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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20084S9121977-03-25025 March 1977 Telecopy Ao:On 770324,containmet Spray Pump a Out of Svc During Training Startup,Violating Tech Spec ML20084S9091976-05-31031 May 1976 Ao:On 770527,HPCI Pressure Switches E41-PSH-NO12 A,B,C & D Exceeded Tech Spec Calibr Limits.Switches Immediately Recalibr ML20086D4211976-02-0909 February 1976 AO 50-261/76-3:on 760128,high Level Alarm Received on Safety Injection Accumulator B.Caused by Check Valve 875 Leaking Resulting in Dilution.Accumulator Partially Drained & Refilled ML20086D4421976-02-0202 February 1976 AO 50-261/76-2:on 760121 & 22,failure of One & Delayed Operation of Two Reactor Trip Relays Occurred.Caused by Open Coil Winding.Three Defective Relays Replaced ML20086D4271976-01-29029 January 1976 Telecopy Ao:On 760128,sample of Safety Injection Accumulator B Indicated Boron Concentration of 1,939 Ppm,Below Tech Specs.Accumulator Partially Drained,Refilled & Verified ML20086D4391976-01-22022 January 1976 Ao:On 760124 & 22,discovered That Reactor Trip Relay RT3 in Reactor Protection Logic Train a Operating Erratically. Further Investigation Revealed That Relays RT-4 & RT-8 on Logic Train B Defective.Relays Replaced ML20086D4471976-01-13013 January 1976 AO 50-261/76-1:on 760102,failure of Boric Acid Transfer Pump Resulted in Failure of One ESF Component That Caused or Threatened to Render Sys Incapable of Functioning.Caused by Damaged Rotor ML20086F5211976-01-0202 January 1976 Ao:On 760102,boric Acid Pump B Stopped Running.Caused by Defective Stator & Damaged Rear Bearing.Investigation Continuing NG-75-2222, AO 50-261/75-20:on 751210,channel 950 of Containment Pressure Protection Found Inoperable.Caused by Open Output Fuse in Comparator PC-950.Fuse Replaced1975-12-23023 December 1975 AO 50-261/75-20:on 751210,channel 950 of Containment Pressure Protection Found Inoperable.Caused by Open Output Fuse in Comparator PC-950.Fuse Replaced NG-75-2210, AO 50-261/75-19:on 751208,boron Concentration Found Below Limits in Safety Injection Accumulator B.Cause Not Stated. Accumulator Partially Drained & Refilled from Refueling Water Storage Tank1975-12-22022 December 1975 AO 50-261/75-19:on 751208,boron Concentration Found Below Limits in Safety Injection Accumulator B.Cause Not Stated. Accumulator Partially Drained & Refilled from Refueling Water Storage Tank ML20086F5161975-12-0808 December 1975 Ao:On 751208,boron Sample from Safety Injection Accumulator B Indicated 1,915 ppm,35 Ppm Below Tech Specs.Cause Unknown. Accumulator Partially Drained & Refilled from Refueling Water Storage Tank NG-75-2017, AO 50-261/75-18:on 751102,auxiliary Feedwater Pump a Failed to Start Following Safety Injection Signal.Caused by Tarnished Contacts.Contacts within Local/Remote Switch Cleaned.Further Investigation Underway1975-11-13013 November 1975 AO 50-261/75-18:on 751102,auxiliary Feedwater Pump a Failed to Start Following Safety Injection Signal.Caused by Tarnished Contacts.Contacts within Local/Remote Switch Cleaned.Further Investigation Underway NG-75-2010, AO 50-261/75-17:on 751101,both Containment Personnel Air Lock Doors Opened Simultaneously W/Rcs Temp Above 200 F, Violating Tech Spec 3.6.1.a.Caused by Broken Rod,Bearing & Cam Follower on Outer Door Mechanism1975-11-12012 November 1975 AO 50-261/75-17:on 751101,both Containment Personnel Air Lock Doors Opened Simultaneously W/Rcs Temp Above 200 F, Violating Tech Spec 3.6.1.a.Caused by Broken Rod,Bearing & Cam Follower on Outer Door Mechanism NG-75-2001, AO 50-261/75-16:on 751028,svc Water Booster Pump B Failed to Start.Caused by Actuation of Pump Suction Pressure Switches Provided to Protect Pumps from Low Npsh.Containment Recirculation Fans Stopped to Prevent Overheating Motors1975-11-11011 November 1975 AO 50-261/75-16:on 751028,svc Water Booster Pump B Failed to Start.Caused by Actuation of Pump Suction Pressure Switches Provided to Protect Pumps from Low Npsh.Containment Recirculation Fans Stopped to Prevent Overheating Motors ML20086F5291975-11-0404 November 1975 Ao:On 751102,motor Driven Auxiliary Feedwater Pump a Failed to Start.Remote Electrical Contacts Cleaned ML20086F5401975-11-0303 November 1975 Ao:On 751101,containment Integrity Broken for Approx 10 Minutes Due to Simultaneous Opening of Both Personnel Air Lock Doors ML20086F5491975-10-29029 October 1975 Ao:On 751028,sequence of Switch Operations Resulted in Breakers for Both Svc Water Booster Pumps a & B Tripping on Overload NG-75-1575, AO 50-261/75-15:on 750921,more than One Inoperable Rod Present W/Reactor at Power as Result of Rod Control Urgent Failure.Caused by Defective Fuse in Ac Power Supply to Rod Control Cabinet 1AC.Fuse Replaced1975-10-0101 October 1975 AO 50-261/75-15:on 750921,more than One Inoperable Rod Present W/Reactor at Power as Result of Rod Control Urgent Failure.Caused by Defective Fuse in Ac Power Supply to Rod Control Cabinet 1AC.Fuse Replaced ML20086F5611975-09-22022 September 1975 Ao:On 750921,urgent Failure Alarm Received.Caused by Phase Failure in Cabinet 1AC Which Rendered 12 Rods Inoperable. Reactor Manually Tripped NG-75-1212, Revised AO 50-261/75-11:on 750527,RCS Oxygen Concentration Found to Be 0.16 Ppm,Exceeding Limit.Caused by Inattention to Hydrogen Concentration & Dilution of RCS to Hot Shutdown Boron Concentration.Vol Control Tank Vented1975-08-0404 August 1975 Revised AO 50-261/75-11:on 750527,RCS Oxygen Concentration Found to Be 0.16 Ppm,Exceeding Limit.Caused by Inattention to Hydrogen Concentration & Dilution of RCS to Hot Shutdown Boron Concentration.Vol Control Tank Vented NG-75-1158, AO 50-261/75-14:on 750715,valve V2-14B Steam Driven Auxiliary Feedwater Pump Discharge to Steam Generator B Failed to Open.Caused by Belleville Spring Being Filled W/Grease.Belleville Spring Packs & Shafts to Be Inspected1975-07-25025 July 1975 AO 50-261/75-14:on 750715,valve V2-14B Steam Driven Auxiliary Feedwater Pump Discharge to Steam Generator B Failed to Open.Caused by Belleville Spring Being Filled W/Grease.Belleville Spring Packs & Shafts to Be Inspected ML20086F5961975-07-16016 July 1975 Telecopy Ao:On 750715,steam Drive Auxiliary Feedwater Pump Discharge Valve V2-14B to Steam Generator B Failed to Open Electrically ML20086F6151975-07-14014 July 1975 Ao:On 750711,control Rod L-5 Dropped,Causing Load Runback to Approx 70% Power.Caused by Defective Stationary Gripper Coil NG-75-1089, Revised AO 50-261/75-8:on 750429,RHR Suction Valve RHR-862A Failed.Caused by Torque Switch on Motor Operator Being Out of Adjustment,Causing Valve to Be Wedged Onto Seat & Preventing Motor from Opening Valve1975-07-11011 July 1975 Revised AO 50-261/75-8:on 750429,RHR Suction Valve RHR-862A Failed.Caused by Torque Switch on Motor Operator Being Out of Adjustment,Causing Valve to Be Wedged Onto Seat & Preventing Motor from Opening Valve NG-75-1044, AO 50-261/75-12:on 750625,boric Acid Transfer Pump a Failed. Caused by Pump Shaft Being Broken at Keyway.Pump Rebuilt & Reinstalled.New Pump Model GVH-10K Will Be Installed Upon Receipt1975-07-10010 July 1975 AO 50-261/75-12:on 750625,boric Acid Transfer Pump a Failed. Caused by Pump Shaft Being Broken at Keyway.Pump Rebuilt & Reinstalled.New Pump Model GVH-10K Will Be Installed Upon Receipt ML20086F6081975-06-26026 June 1975 Telecopy Ao:On 750625,boric Acid Transfer Pump a Noted Off. Caused by Pump Shaft Being Broken at Keyway.Also on 750625, Employee Received Whole Body Dose of 3,080 Mrem for Quarter Ending 750630 ML20086F6741975-06-12012 June 1975 Revised AO 50-261/75-9:on 750501,reactor Coolant Pump Seal Failed,Resulting in Discharge of Reactor Coolant Fluid to Containment Floor.Caused by Pump Running W/Seal Leaking. Seals,Shaft,Impeller & Hearings Replaced ML20086F6201975-06-0606 June 1975 AO 50-261/75-11:on 750527,RCS Oxygen Concentration Noted to Be 0.16 Ppm,Exceeding Limit.Caused by Mixture of Hydrogen & Nitrogen in Vol Control Tank,Limiting Hydrogen to Rcs.Vol Control Tank Vented ML20086F6271975-06-0202 June 1975 AO 50-261/75-10:on 750521,boric Acid Transfer Pump B Failed.Caused by Shaft Being Broken at Keyway & Worn Pump Bearing.Pump Rebuilt ML20086F6231975-05-27027 May 1975 Ao:On 750527,RCS Sample Indicated 0.16 Ppm Oxygen,Exceeding Tech Specs.No Cause Stated.Concentration Reduced ML20086F6301975-05-21021 May 1975 Ao:On 750521,boric Acid Pump B Stopped.Caused by Broken Shaft in Keyway Area ML20086F5791975-05-12012 May 1975 AO 50-261/75-9:on 750501,reactor Coolant Pump Seal Failed, Resulting in Discharge of Reactor Coolant Fluid to Containment Floor.New Seal & Associated Parts Being Installed.Parts Shall Be Certified ML20086F6441975-05-0909 May 1975 AO 50-261/75-8:on 750429,RHR Pump Suction Valve RHR-862A Failed.Caused by Torque Switch on SMB-O Motor Operator Being Out of Adjustment.Torque Switch Adjusted.On 750430,complete Insp of Operator Found Excess Grease.Grease Removed ML20086F6911975-05-0202 May 1975 Telecopy Ao:On 750501,seal 1 on Reactor Coolant Pump C Failed,Producing Leak to Containment Floor.Seal 2 Failed on 750502.Cooldown Initiated.Rcs Depressurized & Drained to Below Pump Seals ML20086F6471975-04-29029 April 1975 Ao:On 750429,valve RHR-862A Failed to Open from RTGB When RHR Sys Being Aligned.Cause Under Investigation.Valve Opened Locally Using Manual Operator & All Flow Paths Restored ML20086F6981975-04-10010 April 1975 AO 50-261/75-7:on 750331,diesel B Tripped Due to Low Lube Oil Pressure.Caused by Lube Oil Filter High Differential Pressure Resulting from Dirty Filters.Lube Oil Filters Replaced ML20086F6961975-04-0101 April 1975 Telecopy Ao:On 750331,emergency Diesel B Tripped.Caused by Low Lube Oil Pressure.Filters Changed & Unit Returned to Svc ML20086F6991975-03-27027 March 1975 AO 50-261/75-6:on 750314,contractor Personnel Exposed to Radiation in Excess of Limits.Caused by Exceeding Stay Time in Localized Field of High radiation.Chem-Nuclear,Inc & Util Investigating Use of Addl Shielding ML20086F7001975-03-0707 March 1975 AO 50-261/75-5:on 750225 & 26,boric Acid Transfer Pump B Failed.Cause Not Identified.Pump Replaced ML20086F7011975-02-14014 February 1975 AO 50-261/75-4:on 750206,reactor Protection Overpower Channel Set I Failed to Generate Rod Stop Signal for Simulated Overpower Condition.Caused by Failure of Comparator Circuit in Dual Circuit Signal Comparator ML20086F7051975-02-0707 February 1975 Ao:On 750206,signal Comparator TO-412B Failed to Operate. Portion of Comparator Which Generates Rod Stop & Turbine Runback Signal Failed While Overpower Reactor Trip Signal Still Generated ML20086F7111975-02-0606 February 1975 AO 50-261/75-3:on 750126,component Cooling Water Pump C Tripped Due to Overcurrent.Caused by Backleakage Through Pump Discharge Side Check Valve Due to Debris.Leaking Mechanical Seal & Status Light Module Replaced ML20086F7201975-01-30030 January 1975 AO 50-261/75-2:on 750120,pressurizer Level Channel II Failed to Generate Reactor Trip Signal or Safety Injection Signal Upon Insertion of Simulated High & Low Levels.Caused by Malfunctioning Filter Capacitor C.3 ML20086F7281975-01-27027 January 1975 AO 50-261/75-1:on 750114,boric Acid Transfer Pump a Failed. Caused by Failed Shaft in Vicinity of Impeller Keyway.Pump Replaced.Replacement Pump Model GVH-10K on Order ML20086F7141975-01-27027 January 1975 Telecopy Ao:On 750126,component Cooling Pump C Failed to Start from Rtgb.Cause Under Investigation.Pump Breaker Racked Out,Inspected & Racked in ML20086F7241975-01-20020 January 1975 Telecopy Ao:On 750120,level Comparator LC-460A Failed to Operate.Cause Not Stated ML20086F7351975-01-15015 January 1975 Ao:On 750114,boric Acid Transfer Pump a Noted to Be in Off Indication at Rtgb.Caused by Broken Shaft ML20085D0621973-07-17017 July 1973 Ao:On 730628-0705 & 09-10,changes Performed on Safeguards Equipment W/O Demonstrating Operability of Redundant Equipment Before Removal.Safety Injection Pumps B & C Tripped & Circuit Breaker Tripped,Respectively ML20085D0661973-07-11011 July 1973 Telecopy Ao:On 730709,two Safety Injection Pumps Experienced Overcurrent Trips.Caused by New Overcurrent Trip Devices Tripping at Lower than Desired Value.Trip Setting Increased ML20085D0771973-07-10010 July 1973 Telecopy Ao:On 730710,circuit Breaker for Containment Cooler Fan 2 Tripped.Caused by Overcurrent Due to Misalignment of Calibr Spring in Overcurrent Trip Device.Spring Realigned 1977-03-25
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers RA-97-0258, LER 97-S12-00:on 971119,discovered Uncompensated Security Zone.Caused by Inattention to Detail by Members of Security Force.Provided Event Info to Security Shift Personnel & Changed Practice Re Zone Review1997-12-19019 December 1997 LER 97-S12-00:on 971119,discovered Uncompensated Security Zone.Caused by Inattention to Detail by Members of Security Force.Provided Event Info to Security Shift Personnel & Changed Practice Re Zone Review ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML20217Q2751997-06-30030 June 1997 CP&L Fitness for Duty Program Performance Data for Period 970101-0630 ML14183A6951995-09-18018 September 1995 Safety Evaluation Approving Relocation of Technical Support Ctr ML20059H7721994-01-17017 January 1994 Part 21 Rept Re Virginia Power Notifying Fairbands Morse Via Failure Analysis Rept NESML-Q-058 of Defective Air Start Distributor cam,16104412 ML17352A8691993-05-31031 May 1993 Technical Rept, Assessment of Aging Degradation of Civil/ Structural Features at Selected Operating Nuclear Power Plants. ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML20079H1571991-09-30030 September 1991 Nonproprietary Evaluation of Revised Transfer to Cold Leg Recirculation Procedure,Hb Robinson Unit 2 ML20086T2951991-06-14014 June 1991 Rev 1 to EQ Documentation Package Eqdp 36.0, Boston Insulated Wire Cable ML20086T2861991-03-0808 March 1991 Rev 1 to EQ Documentation Package Eqdp 11.1, Dekoron Instrumentation Cables ML20086T2561991-03-0808 March 1991 Rev 1 to EQ Documentation Package 10.0, Continental Shielded Instrument Cable ML20065K6961990-10-31031 October 1990 Mechanical Licensing Rept for Hb Robinson High Thermal Performance Fuel Assemblies ML20065K6971990-10-31031 October 1990 Thermal Hydraulic Compatibility Analysis of Anf High Thermal Performance Fuel for Hb Robinson,Unit 2 ML20005G6831990-01-0505 January 1990 Part 21 Rept Re Installation Instructions for Grommet Use Range for Patel Conduit Seal P/N 841206.Conduit Seals in Environ Qualification Applications Inspected for Proper Wire Use Range & Grommets Replaced ML20247E0701989-07-20020 July 1989 Info Rept:On 890717-0804,fire Penetration Seals Will Be Removed from Svc to Allow Access for Ventilation Sys Mod. Addl Fire Barrier Penetrations Will Be Made in Wall Between RHR Pump Pit & Fuel Handling Bldg,Per Tech Spec 3.14.7.2 ML20246E9111989-03-31031 March 1989 PDC-3:Advanced Nuclear Fuels Corp Power Distribution Control for PWRs & Application of PDC-3 to Hb Robinson Unit 2 ML20245H0821989-01-25025 January 1989 Criticality Safety Analysis of Hb Robinson Spent Fuel Pool W/4.2% Nominal Enrichment Fuel Assemblies ML20205T0551988-10-31031 October 1988 Responses to NRC Questions on RTD Bypass Elimination Licensing Rept ML20147E2371988-02-29029 February 1988 1987 Annual Rept - Primary Coolant Iodine Spikes ML20147B1971987-12-31031 December 1987 1987 Annual Rept - Primary Safety & Relief Valve Challenges ML20236K7731987-10-31031 October 1987 Monthly Operating Rept for Oct 1987 ML20235W3781987-09-30030 September 1987 Monthly Operating Rept for Sept 1987 ML20238E2741987-08-31031 August 1987 Monthly Operating Rept for Aug 1987 ML20235H3151987-06-30030 June 1987 Monthly Operating Rept for June 1987 ML17261A5301987-06-18018 June 1987 Part 21 Rept Re Potential Util Failure to Comply W/Component Containment Isolation Licensing Commitment If Proposed Mods to Component Cooling Water Sys Instituted.Utils Advised to Evaluate Containment Isolation Sys ML20214W3241987-05-31031 May 1987 Monthly Operating Rept for May 1987 ML20214R5101987-04-30030 April 1987 Rev 1 to Monthly Operating Rept for Apr 1987,correcting Operation Statistics & Shutdown Experience Due to Mathematical Errors ML20215L4941987-04-30030 April 1987 Monthly Operating Rept for Apr 1987 ML20206F3561987-03-31031 March 1987 Monthly Operating Rept for Mar 1987 ML20210B4141987-03-31031 March 1987 Revised Monthly Operating Rept for Mar 1987 ML20205F6021987-03-23023 March 1987 Special Rept:On 870302,noble Gas Effluent Monitor for Main Steam Line B Declared Inoperable & Svc Not Returned Until 870312.Caused by Defective Detector.Detector Replaced.High Voltage for Detector Adjusted & Sys Operation Checked ML20212P3101987-02-28028 February 1987 Monthly Operating Rept for Feb 1987 ML20214Q7891987-01-31031 January 1987 Cycle 12,SAR ML20210R6341987-01-31031 January 1987 Monthly Operating Rept for Jan 1987 ML20207M2451986-12-31031 December 1986 Monthly Operating Rept for Dec 1986 L-18-120, Rev 0 to Supplemental Info in Support of Conservatisms in Criticality Analysis Performed for Hb Robinson Isfsi1986-12-18018 December 1986 Rev 0 to Supplemental Info in Support of Conservatisms in Criticality Analysis Performed for Hb Robinson Isfsi ML20215C7911986-11-30030 November 1986 Monthly Operating Rept for Nov 1986 ML20213F3121986-10-31031 October 1986 Monthly Operating Rept for Oct 1986 ML20215G1081986-09-30030 September 1986 Monthly Operating Rept for Sept 1986 ML20215F0361986-09-29029 September 1986 Special Rept:On 860902,during Cold Shutdown,Pressurizer PORV Lifted Twice to Prevent Overpressurization.Caused by Inadvertent Action by Unit Operators.Operations Personnel Counseled Re Importance of Breaker Position Indicators ML20211C0641986-09-0909 September 1986 Rev 0 to Final Rept Criticality Safety Analysis Hb Robinson Spent Fuel Storage Racks (Unpoisoned,Low Density) W/4.2% Enriched 15x15 Fuel Assemblies ML20211C0491986-09-0202 September 1986 Rev 0 to Final Rept Criticality Safety Analysis Hb Robinson New Fuel Storage Vault W/4.2% Enriched 15x15 Fuel Assemblies ML20212F5321986-07-31031 July 1986 Monthly Operating Rept for Jul 1986 ML20203D0221986-07-14014 July 1986 Part 21 Rept Re Air Monitoring Sys Probes Exhibiting Blue Tip Rather than Normal White Tip & Insensitive to Chlorine. Caused by Improper Handling/Storage.Advisory Bulletin Encl. Item Not Reportable Per Part 21 ML20202G3371986-06-30030 June 1986 Monthly Operating Rept for June 1986 ML20211B5601986-05-31031 May 1986 Monthly Operating Rept for May 1986 ML20197D2651986-04-30030 April 1986 Monthly Operating Rept for Apr 1986 1999-09-22
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' ~/~ o GP&L 0 Carolina Power & Light Company oM liay 12, 1975 Files NG-3513 (R) , Serial: NO-75-701 fir. Noru:an C. Moseley, Director Directorate of Regulatory Operations U. S. Nuclear Regulatory Cou:=ission )
Region II, Suite 818 230 Peachtree Strcot, N. W.
Atlanta, Georgia 30303
Dear Mr. Moseley:
H. B. ROBINSON UNIT NO. 2 LICENSE NO. DPR-23 FAILURE OP "C" REACTOR COOLANT PU'IP STAL SYSTEM In accordance with 6.6.2.a of the Technical Specifications for H. B. Robinson Unit No. 2, the attached Abnormal Occurrence Report is sub-mitted for your infor=ation. This report fulfills the requirement for a written report within ten days of an Abnormal Occurrence and is in accordanca with the format set forth in Regulatory Guideline 1.16.
Yours vary truly, p/: 'gg E E. Utley ' {
Vice-President Bulk Power Supply DBW jwk Attachment cet Messrs. N. B. Bessac P. W. Howe R. E. Jone D. Knuth -
J. B. McGirt D. B. Waters b%GA bg, i ,
840103041605000261 gDRADOCK 751030 PDR
1 -
- O O Abnormal occurrence Report L
- 1. Report Number 50-261/75-9 i
! 2a. Report Date May 9, 1975 2b. Occurrence Date May 1, 1975
- 3. Facility H. B. Robinson Unit No. 2 Hartsville, South Carolina 29550
- 4. Identification of Occurrence Failure of reactor coolant pump (RCP) seal resulting in discharge of reactor coolant fluid to containment floor.
- 5. Conditions Prior to Occurrence t
The reactor was operating at full power. All systems were normal.
Dilution of the primary coolant boron concentration was in progress l
to compensate for the buildup of Xenon. The plant had just reached full power operation early in the morning on May 1, 1975 following a maintenance outage.
! 6. Description of Occurrence I During dilution of primary coolant boron concentration, No. 1 seal leakoff from "C" pump flow responded sensitively to all additions.
This sensitivity had existed since its replacement earlier during the week. Since the leakoff was within the prescribed limits and the variations in flow were gradual instead of " spiking", it was considered satisfactory to operate with this seal.
The dilution was still in process when the following events transpired:
}
May 1, 1975:
"C" Reactor Coolant Pump leakoff " spiked" several times. The 1
1750 pump was monitored for vibrations and found to be normal.
1811 "C" RCP seal leakoff oscillated full range several times and then stabilized high with a seal flow greater than 6 gpm. A l
load reduction was commenced at a rate of 10% per minute so that "C" pump could be idled as per plant operating procedures.
1817 - Load reduction was stopped at 36% power.
1818 "C" RCP was deenergized.
1819 - Reactor trip occurred due to turbine trip on high level in "B" steam generator. Level instabilities created from the rapid load reduction'and initiation of Automatic Steam Dump induced
- the high level.
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- l 1832 - Component cooling water valve 626 closed due to high flow from 1
the reactor coolant pump thermal barrier. This was caused by 4
sudden steam formation in the thermal barrier created when the .
I pump seal failed open. The open seal allowed hot (540'F) primary j coolant to flow upward through the thermal barrier.
i Stopped "A" and "B" Reactor Coolant Pumps. It was the. Shift j Foreman's decision to stop "A" and "B" RCP's when flashing of
! primary coolant in the seal water return line threatened to
- cause loss of seal flow due to the pressure surges. The flashing of primary coolant was created by the high flow rate i of coolant through the No. 1 seal of "C" RCP, Valve 303C, leak-I off isolation from "C" RCP, was not closed prior to stopping j RCP's "A" and "B".
1841 - Received automatic letdown isolation due to low level in the-
- pressurizer. Supply to charging pump suction changed from '
volume control tank (VCT) to refueling water storage tank l (RWST).
l l 1854 - Pressurizer level returned above letdown isolation setpoint. -
Returned charging pump suction to VCT. ,' f I
1915 - Closed valve 303C to decrease pressure surges in letdown 11ne. '
! Seal flow was lost on "A" RCP. N i 1928 - Seal flow was lost *on "B" RCP. Opened valve WD-1708 to relieve l pressure in Reactor Coolant Drain Tank (RCDT). Pressure build- [
up was due to leakage through No. 2 seal of:"C" RCP. WD-1708 ;
- allows drainage of RCDT to containment sump.
c.
i 1942 - First entry following seal failure was made into containment..
Purpose of the entry was to observe "C" RCP and.to close valve
, CCW-728C, "C" pump thermal barrier outlet manual isolation valve. The control panel-operated valve CCW-303C had not fully
- isolated the leakoff and was still causing steam formation in j the thermal barrier. It was not possible to enter "C" RCP bay due to steam escaping from No. 3 seal.' It was previously thought that the thermal barrier on "C" RCP had failed, but
, with no increase on R-17, Component Cooling Water Radiation' Monitor, and the high flow through No.1 seal it was determined -
that steam formation in the thermal _ barrier had caused surges'
- in the-outlet line.- The surges in flow ~ caused automatic closure of CCW-626, which isolated all three RCP thermal' barriers.' . ,
1945 ' Valve CCW-626 was manually blocked-open. 'ThisLallowed cooling water to flow through the thermal barriers thus reducing tempera-tures below the boiling point in "C RCP. ~After temperatures were reduced CCW-626 was unblocked and returned to normal operation 4 l in the open position.. >
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l
- O O 1950 - Containment inspection complete. No breaches in primary system other than steam from "C" pump observed. All personnel exited containment and entrance locked.
2000 - Breakers were pulled on containment sump pumps to prevent overfilling of waste holdup tank. Water was originating from reactor coolant drain tank and floor drains in "C" RCP bay.
2007 - Personnel entered Containment to take air samples and noted no ,
steam or leakage from RCP'c. Primary system apparently tight.
2013 - Started "B" RCP bearing oil lif t pump in an attempt to lower shaft, provide more seal clearance and re-establish seal flow.
2015 - Stopped "B" RCP bearing oil lift pump. Failed to establish seal flow through No. 1 seal.
2026 - Personnel exited Containment.
2110 - An entry was made into containment to manually rotate "A" and "B" RCP's in an effort to re-establish seal flow. No inspections of "C" pump was performed during this entry.
2206 - Personnel exited-containment. Failed to establish seal flow through No. 1 seEl's.'
~
2215 - The Operating Supervisor called Westinghouse project engineer and notified him that seal flows on "A" and "B" Reactor Coolant Pumps were lost, and that "C" pump's No. 1 seal had opened. It was decided that coola6t pump operation was desirable for proper
,' i mixing of boron in pr'epiaration for cooldown. Also a more con-
' - trolled cooldiwn would be possible with pump operation. Westing-house addsed that "C" pump could be operated with No.1 seal
- leakoff isolgted as long as No. 2 seal remained intact.
N 2242 '- Started "E' icP.
2257 - Prepared foe cooldown by use of main condenser.
e e, 2308 - Blocked valve CCW-626 open to prevent possible loss of thermal barrier cColing, water. _
r L*.
~
2310 - Increased ~ seal whter injection flow to RCP "C" by a factor of 5 l to prevent possible overhcating of pump bearing.
L 2316 - Receiv'ed control' panel indication of 0.5 ft. ofLwater in con-i tainment cump not later than 2316 hours0.0268 days <br />0.643 hours <br />0.00383 weeks <br />8.81238e-4 months <br />.
2330 -Reactor Coolant System boron concentration was 1038 ppm which is-approximately cold shutdown concentration.
' 0015 - High Standpipe Alarm on "C" pump was received. Stopped "C"
~
reactor coolant pump. . Pressurizer level started falling rapidly
(- , due to failure of No. 2.and No. 3 seals of "C" RCP,.'
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i 0016 - Started "A" safety injection (SI) pump to supplement charging pump. Deliberately opened valves SI-866A and SI-866B, hot leg safety inj ection to loops "B" and "C". Lowest level reached in pressurizer was 6% on level indicator LI-462 (cold calibration) .
Strip chart indication reached zero and remained there for about 10 minutes.
0018 - Started "B" and "C" safety injection pumps. Pressurizer level decrease stopped.
0035 - Opened valve CVC-307, seal water bypass, in an attempt to reduce a source of the loss of primary coolant to containment.
0036 - Diverted charging flow from the cold leg of loop "B" to auxiliary pressurizer spray (opened valve CVC-311) to reduce Reactor Coolant System pressure, (1150 psig at this time).
The pressurizer steam void was rapidly collapsed by the auxiliary spray and pressure dropped accordingly. It was necessary to use auxiliary spray since normal spray was lost when the coolant pumps were stopped.
0039 - Stopped "C" S.I. pump due to rising pressurizer level. The safety injection pumps and valve CVC-311 were used during the remainder of the cooldown to control pressurizer level and
, pressure.
0043 - Started HVH Unit No. 4, (containment recirculation fan and cooler) to r' educe " containment pressure and temperature. Prior to startup of the fourth unit, three inRI units were in operation.
0048 - The S.I. accumulators partially discharged their volumes into the primary system. The discharge isolation valves were closed at this time to terminate this injection phase.
0100 - Reactor coolant system boron concentration at 1521 ppm.
Containment internal pressure reached a maximum of'3 psig.
0145 - Opened condenser vacuum breaker in preparation to terminate cooldown through the main condenser.
l' 0151 - Started "D" Service Water Pump and "B" Service Water Booster Pump (cooling water to HVH units) to aid in the reduction of containment pressure and temperature.
0215 - Shut main steam isolation valves. Cooldown through the main condenser was terminated.
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l 0223 - Started "A" component cooling water pump _in preparation to go on residual heat removal system. (RHR).
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l 0230 - Started' operating RHR pumps one at a time and opened valves 744A l and 744B (discharge valves) and 750 and 751 (suction valves) to
, warmup RHR system. Pressure in the primary system was approxi-
'i mately 400 psig. Proceeded with plant cooldown as per General Operating Procedure GT-lD.
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.' O O 0330 - Reactor coolant system boron concentration at 1861 ppm.
0341 - Residual Heat Removal System in service. Cooldown proceeding as per GP-lD.
0440 - Stopped using S.I. system to assist maintaining pressurizer level.
0448 - Reactor coolant system at cold shutdown, (less than 200'F).
0517 - Commenced decreasing primary system pressure from 100 psig to O psig.
0629 - Entry into containment was made for purpose of inspection.
Contained air supply packs, (Scott Air Packs), were used during entry. The bottom floor of containment was flooded to a height of 8 to 10 inches. Recovery phase initiated at this time.
1000 - Reactor Coolant System drained below +50" with respect to the vessel flange at which point the leak stopped. The containment floor was flooded to a height of 12.5 inches. The containment temperature vas 100*F and 0 psig with 132,500 gallons of water in the containment. The reactor coolant system boron concen-tration was 1694 ppm.
- 7. Designation of Apparent Cause of Occurrence The failure of the reactor coolant pump seal system created the occurrence.
This is classified as an abnormal occurrence under. Technical Specification-1.8.e, abnormal degradation of one of the several boundaries designed to contain the radioactive materials resulting from the fission process.
This seal system consists of three seal surfaces - No. 1 seal is the point of primary pressure drop, No. 2 seal maintains back pressure on No. 1 and diverts seal leakoff from No. 1 seal to the volume control-tank, and No. 3 seal helps maintain standpipe backpressure on No. 2 seal. Both No. 1 and No. 2 seals are designed to maintain system pressure.
- 8. Analysis of Occurrence The occurrence resulted in no offsite releases or exposures. At no time was there any danger to the personnel involved. Due to the seal failure, overheating of the pump shaf t _and seal housing occurred._ This will necessitate the replacement of the. seals and housing, pump shaft,-and associated equipment.
During the' transient, there was no reversal in coolant flow and the core remained covered. Maximum temperature reached at the core exit was approximately 550*F shortly after the trip. About the time that cold shutdown conditions were reached,- it was determined that another steam bubble existed in the RCS. To reduce the leak rate it was desirable ~to reduce system pressure. This was attempted by cpening valve 311 (auxiliary spray) to collapse the pressurizer bubble. When valve 311
. was opened the RCS pressure did not drop noticeably, but _the pressurizer
. level increased rapidly (more rapidly than charging 'and SI would: raise ?it).
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v l When valve 311 was shut, pressurizer level decreased rapidly as the bubble reformed in the pressurizer. Core thermocouple temperatures showed the reactor temperature to be stable and later when the reactor head vent was opened, little gas or steam escaped. The second bubble probably existed in the steam generator tubes. Due to loss of RCS circulation and the limited steam that had been drawn during the cool-down, none after placing RHR in service, the steam generators remained relatively hot. When pressure in the system was reduced from 400 psig to 100 psig, a bubble could have formed in one or more steam generators.
Proper operation of safeguards equipment and actions taken by the control ,
operators prevented more extensive damage after the seal failure. All systems functioned as designed during the transient and the expected results were achieved.
Apparently pressure surges and high seal leakoff temperatures damaged the No. 2 seal of "C" RCP.
As a result of this incident several other abnormal occurrences took place which were a direct result of the original problem. The primary leakage exceeded those limits given in Section 3.1.5 of the Technical Specifications. This is classified as an Abnormal Occurrence under specification 1.8.b, violation of a limiting condition for operation established in the Technical Specifications. As the leak increased in magnitude the containment pressure, (3 psig at maximum) exceeded 2 psig internal pressure, which is a violation of specification 3.6.2.
This is also classified as an abnormal occurrence under specification 1.8.b. As a result of the subsequent forced cooldown, excessive cool-down rates were experienced, resulting in a violation of Sec. 3.1.2 of the Technical Specifications.
- 9. Corrective Action Plant cooldown was initiated as soon as conditions permitted. When No. 2 and No. 3 seals failed, operations personnel started depressurizing as fast as conditions would allow in order to reduce the coolant loss through the seal. Safeguards equipment was used as needed in order to maintain the reactor in a safe condition. Proper operating and emer-gency procedures were used to reduce pressure and temperature to cold shutdown conditions.
To prevent reoccurrence of this situation, new seal and associated parts are being installed under the direction of pump vendor representatives and CP&L job coordinators. All parts being installed shall be certified and necessary quality assurance documentation and control maintained.
Since this was the first major incident involving a sizable loss of coolant at H. B. Robinson, the special procedures used to gain control over the transient will be reviewed to determine if any areas warrant revision.
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- l 10. Failure Data i . No previous seal failures that resulted in loss of primary coolant to l containment free space have occurred at H. B. Robinson. The following
{ data concerns the affected reactor coolant pump and aeal:
l Controlled Leakage Seal Reactor Coolant Pump - Model V11001-B1 4
No. 1 seal assembly --Identification No. 856C877G01 No. 2 seal ring - Identification No. 856C904G01 No. 3 seal ring - Identification No. 910D670G01 1
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