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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E2061994-05-11011 May 1994 LER 93-025-01:on 931205,Loop a MSIVs Exceeded TS Leakage Limit.Caused by Failure of Fastner Locking Devices.Seating Surface of Main Disc in MSIV 1A Machined & Successfully Pass LLRT on 940116.W/940511 Ltr ML17352B2501993-10-0101 October 1993 LER 93-014-00:on 930902,discovered That IRM 11 & APRM Both in Bypassed Condition W/O Half Scram Being Inserted Due to Work Practices.Irm 11 Taken Out of Bypassed Condition & Individual Involved counselled.W/931001 Ltr ML17352B2511993-10-0101 October 1993 LER 93-019-00:on 930903,RHR Pump 1A Inadvertently Started Due to Personnel Error.Pump Immediately Secured & Individual Involved Counselled on Importance of self-check.W/931001 Ltr ML20046A1801993-07-21021 July 1993 LER 92-007-00:on 930624,Toxic Gas Analyzer Inoperable Due to Personnel Error Caused by Lack of Procedural Adherence. Isolated CR Ventilation,Restarted Sample Pump & Restored CR Ventilation Sys to Outside Air suction.W/930721 Ltr ML20045H5781993-07-13013 July 1993 LER 93-013-00:on 930613,internal Electrical Fault within Main Power Transformer Tripped & Caused Reactor Scram & Unexpected Group I Isolation.Caused by Turbine Stop Valve Closure.Transformer replaced.W/930713 Ltr ML20045G7291993-07-0909 July 1993 LER 93-005-00:on 930609,numerous Alarms Received in CR, Including HPCI Turbine Rupture Disc High Pressure Alarm. Caused by Ruptured Disk,Releasing Steam/Water Mixture. Test Will Be Conducted on Rupture disks.W/930709 Ltr ML20045G0951993-07-0202 July 1993 LER 93-011-00:on 930602,HPCI Declared Inoperable in Order to Perform Qcos 2300-13.Caused by MSC Stem & Stem Gear Being Scored & Worn from Age Causing Excessive Friction.C/As Include Disassembling Gearbox Every 10 yrs.W/930702 Ltr ML20045F3321993-06-30030 June 1993 LER 93-012-00:on 930601,U-2 DG Cooling Water Pump Inoperable Due to Inadequate lubrication.U-2 DG Cooling Water Pump replaced.W/930630 Ltr ML20045F3251993-06-28028 June 1993 LER 93-007-01:on 930307,B Loop MSIV Exceeded TS Leakage Limits for Containment Isolation Valves Caused by Damaged Flexitalic Bonnet Gasket.Replaced Bonnet Gasket & Valve Successfully Retested (WR Q061987).W/930622 Ltr ML20044E6171993-05-14014 May 1993 LER 93-006-00:on 930420,Unit 2 Nso Inadvertently Started Unit 1 DG When Attempting to Start Shared (1/2) Dg.Caused by Personnel Error.Unit 1 DG Shut Down & 1/2 DG Started & Loaded successfully.W/930514 Ltr ML20044C9511993-05-0707 May 1993 LER 93-009-00:on 930408,technician Discovered That Estimate of Sample Flow for U2 Reactor Bldg Vent Sampler Flow Rate Monitor Not Calculated.Caused by Personnel Error.Technician counseled.W/930428 Ltr ML20024G6811991-04-19019 April 1991 LER 91-008-00:on 910322,reactor Bldg Ventilation Isolation Occurred.Caused by Lightning Strike.Control Room Vents Reset & Toxic Gas Sample Point a Selected.Addl Trips Associated W/ Lightning Strike Immediately reset.W/910418 Ltr ML20029C1241991-03-0808 March 1991 LER 91-005-01:on 910131,1/2 B Standby Gas Treatment Sys Autostart During RPS B Power Swap Due to an Inadequate Procedure.Nso Reset 1/2 Scram & 1/2 Groups II & III isolations.W/910306 Ltr ML20029B5901991-03-0808 March 1991 LER 91-004-00:on 910211,standby Liquid Control Sys of Unit 1 & 2 Inoperable.Caused by Inadequate Mod Testing.Engineering Dept Evaluating Data & Temporary Procedure 6589 Generated. W/910308 Ltr ML20028H7841991-01-23023 January 1991 LER 90-032-00:on 901224,1/2A Diesel Fire Pump Taken out-of- Svc on 901217 & Not Returned to Svc Before Seven Day Time Allotment Expired.Caused by Mgt Deficiency.Fire Pump Successfully Tested & Returned to svc.W/910123 Ltr ML20028H6831991-01-21021 January 1991 LER 90-034-00:on 901223,high Chlorine Concentration Caused Control Room Ventilation Manual Isolation & ESF Actuation. Caused by Instrument Error Code & Misinterpretation of Analyzer Indication.Flow reduced.W/910121 Ltr ML20028G9141990-09-28028 September 1990 LER 90-018-00:on 900829,plant Outside Design Spec for Electrical Separation Criteria for Two Redundant Safety Sys. Caused by Inadequate Engineering Review During Leads installation.W/900928 Ltr ML20044B2401990-07-12012 July 1990 LER 90-012-00:on 900612,control Room Ventilation Emergency Air Filtration Unit Declared Inoperable.Caused by Heater Malfunction.Work Request initiated.W/900712 Ltr ML20044B0091990-07-11011 July 1990 LER 90-011-00:on 900611,diesel Fire Pump 1/2 a Out of Svc for Period Exceeding 7 Days Reporting Criteria,To Install New Suction Line.Caused by Required Maint Work.Repairs Completed & Pump Tested & Returned to svc.W/900711 Ltr ML20043H4831990-06-21021 June 1990 LER 90-010-00:on 900522,while Returning RWCU Sys to Svc, Nonregenerative HX High Temp Alarm Received,Challenging ESF Logic & Causing Group III Isolation.Caused by Leaking RWCU Check Valves.Work Requests issued.W/900621 Ltr ML20043H2931990-06-18018 June 1990 LER 90-009-00:on 900518,determined That Various Containment Vols Not Leak Rate Tested Due to Recent 10CFR50,App J Interpretation Re Licensing Design Criteria.Mod M4-1(2)-89-167 initiated.W/900618 Ltr ML20043H9521990-06-13013 June 1990 LER 90-016-01:on 900411,motor Control Ctr Relay 28/29-5 Setpoint Drift Occurred,Resulting in Analyzed Plant Condition.Caused by Utilizing Wrong Relay & Inadequate Review of GE Svc Info Ltr.Relay replaced.W/900613 Ltr ML20043E9121990-06-0707 June 1990 LER 90-006-00:on 900508,Unit 2 RCIC Declared Inoperable Due to Unstable Operation of RCIC Pump Flow Controller.Caused by Proportional Band of Controller Being Set to Respond to Changes in Flow Too Quickly.Flow controlled.W/900607 Ltr ML20043F2341990-06-0101 June 1990 LER 90-001-01:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Test Program.Caused by Misinterpretation of 10CFR50,App J Requirements.Required Vents & Test Taps Will Be installed.W/900601 Ltr ML20043F2161990-06-0101 June 1990 LER 89-024-01:on 891214,main Turbine Unexpectedly Tripped Following Isolation of Reactor Water Level Switch (Lits). Caused by Channel B Lits Having Been Previously Replaced W/ Switch That Operated Reverse function.W/900601 Ltr ML20042E4991990-04-17017 April 1990 LER 90-007-00:on 900318,ESF Actuation Occurred.Caused by Mgt Deficiency in Not Providing Sufficient Guidance for Review of Work Package After Scope Changed.New Work Package Preparation Procedures initiated.W/900417 Ltr ML20012C7231990-03-15015 March 1990 LER 90-004-00:on 900213,loss of Emergency Bus 23-1 Occurred Due to Shorted Conductor Cable While Performing Wiring Verification.Caused by Personnel Error & Improper Installation.Electric Power Supplies recovered.W/900315 Ltr ML20012C7171990-03-15015 March 1990 LER 90-003-00:on 900213,unit Diesel Generator Tripped on Overspeed Upon Manual Startup for Testing.Caused by Misadjustment of Diesel Generator Governor.Diesel Generator Equipment Reset & Governor adjusted.W/900315 Ltr ML20012B2931990-03-0505 March 1990 LER 90-002-00:on 900204,determined That Only Reactor Bldg Differential Pressure of 0.24-inch Water Vacuum Could Be Obtained,In Violation of Tech Spec Required 0.25 Inch.Caused by Testing Deficiency.Leak Paths sealed.W/900305 Ltr ML20012B2961990-03-0505 March 1990 LER 90-003-00:on 900205,determined That Leakage Rate for HPCI Sys Steam Exhaust Check Valve Exceeded Tech Spec Limits.Caused by Excessive Leakage.Check Valve Replaced W/ Mission Check Valve W/Carbon Steel springs.W/900305 Ltr ML20011E1821990-01-30030 January 1990 LER 90-002-00:on 900102,during Annual Water Sprinkler Sys Valve Position Insp,Discovered That Valve 2-4199-072 Not Cycled Per Tech Spec Surveillance Requirement 4.12.Caused by Procedural Deficiency.Procedure to Be revised.W/900130 Ltr ML19354D9431990-01-15015 January 1990 LER 89-025-00:on 891220,determined That Reactor Bldg Overhead Auxiliary Hook May Have Contacted Side of New Fuel Bundle on 891214,causing Extensive Damage.Caused by Personnel Error.Bundle Shipped Back to GE.W/900115 Ltr ML19354D9481990-01-15015 January 1990 LER 89-023-00:on 891219,identified Deficient Temporary Procedures Which Altered Intent of Original Procedure QAP 1100-7.Caused by Mgt Oversight in Preparation of Tech Spec Change.Temporary Procedures revised.W/900115 Ltr ML20005F5881990-01-0808 January 1990 LER 90-001-00:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Testing Program.Caused by Misinterpretation of 10CFR50,App J Testing Requirements.Mod of Sys to Be Performed as necessary.W/900108 Ltr ML20005G0231990-01-0202 January 1990 LER 88-020-01:on 880619,improper Valving Sequence Occurred Which Resulted in Various ESF Actuations.Caused by Inadequate Equipment out-of-svc Procedure.Procedure Revised & Training Lesson Plan developed.W/900102 Ltr ML20005E4531989-12-28028 December 1989 LER 89-022-00:on 891128,HPCI Declared Inoperable Following Unexpected Actuation of HPCI Pump Room Deluge Sys.Actuation Caused Dc Sys Grounds Due to Moisture Intrusion in Electrical Equipment.Equipment dried.W/891228 Ltr ML20005D9551989-12-22022 December 1989 LER 89-021-00:on 891124,HPCI Deluge Sys Functional Test Not Completed within Tech Spec Interval of 6 Months.Caused by Mgt Deficiency & Insufficient Procedure.Procedures Revised to Better Control Tech Specs.W/891222 Ltr ML19351A6391989-12-15015 December 1989 LER 89-020-00:on 891117,full Reactor Scram Occurred Due to Simultaneous Loss of Power to 1A & 1B 24/48-volt Distribution Panels During Panel Transfer.Caused by Personnel Error.Personnel Trained Re event.W/891215 Ltr ML19332E7581989-12-0505 December 1989 LER 89-019-00:on 891105,half Group II & III Isolation Occurred While Performing Valve Flow Check Surveillance. Caused by Leaky Isolation Valve on Transmitter.Surveillance Methods Will Be Reviewed & Procedures revised.W/891205 Ltr ML19332C7581989-11-20020 November 1989 LER 89-017-00:on 891022,discovered That 6-month Functional Test Procedure Qos 500-3 Re Functional Test for Reactor Protection Sys Electrical Assemblies Not Completed in Required Time.Caused by Mgt deficiency.W/891120 Ltr ML19327C0701989-11-0909 November 1989 LER 89-018-00:on 891012,notification Given of Potential Single Failure of Diesel Generator Voltage Regulator That Could Result in Loss of All But One ECCS Loop.Caused by Design Deficiency.New Procedure developed.W/891109 Ltr ML19327C0951989-11-0404 November 1989 LER 89-005-00:on 891012,reactor Scram Occurred Due to Turbine Stop Valve Closure.Caused by Personnel Error in That Work Analyst Overlooked Removal of Two Connections on Limit Switch.Maint Workers Immediately counseled.W/891104 Ltr ML19327C2631989-11-0101 November 1989 LER 87-009-01:on 870801,reactor Scram Occurred from Turbine Generator Load Mismatch Due to Generator Trip.Caused by Electrical Fault in Main Transformer C Phase Windings.Main Transformer Replaced w/spare.W/891103 Ltr ML19325E8261989-10-30030 October 1989 LER 87-012-01:on 870918,while Performing Qos 1600-1, Vacuum Breaker 2-1601-33E Remained Open After Testing.Caused by Binding in Test Cylinder Portion of Vacuum Breaker. Nuclear Work Requests completed.W/891030 Ltr ML19325E5921989-10-24024 October 1989 LER 87-017-01:on 870805,Group IV Isolation Received Which Resulted in Closure of HPCI Steam Supply Valves.Caused by Failed HPCI Steamline Differential Pressure Transmitter Due to Loss of Oil in Sensing cell.W/891024 Ltr ML19325E5971989-10-24024 October 1989 LER 88-003-01:on 880301,while Performing RCIC Monthly Test, RCIC Pump Could Only Achieve 400 Gpm Against Discharge Pressure of 500 Psig.Caused by Failed Hydraulic Actuator on Turbine Governor Valve.Actuator replaced.W/891024 Ltr ML19327B7901989-10-18018 October 1989 LER 89-016-00:on 890921,during Transfer of New Fuel,Fuel Assembly Released from Refueling Grapple & Fell Upon Spent Fuel Racks.Caused by Personnel Error & Procedural Deficiency.Fuel Handling Procedures Revised ML19327B0491989-10-16016 October 1989 LER 89-015-00:on 890916,during Transfer,Loss of Power to Off Gas Monitor a Caused Contacts to Open Giving Upscale Radiation Signal,Thus Starting Off Gas Timer.Caused by Inadequate Procedures.Off Gas Sys reset.W/891016 Ltr ML19325C5341989-10-0202 October 1989 LER 89-014-00:on 890910,determined That Combined Leakage Rate from All Penetrations & Valves Exceeded Tech Spec Limit.Root Cause Unknown.No Corrective Action Taken. Supplemental Rept Will Be issued.W/891002 Ltr ML18052B5541987-08-24024 August 1987 LER 87-015-00:on 870731,capacitor Failed on 1B Reactor Bldg & Refuel Floor Radiation Monitors Resulting in Safety Feature Actuation.Caused by Normal Aging.Capacitor replaced.W/870825 Ltr 1994-05-11
[Table view] Category:RO)
MONTHYEARML20029E2061994-05-11011 May 1994 LER 93-025-01:on 931205,Loop a MSIVs Exceeded TS Leakage Limit.Caused by Failure of Fastner Locking Devices.Seating Surface of Main Disc in MSIV 1A Machined & Successfully Pass LLRT on 940116.W/940511 Ltr ML17352B2501993-10-0101 October 1993 LER 93-014-00:on 930902,discovered That IRM 11 & APRM Both in Bypassed Condition W/O Half Scram Being Inserted Due to Work Practices.Irm 11 Taken Out of Bypassed Condition & Individual Involved counselled.W/931001 Ltr ML17352B2511993-10-0101 October 1993 LER 93-019-00:on 930903,RHR Pump 1A Inadvertently Started Due to Personnel Error.Pump Immediately Secured & Individual Involved Counselled on Importance of self-check.W/931001 Ltr ML20046A1801993-07-21021 July 1993 LER 92-007-00:on 930624,Toxic Gas Analyzer Inoperable Due to Personnel Error Caused by Lack of Procedural Adherence. Isolated CR Ventilation,Restarted Sample Pump & Restored CR Ventilation Sys to Outside Air suction.W/930721 Ltr ML20045H5781993-07-13013 July 1993 LER 93-013-00:on 930613,internal Electrical Fault within Main Power Transformer Tripped & Caused Reactor Scram & Unexpected Group I Isolation.Caused by Turbine Stop Valve Closure.Transformer replaced.W/930713 Ltr ML20045G7291993-07-0909 July 1993 LER 93-005-00:on 930609,numerous Alarms Received in CR, Including HPCI Turbine Rupture Disc High Pressure Alarm. Caused by Ruptured Disk,Releasing Steam/Water Mixture. Test Will Be Conducted on Rupture disks.W/930709 Ltr ML20045G0951993-07-0202 July 1993 LER 93-011-00:on 930602,HPCI Declared Inoperable in Order to Perform Qcos 2300-13.Caused by MSC Stem & Stem Gear Being Scored & Worn from Age Causing Excessive Friction.C/As Include Disassembling Gearbox Every 10 yrs.W/930702 Ltr ML20045F3321993-06-30030 June 1993 LER 93-012-00:on 930601,U-2 DG Cooling Water Pump Inoperable Due to Inadequate lubrication.U-2 DG Cooling Water Pump replaced.W/930630 Ltr ML20045F3251993-06-28028 June 1993 LER 93-007-01:on 930307,B Loop MSIV Exceeded TS Leakage Limits for Containment Isolation Valves Caused by Damaged Flexitalic Bonnet Gasket.Replaced Bonnet Gasket & Valve Successfully Retested (WR Q061987).W/930622 Ltr ML20044E6171993-05-14014 May 1993 LER 93-006-00:on 930420,Unit 2 Nso Inadvertently Started Unit 1 DG When Attempting to Start Shared (1/2) Dg.Caused by Personnel Error.Unit 1 DG Shut Down & 1/2 DG Started & Loaded successfully.W/930514 Ltr ML20044C9511993-05-0707 May 1993 LER 93-009-00:on 930408,technician Discovered That Estimate of Sample Flow for U2 Reactor Bldg Vent Sampler Flow Rate Monitor Not Calculated.Caused by Personnel Error.Technician counseled.W/930428 Ltr ML20024G6811991-04-19019 April 1991 LER 91-008-00:on 910322,reactor Bldg Ventilation Isolation Occurred.Caused by Lightning Strike.Control Room Vents Reset & Toxic Gas Sample Point a Selected.Addl Trips Associated W/ Lightning Strike Immediately reset.W/910418 Ltr ML20029C1241991-03-0808 March 1991 LER 91-005-01:on 910131,1/2 B Standby Gas Treatment Sys Autostart During RPS B Power Swap Due to an Inadequate Procedure.Nso Reset 1/2 Scram & 1/2 Groups II & III isolations.W/910306 Ltr ML20029B5901991-03-0808 March 1991 LER 91-004-00:on 910211,standby Liquid Control Sys of Unit 1 & 2 Inoperable.Caused by Inadequate Mod Testing.Engineering Dept Evaluating Data & Temporary Procedure 6589 Generated. W/910308 Ltr ML20028H7841991-01-23023 January 1991 LER 90-032-00:on 901224,1/2A Diesel Fire Pump Taken out-of- Svc on 901217 & Not Returned to Svc Before Seven Day Time Allotment Expired.Caused by Mgt Deficiency.Fire Pump Successfully Tested & Returned to svc.W/910123 Ltr ML20028H6831991-01-21021 January 1991 LER 90-034-00:on 901223,high Chlorine Concentration Caused Control Room Ventilation Manual Isolation & ESF Actuation. Caused by Instrument Error Code & Misinterpretation of Analyzer Indication.Flow reduced.W/910121 Ltr ML20028G9141990-09-28028 September 1990 LER 90-018-00:on 900829,plant Outside Design Spec for Electrical Separation Criteria for Two Redundant Safety Sys. Caused by Inadequate Engineering Review During Leads installation.W/900928 Ltr ML20044B2401990-07-12012 July 1990 LER 90-012-00:on 900612,control Room Ventilation Emergency Air Filtration Unit Declared Inoperable.Caused by Heater Malfunction.Work Request initiated.W/900712 Ltr ML20044B0091990-07-11011 July 1990 LER 90-011-00:on 900611,diesel Fire Pump 1/2 a Out of Svc for Period Exceeding 7 Days Reporting Criteria,To Install New Suction Line.Caused by Required Maint Work.Repairs Completed & Pump Tested & Returned to svc.W/900711 Ltr ML20043H4831990-06-21021 June 1990 LER 90-010-00:on 900522,while Returning RWCU Sys to Svc, Nonregenerative HX High Temp Alarm Received,Challenging ESF Logic & Causing Group III Isolation.Caused by Leaking RWCU Check Valves.Work Requests issued.W/900621 Ltr ML20043H2931990-06-18018 June 1990 LER 90-009-00:on 900518,determined That Various Containment Vols Not Leak Rate Tested Due to Recent 10CFR50,App J Interpretation Re Licensing Design Criteria.Mod M4-1(2)-89-167 initiated.W/900618 Ltr ML20043H9521990-06-13013 June 1990 LER 90-016-01:on 900411,motor Control Ctr Relay 28/29-5 Setpoint Drift Occurred,Resulting in Analyzed Plant Condition.Caused by Utilizing Wrong Relay & Inadequate Review of GE Svc Info Ltr.Relay replaced.W/900613 Ltr ML20043E9121990-06-0707 June 1990 LER 90-006-00:on 900508,Unit 2 RCIC Declared Inoperable Due to Unstable Operation of RCIC Pump Flow Controller.Caused by Proportional Band of Controller Being Set to Respond to Changes in Flow Too Quickly.Flow controlled.W/900607 Ltr ML20043F2341990-06-0101 June 1990 LER 90-001-01:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Test Program.Caused by Misinterpretation of 10CFR50,App J Requirements.Required Vents & Test Taps Will Be installed.W/900601 Ltr ML20043F2161990-06-0101 June 1990 LER 89-024-01:on 891214,main Turbine Unexpectedly Tripped Following Isolation of Reactor Water Level Switch (Lits). Caused by Channel B Lits Having Been Previously Replaced W/ Switch That Operated Reverse function.W/900601 Ltr ML20042E4991990-04-17017 April 1990 LER 90-007-00:on 900318,ESF Actuation Occurred.Caused by Mgt Deficiency in Not Providing Sufficient Guidance for Review of Work Package After Scope Changed.New Work Package Preparation Procedures initiated.W/900417 Ltr ML20012C7231990-03-15015 March 1990 LER 90-004-00:on 900213,loss of Emergency Bus 23-1 Occurred Due to Shorted Conductor Cable While Performing Wiring Verification.Caused by Personnel Error & Improper Installation.Electric Power Supplies recovered.W/900315 Ltr ML20012C7171990-03-15015 March 1990 LER 90-003-00:on 900213,unit Diesel Generator Tripped on Overspeed Upon Manual Startup for Testing.Caused by Misadjustment of Diesel Generator Governor.Diesel Generator Equipment Reset & Governor adjusted.W/900315 Ltr ML20012B2931990-03-0505 March 1990 LER 90-002-00:on 900204,determined That Only Reactor Bldg Differential Pressure of 0.24-inch Water Vacuum Could Be Obtained,In Violation of Tech Spec Required 0.25 Inch.Caused by Testing Deficiency.Leak Paths sealed.W/900305 Ltr ML20012B2961990-03-0505 March 1990 LER 90-003-00:on 900205,determined That Leakage Rate for HPCI Sys Steam Exhaust Check Valve Exceeded Tech Spec Limits.Caused by Excessive Leakage.Check Valve Replaced W/ Mission Check Valve W/Carbon Steel springs.W/900305 Ltr ML20011E1821990-01-30030 January 1990 LER 90-002-00:on 900102,during Annual Water Sprinkler Sys Valve Position Insp,Discovered That Valve 2-4199-072 Not Cycled Per Tech Spec Surveillance Requirement 4.12.Caused by Procedural Deficiency.Procedure to Be revised.W/900130 Ltr ML19354D9431990-01-15015 January 1990 LER 89-025-00:on 891220,determined That Reactor Bldg Overhead Auxiliary Hook May Have Contacted Side of New Fuel Bundle on 891214,causing Extensive Damage.Caused by Personnel Error.Bundle Shipped Back to GE.W/900115 Ltr ML19354D9481990-01-15015 January 1990 LER 89-023-00:on 891219,identified Deficient Temporary Procedures Which Altered Intent of Original Procedure QAP 1100-7.Caused by Mgt Oversight in Preparation of Tech Spec Change.Temporary Procedures revised.W/900115 Ltr ML20005F5881990-01-0808 January 1990 LER 90-001-00:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Testing Program.Caused by Misinterpretation of 10CFR50,App J Testing Requirements.Mod of Sys to Be Performed as necessary.W/900108 Ltr ML20005G0231990-01-0202 January 1990 LER 88-020-01:on 880619,improper Valving Sequence Occurred Which Resulted in Various ESF Actuations.Caused by Inadequate Equipment out-of-svc Procedure.Procedure Revised & Training Lesson Plan developed.W/900102 Ltr ML20005E4531989-12-28028 December 1989 LER 89-022-00:on 891128,HPCI Declared Inoperable Following Unexpected Actuation of HPCI Pump Room Deluge Sys.Actuation Caused Dc Sys Grounds Due to Moisture Intrusion in Electrical Equipment.Equipment dried.W/891228 Ltr ML20005D9551989-12-22022 December 1989 LER 89-021-00:on 891124,HPCI Deluge Sys Functional Test Not Completed within Tech Spec Interval of 6 Months.Caused by Mgt Deficiency & Insufficient Procedure.Procedures Revised to Better Control Tech Specs.W/891222 Ltr ML19351A6391989-12-15015 December 1989 LER 89-020-00:on 891117,full Reactor Scram Occurred Due to Simultaneous Loss of Power to 1A & 1B 24/48-volt Distribution Panels During Panel Transfer.Caused by Personnel Error.Personnel Trained Re event.W/891215 Ltr ML19332E7581989-12-0505 December 1989 LER 89-019-00:on 891105,half Group II & III Isolation Occurred While Performing Valve Flow Check Surveillance. Caused by Leaky Isolation Valve on Transmitter.Surveillance Methods Will Be Reviewed & Procedures revised.W/891205 Ltr ML19332C7581989-11-20020 November 1989 LER 89-017-00:on 891022,discovered That 6-month Functional Test Procedure Qos 500-3 Re Functional Test for Reactor Protection Sys Electrical Assemblies Not Completed in Required Time.Caused by Mgt deficiency.W/891120 Ltr ML19327C0701989-11-0909 November 1989 LER 89-018-00:on 891012,notification Given of Potential Single Failure of Diesel Generator Voltage Regulator That Could Result in Loss of All But One ECCS Loop.Caused by Design Deficiency.New Procedure developed.W/891109 Ltr ML19327C0951989-11-0404 November 1989 LER 89-005-00:on 891012,reactor Scram Occurred Due to Turbine Stop Valve Closure.Caused by Personnel Error in That Work Analyst Overlooked Removal of Two Connections on Limit Switch.Maint Workers Immediately counseled.W/891104 Ltr ML19327C2631989-11-0101 November 1989 LER 87-009-01:on 870801,reactor Scram Occurred from Turbine Generator Load Mismatch Due to Generator Trip.Caused by Electrical Fault in Main Transformer C Phase Windings.Main Transformer Replaced w/spare.W/891103 Ltr ML19325E8261989-10-30030 October 1989 LER 87-012-01:on 870918,while Performing Qos 1600-1, Vacuum Breaker 2-1601-33E Remained Open After Testing.Caused by Binding in Test Cylinder Portion of Vacuum Breaker. Nuclear Work Requests completed.W/891030 Ltr ML19325E5921989-10-24024 October 1989 LER 87-017-01:on 870805,Group IV Isolation Received Which Resulted in Closure of HPCI Steam Supply Valves.Caused by Failed HPCI Steamline Differential Pressure Transmitter Due to Loss of Oil in Sensing cell.W/891024 Ltr ML19325E5971989-10-24024 October 1989 LER 88-003-01:on 880301,while Performing RCIC Monthly Test, RCIC Pump Could Only Achieve 400 Gpm Against Discharge Pressure of 500 Psig.Caused by Failed Hydraulic Actuator on Turbine Governor Valve.Actuator replaced.W/891024 Ltr ML19327B7901989-10-18018 October 1989 LER 89-016-00:on 890921,during Transfer of New Fuel,Fuel Assembly Released from Refueling Grapple & Fell Upon Spent Fuel Racks.Caused by Personnel Error & Procedural Deficiency.Fuel Handling Procedures Revised ML19327B0491989-10-16016 October 1989 LER 89-015-00:on 890916,during Transfer,Loss of Power to Off Gas Monitor a Caused Contacts to Open Giving Upscale Radiation Signal,Thus Starting Off Gas Timer.Caused by Inadequate Procedures.Off Gas Sys reset.W/891016 Ltr ML19325C5341989-10-0202 October 1989 LER 89-014-00:on 890910,determined That Combined Leakage Rate from All Penetrations & Valves Exceeded Tech Spec Limit.Root Cause Unknown.No Corrective Action Taken. Supplemental Rept Will Be issued.W/891002 Ltr ML18052B5541987-08-24024 August 1987 LER 87-015-00:on 870731,capacitor Failed on 1B Reactor Bldg & Refuel Floor Radiation Monitors Resulting in Safety Feature Actuation.Caused by Normal Aging.Capacitor replaced.W/870825 Ltr 1994-05-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30
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[ 'N C::mmonwealth Edison t . ) Quad Cates Nuclear Power Staten I - ' 22710 206 Avenue North
\ '~' Cordova, Illinois 61242-9740
%_/ Teephone 309/654 2241 GGC-94-080 May 11. 1994 U.S. Nuclear Regulatory Commission Document Control Desk Washington. DC 20555
Reference:
Quad Cities Nuclear Power Station Docket Number 50-265. DPR-30. Unit Two Enclosed is Licensee Event Report (LER)93-025. Revision 01. for Quad Cities Nuclear Power Plant Station.
This report is submitted in accordance with the requirements of the Code of I Federal Regulations. Title 10. Part 50.73(a)(2)(ii)(B). Any event or l condition that resulted in the condition of the nuclear power plant, including l its principal safety barriers being seriously degraded or that resulted in the i nuclear plant being in a condition that was outside the design basis of the plant.
l The following commitments are restated:
- 1. All MSIV's that are disassembled will have new locking devices installed during reassembly.
- 2. Develop a maintenance procedure for disassembly and reassembly of l MSIV's. l
- 3. Review the existing Preventive Maintenance program for MSIV's and revise as necessary to include vendor and industry experience.
If there are any questions or comments concerning this letter. please refer them to Nick Chrissotimos. Regulatory Assurance Administrator at 309-654-2241.
ext. 3100.
l Respectfully.
COMMONWEALTH EDISON
! OUAD CITIES NUCLEAR POWER STATION G. G. Campbell Station Manager
! GGC/TB/plm l
l Enclosure cc: J. Schrage i C. Miller INPO Records Center NRC Region III i
STMGR\08004.GGC i I
] ]'C g UqC 9405170217 940511 {
V PDR ADOCK 05000265 3 S PDR
LICENSEE EVENT RE10RT (LER) Form Rev. 2.0 Facdiry Name (1) Docket Number (2) Page (3)
Quad Cities. Unit Two 0l5l0l0l0l2l6l5 1 l of l 0 l 6 Trde (4)
A Loop Main steam isolation Valves Exceed Tech spec Leakage Limits Event Date (3) LER Number (6) Repon Date (7) Other Facdices Involved (5)
Monta Day Year Year Sequennal Revision Month Day Year Facdsty Docket Numberts) i Number Number Names I 0l5l0l0l0l l l 1l2 0l5 9l3 9l3 C.PERATIN 3 0l2l5 -
0l1 0l5 1 1 9 4 TH15 REPORT 15 5UBMit Atu FU L5UANT TO ITE REQU, REMENTS OF loCFR 0l5l0l0l0l l l l
MODE (9) [ Check one or more of the followmg) (11) 01 20.402(b> zo.403(c) 50.73(aX2Xiv) 73.7 t(b) ,
POWER 20.405(aXIXi) 50.36(cXI) 50.73(aX2Xv) -73.71(c) '
LEVEL -20.405(aX1Xii) 50.36(cX2) 50.73(aX2 Xvii) Other (Spectfy (10) l l 0 -20.405(sXIXiii) 50.73(aX2Xi) 50.73(aX2)(viiiXA) m Abstract 20.405(aXIXiv) T50.73(ax2Xii) 50.73(aX2XviiiXB) below and in
-20.405(aX X Xv) 50.73(aK2Xiii) 50.73(aX2Xx) Text) f LICENSEE CON TACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE Dale Thayer, Regulatory Assurance, Ext. 3109 3l0l9 6l5l4l-l2l2l4l1 '
COMPLLib ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN 11i15 REPORT (13)
CaU5E SYSTEM COMPONENT MANUFACTURER REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS TO NPRDS D l l l l l l l l l l l l l l 1 I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED (14) Expected Month Day Year Submission YES (If yes, complete EXPECTED SUBMISSION DATE) 70 ABSTRACT (Lunit to 1400 spaces. a.c., approximately fifteen smgle-space typewntren imes) (16)
Date (15) l l l I
A. ABSTRACT:
I Unit 2 was in the SHUTDOWN mode at 0% power for a maintenance outage on 12/05/93 at 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> at which time, during the performance of a combined Local Leak Rate Test of the "A" loop Main Steam Isolation Valves (MSIV's) [SB] [ISV], the leakage exceeded l the 11.5 standard cubic feet per hour (scfh) Technical Specification limit of T.S.
, 3.7.A.2.e. The measured leakage was 24.8 scfh. The MSIV's are 20 inch Y-pattern l globe valves. Crane Drawing DR-34289, Revision "H" l
The 1A MSIV was subsequently disassembled for inspection. The cause of the excessive leakage was steam erosion on the pilot and main disc. The fasteners which retain the main valve disc to the valve stem were also found to be loose.
The apparent cause of the valve internai deficiencies was the failure of the fastener locking devices. The primary causal factors of this deficiency are inadequate MAINTENANCE / TESTING and WRITTEN COMMUNICATION which both resulted in the improper use of the fastener locking devices.
LER265\93'.025RI.WPF
LICENSEE EVENT REPORT a.ER)' EXT CONTINUATION Form Rev. 2.0 FACILITY NAME (1) DOCMI NUMBE (2) LER NUMBER (6) PAGL di Year Sequennal Revision
. Number Number Quad Cities Unit Two 0l5l0l0l0l2l6l5 9l3 -
0l2l5 -
0l1 2 lOFl 0 l 6 IEXI Energy Industry Idenuncanon System (Ell 5) codes arc idennhed m the text as [XXJ PLANT AND SYSTEM IDENTIFICATION:
General Electric - Boiling Water Reactor - 2511 MWt rated core thermal ;>ower.
EVENT IDENTIFICATION: A loop main steam isolation valves exceed Tech Spec leakage limits. l A. CONDITIONS PRIOR TO EVENT: )
Unit: Two Event Date: December 5. 1993 Event Time: 2300 Reactor Mode: 1 Mode Name: Shutdown Power Level: 0 ;
This report was initiated by Licensee Report 265\93-025.
SHUTDOWN (1) - In this position, a reactor scram is initiated. aower to the control rod drives is removed. and the reactor protection trip systems lave been deenergized for 10 seconds prior to penaissive for manual reset.
B. DESCRIPTION OF EVENT:
On 12/04/93, during cold shutdown fail-safe testing of the Unit 2 inboard Main Steam Line Isolation Valves (MSIV's) [SB] [ISV), the A0-2-203-1A MSIV failed to completely close. The valve remained open approximately 1-3/4 inches. The 1A MSIV did close when air was valved back into its actuator. The fail-safe test was performed again '
for the 1A MSIV later on 12/04/93. with the same results. All other Unit 2 MSIV's successfully passed the fail-safe test.
On 12/05/93. Local Leak Rate Testing of the 1A and 2A MSIV's (AO-2-203-1A and A0 203-2A) was performed. At 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on 12/05/93, it was determined that the Local Leak Rate Test failed due to a combined leakage rate of 24.8 standard cubic feet per hour (scfh). The MSIV Technical Specification limit is 11.5 scfh for one (1) valve (T.S. 3.7.A.2.a.3).
The 1A MSIV was subsequently disassembled for inspection. An inspection of the valve internals was performed on 12/12/93. with the following results concerning the locking devices and fasteners.
All eight (8) disc plate nuts were found not to be tight. All disc plate studs were still threaded securely to the main disc. but a number of the studs appeared to be bent. One disc plate stud was broke about 1/2 inch from the to). Significant thread damage was noticed at the fractured end of the broken stud. wit 1 less thread damage on the other studs. Remains of two (2) nut locking devices were found.
A determination was made to disassemble and inspect four (4) additional MSIV's on Unit 2. After inspection of these additional valves, the decision was made to shut down Unit 1 and inspect those MSIV's even though the operability determination for Unit 1 indicated " operable, but degraded" LER265\93\025RI.%7F
t .
l l LICENSEE EVENT REPOR f (LER) TEXT CONTINUATION Form Rev. 2.0 I . FACILITY NAME (1) DOCKhl NUMBER (2) LER NUMBhR (6) PAGE Q) l' Year Sequennaj Revison
, Number Number Quad Cities Unit Two 0l5l0l0l0l2l6l5 9l3 -
0l2l5 -
0l1 3 lOFl 0 l 6 ILA1 Energy Indusuy Idenoticanon System th11M codes are adenched m the text as [AAJ C. APPARENT CAUSE OF EVENT:
The apparent cause of the valve damage was the failure of the fastener locking devices due to improper use of the devices, which is believed to have contributed to excessive wear of the main and pilot seats and discs due to vibration of the loose parts. Improper use may include reuse of old locking devices, or locking devices installed, but the tabs not being properly bent, or locking devices not being installed. The primary Casual Factors related to the event were lack of pro)er MAINTENANCE / TESTING and WRITTEN COMMUNICATION. Information describing why t1ese Casual Factors contributed to this event is listed below:
- 1. MAINTENANCE / TESTING Improper reassembly of the component (improper use of the locking devices) was the primary cause. The work instructions contained no provisions for positive control of the installation of the locking devices. ,
System Materials Analysis Department (SMAD) test results were as follows:
i The SMAD test report (#M-00680-94, dated 02/08/94) concludes that the 1A MSIV disc plate stud failed due to fatigue cracking.
Visual inspection of the 1A MSIV disc alate stud revealed that the stud had fractured transversely at the fourth taread root. Over 80% of the fracture i surface of the stud was oxidized and flattened, probably caused by exposure to '
the service environment after the fracture. Due to the condition of the fracture surface, the time of failure was indeterminate. Remnants of beach marks (crack 4 arrest marks) were visible on the fracture surface emanating from a thread root l for approximately 1/8" across the fracture face. Beach marks are characteristic of fatigue crack propagation. The pattern of the remnant beach marks imalies failure under unidirectional bending conditions in the presence of a higi nominal stress.
Although the fracture surface had been flattened, a cross section revealed that the cracking initiated at a thread root and propagated transgranularly. No crack initiation at adjacent thread roots was observed. '
Fatigue cracking of fasteners is most often caused by improper tightening of the fastener. If the disc plate nut is not properly tightened and secured, the disc plate stud experiences cyclic stresses due to the greater than normal operational vibration of the disc ) late. These stresses are concentrated and amplified at the thread roots, whic1 leads to fatigue crack initiation and propagation. The !
disc plate nuts on the 1A MSIV may have come loose due to improper torquing of the nuts or improper installation of the nut locking devices.
LER265\93\025R1.WPF
LICENSEE EVENT REPORT (LER)'MDCT CONTINUATION Form Rev. 2.0 FACILITY NAME (1) DOLAtt NUMBER (2) IER NUhU5EK (6) PAGE (3)
Year Sequenual Revision Number Number l
Quad Cities Unit Two 0l5l0l0l0l2 6l5 9l3 -
0l2l5 -
0l1 4 lOFl 0 l 6 atA1 Energy Industry Idennhcanon System (tin) codes are idenafied m the next as [AAl l
To prevent fatigue cracking of the disc plate studs, the fasteners should be properly tightened. The disc plate nuts should be torqued to the manufacturer's specified torque value. To properly secure the disc plate nuts, the tabs on the nut locking devices should be bent in opposite directions; upward against a nut flat. and downward against the valve disc plate.
SMAD also issued a letter dated 03/28/94 addressing the use of Inconel'600 l locking tabs for securing MSIV disc plate studs. This letter stated the i following l
The failure analysis of pieces of Inconel 600 locking tab, from the Quad Cities 1A MSIV revealed the failures were caused by ductile tearing and fatigue crack i propagation. '
i Inconel 600 is not generally susceptible to stress corrosion cracking (SCC) in a l BWR steam environment. However, highly stressed Inconel 600 material is susceptible to SCC under creviced conditions of a BWR water environment.
Inconel 600 is not susceptible to thermal or radiation embrittlement in the MSIV l application. Radiation embrittlement would only be expected to occur in high influence areas near the reactor core.
SMAD considers Inconel 600 to be an acceptable material for the MSIV locking tab application. However, if water can accumulate in the locking tab area. Type 304L or Type 316L stainless steels should be considered for future replacements due to SCC concerns. It should be noted that the examined tabs from the 1A MSIV did not fail due to SCC.
In tallation of the locking tabs results in severe cold working of the bend areas. Cold working causes an increase in strength and residual stresses along with a reduction in ductility. If the locking tabs are used more than once, the straightening and rebending process will produce additional cold working which may initiate tears. Therefore. SMAD does not recommend re-using the locking tabs.
i
- 2. WRITTEN COMMUNICATION The maintenance work instructions (Work Package Traveler) did no' t contain any statements about proper use of the locking devices. The vendor manual 4 instruction did not address the reuse of the locking devices, and did not address preventive maintenance requirements. In both cases, omission of relevant information contributed to the locking devices being reused.
The above causal factors are based on a review of the completed work package that was used when the valve was last disassembled in 1980. and test results received from-SMAD.
LER265\9335R1.WPF
l 1-I UCENSEE EVENT REPORT (LER) TEXT CONTINUATION Form Rev. 2.0 is FACILIIT NAME (1) DOLLbt NUMBtK (2) LER NUM5tK (b) PAGE (31 Year Sequennal Revison l . Number Number l
l Quad Cities Unit Two 0l5l0l0l0l2l6l5 9l3 -
0l2l5 -
0l1 5 lOFl 0 l 6 i ItA4 Energy Indusny Idennficanon System (bla) codes are utennfed in the text as (AAJ D. SAFETY ANALYSIS OF EVENT:
The sudden closure of an MSIV due to the separation of the disc from the stem is bounded by current licensing based analysis. The transients which bound the event ;
are MSIV closure on a Flux Scram Turbine Trip Without Bypass, and Load Rejection '
Without Bypass at Increased Core Flow. The radiological consequences of the event are minimal since the pressure decay method of Local Leak Rate Testing is conservative and resulted in a combined leakage of 24.8 scfh. The normal practice !
is to perform individual leak rate tests, with the lowest individual valve leakage !
representing the leakage through the line assuming both valves are operable. In this case, individual leak rate tests were not conducted because the 1A MSIV had failed the fail-safe test and was scheduled for disassembly for inspection. The worst case !
assumption would be to assign a leak rate of 12.4 scfh to each valve. Considering the conservatism of the Technical Specification limit of 11.5 scfh, the leakage identified through the "A" main steam line would not result in exceeding the 10CFR100 )
limits. '
E. CORRECTIVE ACTIONS:
- 1. CORRECTIVE ACTIONS COMPLETED: l
- a. Five (5) of the eight (8) MSIV's on Unit 2 have been disassembled and l inspected. (Those inspected are: 2-203-1A. -2A, -1C. -2C, and -10.) This action was determined prudent due to the inspection results cf the 1A MSIV ,
and the fact that these results were similar to the previous event in 1991 in l which the disc separated from the stem on the IB MSIV. All fasteners in all
! valves inspected were found to be tight. All locking devices in all valves l inspected were found to be installed; however, some tabs on the locking i devices in the 2A valve were found to be missing. A review of the work history for the three (3) remaining MSIV's indicated the locking devices were properly installed.
- b. The main seat has been replaced in the 1A MSIV on Unit 2. The pilot seat and disc has also been replaced in the same valve.
- c. Unit 1 was scheduled for a shutdown in order to obtain positive evidence as to the condition of the MSIV disc fastener locking devices so as to provide reasonable assurance that the disc and stem of each MSIV are properly secured. Subsequent to this decision, Unit 1 inadvertently scrammed prior to the scheduled shutdown (LER 1-93-023). and it was decided to keep the unit shut down until the status of the MSIV's could be ascertained,
- d. The maintenance history records were reviewed for all eight (8) MSIV's on Unit 1 in order to obtain positive assurance that locking devices were
)roperly installed during the last time each valve was worked on internally.
Jsing this method, only one (1) MSIV (1-203-1C) could be verified as having the locking devices properly installed. The remaining seven (7) MSIV's on Unit 1 (1-203-1A, -1B, -10. -2A, -2B, -2C. and -20) were radiographically l examined with the linear accelerator. The results indicated all fasteners are installed and locking devices are installed.
i LER265\93\025R1.WPF l
e LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Form Rev. 2.0 FACILITY NAME (1) DOut:1 NUMBt* (2) LER NUMBER (6) PAGE (3i Year Sequennal Revissan Number Number Quad Cities Unit Two 0l5l0l0l0l2l6l5 9l3 -
0l2l5 -
0l0 6 lOF) 0 l 6 l ui Energy indusiry idenaricanon syseem <tais) codes are usennried in ibe iexi s ixxi
- 2. CORRECTIVE ACTIONS TO BE COMPLETED:
- a. Machine the seating surface of the main disc in the 1A MSIV on Unit 2. and successfully pass a Local Leak Rate Test. The valve passed the Local Leak i
. Rate Test on 01/16/94. This item was closed on 03/11/94 l (NTS# 2651809302501).
- b. All MSIV's that are disassembled will have new locking devices installed during re-assembly (NTS# 2651809302502).
- c. Revise Work Package Travelers to include the recuirement for installation of new locking devices when MSIV's are re-assemblec and details pertaining to bending the tabs. This item was completed during the 02M11 outage. This item was closed on 02/23/94 (NTS# 2651809302503). !
- d. Develop a maintenance procedure for disassembly and re-assembly of MSIV's (NTS# 2651809302504).
- e. Review the existing Preventive Maintenance program for MSIV's, and revise as necessary to include vendor and industry experience (NTS# 2651809302505).
F. PREVIOUS EVENTS:
09/18/91 A Unit 2 MSIV (AO-2-203-1B) main disc separated from the valve stem while at power. The unit was shut down. The cause of the failure was attributed to improper installation of the locking devices. Possibly, not all of the locking devices were installed, or the fasteners were not properly torqued. The event was not reported as an LER since the MSIV was disassembled without performing an "as found" Local Leak Rate Test.
LER 1-89-014 Exceeding (T.S.) (LLRT) leakage limits for containment isolation valves and MSIV's.
LER 2-93-007 "B" loop MSIV's failed LLRT.
G. COMPONENT FAILURE DATA:
Component Descriotion Manufacturer /Model As Found (scfh)
Main Steam Isolation Crane 20 inch 24.8
- Valve 2-203-1A/2A 1250 lb model B102681-D
- Combined leakage of both Inboard and Outboard MSIV's.
LER265W3\025RI.WPF i