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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6321994-05-0202 May 1994 LER 94-002-01:on 940115,centrifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to Requirements of TS 3.1.2.3.Caused by hydro-pneumatic Transient.Valves Labeled W/Caution statements.W/940502 Ltr ML20029D6351994-04-27027 April 1994 LER 94-006-01:on 940214,reactor Manually Tripped Following Unanticipated Test Results.Caused by Mod Which Failed post- Mod Test.Test Terminated & Solid State Rod Control Sys Returned to Original Design configuration.W/940427 Ltr ML20029C6951994-04-18018 April 1994 LER 94-011-00:on 940310,safety Injection Actuation Was Received on Trains A,B & C.Cause Was Failure to Adhere to Procedure.Corrective Actions:Restored Cooling Shutdown & Removed Personnel from watchbill.W/940418 Ltr ML17352B2581994-03-25025 March 1994 LER 94-007-00:on 940224,station Procedure for Testing Reactor Trip Bypass Breakers Did Not Satisfy Ts.Caused by Inadequate Procedure Preparation & Review.Surveillance Procedure Enhancement Program underway.W/940325 Ltr ML20046C5471993-08-0606 August 1993 LER 93-018-00:on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST plan.W/930806 Ltr ML20046C4901993-08-0505 August 1993 LER 93-019-00:on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing discrepancy.W/930805 Ltr ML20046B1291993-07-29029 July 1993 LER 93-012-00:on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel cooling.W/930729 Ltr ML20046A6791993-07-21021 July 1993 LER 93-011-00:on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway ML20046A6511993-07-20020 July 1993 LER 93-017-01:on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified ML20045J0281993-07-15015 July 1993 LER 93-016-01:on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 QDPS.W/930715 Ltr ML20045H9171993-07-14014 July 1993 LER 93-008-01:on 930505,discovered That RHR Pump Suction MOV Had Not Been Environ Qualified Since 901129 Because Replacement of Drain T Not Completed.Drain T Missing from RH-0060B Replaced & Bulletin Issued to Maint Dept ML20045H9881993-07-13013 July 1993 LER 93-012-01:on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings. W/930713 Ltr ML20045E1531993-06-25025 June 1993 LER 93-017-00:on 930527,determined That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioner & Solenoids Remained in Svc Beyond Qualified Life.Caused by Incorrect Interpretation of Design Documents.Mod Underway ML20045E1491993-06-25025 June 1993 LER 93-010-00:on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint initiated.W/930625 Ltr ML20045B2731993-06-0909 June 1993 LER-93-016-00:on 930503,TS Violation Occured Due to Circuitry for SG PORVs & RCS Subcooling Monitor Being Inoperable.Caused by Less than Adequate Work Practices. Screws Missings from Qdps Replaced & Walkdown Performed ML20045A3831993-06-0404 June 1993 LER 93-008-00:on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain ML20044G4301993-05-25025 May 1993 LER 93-009-00:on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref values.W/930525 Ltr ML20044F6281993-05-21021 May 1993 LER 93-015-00:on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans monitored.W/930521 Ltr ML20044F1321993-05-20020 May 1993 LER 93-009-01:on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort ML20044E0371993-05-14014 May 1993 LER 93-005-01:on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training ML20024H2571991-05-24024 May 1991 LER 91-014-00:on 910420,erratic Containment Extended Range Pressure Channel Output Occurred.Caused by Bad Control Card. Weekly Channel Checks Performed,Control Card Replaced & Channel calibrated.W/910524 Ltr ML20024H2081991-05-22022 May 1991 LER 91-015-00:on 910422,train C AFW Pump Inadvertently Started Due to Failure of Led in Sequencer Test Circuitry. Faulty Led Replaced & Blocking Circuit Satisfactorily tested.W/910522 Ltr ML20029C1221991-03-15015 March 1991 LER 91-004-00:on 910215,loss of Offsite Power Actuation Occurred During Routine Maint.Caused by Lack of Attention to Work Performance Methods.Training Conducted for Maintenance personnel.W/910315 Ltr ML20029B0421991-02-25025 February 1991 LER 91-002-00:on 910126,automatic Actuation of Safety Injection Sys Occurred in One of Three Train C Trains.Caused by Inadequate Work Instructions for Maint Activity.Training Bulletin Issued & Supervisors counseled.W/910225 Ltr ML20024F7451990-12-12012 December 1990 LER 90-017-00:on 901104,discovered That Train a of Class IE 120-volt Distribution Panel DP001 Energized from Alternate Power Supply.Caused by Less than Adequate Administrative Controls.Log Will Be utilized.W/901212 Ltr ML20044B1691990-07-0606 July 1990 LER 90-011-00:on 900612,chemical Technician Supervisor Discovered That No Sample Collected in Condenser Air Removal Sys Radiation Monitor Moisture Collection Tank. Caused by Inadequate procedure.W/900706 Ltr ML20043G2091990-06-14014 June 1990 LER 90-010-00:on 900515,determined That Leak & Contamination Test Interval for Some Radioactive Sources Exceeded Tech Specs.Caused by Insufficient Detail in Procedures.Test Program revised.W/900614 Ltr ML20043G5191990-06-14014 June 1990 LER 90-010-00:on 900515,unplanned Actuation of ESF Train C Standby Diesel Generator Occurred.Caused by Personnel Error. Training Bulletin Will Be Issued to Maint Personnel Re event.W/900613 Ltr ML20043G1791990-06-13013 June 1990 LER 90-009-00:on 900512,incorrect Wiring in Solid State Protection Sys Discovered.Caused by Inadvertent Installation of Extra Wire by Mfg.Extra Wire Removed & Sys Successfully tested.W/900613 Ltr ML20043G2101990-06-13013 June 1990 LER 90-009-00:on 900514,discovered That Printer for Toxic Gas Analyzer XE-9325 Was Not Updating & Surveillances for Toxic Gas Monitor XE-9325 Incorrectly Performed on 900511. Caused by Inadequate training.W/900613 Ltr ML20043G7681990-06-0808 June 1990 LER 90-008-00:on 900508,Tech Spec Required Shutdown Initiated Due to Primary Coolant Sys Leakage.Caused by High Cycle Fatigue Failure of Weld on Upstream Side of Drain Valve.Drain Valves replaced.W/900608 Ltr ML20043E7001990-06-0404 June 1990 LER 90-008-00:on 891007,Tech Spec Violation Occurred Due to Failure to Perform post-maint Testing.Caused by Incorrect Determination That No post-maint Testing Required.Personnel counseled.W/900604 Ltr ML20043C7401990-05-30030 May 1990 LER 90-007-00:on 900430,discovered That All Three Trains of ESFAS Placed in Test & Incapable of Actuating for Approx 35 Minutes.Caused by Inadequate Prerequisite Conditions in Maint Procedure.Procedure Being modified.W/900530 Ltr ML20043C4791990-05-29029 May 1990 LER 90-007-00:on 900426,standby Diesel Generator 22 Room High Sump Level Alarm Actuated in Control Room.Caused by Flooding & Inadequate Spec of Sealing & Testing Requirements.Seals on Removable Panels caulked.W/900529 Ltr ML20043B6611990-05-25025 May 1990 LER 90-006-00:on 900426,control Room Ventilation Sys Actuated to Recirculation Mode Due to High Level Trip of Vinyl Acetate Channel on Gas Analyzer.Caused by Failure of electro-mechanical Positioner.Part replaced.W/900525 Ltr ML20043A7811990-05-15015 May 1990 LER 90-005-00:on 900414,simultaneous Reactor & Turbine Trip Occurred Due to Failure of Main Turbine Electrohydraulic Control Line.Caused by Fatigue Stress of Weld.Valve Modified to Add anti-swirl Baffles & anti-rotation pins.W/900515 Ltr ML20042F2191990-05-0202 May 1990 LER 90-005-00:on 900329,feedwater Booster Pump 11 Tripped Upon Actuation of Ground Fault Relay & Standby Pump 13 Started But Did Not Deliver Sufficient Flow to Prevent Trip. Cause Not Found.Inlet Filters to Be cleaned.W/900502 Ltr ML20042E3561990-04-0505 April 1990 LER 89-015-01:on 890704,reactor Trip Occurred.Caused by Failure of Relay in Generator Breaker Trip Circuit.Relays in Generator Breaker Trip Circuits Replaced W/Correct Models & Checked to Ensure Proper rating.W/900405 Ltr ML20012C7211990-03-16016 March 1990 LER 90-003-00:on 900214,discovered That Train B Fuel Handling Bldg Exhaust Air Filter Outlet Damper Would Not Open.Caused by Wiring Error Due to Failure of Technicians to Follow Work Instructions.Technicians counseled.W/900316 Ltr ML20012B4381990-03-0101 March 1990 LER 90-002-00:on 900202,Train s Reactor Trip Breaker Opened, Initiating Turbine & Reactor Trip & Feedwater Isolation on Low Average RCS Temp.Cause Unknown.Universal Logic Cards Replaced & Monitoring Instruments installed.W/900301 Ltr ML20006E3781990-02-16016 February 1990 LER 90-001-00:on 900103,containment Ventilation Isolation Occurred Due to Loss of Power to Radiation Monitor Actuation Relay.Caused by Technician Lifting Power Lead. Technicians Trained & counseled.W/900216 Ltr ML20006E4001990-02-12012 February 1990 LER 90-001-00:on 900108,Train s Low Steam Line Pressure Blocking Switch Placed in Blocked Position,Causing Actuation of Safety Injection & ESF Sys.Caused by Lack of Instructions.Training Program modified.W/900212 Ltr ML20006D4231990-02-0202 February 1990 LER 90-002-00:on 900103,redundant Solenoid Valve Which Actuates Train C Feedwater Valve Failed.Caused by Excessive Particulate Buildup.Solenoids Cleaned & Hydraulic Oil Flushed & Filtered to Remove particulate.W/900202 Ltr ML20006D5591990-02-0202 February 1990 LER 89-023-01:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Declared Inoperable. Caused by Contact Oxidation & Low Contact Pressure.Chiller Auxiliary Relay Cleaned & adjusted.W/900202 Ltr ML20006B4731990-01-25025 January 1990 LER 89-024-00:on 891226,required Sample from Safety Injection Accumulator 1C of Boron Concentration Not Taken. Caused by Insufficient Administrative Controls to Track Surveillance Tests.Bulletin Will Be issued.W/900125 Ltr ML20006B2551990-01-19019 January 1990 LER 89-022-00:on 891205,discovered That ASME Section XI Pressure Test of Train C of Component Cooling Water Sys Not Performed Prior to Returning Sys to Svc.Sys Inoperable from 890909-1206.Test Control Procedures revised.W/900119 Ltr ML20006B2221990-01-16016 January 1990 LER 89-023-00:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Attempt to Secure Essential Chiller 12C Resulted in Trip.Caused by Failure of Voltage Regulator.Regulator Returned to mfg.W/900116 Ltr ML20005E2471989-12-29029 December 1989 LER 89-028-00:on 891130,control Room Ventilation Sys Actuated to Recirculation Mode as Result of Spurious Signal. Caused by Memory Error Causing Microprocessor to Energize Relay Incorrectly.Troubleshooting planned.W/891229 Ltr ML19332D7741989-11-24024 November 1989 LER 89-018-01:on 890922,discovered That Const Installation Procedure for Reg Guide 1.97,Rev 2 Instrumentation Did Not Include Details to Ensure Qualification Per 10CFR50.49 or IEEE 323-1974.Caused by Installation error.W/891124 Ltr ML19332C8661989-11-21021 November 1989 LER 89-027-00:on 891025,discovered That Closed Limit Switch on Main Turbine Throttle Valve 2 Disconnected.Caused by Failure of Limit Switch Linkage.Review to Be Performed of Limit Switch Linkage design.W/891122 Ltr 1994-05-02
[Table view] Category:RO)
MONTHYEARML20029D6321994-05-0202 May 1994 LER 94-002-01:on 940115,centrifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to Requirements of TS 3.1.2.3.Caused by hydro-pneumatic Transient.Valves Labeled W/Caution statements.W/940502 Ltr ML20029D6351994-04-27027 April 1994 LER 94-006-01:on 940214,reactor Manually Tripped Following Unanticipated Test Results.Caused by Mod Which Failed post- Mod Test.Test Terminated & Solid State Rod Control Sys Returned to Original Design configuration.W/940427 Ltr ML20029C6951994-04-18018 April 1994 LER 94-011-00:on 940310,safety Injection Actuation Was Received on Trains A,B & C.Cause Was Failure to Adhere to Procedure.Corrective Actions:Restored Cooling Shutdown & Removed Personnel from watchbill.W/940418 Ltr ML17352B2581994-03-25025 March 1994 LER 94-007-00:on 940224,station Procedure for Testing Reactor Trip Bypass Breakers Did Not Satisfy Ts.Caused by Inadequate Procedure Preparation & Review.Surveillance Procedure Enhancement Program underway.W/940325 Ltr ML20046C5471993-08-0606 August 1993 LER 93-018-00:on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST plan.W/930806 Ltr ML20046C4901993-08-0505 August 1993 LER 93-019-00:on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing discrepancy.W/930805 Ltr ML20046B1291993-07-29029 July 1993 LER 93-012-00:on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel cooling.W/930729 Ltr ML20046A6791993-07-21021 July 1993 LER 93-011-00:on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway ML20046A6511993-07-20020 July 1993 LER 93-017-01:on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified ML20045J0281993-07-15015 July 1993 LER 93-016-01:on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 QDPS.W/930715 Ltr ML20045H9171993-07-14014 July 1993 LER 93-008-01:on 930505,discovered That RHR Pump Suction MOV Had Not Been Environ Qualified Since 901129 Because Replacement of Drain T Not Completed.Drain T Missing from RH-0060B Replaced & Bulletin Issued to Maint Dept ML20045H9881993-07-13013 July 1993 LER 93-012-01:on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings. W/930713 Ltr ML20045E1531993-06-25025 June 1993 LER 93-017-00:on 930527,determined That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioner & Solenoids Remained in Svc Beyond Qualified Life.Caused by Incorrect Interpretation of Design Documents.Mod Underway ML20045E1491993-06-25025 June 1993 LER 93-010-00:on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint initiated.W/930625 Ltr ML20045B2731993-06-0909 June 1993 LER-93-016-00:on 930503,TS Violation Occured Due to Circuitry for SG PORVs & RCS Subcooling Monitor Being Inoperable.Caused by Less than Adequate Work Practices. Screws Missings from Qdps Replaced & Walkdown Performed ML20045A3831993-06-0404 June 1993 LER 93-008-00:on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain ML20044G4301993-05-25025 May 1993 LER 93-009-00:on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref values.W/930525 Ltr ML20044F6281993-05-21021 May 1993 LER 93-015-00:on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans monitored.W/930521 Ltr ML20044F1321993-05-20020 May 1993 LER 93-009-01:on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort ML20044E0371993-05-14014 May 1993 LER 93-005-01:on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training ML20024H2571991-05-24024 May 1991 LER 91-014-00:on 910420,erratic Containment Extended Range Pressure Channel Output Occurred.Caused by Bad Control Card. Weekly Channel Checks Performed,Control Card Replaced & Channel calibrated.W/910524 Ltr ML20024H2081991-05-22022 May 1991 LER 91-015-00:on 910422,train C AFW Pump Inadvertently Started Due to Failure of Led in Sequencer Test Circuitry. Faulty Led Replaced & Blocking Circuit Satisfactorily tested.W/910522 Ltr ML20029C1221991-03-15015 March 1991 LER 91-004-00:on 910215,loss of Offsite Power Actuation Occurred During Routine Maint.Caused by Lack of Attention to Work Performance Methods.Training Conducted for Maintenance personnel.W/910315 Ltr ML20029B0421991-02-25025 February 1991 LER 91-002-00:on 910126,automatic Actuation of Safety Injection Sys Occurred in One of Three Train C Trains.Caused by Inadequate Work Instructions for Maint Activity.Training Bulletin Issued & Supervisors counseled.W/910225 Ltr ML20024F7451990-12-12012 December 1990 LER 90-017-00:on 901104,discovered That Train a of Class IE 120-volt Distribution Panel DP001 Energized from Alternate Power Supply.Caused by Less than Adequate Administrative Controls.Log Will Be utilized.W/901212 Ltr ML20044B1691990-07-0606 July 1990 LER 90-011-00:on 900612,chemical Technician Supervisor Discovered That No Sample Collected in Condenser Air Removal Sys Radiation Monitor Moisture Collection Tank. Caused by Inadequate procedure.W/900706 Ltr ML20043G2091990-06-14014 June 1990 LER 90-010-00:on 900515,determined That Leak & Contamination Test Interval for Some Radioactive Sources Exceeded Tech Specs.Caused by Insufficient Detail in Procedures.Test Program revised.W/900614 Ltr ML20043G5191990-06-14014 June 1990 LER 90-010-00:on 900515,unplanned Actuation of ESF Train C Standby Diesel Generator Occurred.Caused by Personnel Error. Training Bulletin Will Be Issued to Maint Personnel Re event.W/900613 Ltr ML20043G1791990-06-13013 June 1990 LER 90-009-00:on 900512,incorrect Wiring in Solid State Protection Sys Discovered.Caused by Inadvertent Installation of Extra Wire by Mfg.Extra Wire Removed & Sys Successfully tested.W/900613 Ltr ML20043G2101990-06-13013 June 1990 LER 90-009-00:on 900514,discovered That Printer for Toxic Gas Analyzer XE-9325 Was Not Updating & Surveillances for Toxic Gas Monitor XE-9325 Incorrectly Performed on 900511. Caused by Inadequate training.W/900613 Ltr ML20043G7681990-06-0808 June 1990 LER 90-008-00:on 900508,Tech Spec Required Shutdown Initiated Due to Primary Coolant Sys Leakage.Caused by High Cycle Fatigue Failure of Weld on Upstream Side of Drain Valve.Drain Valves replaced.W/900608 Ltr ML20043E7001990-06-0404 June 1990 LER 90-008-00:on 891007,Tech Spec Violation Occurred Due to Failure to Perform post-maint Testing.Caused by Incorrect Determination That No post-maint Testing Required.Personnel counseled.W/900604 Ltr ML20043C7401990-05-30030 May 1990 LER 90-007-00:on 900430,discovered That All Three Trains of ESFAS Placed in Test & Incapable of Actuating for Approx 35 Minutes.Caused by Inadequate Prerequisite Conditions in Maint Procedure.Procedure Being modified.W/900530 Ltr ML20043C4791990-05-29029 May 1990 LER 90-007-00:on 900426,standby Diesel Generator 22 Room High Sump Level Alarm Actuated in Control Room.Caused by Flooding & Inadequate Spec of Sealing & Testing Requirements.Seals on Removable Panels caulked.W/900529 Ltr ML20043B6611990-05-25025 May 1990 LER 90-006-00:on 900426,control Room Ventilation Sys Actuated to Recirculation Mode Due to High Level Trip of Vinyl Acetate Channel on Gas Analyzer.Caused by Failure of electro-mechanical Positioner.Part replaced.W/900525 Ltr ML20043A7811990-05-15015 May 1990 LER 90-005-00:on 900414,simultaneous Reactor & Turbine Trip Occurred Due to Failure of Main Turbine Electrohydraulic Control Line.Caused by Fatigue Stress of Weld.Valve Modified to Add anti-swirl Baffles & anti-rotation pins.W/900515 Ltr ML20042F2191990-05-0202 May 1990 LER 90-005-00:on 900329,feedwater Booster Pump 11 Tripped Upon Actuation of Ground Fault Relay & Standby Pump 13 Started But Did Not Deliver Sufficient Flow to Prevent Trip. Cause Not Found.Inlet Filters to Be cleaned.W/900502 Ltr ML20042E3561990-04-0505 April 1990 LER 89-015-01:on 890704,reactor Trip Occurred.Caused by Failure of Relay in Generator Breaker Trip Circuit.Relays in Generator Breaker Trip Circuits Replaced W/Correct Models & Checked to Ensure Proper rating.W/900405 Ltr ML20012C7211990-03-16016 March 1990 LER 90-003-00:on 900214,discovered That Train B Fuel Handling Bldg Exhaust Air Filter Outlet Damper Would Not Open.Caused by Wiring Error Due to Failure of Technicians to Follow Work Instructions.Technicians counseled.W/900316 Ltr ML20012B4381990-03-0101 March 1990 LER 90-002-00:on 900202,Train s Reactor Trip Breaker Opened, Initiating Turbine & Reactor Trip & Feedwater Isolation on Low Average RCS Temp.Cause Unknown.Universal Logic Cards Replaced & Monitoring Instruments installed.W/900301 Ltr ML20006E3781990-02-16016 February 1990 LER 90-001-00:on 900103,containment Ventilation Isolation Occurred Due to Loss of Power to Radiation Monitor Actuation Relay.Caused by Technician Lifting Power Lead. Technicians Trained & counseled.W/900216 Ltr ML20006E4001990-02-12012 February 1990 LER 90-001-00:on 900108,Train s Low Steam Line Pressure Blocking Switch Placed in Blocked Position,Causing Actuation of Safety Injection & ESF Sys.Caused by Lack of Instructions.Training Program modified.W/900212 Ltr ML20006D4231990-02-0202 February 1990 LER 90-002-00:on 900103,redundant Solenoid Valve Which Actuates Train C Feedwater Valve Failed.Caused by Excessive Particulate Buildup.Solenoids Cleaned & Hydraulic Oil Flushed & Filtered to Remove particulate.W/900202 Ltr ML20006D5591990-02-0202 February 1990 LER 89-023-01:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Declared Inoperable. Caused by Contact Oxidation & Low Contact Pressure.Chiller Auxiliary Relay Cleaned & adjusted.W/900202 Ltr ML20006B4731990-01-25025 January 1990 LER 89-024-00:on 891226,required Sample from Safety Injection Accumulator 1C of Boron Concentration Not Taken. Caused by Insufficient Administrative Controls to Track Surveillance Tests.Bulletin Will Be issued.W/900125 Ltr ML20006B2551990-01-19019 January 1990 LER 89-022-00:on 891205,discovered That ASME Section XI Pressure Test of Train C of Component Cooling Water Sys Not Performed Prior to Returning Sys to Svc.Sys Inoperable from 890909-1206.Test Control Procedures revised.W/900119 Ltr ML20006B2221990-01-16016 January 1990 LER 89-023-00:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Attempt to Secure Essential Chiller 12C Resulted in Trip.Caused by Failure of Voltage Regulator.Regulator Returned to mfg.W/900116 Ltr ML20005E2471989-12-29029 December 1989 LER 89-028-00:on 891130,control Room Ventilation Sys Actuated to Recirculation Mode as Result of Spurious Signal. Caused by Memory Error Causing Microprocessor to Energize Relay Incorrectly.Troubleshooting planned.W/891229 Ltr ML19332D7741989-11-24024 November 1989 LER 89-018-01:on 890922,discovered That Const Installation Procedure for Reg Guide 1.97,Rev 2 Instrumentation Did Not Include Details to Ensure Qualification Per 10CFR50.49 or IEEE 323-1974.Caused by Installation error.W/891124 Ltr ML19332C8661989-11-21021 November 1989 LER 89-027-00:on 891025,discovered That Closed Limit Switch on Main Turbine Throttle Valve 2 Disconnected.Caused by Failure of Limit Switch Linkage.Review to Be Performed of Limit Switch Linkage design.W/891122 Ltr 1994-05-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K9441999-10-15015 October 1999 SER Accepting Util Alternative Proposed Relief Request RR-ENG-2-4 for Second 10-year ISI Interval at Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) ML20217K9151999-10-15015 October 1999 SER Authorizing Util Relief Request RR-ENG-2-3 for Second 10-year ISI Interval of Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) NOC-AE-000676, Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With ML20217D0531999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 2 Cycle 7 Colr ML20217D0481999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 1 Cycle 9 Colr ML20211P8411999-09-0909 September 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Surface Exam to Perform Boroscopic VT-1 Visual Exam of Pump Casing Welds within Pump Pits for Welds Covered by Relief Request RR-ENG-24 ML20211P7811999-09-0909 September 1999 SER Approving Second 10-year Interval Inservice Insp Program Plan Relief Request RR-ENG-2-8 (to Use Code Case N-491-2) for South Texas Project,Units 1 & 2 ML20211Q6731999-09-0909 September 1999 Safety Evaluation Accepting First 10-yr Interval ISI Program Plan Request for Relief from ASME Code Case N-498 NOC-AE-000643, Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With ML20212E5191999-08-31031 August 1999 Rev 3 to SG-99-04-005, STP 1RE08 Outage Condition Monitoring Rept & Final Operational Assessment ML20211F4531999-08-24024 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative to Defer Partial First Period Exams of flange-to-shell Weld to Third Period & Perform Required Ultrasonic Exams,Both Manual & Automated,During Third Period ML20211F5111999-08-23023 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative Contained in Request for Relief RR-ENG-30 ML20210C9411999-07-31031 July 1999 Rev 1 to SG-99-07-002, South Tx,Unit 1 Cycle 9 Voltage- Based Repair Criteria 90-Day Rept, Jul 1999 ML20210R3631999-07-31031 July 1999 Monthly Operating Repts for July 1999 for South Tx Project, Units 1 & 2.With ML20210D9161999-07-23023 July 1999 Safety Evaluation Accepting Inservice Testing Relief Request RR-56 Re Component Cooling Water & Safety Injection Sys Containment Isolation Check Valve Closure Test Frequency ML20210D4821999-07-21021 July 1999 1RE08 ISI Summary Rept for Steam Generator Tubing of South Texas Project Electric Generating Station Unit 1 ML20210D4491999-07-21021 July 1999 Revised Chapters to Operations QA Plan, Including Rev 9 to Chapter 1.0, Organization & Rev 6 to Chapter 16.0, Independent Technical Review NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With ML20207H6361999-07-0808 July 1999 Safety Evaluation Approving 2nd 10 Yr Interval ISI Program Plan Request to Use ASME Section XI Code Case N-546 for Licenses NPF-76 & NPF-80,respectively ML20216D7481999-07-0707 July 1999 1RE08 ISI Summary Rept for Welds & Component Supports of STP Electric Generating Station,Unit 1 NOC-AE-000593, Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program ML20195J6871999-06-17017 June 1999 Safety Evaluation Supporting Proposed Alternative Contained in RR-ENG-2-5.Proposed Alternative Authorized Per 10CFR50.55a(a)(3)(i) for 2nd ISI Interval ML20196A2391999-06-15015 June 1999 Change QA-042 to Rev 13 of Operations QAP, Reflecting Current Organizational Alignment for South Texas Project & Culminating Organizational Realigment That Has Been Taking Place During Past Several Months NOC-AE-000563, Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with ML20206U5411999-05-18018 May 1999 Non-proprietary Errata Pages for Rev 2,Addendum 1 to WCAP-13699, Laser Welded Sleeves for 3/4 Inch Diamete Tube Feedring Type & W Preheater SGs Generic Sleeving Rept ML20206A7721999-04-30030 April 1999 STP Electric Generating Station Unit 1 Cycle 9 Colr NOC-AE-000543, Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with ML20205H0321999-03-31031 March 1999 Change QA-040 to Rev 13 of Operations QA Plan NOC-AE-000507, Monthly Operating Repts for Mar 1999 for Stp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Stp,Units 1 & 2. with ML20205A3781999-03-22022 March 1999 STP Electric Generating Station Simulator Certification Four Yr Rept for Units 1 & 2 ML20204B2711999-03-15015 March 1999 Safety Evaluation Authorizing 990201 Request to Authorize Alternative to Regulations Per 10CFR50.55a(a)(3)(i) That Would Revise Start of Second 120-month IST Interval to No Later than 011201 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results NOC-AE-000468, Monthly Operating Repts for Feb 1999 for South Texas Project Electric Generating Station.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for South Texas Project Electric Generating Station.With ML20207D1101999-02-24024 February 1999 Change QA-039 to Rev 13 of Operations QA Plan, for STP ML20203H8361999-02-17017 February 1999 Safety Evaluation Supporting Request for Relief from ASME Code Requirements for Class 3 Piping for Plant ML20202H9621999-02-0303 February 1999 SER Accepting Change to EALs Used in Classification of Emergency Conditions ML20202E8471999-01-31031 January 1999 2RE06 ISI Summary Rept for SG Tubing of STP Electric Generating Station,Unit 2 ML20216G2011999-01-31031 January 1999 City Public Svc of San Antonio Annual Rept 1998-1999 ML20199G5961999-01-31031 January 1999 Cycle 7 Voltage-Based Repair Criteria Rept for Jan 1999 ML20199K7711999-01-21021 January 1999 Safety Evaluation Accepting ISI Program Request for Relief for ASME Cose Repair Requirements for Code Class 3 Piping ML20199G8161999-01-19019 January 1999 SER Accepting Util 970707 Response to NRC 970509 RAI Re GL 92-08, Thermo-Lag 330-1 Fire Barriers. NRC Finds No Significant Safety Hazards Based on Application of Util Ampacity Derating Methodology ML20199H4981999-01-11011 January 1999 2RE06 ISI Summary Rept for Welds & Component Supports of Stp,Unit 2 ML20206Q3751999-01-0404 January 1999 2RE06 ISI Summary Rept for Sys Pressure Tests (Class 1 & 2) ML20206Q3721999-01-0404 January 1999 2RE06 ISI Summary Rept for Repairs & Replacements ML20216G2171998-12-31031 December 1998 Houston Industries 1998 Annual Rept. App a 1998 Financial Statements & Us Securities & Exchange Commission Form 10-K Encl NOC-AE-000403, Monthly Operating Repts for Dec 1998 for South Texas Project Unit 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for South Texas Project Unit 1 & 2.With ML20216G1521998-12-31031 December 1998 Central & South West Corp 1998 Summary Annual Rept & Securities & Exchange Commission Form 10-K ML20198M3431998-12-28028 December 1998 SER Accepting Util Request for Relief from ASME Code Repair Requirements for ASME Code Class 3 Piping for South Texas Project,Unit 2 1999-09-09
[Table view] |
Text
'
. The Light c o mp ;a n y gp South Texas Project Electric Generating P. O.Station Box 289 Wadsworth, Texas 77483 July 15, 1993 ST-HL-AE-4506 File No.: G26 10CFR50.73 U. S. Nuclear Regulatory Commission Attention: Document Control Desk ,
Washington, DC 20555 South Texas Project Unit 1 Docket No. STN 50-498 )
Revision 1 to Licensee Event Report 93-016 ;
Technical Specifications Violation Due to ;
Circuitry for the Steam Generator Power Operated Relief Valves and Post Accident Monitorina Instruments Beina Inocerable Pursuant to 10CFR50.73, Houston Lighting & Power (HL&P) l submits the attached revision to Unit 1 Licensee Event Report l 93-016 regarding a Technical Specifications violation due to circuity for the Steam Generator Power Operated Relief Valves and Post Accident Monitoring Instruments being technically inoperable for time periods that exceeded their allowed outage times. This event did not have an adverse effect on the health and safety of the public.
This revision provides the final results of the analysis of I the event. The results demonstrate that even if'a seismic event l had occurred, both Units 1 and 2 would have been able to safely shut down. Changes are indicated by revision bars.
The expected submission date for this revision was originally l projected as July 1, 1993. In a telephone conversation on July 1, 1993, with Mr. W. Johnson of NRC Region IV, the submission date was extended to July 15, 1993. l l
If you should have any questions on this matter, please contact Mr. J. M. Pinzon at (512) 912-8027 r;me at (512) 972-8664.
T k
'J . F.<Croth t' 1 Vice President, Nuclear Generation 1 DNB/pa
Attachment:
Revision 1 to LER 93-016 (South Texas, Unit 1)
LER-93\L93016R1.01 Project Manager on Behalf of the Participants in the South Texas Project 9307220320 DR 930715 m / f, g ADOCK 05000498 y 1 j]
7 k;W
1 Houston Lighting & Power Company South Texas Project Electric Generating Station ST-HL-AE-4506 File No.: G26 Page 2 l I
1 l c:
l Regional Administrator, Region IV Rufus S. Scott i Nuclear Regulatory Commission Associate General Counsel 611 Ryan Plaza Drive, Suite 400 Houston Lighting & Power Company j i Arlington, TX 76011 P. O. Box 61867 l
! Houston, TX 77208 I L. E. Kokajko Project Manager U.S. Nuclear Regulatory Commission Institute of Nuclear Power Washington,.DC 20555 13H15 Operations - Records Center 700 Galleria Parkway Atlanta, GA 30339-5957 Senior Resident Inspector c/o U. S. Nuclear Regulatory Dr. Joseph M. Hendrie l Commission 50 Bellport Lane
- P. O. Box 910 Bellport, NY 11713 )
Bay City, TX 77414 i D. K. Lacker ,
J. R. Newman, Esquire Bureau of Radiation Control i Newman & Holtzinger, P.C., STE 1000 Texas Department of Health 1615 L Street, N.W. 1100 West 49th Street Washington, DC 20036 Austin, TX 78756-3189 D. E. Ward /T. M. Puckett U.S. Nuclear Regulatory Comm.
Central Power and Light Company Attn: Document Control Desk j P. O. Box 2121 Washington, D.C. 20555 ;
Corpus Christi, TX 78403 l J. C. Lanier/M. B. Lee City of Austin Electric Utility Department 721 Barton Springs Road Austin, TX 78704 K. J. Fiedler/M. T. Hardt City Public Service P. O. Box 1771 San Antonio, TX 78296 LER 93\L93016R1.U1
NRC FC3M 366 U.S. NUCLEAR REGULATORY 00pO4]SSIC) APPROVED BY (M8 NO. 3150-0104 (542) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH
' LICENSEE EVENT REPORT (LER) M"$I3fS gu RE RDlWG BUR EN S THE INFORMATION AND RECORDS MANAGEMENT BRANCH TE O I (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION,
! (See reverse for required ruber of digits / characters for each block) WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK i REDUCTION PROJECT (3150 0104), OFFICE OF l MANAGEMENT AND BUDGET. WASHINGTON. DC ?O503.
l FACILITY NAE (1) DOCKET NLMBER (2) PAGE (3) l South Texas Unit 1 05000 498 1 OF 6 1
TITLE (4) Technical Specifications Violation due to Circuitry for the Steam Generator Power Operated Relief Valves and Post Accident Monitoring Instruments Being inoperable EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
SE T AL RE FACILITY WAME DOCKET NUMBER MC31H DAY YEAR YEAR MONTH DAY TEAR STP UM T 2 05000 499 FA n NAM CKET E 05 03 93 93 -- 016 -- 01 07 15 93 g 90 OPERATING THIS umi IS SusMinrD mSuANT TO THE RmiREMENTS OF 10 CrR e peck = or mmi (n)
C]DE (9) 5 20.402(b) 20.405(c) $0.73(a)(2)(iv) 73.71(b)
POWER 20.405(a)(1)(1) 50.36(c)(1) 50.73(a)(2)(v) 73. 71(c)
LEVEL (10) 0 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405(a)(1)(iii) X 50.73(a)(2)(1) 50.73(a)(2)(vii i )( A) (specify in Abst et ow 20.405(a)(1)(iv) 50.73(a)(2)(li) 50.73(a)(2)(vill)(B) 20.405(a)(1)(v) 50.73(a)(2)(il1) 50.73(a)(2)(x) NRC Form 366A) llCENSEE CONTACT FOR THIS LER (12)
NAM TELEPHONE NUMBER (include Area Code)
Jairo Pinzon - Senior Engineer (512) 972-8027 CCNPLETE ONE LINE FOR EACH CEMPONENT FAltURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER
[ g l
l l l l SUPPLEMENTAL REPORT EXPECit.) (14) EXPECTED MONTH DAY YEAR I l YES SUBMISSION (If yes, complete EXPECTED SUBMIS$10N DATE). X WO DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On May 3, 1993, at 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br />, Unit 1 was in Mode 5 at 0% power and Unit 2 defueled. It was discovered that circuitry for the Unit 1 Steam Generator Power Operated Relief Valves and Post Accident Monitoring Instruments had not been configured in its qualified condition since January 4, 1993. This discovery was made during review of a work package. The work package indicated that screws were missing from the circuit card cages and power supply racks in the Qualified Display Processing System and an engineering evaluation that had been requested had not been performed. The cause of the event is less than adequate work practices in not replacing the screws following maintenance activities. Contributing factors include less than adequate knowledge of seismic fastener requirements and the failure to assess the impact of the missing screws in a timely manner. Corrective actions for this event include replacing the missing screws, inspecting other similar equipment for missing screws, reviewing work documents for other uncompleted engineering evaluations, improving maintenance work practices, training with regard to equipment qualification, and enhancing the process by which deficient conditions are evaluated by engineering.
N2C FORM 366 (5-92)
LER-93\L93016R1.U1
NRC FORM 366A U.S. ILICLEAR REGJLATORY C0041SS10N APPROVED BY OMB NO. 3150-0104 (5 9?) EXPlRES 5/31/95 ESilMATED BURDEN PER RESPONSE TO COMPLY WITH THl$
INFORMATION COLLECTION REQUEST: 50.0 HRS.
"" " ' ^ " " ""
LICENBEE EVENT REPORT (LER) $R 7714),
T ON AND RECORD LANAGEMENT BR NCH MN TEXT CONTINUATION u.S. NUCLEAR REGULATORY COMMISSION, WASHikGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (31$0-0104), OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC 20503.
FAcitITY NAME (1) DOCKET WUMBfR (2) tra NUMarR (61 PAGF (3)
YEAR SEQUENTIAL REVISION South Texas, Unit 1 05000 498 2 OF 6 93 --
016 -- 01 TEXT (If more space is reouired use additional cooles of NRC Form 366A) (17)
DESCRIPTION OF EVENT:
4 On May 3, 1993, at 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br />, Unit 1 was in Mode 5 at 0% power and Unit 2 dofueled. It was discovered that circuitry for the Unit 1 Steam Generator Power Operated Relief Valves (S/G PORVs) and Post Accident Monitoring
, Instruments had not been configured in its qualified seismic condition since January 4, 1993. This discovery was made during review of a work package.
The work package indicated that screws were missing from the circuit card cages and power supply racks in the Qualified Display Processing System (QDPS) and an engineering evaluation that had been requested had not been performed.
On January 4, 1993, a Service Request (SR) was written by the QDPS System Engineer concerning missing seismic hold-in screws in the Unit 1 QDPS. The SR was written to resolve a problem associated with Maintenance workers failing to replace the screws following maintenance activities in the Unit i refueling outage.
The Shift Supervisor reviewed the SR and annetated on the SR that an engineering evaluation, called a Conditional Release Authorization, was nacessary to determine if the QDPS could be relied upon to perform its design function under all analyzed conditions. Neither the System Engineer or Shift Supervisor identified the missing screws as a potential operability issue and the affected equipment was not declared inoperable. The SR was delivered to the Maintenance Planning Division for processing and data entry, but following data entry, the SR was inadvertently filed instead of baing forwarded to the Technical Support Engineering Group for the l Conditional Release Authorization that the Shift Supervisor had determined I was necessary.
On April 28, 1993, during a review of the associated SR package, which was prompted by the NRC Diagnostic Evaluation Team, it was determined that the engineering evaluation had not been performed.
On April 29, 1993, the SR was given to the Design Engineering Department to cvaluate the effect of the missing screws. A walkdown was performed that identified specific locations for missing screws in the QDPS.
On April 30, 1993, the walkdown data was provided to Westinghouse Corporation for seismic review and impact assessment. Westinghouse dstermined that portions of the QDPS were not in a seismically analyzed condition with screws missing from the card cages and power supply racks.
LER-93\L93c .01
NRC FORM 366A U.S. NUCLEAR REEJLATORY CopptlSSION APPROVED BY CMB No. 3150-010.
(5-9?) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY blTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
LICENSEE EVENT REPORT (LER) $0RM$Tf0NAWD RE D MA C M NT BR NCH MN TEXT CONTINUATION 7714), u.s. NUCLEAR REGULATORY COMNISSION, WASHlWGTON, DC 20555-0001 AND TO THE PAPECWORK REDUCTION PROJECT (31$0-0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON OC 20503.
FACILITY MAME (1) DOCKET NUMRER (?) (fR NUMBER (61 PA T (3)
SEQUENTIAL REVISION YEAR
"# 8 ' " " * "
South Texas, Unit 1 05000 498 3 OF 6 93 --
016 -- 01 TEXT (If more space is recuired. use additional coDies of Nec Form 3664) (17)
DESCRIPTION OF EVENT: (Cont'd)
On May 3, 1993, at 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br />, STP personnel determined that violation of Technical Specifications 3.7.1.6 and 3.3.3.6 had occurred because circuitry i for the Unit 1 S/G PORVs and the RCS Subcooling Margin Monitor had been l technically inoperable from January 4, 1993, until February 11, 1993, when l Unit 1 entered Mode 5 and the S/G PORVs and the RCS Subcooling Monitor were l no longer required to be operable.
The NRC Operations Center was notified of this event on May 4, 1993, at 1104 hours0.0128 days <br />0.307 hours <br />0.00183 weeks <br />4.20072e-4 months <br />.
! I l
CAUSE OF EVENT:
The root cause of this event is less than adequate work practiceu in that the screws were not replaced following maintenance activities. Contributing factors include less than adequate knowledge of equipment qualification !
rcquirements, and failure to evaluate the impact of the missing screws in a timely manner.
ANALYSIS OF EVENT:
During investigation of this event, it was revealed that the System Engineer .
had written the SR to resolve a condition that had existed intermittently I I
for the two years he had been the QDPS System Engineer. The System El%;1neer had kept notes, dated back to August 1992, that indicated that the condition )
also affected the Unit 2 QDPS.
Subsequent to the NRC notification on May 4, 1993, Westingis se performed a l more detailed analysis to determine the seismic adequacy of the card cages and power supply racks using the specific locations and numbers of missing i ccrews. The more detailed analysis indicated that some of the card cages and power supply racks that were initially considered to be seismically unacceptable were acceptable in their current configuration.
Using the list developed in the more detailed Westinghouse analysis, HL&P has identified the controls and indications in each unit that could have bsen affected by a seismic event. The Unit 1 S/G PORVs and RCS Subcooling Margin Monitors were not affected as originally reported to the NRC, but the circuitry for other Post Accident Monitoring Instruments on both units, as wall as two S/G PORVs on Unit 2, were affected.
l l
l LER-93\L93016R1.U1
NRC FORN 366A U.S. MUCLEAR RE(11LATORY fXMMISSION APPROVED BY CMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
C" " S RE " " " '
LICENBEE EVENT REPORT (LER) N"! yow"ANoRtCORD g ANAGEM NT BR NCH M TEXT CONTINUATION 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASWikGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (31$0-0104), OFFICE OF MANAGEMENT AND BUDGET. LASHINGTON, DC 20503.
FACIllTY NAME (1) DOCEIT WlMBER (2) LER NLMBFR (6S PAGE (3)
SEQUENTIAL REVISION YEAR South Texas, Unit 1 05000 498 4 OF 6 93 -- 016 -- 01 TEXT (If more soace is reauired, use additional cooles of NRC Form 366A) (17)
ANALYSIS OF EVENT: (Cont'd)
Although the controls and indications may not have failed during a seismic cvent, HL&P assumed that the controls and indications were failed to conservatively assess the operator's ability to shut down the plant if a ;
scismic event had occurred while the screws were not installed. Using the l' lists of controls and indications that were assumed to have failed, and taking credit for other qualified controls and indications that were not affected by missing screws, HL&P has determined that Units 1 and 2 had sufficient redundant capabilities to perform a safe shutdown of the plant after a seismic event even if a loss of offsite power had occurred coincident with the seismic event.
After the affected controls and indications were identified, HL&P determined l that Technical Specification allowed outage times, in addition to those initially reported, were exceeded because the affected controls and indications were not recognized as being unqualified. The list of affected controls and indications differs for each unit, but collectively, allowed outage times were exceeded for action statements located in Technical Specifications 3. 3.1, 3.3.2, 3.3.3.5, 3.3.3.6, 3.4.11, 3.7.1.2 and 3.7.1.6.
4 The allowed outage times varied from 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> to 60 days, depending on the control or indication affected.
The S/G PORVs are required for decay heat removal and safe cooldown in accordance with Branch Technical Position RSB 5-1. In the safety analyses, operation of the S/G PORVs is assumed for mitigation of small break LOCA, feedwater line break, loss of normal feedwater, and loss of offsite power.
Operability of post accident monitoring instrumentation ensures that sufficient information is available on selected plant parameters to monitor and assess these parameters following an accident. The design, gitalification and display criteria for Post Accident Monitoring Instruments are described in the South Texas Project Electric Generating Station Updated Final Safety Analysis Report, Section 7B, and meet the intent of Regulatory Guide 1.97, Revision 2, " Instrumentation for Light Water Cooled Nuclear Power Plants to Assess Plant Conditions During and Following an Accident,"
December 1980.
During the time that the Units 1 and 2 QDPS seismic hold down screws were missing, the systems provided the required indication and control functions needed to safely operate Units 1 and 2. Therefore, this event did not have an adverse affect on public health or safety.
Failure to meet the requirements of the Technical Specifications is reportable pursuant to 10CFR50.73 (a) (2) (1) (B) .
LER 93\L93016R1.U1
NRc FORM 366A u.s. NUCLEAR REGULATORY CXBetISSION APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95
~
ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS
- INFORMATION COLLECTION REQUEST: 50.0 HRS.
MMEN ' ^ "$'
LICENSEE EVENT REPORT (LER) $ $ 1[oN AND REC 0RD A GEM NT BR NCH M TEXT CONTINUATION 7714), U.S. NUCLEAR REGULATORY COMMISSION, I I
WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK l l REDUCTION PROJECT (31$0-0104), OFFICE OF 4 MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
(
FACILITY NAMF (1) DOCKET WlMBER (2) LER NtMBER (6h PAGF (3) l EEQLENTIAL REVISION YEAR
, South Texas, Unit 1 05000 498 5 OF 6 l
93 -- 016 -- 01 l
TEXT (If more sonce is reoutred. use additional cooles of NRC Form 366A) (17)
CORRECTIVE ACTIONS Tha following corrective actions address the specific conditions in Units 1 l and 2 and the generic implications of the event. l
- 1. The screws missing from the Unit 1 QDPS have been replaced.
- 2. Walkdowns of other similar components were performed to determine if other potential operability issues existed due to missing screws. No i other reportable conditions were identified. The screws missing from j the Unit 2 QDPS will be replaced prior to Unit 2 startup.
l 3. Open SRs were reviewed to determine if non-conformances that potentially affect operability have been identified and resolved. No additional issues affecting operability were identified.
- 4. The Operations Work Control Group that screens new SRs has been trained on equipment qualification requirements to enable them to properly identify conditions similar to those which occurred in this event.
- 5. The Maintenance Department has issued a training bulletin to address conficJuration management as it relates to maintenance work practices. l To reinforce the importance of configuration management, the training i bulletin will be discussed in the Maintenance Department Manager's i quarterly meeting by August 1, 1993. l
- 6. The process for obtaining Conditional Release Authorizations will be enhanced to include specific processing requirements and to clearly define process accountability. This enhancement will be completed by l September 17, 1993. Until this enhancement is fully implemented, the Operations Department will track Conditional Release Authorizations to ensure the timely evaluation of indeterminate conditions.
- 7. Training on equipment qualification has been provided to System Engineers.
Additional Information:
No previous events have been reported where the seismic qualification of a component caused a Technical Specification violation. However, Unit 2 Licensee Event Report 93-008, " Technical Specifications Violations Due to Failure to Maintain Equipment Qualification of a Residual Heat Removal System Motor Operated Valve," describes an event where a motor operated valve was not configured in an environmentally qualified condition due to a missing "T" drain. Generic corrective actions, which address the generic implication of the missing screws in the QDPS and the missing "T" drain in the motor operated valve, are being addressed by Unit 2 Licensee Event Report 93-008.
LER-93\L93016R1.U1
NRC FORM 366A U.S. NUCLEAR REGULATORY CG NISSION APPROVED BY (MB NO. 3150-0104 (5 92) ,
EXPIRES 5/31/95 ESilMATED BURDEN PER RESPONSE TO COMPLY WITH THis
- INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESilMATE TO THE LICENSEE EVENT REPORT (LER) INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB TEXT CONTINUATION 7714), U.S. NUCLEAR REGULATORY COMMIS$10N, WASHINGTON, DC 20555 0001 AND TO THE PAPERWORK REDUCTION PROJECT (31$00104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACitITY NAME (1) DOCKET WLMBER (2) LER WLMBER (6S PAGE (3)
SEQUENTIAL REVISION YEAR l South Texas, Unit 1 05000 498 6 OF 6
! 93 -- 016 -- 01 1
TEXT (If more space is reautred, use additional cooles of NRC form 366A) (17) bdditional Informatign:
l Unit 1 Licensee Event Report 90-024, " Failure to take Technical Sp:cification Actions With One Channel of [RCS) Subcooling Margin [ Monitor) l Inoperable," described an event where the Display Processing Units within l the QDPS were inoperable, but the effects of the inoperability were not
[ cppropriately considered. The cause of the event in LER 90-024 was sufficiently different from the cause of this event such that the corrective actions described in LER 90-024 would not have been expected to preclude this event.
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