LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related SysML20044E557 |
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Site: |
Point Beach |
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Issue date: |
05/17/1993 |
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From: |
Weaver D WISCONSIN ELECTRIC POWER CO. |
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To: |
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Shared Package |
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ML20044E554 |
List: |
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References |
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LER-92-009, LER-92-9, NUDOCS 9305250154 |
Download: ML20044E557 (7) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2471994-10-0606 October 1994 LER 94-009-00:on 940909,EDG G-02 Inadvertently Started & Station Battery Charger D-08 Tripped Off Due to Blown Fuse. Caused by Inadequate Procedure.Blown Fuse Replaced & Electrical Distribution Sys Restored to normal.W/941006 Ltr ML20029C8511994-04-22022 April 1994 LER 94-001-00:on 940323,identified That Feedwater Flow May Have Been Underestimated Since Beginning of Operating Cycle. Caused by Degradation of Signals from Transducers.Transducer replaced.W/940422 Ltr ML20044E5571993-05-17017 May 1993 LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related Sys ML20044E6221993-05-17017 May 1993 LER 93-006-00:on 930416,discovered That Outside CIV Not Leak Tested,Per TS 15.4.4.III.D Requirements Due to Review on 840202,recommending That Valve Be Tested During RHR Hydrostatic Testing.Subj Valve replaced.W/930517 Ltr ML20044D8811993-05-14014 May 1993 LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function Changed ML20044D2061993-05-10010 May 1993 LER 93-003-00:on 930328,Point Beach Unit 2 Tripped Due to Surveillance Testing Problems.Test Procedures Can Trip Unit Due to Equipment or Human Failure.Failure Tests Delayed Until Unit 1 & Knpp Restored to power.W/930510 Ltr ML20024H2151991-05-21021 May 1991 LER 91-003-00:on 910429,charging Sys Check Valve 1-370 Discovered W/Leakage in Excess of Limits Due to Worn Disc Arm Bushing Steps.Worn Disc Arm Bushing Steps Cladded W/ E308 Weld Matl & Hand Filed to Design contour.W/910521 Ltr ML20029C2101991-03-20020 March 1991 LER 91-002-01:on 901009,inadvertent Start of Auxiliary Feedwater Pump Occurred.Caused by Inadequate Test Procedures.Auxiliary Feedwater Pump Secured & Maint Work Request Mwr 904517 initiated.W/910320 Ltr ML20029C1141991-03-12012 March 1991 LER 91-010-01:on 900816,axial Flux Differential Outside Tech Specs Limits Due to Malfunction of Turbine Electrohydraulic Governor Control.Operator Training Revised. W/910319 Ltr ML20028H0321990-09-27027 September 1990 LER 90-011-00:on 900829,low Net Positive Suction Head to Containment Spray Pumps W/Eccs in Recirculation Mode Occurred.Caused by Procedural Deficiency.Temporary Procedure Changes initiated.W/900927 Ltr ML20043G2011990-06-0808 June 1990 LER 90-005-00:on 900510,steam Generator lo-lo Level Reactor Trip Occurred During Cold Shutdown.Caused by Inadequate Warning Sign Posting.Nonconformance Rept Written to Document Event & Recommend evaluation.W/900608 Ltr ML20042G7761990-05-0909 May 1990 LER 90-003-00:on 900409,determined That Piping & Supports in Fuel Oil Pumphouse Could Not Be Demonstrated to Perform Support Functions.Caused by Design Base Not Sufficiently Documented.Mod Performed to Support Fuel Oil Piping ML20042G7791990-05-0808 May 1990 LER 90-004-00:on 900404,single Failure Potential in Safeguards Switchgear B03/B04 Tie Breaker Discovered & Could Have Resulted in Failure of Diesel Generator.Control Power Fuses for Tie Breakers Removed ML20042F5361990-05-0404 May 1990 LER 90-001-00:on 900405,auxiliary Feed Pump Inadvertently Started.Caused by Inadequate Design.Schematic Push to Test Lamp Circuitry Will Be Added to Elementary Wiring Diagrams & Personnel Briefed on Potential circuitry.W/900504 Ltr ML20042F1971990-05-0202 May 1990 LER 90-002-00:on 900402,main Steam Safety Valve 1-MS-2013 Failed to Relieve Setpoint During Tech Spec Testing.Caused by Personnel Error During Setpoint Adjustment.Safety Valves 1-MS-2011,1-MS-2006 & 1-MS-2008 restored.W/900502 Ltr ML20011D5131989-12-19019 December 1989 LER 89-010-00:on 891120,auxiliary Feedwater Flow Transmitters Inadvertently Isolated.Caused by Error in Approved Procedure & Personnel Cognitive Error.Unit 1 Transmitters Valved Back Into Svc immediately.W/891219 Ltr ML19351A6721989-12-15015 December 1989 LER 89-009-00:on 891115,unexpected Steam Generator a lo-lo Level & Steam Generator B lo-lo Level Reactor Trip Signals Experienced.Caused by Installation of Analog Signal Generator.Procedures revised.W/891215 Ltr ML19332F7011989-12-11011 December 1989 LER 89-008-01:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power.Caused by Less than Adequate Tech Spec Change.Power Descension to 38% initiated.W/891211 Ltr ML19332E7221989-12-0707 December 1989 LER 89-009-00:on 891107,D05 & D06 Station Batteries Declared Inoperable.Caused by Original Design Deficiency.Mod Completed to Restore Battery D05 to Operable Status by Replacing Eight nonsafety-related breakers.W/891207 Ltr ML19332E8921989-12-0404 December 1989 LER 89-008-00:on 891103,during Refueling,Contractor Personnel Generated False Trip Signal While Investigating Wiring Discrepancy in Reactor Protection Sys Instrument Racks.Caused by Labeling Error.Supply changed.W/891204 Ltr ML19332F0901989-11-28028 November 1989 LER 89-003-01:on 890712,tank B Level Channel 2LE-934 Began to Indicate Spuriously.Caused by Moisture Intrusion Between Halar Insulator & Sensing Rod.Level Detector Replaced & Channel Reestablished for Accumulator Tank B.W/891128 Ltr ML19332C8411989-11-22022 November 1989 LER 89-007-00:on 891027,Train a Safety Injection Signal Generated During Installation of Mod in Containment High Pressure Circuit.Caused by Inadequate Installation Procedure.Procedure changed.W/891122 Ltr ML19327C2001989-11-14014 November 1989 LER 89-006-01:on 891015,steam Generator Tubes Found Degraded,W/Undefined Signal & W/Axial Indications in Tubesheet Area.Degradation Caused by Time.Affected Tubes Plugged or Preventively sleeved.W/891114 Ltr ML19327C0651989-11-0606 November 1989 LER 89-005-00:on 891006,intermediate Range High Level Trip Signal Unexpectedly Generated During Course of Routine Source Range Channel Calibr.Caused by Loose Connection of Input/Output Cable.Connection tightened.W/891106 Ltr ML19327B3061989-10-19019 October 1989 LER 89-008-00:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power, Disenabling Sys.Caused by High Tech Spec Setpoint.Enable/ Disable Setpoint Reset to 30%.W/891019 Ltr ML18041A1611987-11-16016 November 1987 LER 87-004-01:on 870515,voltage Lost on Red Instrument Bus Resulting in Reactor Protection Sys Actuation.Caused by Excessive Current Demand by ferro-resonant Circuit.Plant Mods to Load Bank Proposed ML18041A1341986-07-0303 July 1986 LER 86-003-00:on 860603,reactor Trip Occurred Due to Loss of Power on White Instrument Bus.Caused by Trip of White Inverter Output Breaker.Procedures for Placing Inverter on Line Will Be revised.W/860703 Ltr ML20028E3551983-01-13013 January 1983 LER 82-029/03L-0:on 821216,automatic Monitoring & Alarm Program Constant Found Incorrect.Caused by Unknown Personnel W/Access to on-line Computer.Value of Constant Restored & Control Rods Alignment Verified ML20028E2381983-01-13013 January 1983 LER 82-028/03L-0:on 821215,routine Test on Fire Detection Sys Found Panel D407 Which Monitors Unit 1 Rod Drive Room Inoperable.Caused by Blown Fuse.Fuse & Indication Lights Replaced on 821215.Detection Sys Undergoing Design Review ML20028E1791983-01-13013 January 1983 Updated LER 82-020/01X-1:on 821102,while Performing Type B & C Leakage Tests of Containment Penetrations & Isolation Valves,One Valve Had Leakage Exceeding Limit.Cause Not Stated.Valve Clapper & Seat Lapped ML20028E3031983-01-11011 January 1983 LER 82-027/03L-0:on 821211,operator Noted That Steam Generator Pressure Transmitter 1PT-469 Indicated Higher than Other Channels.Caused by Frozen Sensing Line Due to Inadequate Interim Piping Insulation ML20028E3211983-01-10010 January 1983 Updated LER 82-017/01X-2:on 821030,w/unit Shut Down for Refueling,Eddy Current Exam of Steam Generator Tubes Indicated Four Tubes in Steam Generator a & Three Tubes in Steam Generator B Exceeded Plugging Limit.Caused by Caustic ML20028C2431982-12-27027 December 1982 LER 82-020/01T-0:on 821103,following Type B & C Leak Rate Tests,Total as-measured Leakage Exceeded Tech Spec Limit, Causing Reactor Coolant Pump Component Cooling Water to Have Excessive Leakage.Cause Not Stated.Clapper & Seat Lapped ML20023B3251982-12-10010 December 1982 Updated LER 82-017/01T-1:on 821030,verified That Indications for Four Steam Generator a Tubes & Three Steam Generator B Tubes Exceeded 40% Plugging Limit During Eddy Current Exam on 821026-30.Cause Not Stated.Tubes Mechanically Plugged ML20028B4151982-11-15015 November 1982 LER 82-017/01T-0:on 821030,four Tubes in Steam Generator a & Three Tubes in Steam Generator B Indicated Degradation Greater than 40% Plugging Limit.Caused by Intergranular Attack.Tubes Mechanically Plugged ML20028A0371982-11-0505 November 1982 LER 82-008/03L-0:on 821006,low Steam Line Pressure Setting for Pressure Instrument 2PT-478 Found Lower than Allowed by Tech Specs.Caused by Bumping of Setpoint Adjustment Knob.Instrument Tested & Realigned ML20027D6821982-11-0303 November 1982 LER 82-018/01T-0:on 821015,incorrect Instrument Bus Supply Shifted to Alternate Supply Following Rept of Fire in Supply Breaker for 1GYO4 Motor Generator Set,Causing Loss of Redundancy on Containment Pressure Indicator 1PT-950 ML20052G4501982-05-12012 May 1982 LER 82-002/01T-0:on 820428,during Eddy Current Exam, Discovered Abnormal Degradation in Fuel Cladding,Rcpb & Primary Containment.Seludge Lancing Will Be Performed ML20052G3701982-05-0707 May 1982 LER 82-009/03L-0:on 820408,4.16-kV Safeguards Undervoltage Relays Did Not Meet 0-volt Time Delay Spec.Caused by Manufacturer Characteristic Curves.Relays Not Capable of Less than 0.38-s.Tech Spec Change Requested on 820427 ML20052G3831982-05-0707 May 1982 LER 82-011/03L-0:on 820415,during Biweekly Calibr Check ICP 2.1 of Reactor Protective Sys Functions,Overpower Delta T Setpoint 2 for Channel 2 Found Less Conservative than Tech Spec Limit.Caused by Setpoint Drift in Impulse Summer Unit ML20052G6331982-05-0707 May 1982 LER 82-010/03L-0:on 820414,ICP 2.9 Found Not to Provide for Proper Unblocking of Source Range High Flux Reactor Trip Over Small Range of Instrument Readings.Caused by Failure to Identify Subtle Procedural Flow.Procedure to Be Revised ML20052B4521982-04-23023 April 1982 LER 82-008/03L-0:on 820323,minor Installation Defects Noted on Four of Six Containment Pressure Transmitters Installed as TMI Response Mod.Caused by Backfit Contractor QC Program Breakdown ML20050B2661982-03-25025 March 1982 LER 82-006/01T-0:on 820311,type B & C Valve Leakage Tests Exceeded Tech Spec Limits.Caused by Corrosion.Svc Air Check Valves Disc Replaced & Valve Cover Remachined ML20041F4861982-03-0808 March 1982 LER 82-005/01T-01:on 820222,poison Test Samples & Two Fuel Assemblies W/Less than 1-yr Cooling Period Found Placed Next to Divider Wall in Spent Fuel Pool.Caused by Tech Spec Misinterpretation ML20041E4911982-03-0404 March 1982 LER 82-004/03L-0:on 820206,during Inservice Testing, Differential Pressure Instrument 4007 for Auxiliary Feed Pump P38A Found Isolated.Probably Caused by Failure to Return Instrument to Svc Following Calibr ML20041E6131982-03-0202 March 1982 LER 82-003/01T-0:on 820217,during Surveillance Testing, Emergency Diesel Generator 3D Failed to Operate.Caused by Sticking Shutdown Solenoid Plunger on Woodward Type UG8 Governor.Solenoid Cleaned,Checked & Generator Tested ML20049H6981982-02-23023 February 1982 LER 82-001/03L-0:on 820203,boric Acid Heat Tracing Circuit P-42 Found Inoperable.Caused by Failed Thermon Type 4 Circuit Controller.Circuit Controller Replaced ML20040G6811982-02-0505 February 1982 LER 82-001/03L-0:on 820107,steam Generator Pressure Sensing Lines Discovered Frozen on a Steam Generator.Caused by Inadequate Freeze Protection & Extremely Cold Weather.Addl Heat Lamps Installed ML20040G5801982-02-0505 February 1982 LER 82-002/03L-0:on 820112,during Hot shutdown,1PT-469 Steam Generator Pressure Transmitter Isolated by Maint Personnel Due to Leaking Coupling.Pressure Sensing Tubing Showed Signs of Steam Leak Due to Freezing ML20040D3791982-01-18018 January 1982 LER 81-020/03L-0:on 811219,frozen Sensing Line Caused High Indication of Steam Generator Pressure Instrument 1PT-482. Caused by Incomplete Insulation of Line & by Cold Weather. Instrument Placed in Tripped Position & Tubing Thawed 1994-04-22
[Table view] Category:RO)
MONTHYEARML20024J2471994-10-0606 October 1994 LER 94-009-00:on 940909,EDG G-02 Inadvertently Started & Station Battery Charger D-08 Tripped Off Due to Blown Fuse. Caused by Inadequate Procedure.Blown Fuse Replaced & Electrical Distribution Sys Restored to normal.W/941006 Ltr ML20029C8511994-04-22022 April 1994 LER 94-001-00:on 940323,identified That Feedwater Flow May Have Been Underestimated Since Beginning of Operating Cycle. Caused by Degradation of Signals from Transducers.Transducer replaced.W/940422 Ltr ML20044E5571993-05-17017 May 1993 LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related Sys ML20044E6221993-05-17017 May 1993 LER 93-006-00:on 930416,discovered That Outside CIV Not Leak Tested,Per TS 15.4.4.III.D Requirements Due to Review on 840202,recommending That Valve Be Tested During RHR Hydrostatic Testing.Subj Valve replaced.W/930517 Ltr ML20044D8811993-05-14014 May 1993 LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function Changed ML20044D2061993-05-10010 May 1993 LER 93-003-00:on 930328,Point Beach Unit 2 Tripped Due to Surveillance Testing Problems.Test Procedures Can Trip Unit Due to Equipment or Human Failure.Failure Tests Delayed Until Unit 1 & Knpp Restored to power.W/930510 Ltr ML20024H2151991-05-21021 May 1991 LER 91-003-00:on 910429,charging Sys Check Valve 1-370 Discovered W/Leakage in Excess of Limits Due to Worn Disc Arm Bushing Steps.Worn Disc Arm Bushing Steps Cladded W/ E308 Weld Matl & Hand Filed to Design contour.W/910521 Ltr ML20029C2101991-03-20020 March 1991 LER 91-002-01:on 901009,inadvertent Start of Auxiliary Feedwater Pump Occurred.Caused by Inadequate Test Procedures.Auxiliary Feedwater Pump Secured & Maint Work Request Mwr 904517 initiated.W/910320 Ltr ML20029C1141991-03-12012 March 1991 LER 91-010-01:on 900816,axial Flux Differential Outside Tech Specs Limits Due to Malfunction of Turbine Electrohydraulic Governor Control.Operator Training Revised. W/910319 Ltr ML20028H0321990-09-27027 September 1990 LER 90-011-00:on 900829,low Net Positive Suction Head to Containment Spray Pumps W/Eccs in Recirculation Mode Occurred.Caused by Procedural Deficiency.Temporary Procedure Changes initiated.W/900927 Ltr ML20043G2011990-06-0808 June 1990 LER 90-005-00:on 900510,steam Generator lo-lo Level Reactor Trip Occurred During Cold Shutdown.Caused by Inadequate Warning Sign Posting.Nonconformance Rept Written to Document Event & Recommend evaluation.W/900608 Ltr ML20042G7761990-05-0909 May 1990 LER 90-003-00:on 900409,determined That Piping & Supports in Fuel Oil Pumphouse Could Not Be Demonstrated to Perform Support Functions.Caused by Design Base Not Sufficiently Documented.Mod Performed to Support Fuel Oil Piping ML20042G7791990-05-0808 May 1990 LER 90-004-00:on 900404,single Failure Potential in Safeguards Switchgear B03/B04 Tie Breaker Discovered & Could Have Resulted in Failure of Diesel Generator.Control Power Fuses for Tie Breakers Removed ML20042F5361990-05-0404 May 1990 LER 90-001-00:on 900405,auxiliary Feed Pump Inadvertently Started.Caused by Inadequate Design.Schematic Push to Test Lamp Circuitry Will Be Added to Elementary Wiring Diagrams & Personnel Briefed on Potential circuitry.W/900504 Ltr ML20042F1971990-05-0202 May 1990 LER 90-002-00:on 900402,main Steam Safety Valve 1-MS-2013 Failed to Relieve Setpoint During Tech Spec Testing.Caused by Personnel Error During Setpoint Adjustment.Safety Valves 1-MS-2011,1-MS-2006 & 1-MS-2008 restored.W/900502 Ltr ML20011D5131989-12-19019 December 1989 LER 89-010-00:on 891120,auxiliary Feedwater Flow Transmitters Inadvertently Isolated.Caused by Error in Approved Procedure & Personnel Cognitive Error.Unit 1 Transmitters Valved Back Into Svc immediately.W/891219 Ltr ML19351A6721989-12-15015 December 1989 LER 89-009-00:on 891115,unexpected Steam Generator a lo-lo Level & Steam Generator B lo-lo Level Reactor Trip Signals Experienced.Caused by Installation of Analog Signal Generator.Procedures revised.W/891215 Ltr ML19332F7011989-12-11011 December 1989 LER 89-008-01:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power.Caused by Less than Adequate Tech Spec Change.Power Descension to 38% initiated.W/891211 Ltr ML19332E7221989-12-0707 December 1989 LER 89-009-00:on 891107,D05 & D06 Station Batteries Declared Inoperable.Caused by Original Design Deficiency.Mod Completed to Restore Battery D05 to Operable Status by Replacing Eight nonsafety-related breakers.W/891207 Ltr ML19332E8921989-12-0404 December 1989 LER 89-008-00:on 891103,during Refueling,Contractor Personnel Generated False Trip Signal While Investigating Wiring Discrepancy in Reactor Protection Sys Instrument Racks.Caused by Labeling Error.Supply changed.W/891204 Ltr ML19332F0901989-11-28028 November 1989 LER 89-003-01:on 890712,tank B Level Channel 2LE-934 Began to Indicate Spuriously.Caused by Moisture Intrusion Between Halar Insulator & Sensing Rod.Level Detector Replaced & Channel Reestablished for Accumulator Tank B.W/891128 Ltr ML19332C8411989-11-22022 November 1989 LER 89-007-00:on 891027,Train a Safety Injection Signal Generated During Installation of Mod in Containment High Pressure Circuit.Caused by Inadequate Installation Procedure.Procedure changed.W/891122 Ltr ML19327C2001989-11-14014 November 1989 LER 89-006-01:on 891015,steam Generator Tubes Found Degraded,W/Undefined Signal & W/Axial Indications in Tubesheet Area.Degradation Caused by Time.Affected Tubes Plugged or Preventively sleeved.W/891114 Ltr ML19327C0651989-11-0606 November 1989 LER 89-005-00:on 891006,intermediate Range High Level Trip Signal Unexpectedly Generated During Course of Routine Source Range Channel Calibr.Caused by Loose Connection of Input/Output Cable.Connection tightened.W/891106 Ltr ML19327B3061989-10-19019 October 1989 LER 89-008-00:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power, Disenabling Sys.Caused by High Tech Spec Setpoint.Enable/ Disable Setpoint Reset to 30%.W/891019 Ltr ML18041A1611987-11-16016 November 1987 LER 87-004-01:on 870515,voltage Lost on Red Instrument Bus Resulting in Reactor Protection Sys Actuation.Caused by Excessive Current Demand by ferro-resonant Circuit.Plant Mods to Load Bank Proposed ML18041A1341986-07-0303 July 1986 LER 86-003-00:on 860603,reactor Trip Occurred Due to Loss of Power on White Instrument Bus.Caused by Trip of White Inverter Output Breaker.Procedures for Placing Inverter on Line Will Be revised.W/860703 Ltr ML20028E3551983-01-13013 January 1983 LER 82-029/03L-0:on 821216,automatic Monitoring & Alarm Program Constant Found Incorrect.Caused by Unknown Personnel W/Access to on-line Computer.Value of Constant Restored & Control Rods Alignment Verified ML20028E2381983-01-13013 January 1983 LER 82-028/03L-0:on 821215,routine Test on Fire Detection Sys Found Panel D407 Which Monitors Unit 1 Rod Drive Room Inoperable.Caused by Blown Fuse.Fuse & Indication Lights Replaced on 821215.Detection Sys Undergoing Design Review ML20028E1791983-01-13013 January 1983 Updated LER 82-020/01X-1:on 821102,while Performing Type B & C Leakage Tests of Containment Penetrations & Isolation Valves,One Valve Had Leakage Exceeding Limit.Cause Not Stated.Valve Clapper & Seat Lapped ML20028E3031983-01-11011 January 1983 LER 82-027/03L-0:on 821211,operator Noted That Steam Generator Pressure Transmitter 1PT-469 Indicated Higher than Other Channels.Caused by Frozen Sensing Line Due to Inadequate Interim Piping Insulation ML20028E3211983-01-10010 January 1983 Updated LER 82-017/01X-2:on 821030,w/unit Shut Down for Refueling,Eddy Current Exam of Steam Generator Tubes Indicated Four Tubes in Steam Generator a & Three Tubes in Steam Generator B Exceeded Plugging Limit.Caused by Caustic ML20028C2431982-12-27027 December 1982 LER 82-020/01T-0:on 821103,following Type B & C Leak Rate Tests,Total as-measured Leakage Exceeded Tech Spec Limit, Causing Reactor Coolant Pump Component Cooling Water to Have Excessive Leakage.Cause Not Stated.Clapper & Seat Lapped ML20023B3251982-12-10010 December 1982 Updated LER 82-017/01T-1:on 821030,verified That Indications for Four Steam Generator a Tubes & Three Steam Generator B Tubes Exceeded 40% Plugging Limit During Eddy Current Exam on 821026-30.Cause Not Stated.Tubes Mechanically Plugged ML20028B4151982-11-15015 November 1982 LER 82-017/01T-0:on 821030,four Tubes in Steam Generator a & Three Tubes in Steam Generator B Indicated Degradation Greater than 40% Plugging Limit.Caused by Intergranular Attack.Tubes Mechanically Plugged ML20028A0371982-11-0505 November 1982 LER 82-008/03L-0:on 821006,low Steam Line Pressure Setting for Pressure Instrument 2PT-478 Found Lower than Allowed by Tech Specs.Caused by Bumping of Setpoint Adjustment Knob.Instrument Tested & Realigned ML20027D6821982-11-0303 November 1982 LER 82-018/01T-0:on 821015,incorrect Instrument Bus Supply Shifted to Alternate Supply Following Rept of Fire in Supply Breaker for 1GYO4 Motor Generator Set,Causing Loss of Redundancy on Containment Pressure Indicator 1PT-950 ML20052G4501982-05-12012 May 1982 LER 82-002/01T-0:on 820428,during Eddy Current Exam, Discovered Abnormal Degradation in Fuel Cladding,Rcpb & Primary Containment.Seludge Lancing Will Be Performed ML20052G3701982-05-0707 May 1982 LER 82-009/03L-0:on 820408,4.16-kV Safeguards Undervoltage Relays Did Not Meet 0-volt Time Delay Spec.Caused by Manufacturer Characteristic Curves.Relays Not Capable of Less than 0.38-s.Tech Spec Change Requested on 820427 ML20052G3831982-05-0707 May 1982 LER 82-011/03L-0:on 820415,during Biweekly Calibr Check ICP 2.1 of Reactor Protective Sys Functions,Overpower Delta T Setpoint 2 for Channel 2 Found Less Conservative than Tech Spec Limit.Caused by Setpoint Drift in Impulse Summer Unit ML20052G6331982-05-0707 May 1982 LER 82-010/03L-0:on 820414,ICP 2.9 Found Not to Provide for Proper Unblocking of Source Range High Flux Reactor Trip Over Small Range of Instrument Readings.Caused by Failure to Identify Subtle Procedural Flow.Procedure to Be Revised ML20052B4521982-04-23023 April 1982 LER 82-008/03L-0:on 820323,minor Installation Defects Noted on Four of Six Containment Pressure Transmitters Installed as TMI Response Mod.Caused by Backfit Contractor QC Program Breakdown ML20050B2661982-03-25025 March 1982 LER 82-006/01T-0:on 820311,type B & C Valve Leakage Tests Exceeded Tech Spec Limits.Caused by Corrosion.Svc Air Check Valves Disc Replaced & Valve Cover Remachined ML20041F4861982-03-0808 March 1982 LER 82-005/01T-01:on 820222,poison Test Samples & Two Fuel Assemblies W/Less than 1-yr Cooling Period Found Placed Next to Divider Wall in Spent Fuel Pool.Caused by Tech Spec Misinterpretation ML20041E4911982-03-0404 March 1982 LER 82-004/03L-0:on 820206,during Inservice Testing, Differential Pressure Instrument 4007 for Auxiliary Feed Pump P38A Found Isolated.Probably Caused by Failure to Return Instrument to Svc Following Calibr ML20041E6131982-03-0202 March 1982 LER 82-003/01T-0:on 820217,during Surveillance Testing, Emergency Diesel Generator 3D Failed to Operate.Caused by Sticking Shutdown Solenoid Plunger on Woodward Type UG8 Governor.Solenoid Cleaned,Checked & Generator Tested ML20049H6981982-02-23023 February 1982 LER 82-001/03L-0:on 820203,boric Acid Heat Tracing Circuit P-42 Found Inoperable.Caused by Failed Thermon Type 4 Circuit Controller.Circuit Controller Replaced ML20040G6811982-02-0505 February 1982 LER 82-001/03L-0:on 820107,steam Generator Pressure Sensing Lines Discovered Frozen on a Steam Generator.Caused by Inadequate Freeze Protection & Extremely Cold Weather.Addl Heat Lamps Installed ML20040G5801982-02-0505 February 1982 LER 82-002/03L-0:on 820112,during Hot shutdown,1PT-469 Steam Generator Pressure Transmitter Isolated by Maint Personnel Due to Leaking Coupling.Pressure Sensing Tubing Showed Signs of Steam Leak Due to Freezing ML20040D3791982-01-18018 January 1982 LER 81-020/03L-0:on 811219,frozen Sensing Line Caused High Indication of Steam Generator Pressure Instrument 1PT-482. Caused by Incomplete Insulation of Line & by Cold Weather. Instrument Placed in Tripped Position & Tubing Thawed 1994-04-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARNPL-99-0569, Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with ML20212D5961999-09-15015 September 1999 Safety Evaluation Supporting Licensee IPEEE Process.Plant Has Met Intent of Suppl 4 to GL 88-20 NPL-99-0051, Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with NPL-99-0449, Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with ML20196J4251999-06-30030 June 1999 Safety Evaluation Authorizing Proposed Alternatives Described in Relief Requests VRR-01,ROJ-16,PRR-01 & VRR-02 ML20209D2691999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbnps,Units 1 & 2 ML20196F3341999-06-22022 June 1999 Safety Evaluation for Implementation of 422V+ Fuel Assemblies at Pbnp Units 1 & 2 ML20195F9781999-06-10010 June 1999 Unit 2 Refueling 23 Inservice Insp Summary Rept for Form NIS-1 ML20209D2751999-05-31031 May 1999 Revised MORs for May 1999 for Pbnps,Units 1 & 2 NPL-99-0328, Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with NPL-99-0273, Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With ML20196F3521999-04-30030 April 1999 Non-proprietary WCAP-14788, W Revised Thermal Design Procedure Instrument Uncertainty Methodology for Wepc Point Beach Units 1 & 2 (Fuel Upgrade & Uprate to 1656 Mwt - NSSS Power) NPL-99-0193, Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with NPL-99-0134, Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with ML20207D6751999-02-22022 February 1999 Assessment of Design Info on Piping Restraints for Point Beach Nuclear Plant,Units 1 & 2.Staff Concludes That Licensee Unable to Retrieve Original Analyses That May Have Been Performed to Justify Removal of Shim Collars ML20206R9001999-01-13013 January 1999 SER Accepting Nuclear Quality Assurance Program Changes for Point Beach Nuclear Plant,Units 1 & 2 NPL-99-0008, Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with NPL-99-0091, 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with1998-12-31031 December 1998 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with ML20198C7671998-12-10010 December 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME BPV Code,1986 Edition,Section XI Requirement IWA-2232, to Use Performance Demonstration Initiative Program During RPV Third 10-yr ISI for Plant,Unit 2 NPL-98-1006, Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20195J5101998-11-16016 November 1998 Proposed Revs to Section 1.3 of FSAR for Pbnp QA Program ML20198J5941998-11-0303 November 1998 1998 Graded Exercise,Conducted on 981103 NPL-98-0948, Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With NPL-98-0880, Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored1998-10-21021 October 1998 Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored ML20154M9121998-10-14014 October 1998 Unit 1 Refueling 24 Repair/Replacement Summary Rept for Form NIS-2 ML20154L6751998-10-14014 October 1998 Unit 1 Refueling 24 ISI Summary Rept for Form NIS-1 NPL-98-0826, Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20151W3851998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Pbnp Units 1 & 2 NPL-98-0653, Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4471998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 2 ML20151W4541998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 1 ML20236Q3161998-07-10010 July 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME Code Requirements PTP-3-01 & PTP-3-02 ML20236L6771998-07-0707 July 1998 Safety Evaluation Approving Wepco Implementation Program to Resolve USI A-46 at Point Beach NPP Units 1 & 2 NPL-98-0558, Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 2 ML20151W4261998-06-30030 June 1998 Corrected Page to MOR for June 1998 for Pbnp Unit 2 ML20151W4221998-05-31031 May 1998 Corrected Page to MOR for May 1998 for Pbnp Unit 2 NPL-98-0481, Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4011998-04-30030 April 1998 Corrected Page to MOR for April 1998 for Pbnp Unit 2 NPL-98-0356, Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20217F3131998-04-17017 April 1998 Safety Evaluation Accepting Proposed Alternative to ASME Code for Surface Exam of Nonstructural Seal Welds,For Plant, Unit 1 ML20216D7071998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3981998-03-31031 March 1998 Corrected Page to MOR for March for Pbnp Unit 2 NPL-98-0209, Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable1998-03-30030 March 1998 Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable ML20217A8501998-03-19019 March 1998 SER Accepting Proposed Changes Submitted on 980226 by Wiep to Pbnp Final SAR Section 1.8 Which Will Impact Commitments Made in Pbnp QA Program Description.Changes Concern Approval Authority for Procedures & Interviewing Authority ML20216J0101998-03-17017 March 1998 Safety Evaluation Accepting Third 10-yr Inservice Insp Interval Relief Request RR-1-18 for Plant NPL-98-0159, Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3891998-02-28028 February 1998 Corrected Page to MOR for Feb 1998 for Pbnp Unit 2 ML20216D7121998-02-28028 February 1998 Revised Corrected MOR for Feb 1998 for Point Beach Nuclear Plant,Unit 2 NPL-98-0084, Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 21998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20198L1151998-01-0808 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Point Beach Nuclear Plant,Units 1 & 2 1999-09-30
[Table view] |
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On October 12, 1992, while Point Beach Nuclear Plant (PBNP) Unit 1 was operating at 100% power and Unit 2 was shut down during its annual refueling outage (U2R18), staff engineering personnel identified that component cooling water (CCW) system surge tank Vent Valves 1&2CC-00017 did not meet their design basis. The plant's design basis requires that the CCW system be considered a closed system outside containment. Any portion of the system that cannot be assured of being naintained clored must be isolated by a safety-related isolation signal. Contrary to these requirements, it was identified that the automatic closing signals for Unit 1 and Unit 2 CCW system surge tank Vent Valve 1&2CC-00017 (which are normally open) are high radiation signals from Radiation Monitors 1&2RE-217, which are designated as non-safety-related. In addition, the valve control circuits for Valves 1&2CC-00017 are designated as non-safety-related and are supplied by non-safety-related power supplies. An event causing a radioactive release to containment and a breach of the CCW system inside containment could ;
result in a radioactive release to the primary auxiliary building (PAB) if Radiation Monitor RE-217 did not initiate the closure of Valves CC-00017. A Justification for Continued Operation (JCO) was l approved on October 26, 1992, and subsequently revised on February 25, j 1993, to allow continued operation with valve 1&2CC-00017 open until I l resolution of this issue.
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0 l1 0l2 or 0l 7 Tm er- . .-.4 . .m._.~ n = mu mm EVENT AND EOUIPMENT DESCRIPTION During the electrical design phase of a plant modification to upgrade radioactive waste disposal system component cooling water Isolation Valves LW-63 and LW-64 (Corrective Action C.1 of Licensee Event Report 301/92-002-00), it was identified that the high radiation signals provided to Unit 1 and Unit 2 component cooling water (CCW) system surge tank Vent Valves 1&2CC-00017 (hereinafter referred to as Valve CC-00017) to achieve containment isolation in the CCW system were not designated as safety-related. Radiation Monitors 1&2RE-217 (hereinafter referred to as Radiation Monitor RE-217) are designed to monitor the CCW radioactivity levels at the CCW pump suction headers of both units and provides indication and alarms in the control room of CCW contamination. Although the radiation monitoring system (RMS) is quality assurance (QA) grade and seismically qualified, the RMS is not designated as s.afety-related. Therefors, it is postulated that RE-217 could fail to generate a high radiation signal when necessary, thereby disabling the automatic containment isolation function. Although operator action could compensate for this failure, this does not meet containment isolation design basis requirements.
Point Beach Nuclear Plant was designed before the issuance of the NRC General Design Criteria (GDC) (10 CFR 50, Appendix A, issued in 1971) and was licensed at the same time the proposed Appendix A was published for review (July 1967). The GDC do not recognize the use of a closed system outside of containment as an acceptable means to provide containment isolation. In the standard Westinghouse two-loop pressurized water reactor design, the operation of the reactor coolant pumps (RCPs) was considered desirable following many accidents inside containment and automatic isolation of CCW to the RCPs was not .
provided during all accidents. This decision led to the requirement to demonstrate that public health and safety would not be adversely affected if an accident, which released radioactivity and breached the CCW system, occurred incide containment. Under these accident conditions (according to vendor correspondence) the pressure inside containment would force the cooling water out of the piping, into the surge tank, and eventually out of the tank's vent. Once radioactivity was sensed in the CCW outside containment, the radiation monitor would cause the surge tank vent valve to close and prevent the release of radioactivity to the environment. With the closing of the vent valve, the CCW system would become a closed system with a design pressure greater than the containment, and thus become an extension of containment. The arrangement of the CCW piping to the RCPs was defended in Atomic Energy Commission (AEC) hearings prior to and during the development of the GDC. PBNP was licensed on the basis of considering the CCW system to be a closed system outside containment.
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0l 1 01 3 OF 0l7 TIXT dromre ame a me.arest se esempiW 8rAc Feren JEEA W (TF8 According to Section 5.2 of the PBNP Final' Safety Analysis Report (FSAR), the CCW system is required to be a closed system outside containment. PBNP was designed so that no manual action was required to initiate immediate containment isolation upon receipt of a valid signal. The intent was to provide at least one automatic barrier (trip valve, check valve, or closed system) for each containment penetration. Redundancy would be provided for each penetration by a second isolation barrier which is not required to be automatic. In the CCW system return lines from the RCPs, the automatic barrier is considered to be the closed system outside of containment. Therefore, closed system integrity is required to be established automatically, as-in the case of the CCW surge tank vent valve receiving a high radiation signal from RE-217 insuring closed system integrity if this barrier is required.
CAUSE .
A review of related documentation and discussions with vendor j personhel has not allowed determination of the reason for the design ,
of the isolation signal and control circuit associated with Vent l Valve CC-00017. We believe that this design deficiency was an i apparent oversight during the original design of the CCW system. !
CORRECTIVE ACTIONS l
A. Short Term:
A Justification for Continued Operation (JCO) was approved on pctober 26, 1992, by the PBNP-Manager's Supervisory Staff allowing Valve CC-00017 to remain open during normal operations in order to .
prevent the possible overpressurization or vacuum condition in the CCW system.
The JCO determined operation in the identified configuration is considered acceptable for the following reasons: ;
1
- 1. Valve CC-00017 is safety-related and fails closed on ;
deenergization. !
I
- 2. The valve's control circuit is a control grade circuit which receives a signal from the radiation monitoring system (RMS).
Radiation Monitor RE-217 is powered from 120 VAC vital i Instrument Bus Y114. i 1
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- 3. The valve shuts on a high radiation signal from Radiation i Monitor RE-217.
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- 4. Radiation Monitor RE-217 is QA scope and seismically qualified.
- 5. Remote operation and position indication are available in the control room for Valve CC-00017.
- 6. Radiation Monitor RE-217 has an alarm on Control Panel C-03 located in the control room. The response for the alarm includes verifying that Vent Valve CC-00017 is shut.
The CCW system is normally in continuous operation with CCW surge tank Vent Valve CC-00017 open. According to vendor correspondence, closure of the vent valve could result in the increase of pressure (above normal atmospheric pressure) in the surge tank due to system inleakage or an increase in the system heat load. The pressure in the surge tank could then increase to the set pressure of the surge tank relief valve.
Additionally, Operations Special Order 92-06, "CCW-LW-63&64, 1&2CC-17 Component Cooling System Valve Interim Operations," was revised November 7, 1992, to assure a designated control room operator shuts Valve CC-00017 when containment isolation is required.
C. Long Term:
l Subsequent to our original LER submittal dated November 11, 1992, l we identified several options to resolve this issue. Three l possible hardware modification options and one non-modification l option that would satisfy the containment isolation provisions are l as follows:
l l 1) Replace the existing radiation detector and its associated l control grade circuitry with a dicated safety-related system.
l l 2) Automatically close the surge tank vent valve on a HI-HI l containment pressure signal by adding this additional safety-l related control circuitry.
l l 3) Remove the necessity for a " closed" system outside containment l by adding automatic closure (HI-HI containment pressure) l circuitry to Motor-Operated Valves CC-754A, 754B, 759A, and l 759B. These valves are currently remotely operated from the l control room, are included in the 10 CFR 50, Appendix J leak j testing program, and have safety-related control circuitry.
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011 0l5 OF pl .7 rm er s m .oe.-asecr .a wsm l 4) Operate the system with the surge tank vent valves'normally l closed.
l A meeting with Westinghouse personnel to discuss the proposed
! options was conducted on February 15, 1993. The option of l operating the CCW system with the surge tank vent valves closed was l determined to be the most desirable solution. On February 25, j 1993, the options were presented to the PBNP Manager's-Supervisory l Staff. The Manager's Supervisory Staff concurred with the l recommendation of operating the CCW system with the surge tank vent l_ valves closed. However, in order to implement this option, further l review of potential consequences such as equipment overpressure, j pump performance, surge response, and gasses escaping solution l needed to be performed.
l l Our contractor has completed an assessment of CCW system operation l with the surge tank vent valve closed and has concluded that this j mode of operation is feasible. Tl:ey are proceeding with f formalizing their evaluation which includes finalizing the l calculations that document the system evaluation, a review of .
j system overpressure protection and relief valve sizing, and l identification of procedural or design changes to support the vent
! valve closure modification.
l l We will implement this configuration by September 25, 1993, j following completion of final calculations, revisions to operating j procedures, and post-alignment testing. This date corresponds to l the beginning of our Unit 2 refueling shutdown and will provide l ' appropriate plant conditions for CCW system testing. .
REPORTABILITY This event is being reported under the requirements of 10 CFR 50.73(a)
(2) (ii) (B) , "The licensee shall report...any event or condition that resulted in the nuclear power plant being in a condition that was outside the design basis of the plant," and 10 CFR 50.73 (a) (2) (v) (D) ,
"The licensee shall report...any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident."
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SAFETY ASSESSMENT !
In the unlikely event of a radioactive release to containment and a breach of CCW piping, a radioactive release to the environment would result if Radiation Monitor RE-217 did not fulfill its automatic function and not initiate the closure of CCW surge tank .
Vent Valve CC-00017. This could result in a radioactive release into the primary auxiliary building (PAB), through its ventilation exhaust,-
and to the environment until plant operating personnel could isolate the ,
breach by closing the motor-operated containment isolation valves (which serve as the redundant isolation barrier) or the CCW surge tank vent' ,
valve.
The PAB ventilation exhaust is continuously monitored for radioactivity ~
concentration during normal operations, anticipated transients, and accident conditions. If PAB exhaust ventilation Gas Monitor RE-214 detects radiation levels exceeding acceptable levels, the PAB exhaust is automatically shifted to pass through carbon filters and high efficiency ;
. particulate air (HEPA) filters to minimize the release of radioactive (
isotopes to the environment. Therefore, the automatic switchover function of the PAB exhaust to the carbon filters combined with the compensatory measures listed in the Justification for Continued Operation ensures that the safety of the plant and the health and safety of the public and plant employees are not jeopardized while in' the plant's current configuration.
GENERIC IMPLICATIONS The normally open status of CCW surge tank Vent Valve CC-00017 was confirmed to be an original plant design. This also appears to be a standard Westinghouse two-loop pressurized water reactor design which could be a generic concern of other plants of similar design. On July 12, 1984, Westinghouse notified the NRC under 10 CFR 21 of a potential overpressurization condition in the CCW systems designed by Westinghouse. Westinghouse reported that the overpressurization condition could result from closure of the surge tank vent valve on a high radiation signal from the radiation detectors within the CCW l system. Subsequent to this notification, we replaced the existing CCW j surge tank relief valve with a new relief valve set at a lower pressure j in order to prevent the potential overpressure condition. In related correspondence, there was much discussion regarding the closed system integrity and other containment options available, but there was no discussion of the classification of the associated valves or circuitry.
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Og 1 0l 7 or 0l7 rrxva - - . . - ==ci 3ero,irri SIMILAR OCCURRENCES On August 18, 1992, the Unit 1 reactor protection system, engineered safeguards system, and associated process instrumentation were declared inoperable when a seismic review of the auxiliary feedwater system revealed that the Unit I control room instrumentation cabinets did not meet their original seismic design criteria as specified in the PBNP FSAR. This event was reported in LER 266/92-007-00 on September 15, 1992.
On August 28, 1992, plant personnel discovered component cooling water (CCW) system Isolation Valves LW-63 and LW-64 in a condition outside of the plant's design basis. Valves LW-63 and LW-64 were discovered to not be capable of providing the appropriate interface between the Seismic Class I and Seismic Class III portions of the CCW system as specified in the PENP FSAR. This event was reported in LER 301/92-002-00 on September 28, 1992. ,
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