ML20137T514
ML20137T514 | |
Person / Time | |
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Site: | River Bend ![]() |
Issue date: | 04/11/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
To: | |
Shared Package | |
ML20137T485 | List: |
References | |
50-458-97-06, 50-458-97-6, NUDOCS 9704160111 | |
Download: ML20137T514 (21) | |
See also: IR 05000458/1997006
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ENCLOSURE 2
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U.S. NUCLEAR REGULATORY COMMISSION I
REGION IV
Docket No.: 50-458
License No.. NPF-47
Report No.. 50-458/97-06
Licensee: Entergy Operations, Inc.
Facility: River Bend Station
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Location: 5485 U.S. Highway 61 l
St. Francisville, Louisiana 70775
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Dates: February 2 through March 15,1997
Inspectors: W. F. Smith, Senior Resident inspector
D. L. Proulx, Resident inspector
Approved By: P. H. Harrell, Chief, Project Branch D
Division of Reactor Projects
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Attachment: Supplemental Information l
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9704160111 970411
PDR ADOCK 05000458
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EXECUTIVE SUMMARY
River Bend Station
NRC Inspection Report 50-458/97-06
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This inspection included aspects of licensee operations, maintenance, engineering, and
plant support. The report covers a 6-week period of resident inspection.
Operations
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- In general, the performance of plant operators was professional and reflected a i
focus on safety, with the exception that entry into the at-the-controls area was not I
always properly controlled and the at-the-controls operator spent approximately l
20 minutes filling out nonwork-related paperwork (Section 01.1).
- A nuclear equipment operator (NEO) exhibited good practices and a questioning
attitude during rounds. However, the operator round sheets did not require periodic
checks of standby liquid control (SLC) pump parameters or a tour of the traversing
incore probe (TIP) system area (Section 01.2).
- The licensee appropriately trained the operators and staged materials for the
effective implementation of an emergency operating procedure (EOP)
(Section O2.1).
- A violation was identified for failure to develop administrative procedures with
apecific controls for reviewing and approving overtime for staff that performed
safety-related work. Severalindividuals exceeded the Technical Specification (TS) i
overtime limitations without proper administrative approvals (Gection 06.1). l
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- In general, the Nuclear Review Board (NRB) effectively reviewed plant issues and
recommended corrective actions, with notable exceptions. The excessive backlog
of Facility Review Committee (FRC) minutes impeded the NRB's ability to perform l
timely and effective oversight of FRC activities. Quality Assurance (QA)
surveillance resources were not allocated among the functional areas commensurate l
with performance (Section 07.1). I
Maintenance
- Mechanics performed good troubleshooting and correction of the Control Building
Chiller C low refr.'gerant temperature trip. The trip was caused by an isolated case
of poor workmenship related to a previous improper assembly of the economizer
valve float arm. A noncited violation (NCV) was identified for failure to properly
implement the applicable work instructions during the previous assembly
(Section M1.1).
- The Division il emergency diesel generator (EDG) maintenance outage was generally
well planned and performed. The electricians used a test configuration not
described in the maintenance action item (MAI) and wera unaware of whether or
not they complied with the procedure until reviewing wiring drawings later
(Section M1.2).
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- Personnel performed surveillance testing well. Self-checking was evident
(Section M1.3). i
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= The engineer performing the logic system functional test review exhibited excellent
attention to detailin identifying that the loss of power contact for the Division !! l
EDG rear air starting system was not properly tested. An NCV was identified for ,
failure to comply with TS Surveillance Requirement (SR) 3.0.2. The licensee's initial l
review of the past operability of Division 11 EDG was weak in that the review did not
discover a past outage of the forward air starting system (Section M1.4).
Enaineerina
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Reactor engineers demonstrated poor performance by calculating an incorrect full
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power exposure at which to change the operating limit minimum critical power ratio i
(OLMCPR). Consequently, a nonconservative limit was being monitored by the
reactor operators for 6 days; however, no thermallimits were exceeded
(Section E2.1). l
- The failure to maintain clear procedural guidance for the implementation of a
performance-based local leak rate test (LLRT) program resulted in missed
surveillance testing of some valves and unnecessary testing of other valves which
required taking safety-related systems out of service during plant operation at
power. A violation of TS 5.4.1.a was identified for failure to maintain the proper
guidance (Section E3.1).
Plant Sucoort
- Housekeeping in the plant continued to be excellent (Section 01.1).
- A violation for failure to post a radiation area was identified. On two occasions, the
radiation area posting at the entrance to the alternate decay heat removal (ADHR)
system room was modified without radiation protection (RP) technician approval.
Radiological postings were inappropriately relocated on two previous <.secasions,
which indicated that increased personnel sensitivity to radiologic.c! postings was
required (Section R1.1).
- Security boundaries were maintained properly and entry screening processes were
performed properly. The inspectors noted during night tours that the protected area
was properly illuminated (Section S1.1).
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Report Deta;ls
Summarv of Plant Status
The plant operated at essentially 100 percent power for the duration of this inspection
period.
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1. Operations
01 Conduct of Operations
01.1 General Comments (71707)
The inspectors conducted frequent reviews of ongoing plant operations including
control room observations, attendance at plan-of-the-day meetings, and plant tours.
, in general, the performance of plant operators was professional and reflected a
focus on safety, with minor exceptions. During a sustained control room
observation on February 11,1937, the inspectors noted that entrances into the
control room at-the-controls area were not controlled in accordance with licensee
policies. Several personnel entered the at-the-controls area without permission or a
stated operations purpose. In addition, the inspectors noted that the at-the-controls
operator spent approximately 20 minutes filling out nonwork-related paperwork.
The inspectors discussed these observations with the Operations Manager, who
stated that these observations did not reflect written management policies for
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control room conduct and operations personnel would be briefed on proper control
room conduct.
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Decisions made in support of maintenance were usually conservative based on the
inspectors' reviews of TS limiting conditions for operation entered and exited.
During plant tours, the inspectors found that housekeeping continued to be
excellent. Any minor discrepancies identified by the inepectors were promptly
a corrected.
01.2 NEO Tours
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a. Inspection Scoce (71707)
On February 15,1997, during a backshift tour, the inspector accompanied the
reactor building NEO during the conduct of operator rounds. The operator rounds
included tours of the standby cooling tower, auxiliary building, fuel building, primary
containment, and several tunnels.
b Observations and Findinas
The inspector noted that the NEO demonstrated good self-checking techniques and
a questioning attitude during the tour. The NEO checked severalitems that were
important to safety but not specifically required to be signed off during the operator
rounds. The NEO identified two plant equipment deficiencies and wrote MAls for
the items. However, the inspectors identified two apparent weaknesses with the
operator round signoff sheets.
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The inspectors noted that the operator rounds procedure required the NEOs to
check lubricating oil level in several safety-related pumps and f ans, including the
emergency core cooling system and the standby service water pumps. However,
the operator round sheets only required a general inspection of SLC system area for
housekeeping purposes. Further, the round sheets did not specifically require the
NEOs to check the lubricating oil level of the SLC pumps or other appropriate pump
checks. During this inspection period, an MAI was issued for gasket replacement
on the Division 11 SLO pump because of a lubricating oil leak and a crack was
discovereo on the pump casing, which demonstrated a need to examine the SLC
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system during operator rounds.
The inspectors also noted that the operator round sheets required periodic entry
j (approximately every 2 weeks) into most of the high radiation and locked high
' radiation areas. In addition, the operator round sheets required a visual inspection
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of the suppression pool at the 95-foot elevation of containment. However, the
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round sheets required no entries into the area where the TIP system was located.
This area was identified as a high radiation area and was also located at the 95 foot
elevation of containment. The inspectors noted that, eckhout periodic tours of the
TIP system area, items could be in the suppression pc6 Lelow the TIP system area
and items could be left near the TIP system for a signWiuant period of time without
notice. The licensee performed maintenance in the TIP system area during this
inspection period, which required a number of items to be brought into the TIP
system area. The inspectors discussed improving the operator rounds weaknesses
with the Operations Manager, who stated that Operations would evaluate
improvements to the operator round sheets.
c. Conclusions
The NEO accompanied by the inspectors exhibited good operator practices and a
questioning attitude during reactor building operator rounds. The inspectors noted
areas for improvement with the operator round sheets in that the procedure did not '
require periodic checks of the SLC pumps or a tour of the TIP system area.
02 Operational Status of Facilities and Equipment
O2.1 Walkdown of EOP Suonortina Enclosures
On February 2% 1997, the inspectors evaluated licensee implementation of an EOP
supporting enclosure was contained within Pr2,ceire EOP 5, " Emergency Operating
Procedures-Enclosures," Revision 9. The inspectors walked down Enclosure 4,
which addressed defeating the isolation of the reactor water cleanup . system on low
reactor pressure vessel level and upon initiation of SLC. The inspectors verified that
all keys and tools were staged and that on-shift licensed operators wr e sufficiently
f amiliar with the actions stated in these enclosures. The inspectors t eluded that
the licensee adequately trained the operators and staged materials for effective
implementation of Enclosure 4 of Procedure EOP 5.
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06 Operations Organization and Administration ,
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06.1 Plant Staff Overtime Review
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a. Inspection Scoce (71707)
The inspectors reviewed tha overtime records of Operations, Radiation Protection,
and Plant Engineering personnel for January and February 1997 to ensure that the
licensee met the requirements of TS 5.2.2.e. In addition, the inspectors reviewed
proceoures to ensure that the TS was properly implemented.
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The requirements for controlling on-shift operator overtime were contained in
Procedure ADM-0022, " Conduct of Operations," Revision 19. This procedure
required formal documentation of the reasons for exceeding the TS overtime limits
in the control room operator log. The inspectors reviewed operator time sheets and
noted no instances of operating shift personnel exceeding the overtime 1
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requirements. However, the inspectors noted that everal individuals routinely
worked 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in a 7-day period with the plant cytru sting. This heavy work
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schedule did not meet the intent of TS 5.2.2.e, which states that the operating shift
1 complement shall be met without routine heavy use of overtime. The inspectors l
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also noted that several support staff personnel exceeded 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in a 48-hour
period and 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> in a 24-hour period. The licensee stated that because these
personnel were reviewing condition reports (CR), writing procedures, and I
performing other support functions, the support personnel were not considered
subject to the TS restrictions on working hours.
- The inspectors reviewed the overtime controls for Radiation Protection personnel.
The inspectors noted that Procedure RBNP-024, " Radiation Protection Plan,"
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Revision 7, implemanted the requirements of TS 5.2.2.e. However,
Procedure RBNP-024 merely repeated the words of TS 5.2.2.e, which states that
deviations from the TS overtime guidelines shall be authorized by the Plant Manager
4 or his designee in accordance with approved procedures. Procedure RBNP-024 did
not identify the procedure to be used. The inspectors identified five instances of
pesonnel exceeding 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in a 48-hour period. The Radiation Control
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Superintendent stated that the extra hours worked (up to 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />) were shift
turnover activities. The inspector noted that the extra hours were spent in radiation
protection shop meetings and training, which the licensee considered to be part of
shift turnover.
The inspectors reviewed the overtime of system engineers for January and
February 1997 and noted 14 instances where the TS limits were exceeded. For
exaniple, one individual worked 23 hours2.662037e-4 days <br />0.00639 hours <br />3.80291e-5 weeks <br />8.7515e-6 months <br /> in a 24-hour period. The Manager, Plant
Engineering stated that none of these system engineers had performed
safety-related work, although records indicated that these individuals spent
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significant amounts of time in the plant during their work periods. No procedure
was in place to control overtime of system engineers, as required by the TS.
The inspectors reviewed Procedure ADM-0023, " Conduct of Maintenance,"
Revision 138, to ascertain how the Maintenance Department implemented
TS 5.2.2.e. Section 8.1.5 of Procedure ADM-0023 stated that overtime shall be
controlled per Section 5 of the TS. No further direction was given for how overtime
for maintenance personnel was to be controlled administratively.
The inspectors requested that the licensee provide objective evidence that the Plant
Manager or his designee performed monthly reviews of overtime assigned as
required by TS 5.2.2.e. The licensee did not have objective evidence that these
reviews were performed. However, the licensee stated that when supervisors
reviewed their employees' time sheets, they ensured that excessive hours were not
worked. The inspectors performed a review of CRs dating back 3 years and noted
that no CRs were written concerning excessive overtime during this period of time.
In addition, the last CR written for personnel exceeding overtime controls was
written in 1994 by QA personnel, which appeared to indicate the quality of these
reviews was questionable.
TS 5.2.2.e states, in part, that procedures shall be developed to limit the working
hours of staff who perform safety-related functions, in addition, TS 5.2.2.e
. requires specific controls for the Plant Manager or his designee to document
exceeding the overtime limits and perform monthly reviews of overtime usage. The
procedures did not clearly delineate how each of these functions was to be
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performed for all of the personnel performing safety-related functions and what
specific controls were in place. In addition, the procedures did not define what
constituted safetyw lated work or shift turnover. The failure to maintain specific
administrative procedures that delineated specific controls for reviewing and
approving overtime for personnel who perform safety-related functions is a violation
of TS 5.2.2.e (50-458/9706-01).
c. Conclusions
A violation was identified for failure to develop administrative procedures with
specific controls for reviewing and approving personnel overtime. The licensee's
process for controlling overtime was weak in that the process was fragmented and
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was without clear definitions, lines of responsibility, and administrative processes.
Several individuals exceeded the TS overtime limitations without proper
administrative approvals.
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- 07 Quality Assurance in Operations
07.1 Nuclear Review Board
j a. inspection Scoce (71707)
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l The inspectors attended thc NRB meeting held on February 21,1997, and reviewed
the subcommittee reports and various presentations.
b. Observations and Findinas
The NRB meeting consisted of presentations on several safety and plant
performance issues, which was followed by formal discussion of these issues by
the members. The inspectors noted that, in general, the NRB membership asked
probing questions and recommended appropriate corrective actions.
The subcommittee for the FRC identified that the FRC minutes had not been issued
in a timely manner. There was a backlog of approximately 25 sets of minutes with
some being about 1 year late. The inspectors noted that untimely issuance of FRC
minutes impacted the NRB's ability to perform its oversight function because the
NRB bases much of its review of FRC effectiveness on FRC minutes. The licensee
initiated a CR to enter this item into the corrective action program. Although the
untimely issuance of the FRC minutes was indicative of poor performance, the FRC
charter did not have timeliness goals and no violation of NRC requirements
occurred.
The inspectors also observed the presentation of the NRB subcommittee that
provided oversight of the QA organization. The subcommittee concluded that QA
was effective without an apparent definition of what constituted QA effectiveness
(e.g., was QA reactive or were outside organizations identifying major issues that
QA had audited). The NRB recognized that QA required improvement but did not
emphasize some performance issues. For example, during the past quarter, QA
performed 17 surveillances of Maintenance, 5 of Engineering, and 3 of Operations.
The inspectors noted that these three functional areas have performed at the same -
level, as identified in the recent Systematic Assessment of Licensee Performance
report, so QA allocation of resources for surveillances did not appear to be
performance based. The NRB was not aware of the basis for the number of
surveillances performed in each area, in addition, one NRB member noted that a
number of QA reports were written and reviewed by the sarre person, but no action
was taken by the NRB to review whether or not this was considered a good
practice. The inspectors also noted that none of the subcommittees contained ,
outside members, which could have added to the quality of the subcommittee i
reviews.
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The inspectors discussed these observations with the Director, Nuclear Safety (the
NRB chairman) who agreed with the comments. The licensee initiated actions to
improve the effectiveness of the NRB.
c. Conclusions
The NRB was generally effective in reviewing plant issues and recommending
appropriate corrective actions. The excessive backlog of FRC minutes impeded the
NRB's ability to perform timely and effective oversight of FRC activities. QA
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surveillance resources were not allocated among the functional areas commensurate
with performance.
08 Miscellaneous Operations issues (92901)
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08.1 (Closed) Inspection Followun item (IFI) 50-458/95026-01: Review of methods used
1 by the licensee to manage overall plant risk associated with on-line maintenance.
The inspectors reviewed " River Bend Station On-Lins Maintenance Guidelines,"
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Revision 0, which was prepared by the on-line maintenance natural work team. The
document provided guidelines for integrating quantitative and qualitative risk
insights into the on-line maintenance process. The guidelines described the on-line
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maintenance process, which included the role of the various disciplines involved and
use of the equipment out of service (EOOS) computer.
The inspectors attended a 2-week look-ahead meeting on February 26,1997. This
- meeting was attended by planners from the various Maintenance, Operations, and
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Radiation Protection disciplines, the work week manager for the week being
planned, the outage management senior planner who operated the EOOS computer,
the work control supervisor, and others. The attendees discussed the proposed
work, testing, and operations on the plant planned for the week of March 9. There
was a good exchange of information and the inspectors noted that the EOOS
planner was knowledgeable of the nature of the activities and their impact on the
plant. This individual was also a licensed reactor operator in the past.
On February 27, the inspectors observed the outage management senior planner
apply the EOOS program to the information gained in the February 26 meeting
above. The planne demonstrated proficiency in applying the program and produced
a report that identified the plant safety index for each day and night during the
planned week of March 9. The plant safety index was a simplified graded
representation of core damage frequency. The values for the week of March 9
were Green (nonrisk significant) even though there suas a Division 11 EDG outage
planned. This was expected, however, because the planners staggered the
equipment outages to minimize diverse system outages and the 12-week revolving
schedule restricted the week of March 9 to Division ll only, which eliminated the
potential for a loss of safety fonction.
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The inspectors interviewed the operating personnel on day shift on February 27 and 1
found that the shift technical advisor and the work control supervisor had a working 1
j knowledge of the EOOS computer monitor. They were cognizant of the need to l
. utilize the EOOS program when emergent work or testing appeared or the schedule j
i shifts to the extent that safety-significant equipment could be placed out of service.
This was acceptable.
11. Maintenance
M1 Conduct of Maintenance
M1.1 Troubleshootina of Control Buildina Chiller C
a. Insoection Scope (62707)
The inspectors observed portions of troubleshooting activities associated with tiie
low refrigerant temperature trip of safety-related Control Building Chiller C. The
work was accomplished in accordance with MAI 310606.
b. Observations and Findinas
On February 19,1997, Control BuilJing Chiller C tripped off because of low
refrigerant temperature. This chiller provided air conditioning to the control building,
including the main control room. Chiller D started automatically and assumed the
load, as designed.
The operators declared the chiller inoperable and since there was another operable l
100 percent capacity chiller in Division I, TS limiting conditions for operation were j
met. CR 97-0227 was initiated to enter the prob lem into the corrective action
program. Chiller C was overhauled in the fall of 1996, including the chemical j
cleaning of the chiller heat exchangers. Subsequent to the cleaning, there were
problems experienced after the startup of the chiller with refrigerant strainers
becoming clogged. This was resolved by repeated running of the chiller and
cleaning of the strainers and filters. This appeared to have been successful until the
February 19 trip of the chiller. The licensee suspected that the strainer and filter
were clogged again, so the MAI instructed the mechanics 'io open and inspect the
strainer in the economizer and tho filters in the filter / dehydrator.
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The inspectors reviewed the MAIinstructions and found them to be well written
and concise. The inspectors observed the mechanics as they opened both ends of
the economizer to inspect for clogged strainers or foreign materiai. The work was
performed well and in accordance with the mal instructions. The mechanics were
trained and experienced in working with the chillers.
When mechanics removed the head from the high side of the economizer, the float
valve float was lying in the bottom, disconnected from the valve operating shaft.
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The system engineer explained that failure of the float valve to operate properly 1
caused the chiller to trip on low refrigerant temperature because there was
insufficient refrigerant returning to the evaporator. The system engineer l
documented this problem in CR 97-0227. The inspectors noted that the fastener
compressing the clamp on the end of the float arm was not tight enough to
compress the lock washer and secure the arm to the valve shaft; therefore, the float !
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worked itself off the valve shaft. Because there was a key on the valve shaft, the l
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float valve probably functioned properly until it fell off the valve shaft. l
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System Engineering management evaluated the loose fastener issue and determined j
that this was an isolated workmanship problem not affecting the other three !
- safety related chillers because they had not been dismantled recently for major
cleaning as was Chiller C. The issue of human performance was referred to the '
In-House Events Analysis group for root cause and corrective action determination
in accordance with the corrective action program.
The inspectors questioned maintenance management as to the cause of the i
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improper assembly of the float arm. The inspectors reviewed the documentation of !
the previous installation of the economizer float arm, which occurred on 1
October 13,1996 (MAI 307327). The inspectors found that the instructions were
adequate to properly install the float arm and apparently were not followed. The )
Mechanical Maintenance Superintendent stated that the instructions were adequate !
and the mechanics failed to self-check or peer check the installation. This was
exacerbated by the limited accessibility of the fastener for tightening in accordance i
with MAI 307327.
Corrective actions taken or planned by the licensee included checking the
economizer low side float arm (it was properly installed), ensuring the high side float
arm was properly reassembled by checking for tightness on the valve shaft,
changing the mal instructions to specifically check the float arm for proper
assembly during future work on all the safety-related chillers, and reinforcing
self-checking and peer checking while reviewing this incident with mechanical
maintenance personnel.
Failu e to comply with the written instructions in MAI 307327 for installation of the
Chiller C economizer float arm is a violation of TS 5.4.1.a. However, this
self-identified and licensee-corrected violation is being treated as an NCV consistent
with Section Vll.B.1 of the NRC Enforcement Policy. Specifically, the violation was
self-identified and documented by the licensee, was not willful, actions taken as a
result of a previous violation should not have corrected this problem, and
appropriate corrective actions were completed by the licensee (50-458/9706-02).
c. Conclusions
Mechanics demonstrated good performance as they perfrmed troubleshooting and
correction of the Control Building Chiller C low refrigerant temperature trip. The trip
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resulted from improper assembly of the chiller economizer valve float arm. An NCV
i was identified for failure to properly implement the applicable work instructions
during the previous assembly.
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l M1.2 Dsion 11 EDG Outaae
a. Inmeetion Scoce (62707)
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The inspectors witnessed the following MAls on March 12,1997, during the :
- Division II EDG maintenance outage. )
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' MAI P593078 Calibrate Temperature Switch 1EGS-TS2B l
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MAI P593131 Calibrate Temperature Switch 1EGS-TS9?R
MAI P591340 Preventive maintenance on Breaker 1ENSSWGR-BKR-ACB27
(Division II EDG 4160 Volt Supply Breaker) j
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i b. Observations and Findinas
- The inspectors noted that the Division 11 maintenance outage was well planned with
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the Division ll EDG unavailability time minimized. MAls P593078 and P593131 -
were performed well ent' in accordance with procedures.
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During performance of MAI P591340, the electricians timed the breaker opening
and closing using a test cabinet. Step 9.9.1 required the electricians to connect
, the breaker test cabinet leads to Terminals 6,7, and 9 of the secondary ,
disconnects. The breaker primary disconnects were required to be connected to the i
timer and the timer connected again using the secondary disconr'ects. The
electricians connected the leads from the timer to test ja':ks on the face of the plant
breaker test cabinet,
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The inspectors questioned the electricians on this practice because the timer test ;
leads were not connected directly to Terminals 6,7, and 9. The electricians replied
that the MAI was written for performance of the preventive maintenance in the
shop, rather than using the breaker test cabinet installed in the field. The
electricians further stated that the configuration used was functionally equivalent to I
the setup described in the MAI and they intended to perform the work, then revise
the MAI to fit the methodology used. The electricians did not know if the test
setup that they used actually connected through Terminals 6,7, and 9 of the
breaker. The technicians completed the task and the breaker was retested
satisfactorily.
Following completion of the task, the electricians researched the acceptability of the
test setup using wiring drawings. The electricians found that they had actually
used Contacts 6,7, and 9; therefore, the electricians complied with the procedure.
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The inspectors reviewed the drawings and concurred with the electricians'
conclusion.
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The inspector discussed these observations with electrical maintenance supervision.
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The inspectors noted that although a violation did not occur, the electricians !
. appeared to proceed in the face of uncertainty and had the MAI been worded l
} slightly differently, the electricians would not have been in compliance with the '
MAI. The Electrical Maintenance Supervisor agreed with the inspectors comments j
and discussed them with the electricians. '
c. Conclusions
The Division ll EDG maintenance outage was well planned with the Division 11 EDG
unavailability time minimized. The MAls for the Division ll EDG were generally
performed well.
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M1.3 Surveillance Observations 4
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a. Inspection Scooe (61726) l
The inspectors observed all or portions of the following surveillance tests during this
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inspection period: j
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STP-309-0202 Division 11 EDG operability testing on February 11,1997.
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PEP-0083 Signature testing of Motor Operated Valve 1E51-MOVF059,
tank bypass to the condensate storage tank, a
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postmaintenance test, on February 19.
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STP-051-4522 Emergency core cooling system and reactor core isolation
, cooling response to reactor vessel low water level channel
functional test, on February 24.
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l b. Observations and Findinas
The inspectors found that the surveillance tests listed above were conducted
properly such that meaningful results were obtained. Self-checking and peer
checking wea evident when it was appropriate to do so. During independent
verification, the verifiers demonstrated a conscious effort to maintain independence
from the performers. TS limiting conditions for operation were entered, when
required. Measuring end test equipment was verified to have been in calibration.
The inspectors reviewed the completed test documentation and noted that it was
legible and all acceptance criteria were met.
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c. C_,
o nclusions l
All surveillance tests observed in this section of the report were performed properly l
and in accordance with the applicable procedures. Self checking was evident as the
test performers manipulated valves and switches. l
M 1.4 Missed EDG Surveillance i
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a. Inspection Scope (61726) j
The inspectors evaluated the response to CR 97-01J4, which identified that the
loss of power function to the Division il EDG had not been adequately surveillance
tested.
b. Observations and Findinas
On February 13,1997, during a logic system functional test review, the licensee
identified that they had not been adequately testing the starting circuitry for the
Division ll EDG, The licensee found that individual contacts actuated each of the air
banks for the air starting system. The forward air starting system contact was
adequately tested during refueling outage (RFO) 6, but the contact for the rear air I
starting system had not been verified as operable. Therefore, the licensee noted
that TS 3.3.8.1 (EDG instrumentation) requirements may not have been met.
The licensee wrote an operability evaluation, which stated that the EDG was
operable because either the forward or rear air starting system was adequate to
meet the system design basis, and as long as the forward air starting system was
operable, the Division ll EDG was operable. The inspector reviewed the licensee's
operability assessment and identified no concerns.
However, the inspector asked the licensee if the forward air system had been
removed from service such that the licensee was depending on the rear air starting
system (which was not adequately surveillance tested) for operability of the Division
11 EDG. The system engineer stated that, since RFO 6, the forward air starting
system for the Division 11 EDG had not been removed from service. The inspector
independently reviewed the tracking limiting conditions for operation since RFO 6
and identified that the forward air starting system was declared inoperable from
February S-19,1997. In addition, the inspector identified three 2-week periods in
the previoun operating cycle where the forward air starting system was inoperable.
These time periods in which the forward air starting system was inoperable
exceeded the 72-hour limiting condition for operation for the Division 11 EDG. In
addition, the licensee changed operational modes from Mode 4 (Cold Shutdown), to
Mode 2 (Startup) on February 14 with the forward air inoperable.
Therefore, the failure to test the loss-of-power contact for the rear air starting ,
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system of the Division 11 EDG during the time periods when the forward air starting
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system was inoperable constituted a missed surveillance. The licensee revised tne
test procedure to ensure that all of the loss of power functions were properly
tested. Because this test was intrusive while operating at power, the licensee
chose not to perform the test until the next outage or if forward air became
inoperable again. Although the licensee had not performed the surveillance test, the
licensee believed, based on past EDG reliability and engineering judgment, that the
surveillance of the rear air starting circuitry would probably pass; therefore, the
Division 11 EDG was capable of meeting its intended safety function even during
times that forward air was inoperable.
The failure to perform the required surveillance of the loss-of-power contact for the
rear air starting system of the Division 11 EDG was a violation of TS SR 3.0.2. This
licensee-identified and corrected violation is being treated as an NCV consistent
with Section Vll.B.1 of the NRC Enforcement Policy. Specifically, the violation was
identified by the licensee, was not willful, actions taken as a result of a previous
violation should not have corrected this problem, and appropriate corrective actions
were completed by the licensee (50-458/9706-03).
c. Conclusions l
The engineer performing the logic system functional test review exhibited excellent
attention to detail in identifying that the loss of power contact for the Division il l
EDG rear air starting system was not properly tested. An NCV was identUied for )
failure to comply with TS SR 3.0.2. The licensee's initial review of the Division 11 ;
EDG past operability was weak in that the review did not discover a past outage of !
the forward air starting system.
Ill. Enaineerina
E2 Engineering Support of Facilities and Equipment
E2.1 Inaoorooriate Acolication of Core Ooeratina Limits Reoort ;
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a. Insoection Scoce (37551)
The inspectors reviewed the actions in response to CR 97-0256, where the reactor
engineers identified an error in applying required changes in the OLMCPR at the
correct time within the current fuel cycle, as required for GE-11 fuel.
b. Observations and Findinas
On February 25,1997, while monitoring and reviewing the approach of the reactor
full power exposure at which the OLMCPR for the newer GE-11 fuelin the reactor
must be changed from 1.28 to 1.32, the reactor engineers realized that the date
should have been February 19. Consequently, from February 19-25, the reactor
operators had been monitoring a maximum fraction limiting critical power ratio
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(MFLCPR) that was nonconservative and could have allowed the OLMCPR limit to
be exceeded.
The reactor engineers immediately implemented an administrative limit of 0.969 for
1.32 until the correct limit was programmed into the 3D Monicore computer
i monitor. The program was subsequently adjusted on February 26 and the
monitored parameters were restored to those normally observed by the reactor
operators.
, The core operating limits were not exceeded during the above 6-day period. The
reactor engineers reviewed the historic core performance edits and found that the
highest MFLCPR was 0.911, which translated to 0.9395 with an OLMCPR of 1.32.
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The licensee stated that the cause of the above problem was human arror. The
supplemental reload licensing report from General Electric indicated ;.: dicted
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end-of-cycle full pnwer exposure of 11,850 megawatt days per short ton of fue:.
The report indicated that the OLMCPR should be changed from 1.28 to 1.32 when
the exposure reached end-of-cycle, minus 3350 megawatt days per short ton.
Subsequent to startup from RFO 6, the startup and operations report stated that the
predicted eno-of-cycle full power exposure would be 12,626.2. The reactor
engineer subtracted 3350 from 12,626.2 instead of 11,850, in error, and tracked
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core exposure to the longer exposure time.
To prevent a recurrence, the licensee was considering requesting software for the
i 3D Monicore System to automatically shift the OLMCPR limit at the appropriate time
during the fuel cycle. The appropriate actions were taken to reduce personnel
, errors.
The inspectors concluded that there was no violation of regulatory requirements;
] however, this was poor human performance. The safety significance was mitigated
by the fact that the reactor was being operated with sufficient margin from thermal
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limits such that minor errors, as discussed above, did not result in exceeding the
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c. Conclusions
The reactor engineers demonstrated poor performance by calculating the incorrect
full power exposure at which to change the OLMCPR for GE-11 fuelin the reactor in
accordance with the license. Consequently, a nonconservative limit was being
monitored by the reactor operator for 6 days. No licensed thermallimits were
exceeded because the reactor was being operated with sufficient margin below the
limits.
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E2.2 Review of Facihtv Conformance to Updated Final Safety Analysis Report
Descriptions
Discovery of a licensee operating a facility in a manner contrary to the Updated
Final Safety Analysis Report highlighted the need for a special focused review that
compares plant practices, procedures, and/or parameters to the Updated Final
Safety Analysis Report. While performing the inspections dic,assed in this report,
the inspectors reviewed the applicable portions of the Updated Final Safety Analysis
Report that related to the areas inspected. The inspectors verified that the Updated
Final Safety Analysis Report wording was consistent with the observed plant
practices, procedures, and/or parameters. No inconsistencies were noted.
.E3 Engineering Procedures and Documentation
E3.1 Deficiencies in Determinina Extended LLRT Intervals
a. Insoection Scope (37551)
The inspectors reviewed the response to CR 97-0127, which identified four
safety-related valves that were inappropriately selected for an extended LLRT
interval of 5 years, and therefore were not tested within the 2-year interval required
by the LLRT program,
b. Observations and Findinas
On February 4,1997, while reviewing LLRT intervals in preparation for testing to be
performed during the upcoming refueling outage in September 1997 (RFO 7), Plant
Engineering determined that four safety-related valves were not tested during the
previous refueiing outage in January 1996 (RFO 6). The valves were not tested
because they were selected for a 5-year LLRT interval pursuant to the
performance-based LLRT program, which implemented Option B of 10 CFR Part 50,
Appendix J.
The four containment isolation valves in question were: (1) E12-MOVF027B, Low
Pressure Coolant Injection B to the reactor, (2) E12-MOVF0378, Low Pressure
Coolant injection B to the reactor, (3) E51-MOVF068, reactor core isolation cooling
turbine exhaust to the suppression pool, and (4) SWP-MOV503B, standby service
water return from Containment Unit Cooler B.
The operators entered TS SR 3.0.3, which allowed 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for the licensee to
accomplish the LLRT for the valves before declaring the effected systems inoperable
because of the missed surveillance. The LLRT was completed satisfactorily for each
of the four valves by February 7. It was r.ecessary to declare the effected systems
inoperable in order to support testing and the operators entered the appropriate
TS limiting conditions for operation.
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The licensee explained that the personnel in charge of the LLRT program prior to l
RFO 6 did not document why they selected the four valves for the extended
interval. The licensee stated they assumed the decision was based on the criteria
stated in Procedure ADM-0050, " Primary Containment Leakage Rate Testing,"
Revision 4. Procedure ADM-0050 implemented a performance-based LLRT program
pursuant to 10 CFR Part 50, Appendix J, Option B. According to
Procedure ADM-0050, in order to select a given valve for extended LLRT interval,
among other criteria, the two previous consecutive LLRT as-found results must not
have' exceeded the administrative limits. The four valves had satisf actory results in
RFO 4; however, the RFO 5 results were as-left after maintenance was performed
on the actuators.
On February 4,1997, Plant Engineering determined that the criteria had not been
met, and therefore, an LLRT should have been performed on the four valves during
RFO 6. While this was considered to be a missed surveillance, the licensee stated
that this was probably a conservative decision, because the nature of the
maintenance done during RFO 5 probably had no significant effect on the leak
tightness of the valves. The inspectors reviewed the documentation of the
maintenance performed on the four valves and found that the actuators were
removed from the valves, dismantled in the shop, cleaned and lubricated, and in
two cases, the torque switches were balanced. This was clearly more work than
Procedure ADM-0050 allowed in order to accept an as-left LLRT for an as-found
value.
On February 13, the licensee informed the inspectors that they had looked more
thoroughly into the LLRT history of the valves and found in each case that an
acceptable as-found LLRT was completed during RFO 3 and no maintenance was
done at that time. Furthermore, the licensee demonstrated to the inspectors'
satisfaction that the actuator maintenance performed during RFO 5 would not have
had any significant impact on valve leakage and thus would not have masked a
problem if it had occurred with valve seat tightness. Therefore, it was not
necessary to perform the LLRTs on the four valves on February 4 as described
above. The inspectors questioned why this did not come to light during the Plant
Engineering review ano the reply was that the RFO 3 data was not on the matrix
they were using.
The inspectors expressed concern that the licensee appeared to have been
unsuccessful in implementing and prescribing a program that effectively reflected
the test interval guidance provided by NUREG-1493, " Performance-Based ,
Containment Leak-Test Program," September 1995, and the " Nuclear Energy I
Institute industry Guideline for implementing Performance-Based Option of
10 CFR Part 50, Appendix J," July 26,1995. It was evident that the licensee had
several opportunities to correct the problem. For example, in January 1996, a
programmatic review identified 18 valves that may not have met the criteria for
extended intervals (CR 96-0319). The CR was closed in March 1996. In
July 1996, during a Quality Assurance review, another valve was identified as
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having been placed on extended interval inappropriately (CR 96-1327). No other
similar examples were identified during that review. The CR was closed in
August 1996.
In September 1996, a reevaluation of CR 96-0319 identified two valves that should
have been tested during RFO 6 (CR 96-0319A). An NCV was identified on this
issue in NRC Inspection Report 50-458/96-14, Section M1.3. Also in
September 1996, the inspectors identified that Procedure ADM-0050 permitted a
25 percent extension on LLRT test intervals, when TS 5.5.13 does not allow it.
Although there were no examples found where the extension was inappropriately
used, as of February 1997, the procedure error had not been corrected
(CR 96-1564). During this inspection period, because of ambiguities in the
performance-based LLRT program, safety-related systems were taken out of service
unnecessarily during power operation to accomplish testing that was not needed.
The licensee explained that in January 1996, because of the complexity and
newness of the performance-based LLRT program at River Bend, experienced and
knowledgeable people were brought in from another plant and established the first
program for Entergy Operations, Inc., to make sure that proper decisions were made -
for testing during RFO 6. Again in February 1997, industry experts were brought in
to review the program in preparation for testing during the upcoming RFO 7.
Although these were proactive initiatives to ensure proper implementation of their
new performance-based LLRT program, the inspectors considered the program
should have been corrected early in 1996.
Corrective actions initiated during this inspection period included clarifying the
requirements associated with the performance-based LLRT program by revising
Procedure ADM-0050 and providing the appropriate training for personnel
responsible for implementation of the program. The licensee also indicated that
Engineering would be documenting the basis of each component placed on
extended test intarval. On February 13,1997, the General Manager, Plant
Operations directed the establishment of a review team whose charter would be to
step back and review the overall surveillance program and recent initiatives to
determine if an adjustment was warranted, based on the above CRs.
Because the licensee identified and was in the process of correcting nearly all of the
above problems associated with the LLRT program, the inspectors considered
exercising enforcement discretion. However, Section Vll.B.1.(b) of the NRC's
Enforcement Policy, NUREG-1600 could not be satisfied, in that this was a violation
that could reasonably have been expected to have been prevented by the corrective
actions for previuus licansee findings. Failure to establish and maintain adequate
procedures to implement a satisfactory performance-based LLRT program pursuant
to 10 CFR Part 50, Appendix J, is a violation of TS 5.4.1.a (50-458/9706-04).
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c. Conclusions
. The failure to establish clear procedural guidance for the implementation of a
performance-based LLRT program pursuant to 10 CFR Part 50, Appendix J,
Option B, resulted in missed td.ing of valves and unnecessary testing of other
valves that required taking safety-related systems out of service during plant '
,
operation at power. A violation of TS 5.4.1.a was identified.
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IV. Plant Support
R1 Radiological Protection and Chemistry Controls
R1.1 Insoection Scone (71750)
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a. Throughout this inspection period, the inspectors observed performance in
radiological protection. The inspectors observed a sample of radiation, high
, radiation, and locked high radiation areas to verify that these areas were properly
posted and controlled.
b. Observations and Findinas
On February 20,1997, the inspectors noted that Door TUO70-001 was propped
open to support the ADHR modification. The personnel involved properly obtained
permission from the control room to prop this door open and an hourly fire watch
patrol was assigned. However, the sign posted to inform personnel that this area
was a radiation area was hung on this door. Therefore, when door TUO70-001 was
propped open, the radiation area sign was obscured from view such that not all
personnal entering the area would not be aware that they were entering a radiation J
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The inspectors informed RP that the entrance to the ADHR room was not
adequately posted. An RP technician relocated the radiation area sign from the door
to a stanchion placed at the doorway. The licensee initiated CR 97-0257 to enter
this item into the corrective action program.
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On February 24, an RP technician reinspected the radiological postings near the
ADHR room. The RP technician noted that the stanchion with the radiation area
sign that was previously located in the doorway cf the ADHR room had been moved
to a corner of the room. RP personnel reposted the area by hanging the radiation
area sign on a rope across the doorway. This additional unauthorized movement of
the radiation area sign was added to CR 97-0257.
10 CFR 20.1902(a) requires each radiation area to be conspicuously posted with
signs stating " CAUTION, RADIATION AREA." Because the radiation area sign et
the entrance to the ADHR room was obscured from view, this radiation area was
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not conspicuously posted as required. The failure to conspicuously post a radiation
area is a violation of 10 CFR 20.1902(a) (50-458/9706-05).
The inspectors noted that this violation was mitigated because no unauthorized
personnel entered the radiation area without proper dosimetry. However, the
inspectors noted that River Bend general employee training information directed
radiation workers to obey all radiological postings and stated that any unauthorized
removal or movement of radiological postings will not be tolerated. The above
violation indicated that personnel involved with the ADHR modification were not
adequately implementing their training on basic radiological work practices. In
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addition, NRC Inspection Report 50-458/96-06 discussed two previous instances in
which radiological postings were inappropriately relocated, which indicated that
improvement in ensuring radiological postings were intact was required.
, c. Conclusions
A violation was identified for failure to conspicuously post a radiation area. On two
occasions the radiation area posting at the entrance to the ADHR room was
modified without RP approval, which indicated that personnel were not sufficiently
sensitive to following basic radiation prctection practices. No unauthorized entries
or unmonitored dose resulted from these posting deficiencies.
S1 Conduct of Security and Safeguard Activities
S 1.1 General Comments (71750)
Throughout this inspection period, the inspectors observed security and safeguards
practices. Security boundaries were maintained properly and entry screening
processes were performed properly at the primary access point. The inspectors
noted during night tours that the protected area was properly illuminated.
V. Manaaement Meetinas
X1 Exit Meeting Summary
The inspectors presented the inspection results to members of licensee management at the
conclusion of the inspection on March 24,1997. The licensee acknowledged the findings
presented.
The inspectors asked the licensee whether any materials examined during the inspection
should be considered proprietary. No proprietary information was identified.
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ATTACHMENT
SUPPLEMENTAL INFORMATION
PARTIAL LIST OF PERSONS CONTACTED
Licensee
J. P. Dimmette, General Manager, Plant Operations
' M. A. Dietrich, Director, Quality Programs
D. T. Dormady, Manager, System Engineering
J. R. Douet, Manager, Maintenance
J. Holmes, Superintendent, Chemistry
H. B. Hutchens, Superintendent, Plant Security
D. N. Lorfing, Supervisor, Licensing
C. R. Maxson, Senior Lead Licensing Engineer i ,
J. R. McGaha, Vice President-Operations
W. P. O'Malley, Manager, Operations
W. H. Odell, Superintendent, Radiation Control
D. L. Pace, Director, Engineering
INSPECTION PROCEDURES USED
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IP 37551 Onsite Engineering
IP 61726 Surveillance Observations .
IP 62707 Maintenance Observation j
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lP 71707 Plant Operations
IP 71750 Plant Support Activities
IP 92901 Followup - Operations
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ITEMS OPENED AND CLOSED l
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Opened I
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50-458/9706-01 VIO Failure to establish procedure to control overtime l
(Section 06.1)
50-458/9706-04 VIO Failure to adequately maintain LLRT program
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(Section E3.1) )
! 50-458/9706-05 VIO Failure to conspicuously post radiation area ,
(Section R1.1) l
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Closed
50-458/95026-01 IFl Review of plant risk assessment for on-line maintenance l
(Section 08.1) l
Opened and Closed
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50-458/9706-02 NCV Failure to implement MAI on control building emergency
chiller (Section M1.1)
50-458/9706-03 NCV Missed surveillance on EDG air start circuitry
(Section M1.4)
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LIST OF ACRONYMS USEO
ADHR Alternate Decay Heat Removal
CR Condition Report
EDG Emergency Diesel Generator
EOOS Equipment Out of Service
EOP Emergency Operating Procedure
FRC Facility Review Committee
IFl Inspection Followup item
MAI Maintenance Action item
MFLCPR Maximum Fraction Limiting Critical Power Ratio
NCV Noncited Violation
NEO Nuclear Equipment Operator
NRB Nuclear Review Board
OLMCPR Operating Limit Min; mum Critical Power Ratio
PDR Public Document Room
QA Quality Assurance
RFO Refueling Outage
RP Radiation Protection
SR Surveillance Requirement
TIP Traversing incore Probe
TS Technical Specification