable with Normal Start in-Rush Current (page 14)
LER 98-021-00: Inadequate Licensing Basis Documentation Retrievability Results in the Failure
to Meet IST Requirements for Diesel Fuel Oil Day Tank Level Control Valves (page 14)
VIO 98-08-02: Design Settings Not Translated into Installation Procedures for SGTS Breakers
(page 15)
URI 98-80-08: Complete Review of February 25,1998, Submittal (page 22)
Non-cited Violations
NCV 98-14-01: SGTS Maintenance Procedure Implementation (page 7)
NCV 98-14-02: HPCI Steam Line Low Pressure Isolation Instrument Isolated (page 8)
e
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ATTACHMENT 3
Emergency Response Plan and implementing Procedures Reviewed
Procedure
Title
Rev.No.
OP-3504
Emergency Communications
30,D1
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98-413
OP-3505
Emergency Preparedness Exercises and Drills
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OP-3506
Emergency Equipment Readiness Check
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OP-3508
On-Site Medical Emergency Procedure
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OP-3513
Evaluation of Off-Site Radiological Conditions
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98-372
OP-3524
Emergency Actions to Ensure Initial Accountability and Security
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Response
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OP-3531
Emergency Call-in Method
11,DI
98-414
OP-3532
Emergency Preparedness Organization
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OP-3534
Post Accident Sampling of Plant Stack Gaseous Releases
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