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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20210K4721999-08-0303 August 1999 SER Accepting Licensee 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20206A2111999-04-21021 April 1999 Safety Evaluation Authorizing Pump Relief Request PRR-001 & Valve Relief Request VRR-001 & Denying Valve Relief Request VRR-002 ML20205D5481999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Exam Weld AA with Weld Volume Coverage of 62 Percent for First 10-year Insp Interval Pursuant to 10CFR50.55a(a)(3)(ii) & 10CFR50.55a(g)(6)(ii)(A)(5) ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program ML20155H3491998-11-0303 November 1998 Safety Evaluation Granting Requests for Relief RR2-0001, RR2-0002 & RR2-0003 ML20151S5421998-09-0303 September 1998 Safety Evaluation Opposing Licensee Thermal Model as Currently Implemented.Evaluation Recommended to Be Used in Any follow-up Site Insp ML20249A6431998-06-12012 June 1998 SER Accepting 980427 Request for Change to River Bend QA Manual Program Description,Per 10CFR50.54(a)(3) ML20217P8281998-04-0707 April 1998 Safety Evaluation Accepting Relief Authorization for Alternative to Requirements of ASME Section Xi,Subarticle IWA-5250 Bolting Exam for Plants,Per 10CFR50.55a(a)(3)(i) ML20202F0191997-11-28028 November 1997 Safety Evaluation Approving Transfer of License NPF-47 for River Bend Station,Unit 1 ML20199H3711997-11-19019 November 1997 SER Accepting Approving Request Relief from Requirements of Section XI, Rule for Inservice Insp of NPP Components, of ASME for Current or New 10-year Inservice Insp Interval IAW 50.55(a)(3)(i) of 10CFR50 ML20216E9921997-09-0404 September 1997 Safety Evaluation Accepting 970623 Request for Relief Re Authorization for Use of ASME Code Case N-416-1 & N-532,ISI Program for Listed Plants ML20141H8411997-07-30030 July 1997 Safety Evaluation Accepting Use of Code Case N-508-1 for All Four Plants for Rotation of Serviced Snubbers & Pressure Relief Valves for Purpose of Testing in Lieu of ASME Code ML20138C8501997-04-28028 April 1997 Safety Evaluation Authorizing Proposed Alternative to Vibration Measurement Requirements of OM-6,paragraph 4.6.4 (B),For Standby Svc Water Pumps & Diesel Fuel Oil Transfer Pumps,Per 10CFR50.55a(a)(3)(ii) ML20147H4371997-03-31031 March 1997 Safety Evaluation Accepting Proposed P-T Limits for Heatup, Cooldown,Inservice Leak & Hydrostatic Testing & Core Criticality ML20149M4221996-12-12012 December 1996 Safety Evaluation Supporting Update Insvc Insp Programs to 1992 & Portions of 1993 ASME Boiler & Pressure Vessel Code, Sect XI for Licenses DPR-51,NPF-6,NPF-38,NPF-29 & NPF-47. Technical Ltr Rept Encl ML20107F5611996-04-17017 April 1996 Safety Evaluation Providing Guidance on Submitting plant- Specific Info W/Respect to IST Program Alternatives Request ML20149E8831994-08-0202 August 1994 Safety Evaluation Accepting Interim Relief Request IRR-03 Re Drywell Isolation Check Valves in Equipment Drain Lines & Reactor Equipment Closed Cooling Water Sys ML20058H0221993-11-30030 November 1993 Safety Evaluation Accepting Licensee Proposed Alternative to ASME Code Requirements in PRR 15,per 10CFR50.55(a)(3)(i). Denies Pump Relief Request 14 ML20059B2771993-10-22022 October 1993 Safety Evaluation Accepting IST Program Relief Requests ML20056G2001993-08-19019 August 1993 Safety Evaluation Denying 930419 Request for Relief from Requirements for Hydrostatic Testing of ASME Class 3 Pressure Retaining Components ML20126A2971992-12-16016 December 1992 Safety Evaluation Accepting Design for Drywell Hydrogen Concentration & Suppression Pool Water Level,W/Respect to Reg Guide 1.97 ML20128D2251992-12-0202 December 1992 Safety Evaluation Accepting Methodology Described in Topical Rept EA-CA-91-0001-M, Steady State Core Physics Methods for BWR Designs & Analysis ML20055F1891990-06-27027 June 1990 Safety Evaluation Supporting Util Tech Spec Change Request Re Scram Accumulator Check Valves ML20245A1051989-06-15015 June 1989 Safety Evaluation Accepting Util 890515 & 19 Submittals Re Results of Augmented IGSCC Insp & Flaw Evaluation of Feedwater Inlet Nozzle N4-A to Safe End Weld ML20247J7411989-05-25025 May 1989 Safety Evaluation Accepting Existing Intervals for on-line Functional Testing for Achieving High Reactor Trip Sys Reliability at All Operating Reactors,Per Generic Ltr 83-28, Item 4.5.3 ML20235N6031989-02-21021 February 1989 Safety Evaluation Approving Alternate Method for Complying w/10CFR50.55a for Main Steam Positive Leakage Control Sys Valve ML20195H1511988-11-23023 November 1988 Safety Evaluation Accepting Responses Re Item 4.5.2 of Generic Ltr 83-28 Re Reactor Trip Sys Reliability on-line Testing ML20196A6611988-11-18018 November 1988 SER Accepting Util Response to Generic Ltr 83-28,Item 2.1, Part 2 Re Vendor Interface Programs for Reactor Trip Sys Components ML20195G8861988-11-18018 November 1988 SER Accepting Util Responses to Generic Ltr 83-28,Item 2.1, Part 1 Re Reactor Trip Sys Components ML20154M6561988-09-22022 September 1988 Safety Evaluation Supporting Licensee post-trip Review Program & Procedures Per Generic Ltr 83-28,Item 1.1 Re Generic Implications for Salem ATWS Events ML20151Q4701988-08-0101 August 1988 Supplemental Safety Evaluation Re First 10-yr Inservice Insp Program.Nrc Concurs W/Determination Made by Licensee That Section XI of ASME Code Exam Requirements for Category B-A Welds in Reactor Pressure Vessel Are Impractical to Perform ML20150F9501988-07-12012 July 1988 Safety Evaluation Supporting Util 840803 & 870922 Responses to Generic Ltr 83-28,Items 3.1.1,3.1.2,3.2.1 & 3.2.2 Re post-maint Testing of All safety-related Components ML20148D4391988-01-14014 January 1988 Safety Evaluation Supporting Util 870731 & 1030 Submittals on Facility Compliance Re Alternate Rod Injection & Recirculation Pump Trip Sys,Per ATWS Rule 10CFR50.62 ML20236D1851987-10-20020 October 1987 Safety Evaluation Accepting Util 870602 Rev 2 to First 10-yr Interval Inservice Insp Program ML20235K6871987-09-28028 September 1987 Safety Evaluation Accepting Util Monitoring Sys for UHS as Proposed in NUREG-0989, Safety Evaluation Supporting Proposed Turbine Maint Program. Proposal Satisfies Licensee Commitment Prescribed in Sser 5. Commitment Acceptable Resolution of Turbine Maint Issue1987-08-26026 August 1987 Safety Evaluation Supporting Proposed Turbine Maint Program. Proposal Satisfies Licensee Commitment Prescribed in Sser 5. Commitment Acceptable Resolution of Turbine Maint Issue ML20209B4291987-04-22022 April 1987 Safety Evaluation Supporting Util Proposed Rev to Tech Specs Re Drywell Leakage Test Interval ML20234E0491987-03-26026 March 1987 SER Accepting Response to Generic Ltr 83-28,Items 3.1.3 & 3.2.3 Re post-maint Testing of Reactor Trip Sys & All Other safety-related Components ML20205M3691987-03-26026 March 1987 Sser Re Mark III Containment Related Issues ML20212L2351987-01-21021 January 1987 Sser Re Util 860512 & 1119 Rev 4 to Preservice Insp Program & Relief Request R 0012 (a to E) from Certain ASME Code Requirements.Relief Granted.Preservice Insp Program in Compliance w/10CFR50.55a(g)(3) ML20203N7061986-10-0909 October 1986 Safety Evaluation Supporting Amend 2 to License NPF-47 ML20214P2061986-09-19019 September 1986 SER Supporting 860917 & 19 Requests for Amend to License NPF-40,changing Tech Spec Table 3.6.4-1 to Allow Inoperability of Inboard Isolation Valve MOVFO76 Through 861004 ML20207H4151986-07-16016 July 1986 Safety Evaluation Supporting Technical Solution to Address Operability & Reliability of Tdi Emergency Diesel Generators ML20133F8241985-08-0505 August 1985 Marked-up Draft Sser 2 Re Application for Ol,Reporting Status of Certain Items Not Resolved at Time of SER Publication 1999-08-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARRBG-45144, Monthly Operating Rept for Sept 1999 for River Bend Station. with1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for River Bend Station. with ML20216G1201999-09-0909 September 1999 Rev 3 to Rbs,Cycle 9 Colr RBG-45110, Monthly Operating Rept for Aug 1999 for River Bend Station, Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for River Bend Station, Unit 1.With RBG-45087, Special Rept:On 990510,LPCI a & LPCS Injected Into Rv for Less than Two Minutes.Caused by Electrical Transient in One of ECCS Power Supplies.Operators Verified Reactor Cavity Level & Closed Injection Valves to Stop Injection1999-08-0606 August 1999 Special Rept:On 990510,LPCI a & LPCS Injected Into Rv for Less than Two Minutes.Caused by Electrical Transient in One of ECCS Power Supplies.Operators Verified Reactor Cavity Level & Closed Injection Valves to Stop Injection ML20210K4721999-08-0303 August 1999 SER Accepting Licensee 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves RBG-45091, Monthly Operating Rept for July 1999 for River Bend Station, Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for River Bend Station, Unit 1.With ML20210C6391999-07-0202 July 1999 Rev 2 to River Bend Station,Cycle 9 Colr RBG-45055, Monthly Operating Rept for June 1999 for River Bend Station, Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for River Bend Station, Unit 1.With ML20196J8031999-06-24024 June 1999 Rev 1 to Rbs,Cycle 9 Colr RBG-45028, Monthly Operating Rept for May 1999 for River Bend Station, Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for River Bend Station, Unit 1.With RBG-45016, Monthly Operating Rept for Apr 1999 for River Bend Station, Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for River Bend Station, Unit 1.With ML20206A2111999-04-21021 April 1999 Safety Evaluation Authorizing Pump Relief Request PRR-001 & Valve Relief Request VRR-001 & Denying Valve Relief Request VRR-002 RBG-44969, Monthly Operating Rept for Mar 1999 for River Bend Station, Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for River Bend Station, Unit 1.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205D5481999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Exam Weld AA with Weld Volume Coverage of 62 Percent for First 10-year Insp Interval Pursuant to 10CFR50.55a(a)(3)(ii) & 10CFR50.55a(g)(6)(ii)(A)(5) RBG-44930, Monthly Operating Rept for Feb 1999 for River Bend Station, Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for River Bend Station, Unit 1.With RBG-44826, Monthly Operating Rept for Dec 1998 for River Bend Station Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for River Bend Station Unit 1.With ML20198K2701998-12-22022 December 1998 Rev 1 to RBS Cycle 8 Colr RBG-44773, Monthly Operating Rept for Nov 1998 for River Bend Station, Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for River Bend Station, Unit 1.With RBG-44727, LER 98-S01-00:on 981021,identified That Contract Employee with Temporary Access Authorization Failed to Disclose Complete Criminal & Employment History.Individual Denied Access to Plants for Five Years.With1998-11-17017 November 1998 LER 98-S01-00:on 981021,identified That Contract Employee with Temporary Access Authorization Failed to Disclose Complete Criminal & Employment History.Individual Denied Access to Plants for Five Years.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program ML20155H3491998-11-0303 November 1998 Safety Evaluation Granting Requests for Relief RR2-0001, RR2-0002 & RR2-0003 RBG-44719, Monthly Operating Rept for Oct 1998 for River Bend Station, Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for River Bend Station, Unit 1.With ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual RBG-44677, Monthly Operating Rept for Sept 1998 for River Bend Station, Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for River Bend Station, Unit 1.With ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods ML20151S5421998-09-0303 September 1998 Safety Evaluation Opposing Licensee Thermal Model as Currently Implemented.Evaluation Recommended to Be Used in Any follow-up Site Insp RBG-44629, Monthly Operating Rept for Aug 1998 for River Bend Station, Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for River Bend Station, Unit 1.With ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed RBG-44600, Monthly Operating Rept for July 1998 for River Bend Station1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for River Bend Station RBG-44564, Monthly Operating Rept for June 1998 for River Bend Station, Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for River Bend Station, Unit 1 ML20249A6431998-06-12012 June 1998 SER Accepting 980427 Request for Change to River Bend QA Manual Program Description,Per 10CFR50.54(a)(3) RBG-44539, Monthly Operating Rept for May 1998 for River Bend Station, Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for River Bend Station, Unit 1 RBG-44501, Monthly Operating Rept for Apr 1998 for River Bend Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for River Bend Station, Unit 1 ML20217M8951998-04-30030 April 1998 QA Program Manual ML20217P8281998-04-0707 April 1998 Safety Evaluation Accepting Relief Authorization for Alternative to Requirements of ASME Section Xi,Subarticle IWA-5250 Bolting Exam for Plants,Per 10CFR50.55a(a)(3)(i) RBG-44458, Monthly Operating Rept for Mar 1998 for River Bend Station, Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for River Bend Station, Unit 1 RBG-44423, Monthly Operating Rept for Feb 1998 for River Bend Station Unit 11998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for River Bend Station Unit 1 ML20203L6631998-02-11011 February 1998 Rev 0 to River Bend Station,1998 Emergency Preparedness Exercise RBG-44385, Monthly Operating Rept for Jan 1998 for River Bend Station, Unit 11998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for River Bend Station, Unit 1 RBG-44353, Monthly Operating Rept for Dec 1997 for River Bend Station, Unit 11997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for River Bend Station, Unit 1 RBG-44460, Forwards Annual Radiological Environmental Operating Rept, for Period Jan-Dec 19971997-12-31031 December 1997 Forwards Annual Radiological Environmental Operating Rept, for Period Jan-Dec 1997 ML20203H9891997-12-12012 December 1997 Part 21 Rept Re Potential Manufacturing Defect of Enterprise DSR-4 & DSRV-4 Edgs.Cooper Energy Svcs Supplied 1A-7840 Adjusting Screw to Affected Utils & Sites.River Bend Station Replaced W/Acceptable Assemblies ML20202E9941997-12-0101 December 1997 ISI Plan Second Ten-Yr Interval (Dec 1,1997-Nov 30,2007) ML20199K9741997-11-30030 November 1997 Brief Aerial Photography Analysis of RBS at St Francisville,LA:1996-1997 RBG-44337, Monthly Operating Rept for Nov 1997 for River Bend Station, Unit 11997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for River Bend Station, Unit 1 ML20202F0191997-11-28028 November 1997 Safety Evaluation Approving Transfer of License NPF-47 for River Bend Station,Unit 1 ML20199H3711997-11-19019 November 1997 SER Accepting Approving Request Relief from Requirements of Section XI, Rule for Inservice Insp of NPP Components, of ASME for Current or New 10-year Inservice Insp Interval IAW 50.55(a)(3)(i) of 10CFR50 RBG-44295, Monthly Operating Rept for Oct 1997 for River Bend Station Unit 11997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for River Bend Station Unit 1 RBG-44243, LER 97-S03-00:on 970911,contract Employee Was Granted Temporary Access After Failing to List Prior Employment Termination & Access Denial.Caused by Employee Failure to Provide Accurate Info.Updated Info Re Employee1997-10-13013 October 1997 LER 97-S03-00:on 970911,contract Employee Was Granted Temporary Access After Failing to List Prior Employment Termination & Access Denial.Caused by Employee Failure to Provide Accurate Info.Updated Info Re Employee 1999-09-09
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NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20655 4001 o% ...../
l l SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION LICENSEE RESPONSE TO GENERIC LETTER 95-07. " PRESSURE LOCKING l AND THERMAL BINDING OF SAFETY-RELATED POWER-OPERATED GATE VALVES" i l
ENTERGY OPERATIONS. INC.
RIVER BEND STATION. UNIT 1 1
DOCKET Nr 1458
1.0 INTRODUCTION
Pressure locking and thermal binding represent potential common-cause failure mechanisms that can render redundant safety systems incapable of performing their safety functions. The identification of susceptible valves and the determination of when the phenomena might occur require a thorough knowledge of components, systems, and plant operations. Pressure locking occurs in flexible-wedge and double-disk gate valves when fluid becomes pressurized inside the valve bonnet and the actuator is not capable of overcoming the additional thrust
, requirements resulting from the differential pressure created across both valve disks by the l pressurized fluid in the valve bonnet. Thermal binding is generally associated with a wedge gate valve that is cic8ed wniie the system is hot and then is allowed to cool before an attempt is made to open the vwo.
l Pressure locking or thermal binding occurs as a result of the valve design characteristics (wedge and valve body configuration, flexibility, and material thermal coefficients) when the valve is subjected to specific pressures and temperatures during various modes of plant l
operation. Operating experience indicates that these situations were not always considered in many plants as part of the design basis for valves.
2.0 REGULATORY REQUIREMENTS Title 10 of the Code of Federal Reculations (10 CFR) Part 50 (Appendix A, General Design l Criteria 1 and 4) and plant licensing safety analyses require or commit (or both) that licensees l design and test safety-related components and systems to provide adequate assurance that l those systems can perform their safety functions. Other individual criteria in Appendix A to 10 CFR Part 50 apply to specific systems. In accordance with those regulations and licensing commitments, and under the additional provisions of 10 CFR Part 50 (Appendix B, Criterion XVI), licensees are expected to act to ensu.'e that safety-related power-operated gate valves susceptible to pressure locking or thermal binding are capable of performing their l required safety functions.
J Enclosure 9908060135 990003 PDR ADOCK 05000458 ;
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I
. 2-On August 17,1995, the NRC issued Generic Letter (GL) 95-07, " Pressure L , king and Thermal Binding of Safety-Related Power-Operated Gate Valves," to request that licensees take certain actions to ensure that safety-related power-operated gate valves that are susceptibio to pressure locking or thermal binding are capable of performing their safety functions within the current licensing basis of the facility. GL 95-07 requested that each licensee, within 180 days of the date of issuance of the generic letter (1) evaluate the operational configurations of safety-related power-operated gate valves in its plant to identify valves that are susceptible to pressure locking or thermal binding, and (2) perform further analyses and take needed corrective actions (or justify longer schedules) to ensure that the susceptible valves, identified in (1) above, are capable of performing their intended safety functions under all modes of plant operation, including test configuration. In addition, GL 95-07 requested that licensees, within 180 days of the date of issuance of the generic letter, provide to the NRC a summary description of (1) the susceptibility evaluation used to determine that 5
valves are or are not susceptible to pressure locking or thermal binding, (2) the results of the susceptibihty evaluation, including a listing of the susceptible valves identified, and (3) the corrective actions, or other dispositioning, for the valves ides,tified as susceptible to pressure locking or thermal binding. The NRC issued GL 95-07 as a " compliance backfit" pursuant to 10 CFR 50.109(a)(4)(i) because modification may be necessary to bring facilities into compliance with the rules of the Commission referenced above, in a letter of February 13,1996, Entergy Operations, Inc. (EOI), submitted its 180-day response to GL 95-07 f',r River Bend Station, Unit 1. The NRC staff reviewed EOl's submittal and requested additional information in a letter dated May 20,1996. In a letter of June 28,1996, EOl provided the additional information.
3.0 STAFF EVALUATION 3.1 Scope of EOl's Review GL 95-07 requested that Jicensees evaluate the operational configurations of saf,ety-related power-operated gate valves in their plants to identify valves that are susceptible to pressure locking or thermal binding. By letters of February 13 and June 28,1996, EOl described the scope of valves evaluated in response to GL 95-07. The NRC staff has reviewed the scope of EOl's susceptibility evaluation performed in response to GL 95-07 and found it complete and acceptable.
Normally open, safety-related power-operated gate valves, which are closed for test or sunreillance but must return to the open posiiion, were evaluated within the scope of GL 95-07.
Two valves were identified as susceptible to pressure locking when closed for testing and were modified to eliminate the potential for pressure locking. The staff finds the criteria for determining the scope of power-operated valves for GL 95-07 are consistent with the staff's acceptance of the scope of motor-operated valves associated with GL 89-10. " Safety-Related Motor-Operated Valve Testing and Surveillance."
3.2 Correctiva Actions GL 95-07 requestcr1 that licensees, within 180 days, perform further analyses as appropriate, and take appropriate corrective actions (or justify longer schedules), to ensure that the susceptible valves identified are capable of performing their intended safety function under all N
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modes of plant operation, including test configuration. EOl's submittals dincussed proposed corrective actions to address potential pressure-locking and thermal-binding problems. The staff's evaluation of EOl's actions is discussed in the following paragraphs:
- a. EOl stated that the following valves were modified to eliminate the potential for pressure locking:
E12-MOVF004A/B Low Pressure Coolant injection Suppression Pool Suction E12-MOVF042A/B/C Low Pressurc Coolant injection isolation E21-MOVF005 Low Pressure Core Spray injection E22-MOVF004 High Pressure Core Spray (HPCS) Injection E22-MOVF015 HPCS Suppression Pool Suction E51-MOVF013 Reactor Core Isolation Cooling (RCIC) Injection E51-MOVF031 RCIC Suppression Pool Suction The staff finds that physical modification to valves susceptible to pressure locking is an appropriate corrective action to ensure operability of the valves and is thus acceptable.
- b. EOl stated that all flexible and solid wedge gate valves in the scope of GL 95-07 were evaluated for thermal binding. When evaluating whether va!ves were susceptible to thermal binding, EOl assumed that thermal binding would not occur below specific temperature thresholds. The screening criteria used by EOl appear to provido a reasonable approach to identify those valves that might be susceptible to thermal binding. Until more definitive industry criteria are developed, the staff concludes that EOl's actions to address thermal binding of gate valves are acceptable.
4.0 CONCLUSION
On the basis of this evaluation, the NRC staff finds that EOl has performed appropriate evaluations of the operational configurations of safety-related power-operated gate valves to identify valves at the River Bend Station, Unit 1, that are susceptible to pressure locking or therrnal binding. In addition, the NRC staff finds that EOl has taken appropriate corrective actions to ensure that these valves are capable of performing their intended safety functions.
Therefore, the staff concludes that EOl has adequately addressed the requested actions discussed in GL 95-07.
Principal Contributor: S. Tingen Date: August 3, 1999