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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6321994-05-0202 May 1994 LER 94-002-01:on 940115,centrifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to Requirements of TS 3.1.2.3.Caused by hydro-pneumatic Transient.Valves Labeled W/Caution statements.W/940502 Ltr ML20029D6351994-04-27027 April 1994 LER 94-006-01:on 940214,reactor Manually Tripped Following Unanticipated Test Results.Caused by Mod Which Failed post- Mod Test.Test Terminated & Solid State Rod Control Sys Returned to Original Design configuration.W/940427 Ltr ML20029C6951994-04-18018 April 1994 LER 94-011-00:on 940310,safety Injection Actuation Was Received on Trains A,B & C.Cause Was Failure to Adhere to Procedure.Corrective Actions:Restored Cooling Shutdown & Removed Personnel from watchbill.W/940418 Ltr ML17352B2581994-03-25025 March 1994 LER 94-007-00:on 940224,station Procedure for Testing Reactor Trip Bypass Breakers Did Not Satisfy Ts.Caused by Inadequate Procedure Preparation & Review.Surveillance Procedure Enhancement Program underway.W/940325 Ltr ML20046C5471993-08-0606 August 1993 LER 93-018-00:on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST plan.W/930806 Ltr ML20046C4901993-08-0505 August 1993 LER 93-019-00:on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing discrepancy.W/930805 Ltr ML20046B1291993-07-29029 July 1993 LER 93-012-00:on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel cooling.W/930729 Ltr ML20046A6791993-07-21021 July 1993 LER 93-011-00:on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway ML20046A6511993-07-20020 July 1993 LER 93-017-01:on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified ML20045J0281993-07-15015 July 1993 LER 93-016-01:on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 QDPS.W/930715 Ltr ML20045H9171993-07-14014 July 1993 LER 93-008-01:on 930505,discovered That RHR Pump Suction MOV Had Not Been Environ Qualified Since 901129 Because Replacement of Drain T Not Completed.Drain T Missing from RH-0060B Replaced & Bulletin Issued to Maint Dept ML20045H9881993-07-13013 July 1993 LER 93-012-01:on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings. W/930713 Ltr ML20045E1531993-06-25025 June 1993 LER 93-017-00:on 930527,determined That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioner & Solenoids Remained in Svc Beyond Qualified Life.Caused by Incorrect Interpretation of Design Documents.Mod Underway ML20045E1491993-06-25025 June 1993 LER 93-010-00:on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint initiated.W/930625 Ltr ML20045B2731993-06-0909 June 1993 LER-93-016-00:on 930503,TS Violation Occured Due to Circuitry for SG PORVs & RCS Subcooling Monitor Being Inoperable.Caused by Less than Adequate Work Practices. Screws Missings from Qdps Replaced & Walkdown Performed ML20045A3831993-06-0404 June 1993 LER 93-008-00:on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain ML20044G4301993-05-25025 May 1993 LER 93-009-00:on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref values.W/930525 Ltr ML20044F6281993-05-21021 May 1993 LER 93-015-00:on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans monitored.W/930521 Ltr ML20044F1321993-05-20020 May 1993 LER 93-009-01:on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort ML20044E0371993-05-14014 May 1993 LER 93-005-01:on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training ML20024H2571991-05-24024 May 1991 LER 91-014-00:on 910420,erratic Containment Extended Range Pressure Channel Output Occurred.Caused by Bad Control Card. Weekly Channel Checks Performed,Control Card Replaced & Channel calibrated.W/910524 Ltr ML20024H2081991-05-22022 May 1991 LER 91-015-00:on 910422,train C AFW Pump Inadvertently Started Due to Failure of Led in Sequencer Test Circuitry. Faulty Led Replaced & Blocking Circuit Satisfactorily tested.W/910522 Ltr ML20029C1221991-03-15015 March 1991 LER 91-004-00:on 910215,loss of Offsite Power Actuation Occurred During Routine Maint.Caused by Lack of Attention to Work Performance Methods.Training Conducted for Maintenance personnel.W/910315 Ltr ML20029B0421991-02-25025 February 1991 LER 91-002-00:on 910126,automatic Actuation of Safety Injection Sys Occurred in One of Three Train C Trains.Caused by Inadequate Work Instructions for Maint Activity.Training Bulletin Issued & Supervisors counseled.W/910225 Ltr ML20024F7451990-12-12012 December 1990 LER 90-017-00:on 901104,discovered That Train a of Class IE 120-volt Distribution Panel DP001 Energized from Alternate Power Supply.Caused by Less than Adequate Administrative Controls.Log Will Be utilized.W/901212 Ltr ML20044B1691990-07-0606 July 1990 LER 90-011-00:on 900612,chemical Technician Supervisor Discovered That No Sample Collected in Condenser Air Removal Sys Radiation Monitor Moisture Collection Tank. Caused by Inadequate procedure.W/900706 Ltr ML20043G2091990-06-14014 June 1990 LER 90-010-00:on 900515,determined That Leak & Contamination Test Interval for Some Radioactive Sources Exceeded Tech Specs.Caused by Insufficient Detail in Procedures.Test Program revised.W/900614 Ltr ML20043G5191990-06-14014 June 1990 LER 90-010-00:on 900515,unplanned Actuation of ESF Train C Standby Diesel Generator Occurred.Caused by Personnel Error. Training Bulletin Will Be Issued to Maint Personnel Re event.W/900613 Ltr ML20043G1791990-06-13013 June 1990 LER 90-009-00:on 900512,incorrect Wiring in Solid State Protection Sys Discovered.Caused by Inadvertent Installation of Extra Wire by Mfg.Extra Wire Removed & Sys Successfully tested.W/900613 Ltr ML20043G2101990-06-13013 June 1990 LER 90-009-00:on 900514,discovered That Printer for Toxic Gas Analyzer XE-9325 Was Not Updating & Surveillances for Toxic Gas Monitor XE-9325 Incorrectly Performed on 900511. Caused by Inadequate training.W/900613 Ltr ML20043G7681990-06-0808 June 1990 LER 90-008-00:on 900508,Tech Spec Required Shutdown Initiated Due to Primary Coolant Sys Leakage.Caused by High Cycle Fatigue Failure of Weld on Upstream Side of Drain Valve.Drain Valves replaced.W/900608 Ltr ML20043E7001990-06-0404 June 1990 LER 90-008-00:on 891007,Tech Spec Violation Occurred Due to Failure to Perform post-maint Testing.Caused by Incorrect Determination That No post-maint Testing Required.Personnel counseled.W/900604 Ltr ML20043C7401990-05-30030 May 1990 LER 90-007-00:on 900430,discovered That All Three Trains of ESFAS Placed in Test & Incapable of Actuating for Approx 35 Minutes.Caused by Inadequate Prerequisite Conditions in Maint Procedure.Procedure Being modified.W/900530 Ltr ML20043C4791990-05-29029 May 1990 LER 90-007-00:on 900426,standby Diesel Generator 22 Room High Sump Level Alarm Actuated in Control Room.Caused by Flooding & Inadequate Spec of Sealing & Testing Requirements.Seals on Removable Panels caulked.W/900529 Ltr ML20043B6611990-05-25025 May 1990 LER 90-006-00:on 900426,control Room Ventilation Sys Actuated to Recirculation Mode Due to High Level Trip of Vinyl Acetate Channel on Gas Analyzer.Caused by Failure of electro-mechanical Positioner.Part replaced.W/900525 Ltr ML20043A7811990-05-15015 May 1990 LER 90-005-00:on 900414,simultaneous Reactor & Turbine Trip Occurred Due to Failure of Main Turbine Electrohydraulic Control Line.Caused by Fatigue Stress of Weld.Valve Modified to Add anti-swirl Baffles & anti-rotation pins.W/900515 Ltr ML20042F2191990-05-0202 May 1990 LER 90-005-00:on 900329,feedwater Booster Pump 11 Tripped Upon Actuation of Ground Fault Relay & Standby Pump 13 Started But Did Not Deliver Sufficient Flow to Prevent Trip. Cause Not Found.Inlet Filters to Be cleaned.W/900502 Ltr ML20042E3561990-04-0505 April 1990 LER 89-015-01:on 890704,reactor Trip Occurred.Caused by Failure of Relay in Generator Breaker Trip Circuit.Relays in Generator Breaker Trip Circuits Replaced W/Correct Models & Checked to Ensure Proper rating.W/900405 Ltr ML20012C7211990-03-16016 March 1990 LER 90-003-00:on 900214,discovered That Train B Fuel Handling Bldg Exhaust Air Filter Outlet Damper Would Not Open.Caused by Wiring Error Due to Failure of Technicians to Follow Work Instructions.Technicians counseled.W/900316 Ltr ML20012B4381990-03-0101 March 1990 LER 90-002-00:on 900202,Train s Reactor Trip Breaker Opened, Initiating Turbine & Reactor Trip & Feedwater Isolation on Low Average RCS Temp.Cause Unknown.Universal Logic Cards Replaced & Monitoring Instruments installed.W/900301 Ltr ML20006E3781990-02-16016 February 1990 LER 90-001-00:on 900103,containment Ventilation Isolation Occurred Due to Loss of Power to Radiation Monitor Actuation Relay.Caused by Technician Lifting Power Lead. Technicians Trained & counseled.W/900216 Ltr ML20006E4001990-02-12012 February 1990 LER 90-001-00:on 900108,Train s Low Steam Line Pressure Blocking Switch Placed in Blocked Position,Causing Actuation of Safety Injection & ESF Sys.Caused by Lack of Instructions.Training Program modified.W/900212 Ltr ML20006D4231990-02-0202 February 1990 LER 90-002-00:on 900103,redundant Solenoid Valve Which Actuates Train C Feedwater Valve Failed.Caused by Excessive Particulate Buildup.Solenoids Cleaned & Hydraulic Oil Flushed & Filtered to Remove particulate.W/900202 Ltr ML20006D5591990-02-0202 February 1990 LER 89-023-01:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Declared Inoperable. Caused by Contact Oxidation & Low Contact Pressure.Chiller Auxiliary Relay Cleaned & adjusted.W/900202 Ltr ML20006B4731990-01-25025 January 1990 LER 89-024-00:on 891226,required Sample from Safety Injection Accumulator 1C of Boron Concentration Not Taken. Caused by Insufficient Administrative Controls to Track Surveillance Tests.Bulletin Will Be issued.W/900125 Ltr ML20006B2551990-01-19019 January 1990 LER 89-022-00:on 891205,discovered That ASME Section XI Pressure Test of Train C of Component Cooling Water Sys Not Performed Prior to Returning Sys to Svc.Sys Inoperable from 890909-1206.Test Control Procedures revised.W/900119 Ltr ML20006B2221990-01-16016 January 1990 LER 89-023-00:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Attempt to Secure Essential Chiller 12C Resulted in Trip.Caused by Failure of Voltage Regulator.Regulator Returned to mfg.W/900116 Ltr ML20005E2471989-12-29029 December 1989 LER 89-028-00:on 891130,control Room Ventilation Sys Actuated to Recirculation Mode as Result of Spurious Signal. Caused by Memory Error Causing Microprocessor to Energize Relay Incorrectly.Troubleshooting planned.W/891229 Ltr ML19332D7741989-11-24024 November 1989 LER 89-018-01:on 890922,discovered That Const Installation Procedure for Reg Guide 1.97,Rev 2 Instrumentation Did Not Include Details to Ensure Qualification Per 10CFR50.49 or IEEE 323-1974.Caused by Installation error.W/891124 Ltr ML19332C8661989-11-21021 November 1989 LER 89-027-00:on 891025,discovered That Closed Limit Switch on Main Turbine Throttle Valve 2 Disconnected.Caused by Failure of Limit Switch Linkage.Review to Be Performed of Limit Switch Linkage design.W/891122 Ltr 1994-05-02
[Table view] Category:RO)
MONTHYEARML20029D6321994-05-0202 May 1994 LER 94-002-01:on 940115,centrifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to Requirements of TS 3.1.2.3.Caused by hydro-pneumatic Transient.Valves Labeled W/Caution statements.W/940502 Ltr ML20029D6351994-04-27027 April 1994 LER 94-006-01:on 940214,reactor Manually Tripped Following Unanticipated Test Results.Caused by Mod Which Failed post- Mod Test.Test Terminated & Solid State Rod Control Sys Returned to Original Design configuration.W/940427 Ltr ML20029C6951994-04-18018 April 1994 LER 94-011-00:on 940310,safety Injection Actuation Was Received on Trains A,B & C.Cause Was Failure to Adhere to Procedure.Corrective Actions:Restored Cooling Shutdown & Removed Personnel from watchbill.W/940418 Ltr ML17352B2581994-03-25025 March 1994 LER 94-007-00:on 940224,station Procedure for Testing Reactor Trip Bypass Breakers Did Not Satisfy Ts.Caused by Inadequate Procedure Preparation & Review.Surveillance Procedure Enhancement Program underway.W/940325 Ltr ML20046C5471993-08-0606 August 1993 LER 93-018-00:on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST plan.W/930806 Ltr ML20046C4901993-08-0505 August 1993 LER 93-019-00:on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing discrepancy.W/930805 Ltr ML20046B1291993-07-29029 July 1993 LER 93-012-00:on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel cooling.W/930729 Ltr ML20046A6791993-07-21021 July 1993 LER 93-011-00:on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway ML20046A6511993-07-20020 July 1993 LER 93-017-01:on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified ML20045J0281993-07-15015 July 1993 LER 93-016-01:on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 QDPS.W/930715 Ltr ML20045H9171993-07-14014 July 1993 LER 93-008-01:on 930505,discovered That RHR Pump Suction MOV Had Not Been Environ Qualified Since 901129 Because Replacement of Drain T Not Completed.Drain T Missing from RH-0060B Replaced & Bulletin Issued to Maint Dept ML20045H9881993-07-13013 July 1993 LER 93-012-01:on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings. W/930713 Ltr ML20045E1531993-06-25025 June 1993 LER 93-017-00:on 930527,determined That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioner & Solenoids Remained in Svc Beyond Qualified Life.Caused by Incorrect Interpretation of Design Documents.Mod Underway ML20045E1491993-06-25025 June 1993 LER 93-010-00:on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint initiated.W/930625 Ltr ML20045B2731993-06-0909 June 1993 LER-93-016-00:on 930503,TS Violation Occured Due to Circuitry for SG PORVs & RCS Subcooling Monitor Being Inoperable.Caused by Less than Adequate Work Practices. Screws Missings from Qdps Replaced & Walkdown Performed ML20045A3831993-06-0404 June 1993 LER 93-008-00:on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain ML20044G4301993-05-25025 May 1993 LER 93-009-00:on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref values.W/930525 Ltr ML20044F6281993-05-21021 May 1993 LER 93-015-00:on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans monitored.W/930521 Ltr ML20044F1321993-05-20020 May 1993 LER 93-009-01:on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort ML20044E0371993-05-14014 May 1993 LER 93-005-01:on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training ML20024H2571991-05-24024 May 1991 LER 91-014-00:on 910420,erratic Containment Extended Range Pressure Channel Output Occurred.Caused by Bad Control Card. Weekly Channel Checks Performed,Control Card Replaced & Channel calibrated.W/910524 Ltr ML20024H2081991-05-22022 May 1991 LER 91-015-00:on 910422,train C AFW Pump Inadvertently Started Due to Failure of Led in Sequencer Test Circuitry. Faulty Led Replaced & Blocking Circuit Satisfactorily tested.W/910522 Ltr ML20029C1221991-03-15015 March 1991 LER 91-004-00:on 910215,loss of Offsite Power Actuation Occurred During Routine Maint.Caused by Lack of Attention to Work Performance Methods.Training Conducted for Maintenance personnel.W/910315 Ltr ML20029B0421991-02-25025 February 1991 LER 91-002-00:on 910126,automatic Actuation of Safety Injection Sys Occurred in One of Three Train C Trains.Caused by Inadequate Work Instructions for Maint Activity.Training Bulletin Issued & Supervisors counseled.W/910225 Ltr ML20024F7451990-12-12012 December 1990 LER 90-017-00:on 901104,discovered That Train a of Class IE 120-volt Distribution Panel DP001 Energized from Alternate Power Supply.Caused by Less than Adequate Administrative Controls.Log Will Be utilized.W/901212 Ltr ML20044B1691990-07-0606 July 1990 LER 90-011-00:on 900612,chemical Technician Supervisor Discovered That No Sample Collected in Condenser Air Removal Sys Radiation Monitor Moisture Collection Tank. Caused by Inadequate procedure.W/900706 Ltr ML20043G2091990-06-14014 June 1990 LER 90-010-00:on 900515,determined That Leak & Contamination Test Interval for Some Radioactive Sources Exceeded Tech Specs.Caused by Insufficient Detail in Procedures.Test Program revised.W/900614 Ltr ML20043G5191990-06-14014 June 1990 LER 90-010-00:on 900515,unplanned Actuation of ESF Train C Standby Diesel Generator Occurred.Caused by Personnel Error. Training Bulletin Will Be Issued to Maint Personnel Re event.W/900613 Ltr ML20043G1791990-06-13013 June 1990 LER 90-009-00:on 900512,incorrect Wiring in Solid State Protection Sys Discovered.Caused by Inadvertent Installation of Extra Wire by Mfg.Extra Wire Removed & Sys Successfully tested.W/900613 Ltr ML20043G2101990-06-13013 June 1990 LER 90-009-00:on 900514,discovered That Printer for Toxic Gas Analyzer XE-9325 Was Not Updating & Surveillances for Toxic Gas Monitor XE-9325 Incorrectly Performed on 900511. Caused by Inadequate training.W/900613 Ltr ML20043G7681990-06-0808 June 1990 LER 90-008-00:on 900508,Tech Spec Required Shutdown Initiated Due to Primary Coolant Sys Leakage.Caused by High Cycle Fatigue Failure of Weld on Upstream Side of Drain Valve.Drain Valves replaced.W/900608 Ltr ML20043E7001990-06-0404 June 1990 LER 90-008-00:on 891007,Tech Spec Violation Occurred Due to Failure to Perform post-maint Testing.Caused by Incorrect Determination That No post-maint Testing Required.Personnel counseled.W/900604 Ltr ML20043C7401990-05-30030 May 1990 LER 90-007-00:on 900430,discovered That All Three Trains of ESFAS Placed in Test & Incapable of Actuating for Approx 35 Minutes.Caused by Inadequate Prerequisite Conditions in Maint Procedure.Procedure Being modified.W/900530 Ltr ML20043C4791990-05-29029 May 1990 LER 90-007-00:on 900426,standby Diesel Generator 22 Room High Sump Level Alarm Actuated in Control Room.Caused by Flooding & Inadequate Spec of Sealing & Testing Requirements.Seals on Removable Panels caulked.W/900529 Ltr ML20043B6611990-05-25025 May 1990 LER 90-006-00:on 900426,control Room Ventilation Sys Actuated to Recirculation Mode Due to High Level Trip of Vinyl Acetate Channel on Gas Analyzer.Caused by Failure of electro-mechanical Positioner.Part replaced.W/900525 Ltr ML20043A7811990-05-15015 May 1990 LER 90-005-00:on 900414,simultaneous Reactor & Turbine Trip Occurred Due to Failure of Main Turbine Electrohydraulic Control Line.Caused by Fatigue Stress of Weld.Valve Modified to Add anti-swirl Baffles & anti-rotation pins.W/900515 Ltr ML20042F2191990-05-0202 May 1990 LER 90-005-00:on 900329,feedwater Booster Pump 11 Tripped Upon Actuation of Ground Fault Relay & Standby Pump 13 Started But Did Not Deliver Sufficient Flow to Prevent Trip. Cause Not Found.Inlet Filters to Be cleaned.W/900502 Ltr ML20042E3561990-04-0505 April 1990 LER 89-015-01:on 890704,reactor Trip Occurred.Caused by Failure of Relay in Generator Breaker Trip Circuit.Relays in Generator Breaker Trip Circuits Replaced W/Correct Models & Checked to Ensure Proper rating.W/900405 Ltr ML20012C7211990-03-16016 March 1990 LER 90-003-00:on 900214,discovered That Train B Fuel Handling Bldg Exhaust Air Filter Outlet Damper Would Not Open.Caused by Wiring Error Due to Failure of Technicians to Follow Work Instructions.Technicians counseled.W/900316 Ltr ML20012B4381990-03-0101 March 1990 LER 90-002-00:on 900202,Train s Reactor Trip Breaker Opened, Initiating Turbine & Reactor Trip & Feedwater Isolation on Low Average RCS Temp.Cause Unknown.Universal Logic Cards Replaced & Monitoring Instruments installed.W/900301 Ltr ML20006E3781990-02-16016 February 1990 LER 90-001-00:on 900103,containment Ventilation Isolation Occurred Due to Loss of Power to Radiation Monitor Actuation Relay.Caused by Technician Lifting Power Lead. Technicians Trained & counseled.W/900216 Ltr ML20006E4001990-02-12012 February 1990 LER 90-001-00:on 900108,Train s Low Steam Line Pressure Blocking Switch Placed in Blocked Position,Causing Actuation of Safety Injection & ESF Sys.Caused by Lack of Instructions.Training Program modified.W/900212 Ltr ML20006D4231990-02-0202 February 1990 LER 90-002-00:on 900103,redundant Solenoid Valve Which Actuates Train C Feedwater Valve Failed.Caused by Excessive Particulate Buildup.Solenoids Cleaned & Hydraulic Oil Flushed & Filtered to Remove particulate.W/900202 Ltr ML20006D5591990-02-0202 February 1990 LER 89-023-01:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Declared Inoperable. Caused by Contact Oxidation & Low Contact Pressure.Chiller Auxiliary Relay Cleaned & adjusted.W/900202 Ltr ML20006B4731990-01-25025 January 1990 LER 89-024-00:on 891226,required Sample from Safety Injection Accumulator 1C of Boron Concentration Not Taken. Caused by Insufficient Administrative Controls to Track Surveillance Tests.Bulletin Will Be issued.W/900125 Ltr ML20006B2551990-01-19019 January 1990 LER 89-022-00:on 891205,discovered That ASME Section XI Pressure Test of Train C of Component Cooling Water Sys Not Performed Prior to Returning Sys to Svc.Sys Inoperable from 890909-1206.Test Control Procedures revised.W/900119 Ltr ML20006B2221990-01-16016 January 1990 LER 89-023-00:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Attempt to Secure Essential Chiller 12C Resulted in Trip.Caused by Failure of Voltage Regulator.Regulator Returned to mfg.W/900116 Ltr ML20005E2471989-12-29029 December 1989 LER 89-028-00:on 891130,control Room Ventilation Sys Actuated to Recirculation Mode as Result of Spurious Signal. Caused by Memory Error Causing Microprocessor to Energize Relay Incorrectly.Troubleshooting planned.W/891229 Ltr ML19332D7741989-11-24024 November 1989 LER 89-018-01:on 890922,discovered That Const Installation Procedure for Reg Guide 1.97,Rev 2 Instrumentation Did Not Include Details to Ensure Qualification Per 10CFR50.49 or IEEE 323-1974.Caused by Installation error.W/891124 Ltr ML19332C8661989-11-21021 November 1989 LER 89-027-00:on 891025,discovered That Closed Limit Switch on Main Turbine Throttle Valve 2 Disconnected.Caused by Failure of Limit Switch Linkage.Review to Be Performed of Limit Switch Linkage design.W/891122 Ltr 1994-05-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K9441999-10-15015 October 1999 SER Accepting Util Alternative Proposed Relief Request RR-ENG-2-4 for Second 10-year ISI Interval at Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) ML20217K9151999-10-15015 October 1999 SER Authorizing Util Relief Request RR-ENG-2-3 for Second 10-year ISI Interval of Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) NOC-AE-000676, Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With ML20217D0531999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 2 Cycle 7 Colr ML20217D0481999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 1 Cycle 9 Colr ML20211P8411999-09-0909 September 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Surface Exam to Perform Boroscopic VT-1 Visual Exam of Pump Casing Welds within Pump Pits for Welds Covered by Relief Request RR-ENG-24 ML20211P7811999-09-0909 September 1999 SER Approving Second 10-year Interval Inservice Insp Program Plan Relief Request RR-ENG-2-8 (to Use Code Case N-491-2) for South Texas Project,Units 1 & 2 ML20211Q6731999-09-0909 September 1999 Safety Evaluation Accepting First 10-yr Interval ISI Program Plan Request for Relief from ASME Code Case N-498 NOC-AE-000643, Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With ML20212E5191999-08-31031 August 1999 Rev 3 to SG-99-04-005, STP 1RE08 Outage Condition Monitoring Rept & Final Operational Assessment ML20211F4531999-08-24024 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative to Defer Partial First Period Exams of flange-to-shell Weld to Third Period & Perform Required Ultrasonic Exams,Both Manual & Automated,During Third Period ML20211F5111999-08-23023 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative Contained in Request for Relief RR-ENG-30 ML20210C9411999-07-31031 July 1999 Rev 1 to SG-99-07-002, South Tx,Unit 1 Cycle 9 Voltage- Based Repair Criteria 90-Day Rept, Jul 1999 ML20210R3631999-07-31031 July 1999 Monthly Operating Repts for July 1999 for South Tx Project, Units 1 & 2.With ML20210D9161999-07-23023 July 1999 Safety Evaluation Accepting Inservice Testing Relief Request RR-56 Re Component Cooling Water & Safety Injection Sys Containment Isolation Check Valve Closure Test Frequency ML20210D4821999-07-21021 July 1999 1RE08 ISI Summary Rept for Steam Generator Tubing of South Texas Project Electric Generating Station Unit 1 ML20210D4491999-07-21021 July 1999 Revised Chapters to Operations QA Plan, Including Rev 9 to Chapter 1.0, Organization & Rev 6 to Chapter 16.0, Independent Technical Review NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With ML20207H6361999-07-0808 July 1999 Safety Evaluation Approving 2nd 10 Yr Interval ISI Program Plan Request to Use ASME Section XI Code Case N-546 for Licenses NPF-76 & NPF-80,respectively ML20216D7481999-07-0707 July 1999 1RE08 ISI Summary Rept for Welds & Component Supports of STP Electric Generating Station,Unit 1 NOC-AE-000593, Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program ML20195J6871999-06-17017 June 1999 Safety Evaluation Supporting Proposed Alternative Contained in RR-ENG-2-5.Proposed Alternative Authorized Per 10CFR50.55a(a)(3)(i) for 2nd ISI Interval ML20196A2391999-06-15015 June 1999 Change QA-042 to Rev 13 of Operations QAP, Reflecting Current Organizational Alignment for South Texas Project & Culminating Organizational Realigment That Has Been Taking Place During Past Several Months NOC-AE-000563, Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with ML20206U5411999-05-18018 May 1999 Non-proprietary Errata Pages for Rev 2,Addendum 1 to WCAP-13699, Laser Welded Sleeves for 3/4 Inch Diamete Tube Feedring Type & W Preheater SGs Generic Sleeving Rept ML20206A7721999-04-30030 April 1999 STP Electric Generating Station Unit 1 Cycle 9 Colr NOC-AE-000543, Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with ML20205H0321999-03-31031 March 1999 Change QA-040 to Rev 13 of Operations QA Plan NOC-AE-000507, Monthly Operating Repts for Mar 1999 for Stp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Stp,Units 1 & 2. with ML20205A3781999-03-22022 March 1999 STP Electric Generating Station Simulator Certification Four Yr Rept for Units 1 & 2 ML20204B2711999-03-15015 March 1999 Safety Evaluation Authorizing 990201 Request to Authorize Alternative to Regulations Per 10CFR50.55a(a)(3)(i) That Would Revise Start of Second 120-month IST Interval to No Later than 011201 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results NOC-AE-000468, Monthly Operating Repts for Feb 1999 for South Texas Project Electric Generating Station.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for South Texas Project Electric Generating Station.With ML20207D1101999-02-24024 February 1999 Change QA-039 to Rev 13 of Operations QA Plan, for STP ML20203H8361999-02-17017 February 1999 Safety Evaluation Supporting Request for Relief from ASME Code Requirements for Class 3 Piping for Plant ML20202H9621999-02-0303 February 1999 SER Accepting Change to EALs Used in Classification of Emergency Conditions ML20202E8471999-01-31031 January 1999 2RE06 ISI Summary Rept for SG Tubing of STP Electric Generating Station,Unit 2 ML20216G2011999-01-31031 January 1999 City Public Svc of San Antonio Annual Rept 1998-1999 ML20199G5961999-01-31031 January 1999 Cycle 7 Voltage-Based Repair Criteria Rept for Jan 1999 ML20199K7711999-01-21021 January 1999 Safety Evaluation Accepting ISI Program Request for Relief for ASME Cose Repair Requirements for Code Class 3 Piping ML20199G8161999-01-19019 January 1999 SER Accepting Util 970707 Response to NRC 970509 RAI Re GL 92-08, Thermo-Lag 330-1 Fire Barriers. NRC Finds No Significant Safety Hazards Based on Application of Util Ampacity Derating Methodology ML20199H4981999-01-11011 January 1999 2RE06 ISI Summary Rept for Welds & Component Supports of Stp,Unit 2 ML20206Q3751999-01-0404 January 1999 2RE06 ISI Summary Rept for Sys Pressure Tests (Class 1 & 2) ML20206Q3721999-01-0404 January 1999 2RE06 ISI Summary Rept for Repairs & Replacements ML20216G2171998-12-31031 December 1998 Houston Industries 1998 Annual Rept. App a 1998 Financial Statements & Us Securities & Exchange Commission Form 10-K Encl NOC-AE-000403, Monthly Operating Repts for Dec 1998 for South Texas Project Unit 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for South Texas Project Unit 1 & 2.With ML20216G1521998-12-31031 December 1998 Central & South West Corp 1998 Summary Annual Rept & Securities & Exchange Commission Form 10-K ML20198M3431998-12-28028 December 1998 SER Accepting Util Request for Relief from ASME Code Repair Requirements for ASME Code Class 3 Piping for South Texas Project,Unit 2 1999-09-09
[Table view] |
Text
-
ERC FORM 366 U.S. NUCLEN! REGULATCCtf COMMISS!(D QPPCOL'ED B7 OMB WO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BUROEN PER RESPONSE TO COMPLY BITH I I " LL LICENSEE EVENT REPORT (LER) Eggg"'U"c"g*
c MENS REGARDING BU DEN ST) ATE b THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMIS$10N, (See reverse for required number of digits / characters for each block) WASH]NGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJEC1 (3150-0104), OFFICE OF MANAGEMENT AND BUDCET, WASHINGTON, DC 20503.
FACILITY KAME (1) DOCKET NUMBER (2) PAGE (3)
South Texas, Unit 1 05000 498 1 OF 7 TITLE (4) Extension Of FWIBV Positioner and Solenoid Equipment Beyond Oualification Life EVENT DATE (5) LER NUMBE R (6) REPORT DATE (7) OTHE R F ACILITIES INVOLVED (8)
SEQUENTIAL REVIS10N FACILITY KAME DOCKET NUMBER MONTH DAY YEAR YEAR g g MONTH DAY YEAR South Texas, unit 2 05000499 05 27 93 93 -- 017 -- 01 07 20 93 O O OPERATING THM MMT M WBMlHED MWANT T THE RNRW NTS OF 10 CFR D Wck one or nm) (M) 5 20.402(b) 20.405(c) 50.73(a)(2)( i v) 73.71(b)
MODE (5)
POWER 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c) 0 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) x OTHER LEVEL (10) 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) 20.405(a)(1)(iv) 50. 73(a )(2)( i i ) 50.73(a)(2)(viii)(B) in Text, NRC form '
20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) 366A) Volmtary l
LICENSEE CONTACT FOR 1HIS L ER (12) hAME TELEPHONE NUMBER (include Area Code)
Jairo Pinzon - Senior Engineer (512) S72 - 8027 COMPL ETE ONE LINE FOR EACH COMPONE NT FAltVEE DESCRIBE D IN THIS RE PORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER SUPPLEMENTAL REPORT EXPECTED (14) EXPE CT ED MONTH DAY YEAR YES(if yes, complete EXPECTED SUBMISSIDW DATE). X No AT (5 ABS 1RACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) j On May 27, 1993, Unit 1 was in Mode 5 at 0% power and Unit 2 was defueled in a refueling outage. Plant personnel concluded that, based on a May 21, 1993 determination that the Feedwater Isolation Bypass Valves (FWIBVs) in both units were inoperable since the pneumatic positioners and solenoids had remained in service beyond their qualified life, this event was reportable. STP personnel determined that Technical Specification 3.7.1.7 had been violated during various modes of operation since 1992. The inappropriate extension of the equipment qualification life of the FWIBV positioner and solenoids was the result of incorrectly interpreting design documents. Corrective actions include reviewing other safety-related ,
valves with positioners for similar problems, reviewing other solenoid l valves qualified for service in a harsh environment to determine if similar problems could exist, reviewing safety-related components which have been !
classified as non-safety to determine generic implications, and modifying I the pneumatic control scheme of the FWIBV to ensure closure of the valves independent of the positioner upon de-energization of the safety-related solenoid valves. Further evaluation determined that the qualified life of the FWIBV positioners and solenoids had, in fact, not been exceeded and no !
violation of Technical Specifications occurred.
NkC FOAM 366 (542) 9'307290.167 9307po DR ADOCK 05000498 PDR LE R-93 \L93017R1.U1
NRC FORM 3664 U.S. C28 CLEAR REeJLATOV COMMISSIC APPROVED BY OMB Wo. 3150-0104 (5-92) EXP!RES 5/31/95 ESTIMATED DURDEN PER RESPONSE TO COMPLY WITH THis INFORMATION COL LECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS EECARDING BURDEN ESTIMATE TO THE LICENSEE EVENT REPORT (LER) INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB TEXT CONTINUATION 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001 AN3 TO THE PAPERWORK REDUCTION PROJECT (31$0-0104), OFFICE OF MANAGEMENT AND BUDCFT, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKFT NUMRTR (?) LFR WUMBER (6S PACF (3)
YEAR SEQUENTIAL REVISION South Texas, Unit 1 05000 498 2 OF 7 93 -- 017 -- 01 TEXT (if more space is reouired. use additional copies of Not Form 366A) (17)
DESCRIPTION OF EVENT:
On May 27, 1993, Unit 1 was in Mode 5 at 0% power and Unit 2 was defueled in a refueling outage. Plant personnel concluded that, based on a May 21, 1993 determination that the FWIBVs in both units were inoperable since the pneumatic positioner and solenoids had remained in service beyond their qualified life, this event was reportable. STP personnel determined that Technical Specification 3.7.1.7 had been violated during various modes of operation since 1992. Technical Specification 3.7.1.7 requires that each FWIBV be operable while in Modes 1, 2 ar_d 3.
POSITIONERS On May 21, 1993, as a result of an investigation to resolve a FWIBV valve position indication issue, an STP engineer noted that the FWIBV positioner EQ documentation stated that the positioners were classified as non-safety related. The STP engineer questioned the basis of the quality classification, since he understood that the positioners were required to function to close the FWIBV during a Main Feedwater isolation.
The FWIBV positioners were classified, procured and installed as safety related components under the original Main Feedwater system design. However, based on an Architect Engineer's memorandum stating that STP pneumatic positioners do not perform any safety functions and threefore are not subject to EQ requirements, STP Engineering downgreded the FFI?T positioners to non-safety related and extended their life 1.0 40 years cm September 16, 1986. No hardware changes were made as a result of the change in classification.
Further review of the plant design documentatiin acnfirmed that the positioners do perform a safety function during a Mr.>r Feedwater isolation, and therefore, the EQ requirements should have been raintained. Based on these findings, a new qualified life calculation was amediately performed.
A review of the FWIBV positioner EQ report revealed that replacement of the positioner's sensitive parts is required every four yairs based on a maximum continuous operating temperature of 300F and a thres. ,ld radiation dose of 10E6 rads. This replacement interval is based on a worst case effect (under an assumed bounding maximum operating temperature or radiation exposure) to the age-sensitive materials in the positioner. Since the design basis radiation dose for a postulated accident in the Isolation Valve Cubicle at STP is less than the threshold radiation limit, operating temperature is the limiting factor for qualified life of positioners at STP. However, no precise measurement or estimate of positioner operating temperature was available.
As a result, positioner qualified life was re-calculated to be five years based on a conservatively assumed maximum continuous operating temperature less than 212F. Since the Unit 1 FWIBV positioners qualified life expired on June 6,1992, HL&P conservatively concluded that the Unit 1 positioners had LER-93\L93017R1.U1
NRC FORM 366A U.S. CELEAR REGULATORY COMMISSIC APPROVED BY OMB CD. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER ttESPONSE TO COMPLY WITH THl$
. INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN EST! MATE TO THE LICENSEE EVENT REPORT (LER) INr0RMAt!ON AND RECORDS MANAGEMENT BRANCH (MNBB TEXT CONTINUATION 7714), u.S. NUCLEAR REGULA10RY COMMISSION, WASHINGTON, DC 20555-0001 AND TO THE PAFERWORK REDUCTION PROJECT (31$0-0104), OFFICE OF LMANAGEMENT AND BUDGET, WASHINGTON, DC ?0503.
FACllITY NAME (1) DOCKET NUMRER (2) LFR WlMBER (61 PAGE (3)
YEAR SEQUENTIAL REVISION Nuu m Nuw m South Texas, Unit 1 05000 498 3 OF 7 93 -- 017 -- 01 TEXT (If mor e space is reauire<t use additional copies of ARC Form 366A) (17)
DESCRIPTION OF EVENT: (Cont'd) been technically inoperable for 1. 5 years. The Unit 2 FWIBV positioners were found to be operable since they had not yet exceeded a five year life.
As a result of the new life calculations, service requests (SRs) were written to install a modification to the pneumatic control scheme of the FWIBV to ensure closure of the valves, independent of the positioner, upon de-energization of the safety-related solenoid valves. Since the positioner would no longer be required to perform a safety function, the requirement for EQ was deleted.
HLLP continued to evaluate the operability of the positioners. The installed configuration of the positioner has it attached to the FWIBV valve operator yoke. Subsequently, a heat transfer calculation was developed which demonstrated that the maximum yoke temperature during plant operation is 162F.
While actual positioner temperature would be less than 162F because of air flow cooling and because of the limited heat transfer capability of the positioner / yoke attachment, a conservatively assumed positioner operating temperature of 162F was used to calculate a qualified life of over 8 years.
As a result, HL&P has concluded that the FWIBV positioners were within their qualified life and there was no operability concern relative to the positioner.
A five step plan wcs established to address the gencric implication of the declassification of the FWIBVs safety-related positioners and solenoids. This plan included reviews of the classification of all Valtek valve positioners, !
positioners provided for safety-related valves, and Heating, Ventilating and l Air Conditioning system dampers. This plan also provided for reviews of active parts declassified by use of Technical Evaluations for proper consideration of system / component operation, a sample of EQ packages for proper consideration of system / component operation, and reviews of EQ for solenoids which are normally energized but were evaluated as normally de-energized.
This review resulted in identifying twelve additional valves per unit where failure of the positioner could cause the valve to be mispositioned. Further review revealed the valves are located in a mild environment and do not require periodic replacement. Other solenoids of the same model used with the FWIBVs were identified and action taken to replace them. These additional solenoids were on non-safety related Steam Generator Augmented Blowdown valves, which do not have a qualified life limitation.
LER-93\L93017R1.U1
i i
'NRC FORM 366A U.S. Q) CLEAR RECULATC3Y CDtMISSION APPROVED BY OMB NO. 3150-0104 (5-92) ,
EXPIRES 5/31/95 ESilMATED BURDEN PE2 DESPONSE TO COMPLY WITH THIS i INFORMATION COLLECTION REQUEST: 50.0 HRS.
I FORWARD CCMMENTS REGARDING BURDEN ESilMATE TO THE 1 LICENSEE EVENT REPORT (LER) INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB l TEXT CONTINUATION 7714), U.S. NUCLEAR REGULATORY COMMISSION, j WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK i REDUCTION PROJECT (31$0-0104), OFFICE OF MANAGEMENT AND BUDCET, WASHINGTON, DC 20503.
FAClllTY NAME (1) DOCKET Nt#tBER (2) LER NUMBER (65 PAGE (3)
YEAR SEQUENTIAL REVISION ]
South Texas, Unit 1 05000 498 4 OF 7 93 -- 017 -- 01 TEXT (if more space is reouired, use additional copies of NRC Form 366A) (17)
DESCRIPTION OF EVENT: (Cont'd)
SOLENOIDS I
On May 28, 1993, as part of the continuing investigation of the FWIBV issues, an STP engineer reviewing the Equipment Qualification Calculation Package (EQCP) for the FWIBV safety-related solenoids, questioned the assumptions used in determining their qualified life. Calculation E-89-ASCO, Revision 3, indicated that the solenoids are only energized during feedwater heatup and not during normal operation resulting in a qualified life of forty years.
Review of the logic drawings for these valves showed that there are three solenoids for each FWIBV. One non-Class 1E solenoid is controlled by a main control board handswitch and is normally de-energized. The other two Class 1E solenoids are each controlled by a combination of the Main Feedwater Isolation Valve control switches and a Feedwater Isolation signal from the Solid State Protection System. A review of the design documents showed that these two safety-related solenoids are energized during normal plant '
operations. As a result of recalculating the life of the solenoids in the normally energized state using worst case design basis assumptions, the '
qualified life was determined to be 2.5 years. As a result, HL&P conservatively concluded that the FWIBV solenoids qualified life expired in l December 1989 for Unit 1 and June 1991 for Unit 2.
As with the positioners, HL&P continued to evaluate the operability of the FWIBV solenoids. The solenoid coil had been the limiting component in the j qualified life calculation. After several discussions with ASCO's technical representatives, STP engineering determined that the failure of the solenoid's coil did not prevent the valve from performing its safety function. Solenoid '
coil failure would result in the FWIBV failing in the required position. As l a result, the solenoid's qualified life was re-calculated based on the next most limiting component and the new qualified life was determined to be over 30 years. Therefore, HL&P has concluded that the FWIBV solenoids were within their qualified life. Further, HL&P has concluded that the FWIBVs were operable at all times because the FWIBV positioners and solenoids were within their qualified life.
Although the FWIBV solenoids were proven to be operable, other solenoid valves qualified for service in a harsh environment were reviewed to determine if a similar condition could exist where an incorrect assumption that the solenoid was de-energized when they were actually energized was made. The review included ASCO, Valcor and Target Rock solenoids. This review resulted in a reduction in qualified life for the Preheater Bypass valves and the Main Steam Bypass valves ASCO solenoids. Although their qualified lives have been reduced, they have not yet expired.
LER-93\L93017R1.U1 l
'NRC FOR'M 366A U.S. CDCLEAR REGJLATO Y COMMISSI C APPROUED BY OMB C3. 3150-0104 (542) ,
EXPIRES 5/31/95 ESilMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN EST! MATE TO THE LICENSEE EVENT REPORT (LER) INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB TEXT CONTINUATION m 4), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150 0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NLMBER (2) LER MMFIER (61 PAGE (3)
YEAR SEQUENT 14L REVISION South Texas, Unit 1 05000 498 5 OF 7 93 -- 017 -- 01 TEXT (If more sDece is reovired, use additional copies of NRC Form 366A) (17)
CAUSE OF EVENT:
In both cases, the erroneous qualified life extensions of the FWIBV l positioners and solenoid valves were the result of incorrectly interpreting design documents.
ANALYSIS OF EVENT:
Upon discovery of the inappropriate extension of the EQ life the FWIBVs were conservatively declared inoperable. Further evaluation of the operability of the positioners and solenoids revealed that, in fact, the EQ life had not been exceeded and thus, were not inoperable. Had the FWIBV, in fact, been inoperable, the events described in this report would represent an operation or condition prohibited by Technical Specification 3.7.1.7 and would have been reportable pursuant to 10CFR50. 7 3 (a) (2) (i) (B) . Based on the above '
considerations, there is no safety significance from this event. I CORRECTIVE ACTIONS: !
l l
- 1. The Preventive Maintenance (PM) activities for EQ replacement for the PWIBV solenoids have been reactivated. ,
1
- 2. A review of other safety-related valves with positioners was performed to l identify similar concerns. A group of twelve Chilled Water valves was !
identified with a similar configuration; however, these valves are not located in a harsh environment and no periodic parts replacement is required to maintain the qualification. Further investigation revealed that the EQ of the Chilled. Water valve positioners have not been altered.
l
- 3. A modification to revise the pneumatic control scheme of the FWIBVs to ensure closure of the valves independent of the positioner upon de-energization of the safety-related solenoid valves, has been developed.
This modification has been implemented in Unit 1 and will be implemented by the end of the current refueling outage in Unit 2. j l
- 4. A review of other solenoid valves qualified for service in a harsh I environment was performed to determine if a similar problem existed. This review included ASCO, Valcor and Target Rock solenoid valves. This review resulted in a reduction in qualified life for the Preheater Bypass valve and Main Steam Bypass valve ASCO solenoids. Although reduced, their qualified lives, have not yet expired. EQ PM activities will be developed to ensure replacement prior to expiration. !
LER-93\L93017R1.01
'WRC FORM 366A U.S. CUCLEAR RECULATC2Y COMMISSIC2 APPROVED BY OMB WO. 3150-0104 ,
(5-92) ,
EXP!RES 5/31/95 !
l ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH TH]S I INFORMATION COLLCCTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE LICENSEE EVENT REPORT (LER) thF0RMATION AND RECORDS MANAGEMENT BRANCH (MNBB TEXT CONTINUATION 7714), U.S. NUCLEAR REGULATORY COMMISSION, l WASHINGTON, DC 20555 0001, AND TO THE FAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACItITY NAME (1) DOCKET NUMBER (?) LFR NUMBER (61 PAGE (3)
YEAR SEQUENTIAL REVISION j
" " " " " " I South Texas Unit 1 05000 498 6 OF 7 93 -- 017 -- 01 TEXT (11 mre sr> ace is recuired, use additional copies of ARC Form 366A) (17)
CORRECTIVE ACTIONS: (Cont'd)
- 5. Information regarding the positioner and solenoid events has been provided to Engineering personnel as lessons learned. In addition, Engineering personnel were sensitized on the need for attention to detail with regard to EQ and verifying assumptions.
- 6. To address generic implications, a five-step review process was developed to evaluate the part reclassifications and EQ issues indicated as a result of this LER. This review has not resulted in any additional plant safety issues. As a result of this review, the sample scope has been expanded.
This additional review will be completed by July 21, 1993. Based on this additional review, corrective actions and recurrence control measures will be developed as necessary.
bpDITIONAL INFORMATION:
1 The FWIBV positioners are manufactured by Valtek and are model number 80R.
The FWIBV solenoids are manufactured by ASCO and are model numbers 206-832-4VF, NP831655E, and NP8321A2E/A6E.
During the past two years, two LERs have been submitted to the NRC which were related to Equipment / Environmental Qualification problems. These LERs are as follows:
o Unit 1 LER 93-016 regarding a Technical Specification violation due to Circuitry for the Steam Generator Power Operated Relief Valves and Reactor Coolant System Subcooling Margin monitor being inoperable.
o Unit 2 LER 93-008 regarding a Technical Specification violation due to a f ailure to maintain Environmental Qualification of a Residual Heat Removal Motor Operated Valve.
o Unit 2 LER 93-010 regarding a failure of an Essential Cooling Water traveling screen drive coupling.
The following information is with regard to an event that was discovered on April 21, 1993, in which the FWIBV was thought to be open when a Maintenance technician may have observed pointer movement on the stem clamp during 1 maintenance work on the FWIBV. The technician believed that since the perceived pointer movement on the stem clamp was sudden, the valve stem had moved and the valve had been partially open. HL&P conservatively concluded I that the event was reportable because the plant had operated in various modes with the valve inoperable contrary to Technical Specifications. The valve was thought to be open since April 25, 1992. Further investigation determined that the valve, in fact, was closed as required during this time period.
LER-93\L93017R1.U1
v NRCFhRM366A U.S. t:JCLEAR RECULATC27 (XMMISSIC2 APPROVED BY OMB NO. 3150-0104 (5-92) ,
EXPIRES 5/31/95 ESilMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS RECARD!bG BURDEN ESTIMATE TO THE LICENSEE EVENT REPORT (LER) INr0RMATION AND RECORDS MAhAGEMENT BRANCH (MNBB TEXT CONTINUATION 7714), u.S. NUCLEAR REGULATORY COMMISSION, WASHlWGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (31$0-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON. DC 20503.
FACILITY kAMF (1) DOCKFT NUMBER (?) (ER NUMBER (61 PACE (3)
SEQUENTIAL REVISION YEAR South Texas, Unit 1 05000 498 7 OF 7 93 -- 017 -- 01 TEXT (If more space is reovired, use additional copies of KRC Form 366A) (17)
ADDITIONAL INFORMATION: (Cont'd)
On May 22, 1993, Fisher Service Company performed a series of diagnostic tests to determine the overall operating condition of the valve. The tests verified that the valve stroke, packing friction, and seat load were within specifications, but did indicate minor resistance in the upper portion of the stroke. This resistance did not prevent or hinder the valve from stroking.
Fisher felt that the resistance could be from galling in the stem guide area ,
or packing material buildup on the stem of the valve. The actuator spring rate, total travel, and bench settings were within specifications. On May 25, 1993, the FWIBV was disassembled and an inspection performed by Engineering ,
and Maintenance personnel revealed signs of normal wear except for thread damage on the upper 5/8 in. of the actuator stem and valve plug stem. There were no indications of any sticking or binding in the valve actuator or body. i On May 26, 1993 the Valtek vendor was brought in to inspect the valve.
Valtek's inspection concurred with HL&P's finding.
This determination is based on the following: l o The I&C technician was not certain he witnessed valve sten movement. '
1 o Valve travel is limited by plug motion between seat and backseat which was j measured to be 1.672 inches. The limit switch settings were found approximately 1.5 inches apart, indicating that the valve had been stroking fully.
l-o No physical evidence was found upon inspection of the valve components I which could have caused or indicated mechanical binding of the valve.
o The discovered thread damage on the actuator stem and valve plug stem at the point of overlap suggests that when the valve stem clamp was loosened for maintenance, the valve actuator stem moved downward while the valve plug stem was stationary due to the valve plug being seated. This also accounts for the observed pointer movement.
HL&P has analyzed Fisher's diagnostic test and Valtek's report. On the basis of this report and HL&P's investigations, HL&P has determined that the valve was, in fact, not open and this event is no longer reportable.
LE R-93\L93017R1.U1