Letter Sequence Request |
---|
|
|
MONTHYEARML20087M6171984-03-28028 March 1984 Forwards Proprietary & Nonproprietary Versions of, Methodology for Addressing Superheated Steam Releases to Ice Condenser Containments. Proprietary Version Withheld (Ref 10CFR2.790) Project stage: Request ML20092D9801984-06-15015 June 1984 Informs That Westinghouse Determined Main Steam Line Break in Doghouses Can Cause Steam Generator Tubes to Uncover, Allowing Superheated Steam to Form,Generating Higher Steam Line Exit Temps.Equipment Qualification Based on 330 F Project stage: Other ML20090C4421984-07-11011 July 1984 Advises That Confirmatory Item 12, Main Steam Line Break, Reviewed W/Respect to Pending Request to Load Fuel & Perform Precritical Testing.Consequences Less Severe than FSAR Section 15.1.5 Analysis Project stage: Other ML20094M9801984-08-0808 August 1984 Forwards Summary Evaluation of Main Steam Line Break Analysis for Both Inside Containment & in Doghouse.Plant Safety Would Not Be Adversely Affected in Event of Design Basis Main Line Break in Doghouse or Inside Containment Project stage: Other ML20127L7191985-05-31031 May 1985 Evaluation of Main Steam Line Break in Doghouse Project stage: Other ML20127L6971985-06-21021 June 1985 Forwards Evaluation of Main Steam Line Break in Doghouse. Higher Temps Generated in Event of Main Steam Line Break in Doghouse Will Not Affect Capability to Shut Down Main Reactor & Maintain Safe Condition Project stage: Other ML20135H8551985-09-16016 September 1985 Forwards Request for Addl Info on 850621 Submittal Re Main Steam Line Break in Doghouse.Response Requested within 60 Days of Ltr Date Project stage: RAI ML20137C0161985-11-15015 November 1985 Forwards Responses to 850916 Request for Addl Info Re Main Steam Line Break in Doghouse.Heat Transfer Rate Maintained in Excess of Value Calculated W/Combination of Tube Bundle Uncovery & Superheated Steam Heat Transfer Project stage: Request ML20206M5621986-08-13013 August 1986 SER Accepting 840808 & 850621 Responses to IE Info Notice 84-90, Main Steam Line Break Effect on Environ Qualification of Equipment. Higher Temp Will Not Preclude Ability to Shut Down Reactor in Safe Shutdown Condition Project stage: Other ML20206M5571986-08-13013 August 1986 Forwards SER Accepting 840808 & 850621 Responses to IE Info Notice 84-90, Main Steam Line Break Effect on Environ Qualification of Equipment. Higher Temp Will Not Preclude Ability to Shut Down Reactor in Safe Shutdown Condition Project stage: Approval 1985-11-15
[Table View] |
|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H5811999-10-15015 October 1999 Forwards 1999 Update to FSAR, for McGuire Nuclear Station.With Instructions,List of Effective Pages for Tables & List of Effective Pages for Figures ML20217F3261999-10-13013 October 1999 Submits Quantity of Tubes Insp from Either Side of SGs A-D & Lists Tubes with Imperfections,Locations & Size.No Tubes Removed from Svc by Plugging.Total of Eleven Tubing Wear Indications Identified at Secondary Side Supports in SGs ML20217F3591999-10-13013 October 1999 Forwards Info Copy of Cycle 14 COLR for McGuire Nuclear Station,Unit 1 ML20217F8011999-10-13013 October 1999 Informs That on 990930,NRC Completed mid-cycle PPR of McGuire Nuclear Station.Areas That Warranted More than Core Insp Program Over Next Five Months,Not Identified.Historical Listing of Plant Issues Encl ML20217G7861999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20217H0041999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217F8231999-10-13013 October 1999 Informs That on 990930,NRC Completed mid-cycle PPR of Catawba Nuclear Station.Based on Review,Nrc Did Not Identify Any New Areas That Warranted More than Core Insp Program Over Next Five Months.Historical Listing of Issues,Encl ML20217F1301999-10-0707 October 1999 Forwards Rev 1 to Request for Relief 99-03 from Requirements of ASME B&PV Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting (Vg) Sys ML20217J5091999-10-0606 October 1999 Forwards Revs to Section 16.15-4.8.1.1.2.g of McGuire Selected Licensee Commitments Manual.Section Has Been Revised to Allow Testing of Portions of DG Fuel Oil Sys Every 10 Yrs ML20217C8351999-10-0505 October 1999 Communicates Correction to Info Provided During 990917 Meeting with Duke Energy & NRC Region Ii.Occupational Radiation Safety Performance Indicator Values Should Have Been Presented as 1 Instead of 0 ML20217C4471999-10-0404 October 1999 Forwards Insp Repts 50-369/99-06 & 50-370/99-06 on 990801- 0911.Determined That One Violation Occurred & Being Treated as Non-Cited Violation ML20212J2191999-10-0404 October 1999 Informs That Util 980326 Response to GL 97-06, Degradation of SG Internals Provides Reasonable Assurance That Condition of Steam Generator Internals Are in Compliance with Current Licensing Bases for Facility ML20212J7801999-10-0404 October 1999 Discusses GL 98-01 Issued by NRC on 980511 & DPC Responses for McGuire NPP & 990615.Informs That NRC Reviewed Responses & Concluded That All Requested Info Re Y2K Readiness Provided.Subj GL Considers to Be Closed ML20212J3011999-10-0101 October 1999 Forwards Exemption from Certain Requirements of 10CFR54.17(c) Re Schedule for Submitting Application for Operating License Renewal.Se Also Encl ML20217K2651999-10-0101 October 1999 Forwards Retake Exams Repts 50-413/99-302 & 50-414/99-302 on 990921-23.Two of Three ROs & One SRO Who Received Administrative Section of Exam Passed Retake Exam, Representing 75 Percent Pass Rate 05000414/LER-1999-004, Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments1999-09-27027 September 1999 Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments 05000413/LER-1999-015, Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept1999-09-27027 September 1999 Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept ML20217A7911999-09-24024 September 1999 Forwards Insp Repts 50-413/99-05 & 50-414/99-05 on 990718- 0828 at Catawba Facility.Nine NCVs Identified Involving Inadequate Corrective Actions Associated with Degraded Svc Water Supply Piping to Auxiliary Feedwater Sys ML20212E6471999-09-24024 September 1999 Discusses GL 98-01 Issued by NRC on 980511 & DPC Responses for Catawba NPP & 990615.Informs That NRC Reviewed Response for Catawba & Concluded That All Requested Info Provided.Considers GL 98-01 to Be Closed for Catawba ML20212M1651999-09-23023 September 1999 Refers to 990917 Meeting at Region II Office Re Licensee Presentation of self-assessment of McGuire Nuclear Station Performance.List of Attendees & Licensee Presentation Handouts,Encl ML20212F0941999-09-21021 September 1999 Discusses Closeout of GL 97-06, Degradation of Steam Generator Internals for Cns,Units 1 & 2 05000414/LER-1999-005, Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments1999-09-20020 September 1999 Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments ML20212M2001999-09-20020 September 1999 Confirms 990913 Telcon Between M Purser & R Carroll Re Management Meeting to Be Conducted on 991026 in Atlanta,Ga to Discuss Operator Licensing Issues ML20212D1671999-09-20020 September 1999 Forwards Exemption & SER from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Re Isolation of Main Steam Branch Lines Penetrating Containment.Exemption Related to Licensee Application ML20212B6491999-09-15015 September 1999 Informs That Encl Announcement Re 990913 Application for Amend to Licenses NPF-9 & NPF-7 Forwarded to C Observer in North Carolina,For Publication ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20216E8791999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for July 1999 for McGuire Nuclear Station ML20212A4131999-09-14014 September 1999 Informs That TR DPC-NE-2009P Submitted in 990817 Affidavit, Marked Proprietary,Will Be Withheld from Public Disclosure, Pursuant to 10CFR2.709(b) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20212B4641999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for Catawba Nuclear Station,Units 1 & 2 ML20212M1931999-09-13013 September 1999 Refers to 990909 Meeting Conducted at Region II Office Re Presentation of Licensee self-assessment of Catawba Nuclear Station Performance.List of Attendees & Licensee Presentation Handout Encl ML20212A3751999-09-10010 September 1999 Informs That Postponing Implementation of New Conditions Improved by RG 1.147,rev 12,acceptable Since Evaluation on Relief Based on Implementation Code Case for Duration of Insp Interval ML20212A0501999-09-10010 September 1999 Informs That Postponing Implementation of New Conditions Improved by RG 1.147,rev 12,acceptable Since Evaluation on Relief Based on Implementing Code Case for Duration of Insp Interval ML20212A2631999-09-0909 September 1999 Forwards Rev 25 to McGuire Nuclear Station,Units 1 & 2 Pump & Valve Inservice Testing Program, IAW 10CFR50.55a. Section 8.0 Contains Summary of Changes & Detailed Description of Changes Associated with Rev 25 ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 05000413/LER-1999-014, Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment1999-09-0101 September 1999 Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment 05000414/LER-1999-003, Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev1999-08-31031 August 1999 Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev 0 of LER ML20211J3671999-08-31031 August 1999 Forwards Public Notice of Application for Amend to License NPF-9 Seeking one-time Extension of Surveillance Frequency for TS SR 3.1.4.2 Beyond 25% Extension Allowed by TS SR 3.0.2 ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting ML20211K8831999-08-26026 August 1999 Forwards Insp Repts 50-369/99-05 & 50-370/99-05 on 990620-0731.Two Violations Occurred & Being Treated as NCVs ML20211M8191999-08-25025 August 1999 Confirms 990825 Telcon Between G Gilbert & R Carroll Re Mgt Meeting to Be Held on 990909 in Atlanta,Ga,To Allow Licensee to Present self-assessment of Catawba Nuclear Station Performance 05000413/LER-1999-013, Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER1999-08-25025 August 1999 Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER ML20211G5181999-08-24024 August 1999 Forwards SE Re second-10-yr Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211A9641999-08-20020 August 1999 Forwards SE Authorizing Licensee 990118 Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section XI for Plant,Units 2 ML20211B9471999-08-18018 August 1999 Forwards Request for Relief 99-02,associated with Limited Exam Results for Welds Which Were Inspected During Unit 1 End of Cycle 11 RFO ML20211C1191999-08-18018 August 1999 Forwards ISI Rept Unit 1 Catawba 1999 RFO 11, Providing Results of ISI Effort Associated with End of Cycle 11 ML20211C3651999-08-17017 August 1999 Forwards Rev 25 to Catawba Nuclear Station Units 1 & 2 Pump & Valve Inservice Testing Program, Which Includes Reformatting of Manual & Addl Changes as Noted in Attached Summary of Changes ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire 05000413/LER-1999-011, Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment1999-08-16016 August 1999 Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H5811999-10-15015 October 1999 Forwards 1999 Update to FSAR, for McGuire Nuclear Station.With Instructions,List of Effective Pages for Tables & List of Effective Pages for Figures ML20217G7861999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20217F3591999-10-13013 October 1999 Forwards Info Copy of Cycle 14 COLR for McGuire Nuclear Station,Unit 1 ML20217F3261999-10-13013 October 1999 Submits Quantity of Tubes Insp from Either Side of SGs A-D & Lists Tubes with Imperfections,Locations & Size.No Tubes Removed from Svc by Plugging.Total of Eleven Tubing Wear Indications Identified at Secondary Side Supports in SGs ML20217H0041999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217F1301999-10-0707 October 1999 Forwards Rev 1 to Request for Relief 99-03 from Requirements of ASME B&PV Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting (Vg) Sys ML20217J5091999-10-0606 October 1999 Forwards Revs to Section 16.15-4.8.1.1.2.g of McGuire Selected Licensee Commitments Manual.Section Has Been Revised to Allow Testing of Portions of DG Fuel Oil Sys Every 10 Yrs ML20217C8351999-10-0505 October 1999 Communicates Correction to Info Provided During 990917 Meeting with Duke Energy & NRC Region Ii.Occupational Radiation Safety Performance Indicator Values Should Have Been Presented as 1 Instead of 0 05000414/LER-1999-004, Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments1999-09-27027 September 1999 Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments 05000413/LER-1999-015, Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept1999-09-27027 September 1999 Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept 05000414/LER-1999-005, Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments1999-09-20020 September 1999 Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20216E8791999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for July 1999 for McGuire Nuclear Station ML20212B4641999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for Catawba Nuclear Station,Units 1 & 2 ML20212A2631999-09-0909 September 1999 Forwards Rev 25 to McGuire Nuclear Station,Units 1 & 2 Pump & Valve Inservice Testing Program, IAW 10CFR50.55a. Section 8.0 Contains Summary of Changes & Detailed Description of Changes Associated with Rev 25 ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 05000413/LER-1999-014, Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment1999-09-0101 September 1999 Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment 05000414/LER-1999-003, Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev1999-08-31031 August 1999 Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev 0 of LER ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting 05000413/LER-1999-013, Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER1999-08-25025 August 1999 Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER ML20211B9471999-08-18018 August 1999 Forwards Request for Relief 99-02,associated with Limited Exam Results for Welds Which Were Inspected During Unit 1 End of Cycle 11 RFO ML20211C1191999-08-18018 August 1999 Forwards ISI Rept Unit 1 Catawba 1999 RFO 11, Providing Results of ISI Effort Associated with End of Cycle 11 ML20211C3651999-08-17017 August 1999 Forwards Rev 25 to Catawba Nuclear Station Units 1 & 2 Pump & Valve Inservice Testing Program, Which Includes Reformatting of Manual & Addl Changes as Noted in Attached Summary of Changes ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire 05000413/LER-1999-011, Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment1999-08-16016 August 1999 Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment ML20210S2751999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210S2231999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210R0031999-08-10010 August 1999 Forwards Revised TS Bases Pages to NRC for Info & Use. Editorial Changes Were Made to Correct Incorrect UFSAR Ref Number Associated with Certain Reactor Coolant Sys Pressure Isolation Valves ML20210R4311999-08-10010 August 1999 Forwards Summary Rept of Mods,Minor Mods,Procedure Changes & Other Misc Changes Per 10CFR0.59 ML20210T4511999-08-10010 August 1999 Forwards Response to NRC RAI Re 981014 Standby Nuclear Svc Water Pond Dam Audit Conducted by FERC ML20210N9521999-08-0404 August 1999 Forwards Changes to Catawba Nuclear Station Selected Licensee Commitments Manual.Documents Constitutes Chapter 16 of Ufsar.With List of Effective Pages ML20210M6411999-07-29029 July 1999 Forwards Request for Relief 99-03 from Requirements of ASME Boiler & Pressure Vessel Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting Air (Vg) Sys 05000413/LER-1999-010, Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units1999-07-22022 July 1999 Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units 05000413/LER-1999-009, Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept1999-07-19019 July 1999 Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept 05000414/LER-1999-001, Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed1999-07-15015 July 1999 Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed ML20209H4431999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for May 1999 on Unit Shutdowns Also Encl ML20210A5771999-07-14014 July 1999 Forwards Revsied Catawba Nuclear Station Selected Licensee Commitments Manual, Per 10CFR50.71(e),changing Sections 16.7-5,16.8-5,16.9-1,16.9-3,16.9-5 & 16.11-7.Manual Constitute Chapter 16 of UFSAR ML20216D3941999-07-14014 July 1999 Forwards Revs to Catawba Nuclear Station Selected Licensee Commitments Manual ML20209H1551999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for May 1999 Also Encl ML20209G5151999-07-0808 July 1999 Forwards Amended Pages to Annual Radioactive Effluent Release Repts, for 1997 & 1998 for McGuire Nuclear Station. Portion of Rept Was Inadvertently Omitted Due to Administrative Error,Which Has Been Corrected 05000413/LER-1999-008, Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach1999-07-0808 July 1999 Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach ML20196G3721999-06-24024 June 1999 Documents Verbal Info Provided to NRR During Conference Call Re Relief Requests 98-002 & 98-003 ML20196G7461999-06-22022 June 1999 Requests Exemption from Requirements of 10CFR54.17(c) That Application for Renewed Operating License Not Be Submitted to NRC Earlier than 20 Yrs Before Expiration of Operating License Currently in Effect ML20196E9541999-06-18018 June 1999 Forwards SG Tube Insp Conducted During Unit 1 End of Cycle 11 Refueling Outage.Attachments 1,2,3 & 4 Identify Tubes with Imperfections in SGs A,B,C & D,Respectively ML20195K4571999-06-14014 June 1999 Forwards MORs for May 1999 & Revised MORs for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20195K3601999-06-14014 June 1999 Forwards MORs for May 1999 for McGuire Nuclear Station,Units 1 & 2 & Revised MORs for Apr 1999.Line 6 Max Dependable Capacity (Gross Mwe) on Operating Data Rept Should Be Revised to 1114 from Jan 1998 to Apr 1999 ML20195J1691999-06-10010 June 1999 Forwards Written Documentation of Background & Technical Info Supporting Catawba Unit 1,notice of Enforcement Discretion Request Re TS 3.5.2 (ECCS-Operating),TS 3.7.12 (Auxiliary Bldg Filtered Ventilation Exhaust Sys) ML20217G5771999-06-0909 June 1999 Forwards Post Exam Comments & Supporting Reference Matls for Written Exams Administered at Catawba Nuclear Station on 990603 1999-09-09
[Table view] |
Text
e #
1 DUKIs Powicn Coxi>m l'.O. ISOX W11150 CitAHLOTTit, N.C. 215242 stAL 15. Tt:0KEH TELEPHONE vuareessue=,
(704) 373-4fklt mies.aan reessesmes November 15, 1985 L
Mr. liarold R. Denton, Director Office of Nuc1 car Reactor Regulation U. S. Nuclear Regulatory Commission l Washington, D. C. 20555 Attention: Ms. E. G. Adensam, Chief Licensing Branch No. 4
Subject:
McGuire Nucicar Station Catawba Nuc1 car Station Docket Nos. 50-369, -370 -413. -414 Dear Mr. Dentont in response to your letter dated September 16, 1985 which requested additional information regarding main steam line break in the Doghouse, please find attached our responses. i questions 1 through 3 have been answered on behalf of Duke by Westinghouse.
Question 4, which was asked on the McGuiro dockets has been answered by Duke for both McGuire and Catawba.
If there are any questions regarding these responses, please advise.
Very truly yours,
.1-
conservative and that the results submitted in WCAP-9226, " Reactor Core Response to Excessive Secondary Steam Releases," (as referenced in the FEAR) may not be valid for all conditions. Address, in detail the consequenses of modeling superheat and its effect on core response. , Provide detailed comparative analyses of the results calculated with the two models (saturated versus superheated steam models).
Response to Question 2 The analysis results in WCAP-9226 address two general categories of steamline break analyses.
- The first category addresses steamline breaks which occur while the reactor is' critical and operating at power prior to reactor trip. Tube bundle mcovery is not predicted prior to reactor trip and the point of minimun DNBR during these transients and therefore there is no impact on the analysis resulta.
The second category addresses stearr.line breaks which occur while the reactor is in hot zero power condition with the most reactive rod stuck out of the core.
These transients are also analyzed on a plant specific basis in the McGuire plant FSAR.
The analysis methodology used in these analyses conservatively force a delay in the tube buncr'e mcovery well past the predicted tube bundle mcovery point.
Therefore, a heat transfer rate is maintained in excess of the value which would be calculated with the combination of the predicted tube bundle mcovery and the superheated steam heat transfer. This is conservative since it maximizes the cooldown by the faulted steam generator and consequently maximizes the return to power. Therefore, the results presented in the McGuire FSAR and WCAF-9226 recain valid.
RESPONSES 1D NRC QU5TIONS m STEAM LINE BREAK DOGHOUSE ANALYSES QUETION 3 As a consequence of equipment failures from adverse environmental conditions, the main steam isolation valves in the affected Doghouse were assGned to reopen. This led to blowdown of the two steam generators: e (a)
Provide the details and justification of the reactivity methodology used in the analyses as well as the nodalization and the primary coolant mixing coefficients applied in the reactor vessel.
(b) Provide the details and justification to support the mixing coefficients applied to the reactor coolant as well as the reactivity feedback models. (This information was requested by the NRC in 1983 on the WCAP-9226 submittal but Westinghouse has not responded to the request. )
(c) Describe how the analyses were performed when assuming the stuck rod cluster control assembly to be positioned in loop 1 core sector versus loop 2 core sector.
Response to Question 3 (a) The system nodalization methodology is described in Reference 2. The information on primary coolant mixing coefficients and reactivity methodology is being handled generically as discussed in Reference 3.
(b) This information request is being addressed generically as described in Reference 3. (Copy enclosed)
(c) As described in Reference 2, the average density, water temperature, and boron concentration used in LOFTRAN can be weighted to a particular core sector (loop). This method is used to conservatively, simulate the effect of a stuck rod in the indicated loops on the core average reactivity calculation. For both cases, " Loop 1" was asstaned to be the loop which continued to blow down after the initial steamline isolation signal. " Loop 2" was assumed to be the loop which had a steamline isolation valve reopen as a result of the superheated steam generated after tube bundle tacovery in the Loop 1 steam generator. One set of analyses assumed that the core sector associated with Loop 1 contained the stuck rod and therefore weighted the Loop 1 core sector density temperature, and boron concentration heavily in the aver. e core rea,ctivity calculation. The second set of analyses assumed tha*L the core sector associated with Loop 2 contained the stuck rod and therefore weighted the Loop 2 core sector density, temperature, and boron concentration heavily in the average core reactivity calculation.
m
- o. .
RESPONSES 'IO NRC QUESTIONS CN STEAM LINE BREAK DOGHOUSE REFERDIGS
- 1. Letter from E. P. Rahe, Jr. to C. O. Thomas, ENac-E-3009 1 dated February 27, 195 ,
Subject:
Topical Reports WCAP-8822-P-S1 and WCAP-c860-S1, " Mass and Energy Releases Following A Steam Line Rupture". ;
- 2. Burnett, T. W. T., et al, "LOFTRAN Code Description," WCAP-7907-P-A (Proprietary), WCAP-7907-A (Non-Proprietary), April 1984.
3 Letter October dated from E. P. Rahe, Jr. (M) to H. L. Thompson (NRC), ENRC-85-3077, 29,195 G
0 0
0
- 8
\ l
.- x j
% j Westinghouse Water Reactor Electric Corporation Divisions Qyjgnny,,n,,mm3 3 October 29,1985 NS-idic-i.5-3077 Mr. Hugh L. Thompson, Director Division of Licencing U. S. Nuclear Regulatory Comission Washington, D.C. 20555 H.S. 528 (Old Phillips Bldg.)
Subject:
Schedule for Response to Request for Additional Information on WCAP-9226 (P) and WCAP-9227 (NP)
Refs.: NS-TMA-2080, Anderson (W) to Stolz (NRC), 5-17/79 NS-INA-2285, Anderson (W) to Hiller (NRC), 7-30-80 NS-EPR-3007, Rahe (W) to Thomas (NRC), 2-19-C5
Dear Mr. Thompson:
During the course of the NRC review on the Wertint.cuse c topical reports on the steamline break methodology (WCAP-9226 and WCAF-9227), Westin@ouse has provided responses to the staff's requests for additional information on several occasions (referenced letters). There are, however, a number of questions for which responses have not yet been formally supplied, although they have been discussed with members of your staff. Information was also supplied to Argonne National Laboratories in the stumer of 1983 in lieu of fermal responses to some of the requests for additional information in order to facilitate the staff's review of the topical reports.
We'stin@ouse has been preparing responses to the remainder of the questions during this year. We expect to have completed our work in the first quarter of 1986. Accordingly, Westinghouse will submit responses to the retraining questions by April 1,1986. -
If you have any questions, please contact Mr. J. L. Little of my staff (412/374-5054).
Very truly yours,
\
E.P. Rahe,Jf ~
Manager Nuclear Safety Department HIO:pj L 'l(,f
(. ,a" J -. u i v
QUESTION 4: Provide your evaluations of offsite dose, including in particular the case with two steam generator blowdown.
Response to Quention 4: McGuire Main Steam Line Break Dose Evaluation The following two accident scenarios were considered for the MSLB offsite dose evaluations (1) single steam generator blowdown, (2) two steam generator blowdown. Note that the generation of superheated steam does not affect the dose analysis since the entire mass of the defective steam generator (s) is released.
Accident Assumptions
- 1. The primary and secondary side concentrations are at the following Technical Specification limits when the accident occurs: i Primary - 1 pCi/gm dose equivalent I-131 100/Eypci/gm gross activity (assumed to be all noble gases) l Secondary - 0.1 pCi/gm dose equivalent I-131 ,
t
- 2. The spectrum of iodine isotopes in the primary and secondary coolant is the same as the Design Basis primary coolant spectrum.
- 3. The primary-to-secondary leak rate of 1 gpm is distributed between the !
steam generators for the duration of the accident as One Steam Generator Blowdown 0.347 gpm for defective steam generators 0.653 gpm for nondefective steam generators Two Steam Generators Blowdown 0.694 gpm for defective steam generators 0.306 gpm for nondefective steam generators
- 4. All noble gases which leak to the secondary side are released via tne steam reicase.
- 5. Initial steam release for the defective steam generator (s) terminates in 30 minutes. Steam release for the nondefective steam generators terminates in 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.
- 6. The iodine partition factor in the defective steam generator (s) is 1.
- 7. The iodine partition factor in the nondefective steam generators is 0.01.
- 8. Mass Releases From MSLB Accident 1 Steam Generator Blowdown Case Time Mass Release From Faulted S.G. Mass Release From Intact S.Gs.
(hrs) (1bm) (Ibm) 0-2 108.500 ,
378.248 2-8 ------- 963,012 2 Steam Generators Blowdown Case Time Mass Release From Faulted S.Cs. Mass Release From Intact S.Cs.
(hra) (1bm) (ibm) 0-2 217.000 378.248 2-8 -------
963.012
- 9. Accident Dispersion Factors (X/Q)
Exclusion Area Boundary - 9.00E-04 sec/m3 Low Population Zone - 8.00E-05 sec/m3 Two reactor coolant activity cases were evaluated for the MSLB accident.
Case 1 A preaccident iodine spike exists with iodine concentrations that are assumed to be the maximum permitted by Technical Specifications for full power operation, i.e., 60 pCi/gm dose equivalent I-131.
Case 2 In this case the reactor trip and/or primary system depressurization associated with the MSLB creates an iodine spike in the primary system.
The increase in primary coolant iodine concentration is estimated using a spiking model which assumes that the iodine release rate from the fuel rods to the primary coolant increases to a value 500 times greater than the release rate at the Technical Specification equilibrium value. The iodine spike continues for the duration of the accident.
Results One Steam Generator Blowdown - Offsite Doses (Rem)
Exclusion Area Boundary Low Population Zone Whole Body Thyroid, , Whole Body Thyroid
- Case 1 1.48E-02 5.49E+00 4.00E-03 1.32E+0d case 2 1.85E-02 4.02E+00 1.00E-02 2.46E+00 Two Steam Generator Blowdown - Offsite Doses (Rem)
Exclusion Area Boundary Low Population Zone Whole Body Thyroid Whole Body Thyroid Case 1 2.21E-02 1.09E+01 5.33E-03 2.57E+00 l
l Case 2 2.96E-02 7.94E+00 1.73E-02 4.82E+00 The conservatively calculated doses are well within the exposure guideline values set forth in 10 CFR Patt 100, Section 11.
4 m
r QUESTION 4: Provide your evaluations of offsite dose including in particular the case with two steam generator blowdown.
Response to Question 4: Catawba Main Steam Line Break Dose Evaluation The following two accident scenarios were considered for the MSLB offsite dose evaluations (1) single steam generator blowdown, (2) two steam generator blowdown. Note that the generation of superheated steam does not af fect the dose analysis since the entire mass o.f the defective steam generator (s) is released.
Accident Assumptions
- 1. The primary and secondary side concentrations are at the following Technical Specification limits when the accident occurs:
Primary - 1 pCi/gm dose equivalent I-131 100/EypC1/gm gross activity (assumed to be all noble gases)
Secondary - 0.1 uCi/gm dose equivalent I-131
- 2. The spectrum of iodine isotopes in the primary and secondary coolant is the same as the Design Basis primary coolant spectrum.
l
- 3. The primary-to-secondary leak rate of 1 gpm is distributed between the '
steam generators for the duration of the accident as One Steam Generator Blowdown 0.347 gpm for defective steam generators 0.653 gpm for nondefective steam generators Two Steam Centrators Blowdown 0.694 gpm for defective steam generators 0.306 gpm for nondefective steam generators
- 4. All noble gases which leak to the secondary side are released via the steam release.
- 5. Initial steam release for the defective steam generator (s) terninates in 30 minutes. Steam release for the nondefective steam generators terminates in 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.
- 6. The iodine partition factor in the defective steam generator (s) is 1.
- 7. The iodine partition factor in the nondefective steam generators is 0.01.
- 8. Mass Releases From MSLB Accident 1 Steam Generator Blowdown Case Time Mass Release From Faulted S.C. Mass Release From Intact S.cs.
(hre) (1bm) (1bm) 0-2 175,700 ., 403,650 2-B -------
968,638 2 Steam Generators Blowdown Case Time Mass Release From Faulted S.Cs. Mass Release From Intact S.Gs.
(hrs) (ibm) (1bm) 0-2 351,400 429.120 2-8 -------
924,777
- 9. Accident Dispersion Factors (X/Q)
Exclusion Area Boundary - 5.50E-04 sec/m3 Low Fopulation Zone - 1.80E-05 sec/m3 Two reactor coolant activity cases were evaluated for the MSLB accident.
Case 1 A preaccident iodine spike exists with iodine concentrations that are assumed to be the maximum permitted by Technical Specifications for full power operation, i.e., 60 pC1/gm dose equivalent I-131.
Case 2 In this case, the reactor trip and/or primary system depressurization associated with the MSLB creates an iodine spike in the primary system.
The increase in primary coolant iodine concentration is estimated using a spiking model which assumes that the iodine release rate from the fuel rods to the primary coolant increases to a value 500 times greater than the release rate at the Technical Specification equilibrium value. The lodine spike continues for the duration of the accident.
l l
l i
l t
l
Results .
One Steam Generator Blowdown - Offsite Doses (Rem)
Exclusion Area Boundary Low Population Zone Whole Body Thyroid . Whole Body Thyroid Case 1 1.03E-02 4.22E+00 9.38E-04 3.23E-01 Case 2 1.26E-02 3.32E+00 2.29E-03 5.77E-01 Two Steam Generator Blowdown - Offsite Doses (Rem)
Exclusion Area Boundary Low Population Zone Whole Body Thyroid Whole Body Thyroid Case 1 1.61E-02 8.37EH)0 1.28E-03 6.34E-01 Case 2 2.07E-02 6.59E+00 3.97E-03 1.14E+00 The conservatively calculated doses are well within the exposure guideline values set forth in 10 CFR Part 100 Section 11.
l a'
_ _ _ _ _ _ _ _ _ _ _ _ . - . _ _ _ _ . . _ . . _