ML20137U545

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Insp Repts 50-269/85-41,50-270/85-41 & 50-287/85-41 on 851210-860113.Noncompliance Noted:Failure to Follow Exempt Change Procedure & Failure to Shut Down Reactor within 24 H of Discovery of Excessive Leakage
ML20137U545
Person / Time
Site: Oconee  Duke energy icon.png
Issue date: 02/11/1986
From: Brownlee V, Bryant J, Sasser M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20137U501 List:
References
50-269-85-41, 50-270-85-41, 50-287-85-41, NUDOCS 8602190240
Download: ML20137U545 (11)


See also: IR 05000269/1985041

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

REGION ll

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101 MARIETTA STREET.N.W.

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  • 2 ATLANTA, GEORGI A 30323

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Report Nos: -50-269/85-41, 50-270/85-41, and 50-287/85-41

Licensee: Duke Power Company

422 South Church Street

Charlotte, N.C. 28242

Facility Name: Oconee Nuclear Station

Docket Nos.: 50-269, 50-270, and 50-287 License Nos.: DPR-38, DPR-47,

and DPR-55

Inspection Conducted: D ember 10.-19851- January 13, 1986

Inspectors: f, - LM1/J by d )1l

)Mte 41gned

,J. C. Bryant //

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M. K. ia s s'e r

duw Lff shdu

D6t'e gi"gned

Approved by: /M 3 iT/ThV 08 ktI lh

V. L. Brjwn' lee, Section Chief, ( Acting) Ddte S'igned

Division of Reactor Projects

SUMMARY

Scope: This _ routine, announced inspection entailed 224 inspector-hours on site

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- in the areas.of operations, surveillance, maintenance, facility modifications,

LER review, and response to the Rancho Seco event.

Results: Of the six areas inspected, no items of noncompliance or deviations

were ider.ti fied in four areas; Two items of noncompliance were found in two

areas; Failure to follow exempt change procedure and failure to shut down reactor

within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of discovery of excess leakage.

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REPORT DETAILS

1. Licensee Employees Contacted

  • M.S. Tuckman, Station Manager
  • J.N.. Pope, Superintendent of Operations
  • T.B. Owen, Superintendent of Maintenance
  • R.T. Bond, Compliance Engineer
  • T.C.'Matthews, Technical Specialist
  • R.A.-Knoerr, Project Services Engineer
  • R.J. Brackett, Senior Quality Assurance Engineer

Other licensee ~ employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

Resident Inspectors

  • J. C. Bryant
  • M. K. Sasser
  • Attended exit interview.

2. Exit Interview

The inspection scope and findings were summarized on January 13, 1986, with

those persons indicated-in paragraph I above. The licensee did not identify

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as propri. eta ry any of the materials provided to or reviewed by the

inspectors during this inspection.

3. Licensee Action' on Previous Enforcement Matters

(Closed) Violation 269, 270, 287/85-20-02 Failure to Report FSAR Revisions

as Required. -Adequate corrective action has been taken.

4. Unresolved Items

Unresolved items were not identified on this inspection.

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5. Plant Operations

The inspectors reviewed plant operations throughout the reporting period to

verify conformance with regulatory requirements, Technical Specifications

-(TS), and administrative controls. Control room logs, shift turnover

records and equipment removal and restoration records were reviewed

routinely. Interviews were conducted with plant operations, maintenance,

chemistry, health physics and performance personnel.

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Activities within the control rooms were monitored on an almost daily ~ basis.

Inspections were conducted on day and on night shifts, during week days and

on weekends. ' Some inspections were made during shift change in order to

' evaluate shift turnover performance.

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Actions observed were conducted as

required by Operations Management Procedure 2-1. The complement of licensed

personnel on each shift inspected met or exceeded the requirements of TS.

Operators were responsive to plant annunciator alarms and were cognizant of

plant conditions.

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Plant' tours were taken throughout the reporting period on a routine basis.

The areas toured included the following:

Turbine Building

Auxiliary Building

Units 1, 2, and 3 Penetration Rooms

Units 1,2, and'3 Electrical Equipment Rooms

Units 1,2, and 3 Cable Spreading Rooms

Station Yard Zone within the Protected, Area

Standby Shutdown Facility

During the plant tours, ongoing activities, housekeeping, security,

equipment status, and radiation control practices were observed.

Unit 1 operated at essentially full power throughout the reporting period,

December 10, 1985 to January 13, 1986.

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Unit 2 operated at . full power until December.14 when it was shut down to

4 repair a reactor coolant leak at an instrument root valve. The reactor was

returned to power on December 15 and operated at essentially full power

through the remainder of the report period. The shutdown is discussed in

greater detail in paragraph 8 of this report.

Unit 3 began the report period shut down to replace a main turbine bearing.

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The unit was returned to power on December 16 and operated at essentially

full power the remainder of the report period. The unit startup is

discussed in paragraph 11 of this report.

6. Surveillance Testing

The surveillance tests listed below were reviewed and/or witnessed by the

inspectors to verify procedural and performance adequacy.

The completed tests reviewed were examined for necessary test prerequisites,

instructions, acceptance criteria, technical content, authorization to begin

work, data collection, independent verification where required, handling of

deficiencies noted, and review of completed work.

The tests witnessed, in whole or in part, were inspected to determine that

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approved procedures were available, test equipment was calibrated,

prerequisites were met, tests were conducted according to procedure, test

results were acceptable and systems restoration was completed.

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Surveillances witnessed in whole or in part are as follows:

IP/1/A/305/3C RPS Channel C On-Line Test

PT/2/A/600/18 Unit 2 Motor Driven Emergency Feedwater Pump Test

IP/1/A/301/3S Startup & Intermediate Range Channel Test

PT/1/A/0150/22A Operations Valve Functional Test, Valves BS-1 and

BS-2

PT/1/A/251/01 Low Pressure Service Water Pump Test

Surveillance tests reviewed are as follows:

PT/3/A/0150/22A Operational Valve Functional Test, Unit 3.

No violations or deviations were identified.

7. Maintenance Activities

Maintenance activities were observed and/or reviewed during the reporting

period to verify that ' work was performed by qualified personnel and that

approved procedures in use adequately described work that was not within the

skill of the trade. Activities, procedures and work requests were examined

to veri fy proper authorization to begin work, provisions .for fire,

cleanliness, and exposure control, proper return of equipment to service,

and that limiting conditions for operation were met.

During an inspection of the licensee's program on Motor Operated Valve (MOV)

switch setpoints, the inspectors reviewed numerous work requests for

Maintenance I&E to troubleshoot and repair MOVs which would not operate from

their control roc 1 handswitch. In many cases, either Operations or I&E

opened the valve .om the breaker by depressing the contactor in the breaker

compartment, thus bypassing the switches and motor overloads, allowing

sufficient torque to be developed for opening the valve.

In a number of the maint'enance jobs, the inspectors found that I&E did not

use the applicable procedure, did not find the root cause, and did not take

adequate corrective action to prevent recurrence. Bypassing motor overloads

and switches at the breaker without troubleshooting the problem first was

found to be contradictory to the applicable troubleshooting procedure. In

all cases reviewed, the maintenance jobs were dated prior to a violation

written on the same subject in Report No. 50-287/85-37. That violation

concerned inoperability of Valve 3LP2.

The licensee has taken corrective action to upgrade MOV operability as a

result of his own studies as well as due to the violation; because of this

and the concurrent violation on the same subject, an additional violation

will not be cited. The licensee has stated that the appropriate trouble-

shooting procedure will be used when performing maintenance on MOV's.

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Bypassing of torque switches and other controls will not be performed prior

to examination to determine root cause, except 'in cases of operational

emergency.

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8. Unit 2 Reactor Coolant Leakage

On Friday, December 13, at approximately 1:00 am, the unit 2 reactor coolant

system (RCS) leak rate was determined to be 1.32. gallons per minute (gpm).

This determination was the result of the daily surveillance of RCS leakage,

performed during the 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> period from 12 midnight to 1:00 a.m. For. a

period of approximately 2 weeks the leak rate had been higher than normal,

with occasional results above 1 gpm. Subsequent confirmatory results had

always proven to be less than 1 gpm. Attempts by the Operations staff to

identify and isolate any leakage had been unsuccessful.

However, upon detection of excess leakage on December 13, the subsequent

confirmatory results did not prove to be less than 1 gpm. The leak rate

calculations were begun on an hourly basis at 1:00 a.m. on Friday, December

13, and new- efforts to identify the leak were initiated. Several entries

into the reactor building to inspect accessable areas proved unsuccessful.

- Ten of the eighteen RCS leak rates calculated on Friday indicated

unidentified leakage that ranged from 1.02 to 1.65 gpm.

The hourly leak rate calculations were continued on Saturday, December 14.

These results also provided evidence of greater than 1 gpm leakage, with ten

of eleven surveillances ranging from 1.07 to 1.52 gpm. At approximately '12

noon on Saturday, plant management decided to begin shutdown of unit 2,'and

at 5:30 p.m., the unit was taken subcritical . While at hot shutdown, a

thorough . inspection revealed a leaking flow transmitter root valve on the

RCS A loop. The leak was repaired and the unit was taken critical on

Sunday, December 15 at 2:03 p.m. and power was escalated to 100%.

Technical Specification 3.1.6.2 states that, if unidentified reactor coolant

leakage (excluding normal evaporative losses) exceeds I gpm ... the reactor

shall be shut down within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of detection. This 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period

provides a reasonable period of time to; (1) identify the leak and evaluate

its safety significance for continued operation, (2) provide additional

sample results to conclusively prove unidentified leakage less than 1.gpm,

or (3) shutdown the reactor in an orderly fashion if the first two options

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are not sucessful.

Contrary to the above, on Friday, December 13, upon detection of RCS leakage

in excess of 1 gpm, the leakage was not identified nor proven to be less

than 1 gpm. From the time of detection until the reactor was shutdown a

period of over 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> elapsed. This item is identified as a violation of

Technical Specification 3.1.6.2,. -Violation - Failure to Shutdown Reactor

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Within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of Detection of Excess Leakage, (270/85-41-01).

9. Motor Operated Valve (MOV) Switch Setpoints

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! The inspectors continued an inspection to determine whether the licensee has

an effective program to ensure that valve operator switch settings are

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selected, set, and maintained properly (see report 85-38). The inspectors

had become aware of numerous industry problems where improperly adjusted

torque, torque bypass, or limit switches had resulted in valves failing to

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operate when required either in operational events or during testing.

Additionally, the recently issued IE Bulletin 85-03, addresses new

requirements in certain safety related systems. The inspectors conducted

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this inspection to determine the extent, if any, of valve switch problems in

safety related systems at Oconee.

The responsible I&E engineers contacted indicated that no formal program

exists at the Oconee nuclear station for determining setpoints. Torque

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switch setpoints may be derived by any one of the following methods:

(1) from the NSM package if specified, (2) from the electrical (OEE)

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drawing, if specified, or (3) field determined, i.e., setting the switch to

whatever it takes to operate the valve. Thus the setpoints may not be based

on engineering analysis of system pressures, valve operator size, and other

factors. It was noted that switches being adjusted in the field did not

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appear to consider the design or operating pressures.

~ Based on a review of the station Inservice Inspection Program and~

discussions with staff test personnel, the inspectors determined that the

program does not verify the adequacy of switch setpoints through testing of

valves under the appropriate operating or accident pressure conditions. In .

many cases, safety related valves are stroke tested under conditions of no

differential pressure, which may be entirely different from the conditions

for which the ' valve (s) may be called upon to operate.

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The work history of approximately 25 safety related MOVs was reviewed to

determine the number of events where the MOV failed to operate properly,

whether switch setpoints were a significant contributing factor, and whether

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adequate corrective action was taken. A large number of events were

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identified by the computer listing for these MOVs, however, only a se'ected

, number were evaluated by the inspector.

Review of the work histories identified many cases where torque switch

setpoints were adjusted by I&E technicians in the field, using adequately

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' detailed and documented procedures. These completed procedures then became

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the reference for future use by plant personnel for documentation of the

setpoints. However, it is again noted .that the adjustments and subsequent

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stroking for operability testi.ng was completed with little or no pressure on i

the valve (s), a condition entirely different than may exist later.

Based on the above inspecton activities the inspectors have concluded that

the licensee does not presently have an adequate program to determine the

, correct setpoints for switches on safety related motor operators, to

document and control these setpoints, and to verify their adequacy through a

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4 test program based on testing, where possible, under actual system

differential pressure conditions.

The above findings were discussed with the licensee along with a discussion

of IE Bulletin 85-03, Motor Operated Valve Common Mode Failures During Plant

Transients Due to Improper Switch Setpoints were discussed. That bulletin

requires licensees to develop and i mpl eme.,t a program for selecting,

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setting, and maintaining switch setpoints for MOVs on certain safety related

systems.

The licensee is developing a valve improvement program, partly in response

!' to the IE Bulletin, but also in part due to histories of valve maintenance

problems.' The station has recently requested _ Design Engineering to develop

i a document listing the maximum and minimum torque settings for MOVs at the

Oconee Station. Additionally,.the test staff and maintenance engineers are
looking at methods to test valve operators under the actual system operating

conditions or under similar conditions on a test stand.

While the IE Bulletin only requires development of the program for the High

Pressure Injection and Emergency Feedwater systems at Oconee, the station is

considering implementation of the program for other. safety related systems.

The inspectors will follow the development and implementation of this

program.

i 10. Licensee Event Reports

The inspectors reviewed nonroutine event reports to verify that report

details met license requirements, identified the cause of the event,

described corrective actions appropriate for the idenfified cause, and

adequately addressed the event and any generic implications. In addition,

as appropriate, the inspectors examined operating and maintenance logs, and

i records and internal investigation reports.

Personnel were interviewed to verify that the report accurately reflected

the circumstances of the event, that the corrective action had been taken or

i responsioility assigned to assure completion, and that the event was

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reviewed by the licensee, as stipulated in the Technical Specifications. The

following event reports-were reviewed:  ;

(Closed) LER270/85-06 Reactor Trip on High RCS Pressure Following Closure

of Turbine Intercept and Bypass Valves. Event was caused by a spurious

signal generated while trouble shooting.

(Closed) LER287/85-01 Reactor T. rip Due to High RCS Pressure. Problem was

j caused by a failed integrated control system module.

(Closed) LER287/85.-02 Lockout of Startup Transformer. The lockot.t was

caused by an actual fault pressure condition; however, the root cause of the

pressure could not be determined.

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11. Review of Unit 3 Startup

On December 16, Unit 3 was taken critical and returned to power operations

following a 21 day outage to replace a bearing on the high pressure turbine.  !

The inspectors witnessed portions of the startup to verify proper

performance of plant staff, adherence to procedures, and control room

coordination. Following the plant startup, the inspectors conducted a

detailed review of the completed controlling procedure for unit startup,

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OP/3/A/1102/01, and associated procedures required to be performed in

conjunction with the controlling procedure.

The - procedures were reviewed in order to determine correct procedural

adherence, whether required sequences of activities were followed, whether

adequate system lineups were performed or verified, and whether systems and

components were verified operable as required.

No violations or deviations were identified.

12. Review of Non-Conforming Item Reports (71707)

The inspectors reviewed Non-Conforming Item Reports (NCIR) to verify that

identified deficiencies are tracked via the licensee's problem identifica-

tion system and that prompt corrective action is taken. A question as to

the timeliness of operability reviews was raised based on inspector review

of NCIR No. 0-1608, as well as to the nature of the NCIR.

This NCIR dealt with an exempt change which added nipples to two thermowells

on a 3/8 inch line at the pressurizer sample cooler near the primary sample

hood. The addition was necessary to facilitate sampling of the reactor

coolant system (RCS). The 3/8 inch line is isolated from the RCS by two

remotely operated valves, one inside and one outside containment, which are

normally closed except when a sample is taken.

In this Class E system, schedule 40 one inch nipples and 3000 pound one inch

couplings were used to effect the exempt change. Flow diagram 0FD-110A-3.1

specifies that schedule 160 piping and 5000 pound fittings be used. The

inspectors discussed the matter with Duke Power Company Design personnel who

stated that wall thickness, at the thread, of the nipples used was

calculated to be 0.063 inches, while the code requirement for the

application is 0.141 inches.

The inspectors noted that, though an operability review was required, thirty

days were allowed for th'e review. Since the NCI dealt with what amounted to

substandard material in a sample system connected to the RCS, the inspectors

did not agree with the thirty day review. The licensee then isolated the

affected system and reworked the modification with materials of the correct

strength.

In determining the cause of the non-conforming item, the inspectors reviewed

the Oconee Project Services procedure for exempt changes. In substance, the

procedure requires that the site accountable engineer (A/E) contact Design

Engineering for verbal approval of an exempt change (EC) concept; on

approval of the EC the A/E sends detailed drawings of the change in a

variation notice (VN) to Design Engineering for review; on approval by

Design Engineering of final drawings and specifications the work may

proceed. However, the work may proceed prior to Design Engineering

approval, but the system may not be returned to service until the approval

is received.

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In the case -of EC OE-0426, verbal approval was received for the change on

October 5,1985, and the work was performed on October 6 and the system

returned to service. The site engineer who prepared the job apparently

neglected to consider loss of strength due to the 316S-Schedule 40 one inch

nipple and coupling being threaded connections.

A variation notice (VN) detailing the modification was sent to Design

Engineering on October 7 and on December 12, the VN was rejected by Design

Engineering. An NCIR was not issued until January 3, 1986. On January 3 it

was sent by QA to the compliance section for Operability Review. The NRC

inspectors saw the NCI on January 9 and the licensee took immediate

corrective action.

Technical. Specification 6.4.1 ' states that the station will be oper_ated and

maintained ' according to approved procedures. Paragraph 6.4. lc. of this

specification includes actions taken to correct specific and foreseen

malfunctions of systems or components involving nuclear safety and radiation

levels. Failure to follow the exempt change procedure is an apparent

violation of Technical Specification (Violation- Failure to Follow Procedure

on Exempt Change, 85-41-02).

The inspectors pointed out that any conditions which possibly compromised

the integrity of the RCS should have immediate review. The licensee agreed

that the delay was not acceptable and that the system would have to be

revised to prevent recurrence. The licensee pointed out that, due to

earlier identified weaknesses in the program for problem evaluation,

documentation and corrective action, the Problem Investigation Report (PIR)

System had been developed and is scheduled to be implemented by June 1,

1986. The PIR will facilitate the mechanism for any employee to identify a

non-conformance and initiate corrective action. The system will be

coordinated by the Compliance Section. Specific time frames will be

assigned to the di f ferent program elements, including the operability

review, when required.

Implementation of the PIR system should resolve inspector concerns on the

timeliness of performing operability reviews. The residents will follow

implementation of this system, and it is listed as inspector followup item;

IFI 287/85-41-03; Timeliness of Operability Reviews.

13. Inspector Followup Items

(Closed) IFI 270/81-32-03 PORV Block Valve Failures. Corrective action was

taken at the time of the event to prevent recurrence. Corrective actions to

assure proper maintenance on motor operated valves, as a result of plant

problems and in response to Bulletin 85-03, Motor Operated Valve Common Mode

Failures During Plant Transients Due to Improper Switch Settings is

discussed in paragraph 9 of this report.

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14. Facility Modifications (37701)

The inspectors completed their review of selected test procedures performed

during checkout of the Standby Shutdown Facility (SSF). The previous

report, No. 50-269,270,287/85-38, paragraph 12, discussed the SSF diesel

. generator in reference to IE Bulletin 79-23 which pointed out a potential

generator failure due to the flow of circulating currents.

The referenced report stated that, at the factory, connections (shown as

corrections in the referenced report) had not been made between low KVA

rated transformers and high KVA diesel generators without adequate

limitations on the flow of circulating currents. ~ The inspector requested

the licensee to verify that site installation had not compromised these

limitations. The licensee inspected the generator, relative to Bulletin

79-23, and stated that it was determined to be a wye-wye ungrounded

connection, which eliminated the possibility of-high circulating current.

Bulletin 79-23 was closed in 1979 since Oconee, at that time, had no diesel

generators. The licensee has determined that the SSF diesel generator,

subsequently instal. led, meets the requirements of Bulleting 79-23. This

item is closed.

15. TMI Action Items (NUREG-0737)

2.K.9 (Closed) Failure Modes and ' Effects Analysis on ICS. As a result of

the correspondence from the NRC to Duke, Wagner to Parker, dated 02/03/82,

this. item should have been cle' sed. This item is now considered closed.

16. Noble Gas Activity Monitor Out of Service (Unit 2)

Radiation Instrument Alarm (RIA) 45 is one of six monitors in the Unit Vent

Monitoring System and monitors noble gas release. At 4:25 p.m. on

December 18, 1985, 2RIA-45 was declared out of service and turnover given to

repair. Repair would normally be made on the following day shift.

Technical Specifications Table 3.5.5-2.2a shows that if RIA-40 is out of

service, a . grab sample must be analyzed every eight hours.

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personnel did not detect this requirement.

At 8:00 a.m. on December-19, it_was determined that the stack should have

been sampled every eight hours. A sample was taken at 8:30 a.m. on

December 19, 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> after the monitor was declared operable. 2RIA-40 was

returned to service at 10:30 a.m. on December 19.

The licensee immediately took corrective action, reported the event to NRC,

and also took corrective action to cause shift personnel to review technical

specifications when an instrument is taken out of service. Failure to

sample the stack within eight hours of RIA-40 being declared out of service

is a violation. of Technical Specification 3.5.5.2. However, the violation

will not be cited since it meets the requirements of 10 CFR Part 2,

Appendix C, Paragraph A.

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17. Rancho Seco Overcooling Event

Upon hearing of the loss of integrated control system (ICS) power at Rancho

Seco, which resulted in an overcooling event, the inspectors began a

determination of the Oconee staffs reaction to the event. The staff had

already begun an investigation of 'the Oconee plant response and the

differences between Oconee and Rancho Seco, and had initiated an operator

training program. On January 9, the inspectors attended an operator

training class on the simulator _ in which operators were subjected to the '

loss of ICS power, loss of ICS automatic control, and loss of ICS hand

control. All three result in different plant responses.

Based on the inspector's understanding of the Rancho Seco system, apparent

. differences in automatic response to loss of ICS power is as follows:

At Rancho Seco, main fe. ! water valves close to 50%, feedwater pumps run back

.to minimum speed, turbine bypass and atmospheric dump valves open to 50%.

The reactor trip ~ ped on high pressure due to initial underfeed of the steam

generators with 'the overcooling transient following due to steam generator

overfeed and steam flow through the open bypass and dump valves. Operator

response was complicated due to emergency feedwater pumps'and valves having

controls from the ICS, which had lost power.

At Oconee the main feedwater pumps trip on loss of ICS power, thus tripping

the reactor and turbine on an ' anticipatory trip. The turbine bypass valves

fail closed and the atmospheric dump valves have no automatic controls

(chainwheel only). The Oconee engineered safety features and emergency

feedwater pumps and valves are independent of the ICS. l

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