ML20069L921

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Monthly Operating Rept for May 1994 for Calvert Cliffs Nuclear Power Plant Units 1 & 2
ML20069L921
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 05/31/1994
From: Piazza F
BALTIMORE GAS & ELECTRIC CO.
To:
Shared Package
ML20069L915 List:
References
NUDOCS 9406210007
Download: ML20069L921 (12)


Text

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UNIT 1 OPERATING DATA REPORT oc**************************************************************************

Docket No. 50-317 June 15, 1994 Prepared by Frank Piazza Telephone:(410)260-3821 OPERATING STATUS

1. UNIT NAME Calvert Cliffs Unit 1
2. REPORTING PERIOD MAY 1994
3. LICENSED THERMAL POWER (MWT) 2700
4. NAMEPLATE RATING (GROSS MWe) 918
5. DESIGN ELECTRICAL RATING (NET MWe) 845
6. MAXIMUM DEPENDABLE CAP'Y (GROSS MWe) 860
7. MAXIMUM DEPENDABLE CAP'Y (NET MWe) 830
8. CHANGE IN CAPACITY RATINGS NONE
9. POWER LEVEL TO WHICH RESTRICTED N/A
10. REASONS FOR RESTRICTIONS N/A Cumulative This month Year-to-Date to Date
11. HOURS IN REPORTING PERIOD 744 3,623 167,124
12. NUMBER OF HOURS REACTOR WAS CRITICAL 376.5 1,111.1 118,080.1
13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 3,019.4
14. HOURS GENERATOR ON LINE 173.5 894.2 115,472.6
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
16. GROSS THERMAL ENERGY GENERATED (MWH) 245,853 2,149,584 292,464,403
17. GROSS ELECTRICAL ENERGY GEN'TED(MWH) 77,584 715,077 97,188,623
18. NET ELECTRICAL ENERGY GENERATED (MWH) 71,120 681,585 92,485,867
19. UNIT SERVICE FACTOR 23.3 24.7 69.1
20. UNIT AVAILABILITY FACTOR 23.3 24.7 69.1
21. UNIT CAPACITY FACTOR (USING MDC NET) 11.5 22.7 67.1
22. UNIT CAPACITY FACTOR (USING DER NET) 11.3 22.3 65.5
23. UNIT FORCED OUTAGE RATE 41.9 27.7 8.9
24. SHUTDOWNS SCHEDULED OVER THE NEXT SIX MONTHS (TYPE, DATE AND DURATION):

N/A

25. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF START-UP:

June 5, 1994 9406210007 940613 PDR i

ADOCK 05000317 PDR i 1

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKT_:T NO. 50-317 UNIT NAhiE Calvert Cliffs-U1 DATE June 15. IMt CONtPLETED BY Frank Piana TELEPHONE (410)260-3821 REPORT 310NTil Stav 1994 j htEDIOD OF SIIUTriNG LICENSEE CAUSE & CORRECTIVE DURADON DOWN EVENT SYSTEh! CONtPONENT ACHON TO -

NO. DATE TYPEI (IIOURS) REASON 2 REACTOR 3 REPORT # CODE-8 CODES PREVENT RECURRENCE

( 94-02 940209 S 430.3 C 4 N/A N/A N/A Unit shutdown for planned Refueling Outage.

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! 94 03 940520 S 15.1 B 9 N/A JJ 12 Unit removed from grid for hiain Turbine over-l speed trip test. During an attempt to paral!el to the grid a ground was detected. The ground was due to electrical short on a bus. The problem was correct-l ed and the unit was paralleied at 1700 on 5/2094.

j 94-(M 940526 F 16.5 B 5 N/A TA TRB Power was reduced on 5/26,94 at 1615 to correct high dbrations in the #8 hiain Turbine Bearing.

Installation of a balance shot was completed at approximately 1057 on hiay 27,1994.

94 05 940527 F 108.6 A 1 N/A TA TRB During power escalation after balancing the #8 bearing, excessive temperature indications from the

  1. 7 hiain Turbine Bearing was noted due to a bad bearing. The unit was manually shut down and remained off the grid to repair the #7 bearing.

There was a loss of oil pressure from the bearing lift pump due to a missing oil plug in the oil manifold which caused the bearing to fail. The bearing was repaired and returned to service.

I F: Forced 2 Reason: 3 h1ethod: 4 IEEE Standard 805-1984 S: Scheduled A - Equipment Failure 1 - h1anual B - h1aintenance or Test 2 - h1anual Scram. e 5

C - Refueling 3 - Automatic Scram. IEEE Standard 803A-1983 D - Regulatory Restriction 4 - Continued E - Operator Training & License Examination 5 - Reduced Load F- Administrative 9 - Other G - Operational Error H - Other

AVERAGE DAILY UNIT POWER LEVEL co**********************************************************************

Docket No. 50-317 Calvert Cliffs Unit No. 1 June 15, 1994 Prepared by Frank Piazza Telephone: (410) 260-3821 MAY 1994 Average Daily Power Level Average Daily Power Level Day (MWe-Net) Day (MWe-Net) 1 0 17 0 2 0 18 0 3 0 19 136 4 0 20 66 5 0 21 352 6 0 22 475 7 0 23 522 8 0 24 518 9 0 25 519 10 0 26 376 11 0 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0 31 0 16 0

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DOCKET NO. 50-317 i CAINEllT CLIFFS UNIT I June 15,1934 SUMMAllY OF OPEllATING EXPEltlENCE May 1994 i

The unit began the month shutdown because of the continued refueling outage. The refueling i outage ended May 18, IV>4 when the unit was paralleled to the grid at 2215. The unit was removed  !

from the grid on May 20, IV)4 at 0150 for Main Turbine testing. After completion of the Main Turbine testing and during paralleling to the grid procedure, there was an electrical ground detected. l The ground was corrected at 1600 on May 20, IV>4. The unit was again paralleled to the grid on May  ;

20,1994 at 1700.  !

i At 1856 on May 26, IV14 the unit was again removed from the grid to allow for installation of a halance shot in Main Bearing #8. During start.up procedures, Main Turhine llearing #7 experienced high ternperature and the unit was shutdown to repair the bearing.

The unit ended the month in a shut-down condition in mode 5.

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June 6,1994 NFM 94-163 Page 2 of 3 f1EFUELING INFORMATION RE_ QUEST

1. Name of facility: Calvert Cliffs Nuclear Power Plant, Unit No.1.
2. Scheduled date for next refueling shutdown: March,1996*.
3. Scheduled date for restart following refueling: May,1996.*
4. Will refueling or resumption of operation thereafter require a Technical Specification I change or other license amendment?

l None identified at this time.*

5. Scheduled date(s) for submitting proposed licensing action and supporting information.  ;

1 Unknown.

6. Important licensing considerations associated with the refueling.

None identified at this time.

7. Tho number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool.

(a) 217 (b) 1514 (Note 2) l Spent fuel pools are common to Units 1 and 2. l

8. (a) The present licensed spent fuel pool storage capacity, and (b) the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies.

(a) 4710 (Note 1) (b) 0

9. The projected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity and maintaining space for one full core off-load. i l

March 2014 l

NOTE 1: 4710 total licensed site storage capacity.

(1830 pool + 2880 ISFSI)

NOTE 2: 72 Spent Fuel Assemblies in the ISFSI.

Entry has changed since last reported.

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UNIT 2 OPERATING DATA REPORT l

  • o************************************************************************** l Docket No. 50-318 June 15, 1994 Prepared by Frank Piazza Telephone:(410)260-3821 OPERATING STATUS
1. UNIT NAME Calvert Cliffs Unit 2
2. REPORTING PERIOD MAY 1994
3. LICENSED THERMAL POWER (MWT) 2700
4. NAMEPLATE RATING (GROSS MWe) 911
5. DESIGN ELECTRICAL RATING (NET MWe) 845
6. MAXIMUM DEPENDABLE CAP'Y (GROSS MWe) 860
7. MAXIMUM DEPENDABLE CAP'Y (NET MWe) 830
8. CHANGE IN CAPACITY RATINGS NONE
9. POWER LEVEL TO WHICH RESTRICTED N/A
10. REASONS FOR RESTRICTIONS N/A Cumulative This month Year-to-Date to Date
11. HOURS IN REPORTING PERIOD 744 3,623 150,479
12. NUMBER OF llOURS REACTOR WAS CRITICAL 596.9 3,303.1 109,339.9
13. REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 1,296.6
14. HOURS GENERATOR ON LINE 595.2 3,298.2 107,821.8
15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
16. GROSS THERMAL ENERGY GENERATED (MWH) 1,495,495 8,724,505 275,590,048
17. GROSS ELECTRICAL ENERGY GEN'TED(MWH) 502,324 2,936,689 91,092,558
18. NET ELECTRICAL ENERGY GENERATED (MWH) 481,309 2,820,636 87,063,770
19. UNIT SERVICE FACTOR 80.0 91.0 71.7
20. UNIT AVAILABILITY FACTOR 80.0 91.0 71.7
21. UNIT CAPACITY FACTOR (USING MDC NET) 77.9 93.8 70.1
22. UNIT CAPACITY FACTOR (USING DER NET) 76.6 92.1 68.5
23. UNIT FORCED OUTAGE RATE 0.0 5.1 5.7
24. SHUTDOWNS SCHEDULED OVER THE NEXT SIX MONTHS (TYPE, DATE AND DURATION):

N/A ,

25. IF UNIT IS SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF START-UP:

N/A t

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UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-318 .

UNITNAME Calvert Cliffs-U2 DATE June 15.1994 COMPLETED BY Frank Piana TELEPHONE (410) 260-3821 REPORTMONTil Ma51994 MErilOD OF SIIUTIING LICENSEE CAUSE & CORRECTIVE ,

DURATION DOWN EVENT SYSTEM COMPONENT ACTION TO NO. DATE T(PEI (IIOURS) REASON 2 REACf0R3 REPORT # CODE 4 CODES PREVENT RECURRENCE 94-03 940515 S 148.8 B 1 N/A N/A N/A Unit shutdown for planned outage to complete Surveillance tests. The unit was returned to power on May 22 at 2217.

944M 940523 F 0 B 5 N/A SJ P Unit power was reduced for maintenance on 21 Steam Generator Feed Pump. The Steam Generator Feed Pump was experiencing speed oscillations caused by contaminated actuation / lube oit The problem was corrected by disassembling and cleaning the actuator. A portable lube oil purifier was placed in the lube oil system to further clean the oil f

l 1 F: Forced 2 Reason: 3 Method: 4 IEEE Standard 805-1984 S: Scheduled A- Equipment Failure 1 - Manual B - Maintenance or Test 2 - Manual Scram.

C - Refueling 3 - Automatic Scram. 5 IEEE Standard 803A-1983 D - Regulatory Restriction 4 - Continued E - Operator Training & License Examination 5 - Reduced Imad F- Administrative 9 - Other G - Operational Error H - Other

AVERAGE DAILY UNIT POWER LEVEL co**********************************************************************

Docket No. 50-318 Calvert Cliffs Unit No. 2 June 15, 1994 Prepared by Frank Piazza Telephone: (410) 260-3821 MAY 1994 Average Daily Power Level Average Daily Power Level Day (MWe-Net) Day (MWe-Net) 1 866 17 0 2 864 18 0 3 865 19 0 4 867 20 0 5 868 21 0 6 865 22 0 7 864 23 689 8 866 24 539 9 871 25 785 10 868 26 857 11 850 27 859 12 850 28 860 13 871 29 862 14 867 30 863 15 775 31 862 16 0 1

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4 DOCKET NO. 50-318 CAINERT CLIFFS - UNIT 2 June 15,1994

SUMMARY

OF OPERATING EXPERIENCE May 1994 The unit began the month at 100% Reactor power (850 MWe).

On May 15,1994 commenced reducing Reactor power for a planned outage to complete Surveillance Test Procedures. The unit was removed from the grid on May 15,1994 at 2130. After completion of the Surveillance Tests, the unit was started and paralleled to the grid on May 22,1994 at 2217.

On May 23,1994 reduced Reactor power to 65% to perform maintenance on 21 Steam Generator Feed pump. Following completion of the Steam Generator Feed Pump maintenance Reactor power was increased, reaching 100% power at 1340 on May 25,1994.

The unit continued to operate the remainder of the month at 100% Reactor power.

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June 6,1994 NFM 94163 Page 3 of 3 B_EFUELING INFORM ATION REQUEST

1. Name of facility: Calvert Cliffs Nuclear Power Plant, Unit No. 2
2. Scheduled date for next refueling shutdown: February 18,1995,
3. Scheduled date for restart following refueling: May 3,1995.
4. Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?

Unknown.

5. Scheduled date(s) for submitting proposed licensing action and supporting information.

Unknown.

6. Important licensing considerations associated with the refueling.

None identified at this time.

7. The number of fuel assemblics (a) in the core and (b) in the spent fuel storage pool.

(a) 217 (b) 1514 (Note 2) ,

Spent fuel pools are common to Units 1 and 2.

8. (a) The present licensed spent fuel pool storage capacity, and (b) the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies.

(a) 4710 (Note 1) (b) 0

9. The projected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity and maintaining space for one full core off-load.

March 2016.

NOTE 1: 4710 total licensed site storage capacity.

(1830 pool + 2880 ISFSI)

NOTE 2: 72 Spent Fuel Assemblies in the ISFSI.