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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E2061994-05-11011 May 1994 LER 93-025-01:on 931205,Loop a MSIVs Exceeded TS Leakage Limit.Caused by Failure of Fastner Locking Devices.Seating Surface of Main Disc in MSIV 1A Machined & Successfully Pass LLRT on 940116.W/940511 Ltr ML17352B2501993-10-0101 October 1993 LER 93-014-00:on 930902,discovered That IRM 11 & APRM Both in Bypassed Condition W/O Half Scram Being Inserted Due to Work Practices.Irm 11 Taken Out of Bypassed Condition & Individual Involved counselled.W/931001 Ltr ML17352B2511993-10-0101 October 1993 LER 93-019-00:on 930903,RHR Pump 1A Inadvertently Started Due to Personnel Error.Pump Immediately Secured & Individual Involved Counselled on Importance of self-check.W/931001 Ltr ML20046A1801993-07-21021 July 1993 LER 92-007-00:on 930624,Toxic Gas Analyzer Inoperable Due to Personnel Error Caused by Lack of Procedural Adherence. Isolated CR Ventilation,Restarted Sample Pump & Restored CR Ventilation Sys to Outside Air suction.W/930721 Ltr ML20045H5781993-07-13013 July 1993 LER 93-013-00:on 930613,internal Electrical Fault within Main Power Transformer Tripped & Caused Reactor Scram & Unexpected Group I Isolation.Caused by Turbine Stop Valve Closure.Transformer replaced.W/930713 Ltr ML20045G7291993-07-0909 July 1993 LER 93-005-00:on 930609,numerous Alarms Received in CR, Including HPCI Turbine Rupture Disc High Pressure Alarm. Caused by Ruptured Disk,Releasing Steam/Water Mixture. Test Will Be Conducted on Rupture disks.W/930709 Ltr ML20045G0951993-07-0202 July 1993 LER 93-011-00:on 930602,HPCI Declared Inoperable in Order to Perform Qcos 2300-13.Caused by MSC Stem & Stem Gear Being Scored & Worn from Age Causing Excessive Friction.C/As Include Disassembling Gearbox Every 10 yrs.W/930702 Ltr ML20045F3321993-06-30030 June 1993 LER 93-012-00:on 930601,U-2 DG Cooling Water Pump Inoperable Due to Inadequate lubrication.U-2 DG Cooling Water Pump replaced.W/930630 Ltr ML20045F3251993-06-28028 June 1993 LER 93-007-01:on 930307,B Loop MSIV Exceeded TS Leakage Limits for Containment Isolation Valves Caused by Damaged Flexitalic Bonnet Gasket.Replaced Bonnet Gasket & Valve Successfully Retested (WR Q061987).W/930622 Ltr ML20044E6171993-05-14014 May 1993 LER 93-006-00:on 930420,Unit 2 Nso Inadvertently Started Unit 1 DG When Attempting to Start Shared (1/2) Dg.Caused by Personnel Error.Unit 1 DG Shut Down & 1/2 DG Started & Loaded successfully.W/930514 Ltr ML20044C9511993-05-0707 May 1993 LER 93-009-00:on 930408,technician Discovered That Estimate of Sample Flow for U2 Reactor Bldg Vent Sampler Flow Rate Monitor Not Calculated.Caused by Personnel Error.Technician counseled.W/930428 Ltr ML20024G6811991-04-19019 April 1991 LER 91-008-00:on 910322,reactor Bldg Ventilation Isolation Occurred.Caused by Lightning Strike.Control Room Vents Reset & Toxic Gas Sample Point a Selected.Addl Trips Associated W/ Lightning Strike Immediately reset.W/910418 Ltr ML20029C1241991-03-0808 March 1991 LER 91-005-01:on 910131,1/2 B Standby Gas Treatment Sys Autostart During RPS B Power Swap Due to an Inadequate Procedure.Nso Reset 1/2 Scram & 1/2 Groups II & III isolations.W/910306 Ltr ML20029B5901991-03-0808 March 1991 LER 91-004-00:on 910211,standby Liquid Control Sys of Unit 1 & 2 Inoperable.Caused by Inadequate Mod Testing.Engineering Dept Evaluating Data & Temporary Procedure 6589 Generated. W/910308 Ltr ML20028H7841991-01-23023 January 1991 LER 90-032-00:on 901224,1/2A Diesel Fire Pump Taken out-of- Svc on 901217 & Not Returned to Svc Before Seven Day Time Allotment Expired.Caused by Mgt Deficiency.Fire Pump Successfully Tested & Returned to svc.W/910123 Ltr ML20028H6831991-01-21021 January 1991 LER 90-034-00:on 901223,high Chlorine Concentration Caused Control Room Ventilation Manual Isolation & ESF Actuation. Caused by Instrument Error Code & Misinterpretation of Analyzer Indication.Flow reduced.W/910121 Ltr ML20028G9141990-09-28028 September 1990 LER 90-018-00:on 900829,plant Outside Design Spec for Electrical Separation Criteria for Two Redundant Safety Sys. Caused by Inadequate Engineering Review During Leads installation.W/900928 Ltr ML20044B2401990-07-12012 July 1990 LER 90-012-00:on 900612,control Room Ventilation Emergency Air Filtration Unit Declared Inoperable.Caused by Heater Malfunction.Work Request initiated.W/900712 Ltr ML20044B0091990-07-11011 July 1990 LER 90-011-00:on 900611,diesel Fire Pump 1/2 a Out of Svc for Period Exceeding 7 Days Reporting Criteria,To Install New Suction Line.Caused by Required Maint Work.Repairs Completed & Pump Tested & Returned to svc.W/900711 Ltr ML20043H4831990-06-21021 June 1990 LER 90-010-00:on 900522,while Returning RWCU Sys to Svc, Nonregenerative HX High Temp Alarm Received,Challenging ESF Logic & Causing Group III Isolation.Caused by Leaking RWCU Check Valves.Work Requests issued.W/900621 Ltr ML20043H2931990-06-18018 June 1990 LER 90-009-00:on 900518,determined That Various Containment Vols Not Leak Rate Tested Due to Recent 10CFR50,App J Interpretation Re Licensing Design Criteria.Mod M4-1(2)-89-167 initiated.W/900618 Ltr ML20043H9521990-06-13013 June 1990 LER 90-016-01:on 900411,motor Control Ctr Relay 28/29-5 Setpoint Drift Occurred,Resulting in Analyzed Plant Condition.Caused by Utilizing Wrong Relay & Inadequate Review of GE Svc Info Ltr.Relay replaced.W/900613 Ltr ML20043E9121990-06-0707 June 1990 LER 90-006-00:on 900508,Unit 2 RCIC Declared Inoperable Due to Unstable Operation of RCIC Pump Flow Controller.Caused by Proportional Band of Controller Being Set to Respond to Changes in Flow Too Quickly.Flow controlled.W/900607 Ltr ML20043F2341990-06-0101 June 1990 LER 90-001-01:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Test Program.Caused by Misinterpretation of 10CFR50,App J Requirements.Required Vents & Test Taps Will Be installed.W/900601 Ltr ML20043F2161990-06-0101 June 1990 LER 89-024-01:on 891214,main Turbine Unexpectedly Tripped Following Isolation of Reactor Water Level Switch (Lits). Caused by Channel B Lits Having Been Previously Replaced W/ Switch That Operated Reverse function.W/900601 Ltr ML20042E4991990-04-17017 April 1990 LER 90-007-00:on 900318,ESF Actuation Occurred.Caused by Mgt Deficiency in Not Providing Sufficient Guidance for Review of Work Package After Scope Changed.New Work Package Preparation Procedures initiated.W/900417 Ltr ML20012C7231990-03-15015 March 1990 LER 90-004-00:on 900213,loss of Emergency Bus 23-1 Occurred Due to Shorted Conductor Cable While Performing Wiring Verification.Caused by Personnel Error & Improper Installation.Electric Power Supplies recovered.W/900315 Ltr ML20012C7171990-03-15015 March 1990 LER 90-003-00:on 900213,unit Diesel Generator Tripped on Overspeed Upon Manual Startup for Testing.Caused by Misadjustment of Diesel Generator Governor.Diesel Generator Equipment Reset & Governor adjusted.W/900315 Ltr ML20012B2931990-03-0505 March 1990 LER 90-002-00:on 900204,determined That Only Reactor Bldg Differential Pressure of 0.24-inch Water Vacuum Could Be Obtained,In Violation of Tech Spec Required 0.25 Inch.Caused by Testing Deficiency.Leak Paths sealed.W/900305 Ltr ML20012B2961990-03-0505 March 1990 LER 90-003-00:on 900205,determined That Leakage Rate for HPCI Sys Steam Exhaust Check Valve Exceeded Tech Spec Limits.Caused by Excessive Leakage.Check Valve Replaced W/ Mission Check Valve W/Carbon Steel springs.W/900305 Ltr ML20011E1821990-01-30030 January 1990 LER 90-002-00:on 900102,during Annual Water Sprinkler Sys Valve Position Insp,Discovered That Valve 2-4199-072 Not Cycled Per Tech Spec Surveillance Requirement 4.12.Caused by Procedural Deficiency.Procedure to Be revised.W/900130 Ltr ML19354D9431990-01-15015 January 1990 LER 89-025-00:on 891220,determined That Reactor Bldg Overhead Auxiliary Hook May Have Contacted Side of New Fuel Bundle on 891214,causing Extensive Damage.Caused by Personnel Error.Bundle Shipped Back to GE.W/900115 Ltr ML19354D9481990-01-15015 January 1990 LER 89-023-00:on 891219,identified Deficient Temporary Procedures Which Altered Intent of Original Procedure QAP 1100-7.Caused by Mgt Oversight in Preparation of Tech Spec Change.Temporary Procedures revised.W/900115 Ltr ML20005F5881990-01-0808 January 1990 LER 90-001-00:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Testing Program.Caused by Misinterpretation of 10CFR50,App J Testing Requirements.Mod of Sys to Be Performed as necessary.W/900108 Ltr ML20005G0231990-01-0202 January 1990 LER 88-020-01:on 880619,improper Valving Sequence Occurred Which Resulted in Various ESF Actuations.Caused by Inadequate Equipment out-of-svc Procedure.Procedure Revised & Training Lesson Plan developed.W/900102 Ltr ML20005E4531989-12-28028 December 1989 LER 89-022-00:on 891128,HPCI Declared Inoperable Following Unexpected Actuation of HPCI Pump Room Deluge Sys.Actuation Caused Dc Sys Grounds Due to Moisture Intrusion in Electrical Equipment.Equipment dried.W/891228 Ltr ML20005D9551989-12-22022 December 1989 LER 89-021-00:on 891124,HPCI Deluge Sys Functional Test Not Completed within Tech Spec Interval of 6 Months.Caused by Mgt Deficiency & Insufficient Procedure.Procedures Revised to Better Control Tech Specs.W/891222 Ltr ML19351A6391989-12-15015 December 1989 LER 89-020-00:on 891117,full Reactor Scram Occurred Due to Simultaneous Loss of Power to 1A & 1B 24/48-volt Distribution Panels During Panel Transfer.Caused by Personnel Error.Personnel Trained Re event.W/891215 Ltr ML19332E7581989-12-0505 December 1989 LER 89-019-00:on 891105,half Group II & III Isolation Occurred While Performing Valve Flow Check Surveillance. Caused by Leaky Isolation Valve on Transmitter.Surveillance Methods Will Be Reviewed & Procedures revised.W/891205 Ltr ML19332C7581989-11-20020 November 1989 LER 89-017-00:on 891022,discovered That 6-month Functional Test Procedure Qos 500-3 Re Functional Test for Reactor Protection Sys Electrical Assemblies Not Completed in Required Time.Caused by Mgt deficiency.W/891120 Ltr ML19327C0701989-11-0909 November 1989 LER 89-018-00:on 891012,notification Given of Potential Single Failure of Diesel Generator Voltage Regulator That Could Result in Loss of All But One ECCS Loop.Caused by Design Deficiency.New Procedure developed.W/891109 Ltr ML19327C0951989-11-0404 November 1989 LER 89-005-00:on 891012,reactor Scram Occurred Due to Turbine Stop Valve Closure.Caused by Personnel Error in That Work Analyst Overlooked Removal of Two Connections on Limit Switch.Maint Workers Immediately counseled.W/891104 Ltr ML19327C2631989-11-0101 November 1989 LER 87-009-01:on 870801,reactor Scram Occurred from Turbine Generator Load Mismatch Due to Generator Trip.Caused by Electrical Fault in Main Transformer C Phase Windings.Main Transformer Replaced w/spare.W/891103 Ltr ML19325E8261989-10-30030 October 1989 LER 87-012-01:on 870918,while Performing Qos 1600-1, Vacuum Breaker 2-1601-33E Remained Open After Testing.Caused by Binding in Test Cylinder Portion of Vacuum Breaker. Nuclear Work Requests completed.W/891030 Ltr ML19325E5921989-10-24024 October 1989 LER 87-017-01:on 870805,Group IV Isolation Received Which Resulted in Closure of HPCI Steam Supply Valves.Caused by Failed HPCI Steamline Differential Pressure Transmitter Due to Loss of Oil in Sensing cell.W/891024 Ltr ML19325E5971989-10-24024 October 1989 LER 88-003-01:on 880301,while Performing RCIC Monthly Test, RCIC Pump Could Only Achieve 400 Gpm Against Discharge Pressure of 500 Psig.Caused by Failed Hydraulic Actuator on Turbine Governor Valve.Actuator replaced.W/891024 Ltr ML19327B7901989-10-18018 October 1989 LER 89-016-00:on 890921,during Transfer of New Fuel,Fuel Assembly Released from Refueling Grapple & Fell Upon Spent Fuel Racks.Caused by Personnel Error & Procedural Deficiency.Fuel Handling Procedures Revised ML19327B0491989-10-16016 October 1989 LER 89-015-00:on 890916,during Transfer,Loss of Power to Off Gas Monitor a Caused Contacts to Open Giving Upscale Radiation Signal,Thus Starting Off Gas Timer.Caused by Inadequate Procedures.Off Gas Sys reset.W/891016 Ltr ML19325C5341989-10-0202 October 1989 LER 89-014-00:on 890910,determined That Combined Leakage Rate from All Penetrations & Valves Exceeded Tech Spec Limit.Root Cause Unknown.No Corrective Action Taken. Supplemental Rept Will Be issued.W/891002 Ltr ML18052B5541987-08-24024 August 1987 LER 87-015-00:on 870731,capacitor Failed on 1B Reactor Bldg & Refuel Floor Radiation Monitors Resulting in Safety Feature Actuation.Caused by Normal Aging.Capacitor replaced.W/870825 Ltr 1994-05-11
[Table view] Category:RO)
MONTHYEARML20029E2061994-05-11011 May 1994 LER 93-025-01:on 931205,Loop a MSIVs Exceeded TS Leakage Limit.Caused by Failure of Fastner Locking Devices.Seating Surface of Main Disc in MSIV 1A Machined & Successfully Pass LLRT on 940116.W/940511 Ltr ML17352B2501993-10-0101 October 1993 LER 93-014-00:on 930902,discovered That IRM 11 & APRM Both in Bypassed Condition W/O Half Scram Being Inserted Due to Work Practices.Irm 11 Taken Out of Bypassed Condition & Individual Involved counselled.W/931001 Ltr ML17352B2511993-10-0101 October 1993 LER 93-019-00:on 930903,RHR Pump 1A Inadvertently Started Due to Personnel Error.Pump Immediately Secured & Individual Involved Counselled on Importance of self-check.W/931001 Ltr ML20046A1801993-07-21021 July 1993 LER 92-007-00:on 930624,Toxic Gas Analyzer Inoperable Due to Personnel Error Caused by Lack of Procedural Adherence. Isolated CR Ventilation,Restarted Sample Pump & Restored CR Ventilation Sys to Outside Air suction.W/930721 Ltr ML20045H5781993-07-13013 July 1993 LER 93-013-00:on 930613,internal Electrical Fault within Main Power Transformer Tripped & Caused Reactor Scram & Unexpected Group I Isolation.Caused by Turbine Stop Valve Closure.Transformer replaced.W/930713 Ltr ML20045G7291993-07-0909 July 1993 LER 93-005-00:on 930609,numerous Alarms Received in CR, Including HPCI Turbine Rupture Disc High Pressure Alarm. Caused by Ruptured Disk,Releasing Steam/Water Mixture. Test Will Be Conducted on Rupture disks.W/930709 Ltr ML20045G0951993-07-0202 July 1993 LER 93-011-00:on 930602,HPCI Declared Inoperable in Order to Perform Qcos 2300-13.Caused by MSC Stem & Stem Gear Being Scored & Worn from Age Causing Excessive Friction.C/As Include Disassembling Gearbox Every 10 yrs.W/930702 Ltr ML20045F3321993-06-30030 June 1993 LER 93-012-00:on 930601,U-2 DG Cooling Water Pump Inoperable Due to Inadequate lubrication.U-2 DG Cooling Water Pump replaced.W/930630 Ltr ML20045F3251993-06-28028 June 1993 LER 93-007-01:on 930307,B Loop MSIV Exceeded TS Leakage Limits for Containment Isolation Valves Caused by Damaged Flexitalic Bonnet Gasket.Replaced Bonnet Gasket & Valve Successfully Retested (WR Q061987).W/930622 Ltr ML20044E6171993-05-14014 May 1993 LER 93-006-00:on 930420,Unit 2 Nso Inadvertently Started Unit 1 DG When Attempting to Start Shared (1/2) Dg.Caused by Personnel Error.Unit 1 DG Shut Down & 1/2 DG Started & Loaded successfully.W/930514 Ltr ML20044C9511993-05-0707 May 1993 LER 93-009-00:on 930408,technician Discovered That Estimate of Sample Flow for U2 Reactor Bldg Vent Sampler Flow Rate Monitor Not Calculated.Caused by Personnel Error.Technician counseled.W/930428 Ltr ML20024G6811991-04-19019 April 1991 LER 91-008-00:on 910322,reactor Bldg Ventilation Isolation Occurred.Caused by Lightning Strike.Control Room Vents Reset & Toxic Gas Sample Point a Selected.Addl Trips Associated W/ Lightning Strike Immediately reset.W/910418 Ltr ML20029C1241991-03-0808 March 1991 LER 91-005-01:on 910131,1/2 B Standby Gas Treatment Sys Autostart During RPS B Power Swap Due to an Inadequate Procedure.Nso Reset 1/2 Scram & 1/2 Groups II & III isolations.W/910306 Ltr ML20029B5901991-03-0808 March 1991 LER 91-004-00:on 910211,standby Liquid Control Sys of Unit 1 & 2 Inoperable.Caused by Inadequate Mod Testing.Engineering Dept Evaluating Data & Temporary Procedure 6589 Generated. W/910308 Ltr ML20028H7841991-01-23023 January 1991 LER 90-032-00:on 901224,1/2A Diesel Fire Pump Taken out-of- Svc on 901217 & Not Returned to Svc Before Seven Day Time Allotment Expired.Caused by Mgt Deficiency.Fire Pump Successfully Tested & Returned to svc.W/910123 Ltr ML20028H6831991-01-21021 January 1991 LER 90-034-00:on 901223,high Chlorine Concentration Caused Control Room Ventilation Manual Isolation & ESF Actuation. Caused by Instrument Error Code & Misinterpretation of Analyzer Indication.Flow reduced.W/910121 Ltr ML20028G9141990-09-28028 September 1990 LER 90-018-00:on 900829,plant Outside Design Spec for Electrical Separation Criteria for Two Redundant Safety Sys. Caused by Inadequate Engineering Review During Leads installation.W/900928 Ltr ML20044B2401990-07-12012 July 1990 LER 90-012-00:on 900612,control Room Ventilation Emergency Air Filtration Unit Declared Inoperable.Caused by Heater Malfunction.Work Request initiated.W/900712 Ltr ML20044B0091990-07-11011 July 1990 LER 90-011-00:on 900611,diesel Fire Pump 1/2 a Out of Svc for Period Exceeding 7 Days Reporting Criteria,To Install New Suction Line.Caused by Required Maint Work.Repairs Completed & Pump Tested & Returned to svc.W/900711 Ltr ML20043H4831990-06-21021 June 1990 LER 90-010-00:on 900522,while Returning RWCU Sys to Svc, Nonregenerative HX High Temp Alarm Received,Challenging ESF Logic & Causing Group III Isolation.Caused by Leaking RWCU Check Valves.Work Requests issued.W/900621 Ltr ML20043H2931990-06-18018 June 1990 LER 90-009-00:on 900518,determined That Various Containment Vols Not Leak Rate Tested Due to Recent 10CFR50,App J Interpretation Re Licensing Design Criteria.Mod M4-1(2)-89-167 initiated.W/900618 Ltr ML20043H9521990-06-13013 June 1990 LER 90-016-01:on 900411,motor Control Ctr Relay 28/29-5 Setpoint Drift Occurred,Resulting in Analyzed Plant Condition.Caused by Utilizing Wrong Relay & Inadequate Review of GE Svc Info Ltr.Relay replaced.W/900613 Ltr ML20043E9121990-06-0707 June 1990 LER 90-006-00:on 900508,Unit 2 RCIC Declared Inoperable Due to Unstable Operation of RCIC Pump Flow Controller.Caused by Proportional Band of Controller Being Set to Respond to Changes in Flow Too Quickly.Flow controlled.W/900607 Ltr ML20043F2341990-06-0101 June 1990 LER 90-001-01:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Test Program.Caused by Misinterpretation of 10CFR50,App J Requirements.Required Vents & Test Taps Will Be installed.W/900601 Ltr ML20043F2161990-06-0101 June 1990 LER 89-024-01:on 891214,main Turbine Unexpectedly Tripped Following Isolation of Reactor Water Level Switch (Lits). Caused by Channel B Lits Having Been Previously Replaced W/ Switch That Operated Reverse function.W/900601 Ltr ML20042E4991990-04-17017 April 1990 LER 90-007-00:on 900318,ESF Actuation Occurred.Caused by Mgt Deficiency in Not Providing Sufficient Guidance for Review of Work Package After Scope Changed.New Work Package Preparation Procedures initiated.W/900417 Ltr ML20012C7231990-03-15015 March 1990 LER 90-004-00:on 900213,loss of Emergency Bus 23-1 Occurred Due to Shorted Conductor Cable While Performing Wiring Verification.Caused by Personnel Error & Improper Installation.Electric Power Supplies recovered.W/900315 Ltr ML20012C7171990-03-15015 March 1990 LER 90-003-00:on 900213,unit Diesel Generator Tripped on Overspeed Upon Manual Startup for Testing.Caused by Misadjustment of Diesel Generator Governor.Diesel Generator Equipment Reset & Governor adjusted.W/900315 Ltr ML20012B2931990-03-0505 March 1990 LER 90-002-00:on 900204,determined That Only Reactor Bldg Differential Pressure of 0.24-inch Water Vacuum Could Be Obtained,In Violation of Tech Spec Required 0.25 Inch.Caused by Testing Deficiency.Leak Paths sealed.W/900305 Ltr ML20012B2961990-03-0505 March 1990 LER 90-003-00:on 900205,determined That Leakage Rate for HPCI Sys Steam Exhaust Check Valve Exceeded Tech Spec Limits.Caused by Excessive Leakage.Check Valve Replaced W/ Mission Check Valve W/Carbon Steel springs.W/900305 Ltr ML20011E1821990-01-30030 January 1990 LER 90-002-00:on 900102,during Annual Water Sprinkler Sys Valve Position Insp,Discovered That Valve 2-4199-072 Not Cycled Per Tech Spec Surveillance Requirement 4.12.Caused by Procedural Deficiency.Procedure to Be revised.W/900130 Ltr ML19354D9431990-01-15015 January 1990 LER 89-025-00:on 891220,determined That Reactor Bldg Overhead Auxiliary Hook May Have Contacted Side of New Fuel Bundle on 891214,causing Extensive Damage.Caused by Personnel Error.Bundle Shipped Back to GE.W/900115 Ltr ML19354D9481990-01-15015 January 1990 LER 89-023-00:on 891219,identified Deficient Temporary Procedures Which Altered Intent of Original Procedure QAP 1100-7.Caused by Mgt Oversight in Preparation of Tech Spec Change.Temporary Procedures revised.W/900115 Ltr ML20005F5881990-01-0808 January 1990 LER 90-001-00:on 891208,seven Pathways Not Included in Type B & C Local Leak Rate Testing Program.Caused by Misinterpretation of 10CFR50,App J Testing Requirements.Mod of Sys to Be Performed as necessary.W/900108 Ltr ML20005G0231990-01-0202 January 1990 LER 88-020-01:on 880619,improper Valving Sequence Occurred Which Resulted in Various ESF Actuations.Caused by Inadequate Equipment out-of-svc Procedure.Procedure Revised & Training Lesson Plan developed.W/900102 Ltr ML20005E4531989-12-28028 December 1989 LER 89-022-00:on 891128,HPCI Declared Inoperable Following Unexpected Actuation of HPCI Pump Room Deluge Sys.Actuation Caused Dc Sys Grounds Due to Moisture Intrusion in Electrical Equipment.Equipment dried.W/891228 Ltr ML20005D9551989-12-22022 December 1989 LER 89-021-00:on 891124,HPCI Deluge Sys Functional Test Not Completed within Tech Spec Interval of 6 Months.Caused by Mgt Deficiency & Insufficient Procedure.Procedures Revised to Better Control Tech Specs.W/891222 Ltr ML19351A6391989-12-15015 December 1989 LER 89-020-00:on 891117,full Reactor Scram Occurred Due to Simultaneous Loss of Power to 1A & 1B 24/48-volt Distribution Panels During Panel Transfer.Caused by Personnel Error.Personnel Trained Re event.W/891215 Ltr ML19332E7581989-12-0505 December 1989 LER 89-019-00:on 891105,half Group II & III Isolation Occurred While Performing Valve Flow Check Surveillance. Caused by Leaky Isolation Valve on Transmitter.Surveillance Methods Will Be Reviewed & Procedures revised.W/891205 Ltr ML19332C7581989-11-20020 November 1989 LER 89-017-00:on 891022,discovered That 6-month Functional Test Procedure Qos 500-3 Re Functional Test for Reactor Protection Sys Electrical Assemblies Not Completed in Required Time.Caused by Mgt deficiency.W/891120 Ltr ML19327C0701989-11-0909 November 1989 LER 89-018-00:on 891012,notification Given of Potential Single Failure of Diesel Generator Voltage Regulator That Could Result in Loss of All But One ECCS Loop.Caused by Design Deficiency.New Procedure developed.W/891109 Ltr ML19327C0951989-11-0404 November 1989 LER 89-005-00:on 891012,reactor Scram Occurred Due to Turbine Stop Valve Closure.Caused by Personnel Error in That Work Analyst Overlooked Removal of Two Connections on Limit Switch.Maint Workers Immediately counseled.W/891104 Ltr ML19327C2631989-11-0101 November 1989 LER 87-009-01:on 870801,reactor Scram Occurred from Turbine Generator Load Mismatch Due to Generator Trip.Caused by Electrical Fault in Main Transformer C Phase Windings.Main Transformer Replaced w/spare.W/891103 Ltr ML19325E8261989-10-30030 October 1989 LER 87-012-01:on 870918,while Performing Qos 1600-1, Vacuum Breaker 2-1601-33E Remained Open After Testing.Caused by Binding in Test Cylinder Portion of Vacuum Breaker. Nuclear Work Requests completed.W/891030 Ltr ML19325E5921989-10-24024 October 1989 LER 87-017-01:on 870805,Group IV Isolation Received Which Resulted in Closure of HPCI Steam Supply Valves.Caused by Failed HPCI Steamline Differential Pressure Transmitter Due to Loss of Oil in Sensing cell.W/891024 Ltr ML19325E5971989-10-24024 October 1989 LER 88-003-01:on 880301,while Performing RCIC Monthly Test, RCIC Pump Could Only Achieve 400 Gpm Against Discharge Pressure of 500 Psig.Caused by Failed Hydraulic Actuator on Turbine Governor Valve.Actuator replaced.W/891024 Ltr ML19327B7901989-10-18018 October 1989 LER 89-016-00:on 890921,during Transfer of New Fuel,Fuel Assembly Released from Refueling Grapple & Fell Upon Spent Fuel Racks.Caused by Personnel Error & Procedural Deficiency.Fuel Handling Procedures Revised ML19327B0491989-10-16016 October 1989 LER 89-015-00:on 890916,during Transfer,Loss of Power to Off Gas Monitor a Caused Contacts to Open Giving Upscale Radiation Signal,Thus Starting Off Gas Timer.Caused by Inadequate Procedures.Off Gas Sys reset.W/891016 Ltr ML19325C5341989-10-0202 October 1989 LER 89-014-00:on 890910,determined That Combined Leakage Rate from All Penetrations & Valves Exceeded Tech Spec Limit.Root Cause Unknown.No Corrective Action Taken. Supplemental Rept Will Be issued.W/891002 Ltr ML18052B5541987-08-24024 August 1987 LER 87-015-00:on 870731,capacitor Failed on 1B Reactor Bldg & Refuel Floor Radiation Monitors Resulting in Safety Feature Actuation.Caused by Normal Aging.Capacitor replaced.W/870825 Ltr 1994-05-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30
[Table view] |
Text
i 4.
Commomvealth Edison :
osed Cites Nucleat Power Station l i ;,
- . O 32710 20s Avenue Norm Cordova. Illinos 61242 9740 -
TeWhone 30S'654 2241
{
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l; RLB-89-245 l
f October 30, 1989 l t
U.S. Nuclear Regulatory Commission l Document Control Desk !
Washington, DC 20555 !
Reference:
Quad-Cities Nuclear Power Station
- Docket Number 50-265. DPR-30, Unit Two !
Enclosed please find Licensee Event Report (LER)87-012, Revision 01, for Quad-Cities Nuc1 car Power Station. This revision provides an update regarding :
cause and corrective actions. :
This report is submitted in accordance with the requirements of the Code l of Federal Regulations, Title 10,.Part 50.73(a)(2)(11), which requires the !
reporting of any event or condition that resulted in the condition of the ,
nuclear power plant, including its principal safety barrier, being seriously ;
degraded. ;
Respectfully, f
'I COMMONWEALTH EDISON COMPANY OUAD-CITIES NUCLEAR POWER STATION !
[N R. L. Bax !
Station Manager RLB/MJB/e !
Enclosure cc: R. Stols !
R. Higgins INPO Records Center ,
NRC Region III j i
8911090092 891030 ;
~
PDR ADOCK 05000265 S PDC l l 1077H/03712 y i
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LICth5t[ (VENT REPORT (LER)
Facility name (1) Docket humber (2) _Paea f31 0UAD-CIT 1[1 buCLEAR PDWLR_ilA110lL_Qh!T TWO Dl1101O!0121611 1 of G i 6, I Undate on tomarettien thamber to Drywell Vacuum Bregler Failure to Cleig_pge to Tett Cylinder, Pindine
...tvenLjlgte f1) LER humber f61 Repert Date f71 Othgr Facilitig1_1gtyolved fal Month Day Year Year /// Sequential // Revision Month Osy Year Facility hamet cocigLjtyntterf t) ;
/// w ar /j/j f
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, of 11 of el of I I of e 11a al 7 al 7 eI1 12 oi1 110 11o_ _. a l e el 11 o f OL_01 I i Or! RATING
"" " " $ " " " " I f frack ont er feare of the f ollowinal (111 4 20.402(b) 20.405(c) 50.73(a)(2Hiv) .,__ 73.7)(b) j POWER _ 20.40$(a)(1)(1) 50.36(c)(1) 50.73( a H 2 )( v s _ 73.71(c) l LEVEL 20.405(a)(1Hii) 50.36(c)(2) 50.73(a)(2)(vit) Other (Specify
!9 !0 (101 0 ,,,__ 20.405(a)(1)(111) so.73(aH2)(1) 50.73(a)(2)(viii)(A) in Abstract below l
////////////////////////// 20.405(a)(1)(iv) .2 50.73(aH2)(ti) ,_ 50.73(a)(2)(viii)(8) and in Text) l 50.73(a H 2)(iii)
///////////////////'/////// 20.405(a)(I Hv) ,_ ,_ 50.73(a H 2 H z )
LIC[hif E CONTACT FOR THis LER f121 l Name itLtPH0hLjig!$[R l AR(A CODE l tuvatte travant. Technical Staff Ennineer. Extention 2144 310 19 El 11 41 -l 21 fl 411_ '
COMPLETE Dht LINLf,1)R [ACH COM ON[!( FAILURE Df1CRI)[D lh TH11 REPORT f13)
CAuSE SYSTEM COMPONENT MANUFAC. R(PORTABLE CAust SYSTEM COMPONENT MANUFAC. R[ PORTABLE TURER T0 kPRDS_ TURER 70 hPRD1 x alF l VI flV All la 11 Y l I l l l l l l l 1 1 I l l 1 1 I I I I l SUPPLEMthTAL REPORT EXPECTED (141 Expected Month I Day I Yg&I submission lYet f1f vet. complete EXPECTED 10BM11110N DATE) X l ho *'("' I ll l1 A85 TRACT (Limit to 1400 spaces, i.e. approxim.tely fif teen single-space typewritten lines) (16)
On September 18, 1987, Quad Cities Unit Two was in the RUN mode at 90 percent of '
core thermal power. At 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br />, while performing QOS 1600-1 (Suppression Chamber to Drywell Vacuum Breakers Monthly Exercise), the 2-1601-33E vacuum breaker remained open after testing. Efforts were directed at reclosing the vacuum breaker. At 1350 hours0.0156 days <br />0.375 hours <br />0.00223 weeks <br />5.13675e-4 months <br />, these efforts were successful. Because of the stuck open vacuum breaker, NRC notification had been completed at 1346 hours0.0156 days <br />0.374 hours <br />0.00223 weeks <br />5.12153e-4 months <br />. Position indication problems were also identified for vacuum breakers 2-1601-32A and 33A. Suppression enamber to l drywell differential pressure was reestablished at 1725 hours0.02 days <br />0.479 hours <br />0.00285 weeks <br />6.563625e-4 months <br />.
The cause of the 2-1601-33E failure was determined to be due to binding in the test cylinder portion of the vacuum breaker. This is considered an isolated event and does not affect the operation necessary to mitigate the consequences of a loss of coolant accident. The position indication problems on 2-1601-32A and 33A should be l
corrected upon completion of modification M-4-1(2)-88-009 which is the result of the l Inspection and evaluation performed on Unit One's vacuum breakers. This report is submitted per 10 CFR 50.73(a)(2)(11).
1077H/03712
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PLANT AND SYSTEM IDENTIFICATION: !
General Electric - Boiling Water Reactor - 2511 MWt rated core thermal power. Energy Industry Identification System (E!!S) codes are identified in the text as (XX).
EVENT IDENTIFICATION:- While testing suppression chamber to drywell vacuum breakers, ,
the 2-1601-33E stuck open for 50 minutes.
I A .~ CONDITIONS PRIOR TO EVENT:
Unit: Two Event Date: September 18, 1987 Event Time: 1300 Reactor Mode: 4 Mode Name: RUN Power Level: 90%
This report was initiated by Deviation Report 0-4-2-87-044.
l RUN Mode (4) - In this position the reactor system pressure is at or above 825 psig, l and the reactor protection system is energized, with APRM protection and RBM i interlocks in service (excluding the 15% high flux scram).
B. DESCRIPTION OF EVENT:
On September 18, 1987 Quad Cities Unit Two was in the RUN mode at 90 percent of I rated core thermal power. At 0207 hours0.0024 days <br />0.0575 hours <br />3.422619e-4 weeks <br />7.87635e-5 months <br />, 005 1600-1 (Suppression Chamber (NH) to Drywell (NH) Vacuum Breakers (BF, VACB) Monthly Exercise) was begun. The first vacuum breaker valve tested, 2-1601-32A, cycled open successfully but indicated a ,
dual position on both Olvisions I and II after the testing. Technical Specification l 3.7.A.4 b. states:
l "Any pressure-suppression chamber-drywell vacuum breaker may be non-fully closed as indicated by the position indication and alarm systems provided that drywell to
- suppression chamber differential pressure decay rate is
- demonstrated to be not greater than 25% of the differential l pressure decay rate for all vacuum breakers open the '
equivalent of 1/16 inch at all points along the seal surface of the disk."
As a result, the drywell/ suppression differential pressure (dp) was reestablished at 0250 hours0.00289 days <br />0.0694 hours <br />4.133598e-4 weeks <br />9.5125e-5 months <br /> and then QOS 1600-27 (Suppression Chamber to Drywell Pressure Separation I Test with >/=1.2 PSIO Established Between Drywell and Suppression Chamber (Orywell Inerted)) was satisfactorily completed. This test satisfied the requirements of the l above referenced specification.
i l
l l
l 1097H/0371Z l
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//
f N"r naam tillat ynit Two o11IoIeio 1 21 61 1 al7 . eI1 i2 . oI) ois er 011, ftKT At 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />, electrical blocks (numbers 3954 and 3955) were installed to allow !
resetting the vacuum breaker position annunciator alarms on the 902-3 panel in the !
control room, and to clear the red "open" lights at the local control panel !
2252-24 At 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br />, testing resumed per QOS 1600-1. Vacuum breakers 2-1601-32B '
through F ope, rated satisfactorily but vacuum breaker 2-1601-33A, also indicated dual position on Division I.following the testing. At 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br />, the separation test ;
(QOS 1600-27) was performed again successfully to satisfy Specification 3.7.A.4.b. '
referenced above and Specification 3.7.A.4.c. which states:
" reactor operation may continue provided that no more than one quarter of the number of pressure suppression i chamber-drywell vacuum breakers are determined to be ;
inoperable provided that they are secured or known to be in '
the closed position."
Both the 2-1601-32A and 33A were known to be in the closed position because the separation tett was successfully performed. There are twelve suppression chamber-drywell vacuum breakers and only two were displaying indication problems.
At 1140 hours0.0132 days <br />0.317 hours <br />0.00188 weeks <br />4.3377e-4 months <br />, electrical blocks (numbers 3956 and 3957) were installed to reset the annunciator alarms on the 902-3 panel and to clear the red "open" light at the local control panel.
Subsequently, testing per 005 1600-1 resumed and at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br />, vacuum breaker 2-1601-33E stuck fully open when tested. /.ttempts were initiated immediately to reclose the vacuum breaker. These efforts included further manipulations of the l' vacuum breaker test pushbutton and isolation of the air supply to the vacuum breaker test solenold. '
At 1346 hours0.0156 days <br />0.374 hours <br />0.00223 weeks <br />5.12153e-4 months <br />, the NRC was notified via the Emargency Notification System (ENS) to satisfy the requirements of 10 CFR 50.72(b)(1)(11) because of the stuck open vacuum breaker. However, at 1350 hours0.0156 days <br />0.375 hours <br />0.00223 weeks <br />5.13675e-4 months <br />, as a result of the continuing efforts to close the 2-1601-33E vacuum breaker, the vacuum breaker was closed. Then the drywell-suppression chamber dp restoration was begun.
At-1630 hours it was apparent that the drywell-suppression chamber dp restoration :
was not proceeding normally, so the nine vacuum breakers that were considered available were cycled again to ensure that they were all reseated. All but the 2-1601-32A, 33A and 33E were cycled. As a result, dp buildup was improved and at 1703 hours0.0197 days <br />0.473 hours <br />0.00282 weeks <br />6.479915e-4 months <br />, the dp of 1.2 psid required by Technical Specification 3.7.A.6.a. was '
established. This Specification states that:
" differential pressure between the drywell and suppression chamber shall be maintained at equal to or greater than 1.20 psid except this differential may be decreased to less than 1.20 PSID for a maximum of 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> during required operability testing of the HPCI system pump, the RCIC >
system pump, the drywell-pressure suppression chamber vacuum breakers, and reactor pressure relief valves.
l l 1077H/03712 l
b' tittutti tvthf arpaar f ttal ttrf continuarton _
FACILITY ##et (1) DOCKit WuMett (t) __Lta kuMata ts) Pana 131 j t Year seguential Revision j f
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h a citiu unit two o I 1 I o I o I e i 21.61 s ai7 ,
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fixf If the Specifications of 3.7.A cannot be met, and the ;
differential pressure cannot be restored within the ;
subsequent six (6) hour period, an orderly shutdown shall i be initiated and the reactor shall be in a cold shutdown !
condition in the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />." l At 1725 hours0.02 days <br />0.479 hours <br />0.00285 weeks <br />6.563625e-4 months <br />, the separation test (005 1600-27) was completed satisfactorily. The !
dp was lost at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> when the 2-1601-33E was tested and stuck open. By 1703 '
hours the dp was reestablished. As a result, only 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> and 3 minutes of the six hours allowed by the Technical Specification were exhausted. ;
C. APPARENT CAUSE OF EVENT: ;
This report is submitted to comply with 10 CFR 50.73(a)(2)(11), which requires the reporting of any event or condition that resulted in the condition of the nuclear !
power plant, including its principal safety barriers, being seriously degraded. j i
The apparent cause for the 2-1601-33E vacuum breaker initial failure to close was e due to binding of the test cylinder. Furthermore, vacuum breaker 2-1601-33A !
position indication limit switches required adjustment. j D. SAFETY ANALYSIS OF EVENT:
The 2-1601-33E vacuum breaker is one of twelve vacuum breakers that are provided to ,
relieve noncondensables to the drywell from the suppression chamber. The capacity cf the vacuum breakers is designed to limit the dp between the drywell and ;
suppression chamber to 0.5 psi to maintain the structural integrity of the i containment. The design flow can be achieved with 25 percent of the vacuum breakers :
I closed without exceeding the 0.5 pst differential pressure limit.
In the event of a Loss of Coolant Accident (LOCA) with the suppression chamber to '
drywell vacuum breakers stuck opeil, some of the steam created by the LOCA would flow from the drywell to the suppression chamber atmosphere through the vacuum breaker, I resulting in incomplete condensation of the steam during the blowdown. This would :
raise the suppression chamber pressure above the pressure as analyzed with all vacuum breakers closed. Two design features assist with resolution of this ;
equipment problem: >
1077H/0371Z l
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- 1. The high velocity steam passing through the valve would tend to close the valve, 7
- 2. Steam which would be passed through the unclosed valve could be condensed ;
through the use of the Suppression Pool Spray subsystem of the Residual Heat Removal (BO) system. j Station management discussed the problem with this vacuum breaker and concluded that based on the indications observed while trying to reclose the valve, it was apparent '
i' that the problem was with the air operator portion of the valve. Each time the l vacuum breaker test button was operated (given an open signal) from the local control panel, it took longer to have the green " closed" indication go out. Since 7 the air operator is for test purposes only and does not perform any function when -
the valve operates as a vacuum breaker, it wat agreed that the 2-1601-33E would i still perform as required during a LOCA. ;
As a precautionary measure, this vacuum breaker was declared inoperable (but only I for testing) per 005 1600-02 (Suppression Chamber-Drywell Vacuum Brenkers Inoperable).
Because the 2-1601-32A showed dual indication in both 01 vision I and Il position indicating and alarm systems, it was declared inoperable per 005 1600-2. The safety significance of this condition was minimal because this vacuum breaker and the 2-1601-33A were still capable of performing their function during a LOCA. Vacuum breaker position indication is to provide indication that valve opening exceeds the ,
equivalent of 1/16 inch at all joints along the seal surface of the disk. (T.S.
3.7.A.4.a.3) Closure integrity of all valvis is assured by satisfactory completion of the separation test (005 1600-27). The vacuum breakers were tested every 15 days in accordance with Technical Specification 3.7.A.4.d which states:
"if failure occurs in one of the two-position alarm systems I for one or more vacuum breakers, reactor operation may r continue provided that a differential pressure decay rate !
test is initiated immediately and performed every 15 days thereafter untti the failure is corrected."
l l The testing was performed satisfactorily on 10/02/87, 10/17/87, and ,
11/01/87.
l l l E. CORRECTIVE ACTION:
Nuclear Work Requests 060285, Q60288, and 060289 were completed and the testing was ,
satisfactorily completed by November 5, 1987. Vacuum breakers 2-1601-32A and 33E ;
test cylinder lever arm and valve disc arm were adjusted. Additionally, the 2-1601-33E test cylinder was rebuilt. Vacuum breakers 2-1601-32A and 33A position !
l indication limit switches were adjusted.
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l 1077H/0371Z
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[ y etttat unit Tuo e i t i e i e IJLL11 AL.1 al ? - ei1 12 . oI1 016 J L J1L fist h The problem that caused the 2-1601-33E to stick open is considered an isolated event. The dual indicaticas present on vacuum breakers 2-1601-32A and 33A is considered to be primarily indication problems. Correction of the indication problem will be accomplished under modification M-4-1(2)-88-009. The modification t;lil provide a more reliable method of position indication by placing the CLOSED position indication switches at the bottom of each vacuum breaker body. Completion of the modification is being tracked with Nuclear Tracking System (NTS) 2652008800101 for Unit Two and 2542008800503 for Unit One. This modification is the result of the inspection and evaluation performed on Unit One Luring its last refuel and maintenance outage.
- f. PREVIOUS EVENTS Licensee Event Report (LER) 0eserIDtion 265/87-004 2-1601-33A failed to close due to dimpled bushing and/or corroded solenold.
Reportable Occurrence Descriotton 265/82-22/03L 2-1601-33A Stainless steel packing and stuffing box bushing bound to the shaft caused failure to close.
265/82-06/03L 2-1601-32C counterweight mispositioned.
G. COMPONENT FAILURE DATA:
The vacuum breakers are 18 inch swing-check valves manufactured by Atwood and Morrill Company, Incorporated. The air test cylinder is manufactured by Atwood and Morrill, model number 20781-F.
1077H/03712