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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3201994-10-0707 October 1994 LER 94-022-00:on 940907,TS Violation Occurred Due to Inadequate Fire Watch.Retrained Personnel Associated W/ Painting activities.W/941007 Ltr ML20029E2001994-05-13013 May 1994 LER 94-006-00:on 940414,SS Recognized That Required Frequency for Performing STP 057-3705 Had Been Exceeded. Caused by Inadequate Supervisory Methods.Corrective Action: Inhouse Tracking Process Will Be created.W/940513 Ltr ML20029C8741994-04-26026 April 1994 LER 93-026-01:on 931117,isolation of RCIC Sys Occurred Due to Apparent Failure of Relay.Three Relays Associated W/ Isolation Replaced & Shipped to Mfg for Failure Analysis.W/ 940426 Ltr ML20029C7021994-04-19019 April 1994 LER 90-003-05:on 900206,discovered Deficiencies in Thermo-Lag Fire Barrier Envelope Around Redundant Safe Shutdown.Firewatches Established in Areas Where Thermo Lag Used as barrier.W/940419 Ltr ML20046C3891993-08-0202 August 1993 LER 93-014-00:on 930701,installed Sprinkler Sys as Substitute for Passive fire-rated Barrier Due to Deficiency Identified in Fire Barrier Separation Requirements.Declared Fire Barriers Surrounding Valves degraded.W/930802 Ltr ML20046B8981993-07-29029 July 1993 LER 93-013-00:on 930629,high Pressure Core Spray Pump Failed to Start & Run During Surveillance Test Due to Failed Overfrequency Relay.Relay Tested & Installed in Switchgear. W/930729 Ltr ML20046A2361993-07-22022 July 1993 LER 93-008-01:on 930429,relief Request Improperly Prepared for Insvc Testing Program Results in Noncompliance W/Main Steam Isolation Valve Testing Requirement.Caused by Personnel Error.Testing Frequency Revised ML20045G6111993-07-0202 July 1993 LER 93-012-00:on 930603,deficiency in Plant Surveillance Test Procedures Identified.Caused by Primary Causal Factor Inattention to Detail During Initial Procedure Development Process.Surveillance Test Procedures performed.W/930702 Ltr ML20045D6991993-06-21021 June 1993 LER 93-011-00:on 930521,determined That Mode Switch Placed in Refuel Position During Testing of Switch Interlock Functions.Caused by Conflicting Info in Surveillance Procedures.Operating Procedure revised.W/930621 Ltr ML20045C0141993-06-14014 June 1993 LER 93-010-00:on 930514,SDC Lost for Approx Three Minutes When One SDC Suction Valve Closed Due to Initiation of Spurious ESF Actuation Signal.Caused by Personnel Error. Procedural Guidance revised.W/930614 Ltr ML20045C0021993-06-14014 June 1993 LER 93-003-01:on 930225,incidents Discovered Which Caused Interlock Mechanism in Upper Containment Airlocks at Elevation 171 to Operate Improperly.Case Study Training Class Developed for Airlock incidents.W/930614 Ltr ML20045A1461993-06-0404 June 1993 LER 93-009-00:on 930504,discovered That Surveillance Test Procedure for Control Bldg Chilled Water Sys Quarterly Pump Missed Due to Cognitive Personnel Error.Administrative Procedure Will Be revised.W/930604 Ltr ML20045A4261993-06-0101 June 1993 LER 93-002-02:on 930212,discovered That TS SRs Not Properly Implemented in Logic Sys Functional Tests Due to Inattention to Detail While Preparing Revs of Relevant Surveillance Test Procedures (Stp).Relevant STPs revised.W/930601 Ltr ML20044H3571993-06-0101 June 1993 LER 93-008-00:on 930429,investigation Determined That Relief Request for Inservice Testing of Pumps & Valves in Conflict W/Msiv Testing Requirements.Caused by Personnel Error.Relief Request 40 revised.W/930601 Ltr ML20044G7401993-05-26026 May 1993 LER 93-006-00:on 930419,MSIV Failed to Stroke Closed When Given Close Signal from CR Due to Poppet Sticking.Caused by Insufficient poppet-to-guide Rib Clearance.Stricter Controls Imposed to Control clearances.W/930526 Ltr ML20044F2541993-05-20020 May 1993 LER 93-007-00:on 930420,noted That an Isolation of Inboard & Outboard MSIV & Ms Line Drains Occurred.Caused by Lack of Personnel Knowledge of Unique Maint Conditions.Precaution Will Be Added to Sys Operating procedure.W/930520 Ltr ML20044D8511993-05-17017 May 1993 LER 93-005-00:on 930415,discovered That RCIC Steam Line Flow - High Timer Function Never Performed on Monthly Basis. Caused by Failure to Include Test in Initial Procedure Development Process.Procedures revised.W/930517 Ltr ML20024H2381991-05-21021 May 1991 LER 91-003-01:on 910322,Div II Control Power Circuit Deenergized,Resulting in Deenergization of Charcoal Filter Train Suction Dampers.Caused by Inadequate Work Plan.Plan Revised to Document Restoration of wiring.W/910521 Ltr ML20024G7441991-04-22022 April 1991 LER 91-003-00:on 910322,control Bldg Local Air Intake Radiation Monitor Control Power Circuit Deenergized, Resulting in Isolation of air-operated Dampers.Caused by Inadequate Work Plan.Work Plan revised.W/910422 Ltr ML20024G7181991-04-19019 April 1991 LER 91-004-00:on 910321,RCIC Turbine Main Steam Supply Line Outboard Containment Isolation Valve Isolated.Caused by Negative Trip Setpoint of Trip Unit Being Reached.Caution Added to RCIC Sys Operating procedures.W/910419 Ltr ML20029C1211991-03-14014 March 1991 LER 91-001-00:on 910212,use of Inadequate Control Room Filter Initiation Signal Due to Discrepancies Between Logic Diagrams.Main Control Room Doses Due to MSLB Outside Containment recalculated.W/910314 Ltr ML20029B1341991-02-26026 February 1991 LER 90-033-01:on 901104,RWCU Sys Isolation Occurred While Performing Plant Mod to Power Supply Wiring in Control Room Panel 1H13-P642.Caused by Removal of Terminal Screw.Power Supply reterminated.W/910226 Ltr ML20028H3961990-12-18018 December 1990 LER 90-032-01:on 901021,discovered That Five Snubbers Removed from Standby Svc Water Sys Piping in Violation of Tech Spec 3.7.4.Caused by Scheduling Error & Inadequate Review.Training Will Be Completed on 910331.W/901218 Ltr ML20024F7481990-12-10010 December 1990 LER 90-040-00:on 901110,technician Inadvertently Shorted Relay Terminals,Energizing Relay & Causing Emergency Diesel Generator to Start Unexpectedly.Caused by Personnel Error. Generator Manually secured.W/901210 Ltr ML20044B1951990-07-12012 July 1990 LER 90-003-01:on 900206 to 08,deficiencies Found in thermo-lag Fire Barrier Envelopes Redundant Safe Shutdown Circuits.Fire Watch Established.Util Working W/Vendor to Resolve discrepancies.W/900712 Ltr ML20044A3781990-06-22022 June 1990 LER 90-023-00:on 900523,discovered That Annulus Ventilation Radiation monitor,1RMS*RE11A Inoperable.Caused by Failure of Radiation Monitor Sample Pump & Failure of Switch to Actuate.Flow Switches replaced.W/900622 Ltr ML20043F4721990-06-0808 June 1990 LER 90-021-00:on 900509,RWCU Sys Differential Flow High Trip Instrumentation Inoperable for Period Greater than Allowed by Tech Spec.Caused by Misinterpretation of Tech Spec 3/4.3.2,Table 3.3.2.-1.4.Personnel retrained.W/900608 Ltr ML20043D5831990-06-0101 June 1990 LER 90-020-00:on 900504,radwaste Operator Entered High Radiation Area W/O Dose Rate Meter,Alarming Dosimeter or Radiation Protection Technician Coverage.Caused by Personnel Error.Training Provided to operators.W/900601 Ltr ML20043B8031990-05-24024 May 1990 LER 90-019-00:on 900425,RWCU Sys Isolation & ESF Actuation Occurred After Completion of Channel Check of Riley Temp Trip Unit.Caused by Unit Exceeding Differential Temp Setpoint of 46 F.Unit replaced.W/900524 Ltr ML20043B3301990-05-21021 May 1990 LER 90-017-00:on 900419,inadequate Fire Barrier in Shake Space Occurred Contrary to Tech Spec.Caused by Oversight. Roving Fire Watch Scheduled.Maint Will Rework Voids & Install Seismic Gap seal.W/900521 Ltr ML20043C0281990-05-19019 May 1990 LER 90-018-00:on 900420,ESF Actuation Occurred Causing Reactor Water Sample Containment Isolation Valve to Close. Caused by Failure of Fuse Which Deenergized Isolation Logic of Valves.Fuse replaced.W/900518 Ltr ML20042G7981990-05-10010 May 1990 LER 90-016-00:on 900414,insulator Fault on Local Grid Resulted in Trip of 500 Kv Breaker.Caused by Spurious Alarm Signal from Control Room Local Intake Radiation Monitor 1RMS*RE13B.Sys Returned to Normal operation.W/900510 Ltr ML20042G8001990-05-0909 May 1990 LER 90-015-00:on 900409,loss of Div II Reactor Protection Sys Bus Occurred Due to Trip of Electrical Protection Assembly.Another Trip Also Occurred on 900415.Caused by Faulty Integrated Circuit logics.W/900509 Ltr ML20042G4501990-05-0707 May 1990 LER 90-013-00:on 900405,discovered That Control Bldg Chiller Motor Current Limiter C Set Incorrectly at 56% Instead of 100%.Caused by Incorrect Setting & Maint Activities.Loop Calibr Data Sheet revised.W/900507 Ltr ML20042G4531990-05-0707 May 1990 LER 90-014-00:on 900407,reactor Scram Occurred While Testing Main Turbine Combined Intermediate Valves.Caused by Low Pressure Signal from Emergency Trip Sys of Electrohydraulic Control Sys.Two Solenoid Valves replaced.W/900507 Ltr ML20042F4731990-05-0101 May 1990 LER 90-012-00:on 900401,ESF Actuations Occurred Due to Electrical Protection Assembly Breakers Trip.Caused by Voltage Regulator Failure.Replacement Voltage Regulator Card Installed in MG 1C71-S001B.W/900501 Ltr ML20042E2231990-04-0909 April 1990 LER 90-007-00:on 900311,control Bldg Ventilation Sys Isolated & Filtration Unit Initiated.Caused by Severe Electrical Transient.Performance of Radiation Monitors Improved Prior to Implementation of procedures.W/900409 Ltr ML20012C0741990-03-12012 March 1990 LER 90-004-00:on 900211,Div II Emergency 125-volt Dc Bus Experienced Voltage Spike,Causing Topaz Inverter to Trip & Resulting in Loss of Power to Control Room Panel.Cause Unknown.Setpoint Changes Being evaluated.W/900312 Ltr ML20012C4191990-03-0808 March 1990 LER 90-003-00:on 900206,found That Several Minor Deficiencies Existed in thermo-lag Fire Barrier Envelopes Redundant Safe Shutdown Circuits.Util Currently Working W/ Vendor to Resolve Identified discrepancies.W/900308 Ltr ML20011E2491990-01-31031 January 1990 LER 88-018-04:on 880825,reactor Scram Occurred Due to Main Generator Exciter Brush Failure.Preventive Maint Procedure Revised to Establish Specific Wear Criteria at Which Brushes to Be replaced.W/900131 Ltr ML20011E2461990-01-31031 January 1990 LER 89-036-01:on 891007,discovered That Various motor- Operated Valves Energized,Contrary to Assumptions Contained in Plant Fire Hazards Analysis.Cause Not Stated.Operations Initiated Required Fire Watches on valves.W/900131 Ltr ML20011E1191990-01-30030 January 1990 LER 90-001-00:on 900103,isolation of RCIC Steam Supply Inboard Isolation Valve Occurred During Surveillance Testing of RCIC Sys.Caused by Technician Lifting Wrong Lead,Causing ESF Actuation.Lead Relanded on terminal.W/900130 Ltr ML20011E1181990-01-30030 January 1990 LER 89-033-01:on 890916,loss of Power to Div II 120-volt Ac Distribution Panel Caused auto-start of Standby Gas Treatment & Annulus Mixing Sys,Resulting in ESF Actuations. Caused by Transformer Failure.Valves opened.W/900130 Ltr ML20005G1641990-01-10010 January 1990 LER 89-044-00:on 891211,unplanned ESF Actuation Occurred, Resulting in Isolation of Rcic.Caused by Technician Failing to Perform Steps of Surveillance Test Procedure in Sequence.Div II Isolation Signal reset.W/900110 Ltr ML20005G1661990-01-10010 January 1990 LER 89-045-00:on 891212,Div I Standby Svc Water Pumps Received Automatic Start Signal Due to Spurious Low Svc Water Pressure Signal When Normal Svc Water Pump Secured. Signal Cleared & Sys Restored to Normal lineup.W/900110 Ltr ML20005E8521990-01-0202 January 1990 LER 89-043-00:on 891201.two Outboard MSIVs Inoperable Due to Failure of Corresponding Fast Closure solenoid-operated Valve.Caused by Incomplete Removal of Silicone Lubricant. Lubricant Removed by Application of Acetone.W/900102 Ltr ML20005E8511990-01-0202 January 1990 LER 89-042-01:on 891201,main Turbine Generator Tripped, Resulting in Reactor Scram.Caused by Sensing Fault on Offsite 230 Kv Line.Sys Maint Procedure Being Revised to Include Test of Failed Portion of relay.W/900102 Ltr ML20005E1381989-12-26026 December 1989 LER 89-041-00:on 891125,unplanned ESF Actuation Occurred as Result of Two Leads Shorted Together During Testing of Control Circuitry,Causing Valve Isolation from Suppression Pool.Sys Lineup Restored to Normal position.W/891226 Ltr ML20011D6201989-12-18018 December 1989 LER 89-040-00:on 891117,surveillance Test of Div II Penetration Valve Leakage Control Sys Air Supply Header Pressure Not Performed within Allowable Tolerance.Addl Training of Scheduling Group Will Be provided.W/891218 Ltr ML20011D1371989-12-14014 December 1989 LER 89-039-00:on 891114,discovered That Required post-maint Overall Leak Rate Test on Upper Containment Airlock Not Performed After Replacement of Inflatable Seal.Caused by Personnel Error.Maint Procedure revised.W/891214 Ltr 1994-05-13
[Table view] Category:RO)
MONTHYEARML20024J3201994-10-0707 October 1994 LER 94-022-00:on 940907,TS Violation Occurred Due to Inadequate Fire Watch.Retrained Personnel Associated W/ Painting activities.W/941007 Ltr ML20029E2001994-05-13013 May 1994 LER 94-006-00:on 940414,SS Recognized That Required Frequency for Performing STP 057-3705 Had Been Exceeded. Caused by Inadequate Supervisory Methods.Corrective Action: Inhouse Tracking Process Will Be created.W/940513 Ltr ML20029C8741994-04-26026 April 1994 LER 93-026-01:on 931117,isolation of RCIC Sys Occurred Due to Apparent Failure of Relay.Three Relays Associated W/ Isolation Replaced & Shipped to Mfg for Failure Analysis.W/ 940426 Ltr ML20029C7021994-04-19019 April 1994 LER 90-003-05:on 900206,discovered Deficiencies in Thermo-Lag Fire Barrier Envelope Around Redundant Safe Shutdown.Firewatches Established in Areas Where Thermo Lag Used as barrier.W/940419 Ltr ML20046C3891993-08-0202 August 1993 LER 93-014-00:on 930701,installed Sprinkler Sys as Substitute for Passive fire-rated Barrier Due to Deficiency Identified in Fire Barrier Separation Requirements.Declared Fire Barriers Surrounding Valves degraded.W/930802 Ltr ML20046B8981993-07-29029 July 1993 LER 93-013-00:on 930629,high Pressure Core Spray Pump Failed to Start & Run During Surveillance Test Due to Failed Overfrequency Relay.Relay Tested & Installed in Switchgear. W/930729 Ltr ML20046A2361993-07-22022 July 1993 LER 93-008-01:on 930429,relief Request Improperly Prepared for Insvc Testing Program Results in Noncompliance W/Main Steam Isolation Valve Testing Requirement.Caused by Personnel Error.Testing Frequency Revised ML20045G6111993-07-0202 July 1993 LER 93-012-00:on 930603,deficiency in Plant Surveillance Test Procedures Identified.Caused by Primary Causal Factor Inattention to Detail During Initial Procedure Development Process.Surveillance Test Procedures performed.W/930702 Ltr ML20045D6991993-06-21021 June 1993 LER 93-011-00:on 930521,determined That Mode Switch Placed in Refuel Position During Testing of Switch Interlock Functions.Caused by Conflicting Info in Surveillance Procedures.Operating Procedure revised.W/930621 Ltr ML20045C0141993-06-14014 June 1993 LER 93-010-00:on 930514,SDC Lost for Approx Three Minutes When One SDC Suction Valve Closed Due to Initiation of Spurious ESF Actuation Signal.Caused by Personnel Error. Procedural Guidance revised.W/930614 Ltr ML20045C0021993-06-14014 June 1993 LER 93-003-01:on 930225,incidents Discovered Which Caused Interlock Mechanism in Upper Containment Airlocks at Elevation 171 to Operate Improperly.Case Study Training Class Developed for Airlock incidents.W/930614 Ltr ML20045A1461993-06-0404 June 1993 LER 93-009-00:on 930504,discovered That Surveillance Test Procedure for Control Bldg Chilled Water Sys Quarterly Pump Missed Due to Cognitive Personnel Error.Administrative Procedure Will Be revised.W/930604 Ltr ML20045A4261993-06-0101 June 1993 LER 93-002-02:on 930212,discovered That TS SRs Not Properly Implemented in Logic Sys Functional Tests Due to Inattention to Detail While Preparing Revs of Relevant Surveillance Test Procedures (Stp).Relevant STPs revised.W/930601 Ltr ML20044H3571993-06-0101 June 1993 LER 93-008-00:on 930429,investigation Determined That Relief Request for Inservice Testing of Pumps & Valves in Conflict W/Msiv Testing Requirements.Caused by Personnel Error.Relief Request 40 revised.W/930601 Ltr ML20044G7401993-05-26026 May 1993 LER 93-006-00:on 930419,MSIV Failed to Stroke Closed When Given Close Signal from CR Due to Poppet Sticking.Caused by Insufficient poppet-to-guide Rib Clearance.Stricter Controls Imposed to Control clearances.W/930526 Ltr ML20044F2541993-05-20020 May 1993 LER 93-007-00:on 930420,noted That an Isolation of Inboard & Outboard MSIV & Ms Line Drains Occurred.Caused by Lack of Personnel Knowledge of Unique Maint Conditions.Precaution Will Be Added to Sys Operating procedure.W/930520 Ltr ML20044D8511993-05-17017 May 1993 LER 93-005-00:on 930415,discovered That RCIC Steam Line Flow - High Timer Function Never Performed on Monthly Basis. Caused by Failure to Include Test in Initial Procedure Development Process.Procedures revised.W/930517 Ltr ML20024H2381991-05-21021 May 1991 LER 91-003-01:on 910322,Div II Control Power Circuit Deenergized,Resulting in Deenergization of Charcoal Filter Train Suction Dampers.Caused by Inadequate Work Plan.Plan Revised to Document Restoration of wiring.W/910521 Ltr ML20024G7441991-04-22022 April 1991 LER 91-003-00:on 910322,control Bldg Local Air Intake Radiation Monitor Control Power Circuit Deenergized, Resulting in Isolation of air-operated Dampers.Caused by Inadequate Work Plan.Work Plan revised.W/910422 Ltr ML20024G7181991-04-19019 April 1991 LER 91-004-00:on 910321,RCIC Turbine Main Steam Supply Line Outboard Containment Isolation Valve Isolated.Caused by Negative Trip Setpoint of Trip Unit Being Reached.Caution Added to RCIC Sys Operating procedures.W/910419 Ltr ML20029C1211991-03-14014 March 1991 LER 91-001-00:on 910212,use of Inadequate Control Room Filter Initiation Signal Due to Discrepancies Between Logic Diagrams.Main Control Room Doses Due to MSLB Outside Containment recalculated.W/910314 Ltr ML20029B1341991-02-26026 February 1991 LER 90-033-01:on 901104,RWCU Sys Isolation Occurred While Performing Plant Mod to Power Supply Wiring in Control Room Panel 1H13-P642.Caused by Removal of Terminal Screw.Power Supply reterminated.W/910226 Ltr ML20028H3961990-12-18018 December 1990 LER 90-032-01:on 901021,discovered That Five Snubbers Removed from Standby Svc Water Sys Piping in Violation of Tech Spec 3.7.4.Caused by Scheduling Error & Inadequate Review.Training Will Be Completed on 910331.W/901218 Ltr ML20024F7481990-12-10010 December 1990 LER 90-040-00:on 901110,technician Inadvertently Shorted Relay Terminals,Energizing Relay & Causing Emergency Diesel Generator to Start Unexpectedly.Caused by Personnel Error. Generator Manually secured.W/901210 Ltr ML20044B1951990-07-12012 July 1990 LER 90-003-01:on 900206 to 08,deficiencies Found in thermo-lag Fire Barrier Envelopes Redundant Safe Shutdown Circuits.Fire Watch Established.Util Working W/Vendor to Resolve discrepancies.W/900712 Ltr ML20044A3781990-06-22022 June 1990 LER 90-023-00:on 900523,discovered That Annulus Ventilation Radiation monitor,1RMS*RE11A Inoperable.Caused by Failure of Radiation Monitor Sample Pump & Failure of Switch to Actuate.Flow Switches replaced.W/900622 Ltr ML20043F4721990-06-0808 June 1990 LER 90-021-00:on 900509,RWCU Sys Differential Flow High Trip Instrumentation Inoperable for Period Greater than Allowed by Tech Spec.Caused by Misinterpretation of Tech Spec 3/4.3.2,Table 3.3.2.-1.4.Personnel retrained.W/900608 Ltr ML20043D5831990-06-0101 June 1990 LER 90-020-00:on 900504,radwaste Operator Entered High Radiation Area W/O Dose Rate Meter,Alarming Dosimeter or Radiation Protection Technician Coverage.Caused by Personnel Error.Training Provided to operators.W/900601 Ltr ML20043B8031990-05-24024 May 1990 LER 90-019-00:on 900425,RWCU Sys Isolation & ESF Actuation Occurred After Completion of Channel Check of Riley Temp Trip Unit.Caused by Unit Exceeding Differential Temp Setpoint of 46 F.Unit replaced.W/900524 Ltr ML20043B3301990-05-21021 May 1990 LER 90-017-00:on 900419,inadequate Fire Barrier in Shake Space Occurred Contrary to Tech Spec.Caused by Oversight. Roving Fire Watch Scheduled.Maint Will Rework Voids & Install Seismic Gap seal.W/900521 Ltr ML20043C0281990-05-19019 May 1990 LER 90-018-00:on 900420,ESF Actuation Occurred Causing Reactor Water Sample Containment Isolation Valve to Close. Caused by Failure of Fuse Which Deenergized Isolation Logic of Valves.Fuse replaced.W/900518 Ltr ML20042G7981990-05-10010 May 1990 LER 90-016-00:on 900414,insulator Fault on Local Grid Resulted in Trip of 500 Kv Breaker.Caused by Spurious Alarm Signal from Control Room Local Intake Radiation Monitor 1RMS*RE13B.Sys Returned to Normal operation.W/900510 Ltr ML20042G8001990-05-0909 May 1990 LER 90-015-00:on 900409,loss of Div II Reactor Protection Sys Bus Occurred Due to Trip of Electrical Protection Assembly.Another Trip Also Occurred on 900415.Caused by Faulty Integrated Circuit logics.W/900509 Ltr ML20042G4501990-05-0707 May 1990 LER 90-013-00:on 900405,discovered That Control Bldg Chiller Motor Current Limiter C Set Incorrectly at 56% Instead of 100%.Caused by Incorrect Setting & Maint Activities.Loop Calibr Data Sheet revised.W/900507 Ltr ML20042G4531990-05-0707 May 1990 LER 90-014-00:on 900407,reactor Scram Occurred While Testing Main Turbine Combined Intermediate Valves.Caused by Low Pressure Signal from Emergency Trip Sys of Electrohydraulic Control Sys.Two Solenoid Valves replaced.W/900507 Ltr ML20042F4731990-05-0101 May 1990 LER 90-012-00:on 900401,ESF Actuations Occurred Due to Electrical Protection Assembly Breakers Trip.Caused by Voltage Regulator Failure.Replacement Voltage Regulator Card Installed in MG 1C71-S001B.W/900501 Ltr ML20042E2231990-04-0909 April 1990 LER 90-007-00:on 900311,control Bldg Ventilation Sys Isolated & Filtration Unit Initiated.Caused by Severe Electrical Transient.Performance of Radiation Monitors Improved Prior to Implementation of procedures.W/900409 Ltr ML20012C0741990-03-12012 March 1990 LER 90-004-00:on 900211,Div II Emergency 125-volt Dc Bus Experienced Voltage Spike,Causing Topaz Inverter to Trip & Resulting in Loss of Power to Control Room Panel.Cause Unknown.Setpoint Changes Being evaluated.W/900312 Ltr ML20012C4191990-03-0808 March 1990 LER 90-003-00:on 900206,found That Several Minor Deficiencies Existed in thermo-lag Fire Barrier Envelopes Redundant Safe Shutdown Circuits.Util Currently Working W/ Vendor to Resolve Identified discrepancies.W/900308 Ltr ML20011E2491990-01-31031 January 1990 LER 88-018-04:on 880825,reactor Scram Occurred Due to Main Generator Exciter Brush Failure.Preventive Maint Procedure Revised to Establish Specific Wear Criteria at Which Brushes to Be replaced.W/900131 Ltr ML20011E2461990-01-31031 January 1990 LER 89-036-01:on 891007,discovered That Various motor- Operated Valves Energized,Contrary to Assumptions Contained in Plant Fire Hazards Analysis.Cause Not Stated.Operations Initiated Required Fire Watches on valves.W/900131 Ltr ML20011E1191990-01-30030 January 1990 LER 90-001-00:on 900103,isolation of RCIC Steam Supply Inboard Isolation Valve Occurred During Surveillance Testing of RCIC Sys.Caused by Technician Lifting Wrong Lead,Causing ESF Actuation.Lead Relanded on terminal.W/900130 Ltr ML20011E1181990-01-30030 January 1990 LER 89-033-01:on 890916,loss of Power to Div II 120-volt Ac Distribution Panel Caused auto-start of Standby Gas Treatment & Annulus Mixing Sys,Resulting in ESF Actuations. Caused by Transformer Failure.Valves opened.W/900130 Ltr ML20005G1641990-01-10010 January 1990 LER 89-044-00:on 891211,unplanned ESF Actuation Occurred, Resulting in Isolation of Rcic.Caused by Technician Failing to Perform Steps of Surveillance Test Procedure in Sequence.Div II Isolation Signal reset.W/900110 Ltr ML20005G1661990-01-10010 January 1990 LER 89-045-00:on 891212,Div I Standby Svc Water Pumps Received Automatic Start Signal Due to Spurious Low Svc Water Pressure Signal When Normal Svc Water Pump Secured. Signal Cleared & Sys Restored to Normal lineup.W/900110 Ltr ML20005E8521990-01-0202 January 1990 LER 89-043-00:on 891201.two Outboard MSIVs Inoperable Due to Failure of Corresponding Fast Closure solenoid-operated Valve.Caused by Incomplete Removal of Silicone Lubricant. Lubricant Removed by Application of Acetone.W/900102 Ltr ML20005E8511990-01-0202 January 1990 LER 89-042-01:on 891201,main Turbine Generator Tripped, Resulting in Reactor Scram.Caused by Sensing Fault on Offsite 230 Kv Line.Sys Maint Procedure Being Revised to Include Test of Failed Portion of relay.W/900102 Ltr ML20005E1381989-12-26026 December 1989 LER 89-041-00:on 891125,unplanned ESF Actuation Occurred as Result of Two Leads Shorted Together During Testing of Control Circuitry,Causing Valve Isolation from Suppression Pool.Sys Lineup Restored to Normal position.W/891226 Ltr ML20011D6201989-12-18018 December 1989 LER 89-040-00:on 891117,surveillance Test of Div II Penetration Valve Leakage Control Sys Air Supply Header Pressure Not Performed within Allowable Tolerance.Addl Training of Scheduling Group Will Be provided.W/891218 Ltr ML20011D1371989-12-14014 December 1989 LER 89-039-00:on 891114,discovered That Required post-maint Overall Leak Rate Test on Upper Containment Airlock Not Performed After Replacement of Inflatable Seal.Caused by Personnel Error.Maint Procedure revised.W/891214 Ltr 1994-05-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARRBG-45144, Monthly Operating Rept for Sept 1999 for River Bend Station. with1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for River Bend Station. with ML20216G1201999-09-0909 September 1999 Rev 3 to Rbs,Cycle 9 Colr RBG-45110, Monthly Operating Rept for Aug 1999 for River Bend Station, Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for River Bend Station, Unit 1.With RBG-45087, Special Rept:On 990510,LPCI a & LPCS Injected Into Rv for Less than Two Minutes.Caused by Electrical Transient in One of ECCS Power Supplies.Operators Verified Reactor Cavity Level & Closed Injection Valves to Stop Injection1999-08-0606 August 1999 Special Rept:On 990510,LPCI a & LPCS Injected Into Rv for Less than Two Minutes.Caused by Electrical Transient in One of ECCS Power Supplies.Operators Verified Reactor Cavity Level & Closed Injection Valves to Stop Injection ML20210K4721999-08-0303 August 1999 SER Accepting Licensee 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves RBG-45091, Monthly Operating Rept for July 1999 for River Bend Station, Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for River Bend Station, Unit 1.With ML20210C6391999-07-0202 July 1999 Rev 2 to River Bend Station,Cycle 9 Colr RBG-45055, Monthly Operating Rept for June 1999 for River Bend Station, Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for River Bend Station, Unit 1.With ML20196J8031999-06-24024 June 1999 Rev 1 to Rbs,Cycle 9 Colr RBG-45028, Monthly Operating Rept for May 1999 for River Bend Station, Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for River Bend Station, Unit 1.With RBG-45016, Monthly Operating Rept for Apr 1999 for River Bend Station, Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for River Bend Station, Unit 1.With ML20206A2111999-04-21021 April 1999 Safety Evaluation Authorizing Pump Relief Request PRR-001 & Valve Relief Request VRR-001 & Denying Valve Relief Request VRR-002 RBG-44969, Monthly Operating Rept for Mar 1999 for River Bend Station, Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for River Bend Station, Unit 1.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205D5481999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Exam Weld AA with Weld Volume Coverage of 62 Percent for First 10-year Insp Interval Pursuant to 10CFR50.55a(a)(3)(ii) & 10CFR50.55a(g)(6)(ii)(A)(5) RBG-44930, Monthly Operating Rept for Feb 1999 for River Bend Station, Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for River Bend Station, Unit 1.With RBG-44826, Monthly Operating Rept for Dec 1998 for River Bend Station Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for River Bend Station Unit 1.With ML20198K2701998-12-22022 December 1998 Rev 1 to RBS Cycle 8 Colr RBG-44773, Monthly Operating Rept for Nov 1998 for River Bend Station, Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for River Bend Station, Unit 1.With RBG-44727, LER 98-S01-00:on 981021,identified That Contract Employee with Temporary Access Authorization Failed to Disclose Complete Criminal & Employment History.Individual Denied Access to Plants for Five Years.With1998-11-17017 November 1998 LER 98-S01-00:on 981021,identified That Contract Employee with Temporary Access Authorization Failed to Disclose Complete Criminal & Employment History.Individual Denied Access to Plants for Five Years.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program ML20155H3491998-11-0303 November 1998 Safety Evaluation Granting Requests for Relief RR2-0001, RR2-0002 & RR2-0003 RBG-44719, Monthly Operating Rept for Oct 1998 for River Bend Station, Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for River Bend Station, Unit 1.With ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual RBG-44677, Monthly Operating Rept for Sept 1998 for River Bend Station, Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for River Bend Station, Unit 1.With ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods ML20151S5421998-09-0303 September 1998 Safety Evaluation Opposing Licensee Thermal Model as Currently Implemented.Evaluation Recommended to Be Used in Any follow-up Site Insp RBG-44629, Monthly Operating Rept for Aug 1998 for River Bend Station, Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for River Bend Station, Unit 1.With ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed RBG-44600, Monthly Operating Rept for July 1998 for River Bend Station1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for River Bend Station RBG-44564, Monthly Operating Rept for June 1998 for River Bend Station, Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for River Bend Station, Unit 1 ML20249A6431998-06-12012 June 1998 SER Accepting 980427 Request for Change to River Bend QA Manual Program Description,Per 10CFR50.54(a)(3) RBG-44539, Monthly Operating Rept for May 1998 for River Bend Station, Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for River Bend Station, Unit 1 RBG-44501, Monthly Operating Rept for Apr 1998 for River Bend Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for River Bend Station, Unit 1 ML20217M8951998-04-30030 April 1998 QA Program Manual ML20217P8281998-04-0707 April 1998 Safety Evaluation Accepting Relief Authorization for Alternative to Requirements of ASME Section Xi,Subarticle IWA-5250 Bolting Exam for Plants,Per 10CFR50.55a(a)(3)(i) RBG-44458, Monthly Operating Rept for Mar 1998 for River Bend Station, Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for River Bend Station, Unit 1 RBG-44423, Monthly Operating Rept for Feb 1998 for River Bend Station Unit 11998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for River Bend Station Unit 1 ML20203L6631998-02-11011 February 1998 Rev 0 to River Bend Station,1998 Emergency Preparedness Exercise RBG-44385, Monthly Operating Rept for Jan 1998 for River Bend Station, Unit 11998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for River Bend Station, Unit 1 RBG-44353, Monthly Operating Rept for Dec 1997 for River Bend Station, Unit 11997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for River Bend Station, Unit 1 RBG-44460, Forwards Annual Radiological Environmental Operating Rept, for Period Jan-Dec 19971997-12-31031 December 1997 Forwards Annual Radiological Environmental Operating Rept, for Period Jan-Dec 1997 ML20203H9891997-12-12012 December 1997 Part 21 Rept Re Potential Manufacturing Defect of Enterprise DSR-4 & DSRV-4 Edgs.Cooper Energy Svcs Supplied 1A-7840 Adjusting Screw to Affected Utils & Sites.River Bend Station Replaced W/Acceptable Assemblies ML20202E9941997-12-0101 December 1997 ISI Plan Second Ten-Yr Interval (Dec 1,1997-Nov 30,2007) ML20199K9741997-11-30030 November 1997 Brief Aerial Photography Analysis of RBS at St Francisville,LA:1996-1997 RBG-44337, Monthly Operating Rept for Nov 1997 for River Bend Station, Unit 11997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for River Bend Station, Unit 1 ML20202F0191997-11-28028 November 1997 Safety Evaluation Approving Transfer of License NPF-47 for River Bend Station,Unit 1 ML20199H3711997-11-19019 November 1997 SER Accepting Approving Request Relief from Requirements of Section XI, Rule for Inservice Insp of NPP Components, of ASME for Current or New 10-year Inservice Insp Interval IAW 50.55(a)(3)(i) of 10CFR50 RBG-44295, Monthly Operating Rept for Oct 1997 for River Bend Station Unit 11997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for River Bend Station Unit 1 RBG-44243, LER 97-S03-00:on 970911,contract Employee Was Granted Temporary Access After Failing to List Prior Employment Termination & Access Denial.Caused by Employee Failure to Provide Accurate Info.Updated Info Re Employee1997-10-13013 October 1997 LER 97-S03-00:on 970911,contract Employee Was Granted Temporary Access After Failing to List Prior Employment Termination & Access Denial.Caused by Employee Failure to Provide Accurate Info.Updated Info Re Employee 1999-09-09
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GULF STATES UTILITIES COMPANY l ama moeur,o mn uen e, w, u enec4au mS.e.uano l Aht A CQ(jf h'44 (M {lL44 346 l@
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January 31,1990 g RBG-32236 -
File Nos. G9.5, G9.25.1.3 i L
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I U.S. Nuclear Regulatory Commission i Document Control Desk-j Washington, D.C. 20555 Gentlemen:
River-Bend Station - Unit 1
! Docket No. 50-458 l i Please find enclosed Licensee Event Report No.89-036, Revision 1 for River Bend Station - Unit 1. This supplemental report is being submitted to provide the results of GSU's' safety assessment concerning valves which were energized contrary to the plant fire hazards analysis.,
Sincerely, '
f, . I. Wf u 'J. E. Booker
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Manager-River Bend Oversight purP River Bend Nuclear Group gk
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3/TFP/ W/DCH/CKC/pg cc: U.S. Nuclear Regulatory Commission 611 Ryan Plaza Drive Suite 1000 Arlington, TX 76011 NRC Resident Inspector P.O. Box 1051 St. Francisville, LA:70775 INPO Records Center 1100 Circle 75 Parkway Atlanta, GA 30339-3064 l
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At 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on 10/17/89, with the reactor at full power in Operational Condition 1, it was reported to the shift supervisor that various motor operated valves in the plant were energized, contrary to the assumptions contained in the plant fire hazards analysis. Because these valves were not de-energized, this event is reportable as a condition that is outside the design basis of the plant.
Operations initiated the required firewatches on the valves and associated raceways, or the valves were de-energized. All valves have been reanalyzed and procedures are being revised to require the valves to be de-energized or provide justification to leave the valves energized. These actions ensure that a fire in any area in the plant would leave at least one method of safe shutdown unaffected.
Therefore, there was no significant impact on the health and safety of the public as a result of this event.
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dl 0 12 0' Ob son n m . m mm a e r n ,. m m m REPORTED CONDITION At 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on 10/17/89, with the reactor at full power in Operational Condition 1, it was reported to the shift supervisor that various motor operated valves (MOVs) (*V*) in the plant were energized, contrary to the assumptions contained in the plant fire hazards analysis (FHA). These valves are listed in Tables 2 and 5 of design Specification 240.201, " Fire Analysis and Evaluation Criteria", I and are shown to be assumed to have power removed during plant l operation. The list of valves affected consists of thirteen valves in I the residual heat removal system (*B0*), three in the fuel pool cooling system (*DA*), one in the reactor core isolation cooling system (*BN*), two in the standby service water system (*KG*), and one
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in the main steam system (*TA*).
Because these valves were not de-energized as assumed in the FHA, compliance with General Design Criteria 3 of Appendix A to 10CFR50 was not assured; therefore, this event is being considered reportable under 10CFR50.73(a)(2)(11)(B) as a condition that is outside the design basis of the plant.
JNVESiljAllpN A detailed study of the FHA was prompted by the investigation of an
, earlier condition involving improperly installed fire walls at the Division I remote shutdown panel (reference LER 88-009). Comparison of the FHA requirements to the valve lineups and station operating procedures (SOPS) noted that the valves listed as ' remove power' in the FHA were instead energized. The reasons why the FHA requirements were not reflected in procedures and operational practice is unknown.
A review of the USAR and the original design criteria, and conversations with the Architect / Engineer (AE) Stone and Webster Engineering Corporation, demonstrated why these valves were shown to be de-energized. Two of the valves, 1E12*MOVF009 and 1821*MOVF019 were considered potential LOCA pathways due to a fire in the main control room or in the remote shutdown panel, in the case of the IE12*M0VF009 valve, the concern is to prevent a fire-induced opening of the low pressure shutdown cooling residual heat removal (RHR) (*BO*) system to the reactor vessel at operating pressure. This high/ low pressure interface valve is identified in section 9.5 of the USAR. An enable switch (*IS*) on valve IE12*MOVF008, the outboard isolation valve (*ISV*), is used to protect the RHR system from spurious actuations generated in a fire in the main control room. This switch is located in the Division I remote shutdown room, along with the controls for 1E12*MOVF009. A fire assumed to affect the remote shutdown room could potentially open both inboard and outboard valves, over pressurizing the RHR system with vessel pressure. A review of the operating requirements for the IE12*MOVF009 valve showed that plant operation in Operational Conditions 1, 2, and 3 with the valve de-energized is acceptable.
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01 1 01 3 0' Ol7 an . . .= =. mu w n l Valve 1821*MOVF019 is the outboard isolation valve for the main steam '
isolation valve (MSIV) (*IS*) drains. A postulated control room fire could cause this valve to open spuriously, along with valves IB21*MOVF016 and 1821*MOVF085, dumping steam to the main condenser .
(*CDV*). When this scenario is considered with a loss of offsite ,
power, as required by the FHA, steam may be vented to the this atmosphere as main condenser vacuum is lost. ,
The remaining valves were listed as ' power removed' by the A/E because the divisional separation of the raceway was never verified to meet 10CFR50 Appendix R standards. As a result of this event, GSU has identified all affected cabling, including associated circuits, and has evaluated their separation and fire area locations. This evaluation shows that all valves listed have adequate Appendix R separation. This analysis considers the effect of a fire anywhere in the plant, with the requisite loss of offsite power.
The three spent fuel pool cooling (SFC) (*DA*) valves require '
administrative control as a fire may effect either the inboard or outboard division, possibly causing a loss of fuel pool cooling to the containment fuel pools. This situation could only occur during refueling, and assuming worst case conditions, 1.25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br /> is required to heat the pool to the upper limit of 150 degrees F. This is more than adequate time to manually reposition the valves if required. >
A review of previously submitted LERs by River Bend Station revealed six previous LERs related to design requirements not being reflected in plant operating procedures. LERs86-066 and 87-026 identified fire doors which were not listed on the appropriate surveillance '.est procedures (STPs), LER 88-010 identified a secondary containment door which was not listed on the appropriate STP, LER 89-003 identified a breaker which was not listed on the appropriate STP, Additionally, IER 86-059 identified that a design modification to the low pressure coolant injection line that changed the location of the piping high point vents was not reflected in the appropriate STP and LER 87-030 identified that the appropriate area temperatures were not being monitored in tne reactor plant component cooling areas as required by the Technical Specifications. However, none of these events were related to ensuring that the assumptions of the FHA were properly reflected in the plant operating procedures.
CORRECTIVE ACTION Engineering identified two possible methods to satisfy the requirements of the analysis and the plant Technical Specifications (TS). One method was to de-energize the M0Vs as assumed in the FHA.
The second method was to treat the valves and the associated electrical raceways as having missing installed fire barriers, and to take' the action prescribed in TS 3/4.7.7, instituting a roving firewatch in the affected areas. The latter method was adopted and
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n t; RIVER BYND STATION # lilo jo le l al gl p gj g -- djg - ol1 ol4 0F ob veu . .se a amewon the required firewatches were initiated. Two valves, 1E12*MOVF009 and 1B21*MOVF019 were in areas not accessible to firewatch personnel and ,
were therefore de-energized. The choice of methods considered the effect on Operations personnel due to a number of de-ehergized valves, including the effect due to lit annunciators, and the additional requirement to enter the auxiliary building to de-energize the valves.
Operations will change the valve lineups to show valve IE12*MOVF009 de-energized until reactor pressure is reduced below 135 psig reactor pressure, which is the system pressure for shutdown cooling piping.
Valve 1821*MOVF019 is required for startup and is used in some operational transients. Therefore, the status of this valve was changed to closed and de-energized. However, administrative controls have been implemented to allow station personnel while at local motor l control centers to open the valve when needed. This will enable positive control of this pathway in the event of a control room fire.
The valves are currently tagged out. Revision of the valve lineup and procedural changes have been completed. The three SFC valves require I administrative control under worst case conditions to be aligned to supply cooling to the upper pools within 1.25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br /> to limit the upper pool temperature to 150 degrees F. This caution will be added to the pre-fire strategy for the area in the fuel building containing these valves by February 28, 1990. A change document revising Tables 2 and 5 of the FHA has been completed.
SAffTf_ ASSESSMENT As identified in the investigation, the majority of the valves and cabling were found to have sufficient separation to enable re-energizing. In the cases of SFC, a~ fire could potentially cause either division to close while the plant was in a refueling cycle and fuel pool cooling to the upper containment pools would be required.
The closure of these valves would be noted with any gradual rise of pool temperature. Assuming a fire did affect these valves, upon detection of increasing pool temperature, valve positions could be determined and repositioned if necessary. Alternate methods exist to provide water to the upper pools (water from fire protection system
(*KP*) for instance). Therefore, pool temperatures would not be expected to exceed design levels, i.e. operator actions would prevent any overheating in the upper pool. For all valves except 1E12*MOVF009 and 1821*MOVF019, analysis demonstrates that a fire in any area would leave at least one method of safe shutdown unaffected.
Valve 1821*MOVF019 is the outboard drain and containment isolation valve serving the inboard MSIVs. This valve, in combination with valves 1821*MOVF016, 1821*MOVF085 and 1821-MOVF021 provide a pathway to the main condenser for condensate and warmup. The piping and instrumentation diagram (PID) shows that valves F016, F019 and F085 are normally open wb11e F021 is normally closed. The only area where the control circuits for all these valves may be potentially affected
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0 11 o l; M nb von se . .ar a an w nn by the same fire event is in the main control room. The concern is that a fire in the main control room may cause the F021 valve to spuriously open, providing a path for steam release to the condenser, ,
Note that the contribution of valve 1821-A0VF033, in parallel with F021, is neglected due to the small (1") line size. The other drains are 3" lines. Steam release to the condenser is of no consequence with condenser vacuum and circulating water operational. Assuming the main control room fire has also damaged these systems, eventually steam will be vented from the condenser through the air release valves (ARVs). A loss of offsite power (LOOP), required to be considered for Appendix R, would have the same effect on the condenser.
The potential effect of steam release on offsite dose through the path outlined above has been evaluated. Several cases were considered as follows:
. Steam release continues unabated for the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> period until cold shutdown.
. Steam release is terminated by operator action at 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.
. Determination of the time required to close the path before 10CFR part 20 limits were exceeded.
. Using the maximum iodine levels, the analysis showed that at a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> duration, offsite dose calculated was less than 1% of the 10CFR 100 limits, and only slightly above those in 10CFR20. Closure of the release path at less than I hour and 39 minutes would limit release to the normal operation limits proscribed by 10CFR20. The results were much less than accidents previously identified, such as a steam line break outside the containment. Another case considered in the calculation was the offsite dose after 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> based on the actual expected iodine levels, rather than the maximum. This analysis shows the calculated offsite dose is less than the 10CFR20 limits.
Any release would be detected by monitoring equipment either inside or outside the plant. The effect on reactor water level would be small but noticeable. These indications would guide the operators to manually close this leakage path. A PRA conducted on this scenario as outlined above indicato that the probability of the event is estimated at 1.9E-04 over the time the valve was energized.
l In summary, the probability of this postulated event was low over the duration of time that the valve was energized. Furthermore, the offsite dose calculation based on the actual expected iodine levels l
provided an offsite dose less than the 10CFR20 limits. Therefore, GSU concludes that this postulated event did not adversely affect the health and safety of the public.
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01 1 Ol 6 0F Ol7 nn, . . sn.=se a mmw nn Valve IE12*MOVF009 operates in tandem with IE12*MOVF008 to provide containment isolation to the RHR normal suction path. These valves also protect the low pressure (200 psig) RHR system from the high pressures (1050 psig) in the reactor pressure vessel (RPV). This pair of valves is protected in the main control room by an enable / disable switch for the F008 valve located in the Division I remote shutdown room. During power operation, there is no power to the circuits for F008 in the control room, although position indication is provided. A fire in the main control room could only affect the F009 valve, preserving the high/ low pressure interface. However, these valves also are both controlled on the Division I remote shutdown panel and a fire in this area could potentially affect both valves, causing them to spuriously open. During power operation, this would flood the RHR system with vessel pressure.
Exposing the RHR system to RPV pressure would certainly cause extensive damage, particularly to thermowells, instrument taps and
. pumps. Damage would occur downstream of F008, as the piping between the valves is designed to RPV pressure. A PRA was performed to determine the effect this event would have on core damage frequency (CDF). This analysis conservatively assumes that: a) RHR piping ruptures in the auxiliary building and cannot be isolated, and b) RHR loops A, B, and C are lost due to flooding, pipe rupture or loss of function due to the original fire. Reactor water inventory would be
, maintained by a combination of HPCS and LPCS. Over the long term, additional water is available from the service water or fire protection water systems injecting into the vessel or suppression pool. The estimated CDF given this scenario is 5.8E-08, lower than the total RBS CDF of 5.0E-06. A LOOP is not a precursor to this event, but is evaluated in the response of the plant.
This PRA is also conservative by not considering the effect of the protection afforded by the Reg Guide 1.75 separation provided in the shutdown cabinet, separating one division from another. Doors in the Division I room are locked, so routine entry is not possible. The room is provided with smoke detection and response to any fire detected would be rapid due to the proximity of the control roou and the fire brigade equipment locker. There is no equipment in the room that requires servicing with flammable or combustible liquids.
An interfacing system LOCA would be a severe accident, but recoverable. The CDF derived from the analysis indicates that the safety significance is low, and is necessarily conservative. There have been no fires at River Bend Station in the areas discussed. The health and safety of the public was not at risk from this postulated low-probability event.
With .the exceptions of valve 1B21*MOVF019 and valve IE12*MOVF009, I engineering evaluation shows all valves listed have adequate Appendix R separation and/or can be administrative 1y controlled. The F009 and I
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