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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20137F3221997-03-26026 March 1997 Part 21 Rept Re Perry Nuclear Power Plant Experiencing False Trip of K600S K-Line Low Voltage Circuit Breaker w/SS-5 Solid State Trip Device.Breaker Removed from Svc & Returned to ABB for Analysis ML20133E8001997-01-0808 January 1997 Deficiency Rept Re Nonconformance Related to Masterflow 713 Grout,Which Master Builders,Inc Has Supplied as Nuclear SR Product to 18 Npps.Cause Unknown.Requests That Listed Info Be Provided to Gain Insight as to Scope & Possible Cause ML20134H3361996-11-0505 November 1996 Part 21 Rept Re Defective Inner Thrust Bearing 1801461-01 Used in PSA 35 Mechanical Shock Arrestor Used as Restraint on Piping Sys for Nuclear Generating Plant.Lot of Defective Parts Located & Isolated to Three Customers ML20115D2001996-07-0909 July 1996 Part 21 Rept Re Mfg Defect of Enterprise DSR-4 & DSRV-4 Edgs,Originally Mfg by Calcon Corp.Amot Control Corp Purchased Calcon Product Line & Maintains Design & Production.Valves Returned to Cooper Energy Svcs on 960131 ML20083R9101995-04-26026 April 1995 Final Part 21 Rept Re Kepco,Inc Model RMX24-D-20804 Power Supplies in Which Transistors Q15 &/Or Q16 Failed to Open & R1 Was Open.Replacement of Transmitters w/XSIS-095 Along W/ Replacement of Electrolytic Capacitors Provides Solution ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20059A7181993-10-19019 October 1993 Part 21 Rept Re Defective Rocker Arms Supplied to TU & Clei. Rocker Arms Machined & Inspected to Incorrect Print & Discovered at Tu.Defective Rocker Arms Recalled from Nuclear Customers.No Corrective Action Required at Respective Utils ML20056D7071993-07-15015 July 1993 Part 21 Rept Re Reportable defect-75 PSIG Relief Check Valve 1 Npt,Emd 9521844,Kepner 416C-1-75 ML20034F7031993-02-25025 February 1993 Amend 1 to Enterprise Rept 162 Re Defect on Starting Air Distributor Housing Assembly,As Followup to 930115 Final Rept.Addl Listed Part Numbers Discovered Which Are Higher Level Assemblies of Housing ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed PY-CEI-NRR-1518, Corrected Part 21 Rept Re Defects in MSIV Poppets Supplied by Atwood & Morrill Co,Inc,Originally Submitted Via .Corrects Info in Corrective Action Section to Indicate That Poppet S/N 4 Not S/N 3 Installed at Facility1992-07-0101 July 1992 Corrected Part 21 Rept Re Defects in MSIV Poppets Supplied by Atwood & Morrill Co,Inc,Originally Submitted Via .Corrects Info in Corrective Action Section to Indicate That Poppet S/N 4 Not S/N 3 Installed at Facility ML17289A6971992-06-26026 June 1992 Amend 1 to Part 21 Rept 158 Re gear-wear Induced Failures in engine-driven Jacket Water Pump in DSRV-16-4 Standby DG Sys. Initially Reported on 911029.Grand Gulf Station Observed Wear Characteristics in as Little as 500 Operating Hours ML20102B2071992-06-24024 June 1992 Part 21 Rept Re Cracking of Stellite 21 Hardfacing on Guide Nose of Poppets Supplied as Part of MSIV Leakage Improvement Mod.Initially Reported by Clei on 920522. Recommends That Liquid Penetrant Exam Be Performed PY-CEI-NRR-1516, Part 21 Rept Re Defects in MSIV Poppets Supplied by Atwood & Morrill Co,Inc.Intially Reported on 920522.Measures Will Be Established to Ensure That Adequate Repair Methods Are Employed During Future Repairs of Modified MSIV Poppets1992-06-19019 June 1992 Part 21 Rept Re Defects in MSIV Poppets Supplied by Atwood & Morrill Co,Inc.Intially Reported on 920522.Measures Will Be Established to Ensure That Adequate Repair Methods Are Employed During Future Repairs of Modified MSIV Poppets ML20101G9211992-06-19019 June 1992 Part 21 Rept Re Rotated Fuel Assemblies Sometimes Inappropriate for Modern Type Fuel Designs.Reevaluation Concluded That Inadvertently Rotated Fuel Assembly for BWR 4/5 C-lattice Plant Could Not Exceed TS Safety Limit MCPR ML20097H1531992-05-22022 May 1992 Part 21 Rept Re Defect in MSIV Poppets Supplied to Plant by Atwood & Morrill Co,Inc.Post Weld Heat Treatment Prescribed & Performed for Poppet to Alleviate Concerns Re Residual Stresses Present.Next Rept Will Be Submitted within 30 Days ML20094L1271992-03-13013 March 1992 Amend 1 to Part 21 Rept 159 Re Potential Defect in Power Cylinder Liner.Initially Reported on 920115.Caused by Liner/ Block Fit & Localized Matl Microstructure.All Drawings & Specs Revised to Address Matl Design Requirements ML20081F6091991-04-23023 April 1991 Part 21 Rept Re Edward Controlled Closure Check Valves & Testable Piston Check Valves Dashplate Bolt Failures Due to Rapid Valve Opening or Impulsive Differential Pressure Surge Across Dashplate.Design Changes Recommended PY-CEI-NRR-1303, Part 21 Rept Re Finding That Nitrile Rather than Ethylene Propylene Diene Monomer (Epdm) Used as Seal Matl in Several E-sys Hydraulic Snubbers.Proper Seal Matl (Epdm) Used to Rebuild Snubbers & Leaking Valves Repaired1991-02-0404 February 1991 Part 21 Rept Re Finding That Nitrile Rather than Ethylene Propylene Diene Monomer (Epdm) Used as Seal Matl in Several E-sys Hydraulic Snubbers.Proper Seal Matl (Epdm) Used to Rebuild Snubbers & Leaking Valves Repaired ML20065T1661990-12-19019 December 1990 Part 21 Rept Re Reportable Event Concerning Chilled Water Sys at Plant.Initially Reported on 901030 & 1130.Util Notified of Results of Evaluation & Reported Addl Details, Per 10CFR50.72 ML17262A2621990-11-30030 November 1990 Part 21 Rept Re Chilled Water Sys.Initially Reported on 901030.Evaluation of Perry Plant Will Be Sent by 901230 ML20011F5971990-02-22022 February 1990 Part 21 Rept Re Solder Connections in ABB 27/59 Relays Deteriorated Due to Thermal Stress,Causing Bonding of Printed Wiring Pattern to Glass Epoxy Circuit Board.Interim Circuit Board W/Larger Pads & Higher Wattage Will Be Used ML20011F1941990-02-22022 February 1990 Part 21 Rept Re ABB 27/59 Relay Catalog Series 211L.Solder Connections to Printed Wiring Runs on Bottom of Circuit Board Deteriorated Due to Thermal Stress.No Actual Failure Occurred & Relays to Be Changed at Next Outage ML20006A3611990-01-17017 January 1990 Part 21 Rept 152 Re Potential Defect in Component of Dsr or Dsrv Standby Diesel Generator Sys Supplied to Listed Sites by Cooper Industries.Qualified Replacement Valve in Process of Being Specified.Info Will Be Available by 900215 ML20248E0121989-09-13013 September 1989 Supplemental Part 21 Rept Re Potential Problem W/Six Specific Engine Control Devices in Air Start,Lube Oil, Jacket Water & Crankcase Sys.Initially Reported on 890429. California Controls Co Will Redesign Valve Seating ML20246K7401989-04-26026 April 1989 Part 21 Rept Re Incorrectly Stamped Name Plates on Certain Asco Nuclear Qualified Valves.Vendor Will Contact Each Affected Facility & Furnish Correctly Stamped Plates & in Near Future Discontinue Sale of Rebuild Kits for Valves ML20207P0451988-10-0505 October 1988 Part 21 Rept 146 Re Defect in Left Intercooler Inlet Adapter on Standby Diesel Engine Generator.Recommends Utils Inspect Left Intake Manifold Drain as Part of Operating Plan.Addl Info Expected by 881015 ML20154J4101988-05-12012 May 1988 Addendum 1 to Supplemental Part 21 Rept 145 Re Potential Problem w/F-573-156 Pressure Sensor/Lube Oil Trip.Initially Reported on 880429.Addl 1-1/8-inch Diameter W/Deep Counterbone in Pressure Head Added to Activate Valve ML18093A8281988-05-0606 May 1988 Part 21 & Deficiency Rept Re Asea Brown Boveri,Power Distribution,Inc Low Voltage K-Line Circuit Breakers. Efforts Underway to Define Quantity & Type of Component Parts That May Need to Be Replaced ML20153B6191988-04-29029 April 1988 Part 21 Rept Re Potential Defect in Component of Dsr or Dsrv Standby Diesel Generators Supplied to Utils.Recommends Return of Subj Components in Onsite Warehouse Storage & Suggests Surveillance of Devices Already Installed ML20151V8941987-12-22022 December 1987 Part 21 Rept Re Installation of Valve B/M RNU-205 W/ Undersized Motor Operator.Caused by Engineer Failure to Change Sizing from Previously Sized Motor Operator on Computer Program.Existing Operator Replaced ML20216E4721987-05-28028 May 1987 Part 21 Rept 140 Re Potential Defect in Air Pressure Regulators Mfg by Bellofram.Dripwell Gasket May Fail Due to Mismachining of Gasket Seating Surface Causing Loss of Control Air & Starting Air Pressure ML20215G5351986-10-10010 October 1986 Part 21 Rept Re Vendor Tests of air-operated Diaphragm Valves Revealing Natural Frequencies Less than Required Values of 33 Hz.Initially Reported on 841227.No Adverse Effects Noted During Testing ML20215G6801986-10-10010 October 1986 Part 21 Rept Re Vendor Tests of air-operated Diaphragm Valves Revealing Natural Frequencies Less than Required Values of 33 Hz.Initially Reported on 841227.No Adverse Effects Noted During Testing ML20210F4741986-09-16016 September 1986 Part 21 Rept Re Possible Sticking in Closed or Partially Open Position on Dresser 3050 Diaphragm Valves.Initially Reported on 850118.Disc Caps,Including Chamfers on Outside Diameter,Will Be Modified ML20214M3181986-09-0404 September 1986 Potential Part 21 Rept Re Contromatics Actuator W/Jackscrew/ Handwheel Emergency Override Operator.Jackscrew/Handwheel Should Be Used for Emergency Manual Operation Only.Encl Ltr Also Sent to Listed Utils/Ae Firms ML20205F6141986-08-13013 August 1986 Part 21 Rept Re Connecting Rod Bolts for Dsrv Engines.Listed Procedures Recommended for Next Connecting Rod Insp, Including Replacement of Bolts Due to Cracked Threads & Large Grooves & Galls in Threads ML20207L1831986-07-18018 July 1986 Final Deficiency Rept (Rdc 146(86)) Re Hydraulic Control Units (Hcus) Not Installed Per Equipment Qualification Program.Initially Reported on 860619.Drawings Will Be Changed to Reflect Correct HCU Mounting Bolts Torque Values ML20206U0591986-07-0202 July 1986 Part 21 Rept Re Potential Defect in Component of Dsrv Standby Diesel Generators,Involving Problem W/Fastening of Engine Connecting Rod Assembly Which Could Result in Engine Nonavailability.Procedure Will Be Issued by 860718 ML20206S0841986-06-30030 June 1986 Part 21 Rept Re Possible Cut Wires in Wire Harness of Bbc Brown Boveri K600/K800 Circuit Breakers.Initially Reported on 860509.Safety Implications Listed.Gear Guard Designed to Prevent Cut Wires ML20198E5401986-05-14014 May 1986 Final Part 21 & Deficiency Rept (Rdc 145(86)) Re Kaman Instrument Co High Voltage Power Circuitry.Initially Reported on 860326.Circuit Board Cards Returned to Supplier for Circuitry Mod ML20203N4761986-04-25025 April 1986 Interim Deficiency & Part 21 Rept (Rdc 145(86)) Re Kaman Instrument Co High Voltage Power Supply in Microprocessors. Initially Reported on 860326.Next Rept Expected by 860414 ML20202F4601986-04-0303 April 1986 Interim Part 21 & Deficiency Rept (Rdc 145(86)) Re Kaman Instrumentation Co High Voltage Power Supply (P/N 450447) Found Oscillating Between 240 & 1,030 Volts at 100 Hz. Initially Reported on 860326.Investigation Continuing ML20141A1081986-03-31031 March 1986 Part 21 Rept 134 Re Potential Defect in K-1 Relay in Generator Voltage Regulator.Initially Reported on 860219. Corrective Action Must Take Into Account Equipment Operating Range of 100-137.5-volt Dc ML20154N4361986-03-10010 March 1986 Part 21 Rept Re Defect on Inflatable Door Seals for Personnel Air Locks Used in Reactor Containment Sys of Nuclear Power Plants.Initially Reported on 830919.Environ Qualification Testing of New Seal Design Completed 1999-04-12
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000440/LER-1999-004, :on 990916,loss of Safety Function Resulted in TS 3.0.3 Entry.Caused by Design Deficiency in Control Complex Architectural Walls.Revised Storm Contingencies Instructions.With1999-10-18018 October 1999
- on 990916,loss of Safety Function Resulted in TS 3.0.3 Entry.Caused by Design Deficiency in Control Complex Architectural Walls.Revised Storm Contingencies Instructions.With
ML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20212J2011999-09-30030 September 1999 Safety Evaluation Supporting Transfer of Dl Ownership Interest in PNPP to Ceico PY-CEI-NRR-2437, Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With 05000440/LER-1999-003-01, :on 990218,post-accident Dose Limits Were Exceeded.Caused by Relief Valve Leakage Outside of Containment.Removed Relief Valve on 990913,by Design Change Package Implemented Under 10CFR50.59.With1999-09-27027 September 1999
- on 990218,post-accident Dose Limits Were Exceeded.Caused by Relief Valve Leakage Outside of Containment.Removed Relief Valve on 990913,by Design Change Package Implemented Under 10CFR50.59.With
PY-CEI-NRR-2429, Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With ML20212A6881999-08-31031 August 1999 Safety Evaluation Supporting Amend 106 to License NPF-58 PY-CEI-NRR-2424, Monthly Operating Rept for July 1999 for Perry Npp.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Perry Npp.With ML20210J3851999-07-28028 July 1999 PNPP - Unit 1 ISI Summary Rept Results for Outage 7 (1999) First Period,Second Interval PY-CEI-NRR-2416, Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With ML20196A1951999-06-17017 June 1999 Instrument Drift Analysis ML20207G2741999-06-0707 June 1999 Safety Evaluation Concluding That Firstenergy Flaw Evaluation Meets Rules of ASME Code & That IGSCC & Thermal Fatigue Crack Growth Need Not Be Considered in Application PY-CEI-NRR-2409, Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2393, Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored1999-05-12012 May 1999 Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored ML20206G6451999-05-0303 May 1999 Safety Evaluation Authorizing Requests for Relief IR-032 to IR-035 & IR-037 to IR-040 Re Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp PY-CEI-NRR-2399, Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With ML20206E2261999-04-29029 April 1999 Safety Evaluation Concluding That Proposed Alternatives Will Result in Acceptable Level of Quality & Safety.Authorizes Use of Code Case N-504 for Weld Overlay Repair of FW Nozzle Weld at PNPP & Use of Table IWB-3514 05000440/LER-1999-002-01, :on 990327,RHR a Pump Failed to Start & LCO 3.0.3 Was Entered Due to TS Bases Misinterpretation.Caused by Failed Optical Isolator That Provided Signal to Pump Start Permissive Circuitry.Subject Circuitry Was Replaced1999-04-26026 April 1999
- on 990327,RHR a Pump Failed to Start & LCO 3.0.3 Was Entered Due to TS Bases Misinterpretation.Caused by Failed Optical Isolator That Provided Signal to Pump Start Permissive Circuitry.Subject Circuitry Was Replaced
ML20206D7911999-04-23023 April 1999 Rev 6 to PDB-F0001, COLR for Pnpp Unit 1 Cycle 8,Reload 7 05000440/LER-1999-001-01, :on 990317,discovered That Control Complex Bldg Architectural Walls Were Not Included in Tornado Dp Loading Design.Caused by Failure to Consider Tornado Dp Loads. Compensatory Measures Were Implemented.With1999-04-16016 April 1999
- on 990317,discovered That Control Complex Bldg Architectural Walls Were Not Included in Tornado Dp Loading Design.Caused by Failure to Consider Tornado Dp Loads. Compensatory Measures Were Implemented.With
ML20205P4371999-04-15015 April 1999 Safety Evaluation Concluding That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking or Thermal Binding ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected PY-CEI-NRR-2389, Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With ML20205G4221999-03-31031 March 1999 Safety Evaluation Accepting Second 10-yr Interval IST Program Releif Requests for Plant,Unit 1 ML20206D8461999-03-31031 March 1999 Rev 1 to J11-03371SRLR, Supplemental Reload Licensing Rept for Pnpp,Unit 1 Reload 7 Cycle 8 ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205E0591999-03-26026 March 1999 Safety Evaluation Supporting Amend 105 to License NPF-58 ML20205D3101999-03-26026 March 1999 Safety Evaluation Supporting Amend 103 to License NPF-58 ML20205D6921999-03-26026 March 1999 Safety Evaluation Supporting Amend 104 to License NPF-58 ML20205C3761999-03-26026 March 1999 Safety Evaluation Supporting Request for Proposed Exemption to 10CFR50,app a GDC 19 ML20204C0711999-03-11011 March 1999 Safety Evaluation Supporting Amend 102 to License NPF-58 ML20207F4361999-03-0303 March 1999 Safety Evaluation Supporting Amend 101 to License NPF-58 PY-CEI-NRR-2369, Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 9902271999-03-0303 March 1999 Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 990227 PY-CEI-NRR-2372, Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With ML20207L4881999-02-24024 February 1999 Safety Evaluation Supporting Amend 100 to License NPF-58 ML20203F8381999-02-0808 February 1999 Safety Evaluation Supporting Amend 97 to License NPF-58 ML20203A5961999-02-0202 February 1999 Safety Evaluation Accepting Licensee Proposed Revs to Responsibilities of Plant Operations Review Committee as Described in Chapter 17.2 of USAR ML20203A5211999-01-27027 January 1999 Safety Evaluation Accepting Licensee Calculations Showing That Adequate NPSH Will Be Available for HPCS Pumps ML20198R8921999-01-0707 January 1999 SER Accepting Licensee Proposed Amend to TSs to Delete Reference to NRC Policy Re Plant Staff Working Hours & Require Administrative Controls to Limit Working Hours to Be Acceptable ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 PY-CEI-NRR-2356, Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With ML20198J0031998-12-22022 December 1998 SER Accepting Licensee Response to GL 92-08,ampacity Derating Issues for Perry Nuclear Power Plant,Unit 1 ML20198K9071998-12-21021 December 1998 Safety Evaluation Supporting Amend 96 to License NPF-58 ML20196J4731998-12-0202 December 1998 Safety Evaluation Supporting Amend 95 to License NPF-58 PY-CEI-NRR-2346, Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With ML20196D2751998-11-23023 November 1998 Safety Evaluation Supporting Amend 94 to License NPF-58 ML20195F6891998-11-0505 November 1998 Safety Evaluation Accepting Proposed Reduction in Commitment in Quality Assurance Program to Remove Radiological Assessor Position 05000440/LER-1998-003, :on 981001,missed TS SR on H Igniters Was Noted.Caused by Personnel Error.Missed Surveillance Was Performed on Day of Discovery of Item & Function of H Igniters Were Verified.With1998-11-0202 November 1998
- on 981001,missed TS SR on H Igniters Was Noted.Caused by Personnel Error.Missed Surveillance Was Performed on Day of Discovery of Item & Function of H Igniters Were Verified.With
PY-CEI-NRR-2335, Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With 1999-09-30
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i ILLUMINATING 8 LOG. s PUBUC SQUARE e CLEVELAND oHlo 44101 m TELEPHONE (216) 6231350 e MAIL ADDRESS: P. O. BOX 5000 Serving The Best Location in the Nation Dalwyn R. Davidson v'CE PAESIDENT SYSTE M ENGINEERING ANO CoNSTRUClioN Augus t 26, 1980 Mr. James G. Keppler Director Region III Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 Re:
Perry Nuclear Power Plant Final Report on
Dear Mr. Keppler:
Post-LOCA H Analyzers 2
This letter is the final report on the deficiency concerning Post-LOCA H2 Analyzers required by 10CFR50.55(e).
This problem was first identified to Mr. Jack Hughes of the NRC Region III, Of fice of Inspection and Enforcement on April 22, 1980, by Mr. M. R. Edelman of The Cleveland Electric Illuminating Company.
Additionally, an interim report dated May 22, 1980, was sent to you documenting the problem and the course of action to be taken.
Description of Deficiency The Cleveland Electric Illuminating Company aw n ded a contract to Comsip Incorporated for the design, f abrication, assembly, testing, inspection and delivery of the hydrogen analyzer systems for the Perry Nuclear Power Plant-Units 1 and 2.
During a functional testing of one of the units, a pump failed because one of the panel outlet valves was closed when the pump was started.
This design did not consider that excessive outlet pressure of the sample pump could cause mechanical separation of the connecting rud and crank shaft, which in turn, could rupture the pump diaphragm.
Analysis of Safety Implication 1
In our interim report, dated May 22, 1980, we identified two (2) potential l
safety hazards:
l l.
Up te one (1) liter of containment gas could be released into the outside atmosphere, should the failure as defined above occur; and/or 2.
If the input / outlet valve is closed while the pump is in operation or if the containment isolation valve inside the containment is closed, there is a risk in damaging the system, thereby rendering the sys tem l
inoperable.
foI9 l
THis DOCUMENT CONTAINSgiO POOR QUAUTY PAGES {,
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Mr. Kepplcr Augus t 26, 1980 Based on further analysis, we now feel that Item 2. is not a potential safety hazard.
In the unlikely event that the redundant hydrogen analyzer woild be rendered inoperable, the other components of the Combustible Gas Control System, Hydrogen Recombiners and Back-Up Purge Systems can be started.
This will allow suf-ficient time for repairs or to manually analyze for hydrogen.
Corrective Action In order to rectify this potential safety hazard, a relief bypass valve was installed across the pume to protect the pump against the possible closing of the isolation valves and over pressurizing the pump outlet. When activated at approximately 100 psig, this valve routes the pressure back to the pump inlet, maintaining a closed sys tem.
The relief action of this valve will reduce the flow through the analyzers and activate the low flow alarm.
Engineering's review and acceptance of this design is documented in the attached letter.
In addition to the design review, we requested Comsip to do an operational test of this new design. This test was witnessed by The Cleveland Electric Illuminating Company personnel.
This basic operational test consisted of a blocked pump output with a pressure gauge and a temperature gauge secured to the output head on the pump.
The relief valve allowed a maximum pump pressure of 108 psig. Af ter 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />, the temperature stabilized at 110*F.
Wh Lle the tests proved that the new design would be adequate to prevent the release of contaminated gas to the atmosphere, an additional problem was encountered when the shaft on the motor driving the pump broke in two (2) pieces during the test.
While this motor failure would not cause any con-taminated gas leakara, this problem is presently being evaluated.
Summary nued on the Engineering analysis perfonned by Comsip and Gilbert Associate Engineers and by the success f the operational test performed on the new design, it is our position that the modifications made to the Post-LOCA H9' Analyzers will rectify the deficiency defined earlier in this report.
Very truly yours, n
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Dalw R. Davidson Vice President System Engineering and Construction l
l DRD:pb T13/A/2 cc:
Mr. Victer Stello, Director Office of Inspection and Enforcement U.S. Nuclear Regulatory Cc==ission Washingten, D.C.
20555
P.'E. Kelly - CEI/QA n
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- P. O. Box 97
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Parry, Ohio
[Q-Gilbert / Commonwealth engineers and consstants GILEERT ASSOCIATES, INC., P. O. Bcx 1498. Peading. PA 1SS03/Tel 215 775-2600/Ccble Gdasoc/Teler 936-431 August 12, 1980 PY-GAI/CEI-lll'11 INFORMATION The Cleveland Electric Illuminating Company Nucle?r Engineering Department Post Office Box 97 Perry, Ohio 44081 Attention:
Mr. E. A. Adams Re:
Perry Nuclear Power P1' ant, Units 1 & 2 SP-611, SR Hydrogen Analyzers Comsip-Delphi, Incorporated Acceptance Testing, PY-GAI/CEl-11106 Gen tlemen :
In reference to subject letter, please add the following to the end of the second paragraph:
Engineering review of the des'ign ' change and results of the test demonstrated that the check / relief valve fix adequately overcame the April 2 failure above.
Very truly yours, RECEIVED
~
RECEfVED A. Bruno I&C Engineer 6 0 1 1980 AUG 141980 U.
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Quuu[E/Eo;ract
'Y S. M. Gresdo Project ISC Engineer u-i P. B. Gudikunst Project Manager Name:
AB/SMG/PBG/dob File Code: S 2-6N Toss cc:
S0/DC - Attn. SP-611 (2)
CEI/NED - Att. SP-611 (2) g H,'/
P. B. Gudikunst (2)
Reviewed: r i/ A A _ u -
P. E. Kelly - CEI/QA J.,
Furness,
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g O riitcod:: so 61) y Perry hio Tcss Gilbert / Commonwealth engineers and consultants gg{g.g,g Glilithi ASSGCAlfS. INC., P. O. Gon W.S. Redng. PA tsCO3/M 2;5 //5-2000/CatJe Ghwc/kle 63ggILITY ASS 8ECE1VED DEPARTMENT 1 3 1930 August 8, 1980 c.*
PY-GAI/CEI-11106 cocyuCNT CQHTROL INFORMATION no Cleveland Electric Illuminating Co:apany RECEIVED Nuclear Engineering Department Post Office Box 97 AUG 181980 Perry, Ohio 44081
,,,,,,,o,,c, QueUff teciettaang Attention:
Mr. E. A. Adams Re:
Perry Nuclear Power Plant, Units 1 & 2 SP-611, Safety-Related Hydrogen Analyzers Comsip-Delphi, Incorporated Acceptance Testing Centlemen:
On April 2,1980, during the acceptance test, the sainpling pump in the subji et system failed when the outlet was closed and the pump became over-pressurin d.
Wis failure was reported to CEI and the USNRC under 10CFR21.
In order to correct chis malfunction a clwek/ relief valve was added to bypass the pump when the pressure rose to about 100 psi.
A test was set up to witness this fix on July 29, 1980.
The pump operated smoothly at a maximum pressure of 100 + 5 psi and its ;;emperature stabilized at about 105 F after about three hours of operation.
The test was allowed to run for about another hour, when the Reliance lE pump motor had a shaf t failure at the point where it necked down to fit the pump coupling.
Reliance Motor Division has been crintacted by Comsip and the pump motors will be replaced with units built with higher strength shaf ts.
When the analyzers are reassembled with the new motors, it is suggested that the acceptance test be repeated for ecch unit.
A3/SMG/PSG/ deb Very truly yours, cc:
S0/DC, Att:
SP-611 (2)
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CEI/NED, Attn:
SP-611 (2)
A. Bruno P. B. Gudikunst (2)
I6C Engineer P. E. Kelly - CEI/QA y
J. Futne ss
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C. M. Reynolds S. M. Cresdo Project I6C Engineer Q3dAJ B. Gudikunst Project Manager m t.uw A.y.
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