ML20197J101

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Monthly Operating Repts for Nov 1997 for Sequoyah Nuclear Plant,Units 1 & 2
ML20197J101
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 11/30/1997
From: Hollomon T, Salas P
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9801020082
Download: ML20197J101 (10)


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Tenneoese Valley Authortty. Post offee Ekx 2000. SoetDasy, Tenrmsoe 37379m December 15, 1997 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Gentlemen:

In the Matter of ) Docket Nos. 50-327 Tennessee Valley Authority ) 50-328 SEQUOYAH NUCLEAA PLANT (SQN) - NOVEMBER 1997 HONTHLY OPERATING REPORT Enclosed is the November 1997 Monthly Operating Report as required by SON Technical Specification 6.9.1.10.

If you have any questions concerning this matter, please telephone me at (423) 843-7170 or J. D. Smith at (4?3) 843-6672.

Sincerely, Pedro Salas Licensing and Industry Affairs Manager Enclosure cc: See page 2

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9001020002 971130 PDR ADOCK 05000327 R PDR l

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U.S. Nuclear Regulatory Commission Page 2 December'15, 1997 1cc (Enclosure):

Mr.lR. W.:Hernan, Project Manager U.S.-~ Nuclear Regulatory Commission One White Flint, North-11555 Rockville Pike-Rockville, Maryland 20852-2739 i

INPO Records Center.

Institute of Nuclear Power Operat .ons-700 Galleria Parkway Atlanta, Georgia 30339-5947 Ms. Barbara Lewis, Assistant Editor, Database McGraw-Hill, Inc.

.1200.G Street, NW, Suite 1100-Washington, D.C. 20005 Mr. James'Lang, Manager-Advanced Reactor Department Electri.c-Power Research' Institute 3340 Hillview Avenue Palo Alto, California 94304

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.NRC Resident Inspector Sequoyah Nuclear Plant "2600 Igou Ferry Road Soddy-Daisy, Tennessee 37379-3624 Regi>nal Administrator

,U.S. Nuclear Regulatory Commission Region 17 Atlanta Federal Center 61 Forsyth St., SW, Suite 23T85 Atlanta, Georgia 30303-3415

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e 9 TENNESSEE VALLEY AUTHORITY sEQUOYAH NUCLTAR PLANT j

l MONTHLY OPERATING REPORT TO THE NUCLEAR REGULATORY CONNISSION NOVEMBER 1997 UNIT 1 DOCKET NUMBER 50-327 LICENSE NUMBER DPR-77 UNIT 2 DOCKET NUMBER 50-328 LICENSE NUMBER DPR-79 I

l OPERATIONAL StGGULRY.

NOVEMBER 1997 i i

UNIT 1 .

Unit 1 generated 854,189 megawatthours (MWh) (gross) electrical power i during November with a capacity factor of 102.7 percent. There were no l outages or power reductions of greater than 20 percent during November.  !

Unit 1 was operating at 100 percent power at the end of November.

UNIT 2 Unit 2 generated 661,925 MWh (gross) electrical power during November with a capacity factor of 79.6 percent. Unit 2 was in Mode 3 at the

-beginning of November and in procces of returning from the Unit 2 Cycle 8  !

refueling outage. On November 4 at 1158 Eastern Stardard Time (EST),

Unit 2 was tied online, ending the Unit 2 dycle 8 refueling outage. The outage was completed in 30.5 days. ,

On November 4 at 1502 EST, plant personnel identified a leak on a raw cooling water vent line on the main generator exciter cooler. Operations initiated actions to remove the turbine from the grid to facilitate repairs. Repairs to the vent line were completed and Unit 2 was tied online at 1924-EST. i On November 5 at 0415 EST, operations conducted a scheduled turbine  ;

overspeed test. Following completion of the overspeed test, Unit 2 was r tied online at 0539 EST that same day. Unit 2 was operating at 100 percent at the end of November.

SineULRY OF POWER-OPERATED RELIEF VALVES (PORVs)

AND SAFETY VALVES CRALLEUGES l

No PORVs or safety valves were challenged in November, L e l

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. . AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-327 tiNIT NO. One DATE: 12-04 97 COMPLETED IlY: T. J. Ilollomon TELEPilONE: (423) 843-7528 MONTil: NOVEMllER 1997 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe-Net) DAY (MWe Net)

I 1141 17 1155 2 1139 18 1154 3 1141 19 1158 4 1147 20 1156 5 1149 21 1154 6 1149 22 1156 7 1150 23 1155 8 1135 24 1154 9 1153 25 1155 10 1153 26 1157 11 1154 27 1156 12 1155 28 1155 13 1154 29 1155

'14 1153 30 1155 15 1156 31 NA 16 1156

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4 AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-328 UNIT No Two DATE: 12-04-97 COMPLETED llY: T. J. Ifollomon TELEPlIONE: (423) 843-7528 MONTil: NOVEMilER 1997 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER Ll! VEL DAY (MWe-Net) DAY (MWe Net) ,

1 0 17 1151 2 0 18 1150 3 0 19 1153 4 23 20 1151 5 209 21 1150 6 238 22 1151 7 474 23 1149 8 783 24 1149 9 861 25 ,

i150 10 1126 26 1151 11 1145 27 1151 12 1146 28 1150 13 1103 29 1150 14 1139 30 1150 15 1151 31 NA 16 1151

OPElt ATING DATA REPORT DOCKET NO.10 327 DATE 12/04/97 COhiPl.ETED IW T. J. llollomon TELEPilONE (423)843 7528 OPHitATINQSTATUS

1. Unit Name: Sequoyah Unit One
2. Reporting Period: November 1997 3.1.icensed Thermal Power (MWt): 3411.0
4. Nameplate Rating (Gross (hiWe): 1220.6
5. Design Electrical Rating (Net MWe): 1148.0
6. Maximum Dependable Capacity (Gross MWe): 1155.0
7. Maximum Dependable Capacity (Net MWe): 1117.0
8. If Changes Occur in Capacity Ratings (Item Numbers 3 Through 7) Since Last Report, Give Reasons:
9. Power 1.evel to Which Restricted,if Any (Net MWe): N/A
10. Reasons for Restrictions, if Any: _N/A This Month Yr.-to-Date Cumulative
11. Ilours in Reporting Period 720 8,016 143,929
12. Number ofIlours Reactor Was Critical 720.0 6,789.0 84,112
13. Reactor Reserve Shutdown llours 0 0 0

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14. Ilours Generator On l.ine 720.0 6,744.0 82.315.6
15. Unit Reserve Shutdown llours 0 0 0
16. Gross Thermal Energy Generated (MWh) 2.452.370.4 22.352.997.4 268,707,985
17. Gross Electrical Energy Generated (MWh) 854,189 7,723.595 91,515.735
18. Net Electrical Energy Generated (MWh) 828,933 7.464.363 87,842.001
19. Unit Service Factor 100.0 84.1 57.2
20. Unit Availability Factor 100.0 84.1 57.2
21. Un'.t Capacity Factor (Using MDC Net) 103.1 83.4 54.6
22. Unit Capacity Factor (Using DER Net) 100.3 81.1 53.2
23. Unit Forced Outage Rate 0.0 0.5 30.3
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
25. If Shut Down At End of Report Period, Estimated Date of Startup: ,

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OPERATING DATA REPORT jl DOCKETNO. 50 328 j DATE 12/04/97 COMPLETED BY T. J. Hollomon l TELEPHONE (423)843-7528  !

OPERATINO STATUS

1. Unit Name: Seauovah Unit Two - l
2. Reponing Period:- November 1997 i
3. Licensed Thermal Power (MWt): 3411.0 [

1220.6  :!

4. Nameplate Rating (Gross (MWe):

1148.0  ;

5. Design Electrical Rating (Net MWe):
6. Maximum Dependable Capacity (Gross MWe): = 1155.0 i 7.~ Maximum Dependable Capacity (Net MWe): _

1117.0 = .

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8. If Changes Occur in Capacity Ratings (Item Numbers 3 Through 7) Since Last Repon, Give Reasons:  !

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9. Power Level to Which Restricted,If Any (Net MWe): N/A  !
10. Reasons for Restrictions, if Any: N/A i

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i This Month Yr. to Date Cumulative i

11. llours in Reporting Period 720 8,016 135,889  !
12. Number ofIlours Reactor Was Csitical 661.5 7,309.5 86,911 ,
13. Reactor Reserve Shutdown llours 0 0 0 .

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14. Ilours Generator On-I.ine 630.3 7,258.0 84,930.5  !

- 15. Unit Reserve Shutdown Hours 0 0 0

16. Gross Thermal Energy Generated (MWh) 1,924,943.1 23,701,540.9 271,441,195 -
17. Gross Electrical Energy Generated (MWh) 661,925 8,145,083 92,344,140 18; Net Electrical Energy Generated (MWh) 637,453 7,868,667 88,548,386  !
19. Unit Sen' ice Factor 87.5 90.5 62.5
20. _ Unit Availability Factor 87.5 90.5 62.5 21p Unit Capacity Factor (Using MDC Net) 79.3 87.9 58.3-  :

-- 22. -_ Unit Capacity Factor (Using DER Net)- 77.1 85.5 56.8

23. Unit Forced Outage Rate 0.7 0.3 29.4 24.1 Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration _of Each):

1 25, if Shut Down At End of Report Period, Estimated Date of Startup: November 4,1997 f

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DOCKET NO.: 50-327 UNIT NAME: - One UNITSHU1 DOWNS AND POWER REDUCTIONS ' DATE: 129597 -

COMPLETED BY: T.1 W ,.

REPORTMONTH: NOVEMBER 1997 TELEPHONE: (423) 543-7528 No. Dese Type' Outage Reason

  • Method of Licensee System Component Cause and Comctive Achon to Ptevent Duracon Shutung Event Report Code' Code' - Recurrence (Hours) Doni No.

Reactor' There were no outages or power rh of reaser E than 20 percent in the average daily powerlevel durmg the M l

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. 'F: Forced - Reasorr ' Method *Edibit G-Instruccons ~

!" S: Scheduled - A-Equipmenn failure (Explain) 1-Manual for Preparanen of Data B-Mamtenance or Test -- 2 Manual Scram Enerv sheets for Licensee C-Refueling 3-Automanc Scram Event Report (LER) File

. D-Regulatory Restncuan 4-Continuanon of Exisung Outage (NUREG-1022)

E-Operator Training and License Exam 5-Reduction F-Administrative 9-Other ' Exhibit I- Same Source G-Operauonal Error (Explain)

H-Other(Explain) 3-r a .

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DOCKET NO.: '4-328 UNIT NAME- Two UNIT SHUTDOWNS AND POWER REDUCTIONS DATE- 120 W 7 -

COMPLETED BY: T.1 Holkwnon ,

REPORTMON~Ill NOVEMBER 1907 TELEPilONE: (423)343-7528 l

l No. Date lype' Outage Reason; Stethod of Licensee System i Compur,c.t Cause and Cvu u6t Action to Proent Duraten Shutting Event Code' Code' Recurrence (Hours) Down Report No. f R& l' C N/A he N/A On November 4 at 1I$8EST, Umt 2 was ned 6 971101 S 83.9 1 online ending the Unit 2 Cycle 8 refueling octage. Unit 2 was in Mode 1 at 100 percent power at the end of the month.

971104 F 4.4 A 5 N/A N/A NfA On November 4, plant giwr.i,cl identified a 7

raw water leak on a main generator exciter cooler vent line. Om&s removed the

' turbine from the grid to facilitate repairs.

The cause of the leak was fatigue. Repairs to the vent line were completed and the unit was returned to service.

On November 5. Operations conducted a 1.4 B 5 N '.". N/A N/A scheduled turbine overspeed test. I oilowing 8 971105 S completion of the test the unit was retumed to service.

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'F: Forced 2

Reason: ' Method " Exhibit G-Ins: ructions 5: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation ofData 3-Maintenance or Test 2-Manual Scram Entry sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restnction 4-Continuation of Existing Outage (NUREG-1022)

E-Operator Training and License Exam 5-Reduction F-Administrative 9-Other ' Exhibit I-Same Source G-Operational Error (Explain)

H-Other (Explain)

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