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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20212J6311999-10-0101 October 1999 SER Accepting Request for Relief from ASME Boiler & Pressure Vessel Code,Section Xi,Requirements for Certain Inservice Insp at Plant,Unit 1 ML20212F0831999-09-23023 September 1999 Safety Evaluation Granting Relief from Certain Weld Insp at Sequoyah Nuclear Plant,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(ii) for Second 10-year ISI Interval ML20212F4761999-09-23023 September 1999 Safety Evaluation Supporting Amends 246 & 237 to Licenses DPR-77 & DPR-79,respectively ML20196J8521999-06-28028 June 1999 Safety Evaluation Authorizing Proposed Alternative to Use Iqis for Radiography Examinations as Provided for in ASME Section III,1992 Edition with 1993 Addenda,Pursuant to 10CFR50.55a(a)(3)(i) ML20239A0631998-08-27027 August 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Sequoyah Nuclear Plant,Units 1 & 2 ML20236Y2091998-08-0707 August 1998 Safety Evaluation Accepting Relief Requests RP-03,RP-05, RP-07,RV-05 & RV-06 & Denying RV-07 & RV-08 ML20217K4471998-04-27027 April 1998 Safety Evaluation Supporting Requests for Relief 1-ISI-2 (Part 1),2-ISI-2 (Part 2),1-ISI-5,2-ISI-5,1-ISI-6,1-ISI-7, 2-ISI-7,ISPT-02,ISPT-04,ISPT-06,ISPT-07,ISPT-8,ISPT-01 & ISPT-05 ML20138D2581997-04-28028 April 1997 Safety Evaluation Authorizing Licensee Proposed Alternative to Use 1989 Edition of ASME Boiler & Pressure Vessel Code, Section XI for Performance of Containment Repair & Replacement Activities Until 970909 ML20057F8441993-10-14014 October 1993 SER Granting Relief Giving Due Consideration to Burden Upon Licensee That Could Result If Requirements Imposed on Facility ML20057D6351993-09-28028 September 1993 SER Granting Relief as Requested for Both ISPT-2 & ISPT-3 Per 10CFR50.55a(a)(3)(i) & 10CFR50.55a(g)(6)(i) ML20057D5321993-09-28028 September 1993 SER Granting Licensee 921117 Relief Requests ISPT-2 & ISPT-3 Re Inservice Pressure Test Program ML20128K0221993-02-11011 February 1993 SE Accepting Util Justification for Break Exclusion of Main Steam Lines in Valve Vaults Provisionally Until End of Refueling Outages ML20128E9161993-01-0606 January 1993 SE Approving Request for Relief from ASME Requirements Re First 10-yr Interval ISI Plan ML20247K3321989-09-14014 September 1989 Safety Evaluation Accepting ATWS Mitigation Sys,Pending Tech Spec Issue Resolution ML20245E6951989-08-0303 August 1989 Safety Evaluation Supporting Inclusion of Alternate Repair Method to Detect microbiologically-induced Corrosion in Previously Granted Request for Relief from ASME Section XI Code Repair Requirements ML20247G8661989-07-21021 July 1989 Safety Evaluation Re Silicone Rubber Insulated Cables. Anaconda & Rockbestos Cables at Plant Environmentally Qualified for Intended Function at Plant & Use Acceptable for 40 Yrs ML20247B4891989-07-19019 July 1989 Safety Evaluation Supporting Util 890330 Request to Eliminate Dynamic Effects of Postulated Primary Loop Pipe Ruptures from Design Basis of Plant,Using leak-before- Break Technology as Permitted by Revised GDC 4 ML20246N0321989-07-11011 July 1989 Safety Evaluation Supporting Util Responses to Generic Ltr 83-28,Item 1.2, Post-Trip Review,Data & Info Capability ML20244D1771989-06-0909 June 1989 Safety Evaluation Re Generic Ltr 83-28,Items 2.1.1 & 2.1.2 NUREG-0612, Safety Evaluation Supporting Util Request to Delete Three Commitments in Response to NUREG-0612 Re Heavy Load Control on 5-ton Electric Monorail Hoist W/Integral Trolley & 4-ton Monorail Chain Hoist W/Geared Trolley1989-05-26026 May 1989 Safety Evaluation Supporting Util Request to Delete Three Commitments in Response to NUREG-0612 Re Heavy Load Control on 5-ton Electric Monorail Hoist W/Integral Trolley & 4-ton Monorail Chain Hoist W/Geared Trolley ML20245A1301989-04-14014 April 1989 Safety Evaluation Re Shutdown Margin.Procedural,Hardware & Training Enhancements Implemented & Committed to by Util Will Provide Reasonable Assurance That Adequate Shutdown Margin Will Be Maintained at Plant ML20244D8821989-03-14014 March 1989 Safety Evaluation Supporting Procedural,Hardware & Training Enhancements Implemented & Committed to by Util to Provide Reasonable Assurance That Adequate Shutdown Margin Will Be Maintained at Plants ML20195J0891988-11-28028 November 1988 Safety Evaluation Accepting Program for Plant in Response to Items 4.2.1 & 4.2.2 of Generic Ltr 83-28 Re Reactor Trip Sys Reliability ML20205T1621988-11-0707 November 1988 Safety Evaluation Supporting Improvement Plan for Emergency Diesel Generators Transient Voltage Response ML20206G5341988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 30114, Malfunction of Doors ML20206G4971988-11-0404 November 1988 SER Supporting Employee Concern Element Rept 23501, 480 Volt Power Receptacles Unsafe ML20206G3961988-11-0404 November 1988 SER Supporting Util Investigation of Employee Concerns as Described in Element Rept 308.03 ML20206G4571988-11-0404 November 1988 SER Supporting Employee Concern Element Rept Co 15105-SQN, Flex Hose Connections ML20206G4591988-11-0404 November 1988 SER Supporting Employee Concern Element Rept 204.7(B), Vendor Documents Legibility & Dissemination Sys ML20206G4621988-11-0404 November 1988 SER Supporting Employee Concern Element Rept 204.8(B), Communication & Interface Control ML20206G4661988-11-0404 November 1988 SER Supporting Employee Concern Element Rept EN 229.6(B), Lack of Valves in Sampling & Water Quality Sys ML20206G4721988-11-0404 November 1988 SER Supporting Employee Concern Element Rept 22912, Panel- to-Equipment Distances ML20206G4801988-11-0404 November 1988 SER Supporting Element Rept EN 232.2, Carbon Steel Vs Stainless Steel Drain Pipes ML20206G4531988-11-0404 November 1988 SER Supporting Employee Concern Element Rept Co 15101, Floor Drains ML20206G5291988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 301112, Sys 31 Not Operated Properly ML20206G5241988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 30111, Valve Closure ML20206G5191988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 30105, Questionable Design & Const Practices ML20206G5091988-11-0404 November 1988 SER Supporting Employee Concern Element Rept 23706, Gassing of Current Transformers ML20206G5021988-11-0404 November 1988 SER Supporting Employee Concern Element Rept 23504, Exposed HV Cable Routed W/O Raceway - Personnel Hazard ML20206G4861988-11-0404 November 1988 SER Supporting Employee Concern Element Rept EN 232.9(B), Freezing of Condensate Lines ML20206G5391988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 30204, Ground Detector Problem ML20206G5431988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 30301, Difficulty in Obtaining Obsolete Equipment ML20206G6111988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 31105, Alara ML20206G6161988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 31106, Health Physics Facilities,Clothing & Protective Equipment ML20206G6211988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 31204-SQN, Mgt & Personnel Issues ML20206G6321988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 31208-SQN, Security at Plant Entrances ML20206G6371988-11-0404 November 1988 SER Supporting Employee Concern Element Rept OP 31201-SQN, Adequacy of Public Safety Svc (Pss) Officer Uniforms in Nuclear Plant Environ ML20206G4351988-11-0404 November 1988 SER Supporting Employee Concern Element Rept Co 11101-SQN, Contact Between Dissimilar Metals ML20206G4381988-11-0404 November 1988 SER Supporting Employee Concern Element Rept Co 11202-SQN, Craft-Designed Hangers as Related to Const ML20206G4081988-11-0404 November 1988 SER Supporting Employee Concern Element Rept Co 10307-SQN, Uncoated Welds as Related to Const 1999-09-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J6311999-10-0101 October 1999 SER Accepting Request for Relief from ASME Boiler & Pressure Vessel Code,Section Xi,Requirements for Certain Inservice Insp at Plant,Unit 1 ML20217G3721999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Sequoyah Nuclear Plant.With ML20212F0831999-09-23023 September 1999 Safety Evaluation Granting Relief from Certain Weld Insp at Sequoyah Nuclear Plant,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(ii) for Second 10-year ISI Interval ML20212F4761999-09-23023 September 1999 Safety Evaluation Supporting Amends 246 & 237 to Licenses DPR-77 & DPR-79,respectively ML20212C4761999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Sequoyah Nuclear Plant.With ML20210L4361999-08-0202 August 1999 Cycle 9 12-Month SG Insp Rept ML20216E3781999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20210L4451999-07-31031 July 1999 Unit-2 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20210G6631999-07-28028 July 1999 Cycle 9 90-Day ISI Summary Rept ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20209H3831999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Sequoyah Nuclear Plant.With ML20211F9031999-06-30030 June 1999 Cycle 9 Refueling Outage ML20196J8521999-06-28028 June 1999 Safety Evaluation Authorizing Proposed Alternative to Use Iqis for Radiography Examinations as Provided for in ASME Section III,1992 Edition with 1993 Addenda,Pursuant to 10CFR50.55a(a)(3)(i) ML20195K2951999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20206Q8951999-05-0505 May 1999 Rev 0 to L36 990415 802, COLR for Sequoyah Unit 2 Cycle 10 ML20206R5031999-04-30030 April 1999 Monthly Operating Repts for April 1999 for Sequoyah Units 1 & 2.With ML20205P9811999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20204C3111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20205B6631999-02-28028 February 1999 Underground Storage Tank (Ust) Permanent Closure Rept, Sequoyah Nuclear Plant Security Backup DG Ust Sys ML20203H7381999-02-18018 February 1999 Safety Evaluation of Topical Rept BAW-2328, Blended U Lead Test Assembly Design Rept. Rept Acceptable Subj to Listed Conditions ML20211A2021999-01-31031 January 1999 Non-proprietary TR WCAP-15129, Depth-Based SG Tube Repair Criteria for Axial PWSCC Dented TSP Intersections ML20198S7301998-12-31031 December 1998 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20199G3641998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20197J5621998-12-0303 December 1998 Unit 1 Cycle 9 90-Day ISI Summary Rept ML20197K1161998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20195F8061998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Sequoyah Nuclear Plant.With ML20154H6091998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20154H6251998-09-17017 September 1998 Rev 0 to Sequoyah Nuclear Plant Unit 1 Cycle 10 Colr ML20153B0881998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Sequoyah Nuclear Plant.With ML20239A0631998-08-27027 August 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Sequoyah Nuclear Plant,Units 1 & 2 ML20236Y2091998-08-0707 August 1998 Safety Evaluation Accepting Relief Requests RP-03,RP-05, RP-07,RV-05 & RV-06 & Denying RV-07 & RV-08 ML20237B5221998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Snp ML20237A4411998-07-31031 July 1998 Blended Uranium Lead Test Assembly Design Rept ML20236P6441998-07-10010 July 1998 LER 98-S01-00:on 980610,failure of Safeguard Sys Occurred for Which Compensatory Measures Were Not Satisfied within Required Time Period.Caused by Inadequate Security Procedure.Licensee Revised Procedure MI-134 ML20236R0051998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Sequoyah Nuclear Plant ML20249A8981998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Sequoyah Nuclear Plant,Units 1 & 2 ML20247L5141998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Sequoyah Nuclear Plant ML20217K4471998-04-27027 April 1998 Safety Evaluation Supporting Requests for Relief 1-ISI-2 (Part 1),2-ISI-2 (Part 2),1-ISI-5,2-ISI-5,1-ISI-6,1-ISI-7, 2-ISI-7,ISPT-02,ISPT-04,ISPT-06,ISPT-07,ISPT-8,ISPT-01 & ISPT-05 ML20217E2221998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sequoyah Nuclear Plant ML20248L2611998-02-28028 February 1998 Monthly Operating Repts for Sequoyah Nuclear Plant,Units 1 & 2 ML20199J2571998-01-31031 January 1998 Cycle 9 Voltage-Based Repair Criteria 90-Day Rept ML20202J7911998-01-31031 January 1998 Monthly Operating Repts for Jan 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20199J2441998-01-29029 January 1998 Snp Unit 2 Cycle Refueling Outage Oct 1997 ML20199F8531998-01-13013 January 1998 ASME Section XI Inservice Insp Summary Rept for Snp Unit 2 Refueling Outage Cycle 8 ML20199A2931997-12-31031 December 1997 Revised Monthly Operating Rept for Dec 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20198M1481997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20197J1011997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20199C2951997-11-13013 November 1997 LER 97-S01-00:on 971017,vandalism of Electrical Cables Was Observed.Caused by Vandalism.Repaired Damaged Cables, Interviewed Personnel Having Potential for Being in Area at Time Damage Occurred & Walkdowns ML20199C7201997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Sequoyah Nuclear Plant L-97-215, SG Secondary Side Loose Object Safety Evaluation1997-10-23023 October 1997 SG Secondary Side Loose Object Safety Evaluation 1999-09-30
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ENCLOSVRE SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATfD TO THE JUSTIFICATION FOR CONTINUING OPERATION BY THE TENNESSEE VALLEY AUTHORITY SE0VOYAH NUCLEAR PLANT. UNITS 1 AND 2
. DOCKET NOS. 50-327 AND 50-328
1.0 BACKGROUND
By Licensee Event Report No. 50-327/92013, the Tennessee Valley Authority (TVA) reported a deficiency in the calculation by Westinghouse (W) of the mass and energy releases used to calculate the pressure which would be experienced in the main steam vaults at the Sequoyah Nuclear Plant, Units 1 and 2, as a result of a postulated main steam line break. These calculated releases were determined based on a non-conservative methodology, and TVA concluded that the pressure used in the safety design of these vaults was underestimated. W recommended that TVA use a methodology outlined in ANSI /ANS Standard 58.2, 1980 (Reference 2) to generate bounding mass and energy releases for vault pressurization calculation. The use of this methodology increased significantly the mass and energy releases, and thus also increased the pressures which the reinforced concrete walls and slabs of the valve vaults would experience, should a postulated main steam line break (MSLB) occur. TVA concluded that there would be inadequate design margin and that the structural integrity of the vaults could not be assured in such an event.
To prevent an immediate shutdown of the plant, TVA submitted to Region 11 a Justification for Continued Operation (JCO), which was submitted by letter dated November 30, 1992.
2.0 EVALVATION TVA has stated that an MSLB is the only applicable pipe-break design condition for verifying the structural integrity of the vaults. Based on the criteria specified in Standard Review Plan (SRP) Section 3.6.2, Branch Technical Position (BTP) MEB 3-1, " Postulated Rupture Locations In Fluid System Piping Inside And Outside Containment", for postulating pipe breaks in Class 2 piping, the only break which needs to be postulated is a double-ended guillotine break at the terminal end of the flued head anchor where the main steam piping exits the vaults. No intermediate breaks were required to be postulated at other locations, since the stress criteria of BTP MEB 3-1 were stated to be satisfied.
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1 Based on the geometry of the flued head anchor and the existing pipe restraint system, TVA determined that the resulting break size would be significantly smaller than a full guillotine break. For this break size it was found that the peak pressure in the vaults would be less than the current design values, However, the static pressure existing after the initial pressure peak was calculated to be higher than the current design values, which would affect the structural integrity of the vaults. TVA evaluated the consequences of the failure of the structural slabs and walls, and concluded that the intact main steam line could be damsged, resulting in the blow-down of a second steam generator, and/or that essential equipment or piping associated with the feedwater or auxiliary feedwater systems could also be damaged.
To justify continued operation, TVA invoked a provision of SRP Section 3.6.1, BTP ASB 3-1, " Protection Against Postulated Piping Failures In Fluid Systems Outside Containment", whereby certain pipe breaks may be excluded from design basis consideration, provided certain criteria are met. These criteria for pipe break exclusion are contained in BTP MEB 3-1, and are actually applicable to piping in containment penetration areas only. However, TVA stated that they could also be applicable to the main steam lines passing through the vaults since the design requirements are the same in both locations, s
TVA reviewed the pipe break exclusion criteria for Class 2 piping in containment penetrations, and demonstrated that all but one of these criteria are satisfied for the main steam lines passing through the vaults. This criterion consists of the requirement for 100% volumetric inservice
, examination of all pipe welds in the break exclusion area to be conducted during each inspection interval as defined in !WA-2400, ASME Section XI. TVA has stated that these inspections have not been performed for the pipe welds within the vaults; however, these welds were inspected during the original installation. In addition, selected welds have been inspected under the TVA ins 9rvice inspection program; welds inspected to-date have been found to be acceptable. However, these welds represent a small number of the total welds.
TVA has also estimated the erosion / corrosion rate of the main steam piping and components from the stearn generator nozzle to the flued head, using the EPRI program CHECMATE, and determined that it is acceptably low. On this basis, TVA has concluded that it meets the intent of BTP MEB 3-1 for the exclusion of breaks in the main steam valve vaults.
3.0 CONCLUSION
Based on the data submitted by TVA, the staff concludes that there is a very small likelihood that a double-ended guillotine break will occur at the flued heads in the main steam pipe vaults before the upcoming refueling outages at Units 1 and 2 (presently scheduled to start in April and August 1993, respectively). We, therefore, find the justification for break exclusion of the main steam lines in the valve vaults provisionally acceptable until the
i ._. . ..o i
_3 end of these refueling outages. To continue to implement the JC0 provisions beyond these refueling outages, the staff requires that TVA commit to satisfy all relevant break exclusion requirements of BlP MEB 3-1, including the requirement of 100% volumetric inservice inspection of all pipe welds, beginning with the upcoming refueling outages (unless the original design analysis criteria is re-established).
Principal Contributor: M. Hartzman Dated: February 11, 1993
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