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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217F8231999-10-13013 October 1999 Informs That on 990930,NRC Completed mid-cycle PPR of Catawba Nuclear Station.Based on Review,Nrc Did Not Identify Any New Areas That Warranted More than Core Insp Program Over Next Five Months.Historical Listing of Issues,Encl ML20217H0041999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217F1301999-10-0707 October 1999 Forwards Rev 1 to Request for Relief 99-03 from Requirements of ASME B&PV Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting (Vg) Sys ML20212J3011999-10-0101 October 1999 Forwards Exemption from Certain Requirements of 10CFR54.17(c) Re Schedule for Submitting Application for Operating License Renewal.Se Also Encl ML20217K2651999-10-0101 October 1999 Forwards Retake Exams Repts 50-413/99-302 & 50-414/99-302 on 990921-23.Two of Three ROs & One SRO Who Received Administrative Section of Exam Passed Retake Exam, Representing 75 Percent Pass Rate 05000414/LER-1999-004, Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments1999-09-27027 September 1999 Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments 05000413/LER-1999-015, Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept1999-09-27027 September 1999 Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept ML20217A7911999-09-24024 September 1999 Forwards Insp Repts 50-413/99-05 & 50-414/99-05 on 990718- 0828 at Catawba Facility.Nine NCVs Identified Involving Inadequate Corrective Actions Associated with Degraded Svc Water Supply Piping to Auxiliary Feedwater Sys ML20212E6471999-09-24024 September 1999 Discusses GL 98-01 Issued by NRC on 980511 & DPC Responses for Catawba NPP & 990615.Informs That NRC Reviewed Response for Catawba & Concluded That All Requested Info Provided.Considers GL 98-01 to Be Closed for Catawba ML20212F0941999-09-21021 September 1999 Discusses Closeout of GL 97-06, Degradation of Steam Generator Internals for Cns,Units 1 & 2 ML20212M2001999-09-20020 September 1999 Confirms 990913 Telcon Between M Purser & R Carroll Re Management Meeting to Be Conducted on 991026 in Atlanta,Ga to Discuss Operator Licensing Issues 05000414/LER-1999-005, Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments1999-09-20020 September 1999 Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20212B4641999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for Catawba Nuclear Station,Units 1 & 2 ML20212A4131999-09-14014 September 1999 Informs That TR DPC-NE-2009P Submitted in 990817 Affidavit, Marked Proprietary,Will Be Withheld from Public Disclosure, Pursuant to 10CFR2.709(b) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20212M1931999-09-13013 September 1999 Refers to 990909 Meeting Conducted at Region II Office Re Presentation of Licensee self-assessment of Catawba Nuclear Station Performance.List of Attendees & Licensee Presentation Handout Encl ML20212A3751999-09-10010 September 1999 Informs That Postponing Implementation of New Conditions Improved by RG 1.147,rev 12,acceptable Since Evaluation on Relief Based on Implementation Code Case for Duration of Insp Interval ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 05000413/LER-1999-014, Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment1999-09-0101 September 1999 Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment 05000414/LER-1999-003, Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev1999-08-31031 August 1999 Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev 0 of LER ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting 05000413/LER-1999-013, Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER1999-08-25025 August 1999 Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER ML20211M8191999-08-25025 August 1999 Confirms 990825 Telcon Between G Gilbert & R Carroll Re Mgt Meeting to Be Held on 990909 in Atlanta,Ga,To Allow Licensee to Present self-assessment of Catawba Nuclear Station Performance ML20211A9641999-08-20020 August 1999 Forwards SE Authorizing Licensee 990118 Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section XI for Plant,Units 2 ML20211C1191999-08-18018 August 1999 Forwards ISI Rept Unit 1 Catawba 1999 RFO 11, Providing Results of ISI Effort Associated with End of Cycle 11 ML20211B9471999-08-18018 August 1999 Forwards Request for Relief 99-02,associated with Limited Exam Results for Welds Which Were Inspected During Unit 1 End of Cycle 11 RFO ML20211C3651999-08-17017 August 1999 Forwards Rev 25 to Catawba Nuclear Station Units 1 & 2 Pump & Valve Inservice Testing Program, Which Includes Reformatting of Manual & Addl Changes as Noted in Attached Summary of Changes ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 05000413/LER-1999-011, Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment1999-08-16016 August 1999 Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire ML20210V0321999-08-13013 August 1999 Forwards Insp Repts 50-413/99-04 & 50-414/99-04 on 990606- 0717.Six Violations of NRC Requirements Identified & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy ML20210S2751999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210Q3751999-08-0505 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Authorized Representative of Facility Must Submit Ltr as Listed,Thirty Days Before Exam Date,In Order to Register Individuals for Exam ML20210N9521999-08-0404 August 1999 Forwards Changes to Catawba Nuclear Station Selected Licensee Commitments Manual.Documents Constitutes Chapter 16 of Ufsar.With List of Effective Pages IR 05000413/19980131999-08-0202 August 1999 Discusses Integrated Insp Repts 50-413/98-13,50-414/98-13, 50-413/98-16,50-414/98-16 & NRC Special Repts 50/413/99-11 & 50-414/99-11 Conducted Between Aug 1998 & May 1999.Six Violations Occurred,Based on OI Investigation & Insp ML20210M6411999-07-29029 July 1999 Forwards Request for Relief 99-03 from Requirements of ASME Boiler & Pressure Vessel Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting Air (Vg) Sys 05000413/LER-1999-010, Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units1999-07-22022 July 1999 Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units IR 05000413/19990101999-07-22022 July 1999 Discusses Insp Rept 50-413/99-10 & 50-414/99-10 on 990314- 0424 & Forwards Notice of Violation Re Failure to Comply with TS 3.7.13,when Misalignment of Two Electrical Breakers Rendered SSS Inoperable from 981216-29 ML20217G5241999-07-20020 July 1999 Forwards Exam Repts 50-413/99-301 & 50-414/99-301 on 990524- 27,0603,07-10 & 16.Of Fourteen SRO & RO Applicants Who Received Written Exams & Operating Tests,Eight Applicants Passed & Six Failed Exam 05000413/LER-1999-009, Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept1999-07-19019 July 1999 Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept 05000414/LER-1999-001, Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed1999-07-15015 July 1999 Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed ML20209H4431999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for May 1999 on Unit Shutdowns Also Encl ML20210A5771999-07-14014 July 1999 Forwards Revsied Catawba Nuclear Station Selected Licensee Commitments Manual, Per 10CFR50.71(e),changing Sections 16.7-5,16.8-5,16.9-1,16.9-3,16.9-5 & 16.11-7.Manual Constitute Chapter 16 of UFSAR ML20216D3941999-07-14014 July 1999 Forwards Revs to Catawba Nuclear Station Selected Licensee Commitments Manual NUREG-1431, Forwards SER Agreeing with Util General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation1999-07-0909 July 1999 Forwards SER Agreeing with Util General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196L0371999-07-0808 July 1999 Approves Requested Schedule Change of Current two-year Requalification Examinations to non-outage dates.Two-year Cycle Will Start on 991001 & Will End on 020930 05000413/LER-1999-008, Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach1999-07-0808 July 1999 Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach ML20196J9001999-07-0606 July 1999 Informs That 990520 Submittal of Rept DPC-NE-3004-PA,Rev 1, Mass & Energy Release & Containment Response Methodology, Marked Proprietary Will Be Withheld Per 10CFR2.790(b)(5) & Section 103(b) of AEA of 1954 IR 05000413/19990031999-07-0101 July 1999 Discusses Insp Repts 50-413/99-03 & 50-414/99-03 Completed on 990605 & Transmitted by Ltr .Results of Delibrations for Violation Re Discovery of Potentially More Limiting Single Failure Affecting SGTS Analysis Provided 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H0041999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217F1301999-10-0707 October 1999 Forwards Rev 1 to Request for Relief 99-03 from Requirements of ASME B&PV Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting (Vg) Sys 05000414/LER-1999-004, Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments1999-09-27027 September 1999 Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments 05000413/LER-1999-015, Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept1999-09-27027 September 1999 Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept 05000414/LER-1999-005, Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments1999-09-20020 September 1999 Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20212B4641999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for Catawba Nuclear Station,Units 1 & 2 ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 05000413/LER-1999-014, Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment1999-09-0101 September 1999 Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment 05000414/LER-1999-003, Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev1999-08-31031 August 1999 Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev 0 of LER ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting 05000413/LER-1999-013, Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER1999-08-25025 August 1999 Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER ML20211B9471999-08-18018 August 1999 Forwards Request for Relief 99-02,associated with Limited Exam Results for Welds Which Were Inspected During Unit 1 End of Cycle 11 RFO ML20211C1191999-08-18018 August 1999 Forwards ISI Rept Unit 1 Catawba 1999 RFO 11, Providing Results of ISI Effort Associated with End of Cycle 11 ML20211C3651999-08-17017 August 1999 Forwards Rev 25 to Catawba Nuclear Station Units 1 & 2 Pump & Valve Inservice Testing Program, Which Includes Reformatting of Manual & Addl Changes as Noted in Attached Summary of Changes ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 05000413/LER-1999-011, Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment1999-08-16016 August 1999 Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire ML20210S2751999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210N9521999-08-0404 August 1999 Forwards Changes to Catawba Nuclear Station Selected Licensee Commitments Manual.Documents Constitutes Chapter 16 of Ufsar.With List of Effective Pages ML20210M6411999-07-29029 July 1999 Forwards Request for Relief 99-03 from Requirements of ASME Boiler & Pressure Vessel Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting Air (Vg) Sys 05000413/LER-1999-010, Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units1999-07-22022 July 1999 Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units 05000413/LER-1999-009, Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept1999-07-19019 July 1999 Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept 05000414/LER-1999-001, Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed1999-07-15015 July 1999 Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed ML20216D3941999-07-14014 July 1999 Forwards Revs to Catawba Nuclear Station Selected Licensee Commitments Manual ML20209H4431999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for May 1999 on Unit Shutdowns Also Encl ML20210A5771999-07-14014 July 1999 Forwards Revsied Catawba Nuclear Station Selected Licensee Commitments Manual, Per 10CFR50.71(e),changing Sections 16.7-5,16.8-5,16.9-1,16.9-3,16.9-5 & 16.11-7.Manual Constitute Chapter 16 of UFSAR 05000413/LER-1999-008, Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach1999-07-0808 July 1999 Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach ML20196G7461999-06-22022 June 1999 Requests Exemption from Requirements of 10CFR54.17(c) That Application for Renewed Operating License Not Be Submitted to NRC Earlier than 20 Yrs Before Expiration of Operating License Currently in Effect ML20196E9541999-06-18018 June 1999 Forwards SG Tube Insp Conducted During Unit 1 End of Cycle 11 Refueling Outage.Attachments 1,2,3 & 4 Identify Tubes with Imperfections in SGs A,B,C & D,Respectively ML20195K4571999-06-14014 June 1999 Forwards MORs for May 1999 & Revised MORs for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20195J1691999-06-10010 June 1999 Forwards Written Documentation of Background & Technical Info Supporting Catawba Unit 1,notice of Enforcement Discretion Request Re TS 3.5.2 (ECCS-Operating),TS 3.7.12 (Auxiliary Bldg Filtered Ventilation Exhaust Sys) ML20217G5771999-06-0909 June 1999 Forwards Post Exam Comments & Supporting Reference Matls for Written Exams Administered at Catawba Nuclear Station on 990603 05000414/LER-1999-002, Forwards Abstract of LER 99-002-00 Re Forced Shutdown of Plant as Result of Flow Restriction Caused by Corrosion of Afs Assured Suction Source Piping Due to Inadequate Testing. Final LER Will Be Submitted No Later than 9907081999-06-0303 June 1999 Forwards Abstract of LER 99-002-00 Re Forced Shutdown of Plant as Result of Flow Restriction Caused by Corrosion of Afs Assured Suction Source Piping Due to Inadequate Testing. Final LER Will Be Submitted No Later than 990708 ML20207F2381999-06-0101 June 1999 Forwards Copy of Catawba Nuclear Station Units 1 & 2 1998 10CFR50.59 Rept, for NRC Files ML20195J1131999-05-26026 May 1999 Requests Approval to Change Cycle Dates for Two Year Requalification Training Program Required by 10CFR55.59,to Improve Scheduling of Requalification Exams to non-outage Periods 05000413/LER-1999-007, Forwards LER 99-007-00,re Operation Prohibited by TS 3.4.7. Commitments Identified in LER Are Listed in Planned Corrective Actions Section1999-05-26026 May 1999 Forwards LER 99-007-00,re Operation Prohibited by TS 3.4.7. Commitments Identified in LER Are Listed in Planned Corrective Actions Section ML20195B4751999-05-24024 May 1999 Forwards Rev 7 to UFSAR Chapter 2 & Chapter 3 from 1998 UFSAR for Catawba Nuclear Station.List of Instructions on Insertion Encl ML20196L1851999-05-20020 May 1999 Forwards Proprietary & non-proprietary Version of Rev 1 to TR DPC-NE-3004, Mass & Energy Release & Containment Response Methodology, Consisting of Finer Nodalization of Ice Condenser Region.Proprietary Info Withheld ML20196L1791999-05-20020 May 1999 Communicates Util Licensing Position Re Inoperable Snubbers. Licensee Has Determined That Structure of ITS Has Resulted in Certain Confusion Re Treatment of Inoperable Snubbers 05000413/LER-1997-009, Forwards LER 97-009-02, Unanalyzed Postulated Single Failure Affecting SG Tube Rupture Analysis, Suppl Revises Planned C/A Described in Suppl 1 to Ler.Current Status of C/As & Addl C/As Planned,Provided in Rept1999-05-17017 May 1999 Forwards LER 97-009-02, Unanalyzed Postulated Single Failure Affecting SG Tube Rupture Analysis, Suppl Revises Planned C/A Described in Suppl 1 to Ler.Current Status of C/As & Addl C/As Planned,Provided in Rept ML20206T4481999-05-13013 May 1999 Forwards Rev 3 to Topical Rept DPC-NE-3002-A, UFSAR Chapter 15 Sys Transient Analysis Methodology, IAW Guidance Contained in NUREG-0390 ML20206R1721999-05-13013 May 1999 Forwards Monthly Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 & Revised Monthly Operating Repts for Mar 1999 ML20206T0281999-05-12012 May 1999 Forwards Changes to Catawba Nuclear Station Selected Licensee Commitments Manual. Document Constitutes Chapter 16 of UFSAR 05000413/LER-1999-006, Forwards LER 99-006-00,re CR Ventilation Sys Inoperability. Root Cause & Corrective Actions for Occurence Are Being Finalized & Will Be Reported in Supplement Rept on 9906071999-05-10010 May 1999 Forwards LER 99-006-00,re CR Ventilation Sys Inoperability. Root Cause & Corrective Actions for Occurence Are Being Finalized & Will Be Reported in Supplement Rept on 990607 ML20206N8201999-05-10010 May 1999 Forwards Revs 15 & 16 to Catawba Unit 1 Cycle 12 COLR, Per TS 5.6.5.Rev 15 Updates Limits for New Catawba 1 Cycle 12 Reload Core & Rev 16 Revises Values Re Min Boron Concentrations for Rwst,Cla & SFP ML20206J4431999-05-0303 May 1999 Forwards Changes to Catawba Nuclear Station Selected Licensee Commitments Manual, Per 10CFR50.71(e).Document Constitutes Chapter 16 of UFSAR ML20206D2141999-04-29029 April 1999 Forwards 1998 Annual Radioactive Effluent Release Rept for Catawba Nuclear Station,Units 1 & 2, Per Plant TS 5.6.3. Rept Contains Listed Documents ML20206E4101999-04-26026 April 1999 Forwards Four Copies of Rev 9 Todpc Nuclear Security & Contingency Plan,Per 10CFR50.54(p)(2).Changes Do Not Decrease Safeguards Effectiveness of Plan.Encl Withheld,Per 10CFR73.21 1999-09-08
[Table view] |
Text
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e p i Duke Energy Corporation
~ hb' ,,
Catawba Nudear Station 4800 Concord Road York. SC 29745 Cary R. Peterson I# # "
y;g;g, (803) 8313426 FM l
1 June 10, 1999 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555
Subject:
Duke Energy Corporation Catawba Nuclear Station, Unit 1 Docket Number 50-413 Notice of Enforcement Discretion (NOED) Request Technical Specifications (TS) 3.5.2 (ECCS-Operating)
TS 3.7.12 (Auxiliary Building Filtered Ventilation Exhaust System (ABFVES))
Attached is the written documentation of the background and technical information supporting the Catawba Unit 1 Notice of
' Enforcement Discretion (NOED) request. This information was discussed with the NRC staff in a telephone conference call on June 10, 1999.
As discussed in detail in Attachment 1, Catawba is requesting !
discretion from enforcing TS Limiting Condition for Operation l (LCO) 3.5.2. This specification governs the Emergency Core Cooling System (ECCS) for Modes 1, 2, and 3. Also, Catawba is requesting discretion from enforcing TS LCO 3.7.12, insofar as the ability to comply with Surveillance Requirement (SR) 3.7.12.4 is concerned. LCO 3.7.12 governs the ABFVES for Modes 1, 2, 3, and 4. SR 3.7.12.4 requires'that each ABFVES train be able to maintain the ECCS pump rooms at negative pressure relative to adjacent areas. As shown in the attached justification, Duke Energy maintains that granting of discretionary. enforcement in this case is in the best interests of nuclear safety.
f This. request:for enforcement discretion was approved by the f Catawba Plant Operations Review Committee (PORC) on June 10, 1999.
Should you have any questions concerning this information, please call L.J. Rudy at (803) 831-3084.
9906190108 990610 PDR ADOCK 05000413
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U Nuclear Regulatory Commission Pag: 2 June 10, 1999 Very.truly your (f _- 1_ -
R. Peterson Attachment LJR/s xc (with. attachment):
- L.A. Reyes U.S. Nuclear Regulatory Commission Regional Administrator, Region II
. Atlanta Federal Center 61 Forsyth-St., SW, Suite 23T85 Atlanta, GA 30303 D.J.. Roberts Senior Resident Inspector (CNS)
U.S. Nuclear Regulatory Commission Catawba Nuclear Station P.S. Tam NRC Senior Project Manager (CNS)
U.S. Nuclear Regulatory Commission Mail Stop O-8 H12 Washington, D.C. 20555-0001
-V.R. Autry, Director Division of Radioactive Waste Management i Bureau of Land and Waste Management Department of Health and Environmental Control 2600. Bull St.
Columbia, SC 29201
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I Attachment 1 i Catawba Nuclear Station, Unit 1 Request for Enforcement Discretion TS 3.5.2 (ECCS-Operating)
TS 3.7.12 (ABFVES) )
Duke Energy hereby requests that the NRC grant discretion in enforcing TS LCOs 3.5.2 (ECCS-Operating) and 3.7.12 (ABFVES), j relative to compliance with SR 3.7.12.4, and allow the unit to remain in Mode 1 (Power Operation) until work is completed to replace the rotating element for centrifugal charging pump (CCP) 1B. This pump was declared inoperable on June 8, 1999 at 2320 hours0.0269 days <br />0.644 hours <br />0.00384 weeks <br />8.8276e-4 months <br />. Duke Energy is requesting that the completion time of Condition A of LCO 3.5.2 be extended from the current 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> by {
an additional 4 days, for a total of 7 days, so that this work can be completed. The basis for this request is delineated in the discussion below.
- 1. TS violated Catawba is requesting enforcement discretion from TS LCO 3.5.2.
This LCO governs the ECCS for Modes 1, 2, and 3. LCO 3.5.2 requires two ECCS trains to be operable. Condition A for this LCO states that with one or more trains inoperable and at least .
100% of the ECCS flow equivalent to a single operable ECCS train i available, the inoperable train (s) must be restored to operable !'
status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Condition B states that if the required action and associated completion time is not met, the unit must be in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Mode 4 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. 4 l
Catawba is also requesting enforcement discretion from TS LCO !
3.7.12, insofar as the ability to comply with SR 3.7.12.4 is I concerned. This LCO governs the ABFVES for Modes 1, 2, 3, and 4.
LCO 3.7.12 requires two ABFVES trains to be operable. Condition A for this LCO states that with one ABFVES train inoperable, the inoperable train must be restored to operable status within 7 days. There is no condition for two ABFVES trains inoperable; therefore, LCO 3.0.3 would apply in the event that both trains are inoperable.. SR 3.7.12.4 requires that each ABFVES train be capable of maintaining the ECCS pump rooms at a negative pressure relative to adjacent areas.
- 2. Circumstances surrounding the situation The Catawba ECCS is composed, in part, of three separate subsystems: the high head centrifugal charging subsystem, the intermediate head safety injection subsystem, and the low head residual heat removal subsystem. Each subsystem consists of two 1
l redundant, 100% capacity trains that are interconnected such that l either train is capable of supplying 100% of the flow required to mitigate accident consequences. The interconnecting and redundant subsystem design provides the operators with the I ability to utilize components from opposite trains to achieve the required 100% flow to the core.
1 The ABFVES filters air exhausted from all potentially contaminated areas of the auxiliary building, which includes the ECCS area and non safety portions of the auxiliary building. The ABFVES, in conjunction with other normally operating systems, also provides ventilation for these areas of the auxiliary building. The ABFVES consists of two independent and redundant trains. Following receipt of a safety injection signal, the system isolates non safety portions of the ABFVES and exhausts air only from the ECCS pump rooms. Either ABFVES train is designed to be capable of maintaining a negative pressure in any of the ECCS pump rooms, regardless of train designation.
On June 8, 1999, Operations was alerted by annunciation of a high differential pressure (dp) on seal water injection filter 1B.
Upon shifting the filters, Operations noticed that valve 1NV-294 (CCP A and B Discharge Flow Control Valve) was indicating full open with no noticeable increase in charging line flow. The unit operating parameters returned to normal when CCP 1A was placed in service and CCP 1B was secured. A brief synopsis is indicated below:
Date/ Time Event Description 1
6/5/99 CCP 1B placed in service.
6/8/99/ 0900 CCP motor 1B stator temperatures started to increase.
~1700 Seal injection filter 1B dp increased at a more rapid rate. l 1938 1NV-294 opened more than normal.
1941 1NV-294 was full open.
1 2030 Seal water injection filter 1B high dp annunciator alarm came in.
2045-2050 1NV-294 and 1NV-309 (Seal Water Injection Flow Control Valve) were taken to manual in an attempt to increase charging flow. No effect was observed.
2
2217 CCP 1A was placed in service. CCP 1B was secured.-
2227-2251 1NV-309 and 1NV-294 were returned to automatic control.
2320- CCP 1B was declared inoperable.
'A Failure Investigation Process (FIP) Team was subsequently initiated to investigate the event. The team evaluated a number of possible' scenarios for the observed conditions. These included:
- Failure of CCP 1B e CCP 1B drain valve diverting flow
- CCP 1B recirculating back through CCP 1A
- CCP.1B recirculating back to the Volume Control Tank
- Decrease in available suction flow to CCP 1B
- Obstruction in the CCP 1B discharge
- CCP 1E motor running at reduced speed e CCP 1B speed reducer failure
- Gas voids in CCP 1B All-failure modes were subsequently discounted, with the exception of the failure of CCP 1B itself. A work order was written.to replace the pump rotating element. In order to replace the rotating element, the equipment access hatch above the pump will have to be removed to allow the removal of equipment too large to be carried through the pump room door.
Additionally, it may be necessary to allow the pump room door to be secured open for the placement and removal of equipment required to support disassembly and reassembly of the pump.
Either the open hatch or the open door will create a breach in the pump room ventilation boundary of sufficient size such that neither ABFVES train will be capable of maintaining a negative pressure-in the pump room relative to adjacent areas as required by'SR 3.7.12.4.
- 3. The safety basis for the request, including the evaluation of the safety significance and potential consequences of the proposed action.
There is minimal safety consequence associated with this request.
Granting of enforcement discretion will not have any significant adverse safety impact, as CCP 1A is fully operable and remains
' capable of fulfilling its design basis accident mitigation 3
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function. Catawba is maintaining all ECCS Train A components fully operable, and with the exception of CCP 1B, all ECCS Train B components will remain fully operable.
During the maintenance activities, while the CCP 1B room pressure boundary is breached and the ABFVES is incapable of maintaining a negative pressure in that room relative to adjacent areas, the pump will be isolated. Therefore, the potential of significant leakage of containment sump fluids in the room through the pump seal is_ eliminated. Any minor leakage present in the room will be compared to limits established in the dose analysis for containment sump fluid leakage outside of the ECCS pump room areas. If leakage values exceed the limits established by the dose analysis, then corrective action will be initiated to bring the leakage to within allowable values prior to the ventilation boundary being breached.
The. alteration of the CCP 1B room boundary will not adversely affect the performance of the ABFVES filters. System flow rates will remain below the required TS limits and HEPA and carbon bed iodine removal efficiencies will not be affected. Additionally, even with the ventilation boundary of the CCP 1B room breached, the ABFVES will still be capable of maintaining a negative pressure in the other ECCS pump rooms. Therefore, the Catawba dose analysis results will not be adversely affected and dose rates will remain within the values established by regulations.
Duke Energy estimates that the total length of time that the CCP 1B room hatch is removed will be approximately 8 to 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />.
Duke Energy has evaluated this NOED request from a probabilistic risk standpoint concerning the extended inoperability of CCP 1B and has found that the incremental increase in risk would be i acceptable. In order to determine the impact of core damage l risk, a calculatiot has been performed using the zero-maintenance i model developed from Revision 2 of the Catawba Probabilistic Risk Assessment (PRA). The zero-maintenance PRA model is similar to
)
I the Revision 2 Catawba PRA model except that all maintenance !
events have been set to zero and seismic events have been I excluded. This calculation shows that with CCP 1B out of service {
the change in Core Damage Frequency (CDF) is 6.lE-09/ day. The Incremental Conditional- Core Damage Probability (ICCDP) for a 3- I day Allowable Outage Time-(AOT) is 1.8E-08. The ICCDP for a 7- !
day AOT is 4.2E-08. The difference between the two ICCDPs is 2.4E-08. This value represents the increase in risk associated with the extension of the AOT to 7 days. The increase is I considered a very small change as discussed in Section 2.4.2 of :
Regulatory Guide (RG) 1.174, "An Approach for Using Probabilistic l Risk Assessment-in Risk-Informed Decisions on Plant-Specific i Changes to the Current Licensing Basis." The CDF from Revision 2 4
{
of the Catawba PRA is 7.2E-5/yr (6.4E-5/yr excluding the seismic events).
From Revision 2 of the Catawba PRA, the major contributors to Large Early Release Frequency (LERF) are an interfacing systems loss of coolant accident, a steam generator tube rupture (as an initiating event or an induced tube rupture), and large isolation failures due to seismic events or a station blackout. The sequences associated with a train of centrifugal charging in maintenance do not contribute significantly to these plant damage states. The impact on LERF is therefore very small. In addition, if the increase in LERF were the same as the increase in CDF (2.4E-08), the change would still be considered very small as discussed in Section 2.4.2 of RG 1.174. The calculated LERF for Revision 2 of the Catawba PRA is approximately 4E-07/yr. It has been determined that the breaching of the CCP 1B room pressure boundary and the resultant effect on ABFVES performance has no effect on either the CDF or the LERF.
- 4. The basis for the licensee's-conclusion that noncompliance will not be of potential detriment to the public health and safety and that no significant hazard consideration is involved.
NRC granting of this request for enforcement discretion will not have any adverse consequences from the standpoint of public health and safety. Relief from the applicable LCO 3.5.2 and 3.7.12 requirements to support online pump replacement is preferable to the transient that would be incurred if Unit 1 were forced to shut down while the pump work is in progress. Duke Energy has evaluated the consequences of this request from a probabilistic risk standpoint and the results were found to be acceptable. During the period covered by this request, all ECCS Train A components and all ECCS Train B components with the exception of CCP 1B will continue to remain fully operable and capable of fulfilling their required safety functions. Should any unplanned adverse situation occur which renders CCP 1A inoperable, Unit 1 would be shut down in accordance with LCO 3.0.3.
There - 'gnificant hazards considerations associated with this req. . ror enforcement discretion. This is demonstrated as follows:
1 This request for enforcement discretion does not involve a !
significant increase in the probability or consequences of an accident previously evaluated. Granting of this request will I have no effect on accident probabilities, since the CCPs are not considered accident initiating equipment and no physical changes are being made to the plant which would impact accident 5
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probabilities. Granting of this' request would not result in any adverse' impact from the standpoint of availability or reliability l of CCP 1A. Also, this request was evaluated and found to be
- acceptable from a risk standpoint. Therefore, there will be no significant increase in any accident consequences.
This request for enforcement discretion does not create the possibility of a new or different kind of accident from any accident previously evaluated. No new accident causal mechanisms l
are created as a result of the NRC granting of this request for enforcement discretion. No changes are being made to the plant which will introduce any new accident causal mechanisms.
This request for enforcement discretion does not involve a
. significant. reduction in a margin of safety. Margin of safety is I related to the confidence in the ability of the fission product barriers to perform their design functions during and following an accident situation. These barriera include the fuel cladding, the reactor coolant system, and the containment system. The performance of these fission product barriers will not be degraded by the NRC's granting of this request. No safety margins will be impacted. The risk implications of this request were evaluated and found to be acceptable.
- 5. The basis for the licensee's conclusion that the noncompliance will not involve adverse consequences to the environment.
This request for enforcement discretion will not result in any significant changes in the types, or significant increase in the amounts, of any effluents that may be released offsite. In addition, no significant increase in individual or cumulative occupational radiation exposures will be involved as a result of the request. Therefore, it can be concluded that the NRC's granting of this request for enforcement discretion will not involve any adverse consequences to the environment.
- 6. Proposed compensatory measures In conjunction with this request, Catawba has taken or will take the following compensatory measures:
- The continued operability of CCP 1A will be ensured for the period during which the request is applicable. Precautionary signs have been placed in the vicinity of CCP 1A, diesel generator 1A, and essential switchgear 1 ETA. The CCP 1A breaker has been roped off as,a protected area. Vibration levels associated with CCP 1A will be closely monitored while the NOED is-in effect. Monitoring of parameters associated 6
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with CCP 1A will be increased to'twice per shift while the NOED is in effect.
- Operations has initiated action to review Standby Shutdown System (SSS) activation plans. The SSS is designed to
-mitigate the consequences of certain postulated fire, security, and station blackout incidents by providing capability to maintain hot standby conditions and by controlling and monitoring vital systems from locations external to the main control room. The standby makeup pump is part of the SSS design. The standby makeup pump provides for the capability to maintain reactor coolant pump seal integrity under conditions requiring SSS operation to preclude the possibility of a reactor coolant pump seal loss of coolant
. accident.
- No planned work on Train A or B ECCS components or their supporting systems will be undertaken while the NOED is in effect.
- During the period that the CCP 1B room pressure boundary is breached, appropriate compensatory measures will be established to quantify minor leakage in the room and to ensure that it remains within allowable limits.
- For periods where the CCP 1B room door is secured open, a dedicated individual will be stationed at the door with instructions to-reclose the door upon notification that a safety injection signal has occurred.
- 7. Justification for the duration of the non-compliance The duration of the non-compliance is limited to the time required to replace the CCP 1B rotating element assembly plus margin to accommodate unforeseen circumstances. Catawba is l therefore requesting that the current '/2 hour completion time associated with LCO 3.5.2, Condition A, be extended to 7 days.
Catawba is also requesting that the NRC exercise discretion in enforcing the requirements of SR 3.7.12.4 with respect to the CCP 1B-room during the 7-day AOT requested for LCO 3.5.2. This will provide for adequate time to complete the pump repairs. As stated in items 3 and 4, there is no safety significance or potential detriment to the health and safety of the public.
- 8. Statement that the request has been approved by the facility organization that normally reviews safety issues.
This request was reviewed and approved by the Catawba Plant Operations Review Committee in a special meeting on June 10, 1999.
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- 9. How one of the NOED criteria for appropriate plant conditions specified in Section B is satisfied.
This request is intended to avoid an undesirable unit shutdown transient as a result of' requiring compliance with the TS and, thus, minimize potential safety consequences and operational risks.
- 10. If a follow-up license amendment is required, the NOED request must include marked-up TS pages showing the proposed TS changes.
No follow-up_ license amendment is required in conjunction with this NOF.D request.
- 11. Other related information for NRC consideration pertaining to this NOED request.
Catawba Selected Licensee Commitments (SLCs) 16,9-8 and 16.9-10 also delineate requirements for the CCPs. The SLC Manual is Chapter 16 of the Updated Final Safety Analysis Reports SLC 16.9-8 is titled "Boration Systems Flow Paths-Operating." SLC 16.9-10 is titled "Boration Systems Charging Pumps-Operating.-
These SLCs were formerly part of the TS and were rel.ocated to the SLC Manual with the conversion to the Improved TS in January 1999. SLC 16.9-8 requires at least two boron injection flow paths utilizing charging pumps to be operable. SLC 16.9-10 also requires at least two charging pumps to be operable. Each of ,
these SLCs has a 72-hour AOT for one inoperable flow path or I charging pump. The remedial actions for these SLCs state that with only one flow path / charging pump operable, at least two flow paths / charging pumps must be restored to operable status within ,
72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, or the unit must be in at least hot standby and borated to a shutdown margin equivalent to at least 1% delta k/k at 200F i within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.
Catawba wishes to inform the NRC that with the granting of this NOED request, these commitments will not be inet on a one-time basis for the duration of this request.
Finally, Catawba wishes to inform the NRC that following the !
completion of the pump rotating assembly replacement, a single !
point pump verification will be performed. A complete flow test of the system will be conducted during the first outage opportunity which facilitates full flow testing. j i
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