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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000458/LER-1998-003, :on 980624,design Error Found on Two of Three Sdgs That Could Potentially Degrade Ability of DGs to Perform Safety Function.Caused of Design Error Unknown.Dg Control Logic Modified to Remove Design Error1999-09-0909 September 1999
- on 980624,design Error Found on Two of Three Sdgs That Could Potentially Degrade Ability of DGs to Perform Safety Function.Caused of Design Error Unknown.Dg Control Logic Modified to Remove Design Error
05000458/LER-1999-008, :on 990418,uplanned Automatic Closure of Div III DG Output Breaker Was Noted Due to Loss of Normal Power to Div III Switchgear During Testing.Caused by Personnel Error.Returned Electrical Lineup to Normal.With1999-05-18018 May 1999
- on 990418,uplanned Automatic Closure of Div III DG Output Breaker Was Noted Due to Loss of Normal Power to Div III Switchgear During Testing.Caused by Personnel Error.Returned Electrical Lineup to Normal.With
05000458/LER-1999-004, :on 990325,automatic Actuation of CIV Due to Inadvertent Water Movement Was Noted.Caused by Failure to Coordinate Separate Activities of Different Workers.Dryer Pool Was Returned to Normal Level.With1999-04-26026 April 1999
- on 990325,automatic Actuation of CIV Due to Inadvertent Water Movement Was Noted.Caused by Failure to Coordinate Separate Activities of Different Workers.Dryer Pool Was Returned to Normal Level.With
05000458/LER-1999-003-03, :on 990324,Division I DG Was Declared Inoperable.Caused by Inadequate Assembly of Fuel Pump.Fuel Pump Coupling Was Repaired & DG Was Returned to Svc1999-04-25025 April 1999
- on 990324,Division I DG Was Declared Inoperable.Caused by Inadequate Assembly of Fuel Pump.Fuel Pump Coupling Was Repaired & DG Was Returned to Svc
05000458/LER-1999-002-02, :on 990204,discovered That Potentially Rendered safety-related Unit Coolers in Primary Containment Inoperable.Cause Being Investigated.Corrective Action Plan Will Be Submitted in Suppl to Ler.With1999-03-0808 March 1999
- on 990204,discovered That Potentially Rendered safety-related Unit Coolers in Primary Containment Inoperable.Cause Being Investigated.Corrective Action Plan Will Be Submitted in Suppl to Ler.With
RBG-44727, LER 98-S01-00:on 981021,identified That Contract Employee with Temporary Access Authorization Failed to Disclose Complete Criminal & Employment History.Individual Denied Access to Plants for Five Years.With1998-11-17017 November 1998 LER 98-S01-00:on 981021,identified That Contract Employee with Temporary Access Authorization Failed to Disclose Complete Criminal & Employment History.Individual Denied Access to Plants for Five Years.With 05000458/LER-1998-004-03, :on 980514,noted That Surveillance Test Had Not Been Completed for Primary Containment Leakage Rate Testing Program.Caused by Lack of Proper Emphasis on Procedure Step Re Summation.Revised Pertinent Surveillance Procedures1998-08-11011 August 1998
- on 980514,noted That Surveillance Test Had Not Been Completed for Primary Containment Leakage Rate Testing Program.Caused by Lack of Proper Emphasis on Procedure Step Re Summation.Revised Pertinent Surveillance Procedures
05000458/LER-1998-003-02, :on 980624,adequacy of Division 1 & 2 DG Control Air Sys Was Noted.Root Cause Analysis Is Being performed.Multi-disciplinary Team Was Formed to Address Immediate & long-term Corrective Actions1998-07-24024 July 1998
- on 980624,adequacy of Division 1 & 2 DG Control Air Sys Was Noted.Root Cause Analysis Is Being performed.Multi-disciplinary Team Was Formed to Address Immediate & long-term Corrective Actions
05000458/LER-1998-002, :on 980425,failure of Two Trains of Annulus Mixing Was Noted.Caused by Problem W/Instantaneous Trip of Setpoint a & B Supply Breakers.Corrected Trip Settings & Replaced B Breaker1998-07-15015 July 1998
- on 980425,failure of Two Trains of Annulus Mixing Was Noted.Caused by Problem W/Instantaneous Trip of Setpoint a & B Supply Breakers.Corrected Trip Settings & Replaced B Breaker
05000458/LER-1998-001, :on 980417,flow Rate Through SGTS Filter Assembly Units Were Found to Be Higher than Design Flow Rate.Caused by Personnel Error.Reviewed & Updated Design & Licensing Basis Documents1998-06-30030 June 1998
- on 980417,flow Rate Through SGTS Filter Assembly Units Were Found to Be Higher than Design Flow Rate.Caused by Personnel Error.Reviewed & Updated Design & Licensing Basis Documents
05000458/LER-1998-002-02, :on 980425,each of Two Trains of Annulus Mixing Sys Failed to Start During Testing Due to Different, Apparently Independent Causes.Eoi Personnel Performing Root Cause Analyses.Breaker Replaced1998-05-26026 May 1998
- on 980425,each of Two Trains of Annulus Mixing Sys Failed to Start During Testing Due to Different, Apparently Independent Causes.Eoi Personnel Performing Root Cause Analyses.Breaker Replaced
05000458/LER-1998-001-04, :on 980417,flow Rate Through SBGTS Filter Assembly Units Was Found to Be Higher than Design Flow Rate. Cause Analysis Is Currently Being Performed.Detailed Evaluation of Sys Ability to Perform Was Done1998-05-18018 May 1998
- on 980417,flow Rate Through SBGTS Filter Assembly Units Was Found to Be Higher than Design Flow Rate. Cause Analysis Is Currently Being Performed.Detailed Evaluation of Sys Ability to Perform Was Done
05000458/LER-1997-010-01, :on 971111,high Pressure Core Spray Minimum Flow Valve Was Discovered in Closed Position.Caused by Air in Transmitter Sensing Lines.Sensing Lines from HPCS Pipe to Flow Transmitter Vented at High Point Vents to Remove Air1997-12-11011 December 1997
- on 971111,high Pressure Core Spray Minimum Flow Valve Was Discovered in Closed Position.Caused by Air in Transmitter Sensing Lines.Sensing Lines from HPCS Pipe to Flow Transmitter Vented at High Point Vents to Remove Air
05000458/LER-1997-009-01, :on 971016,inadequate Pressure Test Performance Was Noted.Caused by Inappropriate Testing Lineups.Llrt Valves,Were Retested Utilizing Revised Test Configurations1997-11-17017 November 1997
- on 971016,inadequate Pressure Test Performance Was Noted.Caused by Inappropriate Testing Lineups.Llrt Valves,Were Retested Utilizing Revised Test Configurations
05000458/LER-1997-008-02, :on 971004,inadvertent Closure of RHR Shutdown Cooling Inboard Isolation Valve Occurred.Caused by Inadequate Administrative Controls,Supervision & Work Practices.Procedures Revised1997-11-0303 November 1997
- on 971004,inadvertent Closure of RHR Shutdown Cooling Inboard Isolation Valve Occurred.Caused by Inadequate Administrative Controls,Supervision & Work Practices.Procedures Revised
05000458/LER-1997-002, :on 970506,through-wall Crack in Weld on RRS Vent Valve Was Noted.Caused by Low Stress,High Cycle Fatigue Induced by Vibration.Valve Replaced Prior to Returning to Power Operations1997-10-27027 October 1997
- on 970506,through-wall Crack in Weld on RRS Vent Valve Was Noted.Caused by Low Stress,High Cycle Fatigue Induced by Vibration.Valve Replaced Prior to Returning to Power Operations
05000458/LER-1997-007-02, :on 970926,discovered Cracked EDG Valve Adjusting Screw Assembly Swivel Pads (Vasasps).Caused by Mfg Defect.Replaced Vasasps in EDGs W/New Components & Returned Defective Vasasps to Vendor for Analysis1997-10-23023 October 1997
- on 970926,discovered Cracked EDG Valve Adjusting Screw Assembly Swivel Pads (Vasasps).Caused by Mfg Defect.Replaced Vasasps in EDGs W/New Components & Returned Defective Vasasps to Vendor for Analysis
05000458/LER-1997-006-01, :on 970913,unplanned Mode Change During Initial Test of New Alternate Decay Heat Removal Function Occurred. Caused by Failure to Ref & Use Time-to-Boil Curves. Procedures Revised1997-10-14014 October 1997
- on 970913,unplanned Mode Change During Initial Test of New Alternate Decay Heat Removal Function Occurred. Caused by Failure to Ref & Use Time-to-Boil Curves. Procedures Revised
RBG-44243, LER 97-S03-00:on 970911,contract Employee Was Granted Temporary Access After Failing to List Prior Employment Termination & Access Denial.Caused by Employee Failure to Provide Accurate Info.Updated Info Re Employee1997-10-13013 October 1997 LER 97-S03-00:on 970911,contract Employee Was Granted Temporary Access After Failing to List Prior Employment Termination & Access Denial.Caused by Employee Failure to Provide Accurate Info.Updated Info Re Employee 05000458/LER-1997-005-02, :on 970822,reactor Scram Occurred Due to Failure of Connector to Electrical Trip Solenoid Valve. Replaced Shorted Connector Prior to Plant start-up1997-09-22022 September 1997
- on 970822,reactor Scram Occurred Due to Failure of Connector to Electrical Trip Solenoid Valve. Replaced Shorted Connector Prior to Plant start-up
RBG-44204, LER 97-S02-00:on 970717,contract Employee Failed to List Prior Employment Termination Due to Positive Drug Test & Was Granted Temporary Access.Caused by Incomplete Info Provided by Licensee.Deleted Employees Key Card1997-09-11011 September 1997 LER 97-S02-00:on 970717,contract Employee Failed to List Prior Employment Termination Due to Positive Drug Test & Was Granted Temporary Access.Caused by Incomplete Info Provided by Licensee.Deleted Employees Key Card RBG-44187, LER 97-S01-00:on 970514,contract Employee Did Not Identify Criminal Background & Was Granted Temporary Access.Caused by Inaccurate & Incomplete Info Provided by Employee.Employees Key Card Was Suspended1997-08-28028 August 1997 LER 97-S01-00:on 970514,contract Employee Did Not Identify Criminal Background & Was Granted Temporary Access.Caused by Inaccurate & Incomplete Info Provided by Employee.Employees Key Card Was Suspended 05000458/LER-1997-004-02, :on 970724,inadequate Surveillance of Division III Battery Occurred Due to Calculation Error.Performed Revised Division III Battery Svc Discharge Test Procedure Using Correct Battery Profile1997-08-25025 August 1997
- on 970724,inadequate Surveillance of Division III Battery Occurred Due to Calculation Error.Performed Revised Division III Battery Svc Discharge Test Procedure Using Correct Battery Profile
05000458/LER-1997-003-05, :on 970722,high Pressure Core Spray Pump Breaker Trip Occurred During Testing.Caused by Failure of a Phase Time Overcurrent Relay.Replaced Failed Relay & Adjusted Contacts on 51-A Relay1997-08-21021 August 1997
- on 970722,high Pressure Core Spray Pump Breaker Trip Occurred During Testing.Caused by Failure of a Phase Time Overcurrent Relay.Replaced Failed Relay & Adjusted Contacts on 51-A Relay
05000458/LER-1997-001-04, :on 970506,manual Reactor Scram on Lowering Vessel Level Occurred.Caused by Cut Cable Event Determined to Be Site Stds,Procedures & Formal Guidance for Breaching Penetrations.Cut Cable Repaired1997-06-0505 June 1997
- on 970506,manual Reactor Scram on Lowering Vessel Level Occurred.Caused by Cut Cable Event Determined to Be Site Stds,Procedures & Formal Guidance for Breaching Penetrations.Cut Cable Repaired
05000458/LER-1997-002-03, :on 970506,small Leak at Inlet of Vent Valve for RRS FCV B.Root Cause Is Undetermined.Valve Was Replaced Prior to Returning to Power Operations1997-06-0404 June 1997
- on 970506,small Leak at Inlet of Vent Valve for RRS FCV B.Root Cause Is Undetermined.Valve Was Replaced Prior to Returning to Power Operations
05000458/LER-1996-007, :on 960214,failure of Containment Airlock Pneumatic Sys Ball Valve Occurred.Caused by Debris Internal to Sys.Inspected,Lubricated & Properly Torqued Ball Valves & Initiated Design Modification1997-06-0404 June 1997
- on 960214,failure of Containment Airlock Pneumatic Sys Ball Valve Occurred.Caused by Debris Internal to Sys.Inspected,Lubricated & Properly Torqued Ball Valves & Initiated Design Modification
05000458/LER-1996-016, :on 960806,control Bldg Chiller Timer Defeat Switch Was Left in Test Position.Caused by Inadequate Turnover During Test Evolution.Switch Was Returned to Normal & Sys Lineup Was Performed1996-12-13013 December 1996
- on 960806,control Bldg Chiller Timer Defeat Switch Was Left in Test Position.Caused by Inadequate Turnover During Test Evolution.Switch Was Returned to Normal & Sys Lineup Was Performed
05000458/LER-1996-015-01, :on 961030,inadvertent Bumping of Recently Installed Power Supply Fuse Resulting in Isolation Valve Closure Occurred.Caused by Risk & Consequences Associated with Depressing.Rcic Isolation Were Identified1996-11-27027 November 1996
- on 961030,inadvertent Bumping of Recently Installed Power Supply Fuse Resulting in Isolation Valve Closure Occurred.Caused by Risk & Consequences Associated with Depressing.Rcic Isolation Were Identified
05000458/LER-1996-010, :on 960429,reactor SLMCPR Value Given in TS Was non-conservative.Caused by Default Passed to Engineer Performing Analysis.Ge Has Calculated Revised SLMCPR & Associated Operating Limit MCPRs1996-10-0404 October 1996
- on 960429,reactor SLMCPR Value Given in TS Was non-conservative.Caused by Default Passed to Engineer Performing Analysis.Ge Has Calculated Revised SLMCPR & Associated Operating Limit MCPRs
05000458/LER-1996-013, :on 960617,Division I RCIC Isolation Occurred Due to Spurious Signal Generated from Failed Trip Unit. Failed Trip Was Replaced & RCIC Sys Was Restored to Operability 9606181996-07-16016 July 1996
- on 960617,Division I RCIC Isolation Occurred Due to Spurious Signal Generated from Failed Trip Unit. Failed Trip Was Replaced & RCIC Sys Was Restored to Operability 960618
05000458/LER-1996-012, :on 960606,manual Reactor Scram Occurred Due to Faulty electro-hydraulic Control Power Supplies.Replaced Power Supplies W/Acceptable Ones1996-07-0303 July 1996
- on 960606,manual Reactor Scram Occurred Due to Faulty electro-hydraulic Control Power Supplies.Replaced Power Supplies W/Acceptable Ones
05000458/LER-1996-011, :on 960516,personnel Error Resulted in Missed Surveillance & Dry Floor Drain Sump Leakage Detection Monitoring Instrumentation Exceeded TS Allowed Outage Times. Appropriate Disciplinary Actions Taken1996-06-17017 June 1996
- on 960516,personnel Error Resulted in Missed Surveillance & Dry Floor Drain Sump Leakage Detection Monitoring Instrumentation Exceeded TS Allowed Outage Times. Appropriate Disciplinary Actions Taken
05000458/LER-1996-008, :on 960214,mispositioned Drywell Pressure Transmitter Isolation Valve Caused Condition Prohibited by Ts.Restored & Verified Position of Other SR Instrumentation Valves1996-04-10010 April 1996
- on 960214,mispositioned Drywell Pressure Transmitter Isolation Valve Caused Condition Prohibited by Ts.Restored & Verified Position of Other SR Instrumentation Valves
05000458/LER-1996-009, :on 960214,DG Overspeed Tripped.Caused by Field Flash Relay Failure.Component Replaced & in-depth Evaluation Performed on Effects of Max Temp in Cabinet1996-03-14014 March 1996
- on 960214,DG Overspeed Tripped.Caused by Field Flash Relay Failure.Component Replaced & in-depth Evaluation Performed on Effects of Max Temp in Cabinet
05000458/LER-1996-006, :on 960118,misinterpretation of Containment isolation-shutdown Requirements Occurred.Caused by Failure to Have Adequately Considered Plant Operating Practices. In-progress Fuel Movement Activities Suspended1996-02-20020 February 1996
- on 960118,misinterpretation of Containment isolation-shutdown Requirements Occurred.Caused by Failure to Have Adequately Considered Plant Operating Practices. In-progress Fuel Movement Activities Suspended
05000458/LER-1996-005, :on 960116,discovered Noncompliance W/License Condition by Inadequate Tagging of Hose & Cabling Due to Mgt Change.Trained Operator & Revised Controlling Procedure1996-02-15015 February 1996
- on 960116,discovered Noncompliance W/License Condition by Inadequate Tagging of Hose & Cabling Due to Mgt Change.Trained Operator & Revised Controlling Procedure
05000458/LER-1996-004, :on 960115,CI of Various BOP Valves Occurred Due to Inattention to Detail.I&C Technician Counseled1996-02-12012 February 1996
- on 960115,CI of Various BOP Valves Occurred Due to Inattention to Detail.I&C Technician Counseled
05000458/LER-1996-003, :on 960113,ESF Actuations Occurred Due to Electrical Protection Assembly Breaker Trip.Electrical Protection Assembly Replaced1996-02-12012 February 1996
- on 960113,ESF Actuations Occurred Due to Electrical Protection Assembly Breaker Trip.Electrical Protection Assembly Replaced
05000458/LER-1996-002, :on 960105,return Piping Weld for RHR Was Missing from Suppression Pool Level.Caused by Lack of Fusion on C Steel Side of Weld.Reassembled Pipe in Sys During Scheduled Maint Period Outage1996-02-0101 February 1996
- on 960105,return Piping Weld for RHR Was Missing from Suppression Pool Level.Caused by Lack of Fusion on C Steel Side of Weld.Reassembled Pipe in Sys During Scheduled Maint Period Outage
05000458/LER-1996-001-01, :on 960104,reactor Manually Scrammed Due to High Turbine Vibration.Due to Tight Clearance Between Low Pressure Turbine B Rotor & Stationary Parts.High Loads/Low Load Valves Being Modified1996-01-31031 January 1996
- on 960104,reactor Manually Scrammed Due to High Turbine Vibration.Due to Tight Clearance Between Low Pressure Turbine B Rotor & Stationary Parts.High Loads/Low Load Valves Being Modified
05000458/LER-1995-013-02, :on 951228,operation Was Outside TS Limits Due to Trip,Maint & Repair of EDG Ii.Repaired Lube Oil Cooler Leak1996-01-30030 January 1996
- on 951228,operation Was Outside TS Limits Due to Trip,Maint & Repair of EDG Ii.Repaired Lube Oil Cooler Leak
05000458/LER-1995-012-01, :on 951219,recirculation Pump Tripped.Caused by Spurious Actuation of Cavitation Interlock.Recirculation Pump Cavitation Loops Recalibrated1996-01-18018 January 1996
- on 951219,recirculation Pump Tripped.Caused by Spurious Actuation of Cavitation Interlock.Recirculation Pump Cavitation Loops Recalibrated
05000458/LER-1995-013-01, :on 951215,RCIC Div 1 Isolation Occurred Due to Failed Transmitter.Faulty Transmitter Replaced1996-01-11011 January 1996
- on 951215,RCIC Div 1 Isolation Occurred Due to Failed Transmitter.Faulty Transmitter Replaced
05000458/LER-1995-010-02, :on 951130,reactor Thermal Power Limit Exceeded Due to Failure to Consider Required Heat Balance Inputs.No Recommended Corrective Actions Since All New Plant Designs Will Be Implemented as Mods1995-12-27027 December 1995
- on 951130,reactor Thermal Power Limit Exceeded Due to Failure to Consider Required Heat Balance Inputs.No Recommended Corrective Actions Since All New Plant Designs Will Be Implemented as Mods
05000458/LER-1995-009-02, :on 951101,surveillance Was Missed Due to Error in Change of Surveillance Test Interval Scheduling.Caused by Human Error & Inadequate Review.Discussed Inappropriate Schedule Frequency Change1995-12-0101 December 1995
- on 951101,surveillance Was Missed Due to Error in Change of Surveillance Test Interval Scheduling.Caused by Human Error & Inadequate Review.Discussed Inappropriate Schedule Frequency Change
05000458/LER-1995-007, :on 950905,HPCS Unit Cooler Fan Hub Failed. Caused by Casting Defect Consisting of High Porosity & Iron Rich Precipitates Along Grain Boundaries.Repaired & Restored HPCS Unit Cooler to Operational Status1995-11-28028 November 1995
- on 950905,HPCS Unit Cooler Fan Hub Failed. Caused by Casting Defect Consisting of High Porosity & Iron Rich Precipitates Along Grain Boundaries.Repaired & Restored HPCS Unit Cooler to Operational Status
05000458/LER-1995-008-02, :on 951024,Div II RCIC Sys Isolated Due to Spurious Trip Caused by Faulty Temp Switch for RCIC Isolation Main Steam Tunnel Ventilation.Compliance W/Ts 3.3.6.1 & 3.5.3 Immediately Established1995-11-20020 November 1995
- on 951024,Div II RCIC Sys Isolated Due to Spurious Trip Caused by Faulty Temp Switch for RCIC Isolation Main Steam Tunnel Ventilation.Compliance W/Ts 3.3.6.1 & 3.5.3 Immediately Established
05000458/LER-1995-007-02, :on 950905,fan Hub for HPCS Pump Room Unit Cooler Failed.Cause Presently Being Investigated.Unit Cooler Repaired & Restored to Operations1995-10-0505 October 1995
- on 950905,fan Hub for HPCS Pump Room Unit Cooler Failed.Cause Presently Being Investigated.Unit Cooler Repaired & Restored to Operations
05000458/LER-1995-006-02, :on 950627,identified Electrical Containment Penetration Overcurrent Protection Device Not Adequately Tested Due to Inadequate Development & Implementation of Historic Mod request.ENG-3-033 Revised1995-07-27027 July 1995
- on 950627,identified Electrical Containment Penetration Overcurrent Protection Device Not Adequately Tested Due to Inadequate Development & Implementation of Historic Mod request.ENG-3-033 Revised
1999-09-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARRBG-45144, Monthly Operating Rept for Sept 1999 for River Bend Station. with1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for River Bend Station. with 05000458/LER-1998-003, :on 980624,design Error Found on Two of Three Sdgs That Could Potentially Degrade Ability of DGs to Perform Safety Function.Caused of Design Error Unknown.Dg Control Logic Modified to Remove Design Error1999-09-0909 September 1999
- on 980624,design Error Found on Two of Three Sdgs That Could Potentially Degrade Ability of DGs to Perform Safety Function.Caused of Design Error Unknown.Dg Control Logic Modified to Remove Design Error
ML20216G1201999-09-0909 September 1999 Rev 3 to Rbs,Cycle 9 Colr RBG-45110, Monthly Operating Rept for Aug 1999 for River Bend Station, Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for River Bend Station, Unit 1.With RBG-45087, Special Rept:On 990510,LPCI a & LPCS Injected Into Rv for Less than Two Minutes.Caused by Electrical Transient in One of ECCS Power Supplies.Operators Verified Reactor Cavity Level & Closed Injection Valves to Stop Injection1999-08-0606 August 1999 Special Rept:On 990510,LPCI a & LPCS Injected Into Rv for Less than Two Minutes.Caused by Electrical Transient in One of ECCS Power Supplies.Operators Verified Reactor Cavity Level & Closed Injection Valves to Stop Injection ML20210K4721999-08-0303 August 1999 SER Accepting Licensee 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves RBG-45091, Monthly Operating Rept for July 1999 for River Bend Station, Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for River Bend Station, Unit 1.With ML20210C6391999-07-0202 July 1999 Rev 2 to River Bend Station,Cycle 9 Colr RBG-45055, Monthly Operating Rept for June 1999 for River Bend Station, Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for River Bend Station, Unit 1.With ML20196J8031999-06-24024 June 1999 Rev 1 to Rbs,Cycle 9 Colr ML20195G1621999-06-11011 June 1999 Safety Evaluation Supporting Amend 107 to License NPF-47 RBG-45028, Monthly Operating Rept for May 1999 for River Bend Station, Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for River Bend Station, Unit 1.With 05000458/LER-1999-008, :on 990418,uplanned Automatic Closure of Div III DG Output Breaker Was Noted Due to Loss of Normal Power to Div III Switchgear During Testing.Caused by Personnel Error.Returned Electrical Lineup to Normal.With1999-05-18018 May 1999
- on 990418,uplanned Automatic Closure of Div III DG Output Breaker Was Noted Due to Loss of Normal Power to Div III Switchgear During Testing.Caused by Personnel Error.Returned Electrical Lineup to Normal.With
ML20206H3141999-05-0505 May 1999 Safety Evaluation Supporting Amend 106 to License NPF-47 RBG-45016, Monthly Operating Rept for Apr 1999 for River Bend Station, Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for River Bend Station, Unit 1.With ML20206D5591999-04-27027 April 1999 Safety Evaluation Supporting Amend 105 to License NPF-47 05000458/LER-1999-004, :on 990325,automatic Actuation of CIV Due to Inadvertent Water Movement Was Noted.Caused by Failure to Coordinate Separate Activities of Different Workers.Dryer Pool Was Returned to Normal Level.With1999-04-26026 April 1999
- on 990325,automatic Actuation of CIV Due to Inadvertent Water Movement Was Noted.Caused by Failure to Coordinate Separate Activities of Different Workers.Dryer Pool Was Returned to Normal Level.With
05000458/LER-1999-003-03, :on 990324,Division I DG Was Declared Inoperable.Caused by Inadequate Assembly of Fuel Pump.Fuel Pump Coupling Was Repaired & DG Was Returned to Svc1999-04-25025 April 1999
- on 990324,Division I DG Was Declared Inoperable.Caused by Inadequate Assembly of Fuel Pump.Fuel Pump Coupling Was Repaired & DG Was Returned to Svc
ML20206A2111999-04-21021 April 1999 Safety Evaluation Authorizing Pump Relief Request PRR-001 & Valve Relief Request VRR-001 & Denying Valve Relief Request VRR-002 ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 RBG-44969, Monthly Operating Rept for Mar 1999 for River Bend Station, Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for River Bend Station, Unit 1.With ML20205D3431999-03-26026 March 1999 Safety Evaluation Supporting Amend 104 to License NPF-47 ML20205D5481999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Exam Weld AA with Weld Volume Coverage of 62 Percent for First 10-year Insp Interval Pursuant to 10CFR50.55a(a)(3)(ii) & 10CFR50.55a(g)(6)(ii)(A)(5) 05000458/LER-1999-002-02, :on 990204,discovered That Potentially Rendered safety-related Unit Coolers in Primary Containment Inoperable.Cause Being Investigated.Corrective Action Plan Will Be Submitted in Suppl to Ler.With1999-03-0808 March 1999
- on 990204,discovered That Potentially Rendered safety-related Unit Coolers in Primary Containment Inoperable.Cause Being Investigated.Corrective Action Plan Will Be Submitted in Suppl to Ler.With
ML20207K2221999-03-0303 March 1999 Safety Evaluation Supporting Amend 103 to License NPF-47 RBG-44930, Monthly Operating Rept for Feb 1999 for River Bend Station, Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for River Bend Station, Unit 1.With ML20202C9751999-01-27027 January 1999 Safety Evaluation Supporting Amend 102 to License NPF-47 RBG-44826, Monthly Operating Rept for Dec 1998 for River Bend Station Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for River Bend Station Unit 1.With ML20198K2701998-12-22022 December 1998 Rev 1 to RBS Cycle 8 Colr RBG-44773, Monthly Operating Rept for Nov 1998 for River Bend Station, Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for River Bend Station, Unit 1.With RBG-44727, LER 98-S01-00:on 981021,identified That Contract Employee with Temporary Access Authorization Failed to Disclose Complete Criminal & Employment History.Individual Denied Access to Plants for Five Years.With1998-11-17017 November 1998 LER 98-S01-00:on 981021,identified That Contract Employee with Temporary Access Authorization Failed to Disclose Complete Criminal & Employment History.Individual Denied Access to Plants for Five Years.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program ML20155H3491998-11-0303 November 1998 Safety Evaluation Granting Requests for Relief RR2-0001, RR2-0002 & RR2-0003 RBG-44719, Monthly Operating Rept for Oct 1998 for River Bend Station, Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for River Bend Station, Unit 1.With ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual RBG-44677, Monthly Operating Rept for Sept 1998 for River Bend Station, Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for River Bend Station, Unit 1.With ML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods ML20151S5421998-09-0303 September 1998 Safety Evaluation Opposing Licensee Thermal Model as Currently Implemented.Evaluation Recommended to Be Used in Any follow-up Site Insp RBG-44629, Monthly Operating Rept for Aug 1998 for River Bend Station, Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for River Bend Station, Unit 1.With 05000458/LER-1998-004-03, :on 980514,noted That Surveillance Test Had Not Been Completed for Primary Containment Leakage Rate Testing Program.Caused by Lack of Proper Emphasis on Procedure Step Re Summation.Revised Pertinent Surveillance Procedures1998-08-11011 August 1998
- on 980514,noted That Surveillance Test Had Not Been Completed for Primary Containment Leakage Rate Testing Program.Caused by Lack of Proper Emphasis on Procedure Step Re Summation.Revised Pertinent Surveillance Procedures
ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed RBG-44600, Monthly Operating Rept for July 1998 for River Bend Station1998-07-31031 July 1998 Monthly Operating Rept for July 1998 for River Bend Station 05000458/LER-1998-003-02, :on 980624,adequacy of Division 1 & 2 DG Control Air Sys Was Noted.Root Cause Analysis Is Being performed.Multi-disciplinary Team Was Formed to Address Immediate & long-term Corrective Actions1998-07-24024 July 1998
- on 980624,adequacy of Division 1 & 2 DG Control Air Sys Was Noted.Root Cause Analysis Is Being performed.Multi-disciplinary Team Was Formed to Address Immediate & long-term Corrective Actions
05000458/LER-1998-002, :on 980425,failure of Two Trains of Annulus Mixing Was Noted.Caused by Problem W/Instantaneous Trip of Setpoint a & B Supply Breakers.Corrected Trip Settings & Replaced B Breaker1998-07-15015 July 1998
- on 980425,failure of Two Trains of Annulus Mixing Was Noted.Caused by Problem W/Instantaneous Trip of Setpoint a & B Supply Breakers.Corrected Trip Settings & Replaced B Breaker
RBG-44564, Monthly Operating Rept for June 1998 for River Bend Station, Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for River Bend Station, Unit 1 05000458/LER-1998-001, :on 980417,flow Rate Through SGTS Filter Assembly Units Were Found to Be Higher than Design Flow Rate.Caused by Personnel Error.Reviewed & Updated Design & Licensing Basis Documents1998-06-30030 June 1998
- on 980417,flow Rate Through SGTS Filter Assembly Units Were Found to Be Higher than Design Flow Rate.Caused by Personnel Error.Reviewed & Updated Design & Licensing Basis Documents
ML20249A6431998-06-12012 June 1998 SER Accepting 980427 Request for Change to River Bend QA Manual Program Description,Per 10CFR50.54(a)(3) RBG-44539, Monthly Operating Rept for May 1998 for River Bend Station, Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for River Bend Station, Unit 1 05000458/LER-1998-002-02, :on 980425,each of Two Trains of Annulus Mixing Sys Failed to Start During Testing Due to Different, Apparently Independent Causes.Eoi Personnel Performing Root Cause Analyses.Breaker Replaced1998-05-26026 May 1998
- on 980425,each of Two Trains of Annulus Mixing Sys Failed to Start During Testing Due to Different, Apparently Independent Causes.Eoi Personnel Performing Root Cause Analyses.Breaker Replaced
05000458/LER-1998-001-04, :on 980417,flow Rate Through SBGTS Filter Assembly Units Was Found to Be Higher than Design Flow Rate. Cause Analysis Is Currently Being Performed.Detailed Evaluation of Sys Ability to Perform Was Done1998-05-18018 May 1998
- on 980417,flow Rate Through SBGTS Filter Assembly Units Was Found to Be Higher than Design Flow Rate. Cause Analysis Is Currently Being Performed.Detailed Evaluation of Sys Ability to Perform Was Done
1999-09-09
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GULF STATES UTILITIES COMPANY NMEFI BEND ST ATION POST Of TICE BOX 220 51 rRANCJSVILLE LOViSLANA 70775 AREA CODE 504 635 fKl94 346 8651 August 2, 1993 RBG-38820 File Nos. G9.5, G9.25.1.3 li U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Gentlemen:
River Bend Station - Unit i Docket No. 50-458 Please find enclosed Licensee Event Report No.93-014 for River Bend Station -
Unit 1. This report is submitted pursuant to 10CFR50.73.
Sincerely, f.
Anbj "J. E. Booker Manager - Safety Assessment and Quality Verification River Bend Nuclear Group JPi #
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JPS/FRC
/ MAS /DC / K 9308100240 930802 f
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ki PDR ADOCK 05000459 S
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U.S.- Nuclear Regulatory Commission 611 Ryan Plaza Drive, Suite 400 Arlington, TX 76011 NRC Resident Inspector i
P.O. Box 1051 St. Francisville, LA 70775 INPO Records Center 700 Galleria Parkway Atlanta, GA 30339-5957 Mr. C.R. Oberg Public Utility Commission of Texas 7800 Shoal Creek Blvd., Suite 400 Nonh Austin, TX 78757 r
Department of Environmental Quality Radiation Protection Division P.O. Box 82135 Baton Rouge, LA 70884-2135 ATTN: Administrator 4
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fdRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104
[
p sm EXPIRES S/31/95 f
EST MATED BURDEN PER RESPONSE TO COMPLY WTH TH:S INFORMAT!ON COLLFCTON REQUE ST: 50.0 HR3 TOFMARD LICENSEE EVENT REPORT (LER)
COMME'FS REGARONG BURDEN EsimTE TO THE M ORMMON AND RECORDS MANAGEMENT E8 RANCH (MNB9 77t4L U L. NUCLEAR REGULATORY COMM:ES!ON. W ASHrNGTON. DC 20E55 0001. AND TO 1
THE PAPERWORA REDUCTON PROJECT 1315crO104), OFFICE OF (See reverse for required number of digits / characters for each block)
MANAGEMENT AND BUDGET, WASHtNGTON, DC 205a3.
FACILITY NAME (1)
DOCKET NUMBER (2).
PAGE (3)
RIVER BEND STATION 05000 4 5 8 1 OF 4 nTu t9 Improper substitution of a sprinkler system for passive lire-rated barrier EVENT DATE (5)
LER NUMBER (61 REPORT NUMBER (7)
OTHER FACILITIES INVOLVED (8)
=
F AQUTY NAME DUGKE I NUMBEH SEQUENTIAL REVtSiON r
MONTH DAY YEAR YEAR "N"
^
E' W MBER NUMBER 05000 i AUUlY NAME DOQTT NUMBER i
07 01 93 93
~ 014
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00 08 02 93 05000 l
OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR O (Check one or morel (11) 7 MODE (9) 1 20 402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)
POWER 20.405(a)(1)(i) 50.36(c)(1) 50 73(a)(2)(v) 73.71(c)
LEVEL (10) 100 20 405(a)(1 Ha) 50.36(c)(2) 50.73(a)(2)(vid OTHER 20 405(a)(1)(m) x 50.73(a)(2)(i) 50.73(a)(2)(viii)(A)
20.405(a)(1)(iv) 50 73(a)(2)(u) 50 73(a)(2)(viii)(B) 4f 20.405(a)(1)(v) 50.73(a)(2)(in) 50.73(a)(2)(x)
LICENSEE CONTACT FoR THIS LER (12)
NAME TELEPHONE NUMBFH mcWo* Area Gude) t D.N.
Lorfing, Supervisor-Nuclear Licensing 504-381-4145 COMPLETE ONE LtNE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTE M COMPONE NT MANUFACTURER
CAUSE
SYSTEM COMDONENT M ANUF ACTURf R pg l
SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONT H DAY YE.AR YEs NEO no pe yes. empire EFECTED SUBM:SQON DATE) x DATE (15)
I ABSTRACT (Limit to 1400 spaces, i e, approximately 15 single-spaced typewntien lines) (16) i On July 1,1993, as pan of a corrective action review of modification requests and associated 10CFR50.59 evaluations, GSU identified a deficiency in fire barrier separation requirements.
Contrary to Branch Technical Position BTP CMEB 9.5-1, a sprinkler. system was installed as a substitute for a passive fire-rated barrier under modification request (MR) 85-0548. From January 10,1989 until a firewatch was established on October 26,1989, compliance with Technical Specification 3.7.7 was not maintained. Therefore, this report is submitted pursuant to 10CFR50.73(a)(2)(i)(b).
Although the installed sprinkler systems are not equivalent to a rated fire barrier the water density provided by the sprinklers furnishes a level of protection sufficient for the fire risk in each fire area.
The hourly firewatch patrols currently in place, provide the proper compensatory action pursuant to Technical Specification 3.7.7 NRC FORM 366 ($ W)
f.-
I REQUIRED NUMBER OF DIGITS / CHARACTERS FOR EACH BLOCK
' 5 r
BLOCK NUMBER OF b
NUMBER DIGITS / CHARACTERS 1
UP TO 46 FACILITY NAME 8 TOTAL
+
DOCKET NUMBER 3 IN ADDITION TO 05000 3
VARIES PAGE NUMBER 4
UP TO 76 TITLE F
6 TOTAL WENT DATE 2 PER BLOCK 7 TOTAL 2 FOR YEAR LER NUMBER 3 FOR SEQUENTIAL NUMBER 2 FOR REVISION NUMBER 6
7 REPORT DATE p pER B CK UP TO 18 - FACILITY NAME 8
ON FACmlES MOWED 8 TOTAL - DOCKET NUMBER 3 IN ADDITION TO 05000 9
1 OPERATING MODE 10 3
POWER LEVEL
'I REQWEMENTS OF 10 UR f
CHECK BOX THAT APPLIES UP TO 50 FOR NAME 12 LICENSEE CONTACT i
14 FOR TELEPHONE 3
CAUSE VARIES 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARIES EMAL REPOM NECMD CHECK BOX THAT APPLIES 15 EXPECTED SUBMISSION DATE 2 PER BLOCK Y
1 l
REQUIRED NUMBER OF DIGITS / CHARACTERS FOR EACH BLOCK BLOCK NUMBER OF NUMBER DIGITS / CHARACTERS 1
UP TO 46 FACILITY NAME 2
DOCE NWBER 3 IN ADDITION TO 05000 3
VARIES PAGE NUMBER 4
UP TO 76 TITLE 5
T DATE 2 PER BLOCK 7 TOTAL FOR YEAR 6
LER NUMBER 3 FOR SEQUENTIAL NUMBER 2 FOR REVISION NUMBER 7
T DATE 2 PER BL CK UP TO 18 - FACILITY NAME 8
OTHER FACmES MOWED 8 TOTAL - DOCKET NUMBER 3 IN ADDITION TO 05000 9
1 OPERATING MODE 10 3
POWER LEVEL REQUIREMENTS OF 10 CFR II CHECK BOX THAT APPLIES W TO 50 FOR NAME 12 UCENSEE CONTACT 14 FOR TELEPHONE CAUSE VARIES 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARIES I#
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CHECK BOXTHAT APPUES EXPECTED SUBMISSION DATE 2 PER BLOCK
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mU.S. NUCLEAR REGULATORY COMMISSION APPROVED BY oMB NO. 3150-0104 is s.2; EXPIRES 5/31/95 -
ESTtMATED BURDEN PER RESPONSE TO COMPLY WITH THrs LICENSEE EVENT REPORT (LER)
EE7s" REG EE*Ros$5 ATE OUid!%c7 TEXT CONTINUATION
- $80JS"*[$$"'w"$0"788"'*fiss"$'$
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THE FAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEVENT AND 9JDGET. WASHINGTON, DC 20503.
FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER te)
PAGE (31 SEQUENT 1A4.
REVGON ygg NUMBER NUMBER 05000 4 5 8 2OF4 RIVER BEND STATION 93 014 -
00 TLX1 pt enore space os reqwrea, use ea$0orns, coores of Mtc wm 3ESA) (17; REPORTED CONDITION On July 1,1993, GSU identified a deficiency in fire barrier separation requirements. Contrary to Branch Technical Position BTP CMEB 9.5-1, a sprinkler system was installed as a substitute for a passive fire-rated barrier under modification request (MR) 85-0548. From January 10,1989 until a firewatch was established on October 26,1989, compliance with Technical Specification 3.7.7 was not maintained. Therefore, this report is submitted pursuant to 10CFR50.73(a)(2)(i)(b).
LNVESTIGATION Modification request (MR) 85-0548 was written to provide a method of protection, other than fire-rated barrier, for three (3) valves required for the River Bend post-fire safe shutdown methodology.
These valves and their locations are as follows :
D-Tunnel (Fire Area AB-7)
E-Tunnel (Fire Area PT-1) lE12*MOVF068B ISWP*MOV501 A ISWP*MOV096B An unreviewed safety question determination (USQD) was performed and the modification was installed under the provisions of 10CFR50.59. As corrective action for problems with the containment airlocks, GSU has reviewed all MRs and associated USQDs (LER 93-003, supplement 1). During this review effort, problems were identified in MR 85-0548 and in its safety evaluation.
The MR states, "...certain sprinkler densities can equilibrate to hourly fire ratings." However, the use of a " water curtain" as a rated fire barrier has not been endorsed by the National Fire Protection Association (NFPA). A deviation to section C.5.b.(2) of Bmnch Technical Position (BTP) CMEB 9.5-1 such as substitution of a " water curtain" for a rated fire barrier is outside the scope of 10CFR50.59.
A " water curtain" is used as a rated barrier between fire areas in two locations at River Bend Station. However, these applications have been approved and documented in Supplement 3 to the SER (Reference Section 9.5.1.6). The substitution of a " water curtain" for a rated barrier for a single piece of equipment required for post-fire safe shutdown was an incorrect interpretation of the limits to which a modification can be implemented without submittal to the NRC for approval.
Therefom, from suspension of hourly firewatches on January 10,1989 until another firewatch was established on October 26,1989 (Reference CR# 90-1144), neither an acceptable fire barrier nor compensatory action was in place for the above listed valves.
NRC FOAM 366A (5 92)
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eU S. NUCLEAR REGULATORY COMMISSION APPROVED BY oMB No. 3150-0104 s ea
^
EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH TH:S LICENSEE EVENT REPORT (LER)
E % 3 Eo'f4'S E RD T $ $ 8 b E rl E $22 TEXT CONTINUATION Eu"7J" S Zu'^$*o;"',87,'a*178d"y;%o3,"fa 3$
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C THE PAPERWORK REDUCTION PROJECT (3tSoo1M), OMICE 05 MANAGEMENT AND BUDGET, WASHINGTON. DC 20503 FACluTV NAME (1)
DOCF ET NUMBER (2)
LER NUMBER (8)
PAGE (3)
LEQsJENTA f4EVSiON NUMBER NUVBER 05000 458 3 OF 4 RIVER BEND STATION 93
- - 014 00 a mi-,av.c..,.n w..-- - eunC - am on ROOT CAUSE A root cause evaluation was performed using the technique of barrier analysis. The results of the root cause analysis are summarized below.
The engineer who performed the design and prepared the safety determination apparently did not recognize the difference between the use of a water cunain as a barrier between two fire areas, and the use of a water curtain as a barrier to achieve separation between redundant components for post-fire safe shutdown (i.e. Section c.5.b.(2) of BTP CMEB 9.5-1). In the USQD pmpared by the engineer, he stated that the function of both Dre barriers and suppression systems is to contain a Dre. Since a water cunain was allowed elsewhere at RBS as a rated Hre barrier, the engineer applied this substitution to redundant components required for post-Bre safe shutdown. This approach reveals an improper understanding of the extent to which an approved deviation (in this case for fire areas) could be expanded to include post-Gre safe shutdown components under the provisions of 10CFR50.59 and NSAC 125 guidance. Use of a water curtain as a barrier to achieve separation between redundant safe shutdown components requires NRC approval as a deviation from BTP CMEB 9.5-1.
A review of previous LERs revealed none similar.
CORRECTIVE ACTION
Upon discovery of the reponed condition, the fire barriers surrounding the valves in question were declared to be degraded and the identifying condition report was added to the limiting condition for operation (LCO) mquiring hourly firewatches for both fire areas (LCO 93-180). The sprinklers installed appear to be designed in accordance with Standard NFPA 13, " Installation of Sprinkler Systems", Section 5-3.7. However, NFPA 13 does not recognize the use of water spray'as a means to protect a speci6c piece of equipment. A deviation request to BTP CMEB 9.5-1, section C.5.(b).2 will be submitted te d.. "nc far review by November 1,1993.
Intensive training in the prepamtion and review of 10CFR50.59 evaluations has been provided for all engineers within the last year. Engineering supervision has repeatedly emphasized the use of
. NSAC 125 guidance during preparation of USQDs. GSU's increased emphasis on attention to detail j
and technical accuracy of 10CFR50.59 evaluations provides a high level of confidence that this error i
will not be n:peated in the future. In addition, GSU's intensive review of previous 10CFR50.59 evaluations provides confidence that this is the only case of its kind.
NRC FORM St 44 @ 92)
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NRC f ORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (5 ea EXPIRES 5/31/95 ESTtMATED BURDEN PER RESPONSE TO COMPLY WCTH TH:S INFORMATON COLLECTON REQUEST: 50.0 HR5 FORWARD LICENSEE EVENT REPORT (LER)
COMuEN s nEGARo,No BuRoEN ESTiuATE TO THE iNrORMiriON TE CONTI UATa y AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U,$. NUCLEAR REGULATORY COMMIS$CN. WASHINGTON, DC 20S55-0001. AND TO 8
8' THE PADERWORK REDUCTON PROJECT (3150 0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON DC 20$03, FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (4)
PAGE(3)
LEQUENTiAL REV! SON yg NUMBER NUMBER RIVER BEND STATION 05000 458 4 OF 4 93 014 00 uxT g, m,,..:,,, r..,,.oa...oo=- c
, or usc % 3e,sy o 73 The fire amas containing the valves will remain under hourly fimwatch patrol pending NRC action on the deviation to the BTP.
SAFETY ASSESSMENT
Although the installed sprinkler systems are not equivalent to a rated fire barrier the water density provided by the sprinklers furnishes a level of protection sufficient for the fire risk in each fire area.
The hourly firewatch patrols currently in place, provide the proper compensatory action pursuant to Technical Specification 3.7.7.
NRC FORV 366A (5 92)
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05000458/LER-1993-001, :on 930113,determined That RWCU Isolation Setpoint Allowable Value Was Exceeded Due to Faulty Thermocouple Tester.All Three STPs Were Performed in Jan 1993 & Improper Settings Corrected |
- on 930113,determined That RWCU Isolation Setpoint Allowable Value Was Exceeded Due to Faulty Thermocouple Tester.All Three STPs Were Performed in Jan 1993 & Improper Settings Corrected
| 10 CFR 50.73(a)(2)(i) | 05000458/LER-1993-002, :on 930212,discovered That TS SRs Not Properly Implemented in Logic Sys Functional Tests Due to Inattention to Detail While Preparing Revs of Relevant Surveillance Test Procedures (Stp).Relevant STPs Revised |
- on 930212,discovered That TS SRs Not Properly Implemented in Logic Sys Functional Tests Due to Inattention to Detail While Preparing Revs of Relevant Surveillance Test Procedures (Stp).Relevant STPs Revised
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | 05000458/LER-1993-002-01, Forwards LER 93-002-01 Providing Details of Addl Investigation Re Logic Sys Functional Test Not Fulfilling TS SR | Forwards LER 93-002-01 Providing Details of Addl Investigation Re Logic Sys Functional Test Not Fulfilling TS SR | | 05000458/LER-1993-003, :on 930225,incidents Discovered Which Caused Interlock Mechanism in Upper Containment Airlocks at Elevation 171 to Operate Improperly.Case Study Training Class Developed for Airlock Incidents |
- on 930225,incidents Discovered Which Caused Interlock Mechanism in Upper Containment Airlocks at Elevation 171 to Operate Improperly.Case Study Training Class Developed for Airlock Incidents
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | 05000458/LER-1993-004, :on 930324,deficiency Discovered in Locking of Reactor Bldg Door.Caused by Lack of Understanding of TS Requirements for Locking Airlock Door.Operator Aids Posted & Permanent Locking Device Installed on Doors |
- on 930324,deficiency Discovered in Locking of Reactor Bldg Door.Caused by Lack of Understanding of TS Requirements for Locking Airlock Door.Operator Aids Posted & Permanent Locking Device Installed on Doors
| 10 CFR 50.73(a)(2)(i) | 05000458/LER-1993-005, :on 930415,discovered That RCIC Steam Line Flow - High Timer Function Never Performed on Monthly Basis. Caused by Failure to Include Test in Initial Procedure Development Process.Procedures Revised |
- on 930415,discovered That RCIC Steam Line Flow - High Timer Function Never Performed on Monthly Basis. Caused by Failure to Include Test in Initial Procedure Development Process.Procedures Revised
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000458/LER-1993-006, :on 930419,MSIV Failed to Stroke Closed When Given Close Signal from CR Due to Poppet Sticking.Caused by Insufficient poppet-to-guide Rib Clearance.Stricter Controls Imposed to Control Clearances |
- on 930419,MSIV Failed to Stroke Closed When Given Close Signal from CR Due to Poppet Sticking.Caused by Insufficient poppet-to-guide Rib Clearance.Stricter Controls Imposed to Control Clearances
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | 05000458/LER-1993-007, :on 930420,noted That an Isolation of Inboard & Outboard MSIV & Ms Line Drains Occurred.Caused by Lack of Personnel Knowledge of Unique Maint Conditions.Precaution Will Be Added to Sys Operating Procedure |
- on 930420,noted That an Isolation of Inboard & Outboard MSIV & Ms Line Drains Occurred.Caused by Lack of Personnel Knowledge of Unique Maint Conditions.Precaution Will Be Added to Sys Operating Procedure
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | 05000458/LER-1993-008, Forwards Rev 1 to LER 93-008 Re Relief Request Improperly Prepared for in-service Testing Program Which Resulted in Noncompliance W/Main Steam Isolation Valve Testing Requirement | Forwards Rev 1 to LER 93-008 Re Relief Request Improperly Prepared for in-service Testing Program Which Resulted in Noncompliance W/Main Steam Isolation Valve Testing Requirement | | 05000458/LER-1993-009, :on 930504,discovered That Surveillance Test Procedure for Control Bldg Chilled Water Sys Quarterly Pump Missed Due to Cognitive Personnel Error.Administrative Procedure Will Be Revised |
- on 930504,discovered That Surveillance Test Procedure for Control Bldg Chilled Water Sys Quarterly Pump Missed Due to Cognitive Personnel Error.Administrative Procedure Will Be Revised
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000458/LER-1993-010, :on 930514,SDC Lost for Approx Three Minutes When One SDC Suction Valve Closed Due to Initiation of Spurious ESF Actuation Signal.Caused by Personnel Error. Procedural Guidance Revised |
- on 930514,SDC Lost for Approx Three Minutes When One SDC Suction Valve Closed Due to Initiation of Spurious ESF Actuation Signal.Caused by Personnel Error. Procedural Guidance Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(b)(2)(iv) | 05000458/LER-1993-011, :on 930521,determined That Mode Switch Placed in Refuel Position During Testing of Switch Interlock Functions.Caused by Conflicting Info in Surveillance Procedures.Operating Procedure Revised |
- on 930521,determined That Mode Switch Placed in Refuel Position During Testing of Switch Interlock Functions.Caused by Conflicting Info in Surveillance Procedures.Operating Procedure Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000458/LER-1993-012, :on 930603,deficiency in Plant Surveillance Test Procedures Identified.Caused by Primary Causal Factor Inattention to Detail During Initial Procedure Development Process.Surveillance Test Procedures Performed |
- on 930603,deficiency in Plant Surveillance Test Procedures Identified.Caused by Primary Causal Factor Inattention to Detail During Initial Procedure Development Process.Surveillance Test Procedures Performed
| 10 CFR 50.73(a)(2)(i) | 05000458/LER-1993-013, :on 930629,high Pressure Core Spray Pump Failed to Start & Run During Surveillance Test Due to Failed Overfrequency Relay.Relay Tested & Installed in Switchgear |
- on 930629,high Pressure Core Spray Pump Failed to Start & Run During Surveillance Test Due to Failed Overfrequency Relay.Relay Tested & Installed in Switchgear
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) | 05000458/LER-1993-014, :on 930701,installed Sprinkler Sys as Substitute for Passive fire-rated Barrier Due to Deficiency Identified in Fire Barrier Separation Requirements.Declared Fire Barriers Surrounding Valves Degraded |
- on 930701,installed Sprinkler Sys as Substitute for Passive fire-rated Barrier Due to Deficiency Identified in Fire Barrier Separation Requirements.Declared Fire Barriers Surrounding Valves Degraded
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000458/LER-1993-015, :on 930723,discovered Time Response Testing of Isolation Instrumentation for RWCU & RCIC Sys Not Performed at Intervals Required by Tss.Caused by Scheduling Error & Misinterpretation of Ts.Schedule Revised |
- on 930723,discovered Time Response Testing of Isolation Instrumentation for RWCU & RCIC Sys Not Performed at Intervals Required by Tss.Caused by Scheduling Error & Misinterpretation of Ts.Schedule Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000458/LER-1993-016, :on 930727,HPCS Sys Actuation Occurred Due to Improperly Prepared Rev to Surveillance Test Procedure. Changed Surveillance Procedure STP-051-4811 |
- on 930727,HPCS Sys Actuation Occurred Due to Improperly Prepared Rev to Surveillance Test Procedure. Changed Surveillance Procedure STP-051-4811
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(o)(2)(v) | 05000458/LER-1993-018, :on 930813,isolation of RCIC Sys Occurred During Surveillance Test When Technician Connected Digital Multimeter to Wrong Terminals of Relay Base.Caution Statement Added to STP-207-4241 |
- on 930813,isolation of RCIC Sys Occurred During Surveillance Test When Technician Connected Digital Multimeter to Wrong Terminals of Relay Base.Caution Statement Added to STP-207-4241
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000458/LER-1993-019, On 930817,determined Hydrogen Igniter Cable Exceeded Equipment Qualification Lifetime Due to Localized High Drywell Temperatures.Replaced Hydrogen Igniter Cable | On 930817,determined Hydrogen Igniter Cable Exceeded Equipment Qualification Lifetime Due to Localized High Drywell Temperatures.Replaced Hydrogen Igniter Cable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | 05000458/LER-1993-020, :on 930821,determined That Exhaust Tornado Dampers for Several Bldgs Would Not Reopen Following Passage of Postulated Tornado Due to Incomplete Purchase Spec.Severe Weather Operation Procedure AOP-0029 Revised |
- on 930821,determined That Exhaust Tornado Dampers for Several Bldgs Would Not Reopen Following Passage of Postulated Tornado Due to Incomplete Purchase Spec.Severe Weather Operation Procedure AOP-0029 Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000458/LER-1993-022, :on 930924,an Esfa Occurred During Performance of Surveillance Test Procedure.Caused by Malfunction of Temp Switch.Mod Request Will Be Initiated to Place Switch W/Keyed Lock Downstream of Terminals |
- on 930924,an Esfa Occurred During Performance of Surveillance Test Procedure.Caused by Malfunction of Temp Switch.Mod Request Will Be Initiated to Place Switch W/Keyed Lock Downstream of Terminals
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000458/LER-1993-023, :on 930922,discovered Improper Engagement of Containment Airlock Door Handwheel Locking Mechanism Due to Inadequate Testing & Acceptance Criteria Supporting Plant Mod.Interlock Levers Modified |
- on 930922,discovered Improper Engagement of Containment Airlock Door Handwheel Locking Mechanism Due to Inadequate Testing & Acceptance Criteria Supporting Plant Mod.Interlock Levers Modified
| | 05000458/LER-1993-024, :on 931014,turbine Trip & Reactor Scram Occurred During Turbine Testing Due to Relay Contacts Failre to Open.Relay K15 Replaced & Successfully Tested.W/ |
- on 931014,turbine Trip & Reactor Scram Occurred During Turbine Testing Due to Relay Contacts Failre to Open.Relay K15 Replaced & Successfully Tested.W/
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) | 05000458/LER-1993-025, :on 931104,TS 3.0.3 Was Entered Due to Inadvertently Inoperability of Loop B of LPCI Sys.Caused by Personnel Failure to Correctly Interpret & Act Upon Caution of Procedure.Returned Loop to Operable Status |
- on 931104,TS 3.0.3 Was Entered Due to Inadvertently Inoperability of Loop B of LPCI Sys.Caused by Personnel Failure to Correctly Interpret & Act Upon Caution of Procedure.Returned Loop to Operable Status
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(s)(2) | 05000458/LER-1993-026, :on 931117,isolation of RCIC Sys Occurred Due to Apparent Failure of Relay.Three Relays Associated W/ Isolation Replaced & Shipped to Mfg for Failure Analysis.W/ |
- on 931117,isolation of RCIC Sys Occurred Due to Apparent Failure of Relay.Three Relays Associated W/ Isolation Replaced & Shipped to Mfg for Failure Analysis.W/
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000458/LER-1993-027, :on 931120,discovered Firewatch Patrol Not Completed in Timely Manner During Computer Sys Outage Due to Conflicting Priorities for Security Personnel.Memo Issued Raising Awareness of Fire Watch Urgency |
- on 931120,discovered Firewatch Patrol Not Completed in Timely Manner During Computer Sys Outage Due to Conflicting Priorities for Security Personnel.Memo Issued Raising Awareness of Fire Watch Urgency
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) |
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