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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3201994-10-0707 October 1994 LER 94-022-00:on 940907,TS Violation Occurred Due to Inadequate Fire Watch.Retrained Personnel Associated W/ Painting activities.W/941007 Ltr ML20029E2001994-05-13013 May 1994 LER 94-006-00:on 940414,SS Recognized That Required Frequency for Performing STP 057-3705 Had Been Exceeded. Caused by Inadequate Supervisory Methods.Corrective Action: Inhouse Tracking Process Will Be created.W/940513 Ltr ML20029C8741994-04-26026 April 1994 LER 93-026-01:on 931117,isolation of RCIC Sys Occurred Due to Apparent Failure of Relay.Three Relays Associated W/ Isolation Replaced & Shipped to Mfg for Failure Analysis.W/ 940426 Ltr ML20029C7021994-04-19019 April 1994 LER 90-003-05:on 900206,discovered Deficiencies in Thermo-Lag Fire Barrier Envelope Around Redundant Safe Shutdown.Firewatches Established in Areas Where Thermo Lag Used as barrier.W/940419 Ltr ML20046C3891993-08-0202 August 1993 LER 93-014-00:on 930701,installed Sprinkler Sys as Substitute for Passive fire-rated Barrier Due to Deficiency Identified in Fire Barrier Separation Requirements.Declared Fire Barriers Surrounding Valves degraded.W/930802 Ltr ML20046B8981993-07-29029 July 1993 LER 93-013-00:on 930629,high Pressure Core Spray Pump Failed to Start & Run During Surveillance Test Due to Failed Overfrequency Relay.Relay Tested & Installed in Switchgear. W/930729 Ltr ML20046A2361993-07-22022 July 1993 LER 93-008-01:on 930429,relief Request Improperly Prepared for Insvc Testing Program Results in Noncompliance W/Main Steam Isolation Valve Testing Requirement.Caused by Personnel Error.Testing Frequency Revised ML20045G6111993-07-0202 July 1993 LER 93-012-00:on 930603,deficiency in Plant Surveillance Test Procedures Identified.Caused by Primary Causal Factor Inattention to Detail During Initial Procedure Development Process.Surveillance Test Procedures performed.W/930702 Ltr ML20045D6991993-06-21021 June 1993 LER 93-011-00:on 930521,determined That Mode Switch Placed in Refuel Position During Testing of Switch Interlock Functions.Caused by Conflicting Info in Surveillance Procedures.Operating Procedure revised.W/930621 Ltr ML20045C0141993-06-14014 June 1993 LER 93-010-00:on 930514,SDC Lost for Approx Three Minutes When One SDC Suction Valve Closed Due to Initiation of Spurious ESF Actuation Signal.Caused by Personnel Error. Procedural Guidance revised.W/930614 Ltr ML20045C0021993-06-14014 June 1993 LER 93-003-01:on 930225,incidents Discovered Which Caused Interlock Mechanism in Upper Containment Airlocks at Elevation 171 to Operate Improperly.Case Study Training Class Developed for Airlock incidents.W/930614 Ltr ML20045A1461993-06-0404 June 1993 LER 93-009-00:on 930504,discovered That Surveillance Test Procedure for Control Bldg Chilled Water Sys Quarterly Pump Missed Due to Cognitive Personnel Error.Administrative Procedure Will Be revised.W/930604 Ltr ML20045A4261993-06-0101 June 1993 LER 93-002-02:on 930212,discovered That TS SRs Not Properly Implemented in Logic Sys Functional Tests Due to Inattention to Detail While Preparing Revs of Relevant Surveillance Test Procedures (Stp).Relevant STPs revised.W/930601 Ltr ML20044H3571993-06-0101 June 1993 LER 93-008-00:on 930429,investigation Determined That Relief Request for Inservice Testing of Pumps & Valves in Conflict W/Msiv Testing Requirements.Caused by Personnel Error.Relief Request 40 revised.W/930601 Ltr ML20044G7401993-05-26026 May 1993 LER 93-006-00:on 930419,MSIV Failed to Stroke Closed When Given Close Signal from CR Due to Poppet Sticking.Caused by Insufficient poppet-to-guide Rib Clearance.Stricter Controls Imposed to Control clearances.W/930526 Ltr ML20044F2541993-05-20020 May 1993 LER 93-007-00:on 930420,noted That an Isolation of Inboard & Outboard MSIV & Ms Line Drains Occurred.Caused by Lack of Personnel Knowledge of Unique Maint Conditions.Precaution Will Be Added to Sys Operating procedure.W/930520 Ltr ML20044D8511993-05-17017 May 1993 LER 93-005-00:on 930415,discovered That RCIC Steam Line Flow - High Timer Function Never Performed on Monthly Basis. Caused by Failure to Include Test in Initial Procedure Development Process.Procedures revised.W/930517 Ltr ML20024H2381991-05-21021 May 1991 LER 91-003-01:on 910322,Div II Control Power Circuit Deenergized,Resulting in Deenergization of Charcoal Filter Train Suction Dampers.Caused by Inadequate Work Plan.Plan Revised to Document Restoration of wiring.W/910521 Ltr ML20024G7441991-04-22022 April 1991 LER 91-003-00:on 910322,control Bldg Local Air Intake Radiation Monitor Control Power Circuit Deenergized, Resulting in Isolation of air-operated Dampers.Caused by Inadequate Work Plan.Work Plan revised.W/910422 Ltr ML20024G7181991-04-19019 April 1991 LER 91-004-00:on 910321,RCIC Turbine Main Steam Supply Line Outboard Containment Isolation Valve Isolated.Caused by Negative Trip Setpoint of Trip Unit Being Reached.Caution Added to RCIC Sys Operating procedures.W/910419 Ltr ML20029C1211991-03-14014 March 1991 LER 91-001-00:on 910212,use of Inadequate Control Room Filter Initiation Signal Due to Discrepancies Between Logic Diagrams.Main Control Room Doses Due to MSLB Outside Containment recalculated.W/910314 Ltr ML20029B1341991-02-26026 February 1991 LER 90-033-01:on 901104,RWCU Sys Isolation Occurred While Performing Plant Mod to Power Supply Wiring in Control Room Panel 1H13-P642.Caused by Removal of Terminal Screw.Power Supply reterminated.W/910226 Ltr ML20028H3961990-12-18018 December 1990 LER 90-032-01:on 901021,discovered That Five Snubbers Removed from Standby Svc Water Sys Piping in Violation of Tech Spec 3.7.4.Caused by Scheduling Error & Inadequate Review.Training Will Be Completed on 910331.W/901218 Ltr ML20024F7481990-12-10010 December 1990 LER 90-040-00:on 901110,technician Inadvertently Shorted Relay Terminals,Energizing Relay & Causing Emergency Diesel Generator to Start Unexpectedly.Caused by Personnel Error. Generator Manually secured.W/901210 Ltr ML20044B1951990-07-12012 July 1990 LER 90-003-01:on 900206 to 08,deficiencies Found in thermo-lag Fire Barrier Envelopes Redundant Safe Shutdown Circuits.Fire Watch Established.Util Working W/Vendor to Resolve discrepancies.W/900712 Ltr ML20044A3781990-06-22022 June 1990 LER 90-023-00:on 900523,discovered That Annulus Ventilation Radiation monitor,1RMS*RE11A Inoperable.Caused by Failure of Radiation Monitor Sample Pump & Failure of Switch to Actuate.Flow Switches replaced.W/900622 Ltr ML20043F4721990-06-0808 June 1990 LER 90-021-00:on 900509,RWCU Sys Differential Flow High Trip Instrumentation Inoperable for Period Greater than Allowed by Tech Spec.Caused by Misinterpretation of Tech Spec 3/4.3.2,Table 3.3.2.-1.4.Personnel retrained.W/900608 Ltr ML20043D5831990-06-0101 June 1990 LER 90-020-00:on 900504,radwaste Operator Entered High Radiation Area W/O Dose Rate Meter,Alarming Dosimeter or Radiation Protection Technician Coverage.Caused by Personnel Error.Training Provided to operators.W/900601 Ltr ML20043B8031990-05-24024 May 1990 LER 90-019-00:on 900425,RWCU Sys Isolation & ESF Actuation Occurred After Completion of Channel Check of Riley Temp Trip Unit.Caused by Unit Exceeding Differential Temp Setpoint of 46 F.Unit replaced.W/900524 Ltr ML20043B3301990-05-21021 May 1990 LER 90-017-00:on 900419,inadequate Fire Barrier in Shake Space Occurred Contrary to Tech Spec.Caused by Oversight. Roving Fire Watch Scheduled.Maint Will Rework Voids & Install Seismic Gap seal.W/900521 Ltr ML20043C0281990-05-19019 May 1990 LER 90-018-00:on 900420,ESF Actuation Occurred Causing Reactor Water Sample Containment Isolation Valve to Close. Caused by Failure of Fuse Which Deenergized Isolation Logic of Valves.Fuse replaced.W/900518 Ltr ML20042G7981990-05-10010 May 1990 LER 90-016-00:on 900414,insulator Fault on Local Grid Resulted in Trip of 500 Kv Breaker.Caused by Spurious Alarm Signal from Control Room Local Intake Radiation Monitor 1RMS*RE13B.Sys Returned to Normal operation.W/900510 Ltr ML20042G8001990-05-0909 May 1990 LER 90-015-00:on 900409,loss of Div II Reactor Protection Sys Bus Occurred Due to Trip of Electrical Protection Assembly.Another Trip Also Occurred on 900415.Caused by Faulty Integrated Circuit logics.W/900509 Ltr ML20042G4501990-05-0707 May 1990 LER 90-013-00:on 900405,discovered That Control Bldg Chiller Motor Current Limiter C Set Incorrectly at 56% Instead of 100%.Caused by Incorrect Setting & Maint Activities.Loop Calibr Data Sheet revised.W/900507 Ltr ML20042G4531990-05-0707 May 1990 LER 90-014-00:on 900407,reactor Scram Occurred While Testing Main Turbine Combined Intermediate Valves.Caused by Low Pressure Signal from Emergency Trip Sys of Electrohydraulic Control Sys.Two Solenoid Valves replaced.W/900507 Ltr ML20042F4731990-05-0101 May 1990 LER 90-012-00:on 900401,ESF Actuations Occurred Due to Electrical Protection Assembly Breakers Trip.Caused by Voltage Regulator Failure.Replacement Voltage Regulator Card Installed in MG 1C71-S001B.W/900501 Ltr ML20042E2231990-04-0909 April 1990 LER 90-007-00:on 900311,control Bldg Ventilation Sys Isolated & Filtration Unit Initiated.Caused by Severe Electrical Transient.Performance of Radiation Monitors Improved Prior to Implementation of procedures.W/900409 Ltr ML20012C0741990-03-12012 March 1990 LER 90-004-00:on 900211,Div II Emergency 125-volt Dc Bus Experienced Voltage Spike,Causing Topaz Inverter to Trip & Resulting in Loss of Power to Control Room Panel.Cause Unknown.Setpoint Changes Being evaluated.W/900312 Ltr ML20012C4191990-03-0808 March 1990 LER 90-003-00:on 900206,found That Several Minor Deficiencies Existed in thermo-lag Fire Barrier Envelopes Redundant Safe Shutdown Circuits.Util Currently Working W/ Vendor to Resolve Identified discrepancies.W/900308 Ltr ML20011E2491990-01-31031 January 1990 LER 88-018-04:on 880825,reactor Scram Occurred Due to Main Generator Exciter Brush Failure.Preventive Maint Procedure Revised to Establish Specific Wear Criteria at Which Brushes to Be replaced.W/900131 Ltr ML20011E2461990-01-31031 January 1990 LER 89-036-01:on 891007,discovered That Various motor- Operated Valves Energized,Contrary to Assumptions Contained in Plant Fire Hazards Analysis.Cause Not Stated.Operations Initiated Required Fire Watches on valves.W/900131 Ltr ML20011E1191990-01-30030 January 1990 LER 90-001-00:on 900103,isolation of RCIC Steam Supply Inboard Isolation Valve Occurred During Surveillance Testing of RCIC Sys.Caused by Technician Lifting Wrong Lead,Causing ESF Actuation.Lead Relanded on terminal.W/900130 Ltr ML20011E1181990-01-30030 January 1990 LER 89-033-01:on 890916,loss of Power to Div II 120-volt Ac Distribution Panel Caused auto-start of Standby Gas Treatment & Annulus Mixing Sys,Resulting in ESF Actuations. Caused by Transformer Failure.Valves opened.W/900130 Ltr ML20005G1641990-01-10010 January 1990 LER 89-044-00:on 891211,unplanned ESF Actuation Occurred, Resulting in Isolation of Rcic.Caused by Technician Failing to Perform Steps of Surveillance Test Procedure in Sequence.Div II Isolation Signal reset.W/900110 Ltr ML20005G1661990-01-10010 January 1990 LER 89-045-00:on 891212,Div I Standby Svc Water Pumps Received Automatic Start Signal Due to Spurious Low Svc Water Pressure Signal When Normal Svc Water Pump Secured. Signal Cleared & Sys Restored to Normal lineup.W/900110 Ltr ML20005E8521990-01-0202 January 1990 LER 89-043-00:on 891201.two Outboard MSIVs Inoperable Due to Failure of Corresponding Fast Closure solenoid-operated Valve.Caused by Incomplete Removal of Silicone Lubricant. Lubricant Removed by Application of Acetone.W/900102 Ltr ML20005E8511990-01-0202 January 1990 LER 89-042-01:on 891201,main Turbine Generator Tripped, Resulting in Reactor Scram.Caused by Sensing Fault on Offsite 230 Kv Line.Sys Maint Procedure Being Revised to Include Test of Failed Portion of relay.W/900102 Ltr ML20005E1381989-12-26026 December 1989 LER 89-041-00:on 891125,unplanned ESF Actuation Occurred as Result of Two Leads Shorted Together During Testing of Control Circuitry,Causing Valve Isolation from Suppression Pool.Sys Lineup Restored to Normal position.W/891226 Ltr ML20011D6201989-12-18018 December 1989 LER 89-040-00:on 891117,surveillance Test of Div II Penetration Valve Leakage Control Sys Air Supply Header Pressure Not Performed within Allowable Tolerance.Addl Training of Scheduling Group Will Be provided.W/891218 Ltr ML20011D1371989-12-14014 December 1989 LER 89-039-00:on 891114,discovered That Required post-maint Overall Leak Rate Test on Upper Containment Airlock Not Performed After Replacement of Inflatable Seal.Caused by Personnel Error.Maint Procedure revised.W/891214 Ltr 1994-05-13
[Table view] Category:RO)
MONTHYEARML20024J3201994-10-0707 October 1994 LER 94-022-00:on 940907,TS Violation Occurred Due to Inadequate Fire Watch.Retrained Personnel Associated W/ Painting activities.W/941007 Ltr ML20029E2001994-05-13013 May 1994 LER 94-006-00:on 940414,SS Recognized That Required Frequency for Performing STP 057-3705 Had Been Exceeded. Caused by Inadequate Supervisory Methods.Corrective Action: Inhouse Tracking Process Will Be created.W/940513 Ltr ML20029C8741994-04-26026 April 1994 LER 93-026-01:on 931117,isolation of RCIC Sys Occurred Due to Apparent Failure of Relay.Three Relays Associated W/ Isolation Replaced & Shipped to Mfg for Failure Analysis.W/ 940426 Ltr ML20029C7021994-04-19019 April 1994 LER 90-003-05:on 900206,discovered Deficiencies in Thermo-Lag Fire Barrier Envelope Around Redundant Safe Shutdown.Firewatches Established in Areas Where Thermo Lag Used as barrier.W/940419 Ltr ML20046C3891993-08-0202 August 1993 LER 93-014-00:on 930701,installed Sprinkler Sys as Substitute for Passive fire-rated Barrier Due to Deficiency Identified in Fire Barrier Separation Requirements.Declared Fire Barriers Surrounding Valves degraded.W/930802 Ltr ML20046B8981993-07-29029 July 1993 LER 93-013-00:on 930629,high Pressure Core Spray Pump Failed to Start & Run During Surveillance Test Due to Failed Overfrequency Relay.Relay Tested & Installed in Switchgear. W/930729 Ltr ML20046A2361993-07-22022 July 1993 LER 93-008-01:on 930429,relief Request Improperly Prepared for Insvc Testing Program Results in Noncompliance W/Main Steam Isolation Valve Testing Requirement.Caused by Personnel Error.Testing Frequency Revised ML20045G6111993-07-0202 July 1993 LER 93-012-00:on 930603,deficiency in Plant Surveillance Test Procedures Identified.Caused by Primary Causal Factor Inattention to Detail During Initial Procedure Development Process.Surveillance Test Procedures performed.W/930702 Ltr ML20045D6991993-06-21021 June 1993 LER 93-011-00:on 930521,determined That Mode Switch Placed in Refuel Position During Testing of Switch Interlock Functions.Caused by Conflicting Info in Surveillance Procedures.Operating Procedure revised.W/930621 Ltr ML20045C0141993-06-14014 June 1993 LER 93-010-00:on 930514,SDC Lost for Approx Three Minutes When One SDC Suction Valve Closed Due to Initiation of Spurious ESF Actuation Signal.Caused by Personnel Error. Procedural Guidance revised.W/930614 Ltr ML20045C0021993-06-14014 June 1993 LER 93-003-01:on 930225,incidents Discovered Which Caused Interlock Mechanism in Upper Containment Airlocks at Elevation 171 to Operate Improperly.Case Study Training Class Developed for Airlock incidents.W/930614 Ltr ML20045A1461993-06-0404 June 1993 LER 93-009-00:on 930504,discovered That Surveillance Test Procedure for Control Bldg Chilled Water Sys Quarterly Pump Missed Due to Cognitive Personnel Error.Administrative Procedure Will Be revised.W/930604 Ltr ML20045A4261993-06-0101 June 1993 LER 93-002-02:on 930212,discovered That TS SRs Not Properly Implemented in Logic Sys Functional Tests Due to Inattention to Detail While Preparing Revs of Relevant Surveillance Test Procedures (Stp).Relevant STPs revised.W/930601 Ltr ML20044H3571993-06-0101 June 1993 LER 93-008-00:on 930429,investigation Determined That Relief Request for Inservice Testing of Pumps & Valves in Conflict W/Msiv Testing Requirements.Caused by Personnel Error.Relief Request 40 revised.W/930601 Ltr ML20044G7401993-05-26026 May 1993 LER 93-006-00:on 930419,MSIV Failed to Stroke Closed When Given Close Signal from CR Due to Poppet Sticking.Caused by Insufficient poppet-to-guide Rib Clearance.Stricter Controls Imposed to Control clearances.W/930526 Ltr ML20044F2541993-05-20020 May 1993 LER 93-007-00:on 930420,noted That an Isolation of Inboard & Outboard MSIV & Ms Line Drains Occurred.Caused by Lack of Personnel Knowledge of Unique Maint Conditions.Precaution Will Be Added to Sys Operating procedure.W/930520 Ltr ML20044D8511993-05-17017 May 1993 LER 93-005-00:on 930415,discovered That RCIC Steam Line Flow - High Timer Function Never Performed on Monthly Basis. Caused by Failure to Include Test in Initial Procedure Development Process.Procedures revised.W/930517 Ltr ML20024H2381991-05-21021 May 1991 LER 91-003-01:on 910322,Div II Control Power Circuit Deenergized,Resulting in Deenergization of Charcoal Filter Train Suction Dampers.Caused by Inadequate Work Plan.Plan Revised to Document Restoration of wiring.W/910521 Ltr ML20024G7441991-04-22022 April 1991 LER 91-003-00:on 910322,control Bldg Local Air Intake Radiation Monitor Control Power Circuit Deenergized, Resulting in Isolation of air-operated Dampers.Caused by Inadequate Work Plan.Work Plan revised.W/910422 Ltr ML20024G7181991-04-19019 April 1991 LER 91-004-00:on 910321,RCIC Turbine Main Steam Supply Line Outboard Containment Isolation Valve Isolated.Caused by Negative Trip Setpoint of Trip Unit Being Reached.Caution Added to RCIC Sys Operating procedures.W/910419 Ltr ML20029C1211991-03-14014 March 1991 LER 91-001-00:on 910212,use of Inadequate Control Room Filter Initiation Signal Due to Discrepancies Between Logic Diagrams.Main Control Room Doses Due to MSLB Outside Containment recalculated.W/910314 Ltr ML20029B1341991-02-26026 February 1991 LER 90-033-01:on 901104,RWCU Sys Isolation Occurred While Performing Plant Mod to Power Supply Wiring in Control Room Panel 1H13-P642.Caused by Removal of Terminal Screw.Power Supply reterminated.W/910226 Ltr ML20028H3961990-12-18018 December 1990 LER 90-032-01:on 901021,discovered That Five Snubbers Removed from Standby Svc Water Sys Piping in Violation of Tech Spec 3.7.4.Caused by Scheduling Error & Inadequate Review.Training Will Be Completed on 910331.W/901218 Ltr ML20024F7481990-12-10010 December 1990 LER 90-040-00:on 901110,technician Inadvertently Shorted Relay Terminals,Energizing Relay & Causing Emergency Diesel Generator to Start Unexpectedly.Caused by Personnel Error. Generator Manually secured.W/901210 Ltr ML20044B1951990-07-12012 July 1990 LER 90-003-01:on 900206 to 08,deficiencies Found in thermo-lag Fire Barrier Envelopes Redundant Safe Shutdown Circuits.Fire Watch Established.Util Working W/Vendor to Resolve discrepancies.W/900712 Ltr ML20044A3781990-06-22022 June 1990 LER 90-023-00:on 900523,discovered That Annulus Ventilation Radiation monitor,1RMS*RE11A Inoperable.Caused by Failure of Radiation Monitor Sample Pump & Failure of Switch to Actuate.Flow Switches replaced.W/900622 Ltr ML20043F4721990-06-0808 June 1990 LER 90-021-00:on 900509,RWCU Sys Differential Flow High Trip Instrumentation Inoperable for Period Greater than Allowed by Tech Spec.Caused by Misinterpretation of Tech Spec 3/4.3.2,Table 3.3.2.-1.4.Personnel retrained.W/900608 Ltr ML20043D5831990-06-0101 June 1990 LER 90-020-00:on 900504,radwaste Operator Entered High Radiation Area W/O Dose Rate Meter,Alarming Dosimeter or Radiation Protection Technician Coverage.Caused by Personnel Error.Training Provided to operators.W/900601 Ltr ML20043B8031990-05-24024 May 1990 LER 90-019-00:on 900425,RWCU Sys Isolation & ESF Actuation Occurred After Completion of Channel Check of Riley Temp Trip Unit.Caused by Unit Exceeding Differential Temp Setpoint of 46 F.Unit replaced.W/900524 Ltr ML20043B3301990-05-21021 May 1990 LER 90-017-00:on 900419,inadequate Fire Barrier in Shake Space Occurred Contrary to Tech Spec.Caused by Oversight. Roving Fire Watch Scheduled.Maint Will Rework Voids & Install Seismic Gap seal.W/900521 Ltr ML20043C0281990-05-19019 May 1990 LER 90-018-00:on 900420,ESF Actuation Occurred Causing Reactor Water Sample Containment Isolation Valve to Close. Caused by Failure of Fuse Which Deenergized Isolation Logic of Valves.Fuse replaced.W/900518 Ltr ML20042G7981990-05-10010 May 1990 LER 90-016-00:on 900414,insulator Fault on Local Grid Resulted in Trip of 500 Kv Breaker.Caused by Spurious Alarm Signal from Control Room Local Intake Radiation Monitor 1RMS*RE13B.Sys Returned to Normal operation.W/900510 Ltr ML20042G8001990-05-0909 May 1990 LER 90-015-00:on 900409,loss of Div II Reactor Protection Sys Bus Occurred Due to Trip of Electrical Protection Assembly.Another Trip Also Occurred on 900415.Caused by Faulty Integrated Circuit logics.W/900509 Ltr ML20042G4501990-05-0707 May 1990 LER 90-013-00:on 900405,discovered That Control Bldg Chiller Motor Current Limiter C Set Incorrectly at 56% Instead of 100%.Caused by Incorrect Setting & Maint Activities.Loop Calibr Data Sheet revised.W/900507 Ltr ML20042G4531990-05-0707 May 1990 LER 90-014-00:on 900407,reactor Scram Occurred While Testing Main Turbine Combined Intermediate Valves.Caused by Low Pressure Signal from Emergency Trip Sys of Electrohydraulic Control Sys.Two Solenoid Valves replaced.W/900507 Ltr ML20042F4731990-05-0101 May 1990 LER 90-012-00:on 900401,ESF Actuations Occurred Due to Electrical Protection Assembly Breakers Trip.Caused by Voltage Regulator Failure.Replacement Voltage Regulator Card Installed in MG 1C71-S001B.W/900501 Ltr ML20042E2231990-04-0909 April 1990 LER 90-007-00:on 900311,control Bldg Ventilation Sys Isolated & Filtration Unit Initiated.Caused by Severe Electrical Transient.Performance of Radiation Monitors Improved Prior to Implementation of procedures.W/900409 Ltr ML20012C0741990-03-12012 March 1990 LER 90-004-00:on 900211,Div II Emergency 125-volt Dc Bus Experienced Voltage Spike,Causing Topaz Inverter to Trip & Resulting in Loss of Power to Control Room Panel.Cause Unknown.Setpoint Changes Being evaluated.W/900312 Ltr ML20012C4191990-03-0808 March 1990 LER 90-003-00:on 900206,found That Several Minor Deficiencies Existed in thermo-lag Fire Barrier Envelopes Redundant Safe Shutdown Circuits.Util Currently Working W/ Vendor to Resolve Identified discrepancies.W/900308 Ltr ML20011E2491990-01-31031 January 1990 LER 88-018-04:on 880825,reactor Scram Occurred Due to Main Generator Exciter Brush Failure.Preventive Maint Procedure Revised to Establish Specific Wear Criteria at Which Brushes to Be replaced.W/900131 Ltr ML20011E2461990-01-31031 January 1990 LER 89-036-01:on 891007,discovered That Various motor- Operated Valves Energized,Contrary to Assumptions Contained in Plant Fire Hazards Analysis.Cause Not Stated.Operations Initiated Required Fire Watches on valves.W/900131 Ltr ML20011E1191990-01-30030 January 1990 LER 90-001-00:on 900103,isolation of RCIC Steam Supply Inboard Isolation Valve Occurred During Surveillance Testing of RCIC Sys.Caused by Technician Lifting Wrong Lead,Causing ESF Actuation.Lead Relanded on terminal.W/900130 Ltr ML20011E1181990-01-30030 January 1990 LER 89-033-01:on 890916,loss of Power to Div II 120-volt Ac Distribution Panel Caused auto-start of Standby Gas Treatment & Annulus Mixing Sys,Resulting in ESF Actuations. Caused by Transformer Failure.Valves opened.W/900130 Ltr ML20005G1641990-01-10010 January 1990 LER 89-044-00:on 891211,unplanned ESF Actuation Occurred, Resulting in Isolation of Rcic.Caused by Technician Failing to Perform Steps of Surveillance Test Procedure in Sequence.Div II Isolation Signal reset.W/900110 Ltr ML20005G1661990-01-10010 January 1990 LER 89-045-00:on 891212,Div I Standby Svc Water Pumps Received Automatic Start Signal Due to Spurious Low Svc Water Pressure Signal When Normal Svc Water Pump Secured. Signal Cleared & Sys Restored to Normal lineup.W/900110 Ltr ML20005E8521990-01-0202 January 1990 LER 89-043-00:on 891201.two Outboard MSIVs Inoperable Due to Failure of Corresponding Fast Closure solenoid-operated Valve.Caused by Incomplete Removal of Silicone Lubricant. Lubricant Removed by Application of Acetone.W/900102 Ltr ML20005E8511990-01-0202 January 1990 LER 89-042-01:on 891201,main Turbine Generator Tripped, Resulting in Reactor Scram.Caused by Sensing Fault on Offsite 230 Kv Line.Sys Maint Procedure Being Revised to Include Test of Failed Portion of relay.W/900102 Ltr ML20005E1381989-12-26026 December 1989 LER 89-041-00:on 891125,unplanned ESF Actuation Occurred as Result of Two Leads Shorted Together During Testing of Control Circuitry,Causing Valve Isolation from Suppression Pool.Sys Lineup Restored to Normal position.W/891226 Ltr ML20011D6201989-12-18018 December 1989 LER 89-040-00:on 891117,surveillance Test of Div II Penetration Valve Leakage Control Sys Air Supply Header Pressure Not Performed within Allowable Tolerance.Addl Training of Scheduling Group Will Be provided.W/891218 Ltr ML20011D1371989-12-14014 December 1989 LER 89-039-00:on 891114,discovered That Required post-maint Overall Leak Rate Test on Upper Containment Airlock Not Performed After Replacement of Inflatable Seal.Caused by Personnel Error.Maint Procedure revised.W/891214 Ltr 1994-05-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARRBG-45144, Monthly Operating Rept for Sept 1999 for River Bend Station. with1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for River Bend Station. with ML20216G1201999-09-0909 September 1999 Rev 3 to Rbs,Cycle 9 Colr RBG-45110, Monthly Operating Rept for Aug 1999 for River Bend Station, Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for River Bend Station, Unit 1.With RBG-45087, Special Rept:On 990510,LPCI a & LPCS Injected Into Rv for Less than Two Minutes.Caused by Electrical Transient in One of ECCS Power Supplies.Operators Verified Reactor Cavity Level & Closed Injection Valves to Stop Injection1999-08-0606 August 1999 Special Rept:On 990510,LPCI a & LPCS Injected Into Rv for Less than Two Minutes.Caused by Electrical Transient in One of ECCS Power Supplies.Operators Verified Reactor Cavity Level & Closed Injection Valves to Stop Injection ML20210K4721999-08-0303 August 1999 SER Accepting Licensee 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves RBG-45091, Monthly Operating Rept for July 1999 for River Bend Station, Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for River Bend Station, Unit 1.With ML20210C6391999-07-0202 July 1999 Rev 2 to River Bend Station,Cycle 9 Colr RBG-45055, Monthly Operating Rept for June 1999 for River Bend Station, Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for River Bend Station, Unit 1.With ML20196J8031999-06-24024 June 1999 Rev 1 to Rbs,Cycle 9 Colr RBG-45028, Monthly Operating Rept for May 1999 for River Bend Station, Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for River Bend Station, Unit 1.With RBG-45016, Monthly Operating Rept for Apr 1999 for River Bend Station, Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for River Bend Station, Unit 1.With ML20206A2111999-04-21021 April 1999 Safety Evaluation Authorizing Pump Relief Request PRR-001 & Valve Relief Request VRR-001 & Denying Valve Relief Request VRR-002 RBG-44969, Monthly Operating Rept for Mar 1999 for River Bend Station, Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for River Bend Station, Unit 1.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205D5481999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Exam Weld AA with Weld Volume Coverage of 62 Percent for First 10-year Insp Interval Pursuant to 10CFR50.55a(a)(3)(ii) & 10CFR50.55a(g)(6)(ii)(A)(5) RBG-44930, Monthly Operating Rept for Feb 1999 for River Bend Station, Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for River Bend Station, Unit 1.With RBG-44826, Monthly Operating Rept for Dec 1998 for River Bend Station Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for River Bend Station Unit 1.With ML20198K2701998-12-22022 December 1998 Rev 1 to RBS Cycle 8 Colr RBG-44773, Monthly Operating Rept for Nov 1998 for River Bend Station, Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for River Bend Station, Unit 1.With RBG-44727, LER 98-S01-00:on 981021,identified That Contract Employee with Temporary Access Authorization Failed to Disclose Complete Criminal & Employment History.Individual Denied Access to Plants for Five Years.With1998-11-17017 November 1998 LER 98-S01-00:on 981021,identified That Contract Employee with Temporary Access Authorization Failed to Disclose Complete Criminal & Employment History.Individual Denied Access to Plants for Five Years.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program ML20155H3491998-11-0303 November 1998 Safety Evaluation Granting Requests for Relief RR2-0001, RR2-0002 & RR2-0003 RBG-44719, Monthly Operating Rept for Oct 1998 for River Bend Station, Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for River Bend Station, Unit 1.With ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual RBG-44677, Monthly Operating Rept for Sept 1998 for River Bend Station, Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for River Bend Station, Unit 1.With ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods ML20151S5421998-09-0303 September 1998 Safety Evaluation Opposing Licensee Thermal Model as Currently Implemented.Evaluation Recommended to Be Used in Any follow-up Site Insp RBG-44629, Monthly Operating Rept for Aug 1998 for River Bend Station, Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for River Bend Station, Unit 1.With ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed RBG-44600, Monthly Operating Rept for July 1998 for River Bend Station1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for River Bend Station RBG-44564, Monthly Operating Rept for June 1998 for River Bend Station, Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for River Bend Station, Unit 1 ML20249A6431998-06-12012 June 1998 SER Accepting 980427 Request for Change to River Bend QA Manual Program Description,Per 10CFR50.54(a)(3) RBG-44539, Monthly Operating Rept for May 1998 for River Bend Station, Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for River Bend Station, Unit 1 RBG-44501, Monthly Operating Rept for Apr 1998 for River Bend Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for River Bend Station, Unit 1 ML20217M8951998-04-30030 April 1998 QA Program Manual ML20217P8281998-04-0707 April 1998 Safety Evaluation Accepting Relief Authorization for Alternative to Requirements of ASME Section Xi,Subarticle IWA-5250 Bolting Exam for Plants,Per 10CFR50.55a(a)(3)(i) RBG-44458, Monthly Operating Rept for Mar 1998 for River Bend Station, Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for River Bend Station, Unit 1 RBG-44423, Monthly Operating Rept for Feb 1998 for River Bend Station Unit 11998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for River Bend Station Unit 1 ML20203L6631998-02-11011 February 1998 Rev 0 to River Bend Station,1998 Emergency Preparedness Exercise RBG-44385, Monthly Operating Rept for Jan 1998 for River Bend Station, Unit 11998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for River Bend Station, Unit 1 RBG-44353, Monthly Operating Rept for Dec 1997 for River Bend Station, Unit 11997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for River Bend Station, Unit 1 RBG-44460, Forwards Annual Radiological Environmental Operating Rept, for Period Jan-Dec 19971997-12-31031 December 1997 Forwards Annual Radiological Environmental Operating Rept, for Period Jan-Dec 1997 ML20203H9891997-12-12012 December 1997 Part 21 Rept Re Potential Manufacturing Defect of Enterprise DSR-4 & DSRV-4 Edgs.Cooper Energy Svcs Supplied 1A-7840 Adjusting Screw to Affected Utils & Sites.River Bend Station Replaced W/Acceptable Assemblies ML20202E9941997-12-0101 December 1997 ISI Plan Second Ten-Yr Interval (Dec 1,1997-Nov 30,2007) ML20199K9741997-11-30030 November 1997 Brief Aerial Photography Analysis of RBS at St Francisville,LA:1996-1997 RBG-44337, Monthly Operating Rept for Nov 1997 for River Bend Station, Unit 11997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for River Bend Station, Unit 1 ML20202F0191997-11-28028 November 1997 Safety Evaluation Approving Transfer of License NPF-47 for River Bend Station,Unit 1 ML20199H3711997-11-19019 November 1997 SER Accepting Approving Request Relief from Requirements of Section XI, Rule for Inservice Insp of NPP Components, of ASME for Current or New 10-year Inservice Insp Interval IAW 50.55(a)(3)(i) of 10CFR50 RBG-44295, Monthly Operating Rept for Oct 1997 for River Bend Station Unit 11997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for River Bend Station Unit 1 RBG-44243, LER 97-S03-00:on 970911,contract Employee Was Granted Temporary Access After Failing to List Prior Employment Termination & Access Denial.Caused by Employee Failure to Provide Accurate Info.Updated Info Re Employee1997-10-13013 October 1997 LER 97-S03-00:on 970911,contract Employee Was Granted Temporary Access After Failing to List Prior Employment Termination & Access Denial.Caused by Employee Failure to Provide Accurate Info.Updated Info Re Employee 1999-09-09
[Table view] |
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r ; NVER BEND STAtlCN POST 08FICE BOX 220 S T. FRANCISVILLE, LOUIS 6ANA 70775 it
- ARE A CODE $04 636-6094 346 8t$1
, January 2 ,1990 RBG- 32044' '"
File Nos. G9.5, G9.25.1.3 i
U.S. Nuclear Regulatory Commission
" Document Control. Desk Washington, D.C. 20555' Gentlemen:
River Bend . Station - Unit 1 '
Docket No.*'50-458 -
Please fin'd enclosed Licensee Event' Report No.89-042 for River Bend Station - Unitol. This report;is being submitted pursuant to 10CFR50.73. >
-Sincerely, J. E. Booker s hc) '
Manager-River Bend Oversight River Bend Nuclear Group a.
JEB/TFP/RGW/DCH/DEH /pg cc: U.S. Nuclear Regulatory Commission-611 Ryan Plaza Drive, Suite 1000-Arlington, TX 76011 NRC Resident Inspector P.O. Box 1051 St; Francisville, LA 70775 INP0. Records Center 1100 Circle 75 Parkway Atlanta, GA 30339-3064 :
! 9001110176 900102 /,
l PDR ADOCK 05000458 I S PDC I
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, APPR!VE) OMS C3 31040104 LICENSEE EVENT REPORT (LER) '"a'ata ersi<es
$ACILITY NAast til DOCKET esutet4R (2) PAGE (F TITLE 141 RIVER BEND STATION ol510l0l01415l8 1 lOFl 015 l
R3 actor Scram Due to a Pault on an Offsite Transmission Line EVENT DAf t (5) LIR NUe481R 14) AtPORT DATE 175 OTHER F ACILITitS INVOLvt0 tel l '.
MONTH DAY YEAR YEAR -
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1l2 0l1 8 '9 8l9 0l4l2 l 0l 1 0l 2 9l0 o1 5l0 loio r i i TMiG EPORT 18 AusMITTED PURSUANT TO THE Rh0VIREMENTS Op 10 CP R I Icaece ene e, me,e er eae feito.*,1 till OPE R ATINC "00'
- 1 20 402tel 20 40sto y o0nieH2H i 72 7 ting i
POwsR 20 406teH114) 90 3sieH1) to.73teH211=l 73.711e1
' I 70 ' 0I917 20 40sieH1Ho iO2iHom so nieH2 Hoc OTata ts r ,a e.. mee l 20 405(aH1HsiH S0.734el(2Hi) 50.734eH2 Husi6H A) .f56Al 20 406(eH1 Hest 80.73teH2 Hun go.73(eH21lvenHel 2J 4CHaH1 Het 60.73teH2l0611 60 73(ell 2Hm)
LICENSit CONTACT FOR TH18 LER (12)
NAME f tLteMONE NUMBER ARtAcOOg L. A.' England - Director, Nuclear Licensing 51014 318111-14111415 !
COMPLETE ONE LINE FOR ( ACH COMPONENT F AILUMt Ot3CRISt0 IN TMit REPORT (131 Sy sT E M MA C. R E POR,T A Lt MA C. R T t CAV88 COMPON E NT CAU$t Sv8TE COMPONENT O N' '
j X EA1 i 15 l9 W l1 l2 l0 Y t i i i i i l ! I l l l l l 1 1 I I I I SUPPLEME*'TAL REPORT E XPECTED 1141 lMONTM DAY vtAR SuevisSION 4t$ 119 yes. comore,e Ex9tCTfD SUBMIS$10N OATil kO l l l AssTRACTro,,,,, , m .-e,,e ... ., e , ,s,ee,. .u,,.e .m e ,,,e.,,,,e,, ,,,,e., o .i At 0628 on 12/1/89 with the unit at 97 percent power (Operational Condition 1), the main turbine generator tripped, resulting in a reactor scram. The generator tripped due to the main generator protection breakers tripping as a result of sensing a fault on an offsite 230KV line. The fault failed to clear at the 230KV. switchyard due to a failed relay and slow breaker response time following the signal from a backup relay. t Immediately following the generator trip, the station 4.16KV normal switchgear (INNS-SWG1A) failed to successfully transfer to offsite power. This caused an undervoltage condition which initiated an automatic start of the Division III high pressure core sprav (HPCS) emergency diesel generator. Initiation of the Division III standby service water pump ISWP*P2C also occurred due to a momentary loss of power to the initiating trip units. The Division III emergency diesel generator restored power to the bus per design.
The reactor scram placed the unit in the safe shutdown condition.
Since all safety systems functioned as designed, there was no impact on the safe operation of the plant or to the health and safety of the public as a result of this event.
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l 0 12 M ob Ygst? W ausse ausse a seeisud ser adisennef NAC Fame W W Uh REPORTED CONDITION At 0628 on 12/1/89 with the unit at 97 percent power (Operational Condition 1), the main turbine generator (*TG*) tripped, resulting in a reactor scram. The generator tripped due to the main generator protection breakers tripping as a result of sensing'a fault on an offsite 230KV line. The fault failed to clear at the 230KV switchyard due to a failed relay (*RLY*) and slow breaker response time following the signal from a backup relay.
Immediately following the generator trip, the station 4.16KV normal switchgear_(lNNS-SWGlA) (*SWGR*) failed to successfully transfer to offsite power. This caused an undervoltage condition which initiated an automatic start of the Division III high pressure core spray (HPCS) emergency diesel generator (*DG*). Initiation of standby service water pump ISWP*P2C also occurred due to a momentary loss of power to the Division III initiating trip units. The Division III emergency diesel generator (DG) restored power to the bus per design. Since this event resulted in the actuation of engineered safety features (ESFs) it is hereby reported under 10CFR50.73 (a) (2) (iv) .
INVESTIGATION The investigation that followed the event revealed that the turbine trip was caused by a severed static line on an offsite 230 KV transmission line which caused a phase to ground fault. The fault did not immediately clear due to a failed relay and a slow 230 KV circuit breaker clearing time at the offsite 230 KV switchyard (Fancy Point substation). The slow fault clearing time was sufficient for the 64M relay protecting the main generator to operate and trip circuit breakers 20635 and 20640 at the offsite switchyard isolating the generator from the fault. The initial evaluation for the static line failure indicates a potentially deficient pole ground connection to the static line.
The investigation revealed that the Zone 1 directional distance ground l relay 21GS1 (Westinghouse type SDG relay) failed to operate properly.
l Per design, the Zone 2 (a backup to the Zone 1 relay) directional distance ground relay (21GS2) operated after a 20 cycle delay and simultaneously sent a trip signal to breaker 20745 and initiated a breaker failure timing sequence. The breaker failure relay was energized because breaker 20745 failed to operate within the expected I
time period upon receiving a trip signal from the Zone 2 directional ground relay. The time from the fault initiation to the trip from the l breaker failure backup relay actuation was approximately 31 cycles.
l This was sufficient time for the 64M (*64*) relay for main generator ,
protection to operate and trip breakers 20640 and 20635 to isolate the l unit from the fault. The SDG relay failure was traced to a failed component in a circuit that is only active when the relay is used in a Zone 1 protection application. All remaining SDG relays at the
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l 0 13 OF gg o"Y1 Tit D T O s E chYard in a Zone 1 application have been tested for the failure mode and were found to be functioning properly.
Immediately following the generator trip, the station 4.16KV normal switchgear (INNS-SWG1A & INNS-SWG1B) did not fast transfer to an oftsite power source. This was per design because the voltage was below the transfer permissive value at that time. Switchgear INNS-SWGlB was able to complete a successful slow transfer however, INNS-SWGIA did not. The transfer schemes for INNS-SWGlA&B rely on sufficient voltage levels on the secondary of the station preferred transformers (IRTX-XSRID and 1RTX-XSRIC). When the fault occurred, voltage on the secondary of station preferred transformers 1RTX-XSRIC and 1RTX-XSRID was depressed to 3504 V and per design the 59R (*59*)
relays (undervoltage/overvoltage) on INNS-SWGlA & INNS-SWGlB dropped out. At that time, the auxiliary relays (59RX) operated and removed the permissive for transfer. When the fault cleared, the 59R relay for INNS-SWGlB energized, resetting the 59RX relay for that switchgear thus allowing a slow transfer of INNS-SWGlB. Switchgear INNS-SWG1A did not slow transfer as expected but did manage to complete the transfer in approximately six (6) minutes. Testing of the 59R relay (Westinghouse KV-1) for INNS-SWG1A revealed that it had failed.
Due to the failure of the non-safety related 4.16KV switchgear INNS-SWGlA to transfer (fast and slow) from normal station service transformer ISTX-XNSIC to preferred station service transformer 1RTX-XSRIC, a loss of power to the high pressure core spray (HPCS) safety-related 4.16KV bus 1E22*S004 and the non-safety related 4.16KV bus 1NNS-SWG1C occurred. As a result of the loss of power to the IE22*S004 bus, the HPCS DG received an automatic initiation signal due l to the bus undervoltage condition. The HPCS D/G successfully started
- and its output breaker automatically closed restoring voltage to the bus per design.
- The initiation of standby service water pump, ISWP*P2C, resulted from I a loss of power to the initiating trip units which actuate on low normal service water pressure. The trip units are supplied by a 120VAC/24VDC power supply which is powered from the HPCS 480VAC bus (lE22*S002). Power was restored to the Division III bus via the Division III emergency diesel generator. Upon restoring power to the Division III bus, the trip signal from trip units ISWP*ES21/J,K,L and M sealed in via relay ISWPN18-63. The initiation of ISWP*P2C occurred following the timing out of relay ISWPC08-62-A.
Immediately following the scram, recirculation pump breakers 3A, 4A, 3B and 4B (normal feed) tripped on an end of cycle-recirc pump trip (EOC-RPT) signal followed by the tripping of recirculation pump breakers SA and SB due to electrical interlocks. As a result of receiving a turbine trip at 97 percent power, the reactor vessel experienced a pressure transient. The highest pressure recorded b" the emergency response information system (ERIS) was 1126.8 PSI. Due I onu 3ece e U S GPO1986-0 624 636,466
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ARI and ATWS/RPT initiated. The ARI signal sealed in per design and the ATWS/RPT immediately cleared per design due to pressure being reduced below the trip setpoint. The pressure reduction was a normal design function of 9 relief valves opening (5 low-low set function and 4 additional safety relief. valves (SRVs)). Following the ARI/ATWS initiation, the recirculation pump low speed RPM permissive was met and recirculation pump breakers 2A & 2B closed from the initial EOC-RPT signal, placing the pumps on low speed.
Similar events have been reported in LERs85-063, 86-021, and 86-055.
The failure of the static line was an external factor that played a role in initiating this event. One of the similar events listed above also involved an external factor, a lightning strike as reported in LER 85-063. The remaining two events are similar due to their sequential nature. In both events a transformer fault progressively led to a reactor scram. A brief description of each event is provided below.
. LER 85-063: GSU reported a reactor scram due to a main turbine generator trip on a false main turbine generator power-load imbalance caused by a failed pressure transducer coupled with a lightning strike on a-500 KV transmission line, i l . LER 86-021: GSU reported an event in which a transformer fault l led to a voltage transient in a 13.8 KV switchgear which '
l resulted in a reactor scram and a HPCS injection.
. LER 86-055: GSU reported an event in which a faulted transformer caused a loss of power to the reactor protection system (RPS) A bus concurrent with a failure in the RPS B train backup scram circuitry which resulted in a reactor scram.
l CORRECTIVE ACTION The offsite static line which initiated this event is undergoing repairs. The failed relay in the offsite 230 KV switchyard was ;
replaced and the replacement has been successfully tested. Although the failure of the Westinghouse SDG relay has been determined to be an isolated failure, GSU is revising system maintenance procedures to include a test of the failed portion of the SDG relay circuitry. 1 The failure of the offsite breaker 20745 to operate immediately upon receipt of the signal from the Zone 2 relay has been evaluated.
Subse'quent testing and inspections (internal and external) have revealed no reason for this breaker to function improperly since it passed all of the testing and inspection requirements. Therefore, the circuit breaker has been approved to be returned to service.
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l 0 15 0F 0 15 van . . . . . sea - mu m m The failed relay (59R) which prevented the station normal switchgear from completing a slow transfer was replaced. GSU has initiated a ,
modification (modification request (MR)89-241) to replace the j Westinghouse KV-1 relay with an ITE 59H relay in-the 59R application. I d
All other station applications of this type'of relay were evaluated with none identified in safety related systems. In addition, busses 1NNS-SWGlA and INNS-SWGlB are currently being served from preferred station service transformers 1RTX-XSRIC and 1RTX-XSRID, respectively.
l SAFETY ASSESSMENT There was no impact on the safe operation of the plant or to the health and safety of the public as a result of this event since the !
reactor scram placed the unit in the safe shutdown condition and all safety systems functioned as designed.
NOTE:. Energy Industry Identification System Codes are identified in the text as (
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