ML20133L664
| ML20133L664 | |
| Person / Time | |
|---|---|
| Site: | Callaway |
| Issue date: | 01/16/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | |
| Shared Package | |
| ML20133K956 | List: |
| References | |
| 50-483-96-14, NUDOCS 9701220099 | |
| Download: ML20133L664 (16) | |
See also: IR 05000483/1996014
Text
. _ _ . .
_ . _
. . _ . . _ . _ . . _ . . _ _ _ . _ _ _ _ _ _ _ _ . . _ . - _ _ . _ _ _ _ . . . . _ _ - _ . _ - . _ _ . . _ . . . _ _ . . . . _
.
4
,
s
.
4
ENCLOSURE 2
I
.
lj -
U.S. NUCLEAR REGULATORY COMMISSION
i
REGION IV
!
1
!.
l
Docket No.:
50-483
'
- .
i
j
License No.:
i
'
i
Report No.:
50-483/96-14
'
]
Licensee:
Union Electric Company
t
l
Facility:
Callaway Plant
'
Location:
Junction Highway CC and Highway O
q
Fulton, Missouri
i
l
Dates:
November 24,1996, through January 4,1997
i
i
inspectors:
D. G. Passehl, Senior Resident inspector
j
F. L. Brush, Resident inspector
- 4
H. F. Bundy, Reactor Engineer
G. M. Good, Senior Emergency Preparedness Analyst
i
Approved By:
W. D. Johnson, Chief, Project Branch B
1
- .
1
'
i
4
,
ATTACHMENT: Supplemental Information
1
i
l
i
'
,
1
I
d
<
!
!
.
i
4
a
U
!
4
1
l
l
9701220099 970116
ADOCK 05000483
G
7
4
-. --
. . .
,.
. , , .
-
- --
"
.
.
EXECUTIVE SUMMARY
Callaway Plant
NRC Inspection Report 50-483/96-14
Operations
The license's decision to shutdown the plant to repair a feedwater isolation valve
actuator was appropriate (Section 01,1).
The control room staff response to a turbine trip during reactor startup was good
(Section 01.2). There were no problems during the subsequent startup
(Section 01.3).
An equipment operator was thorough during rounds. The plant material condition
was good (Section O2.1).
An equipment operator inadvertently pulled the wrong fuses on a bus in the main
circulating water and service water pump house. This resulted in a partialloss of
circulating water flow to the main condenser and required the operators to reduce
plant power. This was a violation caused by a personnel error (Section 04.1).
Maintenance
The licensee's actions to determine the reason for the main feed water isolation
valve hydraulic actuator leaks were thorough. The licensee installed incorrect
0-rings due to inadequate material control which was a noncited violation
(Section M1.3).
"iant Suncort
The commitment to perform onshif t dose assessments was clearly described in the
emergency plan and implementing procedures (Section P3.1).
.-_ _
.
--
.
.
_.
.
.
-
-
. _
..
j
,
4
Report Details
.
4
Summary of Plant Status
i
j
The plant was at 100 percent power at the beginning of the report period.
.
On December 1,1996, due to hydraulic oilleaks on the actuator for feedwater isolation
'
Valve D, the licensee shut down the unit. At 12:48 p.m. on December 5,1996, the plant
was brought back online. However, the turbine tripped a few minutes later due to a hi-hi
steam generator water level. At 8:25 p.m. on December 5,1996, the license returned the
unit online. The unit reached full power on December 6,1996.
At 4:41 p.m. on December 18,1996, the licensee reduced plant power to 92 percent
when an equipment operator inadvertently tripped a main circulating water pump. The
plant was returned to full power approximately four hours later and operated near
100 percent power for the remainder of the report period.
4
I. Operations
'
01
Conduct of Operations
01.1 Plant Shutdown
<
a.
Inspection Scone (71707)
i
l
1
On December 1,1996, the inspectors observed control room operations during
portions of the plant shutdown for a forced outage.
b.
Observations and Findinas
The licensee shut down the unit due to hydraulic fluid leaks on the actuator for main
feedwater isolation Valve AEFV0042. The actuator repair effort is discussed in
paragraph M1.2. The licensee's decision to shut down the unit was appropriate.
The licensee would have been required to enter and exit facdwater isolation valve
Technical Specification action statement 3.7.1.6 repeatediy in order to repair the
valve.
The shift supervisor held good briefings prior to starting the power reduction and
removing major equipment from service. Licensee management was present in the
control room and ensured personnel were aware of expectations. There was good
communication between the control room operators. The shift supervisor exhibited
good command and control. Operators did self-checking prior to manipulating plant
components. The inspectors did not note any problems.
In addition, the inspectors verified compliance to the Technical Specifications and
Final Safety Analysis Report requirements by reviewing logs, touring main control
boards and reviewing status boards.
.
.
-2-
01.2 Plant Startuo with Turbine Trio, Feedwater System isolation and Motor-Driven
Auxiliary Feedwater System Actuation
.
l
a.
Insoection Scoce (71707,93702)
l
On December 5,1996, the inspectors observed portions of the plant startup
following the forced outage discussed in Section 01.1.
During the startup, a hi-hi water levelin Steam Generator B resulted in a main
'
turbine trip, feedwater system isolation, and motor-driven auxiliary feedwater
actuation. The inspectors observed the control room operator response to the trip.
,
b.
Observations and Findinos
l
During the startup prior to entering Mode 2, the control room supervisor held good
- l
briefings. There was good communication among operations personnel. Licensee
management was in the control room and discussed their expectations with onshift
personnel.
At approximately 18 percent power, while transferring feed flow control from the
feedwater flow bypass valves to the main feedwater regulating valves, the steam
generator water levels began to oscillate. A main turbine trip and engineered safety
features actuations occurred when the level in Steam Generator B reached the hi-hi
setpoint of 78 percent. The magnitude of the level oscillations in the steam
generators were exacerbated by the positive moderator temperature coefficient
present at low power levels during this early stage in core life.
Operator response following the turbine trip and feedwater isolation was good. In
order to rapidly establish normal steam generator level, the operators manually
started the turbine-driven auxiliary feedwater pump and used control rods to rapidly
reduce power. This prevented a reactor trip on low steam generator level due to
the isolation of the main feedwater system. The shift supervisor exhibited good
command and control.
c.
Conclusions
The control room staff's response to the turbine trip was good. Operator
communications were good during the startup and subsequent trip. The shif t
supervisor exhibited good command and control. Licensee management ensured
that plant personnel followed expectations.
01.3 Second Plant Startuo on December 5,1996(71707)
Following the trip noted in paragraph 01.2, the licensee reviewed the methods of
starting up and increasing power with a positive temperature coefficient. For the
second startup on December 5,1996, the licensee changed the method for
-
.
_-
--
.
~
,
l
.
l
i
-3-
,
I
'
I
transferring from the main feedwater bypass valves to the main feedwater
regulating valves.
Rather than continuing to increase main generator load just after synchronizing to
the grid, the licensee held the main generator output to approximately 60 MWe.
When steam generator water levels had stabilized and the feedwater bypass valves
were approximately 90 percent open, using the steam dumps, the licensee
increased the main generator output at approximately one half percent per minute.
This allowed a smooth transition from the feedwater bypass to the main feedwater
regulating valves. There were no steam generator level deviation alarms during this
startup. The inspectors did not identify any significant issues.
1
O2
Operational Status of Facilities and Equipment
02.1 Plant Tours
i
'
a.
Inspection Scope (71707)
The inspectors accompanied an equipment operator during rounds of the auxiliary
and fuel buildings. This was to determine the thoroughness of his inspections and
his sensitivity to equipment and plant housekeeping problems.
b.
Observations and Findinas
The operator was appropriately sensitive to the condition and operating status of all
1
equipment inspected. The inspectors noted that the operator wiped oil
accumulatior, from safeguards pumps, which was considered a good practice. The
inspectors also noted that any leaks were appropriately identified with work request
tags.
The operator noted that chemical and volume control system to centrifugal charging
,
Pump A discharge to reactor coolant pump seals throttle Valve BGHV8357A,had
an accumulation of boric acid crystals. The operator stated that this did not meet
expectations from both housekeeping and corrosion control standpoints. The
'
inspectors followed up and found that the valve is being tracked by the licensee's
boric acid leak tracking program iad will be worked at an appropriate time. The
inspectors observed that the operator was thorough in his inspections and was
particularly sensitive to determining the status of previously identified fluid leaks.
,
l
The inspectors observed that material, tools, and equipment were properly stored.
With the exception of clutter in the hot tool and radwaste staging areas, the
buildings were clean and free of debris. The clutter observed in the noted areas
was not unexpected in that refueling outage cleanup was still in progress.
- -
.-
.-
-
-
-
_
_ . -
i
.
.
i
'
-4-
-
I
c.
_ Conclusions
The equiprnent operator was thorough in his inspections and particularly sensitive to
determining the status of existing fluid leaks. The plant material condition was
good.
i
i
02.2 Cold Weather Preparations
a.
Inspection Scone (71707)
The inspectors reviewed the licensee's cold wcather preparations,
b.
Observations and Findinas
The licensee performed a plant walkdown using Procedure OTS-ZZ-00007,
i
I
Revision 3, " Plant Cold Weather," to ensure that equipment required during cold
weather was operational. During the walkdown, the licensee identified a few
deficiencies which were corrected. The inspectors did not note any problems
during subsequent cold weather conditions.
l
04.1 Worker Protection Tao Placed on the Wrona Component which Trioned Main
i
'
j
Circulatina Water Pumo B and Service Water Pumo B
j
1
a.
Insoection Scope (71707)
The inspectors reviewed a December 18,1996, event, which occurred when an
equipment operator inadvertently pulled the metering and relay fuses for electrical
Bus PB122. The bus supplied power fo, main circulating water Pump B and service
water Pump B. When the fuses were pulled, the pump undervoltage protective
circuits tripped the two pumps. The equipment operator was supposed to pull the
l
instrument potential transformer secondary fuses for electrical Bus PB121.
b.
Observations and Findinas
While intending to place a worker protection tag on an instrument potential
transformer secondary fuses for electrical Bus PB121, an equipment operator
!
incorrectly placed the worker protection tag on the metering and relay fuses for
electrical Bus PB122. This action caused main circulating water Pump B and
l
service water Pump B to trip. Main circulating water Pump A and service water
l
Pump A were already secured to allow maintenance on Bus PB121. This left only
service water Pump C and main circulating water Pump C in service.
When the equipment operator pulled the metering and relay fuses, the control room
operators received a number of indications alerting them that the pumps had
tripped. Control room personnel immediately commenced reducing power to
prevent a turbine trip on loss of main condenser vacuum. Condenser pressure
t
1
.
.
5-
increased and stabilized at approximately 4.5 inches Hg after reactor power was
reduced to 92 percent. The condenser pressure turbine trip setpoint was 7.5 inches
Hg. The operators started essential service water Pump A to provide an adequate
service water supply.
After determining that the fuses were inadvertently pulled, the licensee restored
both Bus PB121 and Bus PB122 and restarted main circulating water Pump B.
Service water Pump A was also started and essential service water Pump A was
secured. The plant was returned to 100 percent power.
The licensee initiated an investigation of the event using the corrective action
process.
The licensee identified the following major causes:
Failure to perform self-checking of the worker protection tag against the
component labeling.
Many of the fuses outside the power block were not consistently labeled.
The licensee's corrective actions included reviewing proper tcgout techniques with
1
equipment operators. This includes the expectation that field supervisors resolve
'
any discrepancies between tagout sheet nomenclature and component labels in the
field. The licensee was also reviewing the adequacy of fuse labeling for
components outside the power block. Fuse labeling problems inside the power
block were identified and corrected at an earlier time.
The inspectors agreed with the licensee's findings.
Administrative Procedure ODP-ZZ-00310,"Workmac.'s Protection Assurance
Tagging", Revision 2, Step 4.1.10.3, required that the method and order specified
on the tagout control sheet be followed when hanging tags.
The tagout control sheet for Workman's Protection Assurance 21672, Tag 10,
specified that a tag be hung on the potential transformer secondary fuses for
Bus PB121. Failure to adhere to this requirement is considered a violation of the
licensee's administrative procedure.
NRC Inspection Report 50-483/9611 identified a similar occurrence when an
equipment operator pulled incorrect fuses and rendered centrifugal charging Pump A
inoperable. This licensee-identified and corrected violation is being treated as a
cited violation due to a repeat occurrence of a recent event (483/9614-01).
_ ._
_
. . _ _ .
_ _ . _ . . _ . . _ _ - _ . . _ _ _ - _ _ _
_
. _ _ _ _ _ - .
.
.
-6-
c.
Conclusions
The inspectors concluded that the failure to pull the correct fuses was due to
personnel error.
08
Miscellaneous Operations issues
08.1 Technical Specification interpretations (71707)
During a review of Callaway Technical Specification Interpretations, the inspectors
noted that NRC personnel were identified as giving concurrence for the positions
taken in two of them:
Technical Specification interpretation 1 - Emergency Core Cooling System
Accumulators, and
Technical Specification Interpretation 4 - Turbine Overspeed Protection.
The inspectors informed the licensee that this form of NRC involvement is not
recognized by the Commission and is not an acceptable practice. However, the
referencing of official NRC correspondence in a licensee Technical Specification
Interpretation is acceptable. The inspectors requested that the licensee remove any
informal references to NRC review and/or approval from their Technical
Specification Interpretations. The licensee's Onsite Review Committee had already
approved removing these interpretations from the Technical Specifications.
II. Maintenance
M1
Conduct of Maintenance
l-
i
i
M 1.1 General Comments - Maintenance
a,
inspection Scope (62707)
The inspectors observed or reviewed portions of the following work activities:
Work Activity P541890- Centrifugal Charging Pump A Motor Bearing Oil
Sight Glass Leaks,
Work Activity W175769- Rebuild Spare Feedwater Isolation Valve Actuator,
Work Activity P548345- Clean and inspect Feeder Circuit Breaker to Motor-
l
Driven Auxiliary Feedwater Pump A,
Work Activity P548864- Calibrate Auxiliary Feedwater Flow to Steam
Generator B Feed Flow Transmitter, and
,
.
.
-7-
Work Activity P576360- Cold Weather Preparations.
b.
Observations and Findinas
Except as noted in paragraph M1.3, the inspectors found no concerns with the
maintenance observed. All work observed was performed with the work packages
present and in active use. The inspectors frequently observed supervisors and
system engineers monitoring job progress, and quality control personnel were
present when required. Housekeeping and foreign material exclusion controls were
satisfactory.
M1.2 General Comments - Surveillance
a.
Inspection Scope (61726)
The inspectors observed all or portions of the following test activities:
Surveillance Procedure OSP-EF-P001 A- Emergency Service Water Train A
Operability,
Surveillance Procedure OSP-NE-0001 A- Standby Diesel Generator A Periodic
Tests, and
Surveillance Procedure OSP-SA-0017A- Train A Safety injection System -
Containment Spray Actuation System Slave Relay Test.
b.
Observations and Findinas
Surveillance testing observed during this inspection period was conducted
satisfactorily in accordance with the licensee's approved programs and the
Technical Specifications.
M 1.3 Feedwater Isolation Valve Actuator Hydraulic Leaks
a.
Insnection Scooe (62707)
On November 29,1996, the actuator on feedwater isolation Valve AEFV0042 for
Steam Generator D, developed a hydraulic leak on both hydraulic system trains.
Each train is capable of independently closing the feedwater isolation valve upon
receiving a feedwater system isolation signal. The inspectors reviewed the
licensee's efforts to repair the actuator and determine the root cause of the leaks.
b.
Observations and Findinas
The licensee discovered that the wrong size O-rings had been installed on both
hydraulic system trains for the actuator on Valve AEFV0042. Although the inside
_ - _ - - _ . - - - .
.--- - - -
.~~.-
-- ------
-
f
.
-
.
[
-8-
!
I
diameter of the O-rings was correct, the thickness was incorrect. As the hydraulic
pressure'in the actuator cycled during normal operation, the O-ring material wore '
'
away which established a leak path outside the valve.
The licensee ' determined the root cause to be a maintenance error during
refurbishment of a spare hydraulic actuator for Valve AEFV0042. Workers
refurbished the spare actuator just prior to the recent refueling outage. This
refurbishment included installing new O-rings on the hydraulic trains on October 8,
'
1996. However, some of the O-rings were the incorrect size. The licensee later-
i
replaced the existing actuator on AEFV0042 with the newly refurbished spare (with
the iicorrect 0-rings) during the refueling outage as part of an overall preventive
i
maintenance task.
l
In December 1996, during the licensee's followup investigation after the leak was
discovered, the licensee inspected several dozen 0-rings and found a total of 17
incorrect 0-rings that had been installed in both hydraulic trains in Valve
AEHVOO42. The licensee replaced these with the correct 0-rings.
The licensee held a multidisciplinary review to determine the root cause of and
'
corrective actions for this event. As a result, the licensee initiated a case study of
this event due to the broad scope of potential corrective actions.
The licensee's short term corrective actions included successfully repairing the valve
and testing a representative sample of O-rings in stock to ensure no other O-ring
problems existed. No incorrect 0-rings were identified.
The licensee's long term corrective actions include the case study, which
addresses:
Ensuring correct drawings are specified and available in work packages,
Reviewing material control wording to clear up confusing nomenclature on
parts sizing,
Ensuring adequate work planning and coordination for complex maintenance
efforts, and
Conducting training on the results of the case study for the various
disciplines involved in maintenance activities.
l
The inspectors reviewed the work package used to refurbish the actuator on
AEFV0042 just prior to the refueling outage. The inspectors found that the
i
supervisor in charge of the job did not thoroughly review the work package for
I
information on replacement 0-rings. Information on replacement 0-rings of the
correct size and material was available in the work package.
i
l
._ _
_____
._
. _ _ _ .
_ . _._ _ _ _ _ _ _
.
. _ _
_ _ _ _ _ _ _ _ . . _ _ _ ,
..
l
.
l
i
!
.g.
'
o
,
i
i
'
l
l
'
'
Criterion V of Appendix B to 10 CFR Part 50 requires, in part, that activities
'
affecting quality shall be prescribed by documented instructions, procedures, and
i
drawings appropriate to the circumstances and shall be accomplished in accordance
with these instructions, procedures, or drawings. The failure to adhere to this
l
requirement is considered a violation of Criterion V of Appendix B to 10 CFR
r
Part 50. This licensee-identified and corrected violation is being treated as a
,
noncited violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy
(483/9614-02).
i
c.
Conclusions
The inspectors concluded that the licensee's actions to determine the reason for the
leak were thorough. The inspectors also found the licensee's repair of the leaking
hydraulic components to be satisf actory. The licensee's control of O-ring material
for rebuilding the feedwater isolation valve actuator was lacking.
Ill. Enaineerina
E1
Conduct of Engineering
E1.1
fnaineerina Involvement in Plant Activities (37551)-
The inspectors noted that engineering was appropriately involved in plant activities
during this inspection period. The inspectors noted that system engineers
conducted plant walkdowns of assigned systems for cold weather preparations as
discussed in Section O2.2 of this report. Expectations were included on a
management policy entitled " System Walkdowns," NE-System Walkdown-01,
Revision 1. In addition, plant engineers participated in the multidisciplinary case
study team and root cause evaluation for the failure of feedwater isolation Valve
AEFV0042 (Section M1.3). The inspectors had no concerns,
j
E2
Engineering Support of Facilities and Equipment
E2.1
Review of Facility Conformance to Uodated Final Safety Analvsis Report
Commitments
j
A recent discovery of a licensee operating their f acility in a manner contrary to the
Final Safety Analysis Report description highlighted the need for a special focused
review that compares plant practices, procedures, and/or parameters to the Final
Safety Analysis Report description. While performing the inspections discussed in
this report, the inspectors reviewed the applicable portions of the Final Safety
Analysis Report that related to the areas inspected. No inconsistencies were noted
between the wording of the Updated Safety Analysis Report and the plant practices,
procedures, and/or parameters observed by the inspectors,
i
,
,
_ _ . . .
. . _
..
_ _ . _ _ - _ _
. . _ ,
.
i
e
-10-
IV. Plant SuDDort
R1
Radiological Protection and Chemistry (RP&C) Controls
R 1.1
Radioloaical Protection Proaram Observations
The inspectors toured various areas of the radiologically controlled areas of the
plant. Health physics personnel were observed routinely touring the radiologically
controlled areas. Licensee personnel observed performing work in radiological
control areas exhibited good radiation worker practices. Contaminated areas and
high radiation areas were properly posted. Area surveys posted outside rooms in
the auxiliary building were current.
P3.1
Licensee Onshift Dose Assessment Capabilities
a.
Insoection Scoce (Tl 2515/134)
Using Temporary Instruction 2515/134,the inspectors gathered information
regarding:
Dose assessment commitment in emergency plan,
Onshift dose assessment emergency plan implementing procedure, and
Onshift dose assessment training.
b.
Observations and Findinas
On December 17,1996, the inspectors conducted an inoffice review of the
emergency plan and implementing procedures to obtain the information requested
by the temporary instruction. The inspectors also conducted a telephone interview
with the licensee on December 17,1996, to verify the results of the review. Based
on the documentation review and the licensee interview, the inspectors determined
that the licensee had the capability to perform onshift dose assessments using real-
time effluent monitor and meteorological data and that the commitment was clearly
described in the emergency plan and implementing procedures.
c.
Conclusion
The commitment to perform onshift dose assessments was clearly described in the
emergency plan and implementing procedures. Further evaluation of the information
obtained using the temporary instruction will be conducted by NRC Headquarters
personnel.
I
..
. - .
. - -
. - - - . . -
. . - . - - . - - -
- - - _ . - . . . . . - _ . - . - ~ . . - . . . - - -
r.
!
.
i
t
l
-11-
)
e
i
i
i
I
V. Manaaement Meetinas
X1
Exit Meeting Summary
The exit meeting was conducted on January 3,1997. The licensee expressed a
position on the subject of the violation in this report.
During the discussion of the equipment operator inadvertently pulling the wrong
fuse which caused operators to reduce plant power (Section 04.1), the licensee
stated that the event was not significant enough to merit a violation for the
following reasons:
The licensee disagreed that a procedure violation occurred given a literal
interpretation of the equipment control tagging procedure,
The licensee stated that 10 CFR 50, Appendix B, did not apply to the non-
safety related fuse, and
The licensee stated that the equipment control tagging procedure was a
reference-use procedure.
The inspectors asked the licensee whether any materials examined during the
inspection shou!d be considered proprietary. No proprietary information was
identified.
.
.
- -
i *
,
1
o
ATTACHMENT
SUPPLEMENTAL INFORMATION
PARTIAL LIST OF PERSONS CONTACTED
Licensee
J. D. Blosser, Manager, Operations Support
H. D. Bono, Supervising Engineer, Licensing Fuels and Site Licensing
D. G. Cornwell, General Supervisor, Maintenance
R. T. Lamb, Superintendent, Operations
l
J. V. Laux, Manager, Quality Assurance
D. W. Neterer, Shif t Supervisor
J. R. Peevy, Manager, Emergency Preparedness and
Organizational Support
G. L. Randolph, Vice President, Nuclear Operations
M. A. Reidmeyer, Engineer, Quality Assurance
R. R. Roselius, Superintendent, Chemistry and Rad Waste
J. D. Schnack, Engineer, Quality Assurance
!
T. P. Sharkey, Supervising Engineer, Nuclear Operations
INSP_fCTION PROCEDURES USED
IP 37551:
Onsite Engineering
IP 61726:
Surveillance Observations
IP 62707:
Maintenance Observations
i
IP 71707:
Plant Operations
1
IP 93702:
Prompt Onsite Response to Events at Operating Power Reactors
Tl 2515/134
Licensee Onshift Dose Assessment Capabilities
ITEMS OPENED CLOSED, AND DISCUSSED
l
Ooened
9614-01
Equipment Operator Pulled Incorrect Fuse (Section 04.1)
9614-02
Leaking 0-Rings On Feedwater isolation Valve AEFV0042
For Steam Generator D (Section M1.3)
!
i
i
Closed
!
l
9614-02
Leaking O-Rings On Feedwater Isolation Valve AEFV0042
'
For Steam Generator D (Section M1.3)
i
l
l
'
.
- . -
_
_
_
_
-
. . .
-
.
-
..
. . -
.- -
- - -
1
o
e
't
-2-
LIST OF DOCUMENTS REVIEWED
Emeroency Plan imolementina Procedures
EIP-ZZ-00101
Classification of Emergencies
Revision 19
ElP-ZZ-00102
Emergency implementing Actions
Revision 15
EIP-ZZ-01211
Management Action Guides for
Revision 18
Nuclear Emergencies
Other Documents
Callaway Radiological Emergency Response Plan
Revision 20
CN 96-02