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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D0201994-04-25025 April 1994 LER 94-007-01:on 931014,high Head Safety Injection Flow Balance Testing Found to Be Below TS Requirement.Caused by Unaccounted for Uncertainties.Cold Leg Safety Injection Leg Throttle Valve adjusted.W/940425 Ltr ML20045G9391993-07-0808 July 1993 Lr 93-017-00:on 930616,containment Hydrogen Analyzer Heat Trace Channel Calibration Not Performed on Staggered Test Basis Due to Inadequate Implementation of TS Amend.Test Procedure Satisfactorily performed.W/930708 Ltr ML20044H1591993-05-27027 May 1993 LER 93-016-00:on 930509,discovered That Containment Hydrogen Analyzer Pressure Switch PS-3 Sensing Line Disconnected in Local Panel.Caused by Personnel Error. Pressure Switch Calibr & Line reconnected.W/930527 Ltr ML20044D5711993-05-14014 May 1993 LER 93-002-00:on 930416,automatic Reactor Trip Initiated from Turbine Trip Due to Over Excitation of Main Generator. Emergency Procedure 2-E-0 Entered & Individuals Involved in Event Received Remediated training.W/930514 Ltr ML20044D2281993-05-12012 May 1993 LER 93-003-00:on 930424,manual Reactor Trip Initiated Due to Erratic Feedwater Flow Indications to SG C & Excessive Main Feedwater Regulating Valve Oscillations.Caused by Design Instabilities.Secondary Sys secured.W/930512 Ltr ML20044C9541993-05-0707 May 1993 LER 93-015-00:on 930427,discovered That Portions of Containment Pressure Channels That Input to Containment Spray hi-hi Pressure Not Tested Monthly.Caused by Personnel Error.Test Procedures changed.W/930507 Ltr ML20044C9811993-05-0606 May 1993 LER 93-014-00:on 930411,as-found Speed Setting of Steam Driven AFW Pump 1-FW-P-2 Found Below Required TS Limit. Caused by Incorrect Speed Control Setting.Pump Speed Adjusted & Maint Personnel counseled.W/930506 Ltr ML20024G6841991-04-18018 April 1991 LER 91-006-00:on 910403,discovered That Ac Offsite Power Source Surveillance Not Performed Due to Personnel Error. Surveillance Initiated Immediately & Positive Discipline Administered to supervisor.W/910418 Ltr ML20029B5601991-03-0606 March 1991 LER 91-005-00:on 910209,containment Building Penetrations Breached.Caused by Inadequate Procedural Controls.Core Mapping & Cavity Pump Down Activities Secured,Air Hose Removed & Hydrolase Hose capped.W/910306 Ltr ML20029A6471991-02-22022 February 1991 LER 91-004-00:on 910206,sealed Radioactive Source in Storage Not Leak Tested Prior to Use.Caused by Inadequate Procedures for Verifying Leak Testing of Sources.Procedures Revised.W/ 910222 Ltr ML20028H6681991-01-18018 January 1991 LER 90-009-01:on 900719,discovered That Response Time Testing of Pressurizer High Level Reactor Trip Function Not Performed in Accordance W/Tech Spec 3.3.1.1,Table 3.3-2. Caused by Personnel Error.Procedures revised.W/910118 Ltr ML20043H8321990-06-22022 June 1990 LER 90-007-00:on 900523,discovered That Two Sets of Concrete Roof Blocks on Svc Water Pump House Not in Required Safety Position.Caused by Lack of Administrative Controls.Blocks Restored to Required locations.W/900622 Ltr ML20043D5801990-06-0404 June 1990 LER 90-006-00:on 900504,casing Cooling Pump Not Put Into Alert Status & Surveillance Missed.Caused by Personnel Error.Pump 1-RS-P-3B Placed in Alert status.W/900604 Ltr ML20012E3301990-03-27027 March 1990 LER 90-003-00:on 900228,52 Valves Identified Not Included in Tech Spec Required Monthly Containment Integrity Verification Surveillance Program.Caused by Personnel Error & Inadequate Procedure.Procedure revised.W/900327 Ltr ML20012B6441990-03-0808 March 1990 LER 90-001-00:on 900215,inadvertent Partial Train a ESF Actuation of Containment Depressurization Sys Occurred. Caused by Human Error.Evaluation to Be Performed to Determine If Test Points Can Be moved.W/900308 Ltr ML20006E2371990-02-0808 February 1990 LER 90-001-00:on 900123,reactor Trip Occurred on Steam Feedwater Flow Mismatch.Caused by Failed Circuit Driver Card on Feedwater Regulating Valve.Feedwater Regulating Valve Driver Card replaced.W/900208 Ltr ML20006E3771990-02-0505 February 1990 LER 90-002-00:on 900127,fuel Bldg Ventilation Sys Not Aligned to Discharge Through Auxiliary Bldg HEPA Filter & Charcoal Adsorber Assembly During Fuel Movement.Caused by Personnel Error.Disciplinary Action taken.W/900205 Ltr ML20006A8531990-01-19019 January 1990 LER 89-019-00:on 891228,discovered That Outer Door of Containment Equipment Escape Air Lock Was Drawing in Air & Inner Door Noted as Not Being in Fully Closed Position.Cause Undetermined.Sys Enhancements Being evaluated.W/900119 Ltr ML20005F8781990-01-11011 January 1990 LER 89-018-00:on 891219,determined That Three Pressurizer Pressure Safety Injection Instrumentation Channels May Not Have Adequate Margin Between Actuation Setpoint & Bottom of Instrument span.W/900111 Ltr ML19332D5471989-11-22022 November 1989 LER 85-003-03:on 890907,determined That Situation Could Arise Where Water Level Would Rise to 264 Ft Before Next Required Surveillance Interval.Cause Not Determined.Dike to Be constructed.W/891122 Ltr ML20024B7821983-07-0606 July 1983 LER 83-048/03L-0:on 830606 & 17,intermediate Range Channels N35 & N36 High Neutron Flux Reactor Trip Setpoints Exceeded Tech Spec Requirements.Caused by Administrative Error. Setpoints reduced.W/830706 Ltr ML20024C1361983-06-30030 June 1983 LER 83-031/03L-0:on 830614,w/unit at 100% Power,Fire Door S54/5 from Emergency Switchgear Room to Cable Vault Would Not Latch.Fire Watch Posted Immediately.Caused by Misaligned Strike.Door Repaired within 1 h.W/830630 Ltr ML20024C3721983-06-30030 June 1983 LER 83-042/03L-0:on 830606,vital Bus 1-I Momentarily Deenergized While Trying to Clear Inverter Trouble Alarm. Caused by Operator Error.Bus energized.W/830630 Ltr ML20024B9891983-06-28028 June 1983 LER 83-047/03L-0:on 830530,emergency Diesel Generator 2J Tripped on High Crankcase Pressure During Surveillance Testing.Cause Not Determined.Diesel Tested Satisfactorily. W/830628 Ltr ML20024C2941983-06-23023 June 1983 LER 83-044/03L-0:on 830526,during Mode 3,one Recirculation Valve on Each of Two Casing Cooling Pumps Found Open.Caused by Procedure Inadequacy.Valves Closed Immediately.Maint Procedure Will Be revised.W/830623 Ltr ML20024C3071983-06-22022 June 1983 LER 83-034/03L-0:on 830525,during Mode 1,one Header of Control Room Bottled Air Pressurized Sys Had Lower than Required Pressure.Probably Caused by Leak from B Bank of Air Bottles.Header repressurized.W/830622 Ltr ML20024C0971983-06-22022 June 1983 LER 83-045/03L-0:on 830614,Fire Door S71-18,between Emergency Diesel Generator Room 2H & Turbine Bldg,Would Not Latch & Lock.Caused by Stuck Latch.Latch Adjusted & Lubricated.Door Designs modified.W/830622 Ltr ML20023E0951983-06-0101 June 1983 LER 83-027/03L-0:on 830505,one Header (42 Bottles) of Control Room Bottled Air Pressurized Sys Found to Have Lower than Required Pressure (2,290 Vs 2,300 Psig).Probably Caused by Leakage When Compressor malfunctioned.W/830601 Ltr ML20023E0721983-05-26026 May 1983 LER 83-029/03L-0:on 830509,following Rapid Rampdown from 100% to 4% power,I-131 Dose Equivalent Exceeded 1.0 Uci/G. Caused by Unidentified Fuel Element Defect Worsened by post-rampdown Conditions.Sampling increased.W/830526 Ltr ML20023D5371983-05-13013 May 1983 LER 83-022/03L-0:on 830412,review of ASME XI Iwv Program Identified 192 Valves Not Exercised &/Or Stroke Timed.Caused by Fragmented Implementation of Testing Program.Programs Upgraded ML20023D2491983-05-11011 May 1983 LER 83-032/03L-0:on 830412,during Mode 5,visual Insp of Hydraulic Snubber 2-WGCB-HSS-3B Revealed Damaged Reservoir W/O Fluid.Caused by Personnel Working in Area.Snubber Replaced ML20023C5371983-05-10010 May 1983 LER 83-021/03L-0:on 830411,Fire Door S-71-7 Between Svc Bldg Health Physics Area & Auxiliary Bldg Would Not Self Close.Caused by Removal of Reclosure Device for Maint of Closure Coupling.Reclosure Device Reinstalled ML20023B5931983-04-27027 April 1983 LER 83-029/03L-0:on 830402,during Mode 4,automatic Actuation of ECCS Occurred.Caused by Maint Personnel Standing on Conduit Resulting in Loss of lo-lo Pressurizer Pressure Safety Injection Block.Maint Personnel Reinstructed ML20023B5701983-04-27027 April 1983 LER 83-008/03L-0:on 830410,review Revealed That Procedure Used to Restore Boron Injection Tank Concentration Introduced Potential Unanalyzed Injection Flow Diversions. Caused by Oversight.Emergency Procedures Revised ML20028G6541983-02-0909 February 1983 LER 83-003/03L-0:on 830122,during Mode 5,RHR Flow Was Lost for 4 Minutes.Caused by Failure of 15 Kv a Inverter to Ac Vital Bus 1-III,de-energizing Auxiliary Relay for Pressure Channel P-1403.Vital Bus 1-III & RHR Flow Restored ML20028G6311983-02-0909 February 1983 LER 83-016/03L-0:on 830115 & 16,both Open & Closed Containment Isolation Valves TV-SI-200 & TV-CC-204C,train a Position Indication Lights Found Lit.Caused by Leaking Steam Generator Chemical Feed Line Vent Valve ML20028G0781983-01-31031 January 1983 LER 83-001/03L-0:on 830112,primary Grade Water Isolation Valve to Blender 1-CH-217 Remained Open Longer than Tech Spec Requirements.Caused by Personnel Error.Responsible Operator Reinstructed ML20028G0381983-01-28028 January 1983 LER 83-002/03L-0:on 830104,two of Four 2H Emergency Diesel Generator Surveillance Tests Required by Tech Spec Missed During Nov-Dec 1982.Caused by Scheduling Error.Test Frequency Increased to Meet Tech Spec Requirements ML20028G0131983-01-28028 January 1983 LER 83-011/03L-0:on 821119,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps.Caused by Instrument Drift.Indicator Channel for Rods B-09 & 02 & F-06 Recalibr ML20028F3501983-01-19019 January 1983 LER 83-008/03L-0:on 830107,during Mode 3,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps While Withdrawing Shutdown Bank B. Caused by Instrument Drift.Rods Recalibr ML20028E0391983-01-11011 January 1983 Updated LER 82-079/03X-1:on 821126,flow Path from Boric Acid Tanks to RCS Found Inoperable.Caused by Ruptured Diaphragm of Boric Acid Transfer Pump Suction Header Isolation Valve 1-CH-80.Valve Diaphragm Replaced ML20028E0441983-01-11011 January 1983 LER 82-085/03L-0:on 821215,w/unit at Full Power,Emergency Diesel Generator 2J Removed from Svc for 7 H to Adjust Voltage Regulator Response Time.Caused by Voltage Regulator Drift.Procedures Will Be Revised ML20028E0201983-01-11011 January 1983 LER 82-084/03L-0:on 821216,during Full Power,Input from Range Nuclear Instrument N-42 to Comparator Drawer N-50 Was in Defeat.Caused by Failure to Take N-42 Out of Defeat After Deviation Alarm Determination.Operators to Be Reinstructed ML20028E0781983-01-11011 January 1983 LER 82-078/03X-1:on 821125,w/unit in Mode 3,120-volt Ac Vital Bus 1-IV Lost Voltage.Caused by Failure of Normal Power Supply Inverter 1-VB-I-04,due to Failed Oscillator Board,Transformer & Fuse.Components Replaced ML20028D1311983-01-0505 January 1983 LER 82-083/03L-0:on 821213,emergency Diesel Generator 2J Removed from Svc.Caused by Failure of 40X Unexcitation Alarm Relay Coil.Carbon Deposits & Arcing Damage of 40/76 Relay Contact Prevented Good Contact ML20028D1571983-01-0505 January 1983 Updated LER 81-071/03X-2:on 810911,hydraulic Snubber on Main Steam Line Discovered Inoperable Due to Loss of Oil from Reservoir.Caused by Leak Due to Scored Brass Bushing on Piston Shaft.Snubber Purged & Refilled.Reach Rod Retorqued ML20028C5191982-12-31031 December 1982 LER 82-083/03L-0:on 821204,while Operating at 17% Rated Thermal Power,Turbine Control Sys Malfunctioned Causing Sudden Increase in Load,Resulting in Reactor Trip.Caused by Malfunction of Analog Converter ML20028A8651982-11-16016 November 1982 LER 82-067/03L-0:on 821019,suction to RHR Sys Pumps a & B Lost for 36 Minutes.On 821020,pump Suction Lost for 33 Minutes.Caused by Ambiguous RCS Level Indication While Water Drained to Centerline of Nozzles.Water Added ML20028A8821982-11-16016 November 1982 LER 82-060/03L-0:on 821019,station Battery I-IV Failed 18- Month Discharge Surveillance Test.Caused by Natural End of Life.Battery Replaced ML20028A9781982-11-16016 November 1982 LER 82-071/03L-0:on 821027,control Power for B Casing Cooling Pump Found de-energized.Caused by Opened Circuit Breaker Unintentionally Disturbed by Workers.Circuit Breaker Closed & Power Verified 1994-04-25
[Table view] Category:RO)
MONTHYEARML20029D0201994-04-25025 April 1994 LER 94-007-01:on 931014,high Head Safety Injection Flow Balance Testing Found to Be Below TS Requirement.Caused by Unaccounted for Uncertainties.Cold Leg Safety Injection Leg Throttle Valve adjusted.W/940425 Ltr ML20045G9391993-07-0808 July 1993 Lr 93-017-00:on 930616,containment Hydrogen Analyzer Heat Trace Channel Calibration Not Performed on Staggered Test Basis Due to Inadequate Implementation of TS Amend.Test Procedure Satisfactorily performed.W/930708 Ltr ML20044H1591993-05-27027 May 1993 LER 93-016-00:on 930509,discovered That Containment Hydrogen Analyzer Pressure Switch PS-3 Sensing Line Disconnected in Local Panel.Caused by Personnel Error. Pressure Switch Calibr & Line reconnected.W/930527 Ltr ML20044D5711993-05-14014 May 1993 LER 93-002-00:on 930416,automatic Reactor Trip Initiated from Turbine Trip Due to Over Excitation of Main Generator. Emergency Procedure 2-E-0 Entered & Individuals Involved in Event Received Remediated training.W/930514 Ltr ML20044D2281993-05-12012 May 1993 LER 93-003-00:on 930424,manual Reactor Trip Initiated Due to Erratic Feedwater Flow Indications to SG C & Excessive Main Feedwater Regulating Valve Oscillations.Caused by Design Instabilities.Secondary Sys secured.W/930512 Ltr ML20044C9541993-05-0707 May 1993 LER 93-015-00:on 930427,discovered That Portions of Containment Pressure Channels That Input to Containment Spray hi-hi Pressure Not Tested Monthly.Caused by Personnel Error.Test Procedures changed.W/930507 Ltr ML20044C9811993-05-0606 May 1993 LER 93-014-00:on 930411,as-found Speed Setting of Steam Driven AFW Pump 1-FW-P-2 Found Below Required TS Limit. Caused by Incorrect Speed Control Setting.Pump Speed Adjusted & Maint Personnel counseled.W/930506 Ltr ML20024G6841991-04-18018 April 1991 LER 91-006-00:on 910403,discovered That Ac Offsite Power Source Surveillance Not Performed Due to Personnel Error. Surveillance Initiated Immediately & Positive Discipline Administered to supervisor.W/910418 Ltr ML20029B5601991-03-0606 March 1991 LER 91-005-00:on 910209,containment Building Penetrations Breached.Caused by Inadequate Procedural Controls.Core Mapping & Cavity Pump Down Activities Secured,Air Hose Removed & Hydrolase Hose capped.W/910306 Ltr ML20029A6471991-02-22022 February 1991 LER 91-004-00:on 910206,sealed Radioactive Source in Storage Not Leak Tested Prior to Use.Caused by Inadequate Procedures for Verifying Leak Testing of Sources.Procedures Revised.W/ 910222 Ltr ML20028H6681991-01-18018 January 1991 LER 90-009-01:on 900719,discovered That Response Time Testing of Pressurizer High Level Reactor Trip Function Not Performed in Accordance W/Tech Spec 3.3.1.1,Table 3.3-2. Caused by Personnel Error.Procedures revised.W/910118 Ltr ML20043H8321990-06-22022 June 1990 LER 90-007-00:on 900523,discovered That Two Sets of Concrete Roof Blocks on Svc Water Pump House Not in Required Safety Position.Caused by Lack of Administrative Controls.Blocks Restored to Required locations.W/900622 Ltr ML20043D5801990-06-0404 June 1990 LER 90-006-00:on 900504,casing Cooling Pump Not Put Into Alert Status & Surveillance Missed.Caused by Personnel Error.Pump 1-RS-P-3B Placed in Alert status.W/900604 Ltr ML20012E3301990-03-27027 March 1990 LER 90-003-00:on 900228,52 Valves Identified Not Included in Tech Spec Required Monthly Containment Integrity Verification Surveillance Program.Caused by Personnel Error & Inadequate Procedure.Procedure revised.W/900327 Ltr ML20012B6441990-03-0808 March 1990 LER 90-001-00:on 900215,inadvertent Partial Train a ESF Actuation of Containment Depressurization Sys Occurred. Caused by Human Error.Evaluation to Be Performed to Determine If Test Points Can Be moved.W/900308 Ltr ML20006E2371990-02-0808 February 1990 LER 90-001-00:on 900123,reactor Trip Occurred on Steam Feedwater Flow Mismatch.Caused by Failed Circuit Driver Card on Feedwater Regulating Valve.Feedwater Regulating Valve Driver Card replaced.W/900208 Ltr ML20006E3771990-02-0505 February 1990 LER 90-002-00:on 900127,fuel Bldg Ventilation Sys Not Aligned to Discharge Through Auxiliary Bldg HEPA Filter & Charcoal Adsorber Assembly During Fuel Movement.Caused by Personnel Error.Disciplinary Action taken.W/900205 Ltr ML20006A8531990-01-19019 January 1990 LER 89-019-00:on 891228,discovered That Outer Door of Containment Equipment Escape Air Lock Was Drawing in Air & Inner Door Noted as Not Being in Fully Closed Position.Cause Undetermined.Sys Enhancements Being evaluated.W/900119 Ltr ML20005F8781990-01-11011 January 1990 LER 89-018-00:on 891219,determined That Three Pressurizer Pressure Safety Injection Instrumentation Channels May Not Have Adequate Margin Between Actuation Setpoint & Bottom of Instrument span.W/900111 Ltr ML19332D5471989-11-22022 November 1989 LER 85-003-03:on 890907,determined That Situation Could Arise Where Water Level Would Rise to 264 Ft Before Next Required Surveillance Interval.Cause Not Determined.Dike to Be constructed.W/891122 Ltr ML20024B7821983-07-0606 July 1983 LER 83-048/03L-0:on 830606 & 17,intermediate Range Channels N35 & N36 High Neutron Flux Reactor Trip Setpoints Exceeded Tech Spec Requirements.Caused by Administrative Error. Setpoints reduced.W/830706 Ltr ML20024C1361983-06-30030 June 1983 LER 83-031/03L-0:on 830614,w/unit at 100% Power,Fire Door S54/5 from Emergency Switchgear Room to Cable Vault Would Not Latch.Fire Watch Posted Immediately.Caused by Misaligned Strike.Door Repaired within 1 h.W/830630 Ltr ML20024C3721983-06-30030 June 1983 LER 83-042/03L-0:on 830606,vital Bus 1-I Momentarily Deenergized While Trying to Clear Inverter Trouble Alarm. Caused by Operator Error.Bus energized.W/830630 Ltr ML20024B9891983-06-28028 June 1983 LER 83-047/03L-0:on 830530,emergency Diesel Generator 2J Tripped on High Crankcase Pressure During Surveillance Testing.Cause Not Determined.Diesel Tested Satisfactorily. W/830628 Ltr ML20024C2941983-06-23023 June 1983 LER 83-044/03L-0:on 830526,during Mode 3,one Recirculation Valve on Each of Two Casing Cooling Pumps Found Open.Caused by Procedure Inadequacy.Valves Closed Immediately.Maint Procedure Will Be revised.W/830623 Ltr ML20024C3071983-06-22022 June 1983 LER 83-034/03L-0:on 830525,during Mode 1,one Header of Control Room Bottled Air Pressurized Sys Had Lower than Required Pressure.Probably Caused by Leak from B Bank of Air Bottles.Header repressurized.W/830622 Ltr ML20024C0971983-06-22022 June 1983 LER 83-045/03L-0:on 830614,Fire Door S71-18,between Emergency Diesel Generator Room 2H & Turbine Bldg,Would Not Latch & Lock.Caused by Stuck Latch.Latch Adjusted & Lubricated.Door Designs modified.W/830622 Ltr ML20023E0951983-06-0101 June 1983 LER 83-027/03L-0:on 830505,one Header (42 Bottles) of Control Room Bottled Air Pressurized Sys Found to Have Lower than Required Pressure (2,290 Vs 2,300 Psig).Probably Caused by Leakage When Compressor malfunctioned.W/830601 Ltr ML20023E0721983-05-26026 May 1983 LER 83-029/03L-0:on 830509,following Rapid Rampdown from 100% to 4% power,I-131 Dose Equivalent Exceeded 1.0 Uci/G. Caused by Unidentified Fuel Element Defect Worsened by post-rampdown Conditions.Sampling increased.W/830526 Ltr ML20023D5371983-05-13013 May 1983 LER 83-022/03L-0:on 830412,review of ASME XI Iwv Program Identified 192 Valves Not Exercised &/Or Stroke Timed.Caused by Fragmented Implementation of Testing Program.Programs Upgraded ML20023D2491983-05-11011 May 1983 LER 83-032/03L-0:on 830412,during Mode 5,visual Insp of Hydraulic Snubber 2-WGCB-HSS-3B Revealed Damaged Reservoir W/O Fluid.Caused by Personnel Working in Area.Snubber Replaced ML20023C5371983-05-10010 May 1983 LER 83-021/03L-0:on 830411,Fire Door S-71-7 Between Svc Bldg Health Physics Area & Auxiliary Bldg Would Not Self Close.Caused by Removal of Reclosure Device for Maint of Closure Coupling.Reclosure Device Reinstalled ML20023B5931983-04-27027 April 1983 LER 83-029/03L-0:on 830402,during Mode 4,automatic Actuation of ECCS Occurred.Caused by Maint Personnel Standing on Conduit Resulting in Loss of lo-lo Pressurizer Pressure Safety Injection Block.Maint Personnel Reinstructed ML20023B5701983-04-27027 April 1983 LER 83-008/03L-0:on 830410,review Revealed That Procedure Used to Restore Boron Injection Tank Concentration Introduced Potential Unanalyzed Injection Flow Diversions. Caused by Oversight.Emergency Procedures Revised ML20028G6541983-02-0909 February 1983 LER 83-003/03L-0:on 830122,during Mode 5,RHR Flow Was Lost for 4 Minutes.Caused by Failure of 15 Kv a Inverter to Ac Vital Bus 1-III,de-energizing Auxiliary Relay for Pressure Channel P-1403.Vital Bus 1-III & RHR Flow Restored ML20028G6311983-02-0909 February 1983 LER 83-016/03L-0:on 830115 & 16,both Open & Closed Containment Isolation Valves TV-SI-200 & TV-CC-204C,train a Position Indication Lights Found Lit.Caused by Leaking Steam Generator Chemical Feed Line Vent Valve ML20028G0781983-01-31031 January 1983 LER 83-001/03L-0:on 830112,primary Grade Water Isolation Valve to Blender 1-CH-217 Remained Open Longer than Tech Spec Requirements.Caused by Personnel Error.Responsible Operator Reinstructed ML20028G0381983-01-28028 January 1983 LER 83-002/03L-0:on 830104,two of Four 2H Emergency Diesel Generator Surveillance Tests Required by Tech Spec Missed During Nov-Dec 1982.Caused by Scheduling Error.Test Frequency Increased to Meet Tech Spec Requirements ML20028G0131983-01-28028 January 1983 LER 83-011/03L-0:on 821119,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps.Caused by Instrument Drift.Indicator Channel for Rods B-09 & 02 & F-06 Recalibr ML20028F3501983-01-19019 January 1983 LER 83-008/03L-0:on 830107,during Mode 3,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps While Withdrawing Shutdown Bank B. Caused by Instrument Drift.Rods Recalibr ML20028E0391983-01-11011 January 1983 Updated LER 82-079/03X-1:on 821126,flow Path from Boric Acid Tanks to RCS Found Inoperable.Caused by Ruptured Diaphragm of Boric Acid Transfer Pump Suction Header Isolation Valve 1-CH-80.Valve Diaphragm Replaced ML20028E0441983-01-11011 January 1983 LER 82-085/03L-0:on 821215,w/unit at Full Power,Emergency Diesel Generator 2J Removed from Svc for 7 H to Adjust Voltage Regulator Response Time.Caused by Voltage Regulator Drift.Procedures Will Be Revised ML20028E0201983-01-11011 January 1983 LER 82-084/03L-0:on 821216,during Full Power,Input from Range Nuclear Instrument N-42 to Comparator Drawer N-50 Was in Defeat.Caused by Failure to Take N-42 Out of Defeat After Deviation Alarm Determination.Operators to Be Reinstructed ML20028E0781983-01-11011 January 1983 LER 82-078/03X-1:on 821125,w/unit in Mode 3,120-volt Ac Vital Bus 1-IV Lost Voltage.Caused by Failure of Normal Power Supply Inverter 1-VB-I-04,due to Failed Oscillator Board,Transformer & Fuse.Components Replaced ML20028D1311983-01-0505 January 1983 LER 82-083/03L-0:on 821213,emergency Diesel Generator 2J Removed from Svc.Caused by Failure of 40X Unexcitation Alarm Relay Coil.Carbon Deposits & Arcing Damage of 40/76 Relay Contact Prevented Good Contact ML20028D1571983-01-0505 January 1983 Updated LER 81-071/03X-2:on 810911,hydraulic Snubber on Main Steam Line Discovered Inoperable Due to Loss of Oil from Reservoir.Caused by Leak Due to Scored Brass Bushing on Piston Shaft.Snubber Purged & Refilled.Reach Rod Retorqued ML20028C5191982-12-31031 December 1982 LER 82-083/03L-0:on 821204,while Operating at 17% Rated Thermal Power,Turbine Control Sys Malfunctioned Causing Sudden Increase in Load,Resulting in Reactor Trip.Caused by Malfunction of Analog Converter ML20028A8651982-11-16016 November 1982 LER 82-067/03L-0:on 821019,suction to RHR Sys Pumps a & B Lost for 36 Minutes.On 821020,pump Suction Lost for 33 Minutes.Caused by Ambiguous RCS Level Indication While Water Drained to Centerline of Nozzles.Water Added ML20028A8821982-11-16016 November 1982 LER 82-060/03L-0:on 821019,station Battery I-IV Failed 18- Month Discharge Surveillance Test.Caused by Natural End of Life.Battery Replaced ML20028A9781982-11-16016 November 1982 LER 82-071/03L-0:on 821027,control Power for B Casing Cooling Pump Found de-energized.Caused by Opened Circuit Breaker Unintentionally Disturbed by Workers.Circuit Breaker Closed & Power Verified 1994-04-25
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N9281999-10-20020 October 1999 Special Rept:On 991003,PZR PORV Actuation Mitigated RCS low- Temp Overpressure Transient.Caused by a RCP Facilitating Sweeping of Entrained Air Out of RCS Loops.Operating Procedure 2-OP-5.1 Will Be Revised ML20217H3631999-10-14014 October 1999 Rev 0 to COLR for North Anna 2 Cycle 14 Pattern Su ML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML20212J9251999-10-0101 October 1999 Safety Evaluation Accepting Licensee Relief Request IWE-3 for Second 10-year ISI for Plant ML20217D6851999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for North Anna Power Station,Units 1 & 2.With ML20211N2611999-09-0808 September 1999 Safety Evaluation Concluding That Proposed Irradiation of Fuel Rods Beyond Current Lead Rod Burnup Limit & Clarification of Terminology with Respect to Reconstituted Fuel Assemblies Acceptable ML20211J2561999-08-31031 August 1999 Safety Evaluation Accepting Elimination of Augmented ISI Program for Pressurizer Spray Lines at North Anna Unit 2 ML20216E5011999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Naps,Units 1 & 2. with ML20211J2421999-08-31031 August 1999 Safety Evaluation Supporting Removal of Augmented Insp Program on RCS Bypass Lines from Licensing Basis of North Anna,Units 1 & 2 ML20210T0791999-08-13013 August 1999 Safety Evaluation Concluding That Revised Withdrawal Schedules for North Anna Units 1 & 2 Satisfy Requirements of App H to 10CFR50 & Therefore Acceptable ML20210S1411999-07-31031 July 1999 Monthly Operating Repts for July 1999 for North Anna Power Station.With ML20210Q9931999-07-31031 July 1999 Rev 1 to COLR for North Anna Power Station,Unit 2 Cycle 13 Pattern Ud ML20209E5641999-06-30030 June 1999 Monthly Operating Repts for June 1999 for North Anna Power Stations,Units 1 & 2.With ML20195G1901999-05-31031 May 1999 Monthly Operating Rept for May 1999 for NAPS Units 1 & 2. with ML20206L4831999-05-10010 May 1999 SER Accepting Request to Delay Submitting Plant,Unit 1 Class 1 Piping ISI Program for Third Insp Interval Until 010430, to Permit Development of Risk Informed ISI Program for Class 1 Piping ML20206Q6671999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for North Anna Power Station,Units 1 & 2.With ML20205S0391999-04-21021 April 1999 SER Accepting Request for Relief IWE5,per 10CFR50.55a(a)(3) & Proposed Alternatives for IWE2,IWE4,IWE6 & IWL2 Authorized Per 10CFR50.55a(a)(3)(ii) ML20205K3041999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for North Anna Power Station,Units 1 & 2.With ML20207K5921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for North Anna Power Station,Units 1 & 2.With ML20207E1731999-02-18018 February 1999 Informs Commission of Status of Preparations of IAEA Osart Mission to North Anna Nuclear Power Plant Early Next Year ML20205A0241998-12-31031 December 1998 Summary of Facility Changes,Tests & Experiments,Including Summary of SEs Implemented at Plant During 1998,per 10CFR50.59(b)(2).With ML20199C8781998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for North Anna Power Station,Units 1 & 2.With ML20198H9541998-12-0303 December 1998 Safety Evaluation Authorizing Proposed Alternative for Remainder of Second 10-yr Insp Interval for Plant ML20198J5561998-12-0303 December 1998 ISI Summary Rept for North Anna Power Station,Unit 1 1998 Refueling Outage Owner Rept for Inservice Insps ML20197G8551998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for North Anna Power Station,Units 1 & 2.With ML20196G1381998-11-0303 November 1998 Safety Evaluation Authorizing Rev to Relief Request NDE-32 for Remainder of Second 10-yr Insp Interval for Each Unit ML20195D0571998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for North Anna Power Station,Units 1 & 2.With ML20154L0691998-10-14014 October 1998 COLR for North Anna Power Station Unit 1 Cycle 14 Pattern Xy ML20155J6911998-10-0909 October 1998 Staff Response to Tasking Memorandum & Stakeholder Concerns ML20154H4001998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for North Anna Power Station,Units 1 & 2.With ML20151X8011998-09-10010 September 1998 Special Rept:On 980622,groundwater Level at Piezometer P-22 Was Again Noted to Be Above Max Water Level by 0.71 Feet. Increased Frequency of Piezometer Monitoring & Installed Addl Piezometers at Toe of Slope Along Southwest Section ML20151W4711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for North Anna Power Station Units 1 & 2.With ML20237A4341998-07-31031 July 1998 Monthly Operating Repts for July 1998 for North Anna Power Station,Units 1 & 2 ML20236V1251998-07-14014 July 1998 ISI Summary Rept for Naps,Unit 2,1998 Refueling Outage Owners Rept of Isis ML20236K5531998-07-0707 July 1998 SER Accepting Request for Change in ISI Commitment on Protection Against Pipe Breaks Outside Containment ML20236M3381998-06-30030 June 1998 Monthly Operating Repts for June 1998 for North Anna Power Station,Units 1 & 2 ML20248M1011998-05-31031 May 1998 Monthly Operating Repts for May 1998 for North Anna Power Station,Units 1 & 2 ML20248C8831998-05-29029 May 1998 SER Accepting Alternatives Proposed by Licensee for Use of Code Case N-535,pursuant to 10CFRa(a)(3)(i) in ASME Section XI Inservice Insp Program ML20247K9281998-05-15015 May 1998 Special Rept:On 980428,letdown PCV Exhibited Slow Response When C RCP Was Started.Cause to Be Determined.Review of Operating Procedure Will Be Performed to Determine If Enhancements Are Necessary ML20216A8971998-05-0606 May 1998 Rev 0 to Cycle 13 Pattern Ud COLR for North Anna Unit 2 ML20247F4441998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for North Anna Power Station,Units 1 & 2 ML20217B5321998-04-20020 April 1998 Safety Evaluation Supporting Proposed Alternative to ASME Code for Surface Exam of Seal Welds on Threaded Caps for Plant Reactor Vessel Head Penetrations for part-length CRDMs ML20217H9611998-04-0707 April 1998 Special Rept:On 980216,groundwater Level at Piezometer P-22, Again Noted to Be Above Max Water Level by 0.41 Feet.Design Package for Installation of Addl Standpipe Piezometers at Toe of Slope Southeast Section,Developed ML20216B1891998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for North Anna Power Station,Units 1 & 2 ML20216E8801998-03-0606 March 1998 Safety Evaluation Authorizing Licensee Request for Relief from ASME Code Requirements,Paragraph IWA-2400(c) (Summer Edition W/Summer 1983 Addenda),For Upcoming Naps,Unit 1 Outage,Per 10CFR50.55a(a)(3)(ii) ML20216E2561998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for North Anna Power Station,Units 1 & 2 ML20199J6431998-02-0202 February 1998 Safety Evaluation Approving Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Code Class 3 SW Piping for North Anna,Unit 1,as Submitted in ISI Relief Request NDE-46 on 971218 ML20202D5811998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for North Anna Power Station,Units 1 & 2 ML20198S7571998-01-15015 January 1998 Safety Evaluation Accepting Licensee Request for Approval to Repair Flaws IAW GL-90-05 for ASME Code Class 3 Svc Water Piping ML20198P1351997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for North Anna Power Station,Units 1 & 2 1999-09-08
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NA?.tE CF PREPARER '
Virginia Electric and Power Company North Anna Power Station, Unit #1
Attachment:
Page 1 of 3 Docket No. 50-338 Report No. LER 80-27/99X-0 Description of Event Coincident with a reactor trip on February 20, 1980, an alarm sounded indicating a noise in "C" steam generator and upper reactor vessel. Impact noise could also be heard on the loose parts monitoring speaker. The "C" reactor coolant pump was shut down and the noise disappeared. The noise resumed when the pump was restarted and then disappeared when full flow was reached. Subsequent testing revealed metal impacts from as many as four separate distinct sources possibly originating from inside the Reactor Coolant System.
Probable Consequences of Occurrence Analysis of noise data obtained by Westinghouse concluded that the reactor is presently in a safe and operable condition as long as the indicated loose parts do not migrate and affect internal plant equipment or interfere with control rod movement. Because the unit remained in a hot standby condition throughout the duration of this analysis, the public health and safety were not affected. There are no generic impli-cations associated with this event.
Cause of Event Although the metal impact noises can be attributed to loose parts, the exact cause and origin of these indications is not known at this time.
Immediate Corrective Action '
Westinghouse specialists were called in to obtain noise data and analyze the results. The objectives of this investigation was to determine if actual loose parts exist and if so the number of objects present, their approximate size, and if possible, their origin. To collect the necessary data, special signal conditioners were substituted for the installed Rockwell signal conditioners in the Loose Parts Monitoring System. The in-containment Rockwell equipment was used without modification.
With special test equipment available, data was recorded on a 14 channel FM recorder, allowing for a frequency of 0-20 KHZ. Signals from the tape recorder then allow simultaneous recording of several channels on a visicorder chart, where time differences of the various impacts of a loosa object (s) from different locations may be determined. Additionally, after noting impacts from ty visicorder charts, or by directly scanning the magnetic tapes, the imr e.s may be examined very closely in the time
, and frequency domain by us- . a spectrum analyzer.
Conclusions of th .nalysis were as follows:
- 1. There are no adications of parts in the bottom of the reactor vess , therefore the part is considered to be on I
the Tg side.
- 2. Upper vessel detector signals are approximately the same when the ro/s are latched and the RCC's raised approximately one foot, nen unlatched with the drive shafts free from i
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Attachment:
Page 2 of 3 !
l l the CRDM. Reactor vessel impact signals are independent of steam generator signals and have the same character as those attributed to impacting of the in-core detector pressure thimble against the guideways.
- 3. Steam generator detector signals were obtained from each steam generator during reactor coolant pump transients; however, no impact indications were noticed during steady 1 full flow operation of the pumps. These impacts could I not be detected by listening by ear to a metallic rod that was in contact with the channel head.
Since testing showed that plant instrumentation and rods were operating normally and because no activity was reported in the steam generators, the plant was determined safe for operation provided the indicated loose parts in the steam generator channel head do not migrate so as to affect internal plant equipment. Rod drop tests were satisfac-torily performed which confirmed free rod movement. Attempts to link the noises with loose parts in the plant secondary side were partially successful in that changes in steam and feed flow tended to produce noticeable effects on detected metal impact frequencies.
Actions recommended by Westinghouse have been conducted on a con-tinuing basis to ensure that the indicated loose parts do not migrate and that the plant remains in a safe and operable condition. From the three sets of nuclear noise data taken, it has been observed that the signals in the 5 to 10 hertz frequency range have increased 33%; however, there is no indication of any structural degradation. The latest analysis of observed metal impacts has concluded the following:
- 1. The impacts are originating from the steam generator secondary side and are being transmitted to the sensors (located on outside of steam generator) by indirect mode.
The upper reactor head noises differ from the steam generator soundings in amplitude only and are suspected to be the result of noise carryover.
- 2. The object weight is believed to be a 1/4 pound or less and as a result no safety concerns exist at this time.
- 3. Westinghouse now believes that there is at least one small object in the secondary side of "B" steam generator with the possibility of more in steam generators "A" and "C".
Scheduled Corrective Action During the next outage of sufficient duration, the secondary side of "B" steam generator will be opened and inspected for loose parts.
Due to the conclusions recently deduced from the ongoing evaluations, the following changes will be made to the original eleven Westinghouse recommended actions. These changes will not be implemented until NRC Region II concurrence is obtained.
- 1. Because the loose part(s) is no longer considered to be in the Reactor Coolant System, present primary side surveil-lance frequencies will be reduced to their normal required periodicity.
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Attachment:
Page 3 of 3
- 2. Operation in reverse flow, due to one or more reactor coolant pumps tripping, will no longer require analysis to determine if loose part indications have migrated.
- 3. Investigations will be performed for secondary side transients instead of primary side transients as previously recommended.
With the preceeding changes incorporated, all Westinghouse recommen-dations will continue to be performed on a regular basis to assist in the attempt to identify and resolve the loose parts problem.
Actions Taken to Prevent Recurrence Actions to be taken will be determined af ter further evaluation and identification of the indicated loose part.