LER 93-009-01:on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification EffortML20044F132 |
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Site: |
South Texas |
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Issue date: |
05/20/1993 |
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From: |
Pinzon J HOUSTON LIGHTING & POWER CO. |
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To: |
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Shared Package |
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ML20044F112 |
List: |
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References |
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LER-93-009, LER-93-9, NUDOCS 9305260483 |
Download: ML20044F132 (5) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6321994-05-0202 May 1994 LER 94-002-01:on 940115,centrifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to Requirements of TS 3.1.2.3.Caused by hydro-pneumatic Transient.Valves Labeled W/Caution statements.W/940502 Ltr ML20029D6351994-04-27027 April 1994 LER 94-006-01:on 940214,reactor Manually Tripped Following Unanticipated Test Results.Caused by Mod Which Failed post- Mod Test.Test Terminated & Solid State Rod Control Sys Returned to Original Design configuration.W/940427 Ltr ML20029C6951994-04-18018 April 1994 LER 94-011-00:on 940310,safety Injection Actuation Was Received on Trains A,B & C.Cause Was Failure to Adhere to Procedure.Corrective Actions:Restored Cooling Shutdown & Removed Personnel from watchbill.W/940418 Ltr ML17352B2581994-03-25025 March 1994 LER 94-007-00:on 940224,station Procedure for Testing Reactor Trip Bypass Breakers Did Not Satisfy Ts.Caused by Inadequate Procedure Preparation & Review.Surveillance Procedure Enhancement Program underway.W/940325 Ltr ML20046C5471993-08-0606 August 1993 LER 93-018-00:on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST plan.W/930806 Ltr ML20046C4901993-08-0505 August 1993 LER 93-019-00:on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing discrepancy.W/930805 Ltr ML20046B1291993-07-29029 July 1993 LER 93-012-00:on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel cooling.W/930729 Ltr ML20046A6791993-07-21021 July 1993 LER 93-011-00:on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway ML20046A6511993-07-20020 July 1993 LER 93-017-01:on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified ML20045J0281993-07-15015 July 1993 LER 93-016-01:on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 QDPS.W/930715 Ltr ML20045H9171993-07-14014 July 1993 LER 93-008-01:on 930505,discovered That RHR Pump Suction MOV Had Not Been Environ Qualified Since 901129 Because Replacement of Drain T Not Completed.Drain T Missing from RH-0060B Replaced & Bulletin Issued to Maint Dept ML20045H9881993-07-13013 July 1993 LER 93-012-01:on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings. W/930713 Ltr ML20045E1531993-06-25025 June 1993 LER 93-017-00:on 930527,determined That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioner & Solenoids Remained in Svc Beyond Qualified Life.Caused by Incorrect Interpretation of Design Documents.Mod Underway ML20045E1491993-06-25025 June 1993 LER 93-010-00:on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint initiated.W/930625 Ltr ML20045B2731993-06-0909 June 1993 LER-93-016-00:on 930503,TS Violation Occured Due to Circuitry for SG PORVs & RCS Subcooling Monitor Being Inoperable.Caused by Less than Adequate Work Practices. Screws Missings from Qdps Replaced & Walkdown Performed ML20045A3831993-06-0404 June 1993 LER 93-008-00:on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain ML20044G4301993-05-25025 May 1993 LER 93-009-00:on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref values.W/930525 Ltr ML20044F6281993-05-21021 May 1993 LER 93-015-00:on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans monitored.W/930521 Ltr ML20044F1321993-05-20020 May 1993 LER 93-009-01:on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort ML20044E0371993-05-14014 May 1993 LER 93-005-01:on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training ML20024H2571991-05-24024 May 1991 LER 91-014-00:on 910420,erratic Containment Extended Range Pressure Channel Output Occurred.Caused by Bad Control Card. Weekly Channel Checks Performed,Control Card Replaced & Channel calibrated.W/910524 Ltr ML20024H2081991-05-22022 May 1991 LER 91-015-00:on 910422,train C AFW Pump Inadvertently Started Due to Failure of Led in Sequencer Test Circuitry. Faulty Led Replaced & Blocking Circuit Satisfactorily tested.W/910522 Ltr ML20029C1221991-03-15015 March 1991 LER 91-004-00:on 910215,loss of Offsite Power Actuation Occurred During Routine Maint.Caused by Lack of Attention to Work Performance Methods.Training Conducted for Maintenance personnel.W/910315 Ltr ML20029B0421991-02-25025 February 1991 LER 91-002-00:on 910126,automatic Actuation of Safety Injection Sys Occurred in One of Three Train C Trains.Caused by Inadequate Work Instructions for Maint Activity.Training Bulletin Issued & Supervisors counseled.W/910225 Ltr ML20024F7451990-12-12012 December 1990 LER 90-017-00:on 901104,discovered That Train a of Class IE 120-volt Distribution Panel DP001 Energized from Alternate Power Supply.Caused by Less than Adequate Administrative Controls.Log Will Be utilized.W/901212 Ltr ML20044B1691990-07-0606 July 1990 LER 90-011-00:on 900612,chemical Technician Supervisor Discovered That No Sample Collected in Condenser Air Removal Sys Radiation Monitor Moisture Collection Tank. Caused by Inadequate procedure.W/900706 Ltr ML20043G2091990-06-14014 June 1990 LER 90-010-00:on 900515,determined That Leak & Contamination Test Interval for Some Radioactive Sources Exceeded Tech Specs.Caused by Insufficient Detail in Procedures.Test Program revised.W/900614 Ltr ML20043G5191990-06-14014 June 1990 LER 90-010-00:on 900515,unplanned Actuation of ESF Train C Standby Diesel Generator Occurred.Caused by Personnel Error. Training Bulletin Will Be Issued to Maint Personnel Re event.W/900613 Ltr ML20043G1791990-06-13013 June 1990 LER 90-009-00:on 900512,incorrect Wiring in Solid State Protection Sys Discovered.Caused by Inadvertent Installation of Extra Wire by Mfg.Extra Wire Removed & Sys Successfully tested.W/900613 Ltr ML20043G2101990-06-13013 June 1990 LER 90-009-00:on 900514,discovered That Printer for Toxic Gas Analyzer XE-9325 Was Not Updating & Surveillances for Toxic Gas Monitor XE-9325 Incorrectly Performed on 900511. Caused by Inadequate training.W/900613 Ltr ML20043G7681990-06-0808 June 1990 LER 90-008-00:on 900508,Tech Spec Required Shutdown Initiated Due to Primary Coolant Sys Leakage.Caused by High Cycle Fatigue Failure of Weld on Upstream Side of Drain Valve.Drain Valves replaced.W/900608 Ltr ML20043E7001990-06-0404 June 1990 LER 90-008-00:on 891007,Tech Spec Violation Occurred Due to Failure to Perform post-maint Testing.Caused by Incorrect Determination That No post-maint Testing Required.Personnel counseled.W/900604 Ltr ML20043C7401990-05-30030 May 1990 LER 90-007-00:on 900430,discovered That All Three Trains of ESFAS Placed in Test & Incapable of Actuating for Approx 35 Minutes.Caused by Inadequate Prerequisite Conditions in Maint Procedure.Procedure Being modified.W/900530 Ltr ML20043C4791990-05-29029 May 1990 LER 90-007-00:on 900426,standby Diesel Generator 22 Room High Sump Level Alarm Actuated in Control Room.Caused by Flooding & Inadequate Spec of Sealing & Testing Requirements.Seals on Removable Panels caulked.W/900529 Ltr ML20043B6611990-05-25025 May 1990 LER 90-006-00:on 900426,control Room Ventilation Sys Actuated to Recirculation Mode Due to High Level Trip of Vinyl Acetate Channel on Gas Analyzer.Caused by Failure of electro-mechanical Positioner.Part replaced.W/900525 Ltr ML20043A7811990-05-15015 May 1990 LER 90-005-00:on 900414,simultaneous Reactor & Turbine Trip Occurred Due to Failure of Main Turbine Electrohydraulic Control Line.Caused by Fatigue Stress of Weld.Valve Modified to Add anti-swirl Baffles & anti-rotation pins.W/900515 Ltr ML20042F2191990-05-0202 May 1990 LER 90-005-00:on 900329,feedwater Booster Pump 11 Tripped Upon Actuation of Ground Fault Relay & Standby Pump 13 Started But Did Not Deliver Sufficient Flow to Prevent Trip. Cause Not Found.Inlet Filters to Be cleaned.W/900502 Ltr ML20042E3561990-04-0505 April 1990 LER 89-015-01:on 890704,reactor Trip Occurred.Caused by Failure of Relay in Generator Breaker Trip Circuit.Relays in Generator Breaker Trip Circuits Replaced W/Correct Models & Checked to Ensure Proper rating.W/900405 Ltr ML20012C7211990-03-16016 March 1990 LER 90-003-00:on 900214,discovered That Train B Fuel Handling Bldg Exhaust Air Filter Outlet Damper Would Not Open.Caused by Wiring Error Due to Failure of Technicians to Follow Work Instructions.Technicians counseled.W/900316 Ltr ML20012B4381990-03-0101 March 1990 LER 90-002-00:on 900202,Train s Reactor Trip Breaker Opened, Initiating Turbine & Reactor Trip & Feedwater Isolation on Low Average RCS Temp.Cause Unknown.Universal Logic Cards Replaced & Monitoring Instruments installed.W/900301 Ltr ML20006E3781990-02-16016 February 1990 LER 90-001-00:on 900103,containment Ventilation Isolation Occurred Due to Loss of Power to Radiation Monitor Actuation Relay.Caused by Technician Lifting Power Lead. Technicians Trained & counseled.W/900216 Ltr ML20006E4001990-02-12012 February 1990 LER 90-001-00:on 900108,Train s Low Steam Line Pressure Blocking Switch Placed in Blocked Position,Causing Actuation of Safety Injection & ESF Sys.Caused by Lack of Instructions.Training Program modified.W/900212 Ltr ML20006D4231990-02-0202 February 1990 LER 90-002-00:on 900103,redundant Solenoid Valve Which Actuates Train C Feedwater Valve Failed.Caused by Excessive Particulate Buildup.Solenoids Cleaned & Hydraulic Oil Flushed & Filtered to Remove particulate.W/900202 Ltr ML20006D5591990-02-0202 February 1990 LER 89-023-01:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Declared Inoperable. Caused by Contact Oxidation & Low Contact Pressure.Chiller Auxiliary Relay Cleaned & adjusted.W/900202 Ltr ML20006B4731990-01-25025 January 1990 LER 89-024-00:on 891226,required Sample from Safety Injection Accumulator 1C of Boron Concentration Not Taken. Caused by Insufficient Administrative Controls to Track Surveillance Tests.Bulletin Will Be issued.W/900125 Ltr ML20006B2551990-01-19019 January 1990 LER 89-022-00:on 891205,discovered That ASME Section XI Pressure Test of Train C of Component Cooling Water Sys Not Performed Prior to Returning Sys to Svc.Sys Inoperable from 890909-1206.Test Control Procedures revised.W/900119 Ltr ML20006B2221990-01-16016 January 1990 LER 89-023-00:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Attempt to Secure Essential Chiller 12C Resulted in Trip.Caused by Failure of Voltage Regulator.Regulator Returned to mfg.W/900116 Ltr ML20005E2471989-12-29029 December 1989 LER 89-028-00:on 891130,control Room Ventilation Sys Actuated to Recirculation Mode as Result of Spurious Signal. Caused by Memory Error Causing Microprocessor to Energize Relay Incorrectly.Troubleshooting planned.W/891229 Ltr ML19332D7741989-11-24024 November 1989 LER 89-018-01:on 890922,discovered That Const Installation Procedure for Reg Guide 1.97,Rev 2 Instrumentation Did Not Include Details to Ensure Qualification Per 10CFR50.49 or IEEE 323-1974.Caused by Installation error.W/891124 Ltr ML19332C8661989-11-21021 November 1989 LER 89-027-00:on 891025,discovered That Closed Limit Switch on Main Turbine Throttle Valve 2 Disconnected.Caused by Failure of Limit Switch Linkage.Review to Be Performed of Limit Switch Linkage design.W/891122 Ltr 1994-05-02
[Table view] Category:RO)
MONTHYEARML20029D6321994-05-0202 May 1994 LER 94-002-01:on 940115,centrifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to Requirements of TS 3.1.2.3.Caused by hydro-pneumatic Transient.Valves Labeled W/Caution statements.W/940502 Ltr ML20029D6351994-04-27027 April 1994 LER 94-006-01:on 940214,reactor Manually Tripped Following Unanticipated Test Results.Caused by Mod Which Failed post- Mod Test.Test Terminated & Solid State Rod Control Sys Returned to Original Design configuration.W/940427 Ltr ML20029C6951994-04-18018 April 1994 LER 94-011-00:on 940310,safety Injection Actuation Was Received on Trains A,B & C.Cause Was Failure to Adhere to Procedure.Corrective Actions:Restored Cooling Shutdown & Removed Personnel from watchbill.W/940418 Ltr ML17352B2581994-03-25025 March 1994 LER 94-007-00:on 940224,station Procedure for Testing Reactor Trip Bypass Breakers Did Not Satisfy Ts.Caused by Inadequate Procedure Preparation & Review.Surveillance Procedure Enhancement Program underway.W/940325 Ltr ML20046C5471993-08-0606 August 1993 LER 93-018-00:on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST plan.W/930806 Ltr ML20046C4901993-08-0505 August 1993 LER 93-019-00:on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing discrepancy.W/930805 Ltr ML20046B1291993-07-29029 July 1993 LER 93-012-00:on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel cooling.W/930729 Ltr ML20046A6791993-07-21021 July 1993 LER 93-011-00:on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway ML20046A6511993-07-20020 July 1993 LER 93-017-01:on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified ML20045J0281993-07-15015 July 1993 LER 93-016-01:on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 QDPS.W/930715 Ltr ML20045H9171993-07-14014 July 1993 LER 93-008-01:on 930505,discovered That RHR Pump Suction MOV Had Not Been Environ Qualified Since 901129 Because Replacement of Drain T Not Completed.Drain T Missing from RH-0060B Replaced & Bulletin Issued to Maint Dept ML20045H9881993-07-13013 July 1993 LER 93-012-01:on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings. W/930713 Ltr ML20045E1531993-06-25025 June 1993 LER 93-017-00:on 930527,determined That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioner & Solenoids Remained in Svc Beyond Qualified Life.Caused by Incorrect Interpretation of Design Documents.Mod Underway ML20045E1491993-06-25025 June 1993 LER 93-010-00:on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint initiated.W/930625 Ltr ML20045B2731993-06-0909 June 1993 LER-93-016-00:on 930503,TS Violation Occured Due to Circuitry for SG PORVs & RCS Subcooling Monitor Being Inoperable.Caused by Less than Adequate Work Practices. Screws Missings from Qdps Replaced & Walkdown Performed ML20045A3831993-06-0404 June 1993 LER 93-008-00:on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain ML20044G4301993-05-25025 May 1993 LER 93-009-00:on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref values.W/930525 Ltr ML20044F6281993-05-21021 May 1993 LER 93-015-00:on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans monitored.W/930521 Ltr ML20044F1321993-05-20020 May 1993 LER 93-009-01:on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort ML20044E0371993-05-14014 May 1993 LER 93-005-01:on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training ML20024H2571991-05-24024 May 1991 LER 91-014-00:on 910420,erratic Containment Extended Range Pressure Channel Output Occurred.Caused by Bad Control Card. Weekly Channel Checks Performed,Control Card Replaced & Channel calibrated.W/910524 Ltr ML20024H2081991-05-22022 May 1991 LER 91-015-00:on 910422,train C AFW Pump Inadvertently Started Due to Failure of Led in Sequencer Test Circuitry. Faulty Led Replaced & Blocking Circuit Satisfactorily tested.W/910522 Ltr ML20029C1221991-03-15015 March 1991 LER 91-004-00:on 910215,loss of Offsite Power Actuation Occurred During Routine Maint.Caused by Lack of Attention to Work Performance Methods.Training Conducted for Maintenance personnel.W/910315 Ltr ML20029B0421991-02-25025 February 1991 LER 91-002-00:on 910126,automatic Actuation of Safety Injection Sys Occurred in One of Three Train C Trains.Caused by Inadequate Work Instructions for Maint Activity.Training Bulletin Issued & Supervisors counseled.W/910225 Ltr ML20024F7451990-12-12012 December 1990 LER 90-017-00:on 901104,discovered That Train a of Class IE 120-volt Distribution Panel DP001 Energized from Alternate Power Supply.Caused by Less than Adequate Administrative Controls.Log Will Be utilized.W/901212 Ltr ML20044B1691990-07-0606 July 1990 LER 90-011-00:on 900612,chemical Technician Supervisor Discovered That No Sample Collected in Condenser Air Removal Sys Radiation Monitor Moisture Collection Tank. Caused by Inadequate procedure.W/900706 Ltr ML20043G2091990-06-14014 June 1990 LER 90-010-00:on 900515,determined That Leak & Contamination Test Interval for Some Radioactive Sources Exceeded Tech Specs.Caused by Insufficient Detail in Procedures.Test Program revised.W/900614 Ltr ML20043G5191990-06-14014 June 1990 LER 90-010-00:on 900515,unplanned Actuation of ESF Train C Standby Diesel Generator Occurred.Caused by Personnel Error. Training Bulletin Will Be Issued to Maint Personnel Re event.W/900613 Ltr ML20043G1791990-06-13013 June 1990 LER 90-009-00:on 900512,incorrect Wiring in Solid State Protection Sys Discovered.Caused by Inadvertent Installation of Extra Wire by Mfg.Extra Wire Removed & Sys Successfully tested.W/900613 Ltr ML20043G2101990-06-13013 June 1990 LER 90-009-00:on 900514,discovered That Printer for Toxic Gas Analyzer XE-9325 Was Not Updating & Surveillances for Toxic Gas Monitor XE-9325 Incorrectly Performed on 900511. Caused by Inadequate training.W/900613 Ltr ML20043G7681990-06-0808 June 1990 LER 90-008-00:on 900508,Tech Spec Required Shutdown Initiated Due to Primary Coolant Sys Leakage.Caused by High Cycle Fatigue Failure of Weld on Upstream Side of Drain Valve.Drain Valves replaced.W/900608 Ltr ML20043E7001990-06-0404 June 1990 LER 90-008-00:on 891007,Tech Spec Violation Occurred Due to Failure to Perform post-maint Testing.Caused by Incorrect Determination That No post-maint Testing Required.Personnel counseled.W/900604 Ltr ML20043C7401990-05-30030 May 1990 LER 90-007-00:on 900430,discovered That All Three Trains of ESFAS Placed in Test & Incapable of Actuating for Approx 35 Minutes.Caused by Inadequate Prerequisite Conditions in Maint Procedure.Procedure Being modified.W/900530 Ltr ML20043C4791990-05-29029 May 1990 LER 90-007-00:on 900426,standby Diesel Generator 22 Room High Sump Level Alarm Actuated in Control Room.Caused by Flooding & Inadequate Spec of Sealing & Testing Requirements.Seals on Removable Panels caulked.W/900529 Ltr ML20043B6611990-05-25025 May 1990 LER 90-006-00:on 900426,control Room Ventilation Sys Actuated to Recirculation Mode Due to High Level Trip of Vinyl Acetate Channel on Gas Analyzer.Caused by Failure of electro-mechanical Positioner.Part replaced.W/900525 Ltr ML20043A7811990-05-15015 May 1990 LER 90-005-00:on 900414,simultaneous Reactor & Turbine Trip Occurred Due to Failure of Main Turbine Electrohydraulic Control Line.Caused by Fatigue Stress of Weld.Valve Modified to Add anti-swirl Baffles & anti-rotation pins.W/900515 Ltr ML20042F2191990-05-0202 May 1990 LER 90-005-00:on 900329,feedwater Booster Pump 11 Tripped Upon Actuation of Ground Fault Relay & Standby Pump 13 Started But Did Not Deliver Sufficient Flow to Prevent Trip. Cause Not Found.Inlet Filters to Be cleaned.W/900502 Ltr ML20042E3561990-04-0505 April 1990 LER 89-015-01:on 890704,reactor Trip Occurred.Caused by Failure of Relay in Generator Breaker Trip Circuit.Relays in Generator Breaker Trip Circuits Replaced W/Correct Models & Checked to Ensure Proper rating.W/900405 Ltr ML20012C7211990-03-16016 March 1990 LER 90-003-00:on 900214,discovered That Train B Fuel Handling Bldg Exhaust Air Filter Outlet Damper Would Not Open.Caused by Wiring Error Due to Failure of Technicians to Follow Work Instructions.Technicians counseled.W/900316 Ltr ML20012B4381990-03-0101 March 1990 LER 90-002-00:on 900202,Train s Reactor Trip Breaker Opened, Initiating Turbine & Reactor Trip & Feedwater Isolation on Low Average RCS Temp.Cause Unknown.Universal Logic Cards Replaced & Monitoring Instruments installed.W/900301 Ltr ML20006E3781990-02-16016 February 1990 LER 90-001-00:on 900103,containment Ventilation Isolation Occurred Due to Loss of Power to Radiation Monitor Actuation Relay.Caused by Technician Lifting Power Lead. Technicians Trained & counseled.W/900216 Ltr ML20006E4001990-02-12012 February 1990 LER 90-001-00:on 900108,Train s Low Steam Line Pressure Blocking Switch Placed in Blocked Position,Causing Actuation of Safety Injection & ESF Sys.Caused by Lack of Instructions.Training Program modified.W/900212 Ltr ML20006D4231990-02-0202 February 1990 LER 90-002-00:on 900103,redundant Solenoid Valve Which Actuates Train C Feedwater Valve Failed.Caused by Excessive Particulate Buildup.Solenoids Cleaned & Hydraulic Oil Flushed & Filtered to Remove particulate.W/900202 Ltr ML20006D5591990-02-0202 February 1990 LER 89-023-01:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Declared Inoperable. Caused by Contact Oxidation & Low Contact Pressure.Chiller Auxiliary Relay Cleaned & adjusted.W/900202 Ltr ML20006B4731990-01-25025 January 1990 LER 89-024-00:on 891226,required Sample from Safety Injection Accumulator 1C of Boron Concentration Not Taken. Caused by Insufficient Administrative Controls to Track Surveillance Tests.Bulletin Will Be issued.W/900125 Ltr ML20006B2551990-01-19019 January 1990 LER 89-022-00:on 891205,discovered That ASME Section XI Pressure Test of Train C of Component Cooling Water Sys Not Performed Prior to Returning Sys to Svc.Sys Inoperable from 890909-1206.Test Control Procedures revised.W/900119 Ltr ML20006B2221990-01-16016 January 1990 LER 89-023-00:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Attempt to Secure Essential Chiller 12C Resulted in Trip.Caused by Failure of Voltage Regulator.Regulator Returned to mfg.W/900116 Ltr ML20005E2471989-12-29029 December 1989 LER 89-028-00:on 891130,control Room Ventilation Sys Actuated to Recirculation Mode as Result of Spurious Signal. Caused by Memory Error Causing Microprocessor to Energize Relay Incorrectly.Troubleshooting planned.W/891229 Ltr ML19332D7741989-11-24024 November 1989 LER 89-018-01:on 890922,discovered That Const Installation Procedure for Reg Guide 1.97,Rev 2 Instrumentation Did Not Include Details to Ensure Qualification Per 10CFR50.49 or IEEE 323-1974.Caused by Installation error.W/891124 Ltr ML19332C8661989-11-21021 November 1989 LER 89-027-00:on 891025,discovered That Closed Limit Switch on Main Turbine Throttle Valve 2 Disconnected.Caused by Failure of Limit Switch Linkage.Review to Be Performed of Limit Switch Linkage design.W/891122 Ltr 1994-05-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K9441999-10-15015 October 1999 SER Accepting Util Alternative Proposed Relief Request RR-ENG-2-4 for Second 10-year ISI Interval at Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) ML20217K9151999-10-15015 October 1999 SER Authorizing Util Relief Request RR-ENG-2-3 for Second 10-year ISI Interval of Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) NOC-AE-000676, Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With ML20217D0531999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 2 Cycle 7 Colr ML20217D0481999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 1 Cycle 9 Colr ML20211P8411999-09-0909 September 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Surface Exam to Perform Boroscopic VT-1 Visual Exam of Pump Casing Welds within Pump Pits for Welds Covered by Relief Request RR-ENG-24 ML20211P7811999-09-0909 September 1999 SER Approving Second 10-year Interval Inservice Insp Program Plan Relief Request RR-ENG-2-8 (to Use Code Case N-491-2) for South Texas Project,Units 1 & 2 ML20211Q6731999-09-0909 September 1999 Safety Evaluation Accepting First 10-yr Interval ISI Program Plan Request for Relief from ASME Code Case N-498 NOC-AE-000643, Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With ML20212E5191999-08-31031 August 1999 Rev 3 to SG-99-04-005, STP 1RE08 Outage Condition Monitoring Rept & Final Operational Assessment ML20211F4531999-08-24024 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative to Defer Partial First Period Exams of flange-to-shell Weld to Third Period & Perform Required Ultrasonic Exams,Both Manual & Automated,During Third Period ML20211F5111999-08-23023 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative Contained in Request for Relief RR-ENG-30 ML20210C9411999-07-31031 July 1999 Rev 1 to SG-99-07-002, South Tx,Unit 1 Cycle 9 Voltage- Based Repair Criteria 90-Day Rept, Jul 1999 ML20210R3631999-07-31031 July 1999 Monthly Operating Repts for July 1999 for South Tx Project, Units 1 & 2.With ML20210D9161999-07-23023 July 1999 Safety Evaluation Accepting Inservice Testing Relief Request RR-56 Re Component Cooling Water & Safety Injection Sys Containment Isolation Check Valve Closure Test Frequency ML20210D4821999-07-21021 July 1999 1RE08 ISI Summary Rept for Steam Generator Tubing of South Texas Project Electric Generating Station Unit 1 ML20210D4491999-07-21021 July 1999 Revised Chapters to Operations QA Plan, Including Rev 9 to Chapter 1.0, Organization & Rev 6 to Chapter 16.0, Independent Technical Review NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With ML20207H6361999-07-0808 July 1999 Safety Evaluation Approving 2nd 10 Yr Interval ISI Program Plan Request to Use ASME Section XI Code Case N-546 for Licenses NPF-76 & NPF-80,respectively ML20216D7481999-07-0707 July 1999 1RE08 ISI Summary Rept for Welds & Component Supports of STP Electric Generating Station,Unit 1 NOC-AE-000593, Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program ML20195J6871999-06-17017 June 1999 Safety Evaluation Supporting Proposed Alternative Contained in RR-ENG-2-5.Proposed Alternative Authorized Per 10CFR50.55a(a)(3)(i) for 2nd ISI Interval ML20196A2391999-06-15015 June 1999 Change QA-042 to Rev 13 of Operations QAP, Reflecting Current Organizational Alignment for South Texas Project & Culminating Organizational Realigment That Has Been Taking Place During Past Several Months NOC-AE-000563, Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with ML20206U5411999-05-18018 May 1999 Non-proprietary Errata Pages for Rev 2,Addendum 1 to WCAP-13699, Laser Welded Sleeves for 3/4 Inch Diamete Tube Feedring Type & W Preheater SGs Generic Sleeving Rept ML20206A7721999-04-30030 April 1999 STP Electric Generating Station Unit 1 Cycle 9 Colr NOC-AE-000543, Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with ML20205H0321999-03-31031 March 1999 Change QA-040 to Rev 13 of Operations QA Plan NOC-AE-000507, Monthly Operating Repts for Mar 1999 for Stp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Stp,Units 1 & 2. with ML20205A3781999-03-22022 March 1999 STP Electric Generating Station Simulator Certification Four Yr Rept for Units 1 & 2 ML20204B2711999-03-15015 March 1999 Safety Evaluation Authorizing 990201 Request to Authorize Alternative to Regulations Per 10CFR50.55a(a)(3)(i) That Would Revise Start of Second 120-month IST Interval to No Later than 011201 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results NOC-AE-000468, Monthly Operating Repts for Feb 1999 for South Texas Project Electric Generating Station.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for South Texas Project Electric Generating Station.With ML20207D1101999-02-24024 February 1999 Change QA-039 to Rev 13 of Operations QA Plan, for STP ML20203H8361999-02-17017 February 1999 Safety Evaluation Supporting Request for Relief from ASME Code Requirements for Class 3 Piping for Plant ML20202H9621999-02-0303 February 1999 SER Accepting Change to EALs Used in Classification of Emergency Conditions ML20202E8471999-01-31031 January 1999 2RE06 ISI Summary Rept for SG Tubing of STP Electric Generating Station,Unit 2 ML20216G2011999-01-31031 January 1999 City Public Svc of San Antonio Annual Rept 1998-1999 ML20199G5961999-01-31031 January 1999 Cycle 7 Voltage-Based Repair Criteria Rept for Jan 1999 ML20199K7711999-01-21021 January 1999 Safety Evaluation Accepting ISI Program Request for Relief for ASME Cose Repair Requirements for Code Class 3 Piping ML20199G8161999-01-19019 January 1999 SER Accepting Util 970707 Response to NRC 970509 RAI Re GL 92-08, Thermo-Lag 330-1 Fire Barriers. NRC Finds No Significant Safety Hazards Based on Application of Util Ampacity Derating Methodology ML20199H4981999-01-11011 January 1999 2RE06 ISI Summary Rept for Welds & Component Supports of Stp,Unit 2 ML20206Q3751999-01-0404 January 1999 2RE06 ISI Summary Rept for Sys Pressure Tests (Class 1 & 2) ML20206Q3721999-01-0404 January 1999 2RE06 ISI Summary Rept for Repairs & Replacements ML20216G2171998-12-31031 December 1998 Houston Industries 1998 Annual Rept. App a 1998 Financial Statements & Us Securities & Exchange Commission Form 10-K Encl NOC-AE-000403, Monthly Operating Repts for Dec 1998 for South Texas Project Unit 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for South Texas Project Unit 1 & 2.With ML20216G1521998-12-31031 December 1998 Central & South West Corp 1998 Summary Annual Rept & Securities & Exchange Commission Form 10-K ML20198M3431998-12-28028 December 1998 SER Accepting Util Request for Relief from ASME Code Repair Requirements for ASME Code Class 3 Piping for South Texas Project,Unit 2 1999-09-09
[Table view] |
Text
f NRC FORG 366 U.S. OfCLEAE REGULAT(DY (IPMISSi(O ADR3v1D BT CDS NO. 3950-0104 (5 92) . EXPIRES 5/32/95 ESTIMATED BURDEN PER RESPokSE TO COMPLY KITH r6 tim tECitw R n:
) LICENSEE EVENT REPORT (LER) $5g9 [ cgRct g cw( tgNR c .,
THE 1kFORMATIDW AND RECORDS MAkAGEMENT BRANCH (MkEB 7714), U.S. WUCLE AR REGULATORY COMMISSIDW, (See reverse for regaired neber of digits / characters for each block) 6.A S H I NGTON , DC 20555-0001, AND TO THE PAPERWDRK j REDUCTION PROJECT (3150-0104), OFFICE Of i a MAkAGEMENT AND BUDGET, WASH 1WGTOW, DC 20503. j F ACILITY hAE (1) DOCKET EMBER (2) PAGE (3)
South Texas Unit 1 05000 498 1 OF 5 1
TITLE (4) Technical Specification 3.0.3 Entry Due to Potentially Undersized Punon in tho solid stato Prntor tinn svntom EVENT DATE (5) LER K MP.ER (6) REPORT DATE (7) OTHER F ACilITIES INVOLVID (B)
SEQUEWTIAL REVISION FACILITY KAME DOCKET NUMBER MOWTN DAY YEAR TEAR TH DAY TEAR South Texas, Unit 2 NJMBER NUMBER 05000-499
- ^ "" '"I' 02 17 93 93 009 01 05 20 93 ["
OPE RAT !WG Tuts RrPoRT 15 SusMITir PuesuAwT T Tut RE aterMEw15 or to Cre 5: (Check one or more) (11)
ICDE (9) 5 20.402(b) 20.405(c) 50.73(a)(2)(i v) 73.71(b)
PCMER 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)
LEVEL (10) 0 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405(a)(1)(iii) X 50.73(a)(2)(i) 50.73(a)(2)(vi i i)( A) (Specify in
^ #
20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) 1 3
20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(m) NRC Form 366A) tICENSEE CIniTACT FOR THIS LER (12)
- DAME TELEPHohE WUMBER (include Area Code)
Jairo Pinzon - Senior Engineer (512) 972-8027 COMPLETE ONE t lNE FOR EACH COMPOWENT F AltuRE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPOWENT MANUFACTURER p CAUSE SYSTEM COMPOWEkT MANUFACTURER p SUPPL E MENT AL RE PORT E XPE CTED (14) EXPECTED " I" UA* "##
7gg SUBMISSION (If yes, conplete EXPECTED SUBMISSION DATE). WO X DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., apprcximately 15 single-spaced typewritten lines) (16)
On February 17, 1993, Unit 1 was in Mode 5 and Unit 2 was in Mode 4, both at 0% power. Plant personnel determined that a potentially unanalyzed l '
a condition existed in both units related to a failed fuse event that occurred on February 13, 1993. This unanalyzed condition involved suspected undersized fuses found in the Solid State Protection System g (SSPS) in which an inrush current could cause the fuses to fail and prevent the fulfillment of the SSPS's intended safety function. In response to the inoperable SSPS actuation cabinets, Unit 2 entered Technical Specification
- Section 3.0.3 and plant cooldown to Mode 5 was initiated at 1030 on
- February 17, 1993. Unit 1 was already in Mode 5. The event was caused by j the random age related failure of a SSPS fuse. In response to the event, 4
the 10 amp fuses were replaced with 20 arp fuses in both Units, other 120 volt vital A.C. distribution and class 1E DC circuit panels were reviewed for similar conditions, field verification of selected protective devices .
was conducted, and a failure analysis of the blown fuse was performed by an i independent laboratory and reviewed by the fuse manufacturer. ,
Additionally, lessons learned will be formally factored into the design process.
i NRC FORM 366 (5-92) 93052604B3 930520 PDR ADOCK 05000498 S PDR
NRC FORM 366A U.S. BUCLEAR REGULATORY CD MISSIOt APPROVED Bf 05 00. 3150-0104 (5-02) EXPIRES 5/31/95
. ESTIMATED BURDEN PER RESPONSE TO COMPLV UITH TN!S 1hFDEMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS RE(.ARDlWG BURDEN ESilMATE TO THE LICENBEE EVENT REPORT (LER) IwFORMATIOk AND RECORDS MAkAGEMENT BEAbCH fMkBB TEXT CONTINUATION m 4), u.S. NUCLEAR RE GUL ATORY COMMISSION, WASH 1kGTON, DC 20555-0001 AND TO THE PAPER.0FtK REDUCTION PROJECT (3150-0104), OFFICE OF MAkAGEMENT AND BUDGET, WASHINGTOW, DC 205C3, e ! F ACILITY KW (1) DOCLTT tLMBER (?) I LER NtmBER (69 PAT (3)
YEAR SEQUE hTI AL REVISION South Texas, Unit 1 05000 498 2 OF 5 93 009 01 TEri tif core space is reosired. use additionet copies of WRC Form 366A) (17)
DESCRIPTION OF EVENT:
On February 17, 1993, Unit 1 was in Mode 5 and Unit 2 was in Mode 4, both at 0% power. Plant personnel determined that an unanalyzed condition existed in both units related to a failed fuse event that occurred on February 13, 1993. This unanalyzed condition involved potentially ]
undersized fuses found in the Solid State Protection System (SSPS) in which an inrush current could possibly cause the fuses to fail and prevent the fulfillment of SSPS's intended safety function. [
On February 13, 1993, while performing SSPS Train S reactor trip breaker trip actuating device operational surveillance test in Unit 1, the power was lost to the Train A SSPS actuation cabinet. It was subsequently determined that a 10 amp fuse in the electrical distribution panel EDP 1201 which feeds the Train A SSPS actuation cabinet failed. The unit was in Mode 5 at 0% power at the time of the failure. Testing was suspended and the event was referred to engineering for investigation. Engineering concluded that the fuse, sized for steady state current conditions, may have been undersized based on inrush current. The review determined that Westinghouse had provided 20 amp fuses in the SSPS actuation cabinet but the fuses in the electrical distribution panel feeding this cabinet had been sized at 10 amps. The 10 amp fuses were also installed in Unit 2.
. An initial operability review was performed to determine the impact of l having 10 amp fuses feeding the SSPS actuation cabinet. The initial results concluded that all three SSPS actuation trains were inoperable, and as a result, Unit 2 entered Technical Specification 3.0.3. At 1030 on February 17, 1993, plant cooldown to Mode 5 was initiated in Unit 2. Unit 1 was already in Mode 5 so entry into Technical Specification 3.0.3 was not required. Concurrently, plant change forms were initiated to revise the fuse size from 10 amp to 20 amp. Unit 2 exited Technical Specification 3.0.3 when the 10 amp fuses were replaced with 20 amp fuses.
CAUSE OF EVENT: t
, The cause of this event was a random age related failure of the 10 amp fuse in the electrical distribution panel feeding Train A SSPS actuation cabinet.
ANALYSIS OF EVENT:
1 The SSPS contains three trains of Engincered Safety Features (ESP) actuation cabinets which actuate various ESF equipment via relays providing 1 protection to mitigate the consequences of postulated accidents. When the j correct logic requirements are met, master relays are energized which in turn energize a set of slave relays that operate the various ESF components.
I l
I
NRC FORM 366A U.S. KACLEAR REGJLATORY CDWISSION APPROVD BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY ti1TH THIS IhTORMATION COLLECTION REQUE ST: 50.0 HRS.
' LICENSEE EVENT REPORT (LER) NTEAN RE$RD "NGEMENT BR NCH 7714), U.S. NUCtEAR REcuLATORT CcamlS$10W, TEXT CONTINUATION WASHINGTON, DC 20555-0001 AND TO THE PAPEPWORK REDUCTION PROJECT (3150-0104), OFFICE OF MAhACEME NT AND BUDGET, WASHINGTON, DC 20503.
F ACitITY KME (1) DOCKET EMBir (?) LER NUMRER (6'i PAM (3)
YEAR SEQUENTI AL REVISION South Texas, Unit 1 05000 498 3 OF 5 93 009 01 T0ri (If more space is reasired, use additionet copies of ARC Form 366A) (17)
ANALYSIS OF EVENT: (Cont'd)
The initial evaluation of the design was based on information available from Westinghouse (the actuation cabinets' vendor) that indicated a momentary inrush current of 46.5 amps may be experienced. Based on this, and the fact that Westinghouse had furnished 20 amp fuses in the SSPS actuation cabinets, it was concluded that the installed 10 amp fast acting fuses in the distribution panel feeding this equipment may blow on energization of the maximum number of relays during Modes 1 through 4.
Therefore, the SSPS actuation cabinets were conservatively declared inoperable in these modes.
Further evaluation of the design determined that the worst case accident scenario was a main steam line break, which would initiate the slave relays associated with steam line isolation and safety injection. This condition energizes 45 relays (43 latching and 2 non-latching) in the Train A or B actuation cabinet; 33 (30 latching and 3 non-latching) in the Train C actuation cabinet. Calculated maximum circuit currents during relay inrush for these cabinets is less than the published time-current characteristic for 10 amp fuses (Gould Shawmut type A60X10). Therefore, the SSPS actuation cabinets were, in fact, operable with the originally installed (unblown) 10 amp fuses.
It should be noted that the above evaluation and conclusion was based on Gould Shawmut product information for their A60X10 fuses which indicates an average melting current versus time value of approximately 29 amps at 10 msec. Recently received product information for these same fuses shows an average melting current versus time value of approximately 69 amps at 10 msec. Gould Shawmut attributes this change to improved equipment and techniques used in testing and developing fuse time-current characteristic curves. The results of this improved technology are particularly apparent at short time (millisecond) values. This curve significantly increases the SSPS fuse application design margin and supports that the SSPS actuation cabinets were operable with the originally installed (unblown) 10 amp fuses.
In addition to the design evaluation, Southwest Research Institute (SwRI),
an independent laboratory, was contracted to evaluate the blown fuse in order to determine the cause of failure, if possible. During this i evaluation SwRI examined the blown fuse, several unblown companion fuses and a new fuse. SwRI concluded:
o The blown fuse did not open as a result of a high current fault. ,
o It was not possible to determine whether the blown fuse link had a defect !
that caused it to open. '
o Thermal damage to unopened links in both the blown fuse and the unblown i companion fuses indicate that they had been subjected to greater than I rated current.
1
NRC FORM 366A U.S. IEJCLEAR REGULATORY CGotIESION APPROVED BY 0 e No. 3150-0104 (5 92) EXPIRES 5/31/95
. ESTIMATED B'IDEN PER RESPONSE TO COMPLY If!TH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
.
- FORWARD COMMENTS REGAPD]NG BURDEN ESTIMATE TO THE LICENSEE EVENT REPORT (LER) thf0RMAT10N AND RECORDS MANAGEMENT BRANCH (MNE,B TEXT CONTINUATION 7714), u.s. NUCLEAR REGutATORT COMNISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCT!ON PROJECT (31dD-0104), OFFICE OF MANActMENT AND BUDGET, WASHINCTON, DC 20503.
FACillTT MAM (1) DOCKTT s 4BER (2) t ER IKMBER (6S PAGE (3)
TEAR SEQUENTIAL REVISION South Texas, Unit 1 05000 498 4 OF 5 93 009 01 TEXT (if we spece is reovired, use acrJitionet eccles of WRC form 366A) (17)
ANALYSIS OF EVENT: (Cont'd) o Cracks in ferrules of the blown fuse had no apparent impact on its electrical performance and no apparent role in the fuse opening. l l
Gould Shawmut reviewed the SwRI Failure Analysis Report and in general agreed with the SwRI report. Gould Shawmut agreed that the fuses had been subjected to greater than rated current (eg. 10 amps), however, this is not unusual and fuses are designed for such service. That is, fuses are designed to accept a certain amount of "overcurrent" due to conditions such j as inrushes. Gould Shawmut concl*.2ded that the thermal damage observed in '
both the blown SSPS fuse and the unblown companion fuses was indicative of stress cracking of the zinc element caused by thermal cycling. As such, the most probable cause of the fuse opening was mechanical stressing (aging) of the element. That is, the fuse reached the end Jf its life.
I STP has concluded that the SSPS fuse opening was a random age related l failure event. This conclusion is based on the circuit analysis discussed i above and is supported by the fact that the SSPS actuation system has in l the past operated properly on safety injection actuations wherein the currents experienced by the subject fuses closely approach those of a main steam line break scenario. The design of STP accounts for single random failures and, therefore, this fuse failure was within the plant's design basis. ;
Entry into Technical Specification 3.0.3 is reportable pursuant to 10CFR50.73 (a) (i) (B) .
l l CORRECTIVE ACTIONS:
l
- 1. The electrical distribution panel fuses feeding the three trains of SSPS actuation cabinets in both units were replaced with 20 amp fuses.
l A 20 amp fuse provides adequate protection for this design and provides additional margin to reduce the probability of nuisance fuse blowing due to random age related failure mechanisms.
- 2. A comparative evaluation of vital 120 VAC distribution panel fuses and selected DC circuit breakers and the main incoming protective devices in the panels fed by them has been done to determine if other problems i
exist. Vendor panels were found in which the panel protection is l larger than the distribution panel protection but these cases were determined to be acceptable after review of the supplied load currents.
One case was identified (6 similar radiation monitors per unit) where
- the increased margin provided by a larger size fuse was warranted.
I These 15 amp fuses have been replaced with 30 amp fuses in Unit 1 and an identical change has been designed for Unit 2.
{
NRC FORM 366A U.S. IUCLEAR REGULATORY CO*lSSION APPROWED BT QMB 183. 3150-0104 l (5-9i) EXP!RES 5/39/95
- ESTIMATED BURDEN PER RESPONSE VO COMPLY MITH TH15 INFORMATION COLLECTION REQUEST: 50.0 HRS.
' FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE
. 'LICENBEE EVENT REPORT (LER) INFORMATION AND RECORDS MAhAGEMENT BRANCH (MWBB TEXT CONTINUATION m4), u.S. NUCLEAR REGULATORY COMMIS$10N, WASHINGTON, DC 20555-0001 AND TO THE PAPERW3RK I REDUCTION PROJECT (31$0-0104), OFFICE OF hWACEMENT AND BLOCET, WASHINGTON, DC ?O503.
I FACitITY EAME (1) DOCKET tKMIER (2) LER NLMPER (69 PAGE (3)
YEAR SEQUENTIAL REVISION South Texas, Unit 1 "*" "MR 05000 498 5 OF 5 93 009 01 V9T (If more space is remired. use additionel copies of kRC Form 366A) (17)
CORRECTIVE ACTIONS: (Cont'd) l l 3. A review has been performed by Engineering to determine the adequacy 1,t the station design related to the size selection of fuses and/or circuit breakers within the original architect engineer's design scope which interfaced with vendor designed safety systems. This review was initially conducted on a random sample basis and was later expanded in stages to include 100% of power distribution fuses in Class 1E distribution panels. This review resulted in the conclusion that the potential for undersized protective devices relative to inrush currents appears to be isolated t., fast acting fuses. As a result, fast acting power distribution fuses in Class 1E distribution panels have been reviewed and no operability impacts have been identified, and fast acting fuses feeding the SSPS sctuation cabinets and fast acting fuses in the radiation monitors have been upsized for increased margin.
- 4. A fuse and breaker field verification was performed to assess the accuracy of the documentation used in the engineering review. This effort was initially conducted on a random sample basis and was later expanded in stages to include 100% of the fast acting power distribution fuses in Class 1E distribution panels. The assessment resulted in the conclusion that the molded case circuit breakers agreed j with the design documentation while the fuses had some r;ize/ type I discrepancies with design documentation. However, all of the
! identified fuse discrepancies were minor in nature, were acceptable for use as is and presented no operability concerns.
- 5. To reduce the potential of random age related fuse failures affecting I critical systems, fuses in selected equipment were replaced during the fuse and breaker field verification effort.
- 6. Interim guidance has been issued to the STP Electrical Design Staff to sensitize them to several fuse sizing considerations highlighted by the investigation of this event. STP design practices will be revised to l
formally incorporate this interim guidance by December 31, 1993.
i l
ADDITIONAL INFORMATION:
There have been no previously reported events concerning fuses being undersized causing an unanalyzed event.
l l
1 I