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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H5811999-10-15015 October 1999 Forwards 1999 Update to FSAR, for McGuire Nuclear Station.With Instructions,List of Effective Pages for Tables & List of Effective Pages for Figures ML20217G7861999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20217F3591999-10-13013 October 1999 Forwards Info Copy of Cycle 14 COLR for McGuire Nuclear Station,Unit 1 ML20217F3261999-10-13013 October 1999 Submits Quantity of Tubes Insp from Either Side of SGs A-D & Lists Tubes with Imperfections,Locations & Size.No Tubes Removed from Svc by Plugging.Total of Eleven Tubing Wear Indications Identified at Secondary Side Supports in SGs ML20217F8011999-10-13013 October 1999 Informs That on 990930,NRC Completed mid-cycle PPR of McGuire Nuclear Station.Areas That Warranted More than Core Insp Program Over Next Five Months,Not Identified.Historical Listing of Plant Issues Encl ML20217J5091999-10-0606 October 1999 Forwards Revs to Section 16.15-4.8.1.1.2.g of McGuire Selected Licensee Commitments Manual.Section Has Been Revised to Allow Testing of Portions of DG Fuel Oil Sys Every 10 Yrs ML20217C8351999-10-0505 October 1999 Communicates Correction to Info Provided During 990917 Meeting with Duke Energy & NRC Region Ii.Occupational Radiation Safety Performance Indicator Values Should Have Been Presented as 1 Instead of 0 ML20217C4471999-10-0404 October 1999 Forwards Insp Repts 50-369/99-06 & 50-370/99-06 on 990801- 0911.Determined That One Violation Occurred & Being Treated as Non-Cited Violation ML20212J2191999-10-0404 October 1999 Informs That Util 980326 Response to GL 97-06, Degradation of SG Internals Provides Reasonable Assurance That Condition of Steam Generator Internals Are in Compliance with Current Licensing Bases for Facility ML20212J7801999-10-0404 October 1999 Discusses GL 98-01 Issued by NRC on 980511 & DPC Responses for McGuire NPP & 990615.Informs That NRC Reviewed Responses & Concluded That All Requested Info Re Y2K Readiness Provided.Subj GL Considers to Be Closed ML20212M1651999-09-23023 September 1999 Refers to 990917 Meeting at Region II Office Re Licensee Presentation of self-assessment of McGuire Nuclear Station Performance.List of Attendees & Licensee Presentation Handouts,Encl ML20212D1671999-09-20020 September 1999 Forwards Exemption & SER from Certain Requirements of 10CFR50,App A,General Design Criterion 57 Re Isolation of Main Steam Branch Lines Penetrating Containment.Exemption Related to Licensee Application ML20212B6491999-09-15015 September 1999 Informs That Encl Announcement Re 990913 Application for Amend to Licenses NPF-9 & NPF-7 Forwarded to C Observer in North Carolina,For Publication ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20212A4131999-09-14014 September 1999 Informs That TR DPC-NE-2009P Submitted in 990817 Affidavit, Marked Proprietary,Will Be Withheld from Public Disclosure, Pursuant to 10CFR2.709(b) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20216E8791999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for July 1999 for McGuire Nuclear Station ML20212A0501999-09-10010 September 1999 Informs That Postponing Implementation of New Conditions Improved by RG 1.147,rev 12,acceptable Since Evaluation on Relief Based on Implementing Code Case for Duration of Insp Interval ML20212A2631999-09-0909 September 1999 Forwards Rev 25 to McGuire Nuclear Station,Units 1 & 2 Pump & Valve Inservice Testing Program, IAW 10CFR50.55a. Section 8.0 Contains Summary of Changes & Detailed Description of Changes Associated with Rev 25 ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 ML20211J3671999-08-31031 August 1999 Forwards Public Notice of Application for Amend to License NPF-9 Seeking one-time Extension of Surveillance Frequency for TS SR 3.1.4.2 Beyond 25% Extension Allowed by TS SR 3.0.2 ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211K8831999-08-26026 August 1999 Forwards Insp Repts 50-369/99-05 & 50-370/99-05 on 990620-0731.Two Violations Occurred & Being Treated as NCVs ML20211G5181999-08-24024 August 1999 Forwards SE Re second-10-yr Interval Inservice Insp Program Plan Request for Relief 98-004 for Plant,Unit 1 ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire ML20210V0171999-08-13013 August 1999 Confirms Conversation Between M Cash & M Franovich on 990806 Re Mgt Meeting,Scheduled for 990917 to Present self- Assessment of Plant Performance.Meeting Will Be Held in Atlanta,Ga ML20210S2231999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210T4511999-08-10010 August 1999 Forwards Response to NRC RAI Re 981014 Standby Nuclear Svc Water Pond Dam Audit Conducted by FERC ML20210R4311999-08-10010 August 1999 Forwards Summary Rept of Mods,Minor Mods,Procedure Changes & Other Misc Changes Per 10CFR0.59 ML20210R0031999-08-10010 August 1999 Forwards Revised TS Bases Pages to NRC for Info & Use. Editorial Changes Were Made to Correct Incorrect UFSAR Ref Number Associated with Certain Reactor Coolant Sys Pressure Isolation Valves ML20210Q3701999-08-0505 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Authorized Representative of Facility Must Submit Ltr as Listed,Thirty Days Before Exam Date in Order to Register Individuals to Take Exam ML20210H7691999-07-21021 July 1999 Submits Summary of 990715 Meeting at Facility Re Presentation of Results of Most Recent Periodic Ppr.List of Meeting Attendees Encl ML20209H1551999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for May 1999 Also Encl ML20210E1931999-07-13013 July 1999 Forwards Insp Repts 50-369/99-04 & 50-370/99-04 on 990509-0619.Four Violations of NRC Requirements Occurred & Being Treated as Ncv,Consistent with App C of Enforcement Policy NUREG-1431, Forwards SER Agreeing with Util General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation1999-07-0909 July 1999 Forwards SER Agreeing with Util General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20209G5151999-07-0808 July 1999 Forwards Amended Pages to Annual Radioactive Effluent Release Repts, for 1997 & 1998 for McGuire Nuclear Station. Portion of Rept Was Inadvertently Omitted Due to Administrative Error,Which Has Been Corrected ML20196J9001999-07-0606 July 1999 Informs That 990520 Submittal of Rept DPC-NE-3004-PA,Rev 1, Mass & Energy Release & Containment Response Methodology, Marked Proprietary Will Be Withheld Per 10CFR2.790(b)(5) & Section 103(b) of AEA of 1954 ML20196J4381999-06-29029 June 1999 Informs That as Result of Staff Review of Util Responses to GL 92-01,rev 1,suppl 1,NRC Revised Info in Rvid & Releasing Rvid Version 2 ML20196G3721999-06-24024 June 1999 Documents Verbal Info Provided to NRR During Conference Call Re Relief Requests 98-002 & 98-003 ML20196G7461999-06-22022 June 1999 Requests Exemption from Requirements of 10CFR54.17(c) That Application for Renewed Operating License Not Be Submitted to NRC Earlier than 20 Yrs Before Expiration of Operating License Currently in Effect ML20195K3601999-06-14014 June 1999 Forwards MORs for May 1999 for McGuire Nuclear Station,Units 1 & 2 & Revised MORs for Apr 1999.Line 6 Max Dependable Capacity (Gross Mwe) on Operating Data Rept Should Be Revised to 1114 from Jan 1998 to Apr 1999 ML20195D5691999-06-0303 June 1999 Submits Ltr to Facilitate Closing of Inspector Follow Up Item 50-369,370/97-15-05,re Revising Site Drawings in UFSAR Into Summary one-line Flow Diagrams,Per NRC 990327 Telcon ML20195F1851999-06-0202 June 1999 Forwards Insp Repts 50-369/99-03 & 50-370/99-03 on 990328- 0508.Two Violations of NRC Requirements Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20195E8771999-06-0202 June 1999 Confirms Telcon with M Cash on 990524 Re Public Meeting for 990715.Purpose of Meeting to Discuss Results of NRC Most Recent PPR ML20207D0521999-05-21021 May 1999 Informs That in Telcon on 990519 Between a Orton & Rf Aiello Arrangements Made for Administration of Initial Written Exam for McGuire Nuclear Station on 990603.Exam Will Be Administered at Catawba Simultaneously with Written Exam ML20196L1791999-05-20020 May 1999 Communicates Util Licensing Position Re Inoperable Snubbers. Licensee Has Determined That Structure of ITS Has Resulted in Certain Confusion Re Treatment of Inoperable Snubbers ML20196L1851999-05-20020 May 1999 Forwards Proprietary & non-proprietary Version of Rev 1 to TR DPC-NE-3004, Mass & Energy Release & Containment Response Methodology, Consisting of Finer Nodalization of Ice Condenser Region.Proprietary Info Withheld ML20206T4481999-05-13013 May 1999 Forwards Rev 3 to Topical Rept DPC-NE-3002-A, UFSAR Chapter 15 Sys Transient Analysis Methodology, IAW Guidance Contained in NUREG-0390 ML20206R0791999-05-13013 May 1999 Forwards Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 & Revised Monthly Operating Repts for Mar 1999 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H5811999-10-15015 October 1999 Forwards 1999 Update to FSAR, for McGuire Nuclear Station.With Instructions,List of Effective Pages for Tables & List of Effective Pages for Figures ML20217F3261999-10-13013 October 1999 Submits Quantity of Tubes Insp from Either Side of SGs A-D & Lists Tubes with Imperfections,Locations & Size.No Tubes Removed from Svc by Plugging.Total of Eleven Tubing Wear Indications Identified at Secondary Side Supports in SGs ML20217F3591999-10-13013 October 1999 Forwards Info Copy of Cycle 14 COLR for McGuire Nuclear Station,Unit 1 ML20217G7861999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for McGuire Nuclear Station,Unit 1 & 2 ML20217J5091999-10-0606 October 1999 Forwards Revs to Section 16.15-4.8.1.1.2.g of McGuire Selected Licensee Commitments Manual.Section Has Been Revised to Allow Testing of Portions of DG Fuel Oil Sys Every 10 Yrs ML20217C8351999-10-0505 October 1999 Communicates Correction to Info Provided During 990917 Meeting with Duke Energy & NRC Region Ii.Occupational Radiation Safety Performance Indicator Values Should Have Been Presented as 1 Instead of 0 ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20216E8791999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for July 1999 for McGuire Nuclear Station ML20212A2631999-09-0909 September 1999 Forwards Rev 25 to McGuire Nuclear Station,Units 1 & 2 Pump & Valve Inservice Testing Program, IAW 10CFR50.55a. Section 8.0 Contains Summary of Changes & Detailed Description of Changes Associated with Rev 25 ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire ML20210S2231999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210T4511999-08-10010 August 1999 Forwards Response to NRC RAI Re 981014 Standby Nuclear Svc Water Pond Dam Audit Conducted by FERC ML20210R0031999-08-10010 August 1999 Forwards Revised TS Bases Pages to NRC for Info & Use. Editorial Changes Were Made to Correct Incorrect UFSAR Ref Number Associated with Certain Reactor Coolant Sys Pressure Isolation Valves ML20210R4311999-08-10010 August 1999 Forwards Summary Rept of Mods,Minor Mods,Procedure Changes & Other Misc Changes Per 10CFR0.59 ML20209H1551999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for May 1999 Also Encl ML20209G5151999-07-0808 July 1999 Forwards Amended Pages to Annual Radioactive Effluent Release Repts, for 1997 & 1998 for McGuire Nuclear Station. Portion of Rept Was Inadvertently Omitted Due to Administrative Error,Which Has Been Corrected ML20196G3721999-06-24024 June 1999 Documents Verbal Info Provided to NRR During Conference Call Re Relief Requests 98-002 & 98-003 ML20196G7461999-06-22022 June 1999 Requests Exemption from Requirements of 10CFR54.17(c) That Application for Renewed Operating License Not Be Submitted to NRC Earlier than 20 Yrs Before Expiration of Operating License Currently in Effect ML20195K3601999-06-14014 June 1999 Forwards MORs for May 1999 for McGuire Nuclear Station,Units 1 & 2 & Revised MORs for Apr 1999.Line 6 Max Dependable Capacity (Gross Mwe) on Operating Data Rept Should Be Revised to 1114 from Jan 1998 to Apr 1999 ML20195D5691999-06-0303 June 1999 Submits Ltr to Facilitate Closing of Inspector Follow Up Item 50-369,370/97-15-05,re Revising Site Drawings in UFSAR Into Summary one-line Flow Diagrams,Per NRC 990327 Telcon ML20196L1791999-05-20020 May 1999 Communicates Util Licensing Position Re Inoperable Snubbers. Licensee Has Determined That Structure of ITS Has Resulted in Certain Confusion Re Treatment of Inoperable Snubbers ML20196L1851999-05-20020 May 1999 Forwards Proprietary & non-proprietary Version of Rev 1 to TR DPC-NE-3004, Mass & Energy Release & Containment Response Methodology, Consisting of Finer Nodalization of Ice Condenser Region.Proprietary Info Withheld ML20206R0791999-05-13013 May 1999 Forwards Monthly Operating Repts for Apr 1999 for McGuire Nuclear Station,Units 1 & 2 & Revised Monthly Operating Repts for Mar 1999 ML20206T4481999-05-13013 May 1999 Forwards Rev 3 to Topical Rept DPC-NE-3002-A, UFSAR Chapter 15 Sys Transient Analysis Methodology, IAW Guidance Contained in NUREG-0390 ML20206S9151999-05-11011 May 1999 Forwards Rev 29 to McGuire Nuclear Station Selected Licensee Commitments. Section 16.11-16.2 Has Been Revised to Apply Guidance of NUREG-0133 for Performing Gaseous Effluent Dose Pathway Calculations ML20206K1341999-05-0303 May 1999 Forwards 1999 Interim UFSAR for McGuire Nuclear Station. UFSAR Update Includes Items Relocated During Improved Tech Specs Implementation.Next Regular UFSAR Update as Required 10CFR50.71(e) Is Due in Oct 1999 ML20206F3321999-04-28028 April 1999 Forwards Annual Radioactive Effluent Release Rept for 1998 for McGuire Nuclear Station. Listed Attachments Are Contents of Rept.Revised ODCM Was Submitted to NRC on 990203 ML20206E4101999-04-26026 April 1999 Forwards Four Copies of Rev 9 Todpc Nuclear Security & Contingency Plan,Per 10CFR50.54(p)(2).Changes Do Not Decrease Safeguards Effectiveness of Plan.Encl Withheld,Per 10CFR73.21 ML20206B4791999-04-20020 April 1999 Requests Exemption from GDC 57 Re Reactor Containment - Closed Sys Isolation Valves,As Described in 10CFR,App a for Containment Penetrations M393 & M261.Detailed Technical Evaluation & Justification for Exemption Request,Encl ML20205S9731999-04-19019 April 1999 Submits Info Re Quantity of SG Tubes Inspected,Tube Indications of Imperfections & Tubes Removed from Svc by Plugging,Per TS 5.6.8,part B 05000369/LER-1999-001, Forwards LER 99-01(S)-00 Re Contract Employee Submittal of False Info Resulting in Gaining Unescorted Access.No Licensee Planned Corrective Actions or Other Regulatory Commitments Were Identified as Result of Incidence1999-04-16016 April 1999 Forwards LER 99-01(S)-00 Re Contract Employee Submittal of False Info Resulting in Gaining Unescorted Access.No Licensee Planned Corrective Actions or Other Regulatory Commitments Were Identified as Result of Incidence ML20205P8891999-04-13013 April 1999 Forwards Monthly Operating Repts for Mar 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for Feb 1999 Encl ML20206K3561999-04-13013 April 1999 Forwards Revised McGuire Nuclear Station Selected Licensee Commitments (SLC) Manual. Significant Changes Are Marked by Vertical Bars on Right Margin ML20205K5131999-04-0707 April 1999 Forwards Complete Response to NRC 981209 & 990105 RAIs on Question 11 Re LARs for McGuire & Catawba Nuclear Stations. Addl Info Received from W & Contained in Encl W ML20205B6011999-03-23023 March 1999 Requests That NRC Place Technical Interface Agreement 97-02 Re URI 96-11-03,raising Operability & Design Criteria Conformance Issues Re Hydraulic Snubbers Installed at Plant & NRR Response on Dockets to Provide Record of Issue ML20205C4611999-03-23023 March 1999 Submits Correction to Violation Against 10CFR50 App B, Criterion VII, Control of Purchased Matl,Equipment & Svcs, Issued to McGuire Nuclear Station on 980807 ML20205B6161999-03-23023 March 1999 Provides Addl Info & Correction to Typo in Re License Bases Record Change Re License Amend Submittals ,approved as FOL NPF-9 & NPF-17,amends 184 & 166, respectively.Marked-up TS Pages,Encl ML20204J0051999-03-19019 March 1999 Forwards Response to 990127 & 28 RAIs Re GL 96-05 for Catawba & McGuire Nuclear Stations ML20204E1791999-03-18018 March 1999 Reflects 990318 Telcon Re License Bases Record Change for License Amend Submittals ,approved as Amends 184 & 166,respectively for Licenses NPF-9 & NPF-17.TS Pages Encl ML20204C8821999-03-15015 March 1999 Forwards Monthly Operating Repts for Feb 1999 for McGuire Nuclear Station,Units 1 & 2.Revised Rept for Jan 1999 Encl ML20207C2071999-02-25025 February 1999 Informs of Revised Expected Submittal Date of Proposed License Amend Presented at 990127 Meeting Re Soluble Boron & Boraflex.Util Plans to Submit Proposed License Amend in First Quarter of 1999 ML20207C7691999-02-22022 February 1999 Forwards Annual Occupational Radiation Exposure Rept for 1998. Rept Provides Tabulation of Number of Station,Utility & Other Personnel Receiving Exposure Greater than 100mRem/yr Followed by Total Dose for Each Respective Worker ML20207C6851999-02-22022 February 1999 Forwards Revised TS Bases Pages,Reflecting Removal of SI Signal on Low Steamline Pressure on Page B 3.3.2-16 & Adding Clarification for Increasing Hydrogen Recombiner Power During Testing on Page B 3.6.7-4 ML20206S3341999-01-28028 January 1999 Forwards Proprietary & non-proprietary Responses to NRC 981209 & 990105 RAIs Re Util Lars,Permitting Use of W Fuel at McGuire & Catawba Stations.Proprietary Info Withheld,Per 10CFR2.790 ML20199E0081999-01-12012 January 1999 Forwards MOR for Dec 1998 & Revised MOR for Nov 1998 for McGuire Nuclear Station,Units 1 & 2 ML20199C9861999-01-0707 January 1999 Forwards Annual Lake Norman Environ Summary Rept for 1997,as Required by NPDES Permit NC0024392,including Detailed Results & Data Comparable to That of Previous Years.With Corrected Pages 3 & 19 to 1994-95 Lake Norman Creel Rept 1999-09-09
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. 1I I Duke ker Company T C hichttmv hicGuire Nudear Generation Departrnent Vice President 12700Hagers ferryRoad(AIG01W)
(701)8754800
, Hunterwille,NC280784985 (704)8754809 Far
) DUKEPOWER October 24,1996 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555
Subject:
McGuire Nuclear Station, Units 1 and 2 Docket Nos. 50-369 and 50-370 NRC Inspection Report No. 50-369,370/96-07 Violations 50-369,370/96-07-01,96-07-05,96-07-07 and Deviation 369,370/96-07-04 Reply to a Notice of Violation and Notice of Deviation Gentlemen:
Enclosed is a response to a Notice of Violation dated October 2,1996 conceming failure to perform a Technical Specification surveillance, failure to perform an adequate 50.59 safety evaluation and inadequate corrective actions for an emergency diesel generator fuelline failure. Also enclosed is a response to a Notice of Deviation dated October 2,1996 conceming the use of incorrect resistance temperature detectors to monitor auxiliary feedwater supply line temperature.
Should there be any questions concerning this response, contact Randy Cross at (704) 875-4179.
Very Truly Yours, 1
2001 T. C. McMeekin '
Attachment TECI ' i 9611050032 961024 9 DR ADOCK 0500 050021
4 i' U. S. Nuclear Regulatory Commission Odtober 24,1996 4
t l
i 1
} xc: (w/ attachment) 4 Mr. S. D. Ebneter Mr. Scott Shaeffer Regional Administrator, Region 11 Senior Resident inspector U. S. Nuclear Regulatory Commission McGuire Nuclear Station 101 Marietta St., NW, Suite 2900 Atlanta, Georgia 30323 j
Mr. Victor Nerses U. S. Nuclear Regulatory Commission Office of Nuclear Reactor Regulation One White Flint North, Mail Stop 9H3 ,
Washington, D. C. 20555 '
L i
l l
M:Guira Nuclear Stati:n
, R: ply to a N;tice cf Violati:n Violation 50-369.370/96-07-05 10 CFR 50.59 (a)(1) authorizes the licensee to conduct tests or experiments not described in the safety analysis report without prior commission approval, unless the proposed test or experiment involves a i change in the technical specifications incorporated in the license or an unreviewed safety question.
i 10 CFR 50.59 (b)(1) requires the licensee to maintain records of the conduct of tests and experiments not described in the safety analysis report. These records must include a written safety evaluation that provides the basis for the determination that the test or experiment did not involve an unreviewed safety question.
Contrary to the above, on August 6,1996, the licensee conducted a test not described in the FSAR to verify an operability determination that a water hammer event would not occur with the presence of steam-voids in auxiliary feedwater piping. An adequate 50.59 safety evaluation to provide the basis for the determination that the test did not involve an unreviewed safety question was not performed prior to conducting this test.
This is a Severity Level IV violation (Supplement I).
Reolv to Violation 50-369.370/96-07-05
- 1. Reason for the violation:
The reason for the violation is inappropriate Action. The Reviewer that reviewed restricted change 60A to procedure OP/1/A/6250/02, Auxiliary Feedwater System Operating Procedure, for Unreviewed Safety Question (USO) applicability incorrectly determined that the procedure change was not a test and therefore, the change would not result in a test or experiment not described in the Updated Final Safety Analysis Report (UFSAR).
- 2. Corrective steos that have been tsken and the results achieved:
a) The 50.59 evaluation was immediately reviewed by Engineering personnel to determine its adequacy. The review indicated that the 50.59 screening for Unreviewed Safety Question (USO) consideration had been inappropriate. The review did confirm that Engineering personnel had correctly determined that no USO existed under the test conditions. A revised 50.59 will document the information known to Engineering personnel at the time the initial 50.59 was performed.
b) The inadequacy of the 50.59 was immediately discussed with the Engineering supervisors involved in the August 6,1996 CA system operability evaluation. The Qualified Reviewer that actually performed the 50.59 evaluation was counseled on August 21,1996.
c) On August 20,1996, the inadequate 50.59 evaluation and the related Problem investigation Process (PIP) was discussed during a McGuire Systems Engineering group meeting as a lesson leamed.
No similar events have occurred since implementation of these corrective actions.
1
Y 2 .
McGuira Nuclear Station l , Reply to a N:tice cf VI:lati:n i
, 3. Corrective steos that will be taken to avoid further violations:
j a) A reading package will be provided to all McGuire Qualified Reviewers to address the lessons learned as a result of the inadequate review and emphasize the importance of performing conservative 50.59 safety evaluations. The reading package will be completed by all McGuire Oualified Reviewers by December 31,1996.
b) Nuclear System Directive (NSD) 209,10 CFR 50.59, will be reviewed to determine if additional guidance to Qualified Reviewers is needed. This review will be completed by ,
, November 30,1996. l l
1 c) The initial 50.59 will be revised to document the information known to Engineering personnel j at the time the 50.59 was performed. This corrective action will be completed by November j 25,1996.
- 4. Date when full comoliance will be achieved:
0 McGuire Nuclear Station is now in full compliance with 10 CFR 50.59 requirements. All corrective actions will be completed by December 31,1996.
l 1
l l
l 2
McGuira Nuclear Statlin
, Reply to o Nstice cf VI:lati:n l l
. Violation 50-369.370/96-07-07 10 CFR 50 Appendix B, Criterion XVI, " Corrective Actions," states, that measures shall be established to ensure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment and nonconformances are promptly identified and corrected. In the cases of significant conditions adverse to quality, the measures shall assure that the cause of the l condition is determined and corrective action is taken to preclude repetition.
Contrary to the above, during the period from June 19,1996, to July 30,1996, adequate corrective actions were not taken to preclude repetition of a fuel line coupling failure on the McGuire Unit i B Emergency i Diesel Generator. '
This is a Severity Level IV violation (Supplement 1).
l Reolv to Violation 50-369.370/96-07-07 i
, 1 Reason for the violation: l l
i The reason for the violation is a failure to recognize the need to aggressively implement the identified j
. corrective actions to prevent additional fuel line failures. The decision to implement corrective )
l actions during scheduled maintenance days to minimize emergency diesel generator (EDG) j unavailability was based on an expectation that this was a trendable sub-component failure that l l would not result in the loss of the EDGs safety related function. Previous McGuire EDG-1B runs had !
- shown a slow decrease in the 4-Right cylinder temperature which may have indicated a small
) undetectable fuel leak. There was no indication of any similar cylinder temperature decreases in j- other EDG-1B cylinders or with the other EDGs. McGuire and Brunswick (CP&L) Nordberg EDG
- history indicated no previous similar failures. A previously performed torsional analysis concluded f
that the EDG would continue to operate with failure of a cylinder fuelline. A visualinspection of all l EDG fuellines showed no evidence of tubing ferrule pullout or misalignment.
The second failure of the EDG-1B 4-Right cylinder fuel line occurred prior to implementation of the 1
- corrective actions. This failure occurred rapidly and was not trendable. However, this was also a sub-component failure that did not result in the loss of the EDG safety related function . Subsequent consultation with industry experts resulted in a more comprehensive and timely corrective action j i plan.
- k. 2. Corrective steos that have been taken and the results achieved: 1 1 '
! a) Following the original failure, a new fuel line was installed for the 4-Right cylinder. It was j torqued to a procedure range of 40-60 ft-Ibs. to prevent cracking of fuel oil delivery valve
. holder which was previously experienced. Torquing to 40-60 ft-lbs. had been sufficient in the !
past to prevent fuel leaks while not damaging the delivery valve holder. The EDG-1B 4
successfully completed a monthly surveillance test with normal cylinder exhaust temperatures I and no observed leakage. !
i i Following the EDG-1B retum to service the failure root cause was determined to be inadequate crimping of the ferrule sleeve onto the fuelline during manufacturing. Corrective actions were developed to expeditiously recrimp all fuel lines installed on the EDGs during the i previous 1EOC10 and 2EOC10 outages. Work orders were written to perform the recrimping i
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McGuire Nu lear Station Reply ts e N:tice cf VI:lition 4
during the period July 18,1996 through October 8,1996 concurrent with normal EDG down day schedules to minimize EDG unavailability. On July 30,1996, prior to initiation of these corrective actions, a second fuel line failure occurred on 1B EDG 4-Right cylinder during performance of the monthly surveillance per PT/1/A/4350/02B.
b) . Following the second fuel line failure, a station recovery team developed and implemented a plan to remove the 4-Right injector, fuel hne and fuel pump for testing to determine the root cause of the failure. Industry consultants were included in this team to provide additional expertise conceming diesel fuel injection systems. The Failure Investigation Process (FIP) concluded that the most likely cause of the failure was insufficient crimping of the fuel line ferrule due to inadequate crimping torque during manufacturing. Overpressurization of the fuel line caused by partial spray tip blockage was a possible contributing factor.
Re-evaluation of the root cause for the fuel line failures reconfirmed the initial root cause of inadequate crimping of the ferrule sleeve onto the fuel line during manufacturing. Thus normal fuel oil injection pressure caused the fuel line outer diameter material in contact with the ferrule to yield. This yielding resulted in a failure of the fuel line connection, excessive fuel oil leakage for cylinder 4-Right and loss of cylinder power. The inadequate crimping resulted from the manufacture's use of a procedure that did not adequately specify crimping torque requirements. in addition, the manufacture's procedure did not adequately control the length of the fuel line extending past the ferrule to preclude bottoming the line into the fuel oil delivery valve holder.
c) On August 1,1996, all EDG-1B fuel line assemblies were removed, recrimped to 150 ft-Ibs.
on the pump end, trimmed to 0.060 - 0.085 inches from the ferrule, re-installed, and torqued to 40-60 ft-lbs. per new procedure MP/0/A/7400/87. In addition, a new injector and fuel pump :
were insta!!ed on the EDG-1B 4-Right cylinder. On August 2,1996, the EDG-1B successfully '
completed a sixteen hour run to verify the recrimping process was adequate.
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d) During the period August 3,1996 through August 6,1996, all fuelline assemblies for EDGs 1 A,2A and 2B 'cere removed, recrimped to 150 ft-lbs. on the pump end, trimmed to 0.060 - ,
0.085 inches frc rr the ferrule, re-installed, and torqued to 40-60 ft-lbs. per ne.y procedure MP/0/A/7400/8/.
No similar events have occurred since implementation of these corrective act.ons.
- 3. Corrective steos that will be taken to avoid further violations:
The January 26,1997 completion date for corrective actions 3.a, b and d below was determined based on EDG maintenance scheduled during the upcoming 1997 refueling outages, a) EDG spare parts specification MCS-1301.00-00-0007 will be updated to address new fuelline crimping and dimensional requirements. This update will be completed by January 26,1997.
b) All procedures affecting EDG fuel line installation or removal, including Maintenance procedure MP/0/A/7400/09, Nordberg Diesel Engine Cylinder Head Removal and Installation, and MP/0/A/7400/01, Nordberg Diesel Engine Fuel Oil Injection Pump Removal, Installation and Lift to Port Closure Check, have been placed on administrative hold to prevent use. These 4
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McGuire Nu: lear Station
, Reply is e N:tice cf Violation
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F procedures will be revised to address the new crimping and dimension requirements prior to
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use, otherwise, the procedures will be revised by January 26,1997.
c) Engineering will evaluate the need to add fuel injector spray tip cleaning to the Nordberg Owner's Group six year preventative maintenance and to the McGuire preventative maintenance i
procedure. This evaluation will be completed by January 26,1997.
2 l i d) All spare fuel line assemblies stored in the station warehouse will be recrimped and machined in accordance with procedure MP/0/A/7400/87. This corrective action will be completed by January 26,1997.
, e) A reading package discussing the EDG fuelline failures and the lessons learned will be provided to all McGuire Engineering personnel. The reading package will emphasize the need for i aggressive corrective action when Root Cause Analysis results indicate a potential for recurring 4
failures on similar plant equipment. This corrective action will be completed by December 31, 1996.
- 4. Date when full comoliance will be achieved:
McGuire Nuclear Station is now in full compliance with 10 CFR 50 Appendix B, Criterion XVI. All corrective actions will be completed by January 26,1997. j l
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McGuira Nu: lear Station
, Reply 13c N tice cf Viriation 2
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l Violation 50-369.370/96-07-01 Technical Specification 3.8.1.1 (d) requires that with a diesel generator inoperable, the operability of the other diesel must be demonstrated by performing surveillance requirement 4.8.1.1.2.a.4 and 4.8.1.1.2.a.5 within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
Contrary to the above, the licensee failed to demonstrate the operability of the 1 A emergency diesel I 4
generator within the required time after the 1B emergency diesel generator was determined to be
- inoperable.
This is a Severity Level IV violation (Supplement 1).
Reolv to Violation 50-369.370/96-07-01 i
- 1. Reason for the violation:
I The reason for the violation is inappropriate Action. The operator relied on memory to evaluate the l conditional surveillance requirements for the remaining EDG when the Nuclear Service Water (RN)
- system was declared inoperable and the operator incorrectly determined that a conditional j surveillance was not required. This determination was based on this particular failure not being a common mode failure and, therefore, the conditional surveillance (to run the opposite train EDG) was
- mistakenly felt to not be applicable. In addition, procedure PT/1,2/A/4350/25, Essential Auxiliary Power Source Verification, did not clearly provide guidance on the need to run the opposite train EDG.
j j 2. Corrective steos that have been taken and the results achieved:
1 During the investigation of the failure to perform the conditional surveillance, System Engineering determined that the RN Train B was operable. Therefore, the EDG 1B was operable and the conditional surveillance of EDG 1 A was not required, a) Management expectations were reinforced to ensure that Operations personnel understand the need to thoroughly research each Technical Specification entry for reportability, operability,
- conditional surveillance and notification concems. This corrective action was completed on October 21,1996.
! b) PT/1,2/A/4350/25, Essential Auxiliary Power Source Verification, the procedure for verifying the l conditional surveillance for TS 3.8.1.1(d) Action Statement was revised to indicate that the opposite train EDG needs to be run anytime an EDG becomes inoperable due to an equipment i failure. This corrective action was completed on October 17,1996.
i j No similar events have occurred since implementation of these corrective actions.
1 1 3. Corrective steos that will be taken to avoid further violations:
No additional corrective actions are planned.
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McGuira Nuclear Station
, Reply to c N:tice cf VI:lati:n
- 4. Date when full comoliance will be achieved:
McGuire Nuclear Station is now in full compliance with Technical Specification 3.8.1.1 (d).
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McGuiro Nuclear Stati:n i
, Heply ta e N:tice cf Devi:ti:n Deviation 50-369.370/96-07-04
) McGuire Nuclear Station response to Generic Letter 88-03, Steam Binding of Auxiliary Feedwater Pumps, i
February 17,1988, stated that the licensee would provide continuous mxitoring of auxiliary feedwater piping to detect the formation of steam voids that could prevent the e.uxiliary feedwater pumps from j performing their intended safety function.
- ' Contrary to the above, continuous monitoring to detect steam voiding was not accomp'is'1ed due to the installation of an incorrect type of resistance thermal detector (RTD) to provide accurate indication of I auxiliary feedwater piping temperatures and activation of control room alarms when temperatures l exceeded established administrative limits. This condition was identified on August 1,1996.
Reolv to Deviation 50-369.370/96-07-04 J 1. Bgason for the deviation:
The reason for the deviation is inappropriate Action. McGuire's May 26,1988 response to Generic
. Letter 88-03 stated that strap-on thermocouples had been installed on auxiliary feedwater (CA)
- piping. However, RTD's designed for thermowell applications were installed which resulted in inaccurate temperature readings. McGuire personnel responsible for processing Nuclear Station Modifications (NSMs) when this modification was planned in the mid-1980s selected the incorrect type of RTD for this application.
- 2. Corrective steos that have been taken and the results achieved:
a) Immediate corrective action was taken to begin verifying the CA piping surface temperature once every shift to ensure the CA procedure temperature limits were not exceeded.
Subsequently, the commitment was temporarily revised using the 50.59 process until minor modifications were implemented.
1 o) Minor modifications MGMM-8546 (Unit 1) and MGMM-8547 (Unit 2) were implemented to replace the existing RTD's with a strap-on surface mounted application. This corrective action ;
was completed on September 23,1996.
No similar events have occurred since implementation of these corrective actions.
- 3. Corrective steos that will be taken to avoid further deviations:
No additional corrective actions are planned.
- 4. Date when corrective action will be comolete:
All corrective actions were completed by September 23,1996.
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