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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2471994-10-0606 October 1994 LER 94-009-00:on 940909,EDG G-02 Inadvertently Started & Station Battery Charger D-08 Tripped Off Due to Blown Fuse. Caused by Inadequate Procedure.Blown Fuse Replaced & Electrical Distribution Sys Restored to normal.W/941006 Ltr ML20029C8511994-04-22022 April 1994 LER 94-001-00:on 940323,identified That Feedwater Flow May Have Been Underestimated Since Beginning of Operating Cycle. Caused by Degradation of Signals from Transducers.Transducer replaced.W/940422 Ltr ML20044E5571993-05-17017 May 1993 LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related Sys ML20044E6221993-05-17017 May 1993 LER 93-006-00:on 930416,discovered That Outside CIV Not Leak Tested,Per TS 15.4.4.III.D Requirements Due to Review on 840202,recommending That Valve Be Tested During RHR Hydrostatic Testing.Subj Valve replaced.W/930517 Ltr ML20044D8811993-05-14014 May 1993 LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function Changed ML20044D2061993-05-10010 May 1993 LER 93-003-00:on 930328,Point Beach Unit 2 Tripped Due to Surveillance Testing Problems.Test Procedures Can Trip Unit Due to Equipment or Human Failure.Failure Tests Delayed Until Unit 1 & Knpp Restored to power.W/930510 Ltr ML20024H2151991-05-21021 May 1991 LER 91-003-00:on 910429,charging Sys Check Valve 1-370 Discovered W/Leakage in Excess of Limits Due to Worn Disc Arm Bushing Steps.Worn Disc Arm Bushing Steps Cladded W/ E308 Weld Matl & Hand Filed to Design contour.W/910521 Ltr ML20029C2101991-03-20020 March 1991 LER 91-002-01:on 901009,inadvertent Start of Auxiliary Feedwater Pump Occurred.Caused by Inadequate Test Procedures.Auxiliary Feedwater Pump Secured & Maint Work Request Mwr 904517 initiated.W/910320 Ltr ML20029C1141991-03-12012 March 1991 LER 91-010-01:on 900816,axial Flux Differential Outside Tech Specs Limits Due to Malfunction of Turbine Electrohydraulic Governor Control.Operator Training Revised. W/910319 Ltr ML20028H0321990-09-27027 September 1990 LER 90-011-00:on 900829,low Net Positive Suction Head to Containment Spray Pumps W/Eccs in Recirculation Mode Occurred.Caused by Procedural Deficiency.Temporary Procedure Changes initiated.W/900927 Ltr ML20043G2011990-06-0808 June 1990 LER 90-005-00:on 900510,steam Generator lo-lo Level Reactor Trip Occurred During Cold Shutdown.Caused by Inadequate Warning Sign Posting.Nonconformance Rept Written to Document Event & Recommend evaluation.W/900608 Ltr ML20042G7761990-05-0909 May 1990 LER 90-003-00:on 900409,determined That Piping & Supports in Fuel Oil Pumphouse Could Not Be Demonstrated to Perform Support Functions.Caused by Design Base Not Sufficiently Documented.Mod Performed to Support Fuel Oil Piping ML20042G7791990-05-0808 May 1990 LER 90-004-00:on 900404,single Failure Potential in Safeguards Switchgear B03/B04 Tie Breaker Discovered & Could Have Resulted in Failure of Diesel Generator.Control Power Fuses for Tie Breakers Removed ML20042F5361990-05-0404 May 1990 LER 90-001-00:on 900405,auxiliary Feed Pump Inadvertently Started.Caused by Inadequate Design.Schematic Push to Test Lamp Circuitry Will Be Added to Elementary Wiring Diagrams & Personnel Briefed on Potential circuitry.W/900504 Ltr ML20042F1971990-05-0202 May 1990 LER 90-002-00:on 900402,main Steam Safety Valve 1-MS-2013 Failed to Relieve Setpoint During Tech Spec Testing.Caused by Personnel Error During Setpoint Adjustment.Safety Valves 1-MS-2011,1-MS-2006 & 1-MS-2008 restored.W/900502 Ltr ML20011D5131989-12-19019 December 1989 LER 89-010-00:on 891120,auxiliary Feedwater Flow Transmitters Inadvertently Isolated.Caused by Error in Approved Procedure & Personnel Cognitive Error.Unit 1 Transmitters Valved Back Into Svc immediately.W/891219 Ltr ML19351A6721989-12-15015 December 1989 LER 89-009-00:on 891115,unexpected Steam Generator a lo-lo Level & Steam Generator B lo-lo Level Reactor Trip Signals Experienced.Caused by Installation of Analog Signal Generator.Procedures revised.W/891215 Ltr ML19332F7011989-12-11011 December 1989 LER 89-008-01:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power.Caused by Less than Adequate Tech Spec Change.Power Descension to 38% initiated.W/891211 Ltr ML19332E7221989-12-0707 December 1989 LER 89-009-00:on 891107,D05 & D06 Station Batteries Declared Inoperable.Caused by Original Design Deficiency.Mod Completed to Restore Battery D05 to Operable Status by Replacing Eight nonsafety-related breakers.W/891207 Ltr ML19332E8921989-12-0404 December 1989 LER 89-008-00:on 891103,during Refueling,Contractor Personnel Generated False Trip Signal While Investigating Wiring Discrepancy in Reactor Protection Sys Instrument Racks.Caused by Labeling Error.Supply changed.W/891204 Ltr ML19332F0901989-11-28028 November 1989 LER 89-003-01:on 890712,tank B Level Channel 2LE-934 Began to Indicate Spuriously.Caused by Moisture Intrusion Between Halar Insulator & Sensing Rod.Level Detector Replaced & Channel Reestablished for Accumulator Tank B.W/891128 Ltr ML19332C8411989-11-22022 November 1989 LER 89-007-00:on 891027,Train a Safety Injection Signal Generated During Installation of Mod in Containment High Pressure Circuit.Caused by Inadequate Installation Procedure.Procedure changed.W/891122 Ltr ML19327C2001989-11-14014 November 1989 LER 89-006-01:on 891015,steam Generator Tubes Found Degraded,W/Undefined Signal & W/Axial Indications in Tubesheet Area.Degradation Caused by Time.Affected Tubes Plugged or Preventively sleeved.W/891114 Ltr ML19327C0651989-11-0606 November 1989 LER 89-005-00:on 891006,intermediate Range High Level Trip Signal Unexpectedly Generated During Course of Routine Source Range Channel Calibr.Caused by Loose Connection of Input/Output Cable.Connection tightened.W/891106 Ltr ML19327B3061989-10-19019 October 1989 LER 89-008-00:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power, Disenabling Sys.Caused by High Tech Spec Setpoint.Enable/ Disable Setpoint Reset to 30%.W/891019 Ltr ML18041A1611987-11-16016 November 1987 LER 87-004-01:on 870515,voltage Lost on Red Instrument Bus Resulting in Reactor Protection Sys Actuation.Caused by Excessive Current Demand by ferro-resonant Circuit.Plant Mods to Load Bank Proposed ML18041A1341986-07-0303 July 1986 LER 86-003-00:on 860603,reactor Trip Occurred Due to Loss of Power on White Instrument Bus.Caused by Trip of White Inverter Output Breaker.Procedures for Placing Inverter on Line Will Be revised.W/860703 Ltr ML20028E3551983-01-13013 January 1983 LER 82-029/03L-0:on 821216,automatic Monitoring & Alarm Program Constant Found Incorrect.Caused by Unknown Personnel W/Access to on-line Computer.Value of Constant Restored & Control Rods Alignment Verified ML20028E2381983-01-13013 January 1983 LER 82-028/03L-0:on 821215,routine Test on Fire Detection Sys Found Panel D407 Which Monitors Unit 1 Rod Drive Room Inoperable.Caused by Blown Fuse.Fuse & Indication Lights Replaced on 821215.Detection Sys Undergoing Design Review ML20028E1791983-01-13013 January 1983 Updated LER 82-020/01X-1:on 821102,while Performing Type B & C Leakage Tests of Containment Penetrations & Isolation Valves,One Valve Had Leakage Exceeding Limit.Cause Not Stated.Valve Clapper & Seat Lapped ML20028E3031983-01-11011 January 1983 LER 82-027/03L-0:on 821211,operator Noted That Steam Generator Pressure Transmitter 1PT-469 Indicated Higher than Other Channels.Caused by Frozen Sensing Line Due to Inadequate Interim Piping Insulation ML20028E3211983-01-10010 January 1983 Updated LER 82-017/01X-2:on 821030,w/unit Shut Down for Refueling,Eddy Current Exam of Steam Generator Tubes Indicated Four Tubes in Steam Generator a & Three Tubes in Steam Generator B Exceeded Plugging Limit.Caused by Caustic ML20028C2431982-12-27027 December 1982 LER 82-020/01T-0:on 821103,following Type B & C Leak Rate Tests,Total as-measured Leakage Exceeded Tech Spec Limit, Causing Reactor Coolant Pump Component Cooling Water to Have Excessive Leakage.Cause Not Stated.Clapper & Seat Lapped ML20023B3251982-12-10010 December 1982 Updated LER 82-017/01T-1:on 821030,verified That Indications for Four Steam Generator a Tubes & Three Steam Generator B Tubes Exceeded 40% Plugging Limit During Eddy Current Exam on 821026-30.Cause Not Stated.Tubes Mechanically Plugged ML20028B4151982-11-15015 November 1982 LER 82-017/01T-0:on 821030,four Tubes in Steam Generator a & Three Tubes in Steam Generator B Indicated Degradation Greater than 40% Plugging Limit.Caused by Intergranular Attack.Tubes Mechanically Plugged ML20028A0371982-11-0505 November 1982 LER 82-008/03L-0:on 821006,low Steam Line Pressure Setting for Pressure Instrument 2PT-478 Found Lower than Allowed by Tech Specs.Caused by Bumping of Setpoint Adjustment Knob.Instrument Tested & Realigned ML20027D6821982-11-0303 November 1982 LER 82-018/01T-0:on 821015,incorrect Instrument Bus Supply Shifted to Alternate Supply Following Rept of Fire in Supply Breaker for 1GYO4 Motor Generator Set,Causing Loss of Redundancy on Containment Pressure Indicator 1PT-950 ML20052G4501982-05-12012 May 1982 LER 82-002/01T-0:on 820428,during Eddy Current Exam, Discovered Abnormal Degradation in Fuel Cladding,Rcpb & Primary Containment.Seludge Lancing Will Be Performed ML20052G3701982-05-0707 May 1982 LER 82-009/03L-0:on 820408,4.16-kV Safeguards Undervoltage Relays Did Not Meet 0-volt Time Delay Spec.Caused by Manufacturer Characteristic Curves.Relays Not Capable of Less than 0.38-s.Tech Spec Change Requested on 820427 ML20052G3831982-05-0707 May 1982 LER 82-011/03L-0:on 820415,during Biweekly Calibr Check ICP 2.1 of Reactor Protective Sys Functions,Overpower Delta T Setpoint 2 for Channel 2 Found Less Conservative than Tech Spec Limit.Caused by Setpoint Drift in Impulse Summer Unit ML20052G6331982-05-0707 May 1982 LER 82-010/03L-0:on 820414,ICP 2.9 Found Not to Provide for Proper Unblocking of Source Range High Flux Reactor Trip Over Small Range of Instrument Readings.Caused by Failure to Identify Subtle Procedural Flow.Procedure to Be Revised ML20052B4521982-04-23023 April 1982 LER 82-008/03L-0:on 820323,minor Installation Defects Noted on Four of Six Containment Pressure Transmitters Installed as TMI Response Mod.Caused by Backfit Contractor QC Program Breakdown ML20050B2661982-03-25025 March 1982 LER 82-006/01T-0:on 820311,type B & C Valve Leakage Tests Exceeded Tech Spec Limits.Caused by Corrosion.Svc Air Check Valves Disc Replaced & Valve Cover Remachined ML20041F4861982-03-0808 March 1982 LER 82-005/01T-01:on 820222,poison Test Samples & Two Fuel Assemblies W/Less than 1-yr Cooling Period Found Placed Next to Divider Wall in Spent Fuel Pool.Caused by Tech Spec Misinterpretation ML20041E4911982-03-0404 March 1982 LER 82-004/03L-0:on 820206,during Inservice Testing, Differential Pressure Instrument 4007 for Auxiliary Feed Pump P38A Found Isolated.Probably Caused by Failure to Return Instrument to Svc Following Calibr ML20041E6131982-03-0202 March 1982 LER 82-003/01T-0:on 820217,during Surveillance Testing, Emergency Diesel Generator 3D Failed to Operate.Caused by Sticking Shutdown Solenoid Plunger on Woodward Type UG8 Governor.Solenoid Cleaned,Checked & Generator Tested ML20049H6981982-02-23023 February 1982 LER 82-001/03L-0:on 820203,boric Acid Heat Tracing Circuit P-42 Found Inoperable.Caused by Failed Thermon Type 4 Circuit Controller.Circuit Controller Replaced ML20040G6811982-02-0505 February 1982 LER 82-001/03L-0:on 820107,steam Generator Pressure Sensing Lines Discovered Frozen on a Steam Generator.Caused by Inadequate Freeze Protection & Extremely Cold Weather.Addl Heat Lamps Installed ML20040G5801982-02-0505 February 1982 LER 82-002/03L-0:on 820112,during Hot shutdown,1PT-469 Steam Generator Pressure Transmitter Isolated by Maint Personnel Due to Leaking Coupling.Pressure Sensing Tubing Showed Signs of Steam Leak Due to Freezing ML20040D3791982-01-18018 January 1982 LER 81-020/03L-0:on 811219,frozen Sensing Line Caused High Indication of Steam Generator Pressure Instrument 1PT-482. Caused by Incomplete Insulation of Line & by Cold Weather. Instrument Placed in Tripped Position & Tubing Thawed 1994-04-22
[Table view] Category:RO)
MONTHYEARML20024J2471994-10-0606 October 1994 LER 94-009-00:on 940909,EDG G-02 Inadvertently Started & Station Battery Charger D-08 Tripped Off Due to Blown Fuse. Caused by Inadequate Procedure.Blown Fuse Replaced & Electrical Distribution Sys Restored to normal.W/941006 Ltr ML20029C8511994-04-22022 April 1994 LER 94-001-00:on 940323,identified That Feedwater Flow May Have Been Underestimated Since Beginning of Operating Cycle. Caused by Degradation of Signals from Transducers.Transducer replaced.W/940422 Ltr ML20044E5571993-05-17017 May 1993 LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related Sys ML20044E6221993-05-17017 May 1993 LER 93-006-00:on 930416,discovered That Outside CIV Not Leak Tested,Per TS 15.4.4.III.D Requirements Due to Review on 840202,recommending That Valve Be Tested During RHR Hydrostatic Testing.Subj Valve replaced.W/930517 Ltr ML20044D8811993-05-14014 May 1993 LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function Changed ML20044D2061993-05-10010 May 1993 LER 93-003-00:on 930328,Point Beach Unit 2 Tripped Due to Surveillance Testing Problems.Test Procedures Can Trip Unit Due to Equipment or Human Failure.Failure Tests Delayed Until Unit 1 & Knpp Restored to power.W/930510 Ltr ML20024H2151991-05-21021 May 1991 LER 91-003-00:on 910429,charging Sys Check Valve 1-370 Discovered W/Leakage in Excess of Limits Due to Worn Disc Arm Bushing Steps.Worn Disc Arm Bushing Steps Cladded W/ E308 Weld Matl & Hand Filed to Design contour.W/910521 Ltr ML20029C2101991-03-20020 March 1991 LER 91-002-01:on 901009,inadvertent Start of Auxiliary Feedwater Pump Occurred.Caused by Inadequate Test Procedures.Auxiliary Feedwater Pump Secured & Maint Work Request Mwr 904517 initiated.W/910320 Ltr ML20029C1141991-03-12012 March 1991 LER 91-010-01:on 900816,axial Flux Differential Outside Tech Specs Limits Due to Malfunction of Turbine Electrohydraulic Governor Control.Operator Training Revised. W/910319 Ltr ML20028H0321990-09-27027 September 1990 LER 90-011-00:on 900829,low Net Positive Suction Head to Containment Spray Pumps W/Eccs in Recirculation Mode Occurred.Caused by Procedural Deficiency.Temporary Procedure Changes initiated.W/900927 Ltr ML20043G2011990-06-0808 June 1990 LER 90-005-00:on 900510,steam Generator lo-lo Level Reactor Trip Occurred During Cold Shutdown.Caused by Inadequate Warning Sign Posting.Nonconformance Rept Written to Document Event & Recommend evaluation.W/900608 Ltr ML20042G7761990-05-0909 May 1990 LER 90-003-00:on 900409,determined That Piping & Supports in Fuel Oil Pumphouse Could Not Be Demonstrated to Perform Support Functions.Caused by Design Base Not Sufficiently Documented.Mod Performed to Support Fuel Oil Piping ML20042G7791990-05-0808 May 1990 LER 90-004-00:on 900404,single Failure Potential in Safeguards Switchgear B03/B04 Tie Breaker Discovered & Could Have Resulted in Failure of Diesel Generator.Control Power Fuses for Tie Breakers Removed ML20042F5361990-05-0404 May 1990 LER 90-001-00:on 900405,auxiliary Feed Pump Inadvertently Started.Caused by Inadequate Design.Schematic Push to Test Lamp Circuitry Will Be Added to Elementary Wiring Diagrams & Personnel Briefed on Potential circuitry.W/900504 Ltr ML20042F1971990-05-0202 May 1990 LER 90-002-00:on 900402,main Steam Safety Valve 1-MS-2013 Failed to Relieve Setpoint During Tech Spec Testing.Caused by Personnel Error During Setpoint Adjustment.Safety Valves 1-MS-2011,1-MS-2006 & 1-MS-2008 restored.W/900502 Ltr ML20011D5131989-12-19019 December 1989 LER 89-010-00:on 891120,auxiliary Feedwater Flow Transmitters Inadvertently Isolated.Caused by Error in Approved Procedure & Personnel Cognitive Error.Unit 1 Transmitters Valved Back Into Svc immediately.W/891219 Ltr ML19351A6721989-12-15015 December 1989 LER 89-009-00:on 891115,unexpected Steam Generator a lo-lo Level & Steam Generator B lo-lo Level Reactor Trip Signals Experienced.Caused by Installation of Analog Signal Generator.Procedures revised.W/891215 Ltr ML19332F7011989-12-11011 December 1989 LER 89-008-01:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power.Caused by Less than Adequate Tech Spec Change.Power Descension to 38% initiated.W/891211 Ltr ML19332E7221989-12-0707 December 1989 LER 89-009-00:on 891107,D05 & D06 Station Batteries Declared Inoperable.Caused by Original Design Deficiency.Mod Completed to Restore Battery D05 to Operable Status by Replacing Eight nonsafety-related breakers.W/891207 Ltr ML19332E8921989-12-0404 December 1989 LER 89-008-00:on 891103,during Refueling,Contractor Personnel Generated False Trip Signal While Investigating Wiring Discrepancy in Reactor Protection Sys Instrument Racks.Caused by Labeling Error.Supply changed.W/891204 Ltr ML19332F0901989-11-28028 November 1989 LER 89-003-01:on 890712,tank B Level Channel 2LE-934 Began to Indicate Spuriously.Caused by Moisture Intrusion Between Halar Insulator & Sensing Rod.Level Detector Replaced & Channel Reestablished for Accumulator Tank B.W/891128 Ltr ML19332C8411989-11-22022 November 1989 LER 89-007-00:on 891027,Train a Safety Injection Signal Generated During Installation of Mod in Containment High Pressure Circuit.Caused by Inadequate Installation Procedure.Procedure changed.W/891122 Ltr ML19327C2001989-11-14014 November 1989 LER 89-006-01:on 891015,steam Generator Tubes Found Degraded,W/Undefined Signal & W/Axial Indications in Tubesheet Area.Degradation Caused by Time.Affected Tubes Plugged or Preventively sleeved.W/891114 Ltr ML19327C0651989-11-0606 November 1989 LER 89-005-00:on 891006,intermediate Range High Level Trip Signal Unexpectedly Generated During Course of Routine Source Range Channel Calibr.Caused by Loose Connection of Input/Output Cable.Connection tightened.W/891106 Ltr ML19327B3061989-10-19019 October 1989 LER 89-008-00:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power, Disenabling Sys.Caused by High Tech Spec Setpoint.Enable/ Disable Setpoint Reset to 30%.W/891019 Ltr ML18041A1611987-11-16016 November 1987 LER 87-004-01:on 870515,voltage Lost on Red Instrument Bus Resulting in Reactor Protection Sys Actuation.Caused by Excessive Current Demand by ferro-resonant Circuit.Plant Mods to Load Bank Proposed ML18041A1341986-07-0303 July 1986 LER 86-003-00:on 860603,reactor Trip Occurred Due to Loss of Power on White Instrument Bus.Caused by Trip of White Inverter Output Breaker.Procedures for Placing Inverter on Line Will Be revised.W/860703 Ltr ML20028E3551983-01-13013 January 1983 LER 82-029/03L-0:on 821216,automatic Monitoring & Alarm Program Constant Found Incorrect.Caused by Unknown Personnel W/Access to on-line Computer.Value of Constant Restored & Control Rods Alignment Verified ML20028E2381983-01-13013 January 1983 LER 82-028/03L-0:on 821215,routine Test on Fire Detection Sys Found Panel D407 Which Monitors Unit 1 Rod Drive Room Inoperable.Caused by Blown Fuse.Fuse & Indication Lights Replaced on 821215.Detection Sys Undergoing Design Review ML20028E1791983-01-13013 January 1983 Updated LER 82-020/01X-1:on 821102,while Performing Type B & C Leakage Tests of Containment Penetrations & Isolation Valves,One Valve Had Leakage Exceeding Limit.Cause Not Stated.Valve Clapper & Seat Lapped ML20028E3031983-01-11011 January 1983 LER 82-027/03L-0:on 821211,operator Noted That Steam Generator Pressure Transmitter 1PT-469 Indicated Higher than Other Channels.Caused by Frozen Sensing Line Due to Inadequate Interim Piping Insulation ML20028E3211983-01-10010 January 1983 Updated LER 82-017/01X-2:on 821030,w/unit Shut Down for Refueling,Eddy Current Exam of Steam Generator Tubes Indicated Four Tubes in Steam Generator a & Three Tubes in Steam Generator B Exceeded Plugging Limit.Caused by Caustic ML20028C2431982-12-27027 December 1982 LER 82-020/01T-0:on 821103,following Type B & C Leak Rate Tests,Total as-measured Leakage Exceeded Tech Spec Limit, Causing Reactor Coolant Pump Component Cooling Water to Have Excessive Leakage.Cause Not Stated.Clapper & Seat Lapped ML20023B3251982-12-10010 December 1982 Updated LER 82-017/01T-1:on 821030,verified That Indications for Four Steam Generator a Tubes & Three Steam Generator B Tubes Exceeded 40% Plugging Limit During Eddy Current Exam on 821026-30.Cause Not Stated.Tubes Mechanically Plugged ML20028B4151982-11-15015 November 1982 LER 82-017/01T-0:on 821030,four Tubes in Steam Generator a & Three Tubes in Steam Generator B Indicated Degradation Greater than 40% Plugging Limit.Caused by Intergranular Attack.Tubes Mechanically Plugged ML20028A0371982-11-0505 November 1982 LER 82-008/03L-0:on 821006,low Steam Line Pressure Setting for Pressure Instrument 2PT-478 Found Lower than Allowed by Tech Specs.Caused by Bumping of Setpoint Adjustment Knob.Instrument Tested & Realigned ML20027D6821982-11-0303 November 1982 LER 82-018/01T-0:on 821015,incorrect Instrument Bus Supply Shifted to Alternate Supply Following Rept of Fire in Supply Breaker for 1GYO4 Motor Generator Set,Causing Loss of Redundancy on Containment Pressure Indicator 1PT-950 ML20052G4501982-05-12012 May 1982 LER 82-002/01T-0:on 820428,during Eddy Current Exam, Discovered Abnormal Degradation in Fuel Cladding,Rcpb & Primary Containment.Seludge Lancing Will Be Performed ML20052G3701982-05-0707 May 1982 LER 82-009/03L-0:on 820408,4.16-kV Safeguards Undervoltage Relays Did Not Meet 0-volt Time Delay Spec.Caused by Manufacturer Characteristic Curves.Relays Not Capable of Less than 0.38-s.Tech Spec Change Requested on 820427 ML20052G3831982-05-0707 May 1982 LER 82-011/03L-0:on 820415,during Biweekly Calibr Check ICP 2.1 of Reactor Protective Sys Functions,Overpower Delta T Setpoint 2 for Channel 2 Found Less Conservative than Tech Spec Limit.Caused by Setpoint Drift in Impulse Summer Unit ML20052G6331982-05-0707 May 1982 LER 82-010/03L-0:on 820414,ICP 2.9 Found Not to Provide for Proper Unblocking of Source Range High Flux Reactor Trip Over Small Range of Instrument Readings.Caused by Failure to Identify Subtle Procedural Flow.Procedure to Be Revised ML20052B4521982-04-23023 April 1982 LER 82-008/03L-0:on 820323,minor Installation Defects Noted on Four of Six Containment Pressure Transmitters Installed as TMI Response Mod.Caused by Backfit Contractor QC Program Breakdown ML20050B2661982-03-25025 March 1982 LER 82-006/01T-0:on 820311,type B & C Valve Leakage Tests Exceeded Tech Spec Limits.Caused by Corrosion.Svc Air Check Valves Disc Replaced & Valve Cover Remachined ML20041F4861982-03-0808 March 1982 LER 82-005/01T-01:on 820222,poison Test Samples & Two Fuel Assemblies W/Less than 1-yr Cooling Period Found Placed Next to Divider Wall in Spent Fuel Pool.Caused by Tech Spec Misinterpretation ML20041E4911982-03-0404 March 1982 LER 82-004/03L-0:on 820206,during Inservice Testing, Differential Pressure Instrument 4007 for Auxiliary Feed Pump P38A Found Isolated.Probably Caused by Failure to Return Instrument to Svc Following Calibr ML20041E6131982-03-0202 March 1982 LER 82-003/01T-0:on 820217,during Surveillance Testing, Emergency Diesel Generator 3D Failed to Operate.Caused by Sticking Shutdown Solenoid Plunger on Woodward Type UG8 Governor.Solenoid Cleaned,Checked & Generator Tested ML20049H6981982-02-23023 February 1982 LER 82-001/03L-0:on 820203,boric Acid Heat Tracing Circuit P-42 Found Inoperable.Caused by Failed Thermon Type 4 Circuit Controller.Circuit Controller Replaced ML20040G6811982-02-0505 February 1982 LER 82-001/03L-0:on 820107,steam Generator Pressure Sensing Lines Discovered Frozen on a Steam Generator.Caused by Inadequate Freeze Protection & Extremely Cold Weather.Addl Heat Lamps Installed ML20040G5801982-02-0505 February 1982 LER 82-002/03L-0:on 820112,during Hot shutdown,1PT-469 Steam Generator Pressure Transmitter Isolated by Maint Personnel Due to Leaking Coupling.Pressure Sensing Tubing Showed Signs of Steam Leak Due to Freezing ML20040D3791982-01-18018 January 1982 LER 81-020/03L-0:on 811219,frozen Sensing Line Caused High Indication of Steam Generator Pressure Instrument 1PT-482. Caused by Incomplete Insulation of Line & by Cold Weather. Instrument Placed in Tripped Position & Tubing Thawed 1994-04-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARNPL-99-0569, Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with ML20212D5961999-09-15015 September 1999 Safety Evaluation Supporting Licensee IPEEE Process.Plant Has Met Intent of Suppl 4 to GL 88-20 NPL-99-0051, Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with NPL-99-0449, Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with ML20196J4251999-06-30030 June 1999 Safety Evaluation Authorizing Proposed Alternatives Described in Relief Requests VRR-01,ROJ-16,PRR-01 & VRR-02 ML20209D2691999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbnps,Units 1 & 2 ML20196F3341999-06-22022 June 1999 Safety Evaluation for Implementation of 422V+ Fuel Assemblies at Pbnp Units 1 & 2 ML20195F9781999-06-10010 June 1999 Unit 2 Refueling 23 Inservice Insp Summary Rept for Form NIS-1 ML20209D2751999-05-31031 May 1999 Revised MORs for May 1999 for Pbnps,Units 1 & 2 NPL-99-0328, Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with NPL-99-0273, Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With ML20196F3521999-04-30030 April 1999 Non-proprietary WCAP-14788, W Revised Thermal Design Procedure Instrument Uncertainty Methodology for Wepc Point Beach Units 1 & 2 (Fuel Upgrade & Uprate to 1656 Mwt - NSSS Power) NPL-99-0193, Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with NPL-99-0134, Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with ML20207D6751999-02-22022 February 1999 Assessment of Design Info on Piping Restraints for Point Beach Nuclear Plant,Units 1 & 2.Staff Concludes That Licensee Unable to Retrieve Original Analyses That May Have Been Performed to Justify Removal of Shim Collars ML20206R9001999-01-13013 January 1999 SER Accepting Nuclear Quality Assurance Program Changes for Point Beach Nuclear Plant,Units 1 & 2 NPL-99-0008, Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with NPL-99-0091, 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with1998-12-31031 December 1998 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with ML20198C7671998-12-10010 December 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME BPV Code,1986 Edition,Section XI Requirement IWA-2232, to Use Performance Demonstration Initiative Program During RPV Third 10-yr ISI for Plant,Unit 2 NPL-98-1006, Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20195J5101998-11-16016 November 1998 Proposed Revs to Section 1.3 of FSAR for Pbnp QA Program ML20198J5941998-11-0303 November 1998 1998 Graded Exercise,Conducted on 981103 NPL-98-0948, Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With NPL-98-0880, Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored1998-10-21021 October 1998 Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored ML20154M9121998-10-14014 October 1998 Unit 1 Refueling 24 Repair/Replacement Summary Rept for Form NIS-2 ML20154L6751998-10-14014 October 1998 Unit 1 Refueling 24 ISI Summary Rept for Form NIS-1 NPL-98-0826, Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20151W3851998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Pbnp Units 1 & 2 NPL-98-0653, Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4471998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 2 ML20151W4541998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 1 ML20236Q3161998-07-10010 July 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME Code Requirements PTP-3-01 & PTP-3-02 ML20236L6771998-07-0707 July 1998 Safety Evaluation Approving Wepco Implementation Program to Resolve USI A-46 at Point Beach NPP Units 1 & 2 NPL-98-0558, Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 2 ML20151W4261998-06-30030 June 1998 Corrected Page to MOR for June 1998 for Pbnp Unit 2 ML20151W4221998-05-31031 May 1998 Corrected Page to MOR for May 1998 for Pbnp Unit 2 NPL-98-0481, Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4011998-04-30030 April 1998 Corrected Page to MOR for April 1998 for Pbnp Unit 2 NPL-98-0356, Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20217F3131998-04-17017 April 1998 Safety Evaluation Accepting Proposed Alternative to ASME Code for Surface Exam of Nonstructural Seal Welds,For Plant, Unit 1 ML20216D7071998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3981998-03-31031 March 1998 Corrected Page to MOR for March for Pbnp Unit 2 NPL-98-0209, Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable1998-03-30030 March 1998 Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable ML20217A8501998-03-19019 March 1998 SER Accepting Proposed Changes Submitted on 980226 by Wiep to Pbnp Final SAR Section 1.8 Which Will Impact Commitments Made in Pbnp QA Program Description.Changes Concern Approval Authority for Procedures & Interviewing Authority ML20216J0101998-03-17017 March 1998 Safety Evaluation Accepting Third 10-yr Inservice Insp Interval Relief Request RR-1-18 for Plant NPL-98-0159, Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3891998-02-28028 February 1998 Corrected Page to MOR for Feb 1998 for Pbnp Unit 2 ML20216D7121998-02-28028 February 1998 Revised Corrected MOR for Feb 1998 for Point Beach Nuclear Plant,Unit 2 NPL-98-0084, Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 21998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20198L1151998-01-0808 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Point Beach Nuclear Plant,Units 1 & 2 1999-09-30
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FORM 1 LER SCSS DATA 09-23-91 DOCKET YEAR LER NUMBER REVXSION DCS NUMBER NSIC EVENT DATE 266 1986 003 0 8607090090 199975 06/03/86 DOCKET:266 POINT BEACH 1 TYPE:PWR REGION: 3 NSSS:WE ARCHITECTURAL ENGINEER: BECH FACILITY OPERATOR: WXSCONSIN ELECTRIC POWER CO.
SYMBOL: WEP COMMENTS STEPS 38-43: COMPLETE DESCRXPTXON OF UNIT 2 EVENT GIVEN IN LER 301/86-003.
WATCH 975 TRANSIENT INITIATED ON BOTH UNITS DUE TO SINGLE FAILURE.
WATCH-LIST CODES FOR THIS LER ARE:
975 POSSIBLE SIGNIFICANT EVENT REPORTABILITY CODES FOR THIS LER ARE:
13 10 CFR 50.73(a)(2)(iv): ESF actuations.
REFERENCE LERS 1 301/86-003 ABSTRACT POWER LEVEL 100~os ON 6 3 86i UNIT 1 AT POINT BEACH NUCLEAR PLANT EXPERIENCED A REACTOR TRIP DUE TO THE LOSS OF POWER ON THE WHITE INSTRUMENT BUS. THE POWER LOSS WAS DUE TO THE TRIP OF THE WHITE INVERTER (1DY03) OUTPUT BREAKER FEEDING THE WHITE INSTRUMENT BUS. THE BREAKER TRIP WAS CAUSED WHEN'FTER MAINTENANCEi THE SWING INVERTER (DYOC) WAS INCORRECTLY RESTORED TO OPERATION ON THE DC BUS FEEDING THE WHITE INVERTERS TO BOTH UNIT 1 AND UNIT 2 (1DY03 AND 2DY03 RESPECTIVELY). THE WHITE INSTRUMENT BUS SUPPLIES A CHANNEL OF POWER RANGE NUCLEAR INSTRUMENTATION. WHEN POWER WAS INTERRUPTED, THIS INSTRUMENTATION GENERATED A 204 LOAD REFERENCE TURBINE RUNBACK FROM ITS DROPPED ROD DETECTION CIRCUITRY. THE STEP DECREASE IN POWER CAUSED THE STEAM DUMP SYSTEM TO ARM. BECAUSE THE WHITE BUS ALSO SUPPLIES POWER TO THE TREF XNSTRUMENTi TREF FAILED LOW GENERATING A TEMPERATURE DEVIATION SIGNAL WHICH CAUSED THE STEAM DUMPS TO GO FULL OPEN AND CONTROL RODS TO STEP IN AT MAXIMUM SPEED. THESE EVENTS CREATED A PRIMARY SYSTEM COOLDOWN WHICH CAUSED PRXMARY SYSTEM PRESSURE TO DECRESE BELOW THE REACTOR TRIP SETPOINT. THE REACTOR TRIPPED.
THE PRIMARY SYSTEM CONTINUED TO COOL DOWN AFTER THE REACTOR TRIP WHEN THE AUXILIARY FEEDWATER SYSTEM AUTOMATICALLY STARTED. THIS COOLDOWN RESULTED IN ACTUATION OF THE SAFETY INJECTION SYSTEM. ALL SAFETY SYSTEMS FUNCTIONED AS DESIGN. PLANT SYSTEMS WERE STABILIZED AND SAFEGUARDS CIRCUITS RESET.
'OCKET YEAR LER NUMBER REVISION DCS NUMBER NSIC EVENT DATE 311 1982 145 1 8301250373 181466 11/29/82 DOCKET:311 SALEM 2 TYPE:PWR REGION: 1 NSSS WE ARCHITECTURAL ENGINEER: PSEG FACILITY OPERATOR: PUBLIC SERVICE ELECTRIC & GAS CO.
SYMBOL: PEG ABSTRACT ON NOVEMBER 29'982'OLLOWING A SHIFT OF NO ~ 2B VITAL BUS POWER SOURCE IN PREPARATION FOR PLANNED MAINTENANCE ON NO. 1 STATION POWER TRANSFORMERS THE CONTROL ROOM OPERATOR OBSERVED THAT THE P 250 COMPUTER HAD SHUT DOWN. SINCE IT UTILIZES THE COMPUTER DATA AND MEMORY, THE REACTOR COOLANT SYSTEM (RCS) SUBCOOLING MONITOR WAS RENDERED INOPERABLE, AND ACTION STATEMENT 3.3.3.7A WAS ENTERED.
REDUNDANT WIDE RANGE RCS PRESSURE AND TEMPERATURE INDICATION AND STEAM TABLES WERE AVAILABLE, AND THE EVENT CONSTITUTED OPERATION IN A DEGRADED MODE IN ACCORDANCE WITH TECH SPEC 6.9.1.9.B. INVESTIGATION REVEALED THAT THE COMPUTER HAD SHUT DOWN DUE TO FAILURE OF THE INVERTER POWER SUPPLY. THE POWER SUPPLY PROBLEM RESULTED FROM A FAILED OSCILLATOR CIRCUIT BOARD. THE BOARD WAS REPLACED, THE COMPUTER WAS RESTORED TO OPERATION AND THE ACTION STATEMENT WAS TERMINATED.
II DOCKET YEAR LER NUMBER REVISION DCS NUMBER NSIC EVENT DATE 361 1990 016 0 9101140111 220676 12/06/90 DOCKET:361 SAN ONOFRE 2 TYPE:PWR REGION: 5 NSSS:CE ARCHITECTURAL ENGINEER: BECH FACILITY OPERATOR: SOUTHERN CALIFORNIA EDISON CO.
SYMBOL: SCE COMMENTS STEP 2: REM MANUFACTURED BY CORNELL-DUBLIER ELECTRIC, PART NO. CDE KBXK1056P OR SCI 020138. STEP 17: PART NO. SCX PC201. STEP 9: CAUSE IX MOMENTARY LOSS OF POWER. STEP 16: COMP MSC TRANSISTOR. STEP 11: COMP MSC MECHANICAL LINKAGE. STEP 25: COMP XR SEQUENCE OF EVENTS RECORDER.
WATCH-LIST CODES FOR THIS LER ARE:
20 EQUIPMENT FAILURE 34 DESIGN ERROR OR INADEQUACY 913 UPDATE NEEDED REPORTABILITY CODES FOR THIS LER ARE:
13 10 CFR 50.73(a)(2)(iv): ESF actuations.
REFERENCE LERS:
1 362/89-001 ABSTRACT POWER LEVEL 100'T 2200 ON DECEMBER 6i 1990i UNIT 2 AUTOMATICALLY TRIPPED FROM 1004 POWER ON A REACTOR PROTECTION SYSTEM LOSS OF LOAD (LOL) SIGNAL. THE LOL SIGNAL WAS CAUSED BY A TURBINE TRIP, WHXCH OCCURRED AS A RESULT OF A MOMENTARY LOSS OF POWER FROM THE NON-1E UNXNTERRUPTIBLE POWER SYSTEM (UPS)g MOMENTARILY DE ENERGIZING BUS Q-069. EMERGENCY FEEDWATER ACTUATION SYSTEM (EFAS) 1 AND EFAS 2 ACTUATIONS PROPERLY OCCURRED. ONE 6.9 KV BUS DID NOT AUTOMATICALLY TRANSFER TO OFFSITE POWER FOLLOWING THE TRXPg DE ENERGIZING 2 REACTOR COOLANT PUMPS (RCPS); TWO OTHER RCPS CONTINUED TO PROVIDE FORCED CIRCULATION'PPROXIMATELY 1 TO 2 MINUTES FOLLOWING THE TRIPg A COMPLETE LOSS OF POWER ON Q-069 OCCURRED. APPROPRIATE ACTIONS WERE INITIATED IN ACCORDANCE WITH PROCEDURES TO COMPENSATE FOR THE OPERATION OF CONTROL SYSTEMS WHICH WERE AFFECTED BY THE LOSS OF POWER ON Q-069. ONE MAIN STEAM SAFETY VALVE FOR EACH STEAM GENERATOR MAY HAVE LIFTED FOR A SHORT TIME AND PROPERLY RESEATED. BUS Q-069 POWER WAS RESTORED AT 2220 VIA THE MANUAL BYPASS SWITCH. RECOVERY OF THE PLANT OTHERWISE PROCEEDED NORMALLY. IT IS POSTULATED THAT FAILURE OF
- 1) A CAPACITOR IN THE NON-1E UPS INVERTER OUTPUT AND 2) A TRANSXSTOR IN THE STATIC SWITCH TRANSFER LOGIC CONTROL CIRCUIT COMBINED TO CAUSE THE LOSS OF POWER ON BUS Q-069 (BOTH AT THE ONSET OF THE EVENT AND AT 1-2 MINUTES POST-TRIP). THE ROOT CAUSE EVALUATION IS CONTINUING.
DOCKET YEAR LER NUMBER REVISION DCS NUMBER NSIC EVENT DATE 362 1991 001 0 9104220351 221467 03/15/91 DOCKET:362 SAN ONOFRE 3 TYPE:PWR REGION: 5 NSSS:CE ARCHXTECTURAL ENGINEER: BECH FACILITY OPERATOR: SOUTHERN CALIFORNIA EDISON CO.
SYMBOL: SCE COMMENTS STEP 2: PART NO. CDE KBXK1056PX OR SCI 020138.
NATCH-LIST CODES FOR THXS LER ARE:
20 EQUIPMENT FAILURE REPORTABXLITY CODES FOR THIS LER ARE:
13 10 CFR 50.73(a)(2)(iv): ESF actuations.
REFERENCE LERS:
1 361/86-029 2 361/90-016 3 362/89-001 ABSTRACT POWER LEVEL 100~os AT 0938 ON MARCH 15'991i UNIT 3 AUTOMATICALLY TRIPPED FROM 100~o POWER ON A REACTOR PROTECTION SYSTEM LOSS OF LOAD (LOL) SIGNAL THE LOL SIGNAL WAS CAUSED BY A TURBINE TRIPi WHICH OCCURRED AS THE RESULT OF A MOMENTARY INTERRUPTION IN POWER FROM THE NON-lE UNINTERRUPTIBLE POWER SYSTEM (UPS), DE-ENERGIZING BUS 3Q069.
EMERGENCY FEEDWATER ACTUATION SYSTEM (EFAS) 1 AND EFAS 2 ACTUATIONS PROPERLY OCCURRED. ONE NON-1E 4.16 KV (3A03) BUS DID NOT AUTOMATICALLYTRANSFER FROM ITS NORMAL POWER SOURCE TO ITS ALTERNATE POWER SOURCE RESULTING IN THE LOSS OF THE ALTERNATE POWER SUPPLY (3B012) TO THE NON-1E BUS 3Q069. ONE MAIN STEAM SAFETY VALVE LIFTED FOR A SHORT TIME AND PROPERLY RESEATED. AT 1000, WHEN 3A03 WAS MANUALLY REENERGIZEDi POWER WAS RESTORED TO 3Q069 ~ APPROPRIATE ACTIONS WERE TAKEN IN ACCORDANCE WITH PROCEDURES TO COMPENSATE FOR THE OPERATION OF CONTROL SYSTEMS WHICH WERE AFFECTED BY THE LOSS OF POWER TO THE NON-1E UPS. POST-TRIP PLANT RECOVERY OTHERWISE PROCEEDED NORMALLY. AN OUTPUT CAPACITOR IN THE CONSTANT VOLTAGE TRANSFORMER (CVT) SECTION OF THE NON-1E UPS INVERTER FAILED CAUSING THE MOMENTARY INTERRUPTION IN POWER FROM THE NON-1E UPS. ALL CAPACITORS IN THE UNITS 2 AND 3 NON-1E UPS WERE REPLACED WITH AN UPGRADED MODEL. THE UNIT 3 INSTRUMENT BUSSES POWERED BY THE NON-1E UPS WERE MODIFIED SUCH THAT POWER WILL BE MAINTAINED TO CRITICAL COMPONENT SYSTEMS.
DOCKET YEAR LER NUMBER REVISION DCS NUMBER NSIC EVENT DATE 369 1984 024 0 8412010048 192511 08/21/84 DOCKET:369 MCGUIRE 1 TYPE PWR REGION: 2 NSSS:WE ARCHITECTURAL ENGINEER: DUKE FACILITY OPERATOR: DUKE POWER CO.
SYMBOL: DPC COMMENTS STEP 16: CAUSE XX VOLTAGE SPIKE. STEP 6 COMP RLX CONTROL OUTPUT RELAY.
NATCH-LIST CODES FOR THIS LER ARE:
975 POSSIBLE SI GNIFXCANT EVENT REPORTABILITY CODES FOR THIS LER ARE:
14 10 CFR 50.73(a)(2)(v): Event that could have prevented fulfillment of a safety function.
ABSTRACT POWER LEVEL 100'T 2400 ON 8 20 84i THE MCGUIRE SWITCHYARD COMPUTER WAS REPORTED INOPERABLE. ON 8-21-84, COMPUTER AND INVERTER MAINTENANCE PERSONNEL PERFORMED CORRECTIVE MAINTENANCE ON THE SWXTCHYARD COMPUTER AND STATIC INVERTER. AT 2114, THE SWITCHYARD COMPUTER WAS RE STARTEDi CHECKED FOR OPERABXLITYi AND RETURNED TO SERVICE. AT 2148, WHEN THE SWITCHYARD OPERATOR RE-ENABLED THE I I COMPUTER CONTROL OUTPUTS g 3 0 POWER C RCU T BREAKERS ( PCBS ) AND ASSOCIATED DISCONNECTS OPENED i RESULTING XN MCGUIRE UNIT 1 REACTOR TRIP AND TURBINE TRIP, LOSS OF UNIT 1 OFFSITE AC POWER, AND STARTUP OF UNIT 1 DGS A AND BE UNIT 1 WAS IN MODE 1 AT 100+o POWER AT THE TIME THIS INCIDENT IS CLASSIFIED AS A COMPONENT MALFUNCTION/FAILURE BECAUSE THE CONTROL CIRCUITS WERE CHANGED TO AN UNDESIRABLE STATE WITHOUT A COMMAND FROM THE COMPUTER, DURING COMPUTER AND INVERTER MAINTENANCE. DESIGN DEFICIENCY ALSO CONTRIBUTED BECAUSE THE COMPUTER PROGRAM DID NOT INCLUDE A FUNCTXON TO RESET THE COMPUTER OUTPUT CONTROL CIRCUITS TO A PREDETERMINED STATE WHEN THE COMPUTER IS RESTARTED. THE BEHAVIOR AND CONTROL OF THE TRANSIENT WHICH RESULTED FROM THE REACTOR AND TURBINE TRIP WERE AS COULD BE EXPECTED.
FORM 6 LER SCSS DATA 09-23-91
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DOCKET YEAR LER NUMBER REVISION DCS NUMBER NSIC EVENT DATE 373 1989 009 1 8907110299 214561 03/02/89 DOCKET:373 LA SALLE 1 TYPE:BWR REGION: 3 NSSS:GE ARCHITECTURAL ENGINEER: SLXX FACILITY OPERATOR: COMMONWEALTH EDISON CO.
SYMBOL: CWE COMMENTS STEPS 2,3: MODEL NO. 9L11MHA264.
WATCH-LIST CODES FOR THIS LER ARE:
942 UNUSUAL EVENT 20 EQUIPMENT FAILURE REPORTABILITY CODES FOR THIS LER ARE:
13 10 CFR 50.73(a)(2)(iv): ESF actuations.
REFERENCE LERS:
1 373/87-003 2 373/87-014 3 374/84-020 ABSTRACT POWER LEVEL 0860 'N 3/2/89i AT 2302 HRS A PHASE TO GROUND FAULT OCCURRED AT t'C" PHASE LIGHTNING ARRESTOR ON THE PRIMARY SIDE OF THE UNIT 2 SYSTEM AUX. TRANSFORMER. FAULT WAS AUTOMATICALLY ISOLATED BY THE TRIPPING OF SWITCHYARD OIL CIRCUIT BREAKERS (OCB) 4-6 AND 6-1 AND UNIT 2 FEEDER BREAKERS. ALL LOADS BEING FED FROM THE SAT TRANSFERRED TO UNIT 2 UNIT AUX. TRANSFORMER EXCEPT FOR BUS 243 WHICH WAS SUPPLIED BY 2B DIESEL GENERATOR WHICH SATISFACTORILY AUTO-STARTED ON UNDERVOLTAGE. UNIT 2 REMAINED ON-LINE AFTER THE INCIDENT. AS A RESULT OF TRANSIENT ON THE 345 KV SYSTEM, UNIT 1 GENERATOR PROTECTIVE RELAYING SENSED A HIGH GENERATOR DIFFERENTIAL CURRENT ON PHASE A AND ISOLATED UNIT 1 GENERATOR. UNIT 1 TURBINE TRIPPED ON LOAD REJECTION RESULTING IN A REACTOR SCRAM FROM TURBINE CONTROL VALVE FAST CLOSURE.
UNIT 1 PROCEEDED INTO NORMAL POST-SCRAM CONDITIONS WITH THE EXCEPTION OF TEMPORARY LOSS OF THE SERVICE AIR COMPRESSOR AND PLANT PROCESS COMPUTER. PROBLEMS WERE ALSO ENCOUNTERED WITH THE RESETTING OF THE SCRAM LOGIC. CAUSE OF THIS EVENT WAS THE PHASE TO GROUND FAULT THAT OCCURRED FROM THE LIGHTNING ARRESTOR TOP CAP TO A SPARGER HEAD ON THE TRANSFORMER DELUGE SYSTEM. THIS WAS EVIDENT FROM ARC BURNING IDENTIFIED AT TOP OF LIGHTNING ARRESTOR AND AT SPARGER HEAD. FAULT WAS CAUSED BY DEBRIS THAT HAD BLOWN ONTO THE LIGHTNING ARRESTOR LEAD.
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DOCKET YEAR LER NUMBER REVISION DCS NUMBER NSIC EVENT DATE 395 1988 001 0 8803070227 208519 02/04/88 DOCKET:395 SUMMER 1 TYPE:PWR REGION: 2 NSSS:WE ARCHITECTURAL ENGINEER: GLBT FACILITY OPERATOR: SOUTH CAROLINA ELECTRIC & GAS CO.
SYMBOL: SCC COMMENTS STEP 5: COMP MEI PERIMETER CAMERAS. STEP 10: COMP MEI PORTAL ACCESS CONTROLLER UNITS. STEP 11: COMP MSC ELECTRIC DOOR STRIKES. STEP 12: PSYS SW UNKNOWN VITAL AREAS. STEP 9: PART NUMBERS 200140 AND 200569 SPM/E E/D WATCH-LIST CODES FOR THIS LER ARE:
34 DESIGN ERROR OR INADEQUACY 946 PHYSICAL SECURITY/SAFEGUARDS REPORTABILITY CODES FOR THIS LER ARE:
20 10 CFR 73.71(c): Physical security system threatened.
ABSTRACT POWER LEVEL 100~os AT APPROXIMATELY 0830 HOURSi FEBRUARY 4~ 1988'WO PLANT ELECTRICIANS CRIMPED AN ELECTRICAL LEAD WHILE REPLACING AN ELECTRICAL DISTRIBUTION PANEL COVER. THE CIRCUIT SHORTED TO GROUND AND TRIPPED A CIRCUIT BREAKER WHICH RESULTED IN A LOSS OF THREE PERIMETER CAMERAS. SIMULTANEOUSLY, THE CURRENT TO GROUND SITUATION CAUSED THE ASSOCIATED INVERTER TO TEMPORARILY OVERLOAD CREATING A MOMENTARYi BUT SIGNIFICANT REDUCTION IN VOLTAGE THAT RESULTED IN SIX ELECTRIC DOOR STRIKES FAILING IN THE UNLOCKED (ENERGIZED) POSITION.
AT APPROXIMATELY 0840 HOURS, SECURITY PROCEDURES WERE IMPLEMENTED TO COMPENSATE FOR THE LOSS OF THE CAMERAS AND TOTAL LOSS OF THE SECURITY COMPUTER SYSTEM AT APPROXIMATELY 0907 HOURS'LEVEN ADDITIONAL SECURITY FORCE PERSONNEL REPORTED FOR DUTY FROM THE TRAINING AUGMENTATION TO COMPENSATE FOR THE LOSS OF ALARM CAPABILITY AND LOCKING MECHANISMS AT THE VITAL AREAS AFFECTED BY THE OUTAGE.
OPERATIONAL TESTS WERE CONDUCTED ON ALL VITAL DOORS AND PERIMETER INTRUSION DETECTION SEGMENTS AFFECTED. ALL TESTS WERE SATISFACTORILY COMPLETED AT 1243 HOURS, FEBRUARY 4, 1988. COMPENSATORY POSTS AT EACH VITAL AREA REMAINED IN EFFECT UNTIL EACH DOOR WAS OPERATIONALLY TESTED.
DOCKET YEAR LER NUMBER REVISION DCS NUMBER NSIC EVENT DATE 423 1987 027 0 8707090095 205195 06/05/87 DOCKET:423 MILLSTONE 3 TYPE PWR REGION: 1 NSSS:WE ARCHITECTURAL ENGINEER: SWXX FACILITY OPERATOR: NORTHEAST NUCLEAR ENERGY CO.
SYMBOL: NNE WATCH-LIST CODES FOR THIS LER ARE:
31 ACCIDENTAL ACTION 941 REPORT ASSOCIATED WITH 10 CFR 50.72 REPORTABILITY CODES FOR THIS LER ARE:
13 10 CFR 50.73(a)(2)(iv): ESF actuations.
ABSTRACT POWER LEVEL 100+os AT 1323 ON JUNE 5) 1987) WITH THE PLANT AT 100+o POWERi THE NORMAL SUPPLY BREAKER TO TRAIN nA>> VITAL BUS 34C WAS TRIPPED OPEN. THE MAIN STEAM ISOLATION VALVES IMMEDIATELY CLOSED ON LOSS OF 120VAC TO THEIR SOLENOID TEST CONTROL CIRCUITRY. A REACTOR TRIP FOLLOWED ON LOW-LOW STEAM GENERATOR LEVELS, WHICH SIGNALED A TURBINE TRIP. A TRAIN "A" LOSS OF POWER SIGNAL WAS GENERATED, THE EMERGENCY DIESEL GENERATOR STARTED AND SUCCESSFULLY ENERGIZED VITAL LOADS. THE MAIN STEAM ATMOSPHERIC RELIEF VALVES AND STEAM GENERATOR CODE SAFETIES OPENED AS DESIGNED A TRAIN itAti CONTROL BUILDING ISOLATION, AND TRAIN 'tA't AND "B" FEEDWATER ISOLATION RESULTED FROM THE EVENT ~ THE PLANT WAS IN HOT STANDBY (MODE 3 ) BY 1 600 HOURS ~ JUNE 5 i 1 9 8 7 ~ THE CAUSE OF BUS 3 4 C TRI P WAS A RESULT OF PERSONNEL ERROR i DUE TO AN OPERATOR DROPPING A RACKING MOTOR ONTO THE 4.16KV SWITCHGEAR.
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DOCKET YEAR LER NUMBER REVISION DCS NUMBER NSIC EVENT DATE 424 1990 023 0 9101220420 220828 12/18/90 DOCKET 424 VOGTLE 1 TYPE:PWR REGION: 2 NSSS:WE ARCHITECTURAL ENGINEER: BESS FACILITY OPERATOR: GEORGIA POWER CO.
SYMBOL: GPC COMMENTS STEP 2: CLASS AA/FA, 3 PHASE, DRY TYPE TRANSFORMER. STEP 18: MODEL NO.
5HK350-3000.
WATCH-LIST CODES FOR THIS LER ARE:
20 EQUIPMENT FAILURE REPORTABILITY CODES FOR THIS LER ARE:
13 10 CFR 50.73(a)(2)(iv): ESF actuations.
REFERENCE LERS:
1 424/90-016 ABSTRACT POWER LEVEL 100+os ON 12 18 90 AT 1936 CSTi UNIT WAS OPERATING AT 1004 POWER WHEN A 4160/480 VOLT NON-1E TRANSFORMER (1NB1OX)
EXPERIENCED AN INTERNAL FAULT. THIS FAILURE RESULTED IN A LOSS OF POWER FOR THE SPEED CONTROL CIRCUITRY FOR THE 1B MAIN FEEDWATER PUMP (MFP) TURBINE AND CERTAIN SUPPORT SYSTEMS FOR EMERGENCY DIESEL GENERATOR 1 B ~ FEEDWATER PUMP SPEED / FEEDWATER FLOW i AND STEAM GENERATOR (SG) LEVELS DECREASED. THE REACTOR OPERATOR INITIATED A MANUAL REACTOR TRIP AT 1937 CST AFTER EFFORTS TO MAINTAIN SG LEVELS WERE UNSUCCESSFUL. ALL SAFETY RELATED FUNCTIONS OCCURRED PER DESIGN FOLLOWING THE REACTOR TRIP HOWEVERS A NON 1E 4160 VOLT BUS FAILED TO AUTOMATICALLYTRANSFER TO THE RESERVE AUXILIARY TRANSFORMERS CAUSING A TEMPORARY LOSS OF VARIOUS NON-1E HOUSE LOADS. TRANSFER OF THE 4160 VOLT BUS WAS COMPLETED MANUALLY AND NORMAL PLANT CONDITIONS WERE ESTABLISHED FOR HOT STANDBY BY 1956 CST. THE ROOT CAUSE FOR THE TRANSFORMER FAILURE IS INDETERMINATE; HOWEVER, SEVERAL SIMILAR TRANSFORMER FAILURES HAVE OCCURRED AT VEGP (REFERENCE LER 50-424/1990-016). THE INVOLVED TRANSFORMERS ARE GE CLASS AA/FA, THREE PHASE, DRY TYPE TRANSFORMERS. THE FAILED TRANSFORMER HAS BEEN REPLACED AND FURTHER STUDY OF POSSIBLE FACTORS WHICH MAY HAVE LED TO THE FAILURE IS IN PROGRESS.
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DOCKET YEAR LER NUMBER REVISION DCS NUMBER NSIC EVENT DATE 455 1987 019 1 8806230261 209583 10/02/87 DOCKET:455 BYRON 2 REGION 3 ARCHITECTURAL ENGINEER: SLXX FACILITY OPERATOR: COMMONWEALTH EDISON CO.
SYMBOL: CWE COMMENTS STEP 6: EQUIPMENT OPERATOR OPENED STATION AUX TRANSFORMER DISCONNECT INSTEAD OF THE MAIN TRANSFORMER DISCONNECT.
WATCH-LIST CODES FOR THIS LER ARE:
35 HUMAN ERROR 942 UNUSUAL EVENT 20 EQUIPMENT FAILURE REPORTABILITY CODES FOR THIS LER ARE:
13 10 CFR 50.73(a) (2)(iv): ESF actuations.
ABSTRACT POWER LEVEL 0134 ON OCTOBER 2i 1987i AT 0446i UNIT 2 WAS RETURNING TO SERVICE WHEN UNIT 2 WAS SYNCHRONIZED TO THE GRIDi THE STEAM GENERATOR (SG) LEVELS INCREASED AND CAUSED A HI-2 S/G LEVEL TRIP. THE HI-2 SG LEVEL WAS REACHED ON SG 2C DUE TO EXCESSIVE "LEAK BY" OF THE 2FW530 VALVE. THE HIGH S/G LEVEL CAUSED A TURBINE TRIP AND A SUBSEQUENT REACTOR TRIP BECAUSE REACTOR POWER WAS ABOVE 10+os AN EQUIPMENT OPERATOR (EO) WAS INSTRUCTED TO REALIGN THE SWITCHYARD RING BUS AFTER THE TRIP. THE EO OPENED THE SYSTEM AUX TRANSFORMER DISCONNECTS INSTEAD OF THE MAIN POWER TRANSFORMER DISCONNECTS. THE SAFETY RELATED 4KV BUSES WERE DEENERGIZED CAUSING THE EMERGENCY DIESEL GENERATORS TO STARTi REENERGIZE THE BUSES'ND SEQUENCE THE SAFE SHUTDOWN LOADS. THE ROOT CAUSE OF THE LOSS OF OFFSITE POWER WAS DUE TO PERSONNEL ERROR. THE EO OPENED THE WRONG DISCONNECT. THE CORRETIVE ACTIONS ARE AS FOLLOWS: DISCIPLINARY ACTION WAS TAKEN WITH THE EO; ADMINISTRATIVE PROCEDURES WERE REVISED TO ENSURE THAT NO SWITCHYARD OPERATIONS ARE PERFORMED WITHOUT A SECOND INDIVIDUAL PRESENTi PERMANENTi DESCRIPTIVE LABELS HAVE BEEN PLACED ON MPT & SAT SWITCHYARD DISCONNECTS; A WALK THROUGH OF THE SWITCHYARD WITH DIVISION SUPERINTENDENT OF POWER SUPPLY TO DEMONSTRATE PROPER OPERATIONS AND COMMUNICATIONS WAS CONDUCTED; THE SAT DISCONNECTS ARE LOCKED WITH UNIQUE LOCKS FOR EACH UNIT, ETC.
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1 302/87-021 2 3 02/87-025 3 304/86-001 4 311/83-022 5 311/88-014 6 3 16/89-014 7 331/85-031 8 334/85-018 9 335/81-053 10 362/89-001 11 364/81-004 12 382/85-042 13 410/86-015 14 458/90-026
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I DOCKET YEAR LER NUMBER REVISION DCS NUMBER NSIC EVENT DATE 335 1981 053 0 8201060355 171810 11/25/81 DOCKET:335 ST. LUCIE 1 TYPE:PWR REGION: 2 NSSS:CE ARCHITECTURAL ENGINEER: EBAS FACILITY OPERATOR: FLORIDA POWER 6 LIGHT COMPANY SYMBOL: FPL COMMENTS WATCH 975 LOSS OF CONTROL ROOM ALARM FUNCTION.
WATCH-LIST CODES FOR THIS LER ARE:
975 POSSIBLE SIGNIFICANT EVENT REFERENCE LERS 1 335/79-028 ABSTRACT I I II B2 STAT ON SERVI CE TRANSFORMER FA LED i DEENERG Z NG THE B2 4 8 OV LOAD CENTER. ABOUT 3 MINUTES LATER THE 2 TIE BREAKERS FEEDING THE AB DC BUS FROM THE B BUS TRIPPED'EENERGIZING THE AB DC BUS ~ LOSS OF THIS CAUSED A LOSS OF AB CONTROL POWER AND 120V VITAL AC WHICH FEEDS ALL CONTROL ROOM ALARMS BUT NOT INSTRUMENTS'HE DC BUSg 120V AC AND ALARMS WERE RESTORED WITHIN 15 MINUTES. SEE LER 335-79-28 FOR RELATED EVENTS. THE B TO AB TIE BREAKERS WERE THOROUGHLY TESTED AND INSPECTED. A LOOSE POWER TERMINATION WAS DISCOVERED ON THE B SIDE BREAKER AND THE INSTANTANEOUS OVER CURRENT TRIP WAS SET ON 'LO'N BOTH BREAKERS. THE TRIP WAS RESET TO HI PER DESIGN AND ALL CONNECTIONS WERE TORQUED. ALL SIMILAR BREAKERS WERE CHECKED.