ML20153A858

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Insp Rept 50-293/87-57 on 871207-880119.Violation Noted. Major Areas Inspected:Plant Operations,Radiation Protection, Physical Security,Plant Events,Maint & Surveillance.One Unresolved Item Identified
ML20153A858
Person / Time
Site: Pilgrim
Issue date: 03/11/1988
From: Blough A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20153A853 List:
References
TASK-2.E.4.2, TASK-TM 50-293-87-57, IEB-79-08, IEB-79-8, IEIN-87-030, IEIN-87-30, NUDOCS 8803210189
Download: ML20153A858 (30)


See also: IR 05000293/1987057

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                                                              V. S. NUCLEAR REGULATORY COMMISSION-
                                                                                REGION I
                  . Docket / Report No.                   50-293/87-57
                   Licensee:
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                                                         _ Boston Edison Company
                                                          800 Boylston Street
                                                          Boston, Massachusetts 02199
                   Facility:                              Pilgrim Nuclear Power Station
                   Location:                              Plymouth, Massachusetts
                   Dates:                                 December 7, 1987 - January 19, 1988
                   Inspectors:                            C. Warren, Senior Resident Inspector
                                                          J. Lyash, Resident Inspector
                                                          T. Kim, Resident Inspector
                   Approved By:                                                                                                                                1/ h cI8
                                                          A. Randy Bt6 ugh, Chie,f                                                                                 Date
                                                          Reactor Projects Section No. 3B
                   Areas : Inspected:                 Routine res. dent inspection of plant operations, radiation
                   protection, physical security, plant events, maintenance, surveillance, outage
                   activities, and reports to the NRC. The inspection consisted of 350 hours of
                   direct inspection. Principal licensee management representatives contacted are
                   listed in Attachment I.                           Observations made by the NRC Region I, Regional
                   Administrator during a tour on December 8,1987 are documented in Attachment
                   II of this report. A copy of Attachment II was provided to licensee management
                   for followup.
                 'Results:
                   Violation: Repeated occurrences of locked high radiation area doors being left
                   open and unattended were identified by the licensee. Problems with high radia-
                   tion-area access control have been previously identified and were the subject
                   of . violations during inspections 50-293/87-03 and 50-293/87-11'.                                                                              Corrective
                   actions taken in response to these findings have not prevented their
                   recurrence. (Section 3.b, VIO 87-57-01)
                   Unresolved Item:                  The licensee identified that two reactor vessel level gauges                                                                            .
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                   were incorrectly installed. A licensee investigation is currently ongoing to
                   determine the cause and to assess the adequacy of post installation test.

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                   (Section 4.d, UNR 87-57-02)
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              8803210189 880311
              PDR         ADOCK 05000293
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                  Inspection Results-(Continued)
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                  Concerns:
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                - 1.    The ~ licensee. experienced safety rele+.ed equipment malfunctions upon
                        receiving ~ a spurious reactor- scram ' signal 'on January 17, 1988. -(Section
                        4.d)
                  2.    Inadequa'te procedures and planning of - surveillance tests resulted in un-
                        necessary engineered safety feature actuations. (Section 3.a)
                  3.    Poor preplanning and control of maintenance was noted during an-electrical
                        relay replacement. A similar problem was the subject of a violation dur-
                        ing inspection 50-293/87-50. (Section 4.c)
                  4.   Weak identification and tracking of lifted leads and jumpers led to a
                        water spill in the.high pressure coolant injection system room 'during the
                        integrated leak rate test.    (Section 6.0)
                  5.    The prelube' pump for the "B" emergency diesel generator failed to. restart
                        during a surveillance test. An identical failure occurred during a loss
                        of offsite power event on November '12,1987.. Licensee followup appeared
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                        adequate but the failure root cause has not been identified.          (Section
                        3.b)
                  6.    The inspectors evaluated the erosion of construction dirt into wetlands
                        area. The inspector's independent survey of the area, and the licensee's
                        analyses indicate that the level of activity does not represent a health
                        or safety concern. However, the material should not be allowed to erode.
                        (Section 3.c)
                  Strengths:
                  1.    The licensee's preparation and execution of the reactor vessel hydrostatic
                        test was well organized and controlled.     (Section 5.0)
                  2.   .The licensee's response to a January 17, 1988 reactor scram signal and
                        subsequent equipment malfunctions was prompt, thorough and effective.
                        (Section 4.d)
                  3.    Using non-nuclear steam for testing of high pressure coola1t injection
                        system and reactor core isolation cooling system enabled the licensee to
                        discover problems which may not have been easily identifiable using
                        nuclear steam due to radiological conditions.      (Section 3.b)

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                                                                 TABLE OF CONTENTS
                                                                                                                                  Page
                 1.  . Summary of Facility' Activities ........................                                                     1
                 2.   Followup on Previous Inspection Findings ..............                                                       1
                 3.   Routine Periodic Inspections ..........................                                                       4

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                      a.       Surveillance. Testing
                      b.     ' Radiation Protection and Chemistry                                                                                _
                      c.       Fire Protection
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                 4.   Review of Plant Events ................................                                                      15
                      a.      . Spurious Isolations of RHR Shutdown Cooling System
                      b.       Reactor Water. Cleanup System-Spurious' Isolation
                      c.     -Engineered Safety Feature Actuations Due to a
                                  Failed Logic Relay                                   .
                     'd,       Spurious Reactor Protection System Actuation
                 5.   Review of Reactor Vessel Hydrostatic Test Procedure
                         : a nd - Te s t ' Re s u l t s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .  19
                 6.   Integrated Leak-Rate Testing ..........................                                                      21
                 7.   Licensee Nuclear Organization Managenant
                          Realignment .........................................                                                    23
                 8.   Management Meetings ...................................                                                      24
                 Attachment I - Persons Contacted
                 Attachment AI - Regional Ad:ninistrator's Tour Observations
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                                                           DETAILS
                     1.0 Summary of Facility Activities
                          The plant was shutdown on April 12, 1986 for unscheduled maintenance. On
                          July 25,1986, Boston Edison announced that the outage would be extended
                          to include refueling and ' completion of certain modifications. The reactor
                          core was .defueled on February 13, 1987. The licensee completed fuel re-
                          load on October 14, 1987. Reinstallation of the reactor vessel internal
                          components and the.vessei head was also subsequently completed.
                          During this report period, the licensee performed the reactor' vessel
                          hydrostatic test and the primary containme- . integrated leak rate -test
                          (ILRT) as described in Sections 5.0 and 6.0. On December 9, 1987, Pilgrim
                          Station conducted a partial participation emergency preparedness exercise.
                          On December 14, 1987 the licensee announced as part of a planned manage-
                          ment realignment, the appointment of eight managers to key management
                          positions in the licensee nuclear organization at Pilgrim Station.          The
                          details of the management realignment are described in Section 7.0.
                          NRC inspection activities during the report period included: 1) observa-
                          tion of the licensee's annual emergency preparedness exercise on
                          December 9, 1987, 2) NRC Reactor Operator Licensing examinations were
                          administered to eight candidates on the week of December 7, 1987, 3) ob-
                          servation of the primary containment ILRT and review of the test results
                          during the week of December 21, 1987.      The results of these inspections
                          are documented in inspection reports      50-293/87-54, 50-293/87-56, and
                          50-293/87-58. In addition, representatives of the NRC's Office of Inves-
                          tigation were onsite December 3, December 7, and December 8, 1987 to
                          interview onsite security personnel.         On December 8, 1987, the NRC
                          Regional Administrator for Region I, Mr. William T. Russell, toured the
                          plant      with    the   resident      inspectors.     On   January 7, 198,8,
                          Dr. Thomas E. Murley, Director of the Office of Nuclear Reactor Regulation
                          (NRR) and other NRC representatives toured the plant with the resident
                          inspectors.
                     2.0 Followup on Previous Inspection Findinjs
                          (Closed) Unresolved Item 82-E4-02 - Discrepancies in the Licensee's
                          Response to IE Bulletin 79-08
                          Previous reviews of this item are documented in the inspection reports
                          50-293/82-30, 50-293/83-01, 50-293/83-14, and 50-293/84-26.      IE Bulletin
                          (IEB) 79-08 ano the TMI Action Plan Item II.E.4.2 required licensees to
                           review the containment isolation initiation cesign and procedures to
                          ensure proper initiation of containment isolation, upon receipt of an
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                          automatic containment isolation signal.          The licensee provided the
                          results of their review in letters dated April 25, and August 21, 1979.
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                   The licensee stated that the RBCCW supply and return lines, instrument air
                   line, RHR to spent fuel pool cooling tie line, and torus make ' up line
                   would be manually isolated and that station procedures would specify the
                   requirements for manual isolation if a containment isolation signal was
                   received. Thit was documented as acceptable by NRC:NRR in letters to the
                   licensee cated December 18, 1979 and April 3, 1980. However, an inspector
                   identified that manual isolation of these lines with qualified valves is
                   not possible. Any valve which is used for primary containment isolation
                   must meet Seismic Class I (FSAR section 12.2) and applicable 10 CFR 50,
                   Appendix J, containment leakage testing criteria. Further, if manual
                   operation of a valve is required to effect containment isolation, the
                   isolation point for the valve must also be accessible under those condi-
                   tions which make its use necessary.
                   In response to the inspector's questions, the licensee re-evaluated their
                   response to the IEB 79-08 and TMI Action Plan Item II.E.4.2, and concluded
                   that isolation of these lines is assured by the .use of Seismic Class I
                   check valves.    The licensee also agreed that isolation for the RBCCW
                   supply .line, instrument air line, RHR to spent fuel pool cooling tie line,
                   and torus makeup line cannot be performed by manual valve closure.        The
                   RBCCW return line from the drywell can meet the isolation valve criteria
                   with MOV-4002 which is seismic class I, local leak rate tested and can be
                   closed by a control switch located in the main control room. The licensee
                   subsequently submitted a supplemental response to IE Bulletin 79-08 and
                   TMI Action Plan Item II.E.4.2 on October 24, 1984 correcting the previous
                   response.   The inspector reviewed the supp'emental response and verified
                   that the contents were consistent with the conclusions drawn from the
                   licensee's re-evaluation and the FSAR. Both RBCCW supply line and instru-
                   ment air line are considered Class C lines in Section 7.3 of the FSAR
                   since they penetrate containment but have no interaction with the primary

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                   containment free space or the reactor vessel. According to the original

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                   design criteria, a single check valve is provided to attain isolation for
                   a Class C line. These check valves are seismic class I and local leak
                   rate tested. The inspector reviewed the results of local leak rate test
                   data for these check valves which were performed on June 12 and July 26,
                   1987 and found no discrepancies.       The torus makeup line is identified as
                   Class B in Section 7.3 of the FSAR.       The torus makeup line is non-essen-
                   tial and ties the condensate transfer system into the RHR test line, which
                   penetrate primary containment and ends below the torus water level. Ft e
                   water-sealed Class B lines such as the torus makeup system, the original
                   plant design bases allow one isolation valve in addition to the water seal
                   to meet isolation requirements. Also, the Safety Evaluation by the NRR on
                   Appendix J Review indicate that Type C testing is not required for valves
                   in lines which terminate below the level of the suppression pool. As for
                   the RHR to spent fuel pool line, the licensee revised the operating pro-
                   cedures 2.2.85, Fuel Pool Cooling and Filtering System, prohibiting the
                   use of the RHR to spent fuel pool lines except in cold shutdown.          The
                   inspector had no further questions.      This item is closed.
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                   (Closed) Inspector Follow Item (IFI 87-27-02) - Cracking of Surge Ring
                  Brackets in Large GE Motors
      v           On July ' 2, 1987, IE Information Notice 87-30, Cracking of Surge Ring
                  Brackets in large GE motors, was issued. . The purpose of the notice was
                  to alert recipients of a potential for failure of. surge ring brackets and
                  cracking of felt blocks in l a rge , vertical electric motors' manufactured
                  by General Electric Co. Felt blocks are used in large electric motors to
                 . keep the windings separated where they loop back at the end of the . stator.
                  The blocks are attached to a surge ring that is held in place by L-shaped
                  surge ring brackets welded to the surge ring and bolted to the motor cas-
                   ir g. . Failure of these surge ring brackets and cracking of the felt blocks
                  allows movement and wear of the end-turns, leading to a reduction in
                  insulation resistance and possible - motor failure.        In addition, broken
                  pieces of the surge ring bracket may enter the space between . the stator
                  and the rotor, resulting in electrical or mechanical motor degradation.
                  Following an investigation to determine the applicability of the subject
                  notice to the Pilgrim Station, the licensee found that RHR, core spray,
                  and recirculation pump motors were potentially . af fected. RHR and core
                  spray pump' motors were overhauled on site by GE under contract with the
                  licensee in 1986.     The surge ring brackets were not inspected during the
                  overhaul.     However, small cracks were found on the "A" and "C" RHR pump
                  motor winding felt blocks. The amount of cracking found was dispositioned
                  by GE to be acceptable and a normal phenomenon found in form-wound motors.
                  On July 27 through August 5, 1987, GE performed a surge ring bracket
                  inspection of the RHR and recirculation pump motors using a boroscope with
                  the motors in place. The inspection of the RHR motors (A thru D) revealed
                  absence of cracks on the surge ring brackets. During the inspection of
                  the "B" recirculation pump motor, it was noted that the recirc motor surge
                  ring bracket construction is of the bolt and stud design, whereas the RHR
                  and core spray motor brackets are of the L-shaped design. The L-shaped
                  design configuration is known to have the potential of cracking, accoroing
                  to the IE Notice 87-30 and the GE letter to the licensee dated
                  July 14, 1987.
                  During the week of October 26,1987, "B" core spray pump motor was dis-
                  assembled and the surge ring brackets inspected by G.E. Due to the geo-
                  metry of the core spray pump motor internals, there is limited access for
                  the bore scope, therefore, this inspection could not be accomplished with-
                  out partial disassembly of the estor. It was verified that the design had
                  12 brackets per surge ring and two surge rings for the top end turn assem-
                  bly and two surge rings for the bottom end turn assembly.          None of the
                  brackets had indications of cracking. The licensee scheduled the inspec-
                  tion of tne "A" core spray pump motor during the next outage because of
                  scheduling conflicts. The licensee indicated that based on the inspection

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              results of the RHR and "B" core spray pump motors, postponement of the "A"
              core spray pump motor inspection is justified.       The licensee also added
              that the number of operating hours and starts are similar between the A
              and B core spray pump motors since both core spray systems' testing and
              surveillance requirements are similar.         The inspector had no further
              questions. This item is closed.
              (Closed) Unresolved Item 87-45-05 - Failure to Issue Licensee Event
              Reports
              In inspection report 50-293/87-45 the NRC identified three engineered
              safety feature actuations which appeared to be reportable under 10 CFR
              50.73 but had not been reported by the licensee.       The licensee reviewed
              the three actuations, agreed that they should have been reported and
              agreed to issue License Event. Reports (LER) to document the occurrences.
              In addition the licensee agreed to perform a review of previous actua-
              tions to determine if any additional reports were needed.
              During this inspection period the licensee's compliance section conducted
              a review of all Failure and Malfunction Reports (F&MR) issued from April
              1986 through the present. This review identified four F&MRs that fit the
              description of an ESF actuation under the current BECo interpretation of
              NUREG 1022. The licensee will submit LERs to document the following ESF
              actuations at a later date.
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                    4/28/87   Initiation signal to both Emergency Diesel Generators (EDG)
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                    6/7/87    Actuation of Reactor Building Isolation and Standby Gas
                              Treatment System start signal
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                    9/17/87   Auto start of "A" EDG
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                    10/6/87   Reactor Water Cleanup and Shutdown Cooling System Isolation
              These LERs will be reviewed upon issue as part of the normal resident
               inspection program. The inspector has reviewed the licensee's actions in
              addressing open item 87-45-05 and is satisfied that those actions were
               thorough and timely. This item is closed.
         3.0 Routine Periodic Inspections
              The inspectors routinely toured the f acility during normal and backshif t
               hours to assess general plant and equipment conditions, housekeeping, and
               adherence to fire protection, security and radiological control measures.
               Inspections were conducted between 10:00 p.m. and 6:00 a.m. on January 17,
               18, and 19, 1988 for a total of four hours and during the weekends of
               December 12, 19, 27, 1987 and January 3, 9, 17, 1988 for a total of 17
               hours. Ongoing work activities were monitored to verify that thty were
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           being conducted in accordance with approved administrative and technical
           procedures, and that proper communications with the control room staff had
           been established. The inspector observed valve, instrument and electrical
           equipment lineups in the field to ensure that they were consistent with
           system operability requirements and operating procedures.
           During tours of the control room the inspectors verified proper staffing,
           access control and operator attentiveness.                                   Adherence to procedures and
           limiting conditions for operations was evaluated. The inspectors examined
           equipment lineup and operability, instrument traces and status of control
           room annunciators. Various control room logs and other available licensee
           documentation were reviewed.
           The ir.spector observed and reviewed outage, maintenance and problem inves-
           tigation activities to verify compifance with regulations, procedures,
           codes and standards.               Involvement of QA/QC, safety tag use, personnel
           qualifications,     fire protection precautions, retest requirements, and
           reportability were assessed.
           The inspector observed tests to verify performance in accordance with
           approved procedures and LCO's, collection of valid test results, removal
           and restoration of equipment, and deficiency review and resolution.
           Radiological controls were observed on a routine basis during the report-
           ing period.      Standard industry radiological work practices, conformance
           to radiological control procedures and 10 CFR Part 20 requirements were
           observed.     Independent surveys of radiological boundaries and random
           surveys of nonradiological points throughout the facility were taken by
           the inspector.
           Checks were made to determine whether security conditions met regulatory
           requirements, the physical security plan, and approved procedures. Those
           checks included security staffing, protected and vital area barriers,
           personnel identification, access control, badging, and compensatory
           measures when required.
           a.    Surveillance Testing
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                       Diesel Generator Prelube Pump Failure
                       On December 13, 1987, the prelube pump for the "B" emergency
                       diesel generator (EDG) failed to restart on demand during a
                       routine surveillance test.                                 Upon disassembly it was identified
                       that a small piece tf metal had become lodged between the pump
                       rotor and idler gear.             The interference from the metal caused
                       the pump motor breaker to trip on pump start.                                    An identical
                       failure occurred during a loss of offsite power event on
                       November 12, 1987.            In that case the failure caused a lengthy
                       delay in returning an                    idle diesel to service.                    While not
                       required for diesei operation, the prelube system reduces EDG
                       bearing wear during equipment start.
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                   In response to the failures, the licensee drained and. inspected
                   the lube oil sump, and disassembled and inspected the lube oil
                   filters, strainers and heater.         The lube oil heater _ was found
                   to have failed in the energized mode resulting in significant
                  carbon deposits in the heater and filter.                  No appreciable
                  deposits were found in the. lube oil sump. In addition, a piece
                  of filter element ' packaging material was found in the lube oil
                   filter housing. No foreign material which could have- contrib-
                  uted to' the prelube pump failure, however, was found. The pump
                  was replaced and the diesel was returned to service. No addi-
                  tional failures occurred during the inspection period. The two
                  pumps which failed had in-sequence serial numbers.                 Licensee
                  Quality Control personnel performed magnetic particle and dye-
                  penetrant testing of the internals of a third in-sequence pump
                  in the warehouse. No flaws were noted. The licensee is pursu-
                  ing the root cause of the failures in cooperation with the pump
                  vendor, Viking Pump. The licensee stated at the exit interview
                  that the "A" EDG prelube pump and lube oil heater would be
                  inspected during the next "A" diesel outage. The inspector will
                  continue to monitor licensee followup to this problem.
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                  Steam Testing of the High Pressure Coolant Injection and Reactor
                  Core Isolation Cooling Systems
                  The licensee completed full pressure steam testing of the High
                  Pressure Coolant Injection (HPCI) and Reactor Core Isolation
                  Cooling (RCIC) system turbines by utilizing te.nporary oil fired
                  auxiliary boilers as a source of non-nuclear steam. The full
                  pressure steam testing is part of a post-maintenance and system
                  operability check.     Both HPCI and RCIC systems were overhauled
                  during the current outage. Utilizing temporary test procedures
                  TP 87-198 and TP 87-199, the HPCI/RCIC testing included turbine

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                  overspeed trip, pump full flow capacity and operation from the
                  alternate shutdown panels. Also during the test, the suction
                  path was changed from the condensate storage tank to the torus
                  and back.
                  During the testing, several problems were identified by the
                  licensee in both HPCI and RCIC syste:ns.       In HPCI, problems with
                  the governor control system were noted including a minor oil
                  leak in the servo-motor.      Steam leaks at gauges and turbine
                  drain line were also discovered.          In RCIC, the licensee dis-

l covered a previously installed blank flange in the turbine steam

                  leak off line which caused steam leaks. A few problems were
                  also noted on the RCIC governor control system. The licensee is
                  in the process of dispositioning these items. The inspector
                  noted that using non-nuclear steam for the testing enabled the
licensee to discover problems which may not have been easily

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                  identifiable using nuclear steam due to the radiological condi-

l tions. The inspector will review the results of the tests and ! dispositioning of the problems identified during the tests. l

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                                                             Incorrect Installation of Fire Dampers
                                                            On December 17, 1987, during performance of a. routine surveil-
                                                             lance test the licensee' inadvertently actuated two fire dampers.
                                                            One of the dampers failed to fully close - due to- interference
                                                            with a hook used to secure it in the~ open position. When the
                                                             fusible link was energized, the metal damper retaining strap
                                                             should. have fallen away allowing full closure. The hook attach-
                                                             ing the strap to _the fusible link was oriented -with the open
                                                             side toward the damper. The damper caught on the hook and re-
                                                            mained partially open. Upon discovery the licensee .immediately
                                                            stationed fire watches at all areas containing suspect' dampers.
                                                             Inspections were promptly conducted and it was identified that
                                                            all of the installed hooks were oriented in this manner.         The
                                                            hooks were repositioned so that the open side faces away from
                                                            the damper. Three dampers were inaccessible and compensatory
                                                            measures-remain in place pending inspection.
                                                            The dampers were originally supplied to the licensee without the
                                                            hooks.    A revision to the plant design change (PDC) package
                                                            added the hooks to facilitate surveillance testing. Installa-
                                                            tion instructions contained in the PDC specified hook orienta-
                                                            tion with the open side toward the damper. The vendor data
                                                            sheet supplied by Air Balance Inc. also showed the hoox instal-
                                                            led in this manner.
                                                            Licensee event report (LER) 87-020-00 was issued describing the
                                                            problem and corrective actions taken. The LER states that pre-
                            .                               liminary licensee assessment of the issue determined that it did
                                                            not. meet the reporting threshold of 10 CFR Part 21. The inspec-
                                                            tor discussed the Part 21 reportability with the licensee's
                                                            Nuclear Engineering Department (NED). NED personnel stated that
                                                            the failure mechanism wn created by the licensee when the hook
                                                            was added. .In addition the presence of mitigating factors such
                                                            as fire detection and suppression, and control of combustible
                                                            materials support the conclusion that a substantial safety
                                                            hazard did not exist.     The licensee also feels that LER 87-020-
                                                            00 contains sufficient information to clearly define the
                                                            problem. The inspector had no further questions in this area.
                                                            The inspector examined two dampers in the cable spreading room
                                                            to verify that the hooks had been reoriented.        Both hooks had
                                                            been modified, however, neither of the dampers had locking rings
                                                            installed at the hook to retaining strap connection as required
                                                            by the installation instructions in the PDC.           The licensee
                                                            reviewed the function of the locking rings and concluded that
                                                            they were not required. A change to the PDC was initiated to
                                                            delete the ring.    The inspector had no further questions.
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                          b. Radiation Protection and Chemistry
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                                  Locked High Radiation Area Access Control
                                  During the period covered by inspection report 87-57, four
                                  instances occurred in which the licensee failed-to' properly con-
                                  trol access to areas that had been designated as locked high
                                  radiation areas. In three of these cases, doors to. locked high
                                  radiation areas were found closed but not locked and in the
                                  fourth case a door into a locked high radiation area was found
                                  to not be on the list of doors that were being controlled under
                                  the locked high radiation area door procedure.
                                  On December 15, 1987, a contract painter failed to check that
                                  the door to the locked high radiation area he was exiting was
                                  properly latched. The unlatched door was identified during the
                                  next routine check of high radiation area doors. Licensee par-
                                  sonnel immediately latched the door and initiated a radiological
                                  occurrence report (ROR) to document the occurrence and track all
                                  actions taken during the investigation.               Surveys of the area
                                  showed no dose rates greater than 1000 millirems per hour
                                  (MR/hr). Interviews with the individual involved determined
                                  that the procedures and requirements were well understood and
                                  that the HP technician had informed them of their responsibil-
                                                                                                                          -
                                  ities prior to entry into the area.
                                  On December 27, 1987, and again on January 8,1988, instances
                                  similar to the one described above took place.               In both cases
                                  the licensee initiated RORs and took steps to determine: 1)who
                                  had been in the area, 2) were they aware of the procedure, and
                                  3) had they been properly briefed. prior to entry into the areas
                                  involved. In both of these cases the root cause has been deter-
                                  mined as personnel error.

4 In one instance the licensee identified that one of the multiple s

                                  doors into an area classified as a locked high radiation area
                                  was not on the list of doors to be checked on a routine basis.
                                  The door was immediately checked and found to be locked. Records
                                  have been audited to determine if any unauthorized entry into
                                  the area had occurred and no instances were identified. The
                                  door has been placed on the list and is now routinely checked.
                                                                                                                     .
                                  The inspector reviewed licensee actions as a result of these
                                   instances and is satisfied that in all cases, the immediate and
                                   followup actions were timely and complete. Surveys taken were
                                  comprehensive and conducted almost immediately af ter discovery
                                  of unlocked areas.                 Dose calculations were    performed  and
                                  dosimetry read in all cases.             Involvement by senior HP and plant
                                  management was evident in all instances.

E

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                                     Inadequate control of locked high radiation areas .has been an
                                    area of longstanding NRC concern. Notices of Violation have
                                    been issued in the past, during                  inspectior,# 50-293/87-03,
                                    50-293/87-11', . and 50-293/87-19 - which addressed these concerns.
                                   'In regard to these violations the licensee instituted corrective
                                    actions which have been successful in addressing segments of the-
                                   -problem but have not been successful-in preventing recurrence of
                                    events involving high radiation area door control.
                                    The inspector has independently reviewed the licensee's program
                                     for control of high radiation areas and high radiation area key
                                    control and has found them adequate. Although the programs
                                    themselves are adequate and personnel have been trained on those
                                    programs, instances still occur where locked high radiation
                                    areas are not adequately controlled.
                                    Based on review of these four instances coupled with the review
                                    of Unresolved Item 87-50-08, the inspector determined that the
                                     licensee actions in response to these previous findings have not
                                    prevented ' recurrence, Failure to comply with the requirements
                                    of Technical Specification 6.11 and Implementing Procedure
                                    G.1-012 is an apparent violation of NRC requirements as docu-
                                    mented in Appendix A of the cover letter to this report
                                     (87-57-01).    Licensee response to Appendix A should include
                                     those measures taken to insure that corrective actions are
                                    effective and lasting.
                              -
                                    Contaminated Clothing Offsite
                                    On December 17, 1987, at 7:26 p.m.              hours a Bechtel pipefitter
                                    who-was exiting the reactor building, set off a whole body por-
                                     tal monitor alarm.        The portal monitor indicated contamination
                                     of his chest area and left hand. The health p5ysics technician
                                     on duty at the access point removed the individual from the por-
                                     tal monitor and began performing a survey using a RM-14 with DT
                                     260 probe.    The HP technician identified; 1) contamination on
                                     the individual's left hand, 1-2 thousand dpm per 100 square
                                     centimeters (K OPM), which was removed by washing, 2) contamina-
                                     tion on the shirt in both the chest (80K OPM) and lower stomach
                                     area (1K DPM). The shirt contamination was removed by tape (80K
                                     OPM) and washing with soap and water (1K DPM). The employee,
                                     now wearing an undershirt and trousers, was then sent to clear
                                     the portal monitor which again alarmed and indicated contamina-
                                     tion in the chest area.              The HP technician again surveyed the
                                     individual and identified contamination on the undershirt in the
                                     chest area (70K DPM). The individual was then sent into the
                                     portal monitor bare chested and was cleared. The individual was
                                     given his outer shirt, which was still wet from decontamination
                                     and cleared through portal monitor. At this point, the indi-
                                     vidual removed the wet shirt, put on his jacket, cleared the
                                     portal monitor again, and left for his home.
                                                                                                                i

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                                          10
        .
                 Upon returning to work December 18, 1987, the individual was
                 given a whole body count to determine if any internal contamin-
                 ation had occurred. The whole body count showed no internal'
                 contamination. After completion of the whole body count the
                 individual was interviewed to determine how he had been contam-         '
                 inated, where the occurrence took place and how long he was
                                                                       -
                 contaminated prior to detection, to calculate skin dose received.
                 The interview revealed that the individual had been contaminated
                 when he disconnected a partially pressurized service air hose
                 and . depressurized it.    The interview also revealed that the
                 individual used the portal monitor at the 91 ft, elevation of
                 the reactor building, received an alarm, did not call for HP
                 assistance but instead tried to decontaminate himself prior to
                 proceeding to the reactor building access.      Station procedures
                 require that an individual who finds himself contaminated is to
                 call health physics for assistance.     The individual stated that
                 he was aware of this requirement.        During the interview the
                 individual expressed concern about whether his heavy winter
                 jack ' could have shielded the contamination on his shirt and
                 undershirt from detection by the portal monitors.        To demon-      ,
                 strate that this could not happen, a HP supervisor placed
                 plastic bags, which contained the contamination removed from his
                 shirt, inside the coat and attempted to exit through two por-
                 tals. The portal monitors alarmed on each attempt.        The indi-
                 vidual appeared satisfied with the demonstration put his jacket
                 back on, with the plastic bags removed and attempted to leave
                 the reactor building.       An alarm was actuated on the portal
                 monitor and contamination was indicated on the left arm.         The
                 on duty HP technician removed the individual from the portal
                 monitor and identified 3K DPM contamination on the upper right
                 sleeve (outside) of the jacket even though the jacket had not
                 been worn into the reactor building. At _this juncture the indi-
                 vidual expressed concern over whether the shirt that he had worn
                 the previous day could still be contaminated.     The licensee had
                 a HP technician accompany the individual to his home.            The
                 individual's shirt was found to be contaminated, was bagged and
                 returned to the site.       Surveys of the individual's home and
                 vehicle identified no further contamination.
                 Efforts to determine how the contaminated shirt was worn through
                 the portal monitors without setting of an alarm yielded positive
                 results. The individual stated that he had purposely kept him-
                 self away from the portal monitor in an attempt to keep his wet
                 shirt away from his skin.     The licensee taped the plastic bags,
                 with the contamination in them, back onto the snirt and an HP
                 supervisor attempted to pass through the portal monitors by
                                                                                      _-
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                                                                           11
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                                            mimicking the' body posture used by the individual _when he cicared
                                             the monitor. The HP supervisor was able to pass through six
                                            different monitors without setting off an alarm. The HP super-
                                            visor then used the portal monitors in the correct manner and
                                            all six monitors alarmed proving that the equipment was func-
                                            tional.
                                            The licensee has evaluated the occurrence to identify the root
                                            causes ~ and -immediately implemented corrective action. This
                                            occurrence was _ caused by one sequence of events that involved
                                            two distinct personnel = errors. The primary cause involved the
                                            failure of the HP technician to perform an adequate survey of
                                                                                                                 '
                                            the contaminated individual's clothing when the portal monitor
                                            alarm was received. The second problem involved the f ailure to
                                            properly use the installed portal monitors at the reactor build-
                                            ing access.
                                            In addition to personnel interviews.to identify the sequence of
                                            events the licensee also reviewed procedural adequacy, personnel-
                                            training and portal monitor calibration and performance. These
  F-                                        reviews verified that training was adequate and portal monitor
                                            performance'was as designed. Procedures for control of contam-
                                            inated individuals at the reactor building access did not spec-
                                            ifically require that all articles of clothing require a 100%
                                            frisk prior to this occurrence.                 Instructions have been posted
                                            at the reactor building access which now clarify the procedure
                                            to be followed when an individual is found to be contaminated.
                                           The portal monitors in use at Pilgrim do not presently have a
                                            switch at chest level. which must be actuated to start the moni-
                                            toring process.          Lack of this feature allowed the individual

.,

'
                                           wearing a contaminated shirt to lean away from the machine suf-
                                            ficiently to clear the monitor without any alarm. The licensee
                                           has determined thats the manufacture of the portal monitor now
                                           produces a chest high switch for the installed model and will
                                            install them in the future.
                                           Calculations have been performed by the licensee to determine
                                           the radiation dose received by the individual and the amount of

,

                                           radioactive material that was released from the site on the con-
                                           taminated shirt. The results of these calculations show that
                                           the individual received a localized radiation dose to the skin
                                           of 260 Mrem, which is below the federal limits for skin exposure,
                                           and that the amount of radioactive material on the individuals
                                           clothing was 0.2 microcuries which meets the federal criteria as
                                           an exempt quantity of Co-60.              The inspector is satisfied with
                                           the licensee's analysis and corrective actions and has no
                                           further questions.

.

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         ;.    ..'
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                                                               12
                   -
                      Allegation of I'mproper Disposal of Radioactively Contaminated
                      Shrubs . ( RI-87-A-0107)
                      On August 31 and September 11, 1987, the NRC resident office at

t

                      Pilgrim received. allegations that radioactively contaminated
                      shrubs had been removed from the site and improperly disposed.
                     .The alleged improper disposal occurred on ' July 23, August 26 ar.d
  -
                     August 28,1987. During this time period the licensee removed a
                      large number of shrubs from various areas of the site, including
                      those - planted near the old. administration building and the
                      switchyard.               The shrubs were removed to facilitate site con-
                      struction activities _and to alleviate certain security' concerns.
                     Upon receipt of .he first allegation on August 31, 1987 the NRC
                      requested that the licensee perform -an evaluation and provide
,
                      the results .for review.                    In addition an independent NRC review
                     was initiated.
                      Resident and specialist inspectors reviewed the licensee's con-
                     clusions. The licensee evaluated material release records and
                      interviewed personnel regarding removal of shrubs -during the
!..                  week of July 20,1987. Several truckloads of shrubs that 'were
                      transported offsite during the midnight shif t on July 24 were
!                    examined in de tail. Because trace amounts of Cobalt-60 had pre-
i-                   viously been found in soil onsite, some .of the shrubs had the
                      soil removed from the roots prior to release. Each shrub was
                     hand surveyed and found to meet established offsite release
                     c ri te ri a .           They .were transported first to the licensee's shore-
                     front area and later to a dump site on licensee property.                                                                            The
                      licensee concluded that the shrubs had been adequately surveyed
                     and that no radioactive material had been improperly released.
                     The resident inspectors reviewed the licensee's program for con-
                     trol of release of material from the site.                                                                 This area was also
                     evaluated by NRC specialist inspectors during inspection 50-293/
                     87-19. Both inspections concluded that appropriate surveys and
                     release liniits have been established and implemented. Resident
                     and specialist inspectors examined licensee release records for
                     the dates in question to verify that vehicles leaving the pro-
                     tected area had been properly surveyed. No discrepancies were
                     identified. An NRC resident inspector accompanied by a licensee
                     representative collected four samples of the shrubs which had
                     been deposited in the dump site discussed above. Each of the
                     four samples consisted of root, branch and foliage clippings
                     from a number of different shrubs. The samples were indepen-
                     dently analyzed by the NRC. Three of the samples indicated no
                     contamination. One sample indicated only trace levels of Cobalt
                     -60. Measurements showed that the amount of C0-60 present in
                                                                                                                                                              -
                     this sample was about 2% of the average radioactivity typically
                     found in soil due to naturally occurring isotopes.
 c
       ;.           .
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                      .
              -
        .
                                                                  13
          .
                                      The . licensee's program for release of material from the site
                                      appears adequate.     Appropriate survey . techniques and' release
                                       limits-have been established. Review of -records confirmed that
                                      the program is being implemented. Samples of the shrubs col-
                                    .lected by the NRC showed' zero or negligible contamination and
                                      pose ' no health and safety concern.       Based on the above this
                                     allegat'an is considered closed.          NRC Region I staff provided
                                      status briefings concerning this allegation to. Senator Kennedy's
                                      staff. and to the Massachusetts Department of Public Health.
                                  -
                                    Allegation of Airborne Radioactivity in the Trash Compaction
                                     Facility (RI-87-A-0120)
                                    On October 5, 1987, the resident office received an anonymous
                                     allegation that personnel working at the sort table in the trash
                                    compaction ; facility .(TCF) were being routinely exposed to air-
                                    borne radioactive contamination. The alleger stated that the
                                     two filter systems designed- to treat exhaust air from the sort -
                                     table prior to discharge into the room were not functioning, and
                                    that the filter differential pressure alarm circuits had been
                                    disabled.
                                    On October 7 and 8, 1987, NRC specialist inspectors toured the
                                    TCF and examined the design and condition of the equipment. The
                                     sort table is used to separate contaminated materials for com-
                                    paction and disposal. Potentially contamitated air is exhausted
                                    from the table, passed through two filters operating in parallel,.
                                    and released into the room. Airborne radiation levels in the
                                    room are measured by means of a separate air monitor which is
                                    operated whenever the sorting table is used.                   The alarm is

<

                                    typically set at 3 X 10 -10 (3E-10) microcuries per cubic cen-
                                    timeter (cc). In addition the filters are surveyed daily and
                                    changed if contact dose rates exceed 2mR per hour. The inspec-
                                    tors also examined the trash compaction unit in the area and
                                    found that similar controls had been applied.                   Based on the
                                    above, no immediate health and safety concerns were indicated.
                                    On January 15, 1988, the resident inspectors toured the TCF,
                                    examined equipment operation and interviewed licensee and con-
                                    tractor personnel involved in ongoing work activities. A radia-
                                    tion work permit specifying protective clothing, health physics
                                    coverage, and use of a continuous air monitor is in place to                             -
                                    control work at the sort table.       Personnel involved stated that
                                    trash bags were surveyed prior to sorting and rejected if radia-

, tion levels exceeded Smr/hr, if they contained liquid, or if any l powdery material was present. The health physics technician on

                                    auty stated that filter radiation levels are monitored daily.

L I l

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                      Workers and health physics personnel also' stated that filter:
                                                                              -
                     -differential 1 pressure (dp) instruments are monitored to detect
                                                                         ~
                      filter plugging, however no one had.been clearly assigned this
                      responsibility and no' dp -limit was. established. The inspector-
                      observed the operation of the table and noted that .the '"filter
                      restricted" alarm ' actuated - for one of the two filters.                       The
                      alarm actuated ' for the filter displaying - the -lower differential
                      pressure.- When questioned workers stated ' that much of the -
                      monitoring and alarm circuitry for the table was not functional,
                      and that - the filter alarm was. not reliable.                      The . table was
                      originally part of a larger processing system and much .of the
                      disconnected circuitry was intended to perform functions which
                      are no longer needed. The f aspector verified that current
                      filter dp readings are consistent with the manufactures name
                      plate data.
                     ;It appears that the general-process applied, incibding insoec-
                      tion ana. survey of trash bags' prior to sorting, daily filter
                      surveys . and continuous air monitoring would preclude airborne
                      radioactivity problems. Based on the above this : all.egation is
                      closed. However, th'e inspector noted that no work instructions
                      existed-describing the controls applied and equipment monitoring
                      requirements. When discussed with licensee radiation protection
                      management they promptly committed to review the situation and-
                      issue appropriate guidance.       This was confirmed during the
                      inspector's exit interview.                                                              -
                   -
                      Erosion of Construction Dirt'into Wetland
                      On January 15, 1988, at 5:45 p.m.        the licensee made an ENS
                      notificatfor in accordance with 10 CFR 50.72 (b)(2)(vi) which
                      requires the licensee to inform the NRC of an event or situation
                      related to health and safety of public for.which a news release
                     .was made or notification of another government agency has been
                      made.    During routine environmental monitorin'g, the . licensee
                      observed erosion from a pile of construction dirt into an adja-
                      cent licensee controlled wetland.       The Plymouth Conservation
                      Commission and the Massachusetts Department of Public Health
                      were notified and the press release was made by the licensee.
                      Also on January 16, 1988 two representatives from the Plymouth
                      Conservation Commission toured the area.
                      In the last several years during onsite excavation for plant
                      modifications, dirt, asphalt and concrete containing low le"els
                      of contamination were stored in a fenced in storage area outside
                      the protected area on the licensee's property.                       The licensee
                      estimated that the storage area contains 110,000 cubic feet of
                      material.   Before removal from the protected area, samples of
                                                                  _ _ _ _ _.. _ _ -._ _ _

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                                                                15
        .
                                       material were obtained and isotopic analyses was performed by
                                       the licensee. The activity found was - reasonably uniform at1
                                       levels of 10(1E-6) and 10(1E-7) microcuries of Cobalt-60 and
                                       Cesium-137.per gram. Sampling and- storage of this material was
                                       previously reviewed during inspection 50-293/87-18.             On
                                       January 21, 1988 the inspector toured the area, accompanied by.
                                       a licensee health physics technician, and performed a survey of
                                      'the storage area and found no detectable radiation above .back-
                                       ground levels. During the tour the inspector noted that bales
                                       of hay had been put around the perimeter of the fence which
                                       borders wetlands area to prevent further erosion . of material.
                                       The fenced in storage area was secured with a locked gate.     The
                                       inspector's survey of the area and review of licensee's analyses
                                       indicate that the level of activity does not represent a health
                                       or safety concern. However, the inspector raised a concern to
                                       the licensee management that the material should not be -allowed-
                                       to erode.    The inspectors will continue to monitor the licensee
                                       actions in formulating long term solution to properly dispose of
                                       the material.
                          c.     Fire Protection
                                On January 17,1988, at 4:55 a.m. the control room received a report
                                 from a security guard of smoke coming from a contractor lavatory
                                 trailer, which is located adjacent to. the Bechtel warehouse inside'
                                 the protected area fence.     The onshift fire brigade chief was dis-
                                 patchtd to the scene and confirmed smoke and smoldering in the area.
                                 The fire brigade was immediately dispatched and fire was extinguished
                                 using a portable dry chemical extinguisher and a hose from a nearby
                                 hydrant house.     Electrical maintenance was called to shut off the
                                 power to the trailer. By 5:30 ~ a.m. , .the fire brigade members had
                                 cleared the scene and a continuous fire watch was posted ii, the area.
                               ' The cause of the fire was believed to be overheating of an overhead
                                 heating unit for the trailer. No personnel injury . occurred.        The
                                 inspector toured the scene with a licensee fire protection engineer
                                 on January 18, 1988. Minor damage to a small area of the ceiling in
                                 the trailer was observed. The Plymouth Fire Department was notified
                                 by the licensee in the morning of January 18, 1988.
                     4.0 Review of Plant Events
                          The inspectors followed up on events occurring during the period to deter-
                          mine if licensee response was thorough and effective. Independent reviews
                          of the events were conducted to verify the accuracy and completeness of
                          licensee information.
                                                      __                                                              _                                                                  .. -                 - - - - - -

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                                                         16
                a. Spurious Isolations of RHR Shutdown Cooling System
                   On December 7,1987, at 2:28 p.m. , an inadvertent isolation of both
                   inboard and outboard containment isolation valves on the RHR shutdown
                   cooling suction line occurred.                                                Preparation for the reactor vessel
                   hydrostatic test was in progress.                                                                As part of the hydrostatic test
                   procedure, a technician was installing an electrical jumper in the
                   primary containment isolation system logic panel C-941 to bypass the
                   reactor coolant system (RCS) high pressure interlock on the inboard
                   isolation valve. When the termination screws were loosened to in-
                   stall the jumper, the leads lost contact and caused a false high
                   pressure isolation signal. RHR was in its shutdown cooling mode when
                   the isolation signal was generated, and the shutdown cooling suction
                   valves (MOV 1001-47, 1000-50) automatically closed as designed.
                                                                                                                                                                                                                          -
                   Coincident with the closure of the valves, the "A" and "C" RHR pumps
                   tripped automatically to protect the pumps from loss of adequate
                   suction.    The licensee determined the actuation was due to a person-
                   nel error.    The licensee revised Procedure 2.1.8.1, Class I System
                   Hydrostatic Test, to caution the I&C technician of potential isola-
                   tion of RHR shutdown cooling system while installing the jumper.
                   On December 8, 1987, at 9:45 p.m. , the inboard isolation valve (MOV
                   1001-50) on the RHR shutdown cooling suction line automatically
                   closed.    The automatic isolation occurred when the plant reached
                   100 psig during pressurization for performance of the class I hydro-
                   static test.         The outboard isolation valve (MOV 1001-47) was already
                   closed to form a pressure boundary for the test.                                                                                                                            The licensee's
                   investigation determined that the cause of the isolation was that
                   Procedure 2.1.8.1 did not identify all the jumpers necess4ry to
                   b3 pass the RCS high pressure interlock on the inboard isolation
                   valve.
                   As immediate corrective action, the licensee halted the pressuriza-
                   tion of RCS and reviewed the logic prints.                                                                                                                           The licensee revised
                   Procedure 2.1.8.1 to reflect the need to install an additional jumper
                   in panel C-942.           In reviewing this event along with other similar
                   events documented in previous inspection reports, the inspector noted
                   that inadequate planning and inadequate procedures appear to be a
                   common root cause for several ESF actuations which occurred on
                   September 17, september 22, October 15 and October 24, 1987.                                                                                                                           The
                   inspector expressed this concern at the exit meeting with licensee
                   management.    The licensee informed the inspector that the Technical
                   Group is in the process of developing generic guidance for isolating
                   or jumpering an electrical component which may cause inadvertent
                   safety system actuations. The inspector will continue to monitor the
                   effectiveness of licensee's corrective action to prevent further ESF
                   actuations due to inadequate planning and inadequate procedures.
                                                                                                                                                                                                                            l
                                                                                                                                                                                                                            ,
                                   _ _ _ _ _          _ _ _ _ . _ . _ _ _ _ _ . . _ _ _ _ __ _ _ _ _ _ _ __ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ . . _ _ _ _ _ _ _ _ _ _ _ . _ _ . . . . _
                                   .i  i                               . . . _ . _ . _ . . .

_ _ _

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               a
                                                  17
                 b. Reactor Water Cleanup System Spurious Isolation
                    On December 17, 1987, at 11:05 a.m., the inboard primary containment
                    isolation valve on the reactor water cleanup (RWCV) system suction
                    line automatically isolated.                            I&C technicians conducting a routine
                    surveillance of the RWCL' high area temperature isolation logic inad-
                    vertently grounded a lead which had been lif ted during the test.
                    Grounding the lead resulted in a blown logic power fuse and isolation
                    of the valve (MOV 1201-2). Following investigation by the control
                    room supervisor, the fuse was replaced and the isolation was reset.
                    The licensee's investigation concluded that the root cause is a per-
                    sonnel error. The licensee informed the inspector that the proced-
                    ure, 8.M.2-1.2.2, Reactor Water Cleanup Area High Temperature, will
                    be revised to provide cautions to the control room operators and the
                    I&C technicians. Also, an effort is ongoing to review recent ESF
                    actuations caused by personnel error to formulate appropriate
                    corrective actions.
                 c. Engineered Safety Feature Actuations Due to a Failed Logic Relay
                    On January 6, 1988, at 2: 50 p.m. , the coil of primary containment
                    isolation system (PCIS) electrical relay 16A-K57 failed, creating a
                    f aul t and resulting in blown logic power fuses.                                                                                             The aeenergization
                    of this portion of the PCIS logic caused a partial primary contain-
                    ment isolation along with a reactor building isolation and start of
                    the "8" Standby Gas Treatment system (SBGT).                                                                                                The licensee notified
                    the NRC at 5:12 p.m. via ENS. The failed relay was a GE type CR120A
                    relay.   The licensee has experienced several failures of this type of
                    relay in the last few years. The licensee's evaluation of this nigh
                    failure rate and corrective actions to address it are described in
                    the inspection report 50-293/87-50.
                    On January 7, 1988, the inspector reviewed maintenance request (MR)
                    88-9 which had been initiated to investigate the cause of the above
                    mentioned ESF actuations and to replace the blown fuse and the faulty
                    relay.   The inspector noted that the relay replacement was performed
                    using only procedure 3.M.1-11, Routine Maintenance. This procedure
                    contains general guidance and its stated use is for performing main-                                                                                              '
                    tenance activities which are not complicated or critical enough to
                    require detailed written procedures.                                                                                In this case, no step-by-step
                    instruction was initiated to control the sequence of work, to control
                    and tag lifted leads and jumpers, and to ensure verification and
                    independent verification of system restoration. A similar problem
                    involving lack of a sufficiently detailed controllir g procedure and
                    the appropriate reviews during an electric relay replacement on
                    November 24, 1997 was the subject of a violation as documented in the
                    inspection report 50-293/87-50, The licensee informed the inspector
                    that the corrective actions to address the violation are being
                    formulated and will be submitted to the NRC.
                                                  _ _ _ _ _ _ _ _ __ _ __ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _        __
                                                                                                           _ - _ _ _ _ _ .
      :.      ..-
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                                                     18
        .
                   d. Spurious Reactor Protection System Actuation
                      On January 17, 1988, at 1:13 a.m.,                     a spurious reactor scram signal
                      was generated during the performance of a reactor level instrument
                      calibration. The full scram signai on low water level was received
                      due to a disturbance in the reactor water instrument line when an I&C
                      technician was valving a level instrument (LI-263-59A) back sin ser-
                      vice. The Rosemount level transmitters (LT-263-57 A&B) which initi-
                      ated the. scram signal are on. the same ~ instrument rack. The licen-
                      see's preliminary investigation indicated that the root cause of the
                      event is attributed to a combination of personnel error and inade-
                      quate procedure.     The investigation also identified that' the level
                      instruments (LI-263-59 A&B) were incorrectly installed in that the
                      sensing lines were reversed.          The new Barton level instruments
                      (LI-263-59 A&B) were recently installed during this outage and would
                      only be used for local indication during a shutdown from outside the
                      control room. The licensee is currently reviewing the plant design
                      change (PDC 85-07) records and post-installation test data to deter-
                      mine the cause.    Surveillance test records are also being reviewed
                      by the licensee.     This item -is unresolvea pending the completion of
                      the licensee investigation (87-57-02).
                      Upon receiving the spurious scram the control rnom staff noted that
                      scram discharge i' :trument volume (SDIV) vent valve CV302-238 primary
                      containment vent and purge valves A050448 and A05035B and one of two
                      redundant secondary containment isolation dampers in each line did
                      not close. In addition the "B" standby gas treatment system (SGTS)
                      did not start.      Based on the initiating event, these components
                      should have actuated. The licensee notified the NRC of the failures
                      via ENS at 5:00 a.m. on , January 17, 1988.

l The control room staff conducted an immediate critique with available

                      I&C personnel, and documented observations for management followup.
                      Later on January 17, the licensee inspected the physical condition

l of the SDIV vent and drain valves and noted paint on the stem of

                      CV302-238. The paint was removed and the va'.ve successfully stroke
                      timed.    The licensee htid a second critique with management repre-
                      sentatives on the morning of January 18, 1988 to assess the situa-
                      tion. Subsequently, a walkdown of involved isolation logic components
                      was performed to verify relay contact configuration cnd to identify
                      any jumpers or lif ted leads.       This walkdown was performed to the
                      extent possible without disturbing components. No discrepancies were
                      noted. Early on January 19, the licensee performed a test in which a
                      reactor scram was intentionally initiated. The same equipment failed
                      to actuate as during the January 17 scram.                     Based on this licensee
                      management stopped all work on the affected components. A task force
                      composed of members from the technical staf f, systems group, I&C and
                      operations was designateo to investigate tne incident.                        This team
                      reviewed available information and developed an action plan.
                         _        _         _                _ _ _ _ _ _ _ _                                               __
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                                                       19
                       Walkdowns of the air system piping and components supplying motive
                       air to SDIV vent valve CV302-238 were performed to verify ' hat the
                       as built configuration is in accordance with design doc                       's and
                       that components are in good physical condition.                   No disteepancies
                       were identified. Valves CV302-238 and CV302-228 are supplied air by
                       the same solenoid operated valves. The licensee cecnergized these
                       solenoid valves and observed that CV302-22B closeo while CV302-233
                       did not.     This indicates a mechanical problem with the valve or
                       operator.    The licensee was identifying replacement parts and pre-
                       paring to disassemble the valve by the close of the inspection
                       period.    The inspectors will continue to monitor licensee followup
                       to this failure.
                       Licensee review of logic drawings confirmed that the remaining equip-
                       ment which had not properly actuated shared common isolation logic
                       components.     A series of survefilance tests was performed to allow

,

                       monitoring of key relay ac%ations. A single contact on a General
                       Electric (GE) HFA relay was determined to be misfunctioning. The
                       contact is required to close when an isolation s1gnal is received,
                       actuating the affected equipment.            However, contact resistance
                       remained high with the contact closed.         The relay was replaced and
                       the system successfully tested.       The licensee contacted GE to coor-
                       dinate disassembly and inspection of tt.e relay. Dissassembly had not
                       begun by t he. close of the inspection period.                  The inspector will
                       continue to monitor licen ee investigation of this failure.
                       The inspector exprev.ed concern that ^hree separate equipment mal-
                       functions had occurred during the inadvertent actuation. This may
                       reflect weakness in the surveillance and post-work tect program.
                       However, the licensee's response to the a c'.ua ti on and subsequent
                       malfunctians was prompt, thorough and effec ve.                 Control room aper-
                       ators quickly recognized each of the failures. They held a critique
                       on the same shift with insclved personnel.               Critique observations       -
                       were clearly documented and provided to nanagement. An additional
                       critique with managercent present established pri( rities. Action was
                       taken to freeze equipment until a r. investigation pin could be
                       developed and implemented.       Followup was well cocrdinated and in-
                       volved representatives of several portions of the organization. In
                       this case licensee commitmert to determining and correcting the
                       problem root cause was evident.
                '
                  Review of _ Reactor Vessel Hydrastatic Test Procedure c,d Test Results
                  Duriew -      1spection period the licensee comp.eted the reactor vessel
                    ;  :         est. Several reactor vessel instrument nozzles were repaired
                                outage, prompting performance of a hydrostatic test rather
                                n leakage test.      The reactor vessel reached minimum test
                  .            a all inspections were completed on December 9, 1987.                   Only
                  i --       age associated with mechanical connections, such as flanges and
                  ni         ting was identified.     The reactor vessel was depressurized on
                  Deco    -
                             12, 1987 af ter completioc of excess flow check valve testing.

!

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                         The_ inspector reviewed the licensee's hydrostatic test procedure to verify
                         that appropriate prerequisites, precautions and instructions had 5een
                        : included. A sample of valve lineups was reviewed to datermine the ade-
                         quacy of established test boundaries. Completed valve lineups were~also
                         examined. -Control of temporary electrical and mechanical jumpers was
                         evaluated to ensure proper documentation and restoration. The-inspector
                         observed installed pressure instrumentation and verified appropriate range
                         and calibration status. The adeouacy of staffing - to support test per-
                         formance was periodically verified. The inspector reviewed test results
                         and discussed them with engineering, operations, and quality control
                         oersonnel to ensure that test changes were properly processed, adequate
                         inspections were conducted, and that inspection results were promptly
                         dispositioned.
                                                                                                           \
                         The licensee's preparation for and execution of the test was generally
                         well organized and controlled. Procedures for test performance and con-
                         duct of visual inspections were clear and comprehensive.           A detailed
  1. .
                         Quality Control (QC) work instruction was developed specifying components-
                         and piping requiring inspection.     Inspection assignments were broken down
                         by location, elevation and component. This QC instruction also included
                         a series of piping diagrams depicting the test boundaries which were
                         utilized to assist in inspection performance and documentation. The
                         licensee's Technical Engineering Section, Quality Control           staff and
                         Nuclear Engineering Department each reviewed test boundary adequacy. In-
                         spection results were well documented, and maintenance requests were
                         promptly initiated to correct identified leakage.
                         The licensee experienced two shutdown cooling isolations during implemen-
                         tation of the test procedure. These isolations are discussed in detail in
                         section 4.a of this report. During the test the licensee identified leak-
                         age past the seal ring at the stuffing box to pump casing joint on both
                         racirculation pumps. Leakage flow was estimated to be one to two gallons
                         per minute for each pump. The leakage wet the pump casings and portions
                         of the suction piping, and acceptable inspections could not be completed
.
                         in these areas. The licensee stated that similar leakage on at least one
                         of the pumps was noted during the last outage. That leak sealed as system

,-

                         temperature increased during startup.       The licensee believes that the
                         leakage observcd during the recent test will also stop as temperature is
                         increasM, and no pump repairs are planned. The licanses stated at the
                         ins.nector's exit interview that the pump casings and suction piping will
                         be reinspected during start;p.
                                                                                                       .
                         The inspector noted that the test procedure did not contain valve lineups
                         for manual instrument isolation valves within the test boundary. Many
                          instruments and a significant portion of instrument piping has been
                         replaced this outage. 'lisuai inspections were performed of clas; I piping

-

                         downstream of these v31ves. The inspector questioned the basis for licen-
                          see confidence in instrument line isolation valve positions during the
                         test. The licensee pointed out that hydrostatic :esting of these lines
                         was not required dur'ng this outage.      In addition excess flow check valve
              -
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                                                                                                                                                        _ _ _ _ _ _ _ _ _ _ _ _ _
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                                                   21
                testing was conducted immediately cf ter completion of the hydrostatic test
                with the system still pressurized.                                                   Successful completion of the check
                valve testing requires proper alignment of the manual isolation valves,
                and provides assurance that the piping was pressurized during the visual
                inspections. Tre licensee however, agreed that the intent of the test had
                been to pressurize and inspect this piping and that the current procedure
                does not adequately assure the correct valve alignment. Licensee manage-
                ment stated that the procedure would be revised to address this weakness.
           6.0 Integrated Leak Rate Testing
                On December 21, 1987, the licensee began performance of the primary con-                                                                                                       $
                tainment integrated leak rate test (ILRT). The containment was pressur-
                ized with air to the full test pressure of 45 pounds per square inch and
                maintained at this pressure for 24 hours. The 24 hour test period started
                at 10:15 p.m. on December 21, 1987. A regional specialist inspector was
                onsite during the ILRT to review the adequacy of the test procedure and to
                observe the conduct of the test.                       The preliminary licensee test results
                indicated a succe .sful test, with measured leakage slightly greater than
                20 percent of the allowable leakage.                                                                A primary contributor to the ob-
                cerved leakage was identified as a drywell pressure transmitter piping cap
                which had not been fully tightened.                                                          Upon completion of the specialist
                inspector's review of the ILRT results, inspection report 50-293/87-58
                will be issued documenting the inspectors findings.
                While preparing for the primary containment integrated leak rate test
                (ILRT) the licensee observed that several torus temperature and moisture
                elements were not functioning properly.                                                                                     Troubleshooting identified cir-
                cuit faults at a torus electrical penetration assembly.                                                                                                           The licensee
                removed the penetration assembly protective cover inside the torus and
                found that it was filled with water. The penetration is installed ver-
                tically through the top of the torus.                                                                   On both the inboard and out: 3rd
                sides of the penetration a metal frame is attached on which 28 terminal
                boards are mounted. Cables passing through the pe ietration, and supplying
                instrumentation in the torus also landed on trese terminal boards.                                                                                                           A
                protective cover is bolted over the f rame n.u terminal boards on both
                sides of the penetration.     Design drawings specify that cover joints are
                to be sealed with s'licone tape. The licensee stated that the protective
                cover had not been oroperly sealed, allcwing water intrusion and buildup.
                The water caused significant corrosion of the cable connectors, terminal
                boards and metal framework. This corrosion and water buildup resulted in
                the observed electrical circuit faults.                                                                             Licensee inspection of the other
                torus electrical penetration identified similar conditions.                                                                                                          Temporary
                repairs of the temperature and moisture elements were made to allow ILRT
                performance.    Cables for communications, lighting, and torus to drywell
                vacuum breaker indication also run through the penetration.                                                                                                       The penetra-
                tion is not considered by the licensee to require environmental qualifica-
                tion but is designated as a "Q" component. The licensee is evaluating the
                root cause of the water intrusion and is developing a temporary procedure

_

                to control repair and testing of the penetration. The inspectors will

^

                continue to monitor licensee followup and corrective actions.
                                                    . _ _ _ _ _ _ _ _ _ _ _ _ - - _ _ - _ _ _ _ - - - _ _ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ _ _ .

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                          The licensee informed the inspector that penetration repairs would not be
                          completed until after ILRT performance. The inspector questioned the
                         .effect of the planned repairs on the penetration leak tightness, and the
                          ability to perform adequate leakage test after the planned rework. The
                           licensee stated thr.t the work would not affect penetration leakage but
                          that-adequate testing could _ be performed after work completion. Based on
                          available drawings however, the licensee could not demonstrate adequate
                          testability. In response to NRC concern the licensee obtained the needed
                          drawings from the vendor and verified that the penetration was completely
                          testable. The inspector had no further questions.
                          During the ILRT, the licensee identified a water leak in the high pressure
                          coolant injection (HPCI) turbine room.                                   It was determined that the in-
                          creasing pressure in the torus air space caused the suppression pool water
                          to back up through the HPCI turbine exhaust line and throgh the drain
                                                    ~
                          piping, overflowing the HPCI gland seal condenser onto the HPCI room
                          floor.    The turbine exhaust line disenarges to the torus through a check
                          valve .and a locked open stop-check valve.                                    To prevent any condensation
                          from collecting in the turbine exhaust line downstream of the check valve,
                         a drain piping drains any condensation to the HPCI gland seal condenser
                          through a drain pot. Two solenoid operated drain valves on the drain pot
                         close automatically on a HPCI (Group IV) isolation signal.                                       This is to
                         provide the isolation from the torus to the gland seal condenser. The
                          licensee's investigation determined that leads had been lifted in the HPCI
                          isolation interlock logic circuit since October 30, 1987 in support of the
                         HPCI steam testing . utilizing temporary oil-fired auxiliary boilers. With
                         the HPCI isolation signal bypassed, the drain valves remained open as the
                        - drain pot was filleJ with the suppression pool water. The licensee sub-
                          sequently relanded the leads in the HPCI isolation interlock logic circuit
                         and the drain valves closed.
                         After reviewing the ILRT procedure, HPCI test procedure and interviewing
                         licensee personnel, the inspector concluded that licensee review of the
                         active maintenance requests prior to the ILRT was not thorough in that the
                          lifted leads controlled by the MR 87-663 were not identified. The LtR tags
                         were attached on the HPCI isolation logic circuit inside a logic panel and
                         thus the tags were not identified during a system walkdown prior to the
                          ILRT. The dra:n valve positions were verified by the light indications on
                         the control room panel 903 as prescribed in the ILRT procedure.
                         The inspector also determined that the maintenance                                    <. quest above may not
                         be an adequate method of identifying and tracking jumpers and lifted                                         .
                          leads, especially for a long term application and for components which
                         could affect other ongoing maintenance or surveillance.                                      Station proce-
                         dures do not require temporsy modification controls ;ur jumpers and
                         lif ted leads which are controllea by active maintenance requests.                                       The
                         inspector discussed these findings at the exit interview with licensee
                      ,  management. The licensee informed the inspector that a lifted leads and
                         jumper log will be kept in the control roon to aid the operators in con-
                         trolling lif ted leads and jumpers.
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               7.0 Licensee Nuclear Organization Management Realignment
                               On December 14, and on December 31, 1987, the Boston. Edison Co. announced,
                             .as . part of a planned realignment occurring over the next several weeks,
                               the appointment of the following managers to -key management positions in-
                               the licensee nuclear organization at Pilgrim Station.
                               --
                                               Mr. Kenneth L. Highfill was named to assume the new position of
                                               Station Director. In this capacity, Mr. Highfill will oversee day
                                               to day operation of the Pilgrim Station including plant operations,
                                               planning and outage, nuclear training, plant- support' functions, and
                                               administrative services. Mr. Highfill will report directly to Mrb                                      '
                                               Ralph G. Bird, Senior Vice President-Nuclear.
                              --
                                               Mr. Robert J. Barrett was named the new Plant Manager. Mr. Barrett                                     ,
                                              will report to Mr. dighfill, the Station Director.                                                      1
                              --
                                              Mr. Roy Anderson, currently Deputy Outage Manager, was named to
                                               assume the new position of Planning and Outage Manager.                                 Mr. Anderson
                                              will report to Mr. Highfill, the .itation Director.
                              --
                                              Mr. Ed Kraf t was named to assume the new position of Plant Support
                                              Manager.                In this capacity, Mr. Kraft will oversee radiological,
                                               sacurity, industrial safety and fire protection, and other station
                                               support functions.               Mr. Kraft will report to Mr. Highfill, the
                                              Station Director.
                              --
                                              Mr. Donald Gillespie, currently Director of Planning and Restart, was
                                              appointed to the position of Quality -Assurance Department Manager.
                                              Mr. Gillespie will assume the position after completing his Senior
                                              Reactor Operator' training. The Quality Assurance Department Manager
                                              reports to Mr. J. E. Howard, Vice President-Engineering.
                                  -
                                              Mr.              Frank Famulari, currently Operations Quality Control Group
                                              Leader, was named to assume the newly created posi tion of Deputy
                                              Quality Assurance Department Mananer.                Mr. Famulari will report to
                                              Mr. Gillespie, and be acting Department Manager until Mr. Gillespie
                                              assumes the position after completing the Senior Reactor Operator
                                              training.
                              --
                                              Mr. John F. Alexander was named to assume the position of Operations
                                              Section Manager. Mr. Alexander will report to Mr. Barrett, the Plant
                                              Manager.
                              --
                                              Mr. Donald J. Long was named Security Section Manager. Mr. Long will
                                              report to Mr. Kraft, the Plant Support Manager.
  -           . ~ . , - . - . - . - - . - - , . - - . . - . - . - . .                            . . - . . - - , - - , - - - - , . . ,

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                 8.0 Management Meetings
                                                                                                    l
                      At periodic intervals during the course of the inspection period, meetings
                      were held with senior facility management to discuss the inspection scope
                      and preliminary findings of the resident inspectors.     On January 26, 1988,
                      the inspectors conducted a final inspection exit interview to formally
                      present inspection findings.
 FE      '
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                              Attachment I to Inspection Report 50-293/87-57
                   Persons Contacted                                         ,
                   * R. Bird, Senior Vice President - Nuclear
                   * K. Highfill, Station Director
                     K. Roberts, Plant Manager
                     R. Barrett, Deputy Plant Manager
                     R. Anderson, Planning and Outage Manager
                     E. Kraft, Plant Support Manager
                     F. Famulari, Deputy Quality Assurance Manager
                     D. Swanson, Nuclear Engineering Department Manager
                     J. Alexander, Operations Manager
                     N. Brosee, Maintenance Manager
                     J. Jens, Radiological Protection Manager
                     J. Seery, Technical Manager
                     R. Grazio, Fie!d Engineering Manager
                     P. Mastrangelo, Chief Operating Engineer

,

                     R. Sherry, Chief Maintenance Engineer
                     N. Gannon, Chief Radiological Engineer
                     D. Long, Security Manager
                     F. Woznick, Fire Protection Manager
              *Sonior licensee representatives present at the exit meeting.
         __                     .-
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                                                                                               - ATTACHMENT.1II
                             January 6, 1988
                           - MEMORANDUM'FOR:                      Ken = Roberts
                                                               . Plant Manager
                             FROM:                            . Clay Warren-                                                                                     -
                                                               - Senior Resident Inspector - Pilgrim
                             SUBJECT:                             FACILITY TOUR FINDINGS, DECEMBER 8,1987.
                                                                                                                                                                                 .
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                                                                   .
                                                                                                                                                                          -
                                                                                                                                                                            a
                           - The          items' on - the~ attachment were noted during the - facility tour on
                             December 8,.1987.                       Please-contact the Resident inspector Office when your staff
                             is ready to discuss the evaluation of-the-items and the status'of any actions
                          - taken. Please note. the items and the facility response will be. addressed in a
                           '
                             routine inspection. report.
                             Thank you-for your time and attention to these matters.
                                                                                                         Sincerely,
 i
                                                                                                         Clay C. Warren
                                                                                                         Senior Resident Inspector                                               ,
                             Attachment:                                                                                                                                         ;
                             As stated                                                                                                                                           ,
                             cc w/ attachment:                                                                                                                                 c

,

                             R. Blough
. W. Kane
                             W. Russell
                         - J._Wiggins
                                                                                                                                                                             .   i-
                                                                                                                                                                                 ,

i I. 4

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                                                 ATTACHMENT
                --
                   Numerous motors appear to have failed grease seals caused by overgreasing
                   without first removing grease drains. This condition causes a buildup of
                   grease and dirt in the cooling airflow path and in extreme cases grease
                   in the motor windings.   (SBGT fans and SLC pumps)
                --
                   Nuts and bolts were noted 10ying inside an electrical cabinet in the RCIC
                   room.
                --
                   Multiple cases of open junction boxes, terminal boxes and conduit pulled
                   away from terminal boxes were noted.
                --
                   Motor heaters for the "B" RHR pump appear to have overheated causing the
                   insulation on the heaters to melt.
               --
                   HPCI room cooler drip pan is full of paint scrappings which could lead to
                   drain clogging.
               --
                   Standby Liquid Control system relief valves have boric acid c rystal
                   buildup which could alter setpoints.
               --
                   Painting effort should be more closely controlled to prevent painting
                   inappropriate   surfaces, i.e., linkages,     valve  packing glands,  trip
                   throttle valves, limit switches, etc.
               --
                   Numerous instances of scaffolding materials, i.e., nails and wood chips,
                   laying on floors. This material could migrate to drain systems and cause
                   pump or valva damage. S:af folding was also noted attached to permanent
                   equipment such as piping and conduit.
               --
                   Valve 1001-36A niotor operator conduit had melted plastic cover.
                          :

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