LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function ChangedML20044D881 |
Person / Time |
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Site: |
Point Beach |
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Issue date: |
05/14/1993 |
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From: |
Andreoni D WISCONSIN ELECTRIC POWER CO. |
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To: |
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Shared Package |
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ML20044D876 |
List: |
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References |
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LER-93-005, LER-93-5, NUDOCS 9305210054 |
Download: ML20044D881 (7) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2471994-10-0606 October 1994 LER 94-009-00:on 940909,EDG G-02 Inadvertently Started & Station Battery Charger D-08 Tripped Off Due to Blown Fuse. Caused by Inadequate Procedure.Blown Fuse Replaced & Electrical Distribution Sys Restored to normal.W/941006 Ltr ML20029C8511994-04-22022 April 1994 LER 94-001-00:on 940323,identified That Feedwater Flow May Have Been Underestimated Since Beginning of Operating Cycle. Caused by Degradation of Signals from Transducers.Transducer replaced.W/940422 Ltr ML20044E5571993-05-17017 May 1993 LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related Sys ML20044E6221993-05-17017 May 1993 LER 93-006-00:on 930416,discovered That Outside CIV Not Leak Tested,Per TS 15.4.4.III.D Requirements Due to Review on 840202,recommending That Valve Be Tested During RHR Hydrostatic Testing.Subj Valve replaced.W/930517 Ltr ML20044D8811993-05-14014 May 1993 LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function Changed ML20044D2061993-05-10010 May 1993 LER 93-003-00:on 930328,Point Beach Unit 2 Tripped Due to Surveillance Testing Problems.Test Procedures Can Trip Unit Due to Equipment or Human Failure.Failure Tests Delayed Until Unit 1 & Knpp Restored to power.W/930510 Ltr ML20024H2151991-05-21021 May 1991 LER 91-003-00:on 910429,charging Sys Check Valve 1-370 Discovered W/Leakage in Excess of Limits Due to Worn Disc Arm Bushing Steps.Worn Disc Arm Bushing Steps Cladded W/ E308 Weld Matl & Hand Filed to Design contour.W/910521 Ltr ML20029C2101991-03-20020 March 1991 LER 91-002-01:on 901009,inadvertent Start of Auxiliary Feedwater Pump Occurred.Caused by Inadequate Test Procedures.Auxiliary Feedwater Pump Secured & Maint Work Request Mwr 904517 initiated.W/910320 Ltr ML20029C1141991-03-12012 March 1991 LER 91-010-01:on 900816,axial Flux Differential Outside Tech Specs Limits Due to Malfunction of Turbine Electrohydraulic Governor Control.Operator Training Revised. W/910319 Ltr ML20028H0321990-09-27027 September 1990 LER 90-011-00:on 900829,low Net Positive Suction Head to Containment Spray Pumps W/Eccs in Recirculation Mode Occurred.Caused by Procedural Deficiency.Temporary Procedure Changes initiated.W/900927 Ltr ML20043G2011990-06-0808 June 1990 LER 90-005-00:on 900510,steam Generator lo-lo Level Reactor Trip Occurred During Cold Shutdown.Caused by Inadequate Warning Sign Posting.Nonconformance Rept Written to Document Event & Recommend evaluation.W/900608 Ltr ML20042G7761990-05-0909 May 1990 LER 90-003-00:on 900409,determined That Piping & Supports in Fuel Oil Pumphouse Could Not Be Demonstrated to Perform Support Functions.Caused by Design Base Not Sufficiently Documented.Mod Performed to Support Fuel Oil Piping ML20042G7791990-05-0808 May 1990 LER 90-004-00:on 900404,single Failure Potential in Safeguards Switchgear B03/B04 Tie Breaker Discovered & Could Have Resulted in Failure of Diesel Generator.Control Power Fuses for Tie Breakers Removed ML20042F5361990-05-0404 May 1990 LER 90-001-00:on 900405,auxiliary Feed Pump Inadvertently Started.Caused by Inadequate Design.Schematic Push to Test Lamp Circuitry Will Be Added to Elementary Wiring Diagrams & Personnel Briefed on Potential circuitry.W/900504 Ltr ML20042F1971990-05-0202 May 1990 LER 90-002-00:on 900402,main Steam Safety Valve 1-MS-2013 Failed to Relieve Setpoint During Tech Spec Testing.Caused by Personnel Error During Setpoint Adjustment.Safety Valves 1-MS-2011,1-MS-2006 & 1-MS-2008 restored.W/900502 Ltr ML20011D5131989-12-19019 December 1989 LER 89-010-00:on 891120,auxiliary Feedwater Flow Transmitters Inadvertently Isolated.Caused by Error in Approved Procedure & Personnel Cognitive Error.Unit 1 Transmitters Valved Back Into Svc immediately.W/891219 Ltr ML19351A6721989-12-15015 December 1989 LER 89-009-00:on 891115,unexpected Steam Generator a lo-lo Level & Steam Generator B lo-lo Level Reactor Trip Signals Experienced.Caused by Installation of Analog Signal Generator.Procedures revised.W/891215 Ltr ML19332F7011989-12-11011 December 1989 LER 89-008-01:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power.Caused by Less than Adequate Tech Spec Change.Power Descension to 38% initiated.W/891211 Ltr ML19332E7221989-12-0707 December 1989 LER 89-009-00:on 891107,D05 & D06 Station Batteries Declared Inoperable.Caused by Original Design Deficiency.Mod Completed to Restore Battery D05 to Operable Status by Replacing Eight nonsafety-related breakers.W/891207 Ltr ML19332E8921989-12-0404 December 1989 LER 89-008-00:on 891103,during Refueling,Contractor Personnel Generated False Trip Signal While Investigating Wiring Discrepancy in Reactor Protection Sys Instrument Racks.Caused by Labeling Error.Supply changed.W/891204 Ltr ML19332F0901989-11-28028 November 1989 LER 89-003-01:on 890712,tank B Level Channel 2LE-934 Began to Indicate Spuriously.Caused by Moisture Intrusion Between Halar Insulator & Sensing Rod.Level Detector Replaced & Channel Reestablished for Accumulator Tank B.W/891128 Ltr ML19332C8411989-11-22022 November 1989 LER 89-007-00:on 891027,Train a Safety Injection Signal Generated During Installation of Mod in Containment High Pressure Circuit.Caused by Inadequate Installation Procedure.Procedure changed.W/891122 Ltr ML19327C2001989-11-14014 November 1989 LER 89-006-01:on 891015,steam Generator Tubes Found Degraded,W/Undefined Signal & W/Axial Indications in Tubesheet Area.Degradation Caused by Time.Affected Tubes Plugged or Preventively sleeved.W/891114 Ltr ML19327C0651989-11-0606 November 1989 LER 89-005-00:on 891006,intermediate Range High Level Trip Signal Unexpectedly Generated During Course of Routine Source Range Channel Calibr.Caused by Loose Connection of Input/Output Cable.Connection tightened.W/891106 Ltr ML19327B3061989-10-19019 October 1989 LER 89-008-00:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power, Disenabling Sys.Caused by High Tech Spec Setpoint.Enable/ Disable Setpoint Reset to 30%.W/891019 Ltr ML18041A1611987-11-16016 November 1987 LER 87-004-01:on 870515,voltage Lost on Red Instrument Bus Resulting in Reactor Protection Sys Actuation.Caused by Excessive Current Demand by ferro-resonant Circuit.Plant Mods to Load Bank Proposed ML18041A1341986-07-0303 July 1986 LER 86-003-00:on 860603,reactor Trip Occurred Due to Loss of Power on White Instrument Bus.Caused by Trip of White Inverter Output Breaker.Procedures for Placing Inverter on Line Will Be revised.W/860703 Ltr ML20028E3551983-01-13013 January 1983 LER 82-029/03L-0:on 821216,automatic Monitoring & Alarm Program Constant Found Incorrect.Caused by Unknown Personnel W/Access to on-line Computer.Value of Constant Restored & Control Rods Alignment Verified ML20028E2381983-01-13013 January 1983 LER 82-028/03L-0:on 821215,routine Test on Fire Detection Sys Found Panel D407 Which Monitors Unit 1 Rod Drive Room Inoperable.Caused by Blown Fuse.Fuse & Indication Lights Replaced on 821215.Detection Sys Undergoing Design Review ML20028E1791983-01-13013 January 1983 Updated LER 82-020/01X-1:on 821102,while Performing Type B & C Leakage Tests of Containment Penetrations & Isolation Valves,One Valve Had Leakage Exceeding Limit.Cause Not Stated.Valve Clapper & Seat Lapped ML20028E3031983-01-11011 January 1983 LER 82-027/03L-0:on 821211,operator Noted That Steam Generator Pressure Transmitter 1PT-469 Indicated Higher than Other Channels.Caused by Frozen Sensing Line Due to Inadequate Interim Piping Insulation ML20028E3211983-01-10010 January 1983 Updated LER 82-017/01X-2:on 821030,w/unit Shut Down for Refueling,Eddy Current Exam of Steam Generator Tubes Indicated Four Tubes in Steam Generator a & Three Tubes in Steam Generator B Exceeded Plugging Limit.Caused by Caustic ML20028C2431982-12-27027 December 1982 LER 82-020/01T-0:on 821103,following Type B & C Leak Rate Tests,Total as-measured Leakage Exceeded Tech Spec Limit, Causing Reactor Coolant Pump Component Cooling Water to Have Excessive Leakage.Cause Not Stated.Clapper & Seat Lapped ML20023B3251982-12-10010 December 1982 Updated LER 82-017/01T-1:on 821030,verified That Indications for Four Steam Generator a Tubes & Three Steam Generator B Tubes Exceeded 40% Plugging Limit During Eddy Current Exam on 821026-30.Cause Not Stated.Tubes Mechanically Plugged ML20028B4151982-11-15015 November 1982 LER 82-017/01T-0:on 821030,four Tubes in Steam Generator a & Three Tubes in Steam Generator B Indicated Degradation Greater than 40% Plugging Limit.Caused by Intergranular Attack.Tubes Mechanically Plugged ML20028A0371982-11-0505 November 1982 LER 82-008/03L-0:on 821006,low Steam Line Pressure Setting for Pressure Instrument 2PT-478 Found Lower than Allowed by Tech Specs.Caused by Bumping of Setpoint Adjustment Knob.Instrument Tested & Realigned ML20027D6821982-11-0303 November 1982 LER 82-018/01T-0:on 821015,incorrect Instrument Bus Supply Shifted to Alternate Supply Following Rept of Fire in Supply Breaker for 1GYO4 Motor Generator Set,Causing Loss of Redundancy on Containment Pressure Indicator 1PT-950 ML20052G4501982-05-12012 May 1982 LER 82-002/01T-0:on 820428,during Eddy Current Exam, Discovered Abnormal Degradation in Fuel Cladding,Rcpb & Primary Containment.Seludge Lancing Will Be Performed ML20052G3701982-05-0707 May 1982 LER 82-009/03L-0:on 820408,4.16-kV Safeguards Undervoltage Relays Did Not Meet 0-volt Time Delay Spec.Caused by Manufacturer Characteristic Curves.Relays Not Capable of Less than 0.38-s.Tech Spec Change Requested on 820427 ML20052G3831982-05-0707 May 1982 LER 82-011/03L-0:on 820415,during Biweekly Calibr Check ICP 2.1 of Reactor Protective Sys Functions,Overpower Delta T Setpoint 2 for Channel 2 Found Less Conservative than Tech Spec Limit.Caused by Setpoint Drift in Impulse Summer Unit ML20052G6331982-05-0707 May 1982 LER 82-010/03L-0:on 820414,ICP 2.9 Found Not to Provide for Proper Unblocking of Source Range High Flux Reactor Trip Over Small Range of Instrument Readings.Caused by Failure to Identify Subtle Procedural Flow.Procedure to Be Revised ML20052B4521982-04-23023 April 1982 LER 82-008/03L-0:on 820323,minor Installation Defects Noted on Four of Six Containment Pressure Transmitters Installed as TMI Response Mod.Caused by Backfit Contractor QC Program Breakdown ML20050B2661982-03-25025 March 1982 LER 82-006/01T-0:on 820311,type B & C Valve Leakage Tests Exceeded Tech Spec Limits.Caused by Corrosion.Svc Air Check Valves Disc Replaced & Valve Cover Remachined ML20041F4861982-03-0808 March 1982 LER 82-005/01T-01:on 820222,poison Test Samples & Two Fuel Assemblies W/Less than 1-yr Cooling Period Found Placed Next to Divider Wall in Spent Fuel Pool.Caused by Tech Spec Misinterpretation ML20041E4911982-03-0404 March 1982 LER 82-004/03L-0:on 820206,during Inservice Testing, Differential Pressure Instrument 4007 for Auxiliary Feed Pump P38A Found Isolated.Probably Caused by Failure to Return Instrument to Svc Following Calibr ML20041E6131982-03-0202 March 1982 LER 82-003/01T-0:on 820217,during Surveillance Testing, Emergency Diesel Generator 3D Failed to Operate.Caused by Sticking Shutdown Solenoid Plunger on Woodward Type UG8 Governor.Solenoid Cleaned,Checked & Generator Tested ML20049H6981982-02-23023 February 1982 LER 82-001/03L-0:on 820203,boric Acid Heat Tracing Circuit P-42 Found Inoperable.Caused by Failed Thermon Type 4 Circuit Controller.Circuit Controller Replaced ML20040G6811982-02-0505 February 1982 LER 82-001/03L-0:on 820107,steam Generator Pressure Sensing Lines Discovered Frozen on a Steam Generator.Caused by Inadequate Freeze Protection & Extremely Cold Weather.Addl Heat Lamps Installed ML20040G5801982-02-0505 February 1982 LER 82-002/03L-0:on 820112,during Hot shutdown,1PT-469 Steam Generator Pressure Transmitter Isolated by Maint Personnel Due to Leaking Coupling.Pressure Sensing Tubing Showed Signs of Steam Leak Due to Freezing ML20040D3791982-01-18018 January 1982 LER 81-020/03L-0:on 811219,frozen Sensing Line Caused High Indication of Steam Generator Pressure Instrument 1PT-482. Caused by Incomplete Insulation of Line & by Cold Weather. Instrument Placed in Tripped Position & Tubing Thawed 1994-04-22
[Table view] Category:RO)
MONTHYEARML20024J2471994-10-0606 October 1994 LER 94-009-00:on 940909,EDG G-02 Inadvertently Started & Station Battery Charger D-08 Tripped Off Due to Blown Fuse. Caused by Inadequate Procedure.Blown Fuse Replaced & Electrical Distribution Sys Restored to normal.W/941006 Ltr ML20029C8511994-04-22022 April 1994 LER 94-001-00:on 940323,identified That Feedwater Flow May Have Been Underestimated Since Beginning of Operating Cycle. Caused by Degradation of Signals from Transducers.Transducer replaced.W/940422 Ltr ML20044E5571993-05-17017 May 1993 LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related Sys ML20044E6221993-05-17017 May 1993 LER 93-006-00:on 930416,discovered That Outside CIV Not Leak Tested,Per TS 15.4.4.III.D Requirements Due to Review on 840202,recommending That Valve Be Tested During RHR Hydrostatic Testing.Subj Valve replaced.W/930517 Ltr ML20044D8811993-05-14014 May 1993 LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function Changed ML20044D2061993-05-10010 May 1993 LER 93-003-00:on 930328,Point Beach Unit 2 Tripped Due to Surveillance Testing Problems.Test Procedures Can Trip Unit Due to Equipment or Human Failure.Failure Tests Delayed Until Unit 1 & Knpp Restored to power.W/930510 Ltr ML20024H2151991-05-21021 May 1991 LER 91-003-00:on 910429,charging Sys Check Valve 1-370 Discovered W/Leakage in Excess of Limits Due to Worn Disc Arm Bushing Steps.Worn Disc Arm Bushing Steps Cladded W/ E308 Weld Matl & Hand Filed to Design contour.W/910521 Ltr ML20029C2101991-03-20020 March 1991 LER 91-002-01:on 901009,inadvertent Start of Auxiliary Feedwater Pump Occurred.Caused by Inadequate Test Procedures.Auxiliary Feedwater Pump Secured & Maint Work Request Mwr 904517 initiated.W/910320 Ltr ML20029C1141991-03-12012 March 1991 LER 91-010-01:on 900816,axial Flux Differential Outside Tech Specs Limits Due to Malfunction of Turbine Electrohydraulic Governor Control.Operator Training Revised. W/910319 Ltr ML20028H0321990-09-27027 September 1990 LER 90-011-00:on 900829,low Net Positive Suction Head to Containment Spray Pumps W/Eccs in Recirculation Mode Occurred.Caused by Procedural Deficiency.Temporary Procedure Changes initiated.W/900927 Ltr ML20043G2011990-06-0808 June 1990 LER 90-005-00:on 900510,steam Generator lo-lo Level Reactor Trip Occurred During Cold Shutdown.Caused by Inadequate Warning Sign Posting.Nonconformance Rept Written to Document Event & Recommend evaluation.W/900608 Ltr ML20042G7761990-05-0909 May 1990 LER 90-003-00:on 900409,determined That Piping & Supports in Fuel Oil Pumphouse Could Not Be Demonstrated to Perform Support Functions.Caused by Design Base Not Sufficiently Documented.Mod Performed to Support Fuel Oil Piping ML20042G7791990-05-0808 May 1990 LER 90-004-00:on 900404,single Failure Potential in Safeguards Switchgear B03/B04 Tie Breaker Discovered & Could Have Resulted in Failure of Diesel Generator.Control Power Fuses for Tie Breakers Removed ML20042F5361990-05-0404 May 1990 LER 90-001-00:on 900405,auxiliary Feed Pump Inadvertently Started.Caused by Inadequate Design.Schematic Push to Test Lamp Circuitry Will Be Added to Elementary Wiring Diagrams & Personnel Briefed on Potential circuitry.W/900504 Ltr ML20042F1971990-05-0202 May 1990 LER 90-002-00:on 900402,main Steam Safety Valve 1-MS-2013 Failed to Relieve Setpoint During Tech Spec Testing.Caused by Personnel Error During Setpoint Adjustment.Safety Valves 1-MS-2011,1-MS-2006 & 1-MS-2008 restored.W/900502 Ltr ML20011D5131989-12-19019 December 1989 LER 89-010-00:on 891120,auxiliary Feedwater Flow Transmitters Inadvertently Isolated.Caused by Error in Approved Procedure & Personnel Cognitive Error.Unit 1 Transmitters Valved Back Into Svc immediately.W/891219 Ltr ML19351A6721989-12-15015 December 1989 LER 89-009-00:on 891115,unexpected Steam Generator a lo-lo Level & Steam Generator B lo-lo Level Reactor Trip Signals Experienced.Caused by Installation of Analog Signal Generator.Procedures revised.W/891215 Ltr ML19332F7011989-12-11011 December 1989 LER 89-008-01:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power.Caused by Less than Adequate Tech Spec Change.Power Descension to 38% initiated.W/891211 Ltr ML19332E7221989-12-0707 December 1989 LER 89-009-00:on 891107,D05 & D06 Station Batteries Declared Inoperable.Caused by Original Design Deficiency.Mod Completed to Restore Battery D05 to Operable Status by Replacing Eight nonsafety-related breakers.W/891207 Ltr ML19332E8921989-12-0404 December 1989 LER 89-008-00:on 891103,during Refueling,Contractor Personnel Generated False Trip Signal While Investigating Wiring Discrepancy in Reactor Protection Sys Instrument Racks.Caused by Labeling Error.Supply changed.W/891204 Ltr ML19332F0901989-11-28028 November 1989 LER 89-003-01:on 890712,tank B Level Channel 2LE-934 Began to Indicate Spuriously.Caused by Moisture Intrusion Between Halar Insulator & Sensing Rod.Level Detector Replaced & Channel Reestablished for Accumulator Tank B.W/891128 Ltr ML19332C8411989-11-22022 November 1989 LER 89-007-00:on 891027,Train a Safety Injection Signal Generated During Installation of Mod in Containment High Pressure Circuit.Caused by Inadequate Installation Procedure.Procedure changed.W/891122 Ltr ML19327C2001989-11-14014 November 1989 LER 89-006-01:on 891015,steam Generator Tubes Found Degraded,W/Undefined Signal & W/Axial Indications in Tubesheet Area.Degradation Caused by Time.Affected Tubes Plugged or Preventively sleeved.W/891114 Ltr ML19327C0651989-11-0606 November 1989 LER 89-005-00:on 891006,intermediate Range High Level Trip Signal Unexpectedly Generated During Course of Routine Source Range Channel Calibr.Caused by Loose Connection of Input/Output Cable.Connection tightened.W/891106 Ltr ML19327B3061989-10-19019 October 1989 LER 89-008-00:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power, Disenabling Sys.Caused by High Tech Spec Setpoint.Enable/ Disable Setpoint Reset to 30%.W/891019 Ltr ML18041A1611987-11-16016 November 1987 LER 87-004-01:on 870515,voltage Lost on Red Instrument Bus Resulting in Reactor Protection Sys Actuation.Caused by Excessive Current Demand by ferro-resonant Circuit.Plant Mods to Load Bank Proposed ML18041A1341986-07-0303 July 1986 LER 86-003-00:on 860603,reactor Trip Occurred Due to Loss of Power on White Instrument Bus.Caused by Trip of White Inverter Output Breaker.Procedures for Placing Inverter on Line Will Be revised.W/860703 Ltr ML20028E3551983-01-13013 January 1983 LER 82-029/03L-0:on 821216,automatic Monitoring & Alarm Program Constant Found Incorrect.Caused by Unknown Personnel W/Access to on-line Computer.Value of Constant Restored & Control Rods Alignment Verified ML20028E2381983-01-13013 January 1983 LER 82-028/03L-0:on 821215,routine Test on Fire Detection Sys Found Panel D407 Which Monitors Unit 1 Rod Drive Room Inoperable.Caused by Blown Fuse.Fuse & Indication Lights Replaced on 821215.Detection Sys Undergoing Design Review ML20028E1791983-01-13013 January 1983 Updated LER 82-020/01X-1:on 821102,while Performing Type B & C Leakage Tests of Containment Penetrations & Isolation Valves,One Valve Had Leakage Exceeding Limit.Cause Not Stated.Valve Clapper & Seat Lapped ML20028E3031983-01-11011 January 1983 LER 82-027/03L-0:on 821211,operator Noted That Steam Generator Pressure Transmitter 1PT-469 Indicated Higher than Other Channels.Caused by Frozen Sensing Line Due to Inadequate Interim Piping Insulation ML20028E3211983-01-10010 January 1983 Updated LER 82-017/01X-2:on 821030,w/unit Shut Down for Refueling,Eddy Current Exam of Steam Generator Tubes Indicated Four Tubes in Steam Generator a & Three Tubes in Steam Generator B Exceeded Plugging Limit.Caused by Caustic ML20028C2431982-12-27027 December 1982 LER 82-020/01T-0:on 821103,following Type B & C Leak Rate Tests,Total as-measured Leakage Exceeded Tech Spec Limit, Causing Reactor Coolant Pump Component Cooling Water to Have Excessive Leakage.Cause Not Stated.Clapper & Seat Lapped ML20023B3251982-12-10010 December 1982 Updated LER 82-017/01T-1:on 821030,verified That Indications for Four Steam Generator a Tubes & Three Steam Generator B Tubes Exceeded 40% Plugging Limit During Eddy Current Exam on 821026-30.Cause Not Stated.Tubes Mechanically Plugged ML20028B4151982-11-15015 November 1982 LER 82-017/01T-0:on 821030,four Tubes in Steam Generator a & Three Tubes in Steam Generator B Indicated Degradation Greater than 40% Plugging Limit.Caused by Intergranular Attack.Tubes Mechanically Plugged ML20028A0371982-11-0505 November 1982 LER 82-008/03L-0:on 821006,low Steam Line Pressure Setting for Pressure Instrument 2PT-478 Found Lower than Allowed by Tech Specs.Caused by Bumping of Setpoint Adjustment Knob.Instrument Tested & Realigned ML20027D6821982-11-0303 November 1982 LER 82-018/01T-0:on 821015,incorrect Instrument Bus Supply Shifted to Alternate Supply Following Rept of Fire in Supply Breaker for 1GYO4 Motor Generator Set,Causing Loss of Redundancy on Containment Pressure Indicator 1PT-950 ML20052G4501982-05-12012 May 1982 LER 82-002/01T-0:on 820428,during Eddy Current Exam, Discovered Abnormal Degradation in Fuel Cladding,Rcpb & Primary Containment.Seludge Lancing Will Be Performed ML20052G3701982-05-0707 May 1982 LER 82-009/03L-0:on 820408,4.16-kV Safeguards Undervoltage Relays Did Not Meet 0-volt Time Delay Spec.Caused by Manufacturer Characteristic Curves.Relays Not Capable of Less than 0.38-s.Tech Spec Change Requested on 820427 ML20052G3831982-05-0707 May 1982 LER 82-011/03L-0:on 820415,during Biweekly Calibr Check ICP 2.1 of Reactor Protective Sys Functions,Overpower Delta T Setpoint 2 for Channel 2 Found Less Conservative than Tech Spec Limit.Caused by Setpoint Drift in Impulse Summer Unit ML20052G6331982-05-0707 May 1982 LER 82-010/03L-0:on 820414,ICP 2.9 Found Not to Provide for Proper Unblocking of Source Range High Flux Reactor Trip Over Small Range of Instrument Readings.Caused by Failure to Identify Subtle Procedural Flow.Procedure to Be Revised ML20052B4521982-04-23023 April 1982 LER 82-008/03L-0:on 820323,minor Installation Defects Noted on Four of Six Containment Pressure Transmitters Installed as TMI Response Mod.Caused by Backfit Contractor QC Program Breakdown ML20050B2661982-03-25025 March 1982 LER 82-006/01T-0:on 820311,type B & C Valve Leakage Tests Exceeded Tech Spec Limits.Caused by Corrosion.Svc Air Check Valves Disc Replaced & Valve Cover Remachined ML20041F4861982-03-0808 March 1982 LER 82-005/01T-01:on 820222,poison Test Samples & Two Fuel Assemblies W/Less than 1-yr Cooling Period Found Placed Next to Divider Wall in Spent Fuel Pool.Caused by Tech Spec Misinterpretation ML20041E4911982-03-0404 March 1982 LER 82-004/03L-0:on 820206,during Inservice Testing, Differential Pressure Instrument 4007 for Auxiliary Feed Pump P38A Found Isolated.Probably Caused by Failure to Return Instrument to Svc Following Calibr ML20041E6131982-03-0202 March 1982 LER 82-003/01T-0:on 820217,during Surveillance Testing, Emergency Diesel Generator 3D Failed to Operate.Caused by Sticking Shutdown Solenoid Plunger on Woodward Type UG8 Governor.Solenoid Cleaned,Checked & Generator Tested ML20049H6981982-02-23023 February 1982 LER 82-001/03L-0:on 820203,boric Acid Heat Tracing Circuit P-42 Found Inoperable.Caused by Failed Thermon Type 4 Circuit Controller.Circuit Controller Replaced ML20040G6811982-02-0505 February 1982 LER 82-001/03L-0:on 820107,steam Generator Pressure Sensing Lines Discovered Frozen on a Steam Generator.Caused by Inadequate Freeze Protection & Extremely Cold Weather.Addl Heat Lamps Installed ML20040G5801982-02-0505 February 1982 LER 82-002/03L-0:on 820112,during Hot shutdown,1PT-469 Steam Generator Pressure Transmitter Isolated by Maint Personnel Due to Leaking Coupling.Pressure Sensing Tubing Showed Signs of Steam Leak Due to Freezing ML20040D3791982-01-18018 January 1982 LER 81-020/03L-0:on 811219,frozen Sensing Line Caused High Indication of Steam Generator Pressure Instrument 1PT-482. Caused by Incomplete Insulation of Line & by Cold Weather. Instrument Placed in Tripped Position & Tubing Thawed 1994-04-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARNPL-99-0569, Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with ML20212D5961999-09-15015 September 1999 Safety Evaluation Supporting Licensee IPEEE Process.Plant Has Met Intent of Suppl 4 to GL 88-20 NPL-99-0051, Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with NPL-99-0449, Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with ML20196J4251999-06-30030 June 1999 Safety Evaluation Authorizing Proposed Alternatives Described in Relief Requests VRR-01,ROJ-16,PRR-01 & VRR-02 ML20209D2691999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbnps,Units 1 & 2 ML20196F3341999-06-22022 June 1999 Safety Evaluation for Implementation of 422V+ Fuel Assemblies at Pbnp Units 1 & 2 ML20195F9781999-06-10010 June 1999 Unit 2 Refueling 23 Inservice Insp Summary Rept for Form NIS-1 ML20209D2751999-05-31031 May 1999 Revised MORs for May 1999 for Pbnps,Units 1 & 2 NPL-99-0328, Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with NPL-99-0273, Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With ML20196F3521999-04-30030 April 1999 Non-proprietary WCAP-14788, W Revised Thermal Design Procedure Instrument Uncertainty Methodology for Wepc Point Beach Units 1 & 2 (Fuel Upgrade & Uprate to 1656 Mwt - NSSS Power) NPL-99-0193, Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with NPL-99-0134, Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with ML20207D6751999-02-22022 February 1999 Assessment of Design Info on Piping Restraints for Point Beach Nuclear Plant,Units 1 & 2.Staff Concludes That Licensee Unable to Retrieve Original Analyses That May Have Been Performed to Justify Removal of Shim Collars ML20206R9001999-01-13013 January 1999 SER Accepting Nuclear Quality Assurance Program Changes for Point Beach Nuclear Plant,Units 1 & 2 NPL-99-0008, Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with NPL-99-0091, 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with1998-12-31031 December 1998 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with ML20198C7671998-12-10010 December 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME BPV Code,1986 Edition,Section XI Requirement IWA-2232, to Use Performance Demonstration Initiative Program During RPV Third 10-yr ISI for Plant,Unit 2 NPL-98-1006, Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20195J5101998-11-16016 November 1998 Proposed Revs to Section 1.3 of FSAR for Pbnp QA Program ML20198J5941998-11-0303 November 1998 1998 Graded Exercise,Conducted on 981103 NPL-98-0948, Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With NPL-98-0880, Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored1998-10-21021 October 1998 Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored ML20154M9121998-10-14014 October 1998 Unit 1 Refueling 24 Repair/Replacement Summary Rept for Form NIS-2 ML20154L6751998-10-14014 October 1998 Unit 1 Refueling 24 ISI Summary Rept for Form NIS-1 NPL-98-0826, Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20151W3851998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Pbnp Units 1 & 2 NPL-98-0653, Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4471998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 2 ML20151W4541998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 1 ML20236Q3161998-07-10010 July 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME Code Requirements PTP-3-01 & PTP-3-02 ML20236L6771998-07-0707 July 1998 Safety Evaluation Approving Wepco Implementation Program to Resolve USI A-46 at Point Beach NPP Units 1 & 2 NPL-98-0558, Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 2 ML20151W4261998-06-30030 June 1998 Corrected Page to MOR for June 1998 for Pbnp Unit 2 ML20151W4221998-05-31031 May 1998 Corrected Page to MOR for May 1998 for Pbnp Unit 2 NPL-98-0481, Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4011998-04-30030 April 1998 Corrected Page to MOR for April 1998 for Pbnp Unit 2 NPL-98-0356, Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20217F3131998-04-17017 April 1998 Safety Evaluation Accepting Proposed Alternative to ASME Code for Surface Exam of Nonstructural Seal Welds,For Plant, Unit 1 ML20216D7071998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3981998-03-31031 March 1998 Corrected Page to MOR for March for Pbnp Unit 2 NPL-98-0209, Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable1998-03-30030 March 1998 Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable ML20217A8501998-03-19019 March 1998 SER Accepting Proposed Changes Submitted on 980226 by Wiep to Pbnp Final SAR Section 1.8 Which Will Impact Commitments Made in Pbnp QA Program Description.Changes Concern Approval Authority for Procedures & Interviewing Authority ML20216J0101998-03-17017 March 1998 Safety Evaluation Accepting Third 10-yr Inservice Insp Interval Relief Request RR-1-18 for Plant NPL-98-0159, Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3891998-02-28028 February 1998 Corrected Page to MOR for Feb 1998 for Pbnp Unit 2 ML20216D7121998-02-28028 February 1998 Revised Corrected MOR for Feb 1998 for Point Beach Nuclear Plant,Unit 2 NPL-98-0084, Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 21998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20198L1151998-01-0808 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Point Beach Nuclear Plant,Units 1 & 2 1999-09-30
[Table view] |
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AND REPORTS MAluAGEMEnlT BRANCH GP4301. U S NUCLE AR ?
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PAGE 63!
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hAME TELEPMO%E NUMSim AmE A CODE Dave J. Andreoni, Instrumentation & Control Engineering 4l1 g4 7 5l 5l -l 6: 4l6 l7 l COMPLETE ONE LINE FOR EACH COMPOhENT , AfLURE DESCRitEO IN THis AEPORT 813 I
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i ABSTRACT: I At approximately 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br /> on April 15, 1993, while adjustments were l being made to Point Beach Nuclear Plant Containment Accident Fan 1-W1C1, :
Time Delay Relay 1-TDR-26, Turbine Building Cooler Service Water Inlet l Valve 1SW-2880 unexpectedly closed. The closure of ISW-2880 was caused j by actuation of an Engineered Safety Feature associated with-Relay 1-TDR-26. The closure of 1SW-2880 did not impact.the availability of any Engineered Safety Features. The-Engineered Safety Feature system j i for Unit I was not required to be operable because the' unit was shutdown !
.with.the reactor core defueled for its annual maintenance and refueling l outage. Only nonessential service water loads are serviced through 'j ISW-2880. Office area cooling loads.were isolated as a result of this j ovent. l 9305210054 930514 :
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C'J.*.W nInl 5 OF gl 7 Point Bea-b e -lnne Plw . Unit 3 0l5l0l0l0l3lglg gj, 010 0 12 rErres . w. .u w*an.-mm.awim EVENT DESCRIPTION:
On April 15, 1993, Point Beach Nuclear Plant (PBNP) Unit 1 was in a refueling shutdown with the core defueled. PBNP Unit 2 was operating at 100 percent power. At approximately 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br /> on April 15, 1993, while adjustments were being made to PBNP Unit 1 Containment Accident Fan 1-W1C1, Time Delay Relay 1-TDR-26, Turbine Building Cooler Service Water Inlet Valve ISW-2880 unexpectedly closed. The closure of ISW-2880 was caused by actuation of an Engineered Safety Feature (ESP) associated with Relay 1-TDR-26. Only nonessential service water loads are serviced through 1SW-2880. The following equipment was receiving service water through 1SW-2880 at the time of the event:
o Technical Support Center administrative area cooler, HX-141A, o Technical Support Center administrative area backup cooler, HX-141B, and .
-o Front office area air condition chiller condensers, HX-28B-1
& 2.
All other components which receive service water through 1SW-2880 were secured at the time of the event because Unit 1 was in its annual maintenance and refueling outage.
Because the components receiving service water through 1SW-2880 were not required for plant operation, the valve was left closed while adjustments to 1-TDR-26 were completed. Valve 1SW-2880 was opened at approximately 1110 hours0.0128 days <br />0.308 hours <br />0.00184 weeks <br />4.22355e-4 months <br /> on April 15, 1993 and remained open.
Earlier in the morning on April 15, 1993, the time delay setting of Unit 2 Time Delay Relay 2-TDR-26 was changed from 40 seconds to 38 seconds, and the time delay setting of Time Delay Relay 2-TDR-27 was changed from 50 seconds to 45 seconds. These changes were completed by 0833 hours0.00964 days <br />0.231 hours <br />0.00138 weeks <br />3.169565e-4 months <br /> without incident.
In September 1990, we identified that the existing time delay settings for Containment Accident Fans W1A1 and W1C1 (30 seconds) in both units did not allow for a minimum of 35 seconds from time of accident initiation until time of fan cooler starting, as required by PBNP Final Safety Analysis Report (FSAR) Table 14.3.2-1, "Large Break Containment Data (Dry Containment)." The time delay setting for Fans W1B1 and W1D1 in both units was 35 seconds. During the Unit 2 maintenance and refueling outage in the fall of 1992, the time delay setting for Containment Accident Fans 2-W1A1 and 2-W1C1 was changed to 40 seconds and the time delay setting for Containment Accident Fans 2-W1B1 and 2 W1D1 was changed to 50 seconds. This change ensured that all Unit 2 fans would start no earlier than 35 seconds after accident initiation.
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010 o 17 rixTer . e . - aan asu.nm In March, 1993, it was identified that these time settings may result in exceeding the maximum time delay of 60 seconds from accident initiation to fan cooler initiation as stated in PENP FSAR 14.3.4, " Containment Integrity Evaluation. It was then determined ~that the appropriate time delay setting was 38 seconds for fans W1A1 and W1C1, and 45 seconds for Fans W3731 and W1D1 for both units. These settings ensure the fans start between 35 and 60 seconds from the time of accident initiation.
On April 15, 1993, the time delay settings for Containment Accident Fans 1-W1A1 and 1-WIC1 were changed from 30 to 38 seconds and the time delay settings for Fans 1-W1B1 and 1-W1D1 were changed from 35 to 45 seconds. This event occurred during adjustments to the time delay ,
setting for Containment Accident Fan 1-W1C1.
COMPONENT AND SYSTEM DESCRIPTION:
-The PBNP service water system serves both units and is designed to provide redundant cooling water supplies to the components served by the system. The system is designed to ensure adequate heat removal, based on the highest expected lake temperatures, maximum loading, and leakage allowances.
- The service water system consists of 6 pumps, Zurn strainers, a common -
loop supply header, a discharge header, piping to and from the
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components being cooled, and associated valves, instrumentation, and controls. The common loop supply header is divided into three sections:
the north supply header, south supply header, and west supply header.
The sections can be isolated from one another by shutting normally open, motor operated, butterfly valves.
The south supply header routes water to branch lines which supply cooling flow to the various components. The branch line supplying service water to the Unit 1 turbine hall can be isolated from the south supply header by shutting the Unit 1 Turbine Building Cooler Service Water Inlet Valve 1SW-2880; a Powell, 6 inch, motor operated gate valve.
The ESF function of this valve is to automatically isolate nonessential loads during a safety injection event if at least four service water pumps are not running 30 seconds after the pumps receive a start signal.
This valve can also be operated from the control room.
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0j0 0{4 OF 0l7 rixt o A <. - ==c i 3ma mtn The following components receive service water through 1SW-2880:
o Main turbine lube oil coolers, 1HX-23A & B o Steam generator feed pump lube oil coolers, 1HX-56A & B o Condensate motor pump lube oil coolers, 1HX-84A & B o Electrohydraulic oil coolers, 1HX-54A & B o Seal oil coolers, 1HX-53A & B o Exciter cooler, 1HX-52 !
o Generator bus cooler, 1HX-27 o TSC admin area cooler, HX-141A ,
o TSC admin area backup cooler, HX-141B t o TSC admin records area cooler, HX-141C o Hydrogen dryer, 1Z56 o Office area air conditioning chillers, HX-28B1 & B2 o common vacuum priming pump, P41 ,
o Unit i vacuum priming pump, 1P41
- o. Maintenance shop o Hose Stations A6, A9, and F5 ,
. I All serviced components are isolable from the branch line. Service water flow from components is routed to discharge headers, which combine and connect to either unit's circulating water discharge piping.
Engineered safety features actuation is initiated by redundant channels, each responding to a process parameter (pressurizer pressure, average coolant temperature, etc.). These process measurements cause bistables to trip when certain safety limits are exceeded. Each redundant bistable is wired to logic relays in the two physically and electrically separated trains of safeguards relay racks. These racks are located in the cable spreading room and are identified as the Train "A" and Train' "B" safeguards relay racks.
Point Beach FSAR Section 8.2, " Electrical System," specifies the time requirements for the sequential starting of ESF equipment during a cafety injection event with a loss of off-site power. .
Section 14.3.4, " Containment Integrity Evaluation," of the PBNP FSAR ctates that two containment accident fans were assumed to start 60 seconds after a rupture of the reactor coolant system when calculating peak containment pressures for such an accident.
Section 14.3.2, " Major Reactor Coolant System Pipe Ruptures (Loss-of-Coolant Accident)," of the PBNP FSAR describes the analysis specified by 10 CFR 50.46, " Acceptance Criteria for Emergency Core Cooling Systems for Light Water Power Reactors." The parameters used in the analysis to determine the containment pressure response to the mass and energy release from the rupture are listed in Table 14.3.2-1, "Large Break
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coolers occurring 35 seconds after accident initiation.
Time Delay Relay 1-TDR-26 is in the Unit 1, Train "B" safeguards relay rack. Relay 1-TDR-26 starts Containment Accident Fan 1-W1C1 38 seconds after accident initiation. This relay also shuts 1SW-2880 if four service water pumps have not started 30 seconds after the pumps receive ,
a start signal. In order to change the setpoint for 1-TDR-26, the relay must be actuated. Thus, when 1-TDR-26 was actuated in preparation to change the time delay setting, 1SW-2880 stroked shut.
The configuration for Unit 2 is slightly different. Relay 2-TDR-26 ,
starts Containment Accident Fan 2-W1C1 38 seconds after accident initiation. However, Relay 2-TDR-26 does not shut 2SW-2880 if four of six service water pumps have not started 30 seconds after they receive a start signal. For Unit 2, this function.is performed by Relay 2-SW-BX. Relay 2-SW-BX is in the Unit 2, Train "B" safeguards
-relay rack and is specifically provided to isolate nonessential i service water loads if four service water pumps have not started within 30 seconds of receiving a start signal.
CAUSE AND CORRECTIVE ACTION:
The cause of this event is failure to recognize the presence of the contact in the 1-TDR-26 relay which shuts 1SW-2880 if four service water !
pumps have not started 30 seconds after the pumps receive a start -
l signal. The drawing of Relay 1-TDR-26 indicates the presence of the contact which is in the 1SW-2880 control circuit. The drawing of Relay 2-TDR-26 shows that this contact is a spare. The pre-work review for adjustments to the Unit i relays was not as thorough as that for the Unit 2 relays because it was assumed that the configuration of the relays was the same for both units.
The effect of the closure of 1SW-2880 was evaluated immediately upon discovery. Since the loads to which service water was isolated were not j required for plant operation, the valve was allowed to remain shut until completion of the changes to the time delay for 1-TDR-26. The valve was reopened at approximately 1110 hours0.0128 days <br />0.308 hours <br />0.00184 weeks <br />4.22355e-4 months <br /> on April 15, 1993, and remained ;
open. ;
In order to prevent recurrence of this event, the function that closes l ISW-2880 if four service water pumps have not started 30 seconds after f the pumps receive a start signal, hus been changed from the 1-TDR-26 i relay to the 1-SW-BX relay. This is similar to the configuration for ;
Unit 2. '
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REPORTABILITY:
This Licensee Event Report is being submitted in accordance with the requirements of 10 CFR 50.73 (a) (2) (iv) , "The licensee shall report...any cvent or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF) . . . "
A four hour NRC notification was made at 1345 hours0.0156 days <br />0.374 hours <br />0.00222 weeks <br />5.117725e-4 months <br /> on April 15, 1993 in accordance with 10 CFR 50.72 (b) (2) (ii) .
SAFETY ASSESSMENT:
The closure of ISW-2880 did not impact the availability of any Engineered Safety Features. The Engineered Safety Feature system for Unit I was not required to be operable because the unit was shutdown with the reactor core defueled for its annual maintenance and refueling outage. ,
The safeguards function of 1SW-2880 is to automatically shut if four of cix service water pumps have not started 30 seconds after the pumps receive a start signal in order to isolate nonessential service water loads. Only nonessential service water loads are serviced through ISW-2880 and only office area cooling loads were isolated as a result of his event.
GENERIC IMPLICATIONS:
No generic implications were identified.
SIMILAR DCCURRENCES:
The following Licensee Event Reports describe the inadvertent actuation of an Engineered Safety Feature:
Unit 1 or commgn LER 91-006 Inadvertent Start of Emergency Diesel Generator LER 92-003 Inadvertent Start of Emergency Diesel Generator Due to Personnel Error
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01015 -
0 10 0 17 0F 0I7 tsxt u , a w .-.an ,aa w msawim Unit 2 LER 84-003 Inadvertent ESF Actuation LER 84-005 Inadvertent Start of Emergency Diesel Generator LER 84-006 Inadvertent Start of Emergency Diesel Generator ,
LER 84-007 Inadvertent Start of Emergency Diesel Generator LER 89-010 Inadvertent ESF Actuation; Containment Pressure Trip Signal i
. LER 90-001' Inadvertent Start of a Motor Driven Auxiliary Feedwater Pump LER 90-002 Inadvertent ESF Actuation; Auxiliary Feedwater Pump .
Automatic Start LER 90-004 Inadvertent ESF Actuation; Service Water Low Flow Annunciation LER 90-005 Inadvertent Relay Actuation Causing Loss of Condensate Flow ;
LER 92-006 Inadvertent ESF Actuation as a Result of As-Built Wire >
Tracing ;
LER 92-007 Inadvertent ESF Actuation as a Result of Improper ., !
. Surveillance Testing
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