ML20151C157
ML20151C157 | |
Person / Time | |
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Site: | Vermont Yankee File:NorthStar Vermont Yankee icon.png |
Issue date: | 04/05/1988 |
From: | Haverkamp D NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
To: | |
Shared Package | |
ML20151C143 | List: |
References | |
50-271-88-03, 50-271-88-3, NUDOCS 8804120190 | |
Download: ML20151C157 (22) | |
See also: IR 05000271/1988003
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U. S. NUCLEAR REGULATORY COMMISSION
Region I
Report No.
50-271/88-03
Docket No.
50-271
License No. DPR-28
Licensee:
Vermont Yankee Nuclear Power Corporation
RD 5. Box 169
Brattleboro, Vermont
05301
Facility:
Vermont Yankee Nuclear Power Station
Inspection At: Vernon, Vermont
Inspection Conducted:
February 9, 1988 - March 21, 1988
Inspectors:
Geoffrey E. Grant, Senior Resident Inspector
John B. Macdonald, Resident Inspector
James E. Kau her, Project Engineer
Approved By:
/
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N/M
Donald R.'Haverkamp,
ef "
/ 06te
Reactor Projects Sect; n No. 3C
Inspection Summary:
Inspection on February 9, 1987 - March 21, 1988
(Report No. 50-2'71/88-03)
Areas Inspected:
1.
Routine inspection on daytime and backshif ts by two resident inspectors
(210 hours0.00243 days <br />0.0583 hours <br />3.472222e-4 weeks <br />7.9905e-5 months <br />) of:
actions on previous inspection findings;
routine plant
operations; physical security; licensee potentially reportable occurr-
ences; licensee event reports; operational events; maintenance activities;
cere spray weld overlays; licensee response to NRC initiatives; and
periodic reports.
2.
Safety Issue Management System (SIMS) item number 41 (MPA B-58) on scram
discharge volume capability was closed out through performance of TI
2515/90.
8804120190 880401
ADOCK 05000271
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Inspection Summary (Continued)
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Results:
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1.
General Conclusions on Adequacy, Strength or Weakness in the Licensee's
Program
Based upon the number of long outstanding unresolved issues that were able
to be closed out during this report period, it is apparent that the licen-
see has been successful in improving tracking, resolution and documenta-
tion of these items (Section 3.0).
The licensee approach to and interim resolution of Local Power Range
Monitor (LPRM) spiking problems exhibited thoroughness and sound engineer-
ing judgement (Section 8.1).
The licensee demonstrated strong short-notice maintenance planning and
implementation during the March 18-19, 1988 power reduction (Section
9.1).
2.
Violations
One violation was identified concerning failure to meet the limiting con-
dition for operation in Technical Specifications 3.9.A.1 and Table 3.9.1
concerning requirements for obtaining 24-hour grab samples of the service
water system when the effluent radiation monitor was inoperable (Section
6.0).
3.
New Unresolved Items Identified
The licensee program for identifying, analyzing and reporting plant
occurrences is weak in some areas.
Adequate investigation to determine
reportability of plant events is sometimes lacking. Occasional lapses in
application of reporting requirements by plant personnel have led to non-
conservative, incorrect determinatior.s.
This area is unresolved pending
licensee improvements.
Related to the review of this area was an unre-
solved item addressing the reportability of operations with a service
water (SW) effluent radiation monitor having insufficient sensitivity in
some operational modes (Sections 6.0 through 6.3).
The licensee must resolve the conflict between existing TS requirements
and procedures regarding surveillance testing of reactor vessel head spray
isolation valves RHR-32 and RHR-33 (Section 6.4).
The licensee 1987 Annuai Operating Report did not include all of the
information required by 10 CFR 50.59 and is an unresolved issue pending
licensee review and corrective actions (Section 12.0).
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TABLE OF CONTENTS
PAGE
1.
Persons Contacted. . . . . .
1
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2.
S umma ry o f Fa c i l i ty Ac t i v i t i e s . . . . . . . . . . . .
1
3.
Status of Previous Findings (IP 92701)*. . . . . . . .
2
3.1 (Closed) Follow Item 83-21-03:
NRC Review of Clarification of the Licensee
Response to Item 3.0 of IEB 80-08 . . , . . . . .
2
3.2 (Closed) Unresolved Item 83-17-10:
Service Water System Safety Evaluation. .
2
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3.3 (Closed) Follow Item 84-10-02:
Torus and CST TS Level Setpoint Changes . . . . .
2
3.4 (Closed) Follow Item 84-01-02:
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HPCI and RCIC Steamline Drain Valves. . . . . . .
2
3.5 (Closed) Unresolved Item 84-12-01:
Stack Gas Instrumentation Problems,
. . . . . .
3
3.6 (Closed) Unresolved Item 84-22-02:
Emergency Lighting for Alternate Shutdown . . . .
3
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3.7 (Closed) Unresolved Item 85-20-08:
Testing of the Health Physics Notification
Network (HPN) at the New Emergency Operating
Fa c i l i ty ( EO F) . . . . . . . . . . . . . . . . . .
3
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3.8 (Closed) Unresolved Item 85-18-05:
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Invalidated Environmental Qualification (EQ) of
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Conri Assemblies Containing Teflon in the Pottin
Compound. . . . . . . . . . . . . . . . . . . . g
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3.9 (Closed) Follow Item 85-02-01:
Review of Applicability of IEN 84-86. . . . . . .
4
3.10 (Closed) Follow Item 84-26-04:
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Review of New Revision to LP 3126, Shutdown
Using Alternate Methods . . . . . . . . . . . . .
4
3.11 (Closed) Unresolved Item 85-14-07:
Review of Nitrogen Inerting System.
4
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4.
Operational Safety (IP 71707, 71710, 61726). . . . . .
4
4.1 Plant Operations Review .
4
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4.2 Safety System Review .
5
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4.3 Feedwater Leak Detection System .
5
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4.4 Inoperable Equipment.
6
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4.5 Review of Lif ted Leads, Jumpers and Mechanical
Bypasses. . . . . . . . . . . . . . . . . . . . .
6
4.6 Review of Switching and Tagging Operations. . . .
6
4,7 Operational Safety Findings . .
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Table of Contents (Continued)
PAGE
5.
Observations of Physical Security (IP 71707) . . . . .
7
6.
Reportable Occurrence Review (IP 50712, 90714) . . . .
7
6.1 Requirements. . . . . . . . . . . . .
7
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6.2 Service Water System Effluent Radiation Monitor
Inoperability - PRO 87-38 . . . . . . . . . . . .
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6.3 Post Maintenance Operability Testing of Valve
V10-39A - PRO 87-60 . . . . . . . . . . . . . . .
10
6.4 Missed Surveillance - PRO 88-012. . . . . . . . .
11
6.5 Summary of Findings . . . . . . . . . . . . . . .
12
7.
Licensee Event Reporting (LER) (IP 92700). . . . . . .
12
8.
Operational Event Review (IP 71707, 61726) . . . . . .
12
8.1
Local Power Range Monitor Spiking Problems. . . .
12
9.
Review of Maintenance Activities (IP 62703). . . . . .
13
9.1 Preplanned Power Reduction to Accomplish
Scheduled Maintenance . . . . . . . . . . . . . .
13
10.
Core Spray Safe End Nozzle Weld Overlays (IP 92703). .
14
11.
Review of Licensee Response to NRC Initiatives:
(IP 92703, 25590). . . . . . . .
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15
11.1 TI 2515/90:
Scram Discharge Volume Capability.
15
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11.2 RI TI 88-01:
Fitness for Duty Program.
17
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12.
Review of Periodic and Special Reports (IP 90713). . .
17
13. Management Meetings (IP 30703, 40700), . . ,
. . . .
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- The NRC Inspection Manual inspection procedure (IP) or temporary instruction
(TI) or the Region I temporary instruction (RI TI) that was used as
inspection guidance is listed for each applicable report section.
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DETAILS
1.
Persons Contacted
Interviews and discussions were conducted with members of the licensee
staff and management during the report period to obtain information per-
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tinent to the areas inspected.
Inspection findings were discussed
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periodically with the management a-d supervisory personnel listed below.
Mr. P. Donnelly, Maintenance Superintendent
- Mr. R. Grippardi, Quality Assurance Supervisor
- Mr. S. Jefferson, Assistant to Plant Superintendent
Mr. G. Johnson, Operations Supervisor
Mr. R. Lopriore, Maintenance Supervisor
Mr. R. Pagodin, Technical Services Superintendent
- Mr. J. Pelletier, Plant Manager
- Mr. R. Wanczyk, Operations Superintendent
Mr. T. Watson, I & C Supervisor
- Attendee at post-inspection exit meeting conducted on March 29, 1988.
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2.
Summary of Facility Activities
Vermont Yankee Nuclear Power Station (VYNPS) continued full power opera-
tions during this period except for pre planned power reductions to accom-
plish required surveillances and a rod pattern exchange.
An unplanned
power reduction to 75% of rated power was conducted on March 11, 1988 in
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order to isolate a feedwater heater string to effect repairs on a leaking
The repairs were partially effective and the plant was returned
to full power. Further repairs may be necessary if the leak worsens. The
Institute for Nuclear Power Operations commenced a two-week evaluation of
VYNPC activities on March 14, 1988. A planned downpower to 55% of rated
power on March 19, 1988 included a drywell entry to inspect for the cause
of slightly elevated drywell leakage.
Other maintenance activities were
also performed.
An NRC Region I team completed a review of VYNPC compliance with the
requirements of 10 CFR Part 50, Appendix R during the period of
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February 8-11, 1988 (Inspection Report 88-04).
During the periods March 1-4 and 8-11, 1988, the Resident Inspector
participated in NRC technical training.
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3.
Status of Previous Inspection Findings
3.1 (Closed) Follow Item 83-21-03:
NRC Review of Clarification of the
Licensee Response to Item 3.0 of IEB 80-08.
Item 3.0 of IEB 80-08
stated that for plants which were committed during construction to
perform volumetric examination of certain penetrations on which
radiographic examination was not performed, to justify not performing
radiography or submit plans and schedules to perform radiography.
The licensee has responded that the containment penetrations were
fabricated and installed in accordance with the 1968 Edition of the
ASME Code,Section III. This code edition did not require volumetric
examination to be performed when radiography was not performed and
therefore the requirements of Item 3.0 of IEB 80-08 an not appli-
cable to VYNPS. The inspectors had no further questions.
This item
is closed.
3.2 (Closed)
Unresolved
Item
83-17-10:
Service Water System Safety
Evaluation.
The inspector reviewed procedure OP 2181,
"Service
Water / Alternate Cooling Operating Procedure", Revision 16, and verif-
ied that the service water system crossconnect valve to the fire
system (SW-8) is controlled closed during normal system configura-
tion. Manipulation of valve SW-8 for the purpose of crossconnection
or isolation of the service water and fire systems is directed by
Section K of OP 2181. Normal system configuration with SW-8 closed
is verified in Appendix A.
This item is closed.
3.3 (Closed)
Follow
Item
84-10-02:
Torus and CST TS Level Setpoint
Changes. On October 9,1985, the NRC issued Amendment No. 90 to the
operating license for VYNPS.
This amendment permitted, in part, the
licensee to revise the condensate storage tank (CST) low level switch
f rom "2 inches" to
"3*." in TS Table 3.2.1.
The setting change was
required as a result of the replacement of level instrumentation from
a mechanical float assembly to analog instrumentation which changed
the zero reference level.
The setpoint change from 2 inches to 3%
does not affect actual CST water level.
The torus high water level
switch for automatic HPCI suction transfer from the CST to the torus
was deleted from TS Table 3.2.1, as a result of the Browns Ferry Unit
1 Station Blackout concerns of NUREG/CR-2182, Vol. I.
This item is
closed.
3.4 (Closed) Follow Item 84-01-02: HPCI and RCIC Steamline Drain Valves.
The HPCI steamline drain valves (V23-42 and V23-43) and the RCIC
steamline drain valves (V13-34 and V13-35) were incorrectly identi-
fied in FSAR TABLE 7.3.1 as containment isolation valves.
The cur-
rent FSAR revision has been corrected and these valves have been
removed from FSAR TABLE 7.3.1.
This item is closed.
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3.5 (Closed)
Unresolved
Item
84-12-01:
Stack Gas Instrumentation
Problems.
On June 17, 1984 the licensee determined that both stack
gas instrument channels were inoperable.
The licensee reported the
detector problems to the NRC in LER 84-10, dated July 16, 1984. Stack
gas monitor I had a faulty circuit board in the detector control cir-
cuitry which was repaired.
Stack gas monitor II had a gamma sensi-
tive aluminum window vice a beta sensitive mylar window.
A new
detector was installed and the channel was recalibrated. The inspec-
tors have reviewed the event and have no further questions.
This
item is closed.
3.6 (Closed) Unresolved Item 84-22-02:
Emergency _ Lighting for Alternate
Shutdown.
During a 1984 walkthrough of OP 3126, "Shutdown Using
Alternate Shutdown Methods", an NRC inspector roted several plant
locations where increased emergency de lighting was necessary.
The
licensee reviewed the finding and approved the lighting upgrades
recommended in plant alteration review (PAR) 84-08.
Specifically,
emergency lighting was enhanced in the MCC 9B electrical pressure
regulator cabinet area, the RCIC corner room, the A diesel generator
rcom, the east switchgear room and the torus area between the RCIC
corner room and the HPCI room.
The inspectors had no further ques-
tions.
This item is closed.
3.7 (Closed)
Unresolved Item 85-20-08:
Testing of the Health Physics
Notification Network (HPN) at the New Emergency _ Operations Facility
(E0F). The inspectors reviewed procedure GP 3506, "Emergency Equip-
_
ment Readiness Check," revision 20, to ensure it directs that the HPN
network is tested for operabilty monthly at the E0F and recovery
center.
This item is closed.
3.8 (Closed)
Unresolved
Item
85-18-05:
Invalidated Environmental
Qualification (EQ) of Conax Assemblies Containing Teflon in the
_On May 16, 1985 the licensee was notified by Conax
. Potting Compound.
Buffalo Corporation that some electrical penetrations supplied to
VYNPS by Conax contained teflon insulation and sealant material.
The
presence of teflon, which is highly susceptible to degradation from
radiation exposure, invalidates penetration environmental qualifica-
tion.
A licensee investigation determined that only four penetra-
tions on the outboard bulkhead of the containment personnel airlock
were affected.
The penetrations did not contain any safety class
electronic circuitry.
Failure of these outboard penetrations would
not have resulted in any additional release of radioactivity because
the containment boundary would be established by the inner personnel
airlock.
The licensee reported this material defect to the NRC, in
accordance with the requirments of 10 CFR 21, via correspondence FVY
85-57 dated June 19, 1985. The affected penetrations were replaced
during the first refueling outage following discovery of the issue.
The replacement was performed under MR 85-1363 and was completed on
January 27, 1986.
The inspectors had no further questions.
This
item is closed.
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3.9 (Closed) Follow Item 85-02-01:
Review of Applicabilty of IE Notice
(IEN) 84-86. This notice addressed inadequate isolation between pro-
tection system and non-safety system signals detected during computer
testing.
The licensee evaluation of this Notice concluded that
potential changes in instrument current loops due to computer sam-
pling of mercury-wetted relay failures does not apply at VYNPS. Mon-
itoring of the RPS is accomplished by indirect measurements provided
by auxiliary outputs from Rosemount analog trip units.
This signal
is an electrical duplication of the actual loop current output. The
inspector had no further questions.
This item is closed.
3.10(Closed) Follow Item 84-26-04:
Review of New Revision to OP 3126,
"Shutdown Using Alternate Methods".
The inspectors reviewed revision
3 to OP 3126 issued February 5,1983.
The inspectors observed that:
precautions are highlighted and detailed in that expected plant
respcnses to manual actions are described; immediate actions prior to
abandonment of the control room included manually scramming the
reactor, opening HPCI-24, closing at least one MSIV per steam line
and placing the ADS inhibit switch to bypass if possible; and, en-
hanced detailed riirections have been provided to accomplish a reactor
level trip using the Rosemont trip units.
The licensae has elected
not to direct the shif t supervisor to a specific location in the
event a remote plant shutdown must be accomolished.
The licensee
believes that, due to the varied control room inaccessability scen-
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arios that can be postulated, directing the shif t supervisor to a
specific location by procedure could potentially limit his effective-
ness.
Therefore, the shift supervisor has been provided the latitude
to assess plant conditions and then proceed to the location in which
his effectiveness would be maximized.
The inspectors had no further
question'.
This item is closed,
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3.11 (Closed)
Unresolved
Item
85-14-07:
Review of Nitrogen Inerting
System.
The inspector reviewed the licensee responses to IEB 84-01
and General Electric SIL No. 402 which address potential torus vent
header cracking due to direct impingement of cold nitrogen (less than
40 F). The VYNPS inerting system is designed such that redundant
cold temperature alarms and cutoff valves isolate the system preven-
ting the injection of cold nitrogen into the torus and drywell.
Fur-
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ther, the nitrogen supply lines are 9'6" off the torus centerline,
therefore, the ringheader and downcomers do not align vertically with
the nitrogen injection port.
The inspectors had no further ques-
tions.
This item is closed.
4.
Operational Safety
4.1 plant Operations Review
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The inspector observed plant operations during regular and backshift
tours of the following areas:
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Control Room
Cable Vault
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Reactor Building
Fence Line (Protected Area)
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Diesel Generator Rooms
Intake Structure
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Vital Switchgear Room
Turbine Building
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Control Room iastruments were observed' for correlatior. between
channels, proper functioning, and conformance with Technical Speci-
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fications.
Alarm conditions in effect and alarms received in - the
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control room were reviewed and discussed with the operators.
Oper-
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ator awareness and response to these conditions were-reviewed. Oper-
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ators were found cognizant of board and plant conditions.
Control
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room and shift manning were compared with Technical Specification
requirements.
Posting and control of radiation, contaminated and
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high radiation areas were inspected.
Use of and compliance with
Radiation Work Permits and use of required . personnel monitoring
devices were checked.
Plant housekeeping controls were observed
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including control of flammable and other hazardous. materials.
During
plant tours, logs and records were reviewed to ensure compliance with
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station procedures, to determine if entries were correctly made, and
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to verify correct communication of equipment status.
These records
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included various operating logs, turnover sheets, tagout and jumper
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logs, and Potential Reportable Occurence Reports. Inspections of the
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control room were performed on weeketds and backshifts including
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February 8-11, 16-19 and March. 1-3, 7-10, 14-18, 1988. Operators and
shift supervisors were alert, attentive and responded appropriately
to annunciators and plant conditions.
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4.2 Safety System Review
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The emergency diesel ~ generators, residual heat removal, core spray,
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residual heat removal service water, and high pressure coolant injec-
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unn systems, were reviewed to verify proper alignment and opera-
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tional staws in the standby mode. The review included verification
that (i) accensible major flow path valves were correctly positioned:
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(ii) power si pplies were energized, (iii) lubrication and component
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cooling was proper, and (iv) components were operable based on a
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visual inspection of equipment for leakage and general conditions.
No violations or safety concerns were identified.
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4.3 Feedwater Leak Detection System Status
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The inspector reviewed the feedwater leakage detection system and the
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monthly performance summary provided by the licensee in accordance
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with VYNPC letter FVY 82-105.
The licensee reported that, based on
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the leakage monitoring data reduced as of February 18, 1988, there
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were no deviations in excess of 0.10 from the steady state value of
normalized thermocouple readings, and no failures in the 16 thermo-
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couples installed on the four feedwater nozzles.
Point number 12,
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which previously had shown a downward (cooling) trend (See Inspection
Report No. 50-271/87-21, Section 4.2), did not continue to exhibit
increased cooling during this evaluation period.
Since the initial
cooling indicated at point #12, the temperature has stabilized and
deviations have decreased.
Because the normalized readings have
returned to near pre-outage values, the licenste has determined that
no instrumentation or leakage problems exist.
No inadequacies were
identified and the inspector had no further questions in this area.
4.4 Inoperable Equipment
Actions taken by plant personnel during periods when equipment was
inoperable were reviewed to verify:
technical specification limits
were met; alternate surveillance testing was completed satisfactor-
ily; and, equipment return to seavice upon completion of repairs was
proper.
This review was completed for the following item:
MG foam fire suppression system was inoperable from February 16
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- March 1,1988.
Deluge Valve DV-300 developed seat leakage
requiring the system to be isolated.
A replacement vahe was
not immediately available and was placed on back order. During
the period of system inoperability, compensatory firewatches
were established in accordance with TS and approved procedures.
Maintenance was performed under '4R 38-0343.
4.5 Review of Lif ted Leads, Jumpers and Mechanical Bypasses
Lif ted lead and Jumper (LL/J) requests and Mechanical Bypasses (MB)
were reviewed to verify that controls established by AP 0020 were
met, no conflicts with the technical specifications were created, the
requests were properly approved prior to installation, and a safety
evaluation in accordance with 10 CFR 50.59 was prepared if required.
Implementation of the requests was reviewed on a sampling basis.
The LL/J 88-0005 authorized February 4,1938 was issued to facilitate
installation of leads within lighting panels to improve the flexibil-
ity and reliability of receptacles in the Chemistry Laboratory in the
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event of a loss of offsite power as well as to provide a regulated
voltage circuit for the laboratory computer system.
Work was per-
formed under work request WR 87-0714.
4.6 Review of Switching & Tagging Operations
The switching and tagging log was reviewed and tagging activities
were inspected to verify plant equipment was controlled in accordance
with the requirements of AP 0140, Vermont Local Control Switching
Rules.
The following switching and tagging orders were reviewed:
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88-0221
issued and restored on March 19, 1988 to reposition
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nitrogen spa:tacle flanges in support of the deinerting of the
drywell.
88-0222 -- issued and restored on March 19, 1988 to preclude inadver-
tent nitregen injections into
the drywell
during
the drywell
inspection,
88-0223 -- issued and restored on March 19, 1988 to support mainten-
ance of the MSIV 86A test solenoid.
Maintenance was performed under
MR 88-0441.
Refer to Section 9.1 for more detail.
4.7 Operational Safety Findings
Licensee administrative control of off-normal system configurations
by the use of LL/J, mechanical bypass, and switching and tagging pro-
cedures, as reviewed in Sections 4.5 and 4.6, was in compliance with
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procedural instructions and was consistent with plant safety.
5.
Observations of Physical Security
Selected aspects of plant physical security were reviewed during regular
and backshif t hours to verify that controls were in accordance with the
security plan and approved procedures. This review included the following
security measures:
guard staffing; vital and protected area barrier
integrity; maintenance of isolation zones; and, implementation of access
controls, including authorization, badging, escorting, and searches.
No
inadequacies were identified.
6.
Reportable Occurrence Review
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6.1 Requirements
Licensee Administrative Procedure (AP) 0010 Revision 18, "Occurrence
Reports", details the necessary steps for determining the reporta-
bility of various classes of plant occurrences and includes proce-
dures for processing of the Potential Reportable Occurrence (PRO)
form. The bases for the spectrum of occurrence reporting require-
ments includes plant technical specifications,10 CFR Parts 20, 21,
50 and 73 (and others), AP 0012, "Notifications and Reports Due", AP
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0028,
"Operating
Experience
Review
and
Assessment / Commitment
Tracking", AP 0156, "Notification of Significant Events", and NUREG 1022.
The aggregate of these requirements and guidelines forms the
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basis for licensee determinations of occurrence r? portability and the
method of reporting.
Licensee procedures AP 0010, AP 0012, AP 0028
and AP 0156 generally contain sufficient detail to aid staff person-
nel in the determination of occurrence reportability, method of
reporting, and internal administrative tracking and processing of
reports.
The inspector reviewed the licensee reporting system, and
screened several PRO forms to determine the effectiveness of occur-
rence review and categorization by the licensee.
Two PRO forms had
deficiencies in event classification and are described below.
6.2 Service Water System Effluent Radiation Monitor Inoperability - PRO
87-38
The subject PRO covered an occurrence where the service water (SW)
system effluent radiation monitor was discovered to have no flow
through it and was therefore inoperable.
Discovery was made on
September 3, 1987 by instrumen+.ation and control (I&C) technicians
who were performing a routine calibration cf the SW effluent radia-
tion monitor flow switch.
Initial investigation found the monitor
system suction lined up to the discharge block (normal lineup) but
the monitor system pump was not running.
In accordance with TS 3.9 A.1, during release through the SW system, the effluent radiation
monitor shall be operable in accordance with TS Table 3.9.1.
Per
Table
3.9.1,
if the instrument is inoperable, then 24-hour grab
samples are required to be obtained and analyzed.
In compliance with
this requirement, the plant chemistry department was notifed and
24-hour grab sampling was commenced.
Further investigation could not
determine the reason for Icck of monitor flow and maintenance request
(MR) 87-2094 was initiated to correct the problem. Additionally, I&C
technicians found the monitor system low flow switch plugged with
silt. The switch was cleaned and the calibration completed success-
fully by establishing monitor system flow via an alternate suction
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flowpath (SW return line to the cooling tower deep basin).
Upon
restoration of the flow switch to service, the SW effluent radiation
monitor indicated downscale (an indication of no flow through the
monitor). Actuation of the low flow switch causes deenergization of
the radiation monitor resulting in a downscale reading as an indica-
tion that the monitor system is inoperable.
This condition existed
from September 4-17 when the system was returned to operable status.
Required grab samples were taken during this period.
'
Based on the above, PRO 87-38 was initiated on September 3, 1987.
Review of PRO 87-38 by the engineering support department (ES0)
determined that the occurrence was not reportable.
This finding was
based upon the premise that systems are declared inoperable when they
are "found or made inoperable"; that the condition was found on
Sr ptember 3; and, that the TS limiting condition for operation (LCO)
.
.
9
in Table 3.9.1 was met (24-hour grab samples).
Reviews by plant
management concurred with this determination.
The Plant Manager
assigned an AP 0028 Category A action item to the operations depart-
,
ment to determine the cause of loss of monitor system flow.
This
action item was completed on October 13 and was approved by the
Operations Superintendent on November 19. The finding of this review
,
indicated that flow through the monitor system was decreased when the
SW system was placed in an abnormal lineup to support outage related
activities.
This resulted in insufficient monitor system suction
pressure and probable tripping of the monitor system punp due to
thermal overload. Subsequent investigation revealed that this situa-
tion existed for twelve days from August 22, 1987 to September 3, 1987
during which time required 24-hour grab samples were not taken.
!
>
Various recommendations to prevent recurrence were included in the
response to the action item.
The results of this operations depart-
ment review were not forwarded to the engineering support department
for further review of reportability requirements.
Inspector review of PRO 87-38 indicated that the licensee was most
probably unaware that a TS requirement had been missed (24-hour grab
samples per Table 3.9.1) and was reportable under 10 CFR 50.73. Dis-
cussions with the Engineering Support Supervisor on February 10, 1988
precipitated licensee review of PRO 87-38.
This review established
the technical aspects and sequence of events described above and
determined that the occurrence was reportable under 10 CFR 50.73.
i
Licensee event report (LER)
88-01
was
subsequently
issued
on
March 11, 1988, over six months after the occurrence.
1
The enhanced licensee review that was performed between February 10
and March 11, 1983 uncovered a related condition that is potentially
reportable as well.
This involves a lack of sufficient sensitivity
of the SW ef fluent radiation monitor, during periods when the circu-
lating water (CW) system is shutdown, to ensure river release limits
specified in TS 3.8.A.1 are met.
Initial indications are that, dur-
ing periods when the CW system is secured (and possibly when in
closed cycle operation) and the dilution effect of this flow is lost,
the SW effluent radiation monitor does not exhibit sufficient sensi-
tivity to ensure release limits are being met and therefore 24-hour
grab samples are required.
This item remains unresolved pending
further licensee review and determination of reportability (50-271/
88-03-01).
.
Licensee performance during the initial review of PRO 87-38 raised
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several concerns with the inspector.
First was that an abnormal
system lineup of SW caused an unanticipated and unrecognized loss of
the SW effluent radiation monitor that went undetected and uncompen-
sated for twelve days.
Second was the lack of aggressive investiga-
tion to determine reportability of PRO 87-38.
Third was the failure
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of the operations department, upon completion of the action item
review, to recognize the reportabilty of the occurrence.
Fourth was
the programmatic disconnect betveen completion of the AP 0028 action
item and forwarding pertinent results to the engineering support
department.
The first concern represents a violation of TS Table 3.9.1 require-
ments (50-271/88-03-02). Corrective actions contained in LER 88-01
appear to be responsive.
The remaining concerns are unresolved
pending licensee review of the occurrence investigation, reporting
and tracking programs (50-271/88-03-03).
6.3 Post-Maintenance Operability Testing of Valve V10-39A - PRO 87-60
On September 29, 1987 work was performed on valve V10-39A (RHR-39A)
per maintenance request (MR) 87-2550 to repair a packing leak.
Valve
RHR-39A is the loop
"A"
torus spray / test isolation valve and is a
containment isolation valve.
Required post-maintenance operational
testing was to be stroke and time testing per MR 87-2550. Documen-
tation of this testing did not occur until October 12, 1987,
In the
interim, the reactor was taken critical on October 2 and 5,1987.
The PRO 87-60 was initiated on October 13, 1987 to review the report-
abilty of critical operatiens with RHR-39A in an apparently untested
condition.
The licensee determined that, since the valve tested
operable on October 12, and adjustments to packing nuts do not affect
valve seat leakage, the occurrence was not reportable. The inspector
noted during the review of PRO 87-60 that a component undergoing
maintenance must be considered inoperable until the required post-
maintenance operability testing has been satisfactorily completed.
Licensee procedures AP 0021, "Maintenance Requests" and AP 0025,
"Plant Equipment Control" support this tenet, and control the pro-
cessing of safety-related maintenance.
The inspector furthe
noted
'
that per TS 3.7,0.1, RHR-39A is required to be operable during reac-
tor power operation except as specified in TS 3.7.D.2.
This TS would
allow RHR-39A to be inoperable during reactor power cperation if at
least one valve in the associated line was in a mode corresponding to
the isolated condition (closed in the case of RHR-39A). This was the
case as RHR-34A was closed during this period.
However, TS 4.7.2
requires in this condition that the position of RHR-34A be logged
daily.
This
requirement
was
not
met
during
the
period
of
October 2-12, 1987, and apparently constituted a missed TS required
surveillance requiring reporting under 10 CFR 50.73.
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11
Discussions with the Engineering Support Supervisor on February 10,
1988 did not yield a satisfactory conclusion.
The licensee main-
tained this occurrence was not reportable.
Subsequent discussions
with licensee management have resulted in further review of PRO 87-60
to determine reportability.
The results of this review determined
that stroke and time testing of RHR-39A was in fact accomplished on
October 1,1987 but due to communication and/or documentation errors
this information was not available.
Therefore, RHR-39A was actually
operable af ter October 1 and invoking the requirements of TS 4.7.2
was not necessary.
However, based upon the original information
contained in PRO 87-60, the licensee should have initially determined
the item to be reportable.
6.4 Missed Surveillance - PRO 88-012
In December 1981 the licensee implemented plant design change request
(PDCR) 81-12 which terminated and blank flanged the reactor vessel
head spray system (RVHS) inside primary containment.
The RVHS sys-
tem, which is a subsystem of RHR, was deactivated to reduce reactor
vessel penetrations and because the system was identified as being
susceptible to intergranular stress corrossion cracking. The system
was terminated downstream of the two containment isolation valves,
l
RHR-32 and RHR-33.
The blank flange was seismically qualified and
was leak rate tested satisfactorily after installation.
On February 16, 1988 the licensee generated PRO 88-012 concerning
missed TS-required surveillance testing of CIVs RHR-32 and RHR-33.
These valves are required to be tested at least once per operating
cycle to ensure primary containment isolation capability in accord-
ance with TS 4.7 D.1.a.
The surveillance test had not been accom-
plished for these valves since the system was deactivated.
The
licensee deemed this PRO to be not reportable. The isolation valves
RHR-32 and RHR-33 are exempt from 10 CFR 50 Appendix J Type C leakage
rate testing per TS Table 4.7.2.6.
The blank flange installed meets
the containment integrity requirements of TS 4.7.3.
,
The inspectors expressed the concern to the licensee that, although
containment integrity has been maintained and the RVHS system has
been permanently isolated, a TS requirement exists to test the re-
sponse of RHR-32 and RHR-33 to an isolation signal.
Therefore, the
.
licensee should readdress the ef fect of the PDCR on the ability to
'
perform and meaningfulness of impacted TS requirements and request TS
amendments and revise procedures as appropriate. The inspectors will
follow the resolution of this issue as an unresolved item (50-271/
88-03-04).
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6.5 Summary of Findings
Although the licensee appears to have adequate procedures to cover
occurrence reporting, in at least one case a programmatic weakness
prevented significant information from being disseminated to appro-
priate organizational levels.
The examples above indicate an occas-
ional lack of aggressive investigation of events surrounding a PRO.
Also, occasionally the licensee uses faulty logic in determining
reportability that appears to result in incorrect /non-conservative
findings.
Licensee attention in this area is required. Corrective
actions will be reviewed under the unresolved item in Section 6.2.
7.
Licensee Event Reporting (LER)
,
The inspector reviewed Licensee Event Report (LER) 88-01, Plant Service
Water Effluent Stream not Monitored Due to Procedure Deficiency. This LER
was submitted as a result of a failure to meet TS limiting conditions for
operations as described in Section 6.2 of this inspection report.
The inspector determined that with respect to the general aspects of the
event: (1) the report was not submitted in a timely manner due to poor
analysis by the licensee as described in Section 6.2; (2) description of
the event presented was accurate; (3) root cause analysis was performed;
(4) safety implic4tions were considered; and (5) corrective actions imple-
mented or planned were sufficient to preclude near-term recurrence of a
,
similar event. Violations and reporting concerns, and the need to address
t
in greater scope and specificity related long-term operational corrective
actions to preclude recurrence, were identified and are detailed in
Section 6.2.
8.
Operational Event Review
8.1 Local Power Range Monitor Spiking Problems
,
Recently, VYNPS has experienced an increased incidence of high output
signal spiking in Local Power Range Monitors (LPRMs). Spurious spik-
ing in LPRMs is a historical problem that has existed for years in
boiling water reactors (BWRs).
The recent increase at VYNPS is at-
tributed to new model NA300 detectors installed during the 1987 out-
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age. Of the eight new installed detectors (two strings of four de-
tectors each) five have experienced cne or more random high spikes.
The NA300 LPRMs are an improved de'ign that, among other attributes,
are intended to reduce the frequency of random spiking observed in
earlier models (NA200 and NA1CO).
Licenses communications with the
vendor have indicated that e9aluation and analysis of the phenomenon
are in progress and potential remedies are being formulated.
Interim
'
resolution is expected in the next few months.
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Normally, LPRM spiking is considered a nuisance and does not create
any significant operational problem or concern.
However, due to the
design of the VYNPS average power range monitor (APRM) system and
reactor protection system (RPS), a single randomly spiking LPRM of
sufficient magnitude has the potential of causing a reactor scram.
The system of 80 LPRM detectors (20 strings of four detectors each)
is arranged such that some LPRMs are shared by two APRMs (A and 0, or
C and F) in opposite RPS trip channels (A and B).
In such a condi-
tion, a spike of sufficier.t magnitude in one of these shared LPRMs
-
has the potential for tripping both of the associated APRMs satisfy-
ing the RPS logic for a full reactor scram.
Four of the new NA300
LPRM detectors are assigned to shared APRMs, and three of these
detectors have experienced spiking problems.
In recognition of the
potential for an unnecessary plant trip due to this condition, the
licensee placed two of the shared APRMs (C and 0) in Bypass on
February 25, 1933. This allowed configuration would prevent a single
random
spike
from causing a
reactor
Subsequently, on
'
March 8, 1988, the licensee individually bypassed the four shared
LPRM detectors and returned APRMs C and 0 to normal operation.
The
four remair.ing NA300 detectors (which input to non-shared APRMs) will
remai, in operation and have their performance monitored for the
remainder of the cycle or until interim correction is implemented.
,
,
The licensee approach to this problerr, demonstrated thoroughness and
sound engineering judgement.
Communications with the vendor were
timely and appropriate and adequately documented. Licensee permanent
I
corrective actions are contingent upon final vendor analysis and will
be reviewed by the inspector when available.
No inadequacies were
identified.
9.
Review of Maintenance Act'"ities
9.1 Preplanned Power Reduction to Accomplish Scheduled Maintenance
During the weekend of March 19-20, 1983 the licensee performed a
preplanned power reduction to 55*4 power to facilitate various
maintenance activities.
The containment was deinerted to allow
a drywell entry to identify potential primary leakage paths.
Power was reduced to 55'4 at 7:40
a.m.
on March 19, 1988,
Scheduled maintenance .as completed and the unit returned to
i
100*4
power
after
c:mpleting
PCIOMR
at
10:35
a.m.
on
March 21, 1983.
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Significant maintenance accomplished included:
f
Drywell inspection - minor packing leakage was observed
.
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from valve RHR-88.
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MSIV 86A test solenoid was repaired to correct slow test
,
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response times.
Slow closure and fast closure tests were
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performed satisfactorily.
The IB high pressure heater feed recirculating line flange
--
leak was repaired by use of Fermanite sealing compound.
The 2A high pressure heater drain valve operator was
--
replaced.
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The B feedwater regulating valve control air tubing was
--
replaced.
,
The main condenser tubes were chill shocked and cleaned.
--
All maintenance activities scheduled to be performed during the
'
power reduction were completed.
The licensee exhibited strong
preplanning and interdepartmental scheduling in accomplishing
<
these objectives.
The inspectors had no further questions.
10. Core Speay Safe End Nozzle Weld Overlays
By letter dated March 1,
1988 (FVY 88-19), VYNPC requested NRC:NRR to
approve a plan for long-term operations with the current weld overlays on
the core spray nozzles.
This issue was most recently addressed by the
,
inspector in Inspection Report 50-271/87-21 (Detail 3.1) with a review of
the VYNPC post-outage report of weld overlay inspections (letter datd
October 20, 1987 [FVY 87-100]). In that letter, the licensee committed to
notify NRC:NRR of future plans regarding replacement of the safe ends upon
i
completion of an evaluation of long-term operation with weld overlays.
1
This submittal fulfills the commitment and includes a technical report,
"Vermont Yankee Nuclear Power Station, Justification for Long Term Opera-
tion for Vermont Yankee Core Spray Nozzle Weld Overlays". Based on this
report, VYNPC determined that continued operation with weld overlays on
,
l
the core spray nozzles is acceptable beyond Cycle 13 (current cycle)
operation.
The licensee further committed to periodically confirm the
evaluation results and the acceptability of continued operation with the
weld overlays through performance of periodic ultrasonic examination of
j
the overlays per NUREG-0313, Revision 2 and the inspection program
,
developed for the past outage. Concurrence with VYNPC plans for continued
operation with the weld overlays was requested of NRC:NRR with a target
review completion date of June 1,1988 to suppen planning for the 1989
outage. The inspector reviewed the current submittal and will follow the
.
results of the NRC:NRR review,
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11.
Review of Licensee Response to NRC Initiatives
11.1 Scram Discharge Volume Capability (TI 2515/90)
Temporary Instruction (TI) 2515/90 provides guidance for performing
inspection followup of boiling water reactor (BWR) licensee activ-
ities to ensure scram discharge volume (SDV) capability in accordance
with long-term commitments concerning Multiplant Action (MPA) Item
B-58. As required by TI 2515/90, the inspector conducted an inspec-
tion of VYNPC design / procedures regarding SOV capability. Each item
of TI 2515/90 and the results of the inspection are delineated below:
Item 4.01 - Scram Discharge Header Size:
Generic safety evaluation
report (SER) for all BWR licensees, dated December 9,1980 shows the
status of this item as acceptable for Vermont Yankee.
Item 4.02 - Automatic Scram on High SDV Level: Four trip units from
each instrument volume (two from each instrument volume for each
reactor protection system trip system) initiate a scram to shut down
the reactor while sufficient free volume is still present to receive
the scram discharge.
Item 4.03 - Instrument Taps Not on Connected Piping:
The inspector
performed a field inspection of the instrument volume (IV) and found
that each IV has four separate upper and lower taps located on the IV
proper.
The taps are located 90 degrees apart and are adequately
supported.
Item 4.04 - Detection of Water in the IV: The level sensing instru-
ments on the IV use separate taps (total of four instruments per IV)
and are powered by separate power supplies and therefore meet the
redundancy requirement.
The diversity issue was addressed by NRC in
a letter dated September 10, 1985.
The safety evaluation report
attached to the letter concluded that the Vermont Yankee design
satisfied the diversity requirement for the IV.
Item 4.05 - Vent and Drain Valves System Interfaces:
The vents and
drain are dedicated systems.
They are not intertied with any other
system that could have an adverse ef fect on proper functioning.
The
HVAC ducts have fixed lower openings nearby so that, in effect, the
vents are to atmosphere.
Similarly, the drain pipe terminates open
ended inside a floor drain pipe collar and is not interconnected with
anything else.
This information was provided by the licensee in an
August 11, 1980 response to IE Bulletin 80-17, Supplement 1, and was
accepted by NRC in its generic SER dated December 9, 1980.
Item 4.06 - Vent and Drain Valves _.Close on Loss of Air: The vent and
drain valves at Vermont Yankee are designed such that they are held
i
open with air against spring pressure. Consequently, they will close
'
on loss of air pressure,
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Item 4.07
Operator Aidi
Four differential pressure type level
-
transmitters on each of the two IV's provide signals to analog-to-
digital trip units. One of the trip units on each instrument volume
initiates an alarm for operator action prior to the IV high level
scram setpoint being reached.
-
Item 4.08 - Active Failure in Vent and Drain Lines: There are two
air operated-to-open, spring pressure-to-close, valves in each drain
.
line.
This configuration meets the single active failure criteria.
The vent lines are configured with one air operated-to-open, spring
pressure-to-close valve and one check valve in each line. This con-
figuration was evaluated as acceptable in the NRC generic SER dated
December 9, 1980.
Item 4.09 - Periodic Testing of Vent and Orain Valves: The SDV vent
'
and drain valves are operability tested monthV per surveillance test
OP 4111.
During the conduct of the operability test the valve
closure time is recorded, and is required to be less than 30 seconds.
Item 4.10 - Periodic Testing of Level Detection Instrumentation:
A
functional test of the Whigh water level instruments is performe 1
i
every one-to-three months per surveillance test procedure OP 4310 and
TS Tables 4.1.1.
Calibration of the IV level instrurent loops is
performed once each operating cycle. The functional part of the pro-
cedure tests the IV high level alarm, rod block and reactor scram set
points, and includes restoration of the system configuration.
The
functional test is perfomred using the electronic calibration unit.
The loop calibration 15 performed using an external input to the
transmitter from a manometer.
l
Item 4.11 - periodic Testing Operability of the Entire System:
The
_
technical specifications at Vermont Yankee contain no requirernent to
perform an integrated operability test of the entire system. A one-
time special system functionality test was performed in 1981.
No
commitment was made by the lice' >ee to modify the TS to require this
testing, and no requirement was imposed by the NRC.
However, the VY
i
TS's were amended (Amendment 73) to conform to the NRR model TS
l
regarding this issue,
i
The inspector determined that the licensee has met its long-term
,
commitments to up grade SDV capabilty, and no violations or devia-
,
tions were identified. TI 2515/90 is closed.
)
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11.2 Region I, TI 88-01:
Fitness for Duty Program
'
Region I Temporary Instruction 88-01 (RI TI 88-01), "Fitness for Duty
(Drug Testing) Information and Reporting" was performed to collect
additional data for review of the experience associated with drug
testing as part of the licensee fitness for duty program.
Informa-
t
tion was obtained to support evaluation of program effectiveness and
responsiveness to the NRC policy statement on fitness for duty
(Federal Register 51 FR 27921 August 4, 1986).
This information was provided to the Region I Division of Reactor
Projects Fitness for Duty Coordinator.
Additionally, reportability
under 10 CFR 73.71 of drug related events was discussed with the
licensee.
NRC NUREG 1304, which summarizes NRC guidance in this
area, is currently under licensee review for impact on the program
and associated procedures.
The licensee is striving to balance
reporting guidelines with the need for confidentiality.
No inade-
.
quacies were identified during this review of the licensee fitness
i
for duty program.
T
]
12.
Review of Periodic and Special Reports
)
Upon receipt, the inspector reviewed periodic and special reports submit-
,
ted pursuant to Technical
Specifications.
This review verified, as
'
a
applicable: (1) that the reported information was valid and included the
NRC-required data; (2) that test results and supporting information were
consistent with design predictions and performance specification; and (3)
that planned corrective actions were adequate for resolution of the
t
4
problem. The inspector also ascert.ined whether any reported information
!
should be classified as an abnormal occurrence.
The following reports
(
,
were raviewed:
4
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Monthly Statistical Report for plant operations for the month of
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3
4
February 1988.
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Effluent and Waste Disposal Semi-annual Report for Third and Fourth
,
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Quarters,1987 Including Annual Radiological In' pact on Man for 1987
[
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Vermont Yankee 1937 Annual Operating Report
i
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Review of the VYNPS semi-annual effluent release report included the
following areas:
Liquid and gaseous radioactive effluents and solid waste
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Radiological dose comnitments associated with any ef fluent releases
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Meteorological data
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Changes to the Off-Site Dose Calculation Manual
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18
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The report concluded that since there were no routine or accidental liquid
releases from VYNPS, no doses were attributed to individuals in unre-
stricted areas.
Because noble gas release was below the lower limit of
detectability, no air dose was attributed to this potential release path.
Dose assessments due to iodines and particulates in gaseous effluents were
well below 10 CFR Part 50 Appendix ! and TS 3.8.G.1 criteria. No inade-
quacies were identified.
The VYNPS Annual Operating Report is required to be submitted in accord-
ance with 10 CFR Part 50.59 (b)(2), which states that the report should
contain brief descriptions of facility changes, tests and experiments per-
formed without prior NRC approval per 10 CFR 50.59 (a)(1), as well as a
summary of the safety evaluation associated with each.
Contrary to the
above, the 1987 VYNPS Annual Operating Report did not include summary
safety evaluations for facility changes, tests or experiments.
When
informed by the inspector of this deficiency, the licensee committed to
review and revise as appropriate the report format.
This item is unre-
solved pending documentation of appropriate licensee review and action on
this issue (50-271/83-03-05).
13. Management Meetings
At periodic intervals during this inspection, meetings were held with
senior plant management to discuss the findings.
A summary of findings
for the report period was also discussed after the conclusion of the
inspection and prior to report issuance. No proprietary information was
identified as being included in the report.
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