ML20210P435

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Insp Rept 50-293/86-25 on 860708-0804.Violations Noted: Failure to Follow Surveillance Test Procedures & to Initiate Failure & Malfunction Repts for Deficient Fire Barriers. Deviations Noted:Failure to Hold Fire Brigade Drills
ML20210P435
Person / Time
Site: Pilgrim
Issue date: 09/02/1986
From: Strosnider J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20210P324 List:
References
50-293-86-25, NUDOCS 8610060773
Download: ML20210P435 (27)


See also: IR 05000293/1986025

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U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket / Report No. 50-293/86-25

Licensee: Boston Edison Company

800 Boylston Street

Boston, Massachusetts 02199

Facility: Pilgrim Nuclear Power Station

Location: Plymouth, Massachusetts

Dates: July 8, 1986 - August 4, 1986

Inspectors: M. McBride, Senior Resident Inspector

J. Lyash, Resident Inspector

G. Nejfelt, Resident Inspector

L. Doer 11 , Project Engineer

Approved by: _

A

( . Strosnider, Chief, Reactor Projects

7 /88

Date

ection IB

Summary: July 8, 1986 - August 4, 1986

Inspection Report 50-293/86-25 ,

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Areas Inspected: A routine resident inspection was conducted of the control

room, accessible parts of plant structures, plant operations, radiation protec-

tion, physical security, plant operation records, plant events, maintenance,

surveillance, and reports to the NRC. The inspection totaled 350 hours0.00405 days <br />0.0972 hours <br />5.787037e-4 weeks <br />1.33175e-4 months <br /> by three

resident and one regional inspector.

Results: Two violations were identified regarding the failure to follow sur-

ve111ance test procedures (section 3.e) and failure to initiate Failure and

Malfunction Reports (F&MR) for deficient fire barriers (section 7). A devia-

tion from an NRC commitment concerning fire brigade training was also identified

(section 2). Lack of operations personnel sensitivity to control rod drive ac-

cumulator status lights is discussed in Section 3a. Inadeauacies in the oper-

ating and alarm procedures for the hydrogen and oxygen monitors is discussed in

section 3.b. The licensee's plans to replace secondary containment dampers in

light of a 1985 commitment to the NRC and recent damper problems is discussed

in section 3.d. Possible weaknesses in preventive maintenance on ATWS (antici-

pated transient without scram) equipment, in maintenance records control, and

in the design of the feedwater check valves are also discussed in section 3.d.

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Recent calibration drift in safety bus undervoltage relays is discussed in

section 4.e. Concerns about the control, calibration, and testing of certain

480 VAC and 125 VDC undervoltage relays and concerns about the use of fuses and

solid links in safety-related motor control circuits are discussed in section

4.e and 4.f respectively. An inaccurate NRC safety evaluation supporting an

exemption from the requirement to install a hydrogen recombiner is discussed in

section 4.h. Excessive security guard overtime is discussed in section 5.

8610060773

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TABLE OF CONTENTS

Page

1. Summary of Facility Activities ........................ 1

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2. Followup on Previous Inspection Findings . . . . . . . . . . . . . . 1

3. Routine Periodic Inspections .......................... 6

Daily Inspection, System Alignment Inspection,

Biweekly Inspections, Plant Maintenance and

Surveillance Testing

4. Review of Plant Events ................................ 10

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a. Loss of 480 VAC Bus B-23 and Resulting

Half Scrams

i b. Low Level Contamination of Onsite Sewage Tanks

i c. Anticipated Transient Without Scram Monthly

Functional Test Discrepancies

] d. Reactor Building Ventilation Sample Pump

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Failures

e. 4160 VAC Safety Bus Undervoltage Voltage

j Relay Calibration Failures

f. HPCI Area Unit Cooler Breaker Fire

g. Protective Instrumentation Rack 2205

Upscale Drift

h. Hydrogen Recombiner Safety Evaluation

1. Intermediate Range Neutron Monitors

5. Observations of Physical Security ..................... 14

6. Radiation Protection and Chemistry .................... 15

7. Station Fi re Barrier Deficiencies . . . . . . . . . . . . . . . . . . . . . 15

8. Local Leak Rate Test Program .......................... 16

9. Independent Verification of Operating Activities . . . . . . 16

10. Review of Licensee Event Reports (LER's) . . . . . . . . . . . . . . 17

11. Confi rmatory Action Letter 86-10 Update . . . . . . . . . . . . . . . 19

12. Congressional Staff and NRC Commissioner Visits to .... 19

Pilgrim

13. Management Meetings and Meetings with Local Groups .... 20

Attachment I - Persons Contacted

Attachment II - Summary of Security Force Overtime

Attachment III - NRC Questions Regarding the Supplement of Response to CAL 86-10

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OETAILS

1.0 Summary of Facility Activities

The plant has been shutdown since April 12, 1986 for unscheduled

maintenance. Subsequent to the shutdown, the NRC issued Confirmatory

Action Letter (CAL) 86-10. Discussion of issues raised in CAL 86-10

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continued throughout the report period.

On July 14, 1986, Commissioner James Asselstine met with NRC and licensee

representatives on site to discuss the performance of Pilgrim, and

program improvements made to date. A station tour followed the meetings.

On July 25, 1985, Boston Edison announced that three major tasks will be

added to the current outage which will extend the projected startup date

from September 1986 until early 1987. The tasks are (1) the completion

of fire protection modifications at the station (2) the installation of

certain enhancements to the Pilgrim Mark I primary containment structure,

and (3) refueling the reactor. The Pilgrim outage was discussed during a

i licensee management meeting in the NRC Region I office on July 30, 1986.

2.0 Followup on Previous Inspection Findings

l Violations

(0 pen) Violation (83-23-01), perform IST of ECCS/RCIC injection check

valves. This item was last updated in inspection report 84-16. The

licensee has established procedures for performing a manual exercise test

of the HPCI and RCIC injection check valves. These procedures verify

that the valve discs are free to rotate, but do not verify that the valve

seats on reversal of flow. Similarly, no reverse flow testing of the

core spray system injection check valves is conducted. In response to

the Confirmatory Action Letter (CAL) 86-10, the licensee has commi;ted to

leak test the RHR injection check valves. During followup of CAL 86-10

the inspector questioned the licensee regarding the need to also leak

test the HPCI, RCIC and core spray check valves. No response had been

received from the licensee prior to close of the inspection period.

Unresolved Items

(0 pen) Unresolved Item (86-01-03), review licensee evaluation of the use

of fuses and metal links. This item was last updated in inspection

report 86-21. During the period High Pressure Coolant Injection System

Area Cooler breaker 1822 caught fire due to a control circuit fault, and

installation of a solid link. This event is described in section 4;f of

this report.

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(0 pen) Unresolved Item (86-14-01), operation with unqualified diesel

generator differential relay. The inspector reviewed Boston Edison

Memorandum NED 86-583, Evaluation of Emergency Diesel Generator (EDG)

Differential Relay Issues. The memorandum's conclusions were 1) the use

of the unqualified relays placed the plant configuration beyond the

design basis as set forth in the FSAR, 2) the use of the Engineering

Service Request process for addressing the discrepancies was inadequate

with respect to the timeliness and completeness of the disposition, 3)

the use of the company " corrective action program" would have ensured

adequate and timely action, including 50.59 safety evaluation and 4)

the safety significance of the unqualified relays was small.

If the established corrective action program described in the Boston

Edison Quality Assurance Manual, had been followed comprehensive and timely

engineering analysis and corrective actions could have been taken. This

will be addressed by the licensee in their written response to inspection

report 50-293/86-14. This item will remain open pending an NRC review of

the General Electric station blackout analysis supporting the licensee's

evaluation.

(0 pen) Unresolved Item (86-07-02), review licensee corrective action for

failed secondary containment seals. The inspector reviewed the licensee

evaluation of the two secondary containment boot tears. Thermal movement

of the pipe, vibration, localized harsh environment and some material

degradation were identified as the most probable cause for the boot

failures. The licensee repaired the subject tears by overlaying the area

with sealant. Initial plans were to reinspect all penetrations in the

steam tunnel, including the damaged boots, during RF0 #7. Other

recommendations included replacement of the damaged boots during RF0 #7.

The current maintenance outage has been extended to encompass the

, refueling outage. The inspector questioned the licensee regarding any

revised plans, possibly including replacement of the boots during this

extended outage. Similar boots on the main steam lines were replaced

several years ago. This item remains open pending response from the

licensee regarding future boot inspection / replacement plans.  !

(Closed) Unresolved Item (86-21-01), fire brigade drill requirements not

satisfied. Review of licensee training records for the period of i

January 1,1985 through July 31, 1986 indicate that a significant portion

of the station fire brigade have not participated in scheduled drills.

During calendar year 1985 approximately thirty of sixty-nine brigade

members did not participate in a drill. Thirty-two of seventy-five

brigade members have not drilled in 1986. Fourteen brigade members did

not participate in any drill during the nineteen month period between

January 1,1985 and July 31, 1986. Five individuals added to the brigade

in July, 1985, had not participated in a drill.

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The licensee committed in a letter to the NRC, dated March 1, 1977, to

conduct fire brigade training in accordance with item B.6.e.2 of NRC

Branch Technical Position APCSB 9.5-1, Revision 1. Item B.6.e.2 states

that required training can only be accomplished by conducting drills

several times a year (at least quarterly), so that all members of the

fire brigade have had the opportunity to train as a team, testing itself

in the major areas of the plant. This commitment was reviewed and

accepted by NRC:NRR in its fire protection safety evaluation, as

referenced in the facility operating license. Failure to ensure that all

individuals participate in at least one drill annually raises concern

regarding the ability of members to perform if called upon.

The inspector informed the licensee that the above failure to satisfy

commitments made to the NRC is considered a deviation (86-25-01).

Inspector Follow Items

(0 pen) Follow Item (84-44-02). The individual who performed sludge

lancing of a contaminated tank without supervisor's approval, and removed

his teledosimetry device, was terminated as an employee. The disregard

of radiological monitoring by the individual was outside the expected

reasonable activities addressed in the licensee's procedures such as

reporting lost, damaged, missing, abnormal reading, or off-scale

dosimetry to Health Physics (HP) - PNPS Procedure 6.2-11, Revision 5,

dated October 26, 1984. After a discussion with the inspector who opened

this item, it will remain open pending a specialist review.

(0 pen) Follow Item (84-44-03). The practice of making a verbal change to

a radiological work permit (RWP) is no longer permitted by PNPS Procedure

6.1-027 dated June 12, 1986. RWP revisions must now be in writing and

reviewed by a supervisor at the same level as for the approval of the

original RWP to assure that the radiological controls are within the

scope of the RWP or if a new RWP is required. Enforcement of this

procedure would prevent the potential problem made by a verbal change to

a RWP. After a discussion with the inspector who opened this item, this

item will remain open pending a specialist review.

(0 pen) Followup Item (84-44-05). A HP technician allowed another

technician to perform sludge lancing without a breathing zone air (BZA)

sampler, although required by the RWP. Use of BZA sampler and regulated

air sampler is stated in PNPS Procedure 6.3-160, Revision 9, dated

April 11, 1986. Special precautions and equipment needed to work safely

within existing radiological conditions is stated in PNPS Procedure

6.1-022, Revision 20. The current procedure controlling RWPs, PNPS

Procedure 6.1-027 dated June 12, 1986, requires an HP supervisor to change

the RWP in writing. This item will remain open pending a specialist

review.

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(Closed) Inspector Follow Item (85-27-51), H202 monitor acceptance

criteria not adequate for inspection. The inspector reviewed the

environmental qualification (EQ) files for the containment hydrogen

monitors. The component test report and evaluation sheets originally

identified a required yearly inspection. . Subsequent discussion between

the licensee and vendor determined that a yearly zero adjust and span

adjust is adequate. This determination was documented in a telephone

call record and Revision 1 to the EQ Evaluation Sheet dated November 8,

1985. System calibration is performed on a six month interval as

required by technical specifications. This item is closed.

(Closed) Inspector Follow Item (85-31-02), review licensee evaluation of

potential problems with RHR pump impeller wear rings. This item was last

updated in inspection report 86-21. During the current inspection period

the licensee began disassembly and inspection of all four residual heat

removal pumps and motors. This effort is scheduled to complete in mid

September. The inspectors observed portions of the pump motor work. GE

supervisors and GE QC inspectors were present during NRC review and

appeared actively involved with the ongoing work. The NRC inspectors

will continue to monitor work activities during routine inspections.

Specialist inspection of this activity is documented in NRC inspection

report (86-27).

(0 pen) Inspector Follow Item (86-14-04), evaluate implementation of RHR

minimum flow logic modifications, The inspector reviewed PNPS Plant

Design Change 86-33, Revision 1, MO 1001-18 A&B control modification.

This design change was initiated in response to the si:gle failure

susceptibility of the RHR pump minimum flow protection logic identified

by the licensee and discussed in IE Bulletin 86-01. PDC 86-33 changes

the minimum flow valve position from normally closed to normally open.

It also deletes the valve automatic close input from the flow sensing

instrumentation. The net effect of these changes is that the minimum

flow valves will initially be open and remain open during Low Pressure

Coolant Injection System (LPCI) operation. Because the valves remain

open throughout LPCI injection approximately 500 gpm per pump will be

diverted from the vessel. The licensee evaluation of the affect of the

reduced LPCI flow on the station accident analysis and technical

specifications will be reviewed in a future inspection.

TMI Action Plan Items

(0 pen) TAP Item II.D.3, Safety Relief Valve Position Indication.

Guidance provided in NUREG 0737 indicates that the safety / relief valve

position indication system should be environmentally qualified. The

licensee committed to install environmentally qualified indication prior

to startup from RF0 #5. Qualified indication was installed under Plant

Design Change Request 77-78. The design installation was reviewed in

inspection report 82-10.

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Regulatory Guide 1.97 designates primary system safety / relief valve

position indication as a category two variable. Guidance provioed on

category two equipment qualification states that instrumentation should

be environmentally quali-fied. The licensee, in submittals discussing

compliance with regulatory guide 1.97, designated this equipment as not

requiring environmental qualification. The NRC:NRR safety evaluation

addressing this area is not expected until 1987.

Based on the regulatory guide 1.97 submittals the licensee deleted the

position indication system from the EQ Master List and no longer

believes that the equipment must be maintained as environmentally

qualified. This item remains open pending resolution of this

discrepancy.

(Closed) TAP Item II.F.1.6, Post Accident Containment Hydrogen

Monitoring. The licensee has installed a primary containment hydrogen

M oxygen (H202) monitoring system. The system has been designated as

5 fgty related and applicable quality control requirements applied. The

WMM consists of two redundant safety trains, each independently

cace.ia .of taking samples from two drywell and one torus location.

Samp1M; system control and calibration can be accomplished locally or

remotely from the control room. System components are powered by class

IE power. Sample valves close on a containment isolation signal, but may

be reopened from the control room using an isolation signal override

feature after an accident. Reagent and calibration gas fill connections

outside secondary containment have been provided to allow recharge

following an accident if secondary containment entry is not possible.

Both H202 sample trains are maintained in a standby condition. This

ast.ures their availability within thirty minutes, but does not result in

the excessive equipment wear associated with continuous service. Oxygen

monitoring during normal operations is provided by a separate oxygen

analyzing system which alarms at 3% concentration. Technical

specifications addressing operability of containment combustible gas

monitoring were added undee amendment 55. These specifications were

reviewed by NRC:NRR and found acceptable as documented in a safety

evaluation provided to Boston Edison on July 5, 1985. Based on the above

this item is closed.

The inspector performed a walkdown of accessible system components and

reviewed applicable drawings and procedures. This is described in

section 3.b of this report.

Followup on a Part 21 Report - On March 13, 1986, the Philadelphia

Electric Company submitted a 10 CFR Part 21 report concerning a failure

of a Clow Corporation butterfly valve due to galvanic corrosion between

the valve's carbon bushings and stainless steel shaft. The inspector

questioned BECo to see if they knew of this potential problem. The

licensee indicated that they were aware of the Part 21 report and that it

was currently being reviewed by engineering for applicability. The

licensee further stated that any corrective action required would be

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completed prior to the next reactor startup. The inspector will review

the results of the licensee's evaluation and corrective action during a

subsequent inspection (86-25-02).

3.0 Routine Periodic Inspections

a. Daily Inspection

During routine facility tours, the following were checked: manning,

access control, adherence to procedures and limiting conditions for

operations (LCO's), instrumentation and recorder traces, control

room annunciators, safety equipment operability, control room logs

and other licensee documentation.

During a tour of the control room the inspector noted that several

control rod drive accumulator trouble lights were not in alarm with

accumulator charging water isolated. The inspector verified locally

that all accumulator pressures were below the alarm point. In

addition numerous alarm lights on the local accumulator trouble

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alarm panel were not lit. In response the licensee operations staff

replaced those alarm lights which had burned out, and wrote

maintenance requests for the remaining nonfunctional indications.

These indications should have been in an alarmed state for a period

of days prior to the inspector's observation. Operations personnel

were not sensitive to the indication status. This lack of

sensitivity was also noted in inspection report 86-01.

b. Systems Alignment Inspection

Operability confirmation was made of selected systems. Major motor

operated and manual valve positions were verified during routine

checks of the control room. Valve power supply, breaker alignment,

and safety equipment controller set points were also checked.

The inspector walked down accessible portions of the Primary

i Containment Hydrogen /0xygen (H202) Monitoring System. The accuracy

of system valve / breaker lineups and operating instructions was

reviewed. The adequacy of surveillance testing for the components

was evaluated.

During normal system operation the safety related Comsip post

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accident H202 monitors are in standby mode. A separate nonqualified

02 (C-41) monitor is used to continuously indicate containment

oxygen concentration. If 02 concentration increases to 3% a control

room alarm is received from the C-41 monitor. The Comsip H202

monitors are to be placed in service and alarm at 4% H202

concentrations.

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The inspector noted that alarm response procedure 2.3.2.20,

Revision 7 did not direct the operator to place the safety related

H202 analyzers in service upon receiving the containment Hi/ Low (3%)

02 alarm. Discussion with the control room staff indicated that the

need to place the H202 system in service if the alarm is received had

not been conveyed. The licensee informed the inspector that proce-

dure 2.3.2.20 would be changed to provide this guidance.

Nuclear Operations Procedure 2.2.133, Revision 3, H202 Analyzer and

C-19 system details system alignment and operating instructions.

The valve lineup in the procedure precludes operation of the C-41

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oxygen monitoring system. However, this equipment is normally in

service. The inaccurate procedure had neither been followed nor

corrected. This procedure also provided inaccurate instructions for

overriding a containment isolation signal and reopening the H202

sample valves post accident. The licensee is processing changes to

procedure 2.2.133 to correct the valve lineup and add steps to

recover from an isolation signal.

Technical specifications require measurement of containment oxygen

concentration at least twice weekly. The requirement is satisfied

by reading the C-41 02 analyzer. Periodic calibration of the 02

analyzer is accomplished by procedure 7.4.18. The inspector noted

that procedure 7.4.18 was not included on the Master Surveillance

Tracking Program (MSTP) to ensure its implementation.

Procedure 7.10.7, Calibration Checks of Comsip H202 Analyzers is

performed monthly as a functional test. As part of this test

chemistry department personnel verify that correct calibration gas

concentrations are posted in the main control room. The inspector

noted that no calibration gas concentrations had been posted and

that procedure 7.10.7 was not on the MSTP. The licensee, when

informed, posted the correct gas concentration and added procedures

7.4.18 and 7.10.7 to the MSTP.

c. Biweekly Inspections

During plant tours, the inspector observed shift turnovers, plant

conditions, valve and instrumentation lineup, radiological controls,

security, safety, and general adherence to regulatory requirements.

Plant housekeeping and cleanliness were evaluated. The inspeetor

had no further questions.

d. Plant Maintenance

The inspector observed and reviewed maintenance and problem

investigation activities to verify compliance with regulations,

administrative and maintenance procedures, codes and standards,

proper QA/QC involvement, safety tag use, equipment alignment,

jumper use, personnel qualifications, radiological controls for

worker protection, fire protection, retest requirements, and l

reportability per Technical Specifications. I

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The licensee has begun disassembly and inspection of all four

residual heat removal system pumps. The primary reason for

disassembly is the examination of the pump wear rings for signs

of cracking. The project has been contracted to General

Electric with Boston Edison oversight. A regional inspector

arrived on site August 4,1986 to examine the ongoing work (NRC

Inspection Report 50-293/86-27). Resident inspectors will

continue to monitor work activities.

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The inspector reviewed a series of recent secondary containment

isolation damper problems. The dampers in question appear to

be deficient in design. Failure of the dampers was the subject

of special inspection 85-21. The licensee stated that

replacement of the dampers with a nuclear grade design would be

campleted during this outage. During the inspector's exit

meeting station management reiterated its commitment to replace

the dampers prior to startup.

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During a plant tour on July 8,1986 the inspector noted

deficiency identification (DI) tags hanging from the alternate

rod insertion valves. The maintenance requests had been

written, and the DI tags hung during 1984 to rebuild the ASCO

valves. General Electric Service Information Letter (SIL) 128

advises licensees that valve internal parts made nf Buna N

deteriorate with age, and recommends replacement of these

components at intervals of less than seven years. The licensee

policy has been to rebuild the valves listed in the SIL on a

five year interval. While SIL 128 does not expressly identify

the ARI valves, these valves also have internal components made

of Buna N. The two ARI valves were received January 10, 1980,

approximately six years and six months ago. In response to the

inspectors questions, the licensee scheduled the ARI valves

to be rebuilt prior to startup.

The inspector noted that the requirement to rebuild the

affected valves on a five year interval was not listed on the

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station preventive maintenance program. Because of the large

number of valves the rebuild effort is staggered over a number

of outages; completing a percentage of the valves each time.

In the past, individuals have informally tracked the work

progress. The licensee stated that a formal method of tracking

the valve rebuild program, including the ARI valves, would be

implemented.

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While reviewing the quality assurance records of

post-maintenance testing in the Document Control Center (DCC),

the inspector found that post-maintenance valve actuator

testing was neither maintained with the maintenance request

(MR) package nor filed under surveillance data sheet,

3.M.4-10C. .This was subsequently confirmed by the DCC staff.

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The inspector noted that post-maintenance test records, e.g.

local leak rate testing and motor operator testing, were not

always available in the licensee's document control center.

Although the records could ultimately be produced, the

inspector questioned whether the maintenance test results are

maintained as a quality assurance record (i.e., storage,

preservation, and safekeeping) and are processed into the

Nuclear Records Management System in a timely manner, as

required by the Boston Edison Company Quality Assurance Manual

(BQAM), Chapter 17. At the exit meeting, the licensee agreed

to review these concerns.

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Feedwater Check Valves - All four feedwater check valves were

removed for maintenance to correct excessive back leakage. It

was found while inspecting the valves for repair, that 17 of 32

wrist pin bushing tack welds may have been cracked. However,

none of the bushings, which permits rotation of the check valve

disk on the wris- pins, were able to be moved by hand. A

design change to eliminate the bushing tack welds for the Anchor

Darling feedwater check valves is planned prior to the valve

installation. At the exit meeting, the inspector questioned

the potential reporting requirement for this problem under 10

CFR 21. The acceptability of licensee actions is unresolved

(8C-25-03).

e. Surveillance Testing

The inspector observed tests to assess performance in accordance

with approved procedures and LCO's, test results, removal and

restoration of equipment, and deficiency review and resolution.

During followup of recent containment damper failures, described in

section 3.d of this report, the inspector reviewed the results of

several secondary containment isolation surveillance tests. Proce-

dure 8.M.2-1.5.8.4, Revision 12, Logic System Functional Test of

System B Standby Gas Treatment Initiation, Reactor Building Isolation,

and Outboard Drywell Isolation Valves, was performed on June 26, 1986.

During the test a secondary containment damper failed to fully close.

At that point the test was stopped. Neither restoration of the system

to normal nor independent verification of restoration were documented.

In addition, previous procedure verification steps were not completed

and the operating supervisor and watch engineer review of the test

results were not completed with abnormal test results properly docu-

mented. Failure to verify completed procedure steps and independently

verify restoration of the system following the test is a violation of

procedure 8.M.2-1.5.8.4.

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On July 10, 1986, the inspector observed during the performance of

PNPS Procedure 8.M.2-1.4.1, Revision 12 that the "K2s" and "K7s"

relays were not independently verified, as specified in the

procedure, in the restored energized position. These relays

provided input to the alarm and main steam isolation valve (MSIV)

closure logic, respectively. Upon questioning, the technician was

not aware of the necessity of independently verifying these relays.

Upon further investigation, the same surveillance procedure was

performed on April 5, 1986, and on May 7, 1986 without independent

verification'of the "K2s" and "K7s" relay restoration.

The inspector informed the licensee that failure to adequately

follow procedures as noted in the above examples, constitutes a

violation (86-25-04).

The inspector reviewed surveillance procedures associated with the

H202 analyzer system as described in section 3.b. Other surveillance

testing witnessed by the inspector during this reported period were

HPCI Condensate Storage Tank Level Channel Check, 8.M.2-2.5.6,

Revision 7, Strong Motion Accelerograph Functional Test, 8.M.3-10,

Revision 7, and Reactor Water Level Functional Test, 8.M.1-19. No

discrepancy was observed for these surveillances.

4.0 Review of Plant Events

a. Loss of 480 VAC Bus B-23 and Resulting Half Scrams

The power for Reactor Protection System (RPS) Motar Generator (MG)

set "A" is supplied from Motor Control Center (MCC) B-23. MCC B-23

is in turn supplied through 480 VAC load center breaker B306.

Several times during the report period breaker B-306 tripped,

resulting in loss of powar to RPS MG set "A" and a nalf scram.

Initial performance testing of breaker B306 did not reveal any

performance abnormalities. Supplementary testing at lower current

values identified erratic performance of the breaker overcurrent

trip devices. Preliminary indication is that a missing lock nut on

the "C" phase long time delay trip mechanism may be the cause. The

licensee has shipped all three breaker overcurrent trip devices to

the vendor for root cause analysis and will evaluate the generic

implications of any test results obtained. 1

b. Low Level Contamination of Onsite Sewage Tanks

On July 16, 1986, the reactor building auxiliary bay sewage ejector

pump tank was found to be slightly contaminated. This was

considered by the licensee as a potential unmonitored radioactive

material release path and the system was tagged out for repairs.

Also on July 16, 1986, the licensee initially determined that an

onsite septic tank contained radioactive Cobalt-60 at 1.1E-06

microcuries per milliliter. However, a second sample from this tank

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did not detect any radioactive contamination. Prior to the backup

sample the licensee performed a review which identified possible

sources of contamination into this tank.

The licensee samples the sewage tanks regularly, prior to removing

waste for shipment offsite. Licensee plans are in place for

decontamination of all onsite sewage tanks. Previous traces of

contamination had been detected in onsite sewage tanks and were

reviewed during NRC inspection 50-293/85-22. Sewage pumping trucks

are routinely checked for contamination prior to leaving site. No

activity has been detected in these trucks.

The inspectors aise noted that the licensee is performing a re-review

of IE Bulletin No. 80-10, " Contamination of Nonradioactive System and

Resulting Potential For Unmonitored, Uncontrolled Release to Environ-

ment". The inspectors will review the results of the licensee's

evaluation and any corrective actions during subsequent inspections.

c. ATWS Monthly Functional Test

On July 15, 1986, the licensee notified the NRC via the ENS

telephone line that functional tests for the ATWS (anticipated

transient without scram) system were not conducted in the manner

required by the technical specifications. Specifically, the

licensee's functional test, procedure 8.M.1-29, did not activate the

system primary sensors during the test. Instead, the test injected

test signals directly into the ATWS trip units. The technical

specification definition of instrument functional test requires that

,

the primary sensors be activated.

The technical specification test definition may not be appropriate

for the ATWS instruments because they are Rosement transmitters and

analog trip units. Because of the reliability of these instruments,

the licensee believes that it is common practice to initiate monthly

functional tests at the trip units instead of the primary sensors.

The sensors are normally tested less frequently, i.e., every eighteen

'

months. This minimizes the chances of causing inadvertent reactor

scrams. The licensee is planning to modify the technical specifica-

tions to allow testing in this manner.

The inspector reviewed the QA deficiency report that identified the

'

problem, OR 1559, and the plant's response. The inspector also

verified that the ATWS functional tests were properly scheduled on

the stations Master Surveillance Tracking Program (MSTP). The

inspector discussed the testing problem with licensee personnel and

noted that a similar problem exists for the other analog-trip

devices currently installed, i.e., the scram discharge volume level

, -instruments. The licensee subsequently notified the NRC of the

discharge volume test inadequacy. The inspector had no further

i questions. This item is licensee-identified and will be reviewed

i

during future routine inspections.

I , ,_. - ,- _ _ .- - - - , .

-. . ____ __ ____- ____

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d. Reactor Building Ventilation Sample Pump Failures

On July 17, 1986 the "A" reactor building sample pump tripped due to

pump motor failure. This pump and similar sample pumps are rebuilt

every 3 months because of a history of failures. The other reactor

building sample pump was started when the alarm for the pump trip

was received.

While reviewing the history of this tyoe of sample pump, it was

found that either the wrong number or no equipment number was used

to specify the reactor building sample pump on Maintenance Requests

(MRs) 85-4-68 and 85-628. The correct equipment numbers for the

reactor building sample pumps were P236A and P-2368 according to

1

drawing number M-287. This matter was discussed with the licensee

maintenance personnel.

e. 4160 VAC Safety Bus Undervoltage Relay Calibration Failures

On June 21, 1986 the licensee discovered that surveillance testing

of safety related emergency bus undervoltage relays was overdue. A

discussion of the circumstances leading to the problem is contained

in inspection report 35-21, section 7.0. Followup of the item will

be conducted under unresolved item 85-21-08 as stated in that

report.

,

On July 23, 1986 calibration of the subject relays identified that

eleven of the total population of twenty were outside the calibration

limit. The inspector questioned the acceptability of the current

calibration interval, given the high failure rate. An NRC special

team inspection 86-24, (generic letter 83-28 followup), is evaluating

the adequacy of the licensee's undervoltage protection and

surveillance.

During the review of undervoltage relays at Pilgrim, the inspector

noted that the Low Pressure Coolant Injection (LPCI) valves for both

LPCI loops are pnwered through the same 480 VAC lead center, B6.

Bus B6 can be supplied from either diesel generator through their

associated distribution systems. Two undervoltage relays are

installed on each of these two B6 power supplies. The undervoltage

relays will, if loss of the normal supply is sensed, transfer B6 to

its alternate supply. In order to complete this transfer 125 VDC

control power from bus D6 is required. Bus D6 can be supplied from

either 125 VDC battery "A" or "B". Like 480 VAC bus B6, an auto

transfer from the normal to alternate battery source on loss of

.

voltage is provided for 125 VDC bus D6. These two auto transfer

I functions are critical in supporting the licensees assumptions

regarding available ECCS in the accident analysis. The inspector

noted that these undervoltage relays / functions are not addressed by

technical specifications. Initial indications are that no station

calibration / test procedures are in place. The inspector was informed

_-__ . -, _

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4

that setpoints and testing of these components may be controlled by

the corporate relay test group. This group is not part of the

nuclear organization. The inspector will continue to evaluate the

acceptability of the technical specifications, control, calibrations

and testing of those components during the next inspection period

(86-25-05),

f. HPCI Area Unit Cooler Breaker Fire

On July 28, 1986 smoke was observed coming from breaker 52-1822 in

the reactor building. This breaker supplies power to a High

Pressure Coolant Injection (HPCI) pump compartment unit cooler.

Investigation determined that a circuit lead disengaged from its

terminal block and touched ground. A solid link had been installed

3

rather than a protective fuse in the control power circuit. Because ,

no fuse had been installed the fault was not cleared, and the

control power transformer located in the breaker compartment burned

up. Control of the application of solid links and fuses is the

subject of an ongoing licensee engineering evaluation and is being

reviewed under unresolved item 86-01-03. Previous licensee

indications were that installation of solid links was conservative

because loss of equipment due to spurious fuse failure was

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i eliminated. In response to this incident the inspector pointed out

that a resulting electrical bus fire may not be conservative.

4

The loose lead which caused the fire became disengaged because the

terminal block to which it was secured was cracked. The licensee

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stated that an examination of similar terminal blocks and an

evaluation of the cause of the cracking were being conducted. The

.

inspector will review the licensees evaluation of this matter during

l a future inspection.

g. Protective Instrumentation Rack 2205 Upscale Drift

On July 31, 1986 the licensee noted that all reactor vessel level

instrumentation on instrurint rack 2205 was indicating high. This

instrumentation provides input to the reactor protection system,

emergency core cooling system initiation and primary containment

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isolation system. Indicated level discrepancy between the

instruments on rack 2205 and similar instruments on rack 2206 was

approximately 10 inches. Investigation by the licensee identified

that the reference leg common to all the affected instruments had

partially drained. Daily log information plotted by the inspector

indicates an increasing trend over a number of days for the

instruments in question. Pertinent valve lineups were checked, the

reference leg was backfilled and all indication returned to normal.

The licensee is currently monitoring instrument performance to

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detect any additional problems. The inspector had no further

questions.

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h. Hydrogen Recombiner Safety Evaluation

During the inspection period, the licensee noted that the NRC safety

evaluation dated April 30, 1986, which supports an exemption from

the hydrogen recombiner requirements of 10 CFR 50.44 (c)(3)(ii)

contained statements that did not accurately reflect the condition

of the plant. Specifically, the licensee noted that items 2.b.1 and

2.b.2 in the evaluation might not reflect actual practices at the

plant. These items involve (1) a requirement to shut the plant down

i within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> if the nitrogen supply system (or an alternate

nitrogen system) is not operable and (2) the isolation of the

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instrument air system from the nitrogen supply system by a locked

closed valve.

The inspector discussed the safety evaluation with the licensee and

with the NRR Project Manager. At the end of the inspection period,

the licensee had not completed its review of this issue. This

review will determine which statements are inaccurate and the source

i (licensee or NRC) of any misinformation. The acceptability of the

licensee's actions are unresolved pending the completion of the

licensee's review (86-25-06)).

i 1. Intermediate Range Neutron Monitors

Based on a General Electric (GE) Rapid Information Communication

Services Information Letter (RICSIL) Number 007, the licensee

investigated and found an undetected failure mode of the neutron

intermediate range monitors (IRMs) that may not provide the reactor

protection system scram during startup. Specifically, loss of the

IRM negative power supply voltage will not cause an inoperable IRM

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trip card light, but will cause a signal output from the amplifier.

This causes the IRM to lock above the downscale trip and below the

upscale trip regardless of the actual core neutron flux.

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, GE is examining a relay / contact modification, which would monitor

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the IRM negative power supply and would initiate an inoperable trip

light if a loss of power occurs. The results of GE's final

recommendation will be in a GE Services Information Letter.

i The unit is currently in an outage and reactor power operations are

!

not anticipt.ted until the first quarter of 1987. The resolution of.

this problem will be reviewed during a future routine inspection

(86-25-07).

, 5.0 Observation of Physical Security

,

On July 23, 1986 the inspector received an anonymous allegation concerning

excessive security force overtime. On July 24, 1986 the inspector reviewed

security force time sheets for the period June 16, 1986 through July 20,

1986. This period began after the end of the Boston Edison labor union

, 4 m - - -m-+ < - - . - - , - -s.- e-*a - .- ,p

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strike. In order to focus on the routine schedules maintained by the

normal security guard force, time immediately before, during and after

the security force labor action of June 30, 1986 was not considered. A

summary of individual cases of excessive overtime identified is included

as Attachment II to this rerort.

The inspector noted during the review that security per:onnel routinely

work up to twenty-e'qht hours in a forty-eight hour period. Instances of

up to thirty-si. . cues in a forty-eight hour period were also identified.

One individual tm ked twenty-three of twenty-seven hours. The time

onsite for individuals in twenty-four and forty-eight hour periods is not

monitored by the licensee.

Cases of up to eighty-eight hours worked in a seven day period, with

individuals on duty as many as ten consecutive twelve hour days, were

identified. While the licenses does monitor time worked in a seven-day

period, only the seven-day periods starting Monday and ending Sunday are

reviewed.

The excessive number of security force overtime hours raises concern

regarding the ability of individuals to perform their function. The

inspector discussed these observations with licensee corporate and

station management. The licensee immediately reviewed the overtime

status for onshift security personnel and took steps to reduce or

eliminate the overtime problem. Security overtime was subsequently

discussed during an NRC Management meeting (50-293/86-26) and also

reviewed during a security specialist inspection (50-293/86-26). The

corrective actions will be reviewed during a future inspection

(86-25-08).

6.0 Radiation Protection and Chemistry

Radiological controls were observed on a routine basis during the

reporting period. Standard industry radiological work practices,

conformance to radiological control procedures and 10 CFR Part 20

requirements were observed. Independent surveys of radiological

boundaries and random surveys of nonradiological points throughout the

facility were taken by the inspector.

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7.0 Station Fire Barrier Deficiencies

During 1985 a series of fire barrier walkdowns were conducted to verify

that the required Appendix R barriers provide a minimum 3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> fire

resistance. Nineteen specific deficiencies were identified. On July 2,

1986 a memorandum summarizing these deficiencies was transmitted from the  ;

nuclear engineering department to the station. This memorandum '

recommended that compensatory fire watches be implemented. The results

of the walkdowns were received at the site on July 2,1986. On July 8,

1986 a Failure and Malfunction Report was initiated to officially ,

identify the problem and initiate corrective actions. The licensee is i

reviewing its records to determine whether compensatory fire watches were

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established in 1985. The inspector will review the individual discrepancies,

and any compensatory measures taken, to determine compliance with the

technical specifications during a future inspection (85-25-09).

Boston Edison Quality Assurance Manual (BEQAM) Section 16 establishes the

corrective action program, and requires that deficiencies be identified

and processed in accordance with Section 15 of the BEQAM. Section 15

states that nonconforning components are documented and reported via a

Failure and Malfunction Report (F&MR). PNPS procedure 1.3.24, Revision

12, Failure and Malfunction Reports states that an F&MR shall be

initiated whenever any abnormal plant condition has the potential to

adversely affect safe operations.

1

Timely and effective processing of an F&MR is important in establishing

operations staff awareness of potential or actual problems. Technical

specifications require establishment of a fire watch within one hour of

finding an inoperable fire barrier. Failure to effectively use the

corrective action program both as the individual discrepancies were

identified, and after the summary of discrepancies was compiled on

July 2, 1986, demonstrates a programmatic weakness. The inspector

informed the licensee that the above constitutes a violation of 10 CFR 50

Appendiv B (86-25-09).

8.0 Local Leak Rate Testing Status

During this reporting period, I type "B" as-found local leak rate test

(LLRT) failure was found. The outboard flange of the inboard drywell

purge exhaust valva had leakage greater than 20 sim. This leakage

will be quantified prior to its repair work. Also 3 type "C" as found

LLRT failures were found, i.e., the outboard drywell purge exhaust valve,

the inboard post accident sample system (PASS) return valve, and the

inboard drywell equipment drain valve. Between August 4,1986 and

April 11, 1986, 87 of approximately 101 type "B" components have been

tested with 2 failures, and 123 of approximately 133 type "C" components

have been tested with 15 failures.

During conduct of leak rate testing on the containment floor drain sump

isolation valves the inspector noted that while two LLRTs had been

performed on that day, no test cart bypass valve leak test had been

performed as required by procedure. This concern had been previously

identified by the inspector and discussed with licensee personnel. While

the significance of the incidents is minor, the licensees failure to

correct them raises concern. The inspector discussed this problem at the

exit meeting.

9.0 Independent Verification of Operating Activities

The inspector reviewed fifty eight administrative, operations,

maintenance, and surveillance procedures to determine if the licensee

established an acceptable system of verifying the correct performance of

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17

operating activities. The procedures were reviewed against Section

5.2.6, " Equipment Control", of ANSI N18.7, 1976 as supplemented by NUREG

0737 item I.C.6, " Guidance on procedures for verifying correct

performance of operating activities". The inspector determined that,

with the exception of the tagging procedure, the licensee had revised the

procedures to provide for independent verification. The inspector found

that precedure no. 1.4.5, "PNPS Tagging Procedure", Revision 16, was

inadequate in that it did not require independent verification when

hanging tags or during tag removal / equipment restoration. Similar

problems were also noted in inspections 50-293/85-03 and 86-06. The

licensee informed the inspector that a revision to the tagging procedure

was being prepared which would include independent verification of

tagging activities and the inspector was shown the proposed tag record

which would implement it. The inspector found the propcsed revision

acceptable and will review the revised tagging procedure in a subsequent

inspection.

The inspector also had a concern regarding the implementation of the

independent verification program. As noted in paragraph 3.e of this

report, a violation for failing to perform an independent verification

when required was identified. During discussions with licencee

personnel, the inspector also noted some confusion as to which systems

required independent verification. The inspector noted that procedure

no. 2.1.11, " System Lineup File", is the only procedure which identifies

systems requiring independent verification. However, this procedure is

used for valve lineups after refueling outages and is not used by other

than operations department personnel. The licensee acknowledged the

inspector's concern and indicated that the controlling administrative

procedure (procedure no.1.3.34 " Conduct of Operations") would be revised

to reference procedure 2.1.11. The licensee also indicated that

procedure no. 1.3.34 would be revised to include the management

objectives as stated in memorandum M85-137, Control and Verification of

Operating Actions, as additional guidance on implementation of the

independent verification program.

The inspector informed the licensee that the revised 1.3.34 and 1.4.5

procedures would be reviewed during a subsequent inspection and would be

necessary to complete the licensing action review for NUREG 0737, item

I.C.6.

10.0 Review of LER's

LER's submitted to NRC:RI were reviewed to verify that the details were

clearly rerorted, including accuracy of the description of cause and

adequacy of corrective action. The inspector determined whether further

information was required from the licensee, whether generic implications

were indicated, and whether the event warranted onsite followup. The

following LER's were reviewed:

. _ _ _ _ _ _ _ _ _ _

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LER No. Event Date Report Date Subject

86-13 5/30/86 6/30/86 Use of non-seismic CFD

relays for D/G

differential protection

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86-14 6/10/86 7/9/86 Insufficient once per

cycle RCIC surveillance ,

procedure '

86-15 6/13/86 7/14/86 Primary containment

local leak rate test i

frequency

86-16 6/21/86 7/21/86 Bus AS, Bus A6, and

Startup degraded >

' voltage relay

calibrations overdue'

The following deficiencies in LER 86-13, "Use of Non-Seismic General

Electric Type CFD Relays", were noted:

--

The LER indicates that operator action will be initiated by

non-seismically qualified annunciators after a seismic event.

--

The LER did not clearly indicate that a General Electric evaluation

of a short-term station blackout was not completed until 1986, two

years after the relay problem was identified.

--

The LER indicated that no failure (presumably spurious activation)

of the CFD relays had occurred in thirteen years. However, this

statement may be inaccurate because spurious activations of the

relays would probtbly not have been logged.

This event was also reviewed during NRC inspection 86-14. l

The event described in LER 86-14, " Primary Containment Local Leak Rate

Test Frequency", was discussed in NRC inspection 50-293/86-21. The

adequacy of licensee surveillance test scheduling methods is currently l

unresolved and will be tracked under open item 86-21-08. The inspector l

noted two deficiencies with the LER:

--

The LER stated that containment local leakage tests were previously ,

scheduled on a " program basis". However, the scheduling method '

(i.e., " program basis") was neither explained nor justified in the

'

LER. This description is needed to explain why there was an

apparent conflict between the licensee's scheduling method,10 CFR

50 Appendix J scheduling requirements, and technical specification

scheduling requirements.

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--

The technical specifications have two definitions of ope : ting

cycle. The LER only mentions the less restrictive defin. Lion

(definition "0"). The leakage tests in question were not overdue

using this definitior.. However, if the more restrictive definition

(definition "U") is used, the tests would have been overdue. The

LER should justify using the less restrictive case.

The licensee stated at the exit meeting that the deficiencies identified

by the inspector would be reviewed and the LER's appropriately updated.

]

! The events described in LER 86-16, " Bus A5, Bus A6, and Startup Degraded

Voltage Relay Calibrations Overdue", were initially reviewed during NRC

inspection 50-293/86-21. A followup review is descr9,ed in Section 4.e

,

of this inspection report. No problems were identified. An LER update

will be required if the as-found calibrations of the relays are outside

the plant design bases.

11.0 Confirmatory Action Letter 86-10 Update

Attachment III lists followup NRC questions concerning issues in

Confirmatory Action Letter (CAL) 86-10. These questions were discussed

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between the licensee and the inspector. The preliminary licensee

response was also discussed during a telephone call on July 31, 1986

between the licensee, the inspector, and Region I management. At that

time, the licensee agreed to submit a written response to the questions

to Region I within 30 days of the telephone call. The response will be

reviewed during future followup of CAL 86-10.

O

12.0 Congressional Staff and NRC Commissioner Visits to Pilgrim

1

Members of the congressional staffs of Un,ited States Senator Kennedy,

Senator Kerry, and Congressman Studds toured the Pilgrim site on July 10,

1986. They met with Boston Edison representatives and the Pilgrim

.

resident inspectors during the afternoon. A congressional heering

!

concerning problems at Pilgrim and selected other U.S. power reactors was

held the following week.

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l' On July 14, 1986, NRC Commissioner J. Asselstine and the NRC Region I

Administrator, Dr. T. Murley, also toured the Pilgrim site. Prior to the

tour, they met with the Pilgrim resident inspectors, Boston Edison

officials and local public officials. Commissioner Asselstine held a

press conference at the end of the day. Among the topics discussed

during the tour were deficiency stickers located by the control rod

select panel in the control room, the status of preventative mainterance

for the onsite liquid nitrogen storage tank, and the status of

preoperational testing of the air filtration system for the Emergency

Offsite Facility (EOF). Licensee plans for completing required fire

protection modifications were also reviewed.

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The deficiency stickers in the control room indicated that maintenance

requests had been issued to repair control rod position indication probes

(PIPS). These problems were generally limited to one or two positions on

an individual control rod. The inspectors had previously verified that

the control rod position problems had not prevented the licensee from

conducting required control rod scram tests. The Pilgrim technical

specifications allow PIP's to be out of service as long as redundant

nuclear flux instrumentation is operable.

The licensee indicated that the PIP problems were scheduled to be fixed

during the next refueling outage, when all PIP connectors undervessel

would be changed out. At the time of the discussions, the next refueling

outage was scheduled to start in January 1987. The licensee justified

not fixing the PIPS during the current shutdown, because much of the work

would have to be duplicated during the subsequent PIP connector

changeout, causing over 10 person-rem of duplicated radiation exposure.

The inspector questioned whether some of the indication problems, e.g. ,

no full-in indication, could be caused by faulty light sockets in the

control room. These problems could be fixed immediately. The licensee

rev'ewed the work and stated that the sockets were functioning normally

indicating that the problems will require undervessel repairs. Based on

a review of the maintenance requests and discussions with the licensee

about the nature and scope of planned undervessel work, the inspector

agreed with the licensee's decision to defer the PIP maintenance until

the PIP connectors are changed out.

Subsequent to their announcement to extend the current outage into 1987

BECO decided to fix the PIP problems prior to restart.

13.0 Management Meetings and Meetings with Local Groups

At neriodic intervals during the course of the inspection period,

meetings were held with senior facility management to discuss the

inspection scope and preliminary findings of the resident inspector. No

written material was given to the licensee that was not previously

available to the public.

On July 30, 1986 a meeting between Region I and Boston Edison senior

management was conducted at Region I offices in King of Prussia. The

purpose of the meeting was to discuss licensee management program

improvements and plans for the upcoming plant outage. The meeting is

summarized in NRC Inspection Report 50-293/86-26.

The Pilgrim Senior Resident Inspector addressed a special meeting of the

Plymouth Area Chamber of Commerce on July 23, 1986. The meeting was held

at the request of the Board of Directors of the Chamber of Commerce to

discuss recent activities at Pilgrim. Representatives from Boston Edison

and a local public interest group, Plymouth County Nuclear Information

Committee, also participated in the meeting. The meettna was held in

Memorial Hall in Plymouth.

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j Attachment I to Inspection Report 50-293/86-25

Persons Contacted

L. Oxsen, Vice President, Nuclear Operations ,

j, *A. Pedersen, Nuclear Operations Manager

l P. Mastrangelo, Chief Operating Engineer

j D. Swanson, Nuclear Engineering Department Manager

i K. Roberts, Director Outage Management

.

N. Brosee, Maintenance Section Head

T. Sowdon, Radiological Section Head

,

J. Seery, Technical Section Head

E. Ziemianski, Management Services Section Head

) S. Wollman, On-Site Safety and Performance Group Leader

i B. Eldridge, Acting Chief Radiological Engineer

R. Sherry, Chief Maintenance Engineer

J. McEachern, Resource Protection and Control Group Leader

i E. Graham, Compliance and Administrative Group Leader

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{ * Senior licensee representative present at the exit meeting.

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, Attachment II to Inspection Report 50-293/86-25

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Security force overtime records were reviewed for the period of June 16 to

July 20, 1986. Overtime hours worked in connection with the security force

and Boston Edison union strikes were not included.

A. Seven Day Work Period

Work Period Hours Worked Comments

6/19 - 6/25 84 This individual worked 10

consecutive 12-hour days

6/20 - 6/26 84

6/20 - 6/26 84

6/20 - 6/26 88 This individual worked 8

twelve and one 16-hour days

consecutively

7/3 - 7/9 80

7/3 - 7/9 80 A single individual in two

-

7/10 - 7/16 80 consecutive weeks

,

7/5 - 7/11 78

7/5 - 7/11 88

7/5 - 7/11 88

<

7/6 - 7/12 76

7/11 - 7/17 80

B. Two Day Work Period

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Work Period Hours Worked Comments

, 7/6 - 7/7 32

7/14 - 7/15 36 This individual worked 39

hours in a 51-hour period

7/18 - 7/19 32 This individuai worked 40

hours in a 56-hour period  ;

6/16 - 7/20 28 During the period specified 14

different individuals worked l

28 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br /> in a 4,-iour period '

C. fwenty-four Hour Period

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Work Period Hours Worked Comments

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7/14 - 7/15 20 In a 27 hour3.125e-4 days <br />0.0075 hours <br />4.464286e-5 weeks <br />1.02735e-5 months <br /> period this

individual worked 23 hours2.662037e-4 days <br />0.00639 hours <br />3.80291e-5 weeks <br />8.7515e-6 months <br />'

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ATTACHMENT III

NRC QUESTIONS REGARDING THE SUPPLEMENTAL RESPONSE -

TO CAL 86-10

The following is a list of comments and questions from NRC Region i

about the BECo supplemental response letter, dated June 16, 1986, to

CAL 86-10. This list was given to the licensee on July 21, 1986.

1. Has BECo evaluated the merits of periodic checks of RHR

system pressure and temperature after (1) startups, (2)

any RHR system high pressure alarm, or (3) after the

leakoff system is initially placed in service? Also, has

BECo considered periodic checks of RHR system pressure

in the absence of high pressure alarms?

2. The first paragraph of BECo's response to NRC question

"e" describing the proposed leakoff method appears to

differ from the method in procedure TP 86-85 and should

be clarified. The paragraph infers that the bypass valve

will be opened during a measurement step, closed, and

reopened to establish the leakage path.

3. Will a reactor shutdown just be intitiated or will the

plant be shutdown (pending an engineering evaluation) if i

the 1.0 gpm limit is exceeded? Also, has BECo considered

evaluating leakage rates above 1.0 gpm now; rather than

waiting to conduct the evaluation until the leakage limit

is exceeded?

4. The BECo response and the associated safety evaluation

state that leakage into the RHR system will not be

allowed to exceed 1.0 gpm. This is not strictly true,

since the measured parameter will be leakage through the

bypass valve at 150 psig. Changes in RHR check valve

leakage (such as after a pump has been operated) could

make the leakoff measurements inaccurate and misleading.

Has this been considered? Has BECo considered tracking

the leakage rate into the torus over extended periods of

time as a method of verifying stable RHR system

inleakage?

The safety evaluation also states that all RHR pump flow

will go into the RHR system. However, some flow could be ,

diverted through the leakoff path if the "D" pump is idle

(LPCI only requires 3 pumps operate). BECo should

consider modifying the safety evaluation to address these

two Concerns.

5. The data sheet to procedure TP 85-A2 requires that an RHR

pump suction block valve (MO-1001-7D) be closed during

the initiation of a controlled leakage path but not

reopened (although the procedure does require this). Why

has the latter step been left off the data sheet?

6. The acceptance criteria for tests of the RHR injection

check valves are not included in the response, as

requested (NRC question "f"). The criteria should be

determined and submitted to Region I.

7. The RHR pressure guage calibration frequency was stated

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to be "once per refueling outage" in the response to

question "h." This frequency is not defined in the

technical specifications. How is it defined and what is

the justification for the frequency?

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8. The calibration histories of the RHR high system pressure

alarm switches (PS-1001-74A and B) should be submitted to

Region I. How is the proposed calibration frequency,"once

per cycle," defined and justified?

9. Will the 1001-28 or 29 valve on the "A" RHR loop be

maintained normally closed? Procedure TP 86-84 indicates

that the -28A valve will be left closed, but the licensee

has previously indicated that the 28A will be open and

the 29A closed.

10. What is the accuracy and reliability of the temperature

measuring markers? What specific change in temperature

will require that additional measurements be taken with a

portable measuring device? What are the accuracy and

reliability of the portable temperature measuring device?

11. Will the licensee verify seating of the RHR check valves

after operation? If not, why not?

12. Why will it take 9 months to submit a technical

specification change to reduce compensatory surveillance

testing in LCO's; considering that the issue was

identified mid-1985 in connection with the on-line EQ

modifications and also noted in the 1985 SALP report? Has

the licensee considered contacting other facilities of a

similar age to see if they have information that could be

used to speed the evaluation and submittal process?

13. What is the justification for limiting RHR pipe

temperature to no less than 15 degrees of saturation

temperature? Is this temperature margin adequate,

considering that pipe wall temperature (rather than

interior water temperature) is the measured parameter?

14. Calculation M-269 should be submitted to Region I for

review.

15. The following comments concern the draft procedure TP

86-81 which will control the test for spurious group I

primary containment isolations during the neFl reactor

startup.

-- Will reactor level instrument vibration be

monitored? If not, why not?

-- Step VI.A indicates that the reactor mode switch

will be placed in run for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Why?

-- Was a functional test be conducted of the PCIS

logic after the GETARS modification was installed?

What procedure was used for the functional test?

-- Can the spurious isolation test be conducted at a

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power below the stated 30%?

16. Does BECo plan to conduct a sampling review of other

systems, given the large number of drawing / loose wire

problems discovered during werk on the reactor mode

switch?

17. Why is local venting of the RHR system needed in addition

to the keep fill system?

18. Is the RHR system always filled and vented after the

1001-34 and -36 valves are opened to depressurize the

system?

19. Has BECo considered the personnel safety aspects of the

leakoff measu>ement process? At what location will system

pressure be measured and what will be the expected water

pressure at the measuring point? Will the measurement,

equipment withstand this water pressure?

20. Has BECo considered testing the leakage of injection

check valves in ECCS systems other than LPCI?

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