|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6321994-05-0202 May 1994 LER 94-002-01:on 940115,centrifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to Requirements of TS 3.1.2.3.Caused by hydro-pneumatic Transient.Valves Labeled W/Caution statements.W/940502 Ltr ML20029D6351994-04-27027 April 1994 LER 94-006-01:on 940214,reactor Manually Tripped Following Unanticipated Test Results.Caused by Mod Which Failed post- Mod Test.Test Terminated & Solid State Rod Control Sys Returned to Original Design configuration.W/940427 Ltr ML20029C6951994-04-18018 April 1994 LER 94-011-00:on 940310,safety Injection Actuation Was Received on Trains A,B & C.Cause Was Failure to Adhere to Procedure.Corrective Actions:Restored Cooling Shutdown & Removed Personnel from watchbill.W/940418 Ltr ML17352B2581994-03-25025 March 1994 LER 94-007-00:on 940224,station Procedure for Testing Reactor Trip Bypass Breakers Did Not Satisfy Ts.Caused by Inadequate Procedure Preparation & Review.Surveillance Procedure Enhancement Program underway.W/940325 Ltr ML20046C5471993-08-0606 August 1993 LER 93-018-00:on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST plan.W/930806 Ltr ML20046C4901993-08-0505 August 1993 LER 93-019-00:on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing discrepancy.W/930805 Ltr ML20046B1291993-07-29029 July 1993 LER 93-012-00:on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel cooling.W/930729 Ltr ML20046A6791993-07-21021 July 1993 LER 93-011-00:on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway ML20046A6511993-07-20020 July 1993 LER 93-017-01:on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified ML20045J0281993-07-15015 July 1993 LER 93-016-01:on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 QDPS.W/930715 Ltr ML20045H9171993-07-14014 July 1993 LER 93-008-01:on 930505,discovered That RHR Pump Suction MOV Had Not Been Environ Qualified Since 901129 Because Replacement of Drain T Not Completed.Drain T Missing from RH-0060B Replaced & Bulletin Issued to Maint Dept ML20045H9881993-07-13013 July 1993 LER 93-012-01:on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings. W/930713 Ltr ML20045E1531993-06-25025 June 1993 LER 93-017-00:on 930527,determined That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioner & Solenoids Remained in Svc Beyond Qualified Life.Caused by Incorrect Interpretation of Design Documents.Mod Underway ML20045E1491993-06-25025 June 1993 LER 93-010-00:on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint initiated.W/930625 Ltr ML20045B2731993-06-0909 June 1993 LER-93-016-00:on 930503,TS Violation Occured Due to Circuitry for SG PORVs & RCS Subcooling Monitor Being Inoperable.Caused by Less than Adequate Work Practices. Screws Missings from Qdps Replaced & Walkdown Performed ML20045A3831993-06-0404 June 1993 LER 93-008-00:on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain ML20044G4301993-05-25025 May 1993 LER 93-009-00:on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref values.W/930525 Ltr ML20044F6281993-05-21021 May 1993 LER 93-015-00:on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans monitored.W/930521 Ltr ML20044F1321993-05-20020 May 1993 LER 93-009-01:on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort ML20044E0371993-05-14014 May 1993 LER 93-005-01:on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training ML20024H2571991-05-24024 May 1991 LER 91-014-00:on 910420,erratic Containment Extended Range Pressure Channel Output Occurred.Caused by Bad Control Card. Weekly Channel Checks Performed,Control Card Replaced & Channel calibrated.W/910524 Ltr ML20024H2081991-05-22022 May 1991 LER 91-015-00:on 910422,train C AFW Pump Inadvertently Started Due to Failure of Led in Sequencer Test Circuitry. Faulty Led Replaced & Blocking Circuit Satisfactorily tested.W/910522 Ltr ML20029C1221991-03-15015 March 1991 LER 91-004-00:on 910215,loss of Offsite Power Actuation Occurred During Routine Maint.Caused by Lack of Attention to Work Performance Methods.Training Conducted for Maintenance personnel.W/910315 Ltr ML20029B0421991-02-25025 February 1991 LER 91-002-00:on 910126,automatic Actuation of Safety Injection Sys Occurred in One of Three Train C Trains.Caused by Inadequate Work Instructions for Maint Activity.Training Bulletin Issued & Supervisors counseled.W/910225 Ltr ML20024F7451990-12-12012 December 1990 LER 90-017-00:on 901104,discovered That Train a of Class IE 120-volt Distribution Panel DP001 Energized from Alternate Power Supply.Caused by Less than Adequate Administrative Controls.Log Will Be utilized.W/901212 Ltr ML20044B1691990-07-0606 July 1990 LER 90-011-00:on 900612,chemical Technician Supervisor Discovered That No Sample Collected in Condenser Air Removal Sys Radiation Monitor Moisture Collection Tank. Caused by Inadequate procedure.W/900706 Ltr ML20043G2091990-06-14014 June 1990 LER 90-010-00:on 900515,determined That Leak & Contamination Test Interval for Some Radioactive Sources Exceeded Tech Specs.Caused by Insufficient Detail in Procedures.Test Program revised.W/900614 Ltr ML20043G5191990-06-14014 June 1990 LER 90-010-00:on 900515,unplanned Actuation of ESF Train C Standby Diesel Generator Occurred.Caused by Personnel Error. Training Bulletin Will Be Issued to Maint Personnel Re event.W/900613 Ltr ML20043G1791990-06-13013 June 1990 LER 90-009-00:on 900512,incorrect Wiring in Solid State Protection Sys Discovered.Caused by Inadvertent Installation of Extra Wire by Mfg.Extra Wire Removed & Sys Successfully tested.W/900613 Ltr ML20043G2101990-06-13013 June 1990 LER 90-009-00:on 900514,discovered That Printer for Toxic Gas Analyzer XE-9325 Was Not Updating & Surveillances for Toxic Gas Monitor XE-9325 Incorrectly Performed on 900511. Caused by Inadequate training.W/900613 Ltr ML20043G7681990-06-0808 June 1990 LER 90-008-00:on 900508,Tech Spec Required Shutdown Initiated Due to Primary Coolant Sys Leakage.Caused by High Cycle Fatigue Failure of Weld on Upstream Side of Drain Valve.Drain Valves replaced.W/900608 Ltr ML20043E7001990-06-0404 June 1990 LER 90-008-00:on 891007,Tech Spec Violation Occurred Due to Failure to Perform post-maint Testing.Caused by Incorrect Determination That No post-maint Testing Required.Personnel counseled.W/900604 Ltr ML20043C7401990-05-30030 May 1990 LER 90-007-00:on 900430,discovered That All Three Trains of ESFAS Placed in Test & Incapable of Actuating for Approx 35 Minutes.Caused by Inadequate Prerequisite Conditions in Maint Procedure.Procedure Being modified.W/900530 Ltr ML20043C4791990-05-29029 May 1990 LER 90-007-00:on 900426,standby Diesel Generator 22 Room High Sump Level Alarm Actuated in Control Room.Caused by Flooding & Inadequate Spec of Sealing & Testing Requirements.Seals on Removable Panels caulked.W/900529 Ltr ML20043B6611990-05-25025 May 1990 LER 90-006-00:on 900426,control Room Ventilation Sys Actuated to Recirculation Mode Due to High Level Trip of Vinyl Acetate Channel on Gas Analyzer.Caused by Failure of electro-mechanical Positioner.Part replaced.W/900525 Ltr ML20043A7811990-05-15015 May 1990 LER 90-005-00:on 900414,simultaneous Reactor & Turbine Trip Occurred Due to Failure of Main Turbine Electrohydraulic Control Line.Caused by Fatigue Stress of Weld.Valve Modified to Add anti-swirl Baffles & anti-rotation pins.W/900515 Ltr ML20042F2191990-05-0202 May 1990 LER 90-005-00:on 900329,feedwater Booster Pump 11 Tripped Upon Actuation of Ground Fault Relay & Standby Pump 13 Started But Did Not Deliver Sufficient Flow to Prevent Trip. Cause Not Found.Inlet Filters to Be cleaned.W/900502 Ltr ML20042E3561990-04-0505 April 1990 LER 89-015-01:on 890704,reactor Trip Occurred.Caused by Failure of Relay in Generator Breaker Trip Circuit.Relays in Generator Breaker Trip Circuits Replaced W/Correct Models & Checked to Ensure Proper rating.W/900405 Ltr ML20012C7211990-03-16016 March 1990 LER 90-003-00:on 900214,discovered That Train B Fuel Handling Bldg Exhaust Air Filter Outlet Damper Would Not Open.Caused by Wiring Error Due to Failure of Technicians to Follow Work Instructions.Technicians counseled.W/900316 Ltr ML20012B4381990-03-0101 March 1990 LER 90-002-00:on 900202,Train s Reactor Trip Breaker Opened, Initiating Turbine & Reactor Trip & Feedwater Isolation on Low Average RCS Temp.Cause Unknown.Universal Logic Cards Replaced & Monitoring Instruments installed.W/900301 Ltr ML20006E3781990-02-16016 February 1990 LER 90-001-00:on 900103,containment Ventilation Isolation Occurred Due to Loss of Power to Radiation Monitor Actuation Relay.Caused by Technician Lifting Power Lead. Technicians Trained & counseled.W/900216 Ltr ML20006E4001990-02-12012 February 1990 LER 90-001-00:on 900108,Train s Low Steam Line Pressure Blocking Switch Placed in Blocked Position,Causing Actuation of Safety Injection & ESF Sys.Caused by Lack of Instructions.Training Program modified.W/900212 Ltr ML20006D4231990-02-0202 February 1990 LER 90-002-00:on 900103,redundant Solenoid Valve Which Actuates Train C Feedwater Valve Failed.Caused by Excessive Particulate Buildup.Solenoids Cleaned & Hydraulic Oil Flushed & Filtered to Remove particulate.W/900202 Ltr ML20006D5591990-02-0202 February 1990 LER 89-023-01:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Declared Inoperable. Caused by Contact Oxidation & Low Contact Pressure.Chiller Auxiliary Relay Cleaned & adjusted.W/900202 Ltr ML20006B4731990-01-25025 January 1990 LER 89-024-00:on 891226,required Sample from Safety Injection Accumulator 1C of Boron Concentration Not Taken. Caused by Insufficient Administrative Controls to Track Surveillance Tests.Bulletin Will Be issued.W/900125 Ltr ML20006B2551990-01-19019 January 1990 LER 89-022-00:on 891205,discovered That ASME Section XI Pressure Test of Train C of Component Cooling Water Sys Not Performed Prior to Returning Sys to Svc.Sys Inoperable from 890909-1206.Test Control Procedures revised.W/900119 Ltr ML20006B2221990-01-16016 January 1990 LER 89-023-00:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Attempt to Secure Essential Chiller 12C Resulted in Trip.Caused by Failure of Voltage Regulator.Regulator Returned to mfg.W/900116 Ltr ML20005E2471989-12-29029 December 1989 LER 89-028-00:on 891130,control Room Ventilation Sys Actuated to Recirculation Mode as Result of Spurious Signal. Caused by Memory Error Causing Microprocessor to Energize Relay Incorrectly.Troubleshooting planned.W/891229 Ltr ML19332D7741989-11-24024 November 1989 LER 89-018-01:on 890922,discovered That Const Installation Procedure for Reg Guide 1.97,Rev 2 Instrumentation Did Not Include Details to Ensure Qualification Per 10CFR50.49 or IEEE 323-1974.Caused by Installation error.W/891124 Ltr ML19332C8661989-11-21021 November 1989 LER 89-027-00:on 891025,discovered That Closed Limit Switch on Main Turbine Throttle Valve 2 Disconnected.Caused by Failure of Limit Switch Linkage.Review to Be Performed of Limit Switch Linkage design.W/891122 Ltr 1994-05-02
[Table view] Category:RO)
MONTHYEARML20029D6321994-05-0202 May 1994 LER 94-002-01:on 940115,centrifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to Requirements of TS 3.1.2.3.Caused by hydro-pneumatic Transient.Valves Labeled W/Caution statements.W/940502 Ltr ML20029D6351994-04-27027 April 1994 LER 94-006-01:on 940214,reactor Manually Tripped Following Unanticipated Test Results.Caused by Mod Which Failed post- Mod Test.Test Terminated & Solid State Rod Control Sys Returned to Original Design configuration.W/940427 Ltr ML20029C6951994-04-18018 April 1994 LER 94-011-00:on 940310,safety Injection Actuation Was Received on Trains A,B & C.Cause Was Failure to Adhere to Procedure.Corrective Actions:Restored Cooling Shutdown & Removed Personnel from watchbill.W/940418 Ltr ML17352B2581994-03-25025 March 1994 LER 94-007-00:on 940224,station Procedure for Testing Reactor Trip Bypass Breakers Did Not Satisfy Ts.Caused by Inadequate Procedure Preparation & Review.Surveillance Procedure Enhancement Program underway.W/940325 Ltr ML20046C5471993-08-0606 August 1993 LER 93-018-00:on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST plan.W/930806 Ltr ML20046C4901993-08-0505 August 1993 LER 93-019-00:on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing discrepancy.W/930805 Ltr ML20046B1291993-07-29029 July 1993 LER 93-012-00:on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel cooling.W/930729 Ltr ML20046A6791993-07-21021 July 1993 LER 93-011-00:on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway ML20046A6511993-07-20020 July 1993 LER 93-017-01:on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified ML20045J0281993-07-15015 July 1993 LER 93-016-01:on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 QDPS.W/930715 Ltr ML20045H9171993-07-14014 July 1993 LER 93-008-01:on 930505,discovered That RHR Pump Suction MOV Had Not Been Environ Qualified Since 901129 Because Replacement of Drain T Not Completed.Drain T Missing from RH-0060B Replaced & Bulletin Issued to Maint Dept ML20045H9881993-07-13013 July 1993 LER 93-012-01:on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings. W/930713 Ltr ML20045E1531993-06-25025 June 1993 LER 93-017-00:on 930527,determined That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioner & Solenoids Remained in Svc Beyond Qualified Life.Caused by Incorrect Interpretation of Design Documents.Mod Underway ML20045E1491993-06-25025 June 1993 LER 93-010-00:on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint initiated.W/930625 Ltr ML20045B2731993-06-0909 June 1993 LER-93-016-00:on 930503,TS Violation Occured Due to Circuitry for SG PORVs & RCS Subcooling Monitor Being Inoperable.Caused by Less than Adequate Work Practices. Screws Missings from Qdps Replaced & Walkdown Performed ML20045A3831993-06-0404 June 1993 LER 93-008-00:on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain ML20044G4301993-05-25025 May 1993 LER 93-009-00:on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref values.W/930525 Ltr ML20044F6281993-05-21021 May 1993 LER 93-015-00:on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans monitored.W/930521 Ltr ML20044F1321993-05-20020 May 1993 LER 93-009-01:on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort ML20044E0371993-05-14014 May 1993 LER 93-005-01:on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training ML20024H2571991-05-24024 May 1991 LER 91-014-00:on 910420,erratic Containment Extended Range Pressure Channel Output Occurred.Caused by Bad Control Card. Weekly Channel Checks Performed,Control Card Replaced & Channel calibrated.W/910524 Ltr ML20024H2081991-05-22022 May 1991 LER 91-015-00:on 910422,train C AFW Pump Inadvertently Started Due to Failure of Led in Sequencer Test Circuitry. Faulty Led Replaced & Blocking Circuit Satisfactorily tested.W/910522 Ltr ML20029C1221991-03-15015 March 1991 LER 91-004-00:on 910215,loss of Offsite Power Actuation Occurred During Routine Maint.Caused by Lack of Attention to Work Performance Methods.Training Conducted for Maintenance personnel.W/910315 Ltr ML20029B0421991-02-25025 February 1991 LER 91-002-00:on 910126,automatic Actuation of Safety Injection Sys Occurred in One of Three Train C Trains.Caused by Inadequate Work Instructions for Maint Activity.Training Bulletin Issued & Supervisors counseled.W/910225 Ltr ML20024F7451990-12-12012 December 1990 LER 90-017-00:on 901104,discovered That Train a of Class IE 120-volt Distribution Panel DP001 Energized from Alternate Power Supply.Caused by Less than Adequate Administrative Controls.Log Will Be utilized.W/901212 Ltr ML20044B1691990-07-0606 July 1990 LER 90-011-00:on 900612,chemical Technician Supervisor Discovered That No Sample Collected in Condenser Air Removal Sys Radiation Monitor Moisture Collection Tank. Caused by Inadequate procedure.W/900706 Ltr ML20043G2091990-06-14014 June 1990 LER 90-010-00:on 900515,determined That Leak & Contamination Test Interval for Some Radioactive Sources Exceeded Tech Specs.Caused by Insufficient Detail in Procedures.Test Program revised.W/900614 Ltr ML20043G5191990-06-14014 June 1990 LER 90-010-00:on 900515,unplanned Actuation of ESF Train C Standby Diesel Generator Occurred.Caused by Personnel Error. Training Bulletin Will Be Issued to Maint Personnel Re event.W/900613 Ltr ML20043G1791990-06-13013 June 1990 LER 90-009-00:on 900512,incorrect Wiring in Solid State Protection Sys Discovered.Caused by Inadvertent Installation of Extra Wire by Mfg.Extra Wire Removed & Sys Successfully tested.W/900613 Ltr ML20043G2101990-06-13013 June 1990 LER 90-009-00:on 900514,discovered That Printer for Toxic Gas Analyzer XE-9325 Was Not Updating & Surveillances for Toxic Gas Monitor XE-9325 Incorrectly Performed on 900511. Caused by Inadequate training.W/900613 Ltr ML20043G7681990-06-0808 June 1990 LER 90-008-00:on 900508,Tech Spec Required Shutdown Initiated Due to Primary Coolant Sys Leakage.Caused by High Cycle Fatigue Failure of Weld on Upstream Side of Drain Valve.Drain Valves replaced.W/900608 Ltr ML20043E7001990-06-0404 June 1990 LER 90-008-00:on 891007,Tech Spec Violation Occurred Due to Failure to Perform post-maint Testing.Caused by Incorrect Determination That No post-maint Testing Required.Personnel counseled.W/900604 Ltr ML20043C7401990-05-30030 May 1990 LER 90-007-00:on 900430,discovered That All Three Trains of ESFAS Placed in Test & Incapable of Actuating for Approx 35 Minutes.Caused by Inadequate Prerequisite Conditions in Maint Procedure.Procedure Being modified.W/900530 Ltr ML20043C4791990-05-29029 May 1990 LER 90-007-00:on 900426,standby Diesel Generator 22 Room High Sump Level Alarm Actuated in Control Room.Caused by Flooding & Inadequate Spec of Sealing & Testing Requirements.Seals on Removable Panels caulked.W/900529 Ltr ML20043B6611990-05-25025 May 1990 LER 90-006-00:on 900426,control Room Ventilation Sys Actuated to Recirculation Mode Due to High Level Trip of Vinyl Acetate Channel on Gas Analyzer.Caused by Failure of electro-mechanical Positioner.Part replaced.W/900525 Ltr ML20043A7811990-05-15015 May 1990 LER 90-005-00:on 900414,simultaneous Reactor & Turbine Trip Occurred Due to Failure of Main Turbine Electrohydraulic Control Line.Caused by Fatigue Stress of Weld.Valve Modified to Add anti-swirl Baffles & anti-rotation pins.W/900515 Ltr ML20042F2191990-05-0202 May 1990 LER 90-005-00:on 900329,feedwater Booster Pump 11 Tripped Upon Actuation of Ground Fault Relay & Standby Pump 13 Started But Did Not Deliver Sufficient Flow to Prevent Trip. Cause Not Found.Inlet Filters to Be cleaned.W/900502 Ltr ML20042E3561990-04-0505 April 1990 LER 89-015-01:on 890704,reactor Trip Occurred.Caused by Failure of Relay in Generator Breaker Trip Circuit.Relays in Generator Breaker Trip Circuits Replaced W/Correct Models & Checked to Ensure Proper rating.W/900405 Ltr ML20012C7211990-03-16016 March 1990 LER 90-003-00:on 900214,discovered That Train B Fuel Handling Bldg Exhaust Air Filter Outlet Damper Would Not Open.Caused by Wiring Error Due to Failure of Technicians to Follow Work Instructions.Technicians counseled.W/900316 Ltr ML20012B4381990-03-0101 March 1990 LER 90-002-00:on 900202,Train s Reactor Trip Breaker Opened, Initiating Turbine & Reactor Trip & Feedwater Isolation on Low Average RCS Temp.Cause Unknown.Universal Logic Cards Replaced & Monitoring Instruments installed.W/900301 Ltr ML20006E3781990-02-16016 February 1990 LER 90-001-00:on 900103,containment Ventilation Isolation Occurred Due to Loss of Power to Radiation Monitor Actuation Relay.Caused by Technician Lifting Power Lead. Technicians Trained & counseled.W/900216 Ltr ML20006E4001990-02-12012 February 1990 LER 90-001-00:on 900108,Train s Low Steam Line Pressure Blocking Switch Placed in Blocked Position,Causing Actuation of Safety Injection & ESF Sys.Caused by Lack of Instructions.Training Program modified.W/900212 Ltr ML20006D4231990-02-0202 February 1990 LER 90-002-00:on 900103,redundant Solenoid Valve Which Actuates Train C Feedwater Valve Failed.Caused by Excessive Particulate Buildup.Solenoids Cleaned & Hydraulic Oil Flushed & Filtered to Remove particulate.W/900202 Ltr ML20006D5591990-02-0202 February 1990 LER 89-023-01:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Declared Inoperable. Caused by Contact Oxidation & Low Contact Pressure.Chiller Auxiliary Relay Cleaned & adjusted.W/900202 Ltr ML20006B4731990-01-25025 January 1990 LER 89-024-00:on 891226,required Sample from Safety Injection Accumulator 1C of Boron Concentration Not Taken. Caused by Insufficient Administrative Controls to Track Surveillance Tests.Bulletin Will Be issued.W/900125 Ltr ML20006B2551990-01-19019 January 1990 LER 89-022-00:on 891205,discovered That ASME Section XI Pressure Test of Train C of Component Cooling Water Sys Not Performed Prior to Returning Sys to Svc.Sys Inoperable from 890909-1206.Test Control Procedures revised.W/900119 Ltr ML20006B2221990-01-16016 January 1990 LER 89-023-00:on 891216,standby Diesel Generator 11 Failed Tech Spec Required Operability Test & Attempt to Secure Essential Chiller 12C Resulted in Trip.Caused by Failure of Voltage Regulator.Regulator Returned to mfg.W/900116 Ltr ML20005E2471989-12-29029 December 1989 LER 89-028-00:on 891130,control Room Ventilation Sys Actuated to Recirculation Mode as Result of Spurious Signal. Caused by Memory Error Causing Microprocessor to Energize Relay Incorrectly.Troubleshooting planned.W/891229 Ltr ML19332D7741989-11-24024 November 1989 LER 89-018-01:on 890922,discovered That Const Installation Procedure for Reg Guide 1.97,Rev 2 Instrumentation Did Not Include Details to Ensure Qualification Per 10CFR50.49 or IEEE 323-1974.Caused by Installation error.W/891124 Ltr ML19332C8661989-11-21021 November 1989 LER 89-027-00:on 891025,discovered That Closed Limit Switch on Main Turbine Throttle Valve 2 Disconnected.Caused by Failure of Limit Switch Linkage.Review to Be Performed of Limit Switch Linkage design.W/891122 Ltr 1994-05-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K9441999-10-15015 October 1999 SER Accepting Util Alternative Proposed Relief Request RR-ENG-2-4 for Second 10-year ISI Interval at Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) ML20217K9151999-10-15015 October 1999 SER Authorizing Util Relief Request RR-ENG-2-3 for Second 10-year ISI Interval of Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) NOC-AE-000676, Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With ML20217D0531999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 2 Cycle 7 Colr ML20217D0481999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 1 Cycle 9 Colr ML20211P8411999-09-0909 September 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Surface Exam to Perform Boroscopic VT-1 Visual Exam of Pump Casing Welds within Pump Pits for Welds Covered by Relief Request RR-ENG-24 ML20211P7811999-09-0909 September 1999 SER Approving Second 10-year Interval Inservice Insp Program Plan Relief Request RR-ENG-2-8 (to Use Code Case N-491-2) for South Texas Project,Units 1 & 2 ML20211Q6731999-09-0909 September 1999 Safety Evaluation Accepting First 10-yr Interval ISI Program Plan Request for Relief from ASME Code Case N-498 NOC-AE-000643, Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With ML20212E5191999-08-31031 August 1999 Rev 3 to SG-99-04-005, STP 1RE08 Outage Condition Monitoring Rept & Final Operational Assessment ML20211F4531999-08-24024 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative to Defer Partial First Period Exams of flange-to-shell Weld to Third Period & Perform Required Ultrasonic Exams,Both Manual & Automated,During Third Period ML20211F5111999-08-23023 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative Contained in Request for Relief RR-ENG-30 ML20210C9411999-07-31031 July 1999 Rev 1 to SG-99-07-002, South Tx,Unit 1 Cycle 9 Voltage- Based Repair Criteria 90-Day Rept, Jul 1999 ML20210R3631999-07-31031 July 1999 Monthly Operating Repts for July 1999 for South Tx Project, Units 1 & 2.With ML20210D9161999-07-23023 July 1999 Safety Evaluation Accepting Inservice Testing Relief Request RR-56 Re Component Cooling Water & Safety Injection Sys Containment Isolation Check Valve Closure Test Frequency ML20210D4821999-07-21021 July 1999 1RE08 ISI Summary Rept for Steam Generator Tubing of South Texas Project Electric Generating Station Unit 1 ML20210D4491999-07-21021 July 1999 Revised Chapters to Operations QA Plan, Including Rev 9 to Chapter 1.0, Organization & Rev 6 to Chapter 16.0, Independent Technical Review NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With ML20207H6361999-07-0808 July 1999 Safety Evaluation Approving 2nd 10 Yr Interval ISI Program Plan Request to Use ASME Section XI Code Case N-546 for Licenses NPF-76 & NPF-80,respectively ML20216D7481999-07-0707 July 1999 1RE08 ISI Summary Rept for Welds & Component Supports of STP Electric Generating Station,Unit 1 NOC-AE-000593, Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program ML20195J6871999-06-17017 June 1999 Safety Evaluation Supporting Proposed Alternative Contained in RR-ENG-2-5.Proposed Alternative Authorized Per 10CFR50.55a(a)(3)(i) for 2nd ISI Interval ML20196A2391999-06-15015 June 1999 Change QA-042 to Rev 13 of Operations QAP, Reflecting Current Organizational Alignment for South Texas Project & Culminating Organizational Realigment That Has Been Taking Place During Past Several Months NOC-AE-000563, Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with ML20206U5411999-05-18018 May 1999 Non-proprietary Errata Pages for Rev 2,Addendum 1 to WCAP-13699, Laser Welded Sleeves for 3/4 Inch Diamete Tube Feedring Type & W Preheater SGs Generic Sleeving Rept ML20206A7721999-04-30030 April 1999 STP Electric Generating Station Unit 1 Cycle 9 Colr NOC-AE-000543, Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with ML20205H0321999-03-31031 March 1999 Change QA-040 to Rev 13 of Operations QA Plan NOC-AE-000507, Monthly Operating Repts for Mar 1999 for Stp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Stp,Units 1 & 2. with ML20205A3781999-03-22022 March 1999 STP Electric Generating Station Simulator Certification Four Yr Rept for Units 1 & 2 ML20204B2711999-03-15015 March 1999 Safety Evaluation Authorizing 990201 Request to Authorize Alternative to Regulations Per 10CFR50.55a(a)(3)(i) That Would Revise Start of Second 120-month IST Interval to No Later than 011201 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results NOC-AE-000468, Monthly Operating Repts for Feb 1999 for South Texas Project Electric Generating Station.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for South Texas Project Electric Generating Station.With ML20207D1101999-02-24024 February 1999 Change QA-039 to Rev 13 of Operations QA Plan, for STP ML20203H8361999-02-17017 February 1999 Safety Evaluation Supporting Request for Relief from ASME Code Requirements for Class 3 Piping for Plant ML20202H9621999-02-0303 February 1999 SER Accepting Change to EALs Used in Classification of Emergency Conditions ML20202E8471999-01-31031 January 1999 2RE06 ISI Summary Rept for SG Tubing of STP Electric Generating Station,Unit 2 ML20216G2011999-01-31031 January 1999 City Public Svc of San Antonio Annual Rept 1998-1999 ML20199G5961999-01-31031 January 1999 Cycle 7 Voltage-Based Repair Criteria Rept for Jan 1999 ML20199K7711999-01-21021 January 1999 Safety Evaluation Accepting ISI Program Request for Relief for ASME Cose Repair Requirements for Code Class 3 Piping ML20199G8161999-01-19019 January 1999 SER Accepting Util 970707 Response to NRC 970509 RAI Re GL 92-08, Thermo-Lag 330-1 Fire Barriers. NRC Finds No Significant Safety Hazards Based on Application of Util Ampacity Derating Methodology ML20199H4981999-01-11011 January 1999 2RE06 ISI Summary Rept for Welds & Component Supports of Stp,Unit 2 ML20206Q3751999-01-0404 January 1999 2RE06 ISI Summary Rept for Sys Pressure Tests (Class 1 & 2) ML20206Q3721999-01-0404 January 1999 2RE06 ISI Summary Rept for Repairs & Replacements ML20216G2171998-12-31031 December 1998 Houston Industries 1998 Annual Rept. App a 1998 Financial Statements & Us Securities & Exchange Commission Form 10-K Encl NOC-AE-000403, Monthly Operating Repts for Dec 1998 for South Texas Project Unit 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for South Texas Project Unit 1 & 2.With ML20216G1521998-12-31031 December 1998 Central & South West Corp 1998 Summary Annual Rept & Securities & Exchange Commission Form 10-K ML20198M3431998-12-28028 December 1998 SER Accepting Util Request for Relief from ASME Code Repair Requirements for ASME Code Class 3 Piping for South Texas Project,Unit 2 1999-09-09
[Table view] |
Text
FLORIDA POWER 8r LIGHT COMPAiVY April 2, 1984 L-84-90 Office of Nuclear Reactor Regulation Attention: Mr. Darrell G. Eisenhut, Director Division of Licensing U.S. Nuclear Regul atory Commi ssion Washington, D.C. 20555
Dear Mr. Ei senhut:
Re: Turkey Point Units 3 8 4 Docket No. 50-250, 50-251 Proposed License Amendment Inservice Ins ection and Inservice Test Pro ran In accordance with 10 CFR 50.90, Florida Power 8 Light Company submits herewith three signed originals and forty copies of a request to anend Appendix A of Facility Operating Licenses DPR 31 and DPR 41.
This amendment is submitted as required by 10 CFR 50.55a(g)(5)(ii) when our revised Inservi ce Inspection (IS I ) and Inservi ce Test ( I ST) progr aIIs conflict wi th the current techni c al speci fi cati ons. To make the techni cal specifications current, we propose to adopt the wording of the Standard Technical Specifications for Westinghouse Pressurized Water Reactors (NUREG 0452, Revision 4). This change will keep the Technical Specifications up to date with the periodic changes in the ASME Boiler and Pressure Vessel Code without the need for future license anendments. This submittal is being made concurrently with the submittals of the ISI Second Ten-Year Summary and a revision to the Inservice Test PrograII for Pumps and Valves for Turkey Point Units 3 5 4.
The proposed anendment is described below and shown on the accompanying techni cal speci fi cati on pages.
Pa e 3.3-1 Specification 3.3.3 is revised to delete specifics of isolation valve testing. Testing of these valves is included in the Inservice Test Progran for Pumps and Valves which is addressed in proposed Specification 4.0.3.
S46 4050-VP4-840402 05000250 PDR ADOCK P ~ PDR PEOPLE... SERVING PEOPLE
Office of Nuclear Reactor Regulation Attention: Nr. Oarrell G. Eisenhut, Oirector Page 2 Pa e 3.4-2 Specifications 3.4.l.b.2 and b.4 are revised to delete operable safety injection and residual heat removal pump testing prior to maintenance on inoperable pumps. Testing of these components is included in the Inservice Test Progran for Pumps and Valves which is addressed in proposed Specification 4.0. 3.
Page 3.4-2a Specifications 3.4.1.b.5 and b.6 are revised to delete testing of duplicate function valves and to add a requirement to verify that the remaining residual heat removal heat exchanger and duplicate function valves meet the requirements of proposed Specification 4.0.3.
Pa e 3.4-4 Specifications 3.4.2.b.2 and b.3 are revised to delete operable containment spray pump and valve testing prior to maintenance on inoperable items. These pumps and valves are included is the Pump and Valve Test Progran.
Specification 3.4.3.b.2 is revised to delete operable containment filter valve testing prior to maintenance on inoperable valves. These valves are included 0 in the Pump and Valve Test Progran.
Pa e 3.4-5 Specification 3.4.4.b.2, 3.4.5.b.l and b.2 are revised to delete operable pump and heat exchanger testirig prior to maintenance on inoperable components.
These items are included in the ISI and IST Prograns. Requirements are added to verify that component cooling water pumps and heat exchangers and intake cooling water headers and pumps that remain operable, when other components are inoperable, meet the requirements of proposed Specification 4.0.3.
Pa e 3.4-6 Specification 3.4.6.b.2 is revised to delete testing of operable duplicate function valves.
Pa e 3.8-1 Specification 3.8.1d and 3.8.4 are revised to specify testing in accordance wi th Specifications 4.0. 3 and 4. 40.
Page 4.0-1, -2 4.1-1 Specification 4.0.3 is provided to add the inservice inspection and testing requirements of the ASME Code. Editorial changes are made to page 4.1-1 to facilitate this change.
0
~ ' ~
4~ ~
Office of Nuclear Reactor Regul ation Attention: Mr. Darrell G. Eisenhut, Director Page 3 Table 4.1-2 Sheet 2 of 3 This table is revised to require testing of pressurizer and main stean safety valves in accordance with Specification 4.0.3.
Pa e 4.2-1, -2, and Table 4.2-1 This specification is revised to remove requirements which are addressed oy proposed Specification 4.0.3. Those items formerly in Table 4.2-1 which were not addressed in proposed specification 4.0.3 are placed in the specification as items 4.2.3 and 4.2.4.
Pa e 4.4-2 An editorial change is made to the specification referenced in the acceptance cri teri a.
Pa e 4.4-3 Specifications 4.4.3 and 4.4.4 are revised to reference Specification 4.0.3 for containment isolation valves and delete the specific requirements for inservice testing of portions of the residual heat removal system. These items are included in the Inservice Test Progran for Pumps and Valves, which is addressed in proposed Specification 4.0.3.
Pa e 4.5-1 Specification 4.5 is rev'ised by deleting the surveillance specification for safety injection pumps and valves and inserting a reference to the testing required by proposed Specification 4.0.3.
P a e 4.6-2 Specification 4.6.2 is revised to delete the testing requirements for containment spray pumps and motor operated isolation valves. These items are inciuded in the Inservice Test Progran for Pumps and Valves which is addressed in proposed Specification 4.0.3.
Pa e 4.7-3 Revisions are made to post accident containment vent system valve testing to refer to Specification 4.0.3.
Specification 4.9 i s revised to adopt standard Techni cal specification wording
=
for testing of the Main Steaa Isolation Valves. These valves are included in the Inservice Test Progran for Pumps and Valves, which is addressed in proposed Specification 4.03.
Office of Nuclear Reactor Regulation Attention: Mr. Darrell G. Eisenhut, Director Page 4 0 Pa e 4.10-1 Specification 4.10 is revised to reference Specification 4.0.3 for testing of auxiliary feedwater pumps and valves.
Pa e B4.0-1 B4.2-1 The bases for Specification 4.0 and 4.2 are revised.
Pages i through vi, 3.4-3, 3.8-2, 4.2-2 through 4.2-6, 4.7-4 and B4.2-2 are provided with appropri ate changes to Table of Contents or page numberings to be consistent with the above changes.
In accordance with 10 CFR 50.91(a) (I), it has been determined that the proposed amendment does not involve any significant hazards considerations pursuant to 10 CFR 50.92. The No Significant Hazards Considerations determination i s attached.
In accordance with 10 CFR 50.91(b)(I) a copy of the proposed anendment is being forwarded to the State Designee for the State of Florida.
The proposed anendment has been reviewed by the Turkey Point Pl ant Nuclear Saety Committee and the Florida Power 5 Light Company Nuclear Review Board.
The proposed anendment has been determined to be a Class I and II amendment, and in accordance with 10 CFR 170.22, a check for $ 1,600.00 will follow by separate letter.
Very truly yours, J. W. Willians, Jr.
Vice President Nuclear Energy JWW/PLP/js Attachment CC: J. P. O'ei ly1 Regional Administrator, Region II U. S. Nuclear Regulatory Commission 101 Mari et t a Street, N.W., Sui te 2900 Atl anta, GA 30303 Lyle E. Jerrett, Administrator Radiological Health Ser vices Dept. of Health 8 Rehabilitative Services 0 1323 Wi newood Tal l ahassee, Boulevard Fl ori da Harold F. Reis, Esquire 32301 P NS-L I-84-116
STATE OF FLORIDA )
I ss ~
COUNTY OF DADE J. W. WilliaIIs, Jr., being first duly sworn, deposes and says:
1 That he is Vice President of Florida Power & Light Company, the licensee herei n; That he has executed the foregoing document; that the statements made in this document are true and correct to the best of his knowledge, information, and belief, and that he is authorized to execute the document on behalf of said Licensee.
. Williams, Jr.
t Subs ribed day and sworn of to before me this
, 1984.
NOTARY PUB'C, in and for the County of Dade, State of Florida.
AOTARY 'PUSUC STATs CF FlORIDA gY CGM!AISS IGN EXPIRH PER 12 1987 My commi ssi on expires: I DED THR'J,w:~~ I".'5'.LvlcE UND