ML18005A250

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LER 87-064-00:on 871102 & 1218,waste Processing Bldg Vent Stack 5A Wide Range Gas Monitor 1WV-3547-1 Declared Inoperable W/O Required Special Rept Submitted.Caused by Personnel Error.Procedure OMM-003 revised.W/880118 Ltr
ML18005A250
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 01/18/1988
From: Jerrica Johnson, Watson R
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
HO-880007-(O), LER-87-064, LER-87-64, NUDOCS 8801220204
Download: ML18005A250 (8)


Text

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+CFELERXTED IHSIBUTION DEMONSTEON SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR: 8801220204 DOC. DATE: 88/01/18 NOTARIZED: NO. DOCKET g FACZL:50-400 Shearon Harris Nuclear Power, Plant, Unit 1, Carolina 05000400 AUTH. NAME AUTHOR AFFILIATION JOHNSON,J.R. Carolina Power E Light Co.

WATSON,R.A. Carolina Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 87-064-00:on 871218,special rept re inoperative radiation monitor not submitted within required time frame.

W/8 ltr.

DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ) ENCL SIZE:

TITLE: 50.73 Licensee Event Report (LER), Inci&d nt Rpt, etc.

NOTES:Application for permit renewal filed. 050004008 RECIPIENT ZD CODE/NAME PD2-1 LA COPIES LTTR ENCL 1 1 RECIPIENT ID CODE/NAME

.PD2-1 PD COPIES LTTR ENCL j

A 1 1 BUCKLEY,B 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 AEOD/DOA 1 1 AEOD/DSP/NAS 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 ARM/DCTS/DAB 1 1 DEDRO 1 1 NRR/DE ST/ADS 1 0 , NRR/DEST/CEB 1 1 NRR/DEST/ELB 1 1 NRR/DEST/ICSB 1 1 NRR/DEST/MEB 1 1 NRR/DEST/MTB 1 1 NRR/DEST/PS B 1 1 NRR/DEST/RSB 1 1 NRR/DEST/SGB 1 1 NRR/DLPQ/HFB 1 1 NRR/DLPQ/QAB 1 1 NRR/DOEA/EAB 1 1 NRR/DREP/RAB 1 1 NRR/DREP/RPB 2 2 R- SZB 1 1 NRR/PMAS/ILRB 1 1 EG 02 1 1' RES TELFORD,J 1 1 RES/DE/EI B '

RES/DRPS DIR 1 1 RGN2 FILE 01 1 1 EXTERNAL: EGGG GROH,M 5 5 FORD BLDG HOY g A 1 1 H ST LOBBY WARD 1 1 LPDR ' ( R 1

NRC PDR 1 1 NSIC HARRIS,J 1 1 NSIC MAYS,G 1 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 46 ENCL 45

NRC Form 3 UA. NUCLEAR REOULATORY COMMISSION (943)

APPROVED DMS NO. 31604104 LICENSEE EVENT REPORT (LER) EXPIRES: 8/31/88 FACILITY NAME (II DOCKET NUMBER (2) PACE 3 Shearon Harris Nuclear Power Plant Unit 1 o 6 o o o4pp >'OFO 3 Special Report Concerning Inoperative Radiation Monitor Was Not Submitted Within the Re uired Time Frame EVENT DATE ISI LER NUMBER (8) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)

MONTH DAY YEAR YEAR Q SEClVENTIAL jK<< REVtdlON MONTH

'UMBER NUMBER OAY YEAR FACILITYNAMES DOCKET NUMBER(S) 0 5 0 0 0 1 2 18 87 8 7 0 6 4 0 0 0 1 1 8 8 8 0 5 0 0 0 OPKRATINO THIS REPORT IS SUBMITTED PURSUANT T 0 THE REDUIREMENTB DF 10 cf R (): Icheck one or more of tne follovllnd) (11 MODE (9) 20A02(b) 20AOS(e) 60.73(a) (2) (Iv) 73.71(b)

POWER 20.405(e) (1)(I) 50.38(c)(1) 50.73(e)(2)(v) 73.71(c)

LEVEL

] p p 20AOS(a)(1) (El 50.38(c) (2) 50.73(e I (2) (v8) OTHER ISpeclfy In Abetract below end ln Text, IIRC Form i<'@g

>co /4/ooo/RRE I/44 oANorW //RC Sons 38843/ I(T) o s o o o 40 0 87 0 6 4 0003 oF 0 3 CAUSE: (continued) Specification. However, a "tracking EIR" should have been prepared to alert personnel to the inoperability of this monitor prior to entering Mode 3. Plant procedure OMM-003, Equipment Inoperable Record, did not adequately cover tracking an EIR in a situation such as this. Additional personnel errors occurred as on coming Shift Foremen reviewed the status of EIRs in effect between November 2, 1987 and December 18, 1987, and failed to recognize the requirement for a "tracking EIR," prior to Mode 3, or an active EIR after the plant had entered Mode 3. On November 5, 1987, at 2238, the plant entered Mode 3. The Operations Shift Foreman is required to review all LCOs prior to changing modes to verify that all Technical Specification requirements are met. Another error o'ccurred here in that the Shift Foreman failed to recognize the applicability of Technical Specification 3.3.3.6. ANALYSIS OF EVENT: This event was reportable due to a noncompliance with Technical Specification 3.3.3.6, Action- C, which required a special report to be submitted to the NRC within 14 days. Failure to 'submft the special 're'port within.the TequiTed/ time period had no safety consequences. The compensatory actions required by Technical Specification 3.3.3.11, Table 3.3-13, Actions 46, 47, and 49 required an auxiliary sampler to be hooked up to continuously monitor the stack while the installed monitor was inoperable. This sampler was installed at the purge air inlet connection for the iso-kinetic sampling skid, and was in place the entire time the monitor was inoperable. All compensatory measures for gaseous effluent and accident monitoring for Stack SA vere satisfied. There have been no previous events similar to this. CORRECTIVE ACTIONS:

1. The WRGM was restored to service on December 23, 1987.
2. The event/'as reviewed by all operating shift personnel during shift turnover meetings.
3. Plant procedure OMM-003, Equipment Inoperable Record, is being revised to provide better guidance for tracking EIRs and for maintaining cognizance of time requirements for LCOs.

N/IC SORM 344A (983 l R U.S.OPO:198bOb34 538/465 Carolina Power h Light Company HARRIS NUCLEAR PROJECT P.O. Box 165 New Hill, NC 27562 File Number.'HF/10-13510C Letter Number.'H0-880007 (0) U.ST Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF"63 LICENSEE EVENT REPORT 87-064-00 Gentlemen.'n accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted. report fulfills the requirement for a written report within This thirty (30) days of a reportable occurrence and is in accordance with the format set forth in NUREG-1022, September, 1983; Very truly yours, R. A. Watson Vice President Harris Nuclear Project RAW:dj Enclosure cc: Dr. J. Nelson Grace (NRC - RII) Mr. B. Buckley (NRR) Mr. G. Maxwell (NRC SHNPP) MEM/H0-8800070/1/OS1