ML14209A132

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IR 05000354-14-003, April 1, 2014 - June 30, 2014, Hope Creek Generating Station, Unit 1
ML14209A132
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 07/28/2014
From: Glenn Dentel
Reactor Projects Branch 3
To: Joyce T
Public Service Enterprise Group
DENTEL, GT
References
IR-14-003
Download: ML14209A132 (50)


See also: IR 05000354/2014003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BLVD., SUITE 100

KING OF PRUSSIA, PA 19406-2713

July 28, 2014

Mr. Thomas P. Joyce

President and Chief Nuclear Officer

PSEG Nuclear LLC - N09

P.O. Box 236

Hancocks Bridge, NJ 08038

SUBJECT: HOPE CREEK GENERATING STATION UNIT 1 - NRC INTEGRATED

INSPECTION REPORT 05000354/2014003

Dear Mr. Joyce:

On June 30, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Hope Creek Generating Station (HCGS). The enclosed inspection report documents the

inspection results, which were discussed on July 10, 2014 with Mr. P. Davison, Site Vice

President of Hope Creek, and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents one NRC-identified and four self-revealing findings of very low safety

significance (Green). Three of these findings were determined to involve a violation of NRC

requirements. Additionally, a licensee-identified violation, which was determined to be of very

low safety significance, is listed in this report. However, because of the very low safety

significance, and because they are entered into your corrective action program (CAP), the NRC

is treating the findings as non-cited violations (NCVs) consistent with Section 2.3.2.a of the

NRC Enforcement Policy. If you contest any NCVs in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial, to

the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-

0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement,

United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC

Resident Inspector at HCGS. In addition, if you disagree with the cross-cutting aspect assigned

to any finding, or a finding not associated with a regulatory requirement in this report, you

should provide a response within 30 days of the date of this inspection report, with the basis for

your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at

HCGS.

T. Joyce 2

In accordance with Title 10 of the Code of Federal Regulations (CFR) 2.390 of the NRCs Rules

of Practice, a copy of this letter, its enclosure, and your response (if any) will be available

electronically for public inspection in the NRCs Public Document Room or from the Publicly

Available Records component of the NRCs Agencywide Documents Access Management

System (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Glenn T. Dentel, Chief

Reactor Projects Branch 3

Division of Reactor Projects

Docket Nos.: 50-354

License Nos.: NPF-57

Enclosure: Inspection Report 05000354/2014003

w/Attachment: Supplementary Information

cc w/encl: Distribution via ListServ

ML14209A132

Non-Sensitive Publicly Available

SUNSI Review

Sensitive Non-Publicly Available

OFFICE RI/DRP RI/DRP RI/DRP

NAME JHawkins/ RSB for RBarkley/ RSB GDentel/ GTD

DATE 07/22 /14 07 /22/14 07 / 28 /14

1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos.: 50-354

License Nos.: NPF-57

Report No.: 05000354/2014003

Licensee: Public Service Enterprise Group (PSEG) Nuclear LLC

Facility: Hope Creek Generating Station (HCGS)

Location: P.O. Box 236

Hancocks Bridge, NJ 08038

Dates: April 1, 2014 through June 30, 2014

Inspectors: J. Hawkins, Senior Resident Inspector

S. Ibarrola, Resident Inspector

H. Gray, Senior Reactor Inspector

Approved By: Glenn T. Dentel, Chief

Reactor Projects Branch 3

Division of Reactor Projects

Enclosure

2

TABLE OF CONTENTS

SUMMARY ................................................................................................................................ 3

REPORT DETAILS .................................................................................................................... 7

1. REACTOR SAFETY ........................................................................................................... 7

1R01 Adverse Weather Protection .................................................................................... 7

1R04 Equipment Alignment ............................................................................................... 8

1R05 Fire Protection .......................................................................................................... 9

1R06 Flood Protection Measures .....................................................................................10

1R11 Licensed Operator Requalification Program ...........................................................13

1R12 Maintenance Effectiveness .....................................................................................14

1R13 Maintenance Risk Assessments and Emergent Work Control ................................16

1R15 Operability Determinations and Functionality Assessments ....................................19

1R18 Plant Modifications .................................................................................................20

1R19 Post-Maintenance Testing ......................................................................................20

1R22 Surveillance Testing ...............................................................................................21

1EP6 Drill Evaluation .......................................................................................................22

4. OTHER ACTIVITIES ..........................................................................................................22

4OA1 Performance Indicator (PI) Verification ....................................................................22

4OA2 Problem Identification and Resolution ....................................................................23

4OA3 Follow-Up of Events and Notices of Enforcement Discretion ..................................24

4OA5 Other Activities ........................................................................................................30

4OA6 Meetings, Including Exit ...........................................................................................31

4OA7 Licensee-Identified Violations ..................................................................................31

ATTACHMENT: SUPPLEMENTARY INFORMATION...............................................................31

SUPPLEMENTARY INFORMATION....................................................................................... A-1

KEY POINTS OF CONTACT .................................................................................................. A-1

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED .................................... A-1

LIST OF DOCUMENTS REVIEWED....................................................................................... A-2

LIST OF ACRONYMS ........................................................................................................... A-15

Enclosure

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SUMMARY

IR 05000354/2014003; 4/01/2014 - 6/30/2014; Hope Creek Generating Station; Flood

Protection Measures, Maintenance Effectiveness, Maintenance Risk Assessments and

Emergent Work Control, Follow-up of Events and Notices of Enforcement Discretion.

This report covered a three-month period of inspection by the resident inspectors and

announced inspections performed by regional inspectors. Five findings of very low safety

significance (Green) were identified. Three of the findings were determined to be violations of

NRC requirements. The significance of most findings is indicated by their color (i.e., greater

than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter

(IMC) 0609, Significance Determination Process (SDP), dated June 2, 2011. Cross-cutting

aspects are determined using IMC 0310, Components Within Cross-Cutting Areas, dated

December 19, 2013. All violations of NRC requirements are dispositioned in accordance with

the NRCs Enforcement Policy, dated July 9, 2013. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 5.

Cornerstone: Initiating Events

Green. A self-revealing finding of very low safety significance (Green) was identified for

PSEGs failure to evaluate an identified deficiency in accordance with PSEG procedure

LS-AA-125, Corrective Action Program. Specifically, PSEG failed to take self-

recommended actions in notification (NOTF) 20447050 to evaluate the B moisture

separator (MS) dump valve performance after failing to operate as designed during B MS

drain valve troubleshooting on January 11, 2010. As a result, PSEG did not identify and

correct a potential design flaw associated with thermal binding of the MS dump valves,

which was determined to be the cause of the A MS dump valve failing to stroke open on

December 1, 2013, leading to a reactor scram from 100 percent power. PSEGs corrective

actions include a design change to the MS emergency level control system that eliminates

dump valve cycling on high MS level.

The performance deficiency was determined to be more than minor because it was

associated with the equipment performance attribute of the Initiating Events cornerstone,

and adversely affected the cornerstone objective to limit the likelihood of events that upset

plant stability and challenge critical safety functions during shutdown as well as power

operations. The inspectors determined that this finding was of very low safety significance

(Green) using Exhibit 1 of NRC IMC 0609, Appendix A, The Significance Determination

Process (SDP) for Findings At-Power, dated June 19, 2012, because the finding did not

cause both a reactor trip and the loss of mitigation equipment relied upon to transition the

plant from the onset of the trip to a stable shutdown condition (e.g. loss of condenser, loss

of feed water). The inspectors determined that there was no cross-cutting aspect

associated with this finding because the cause of the performance deficiency occurred

more than three years ago, and was not representative of present plant performance.

(Section 1R12)

Green. A self-revealing Green NCV of Technical Specification (TS) 6.8.1.a, Procedures

and Programs, was identified for PSEGs failure to follow procedure MA-AA-1000,

Maintenance Standards and Practices, during the replacement of Bailey logic modules

(LM) associated with the D vital bus (10A404). Specifically, during the spring 2009

Enclosure

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refueling outage (1R15), PSEG failed to follow a work order (WO) requiring the replacement

of all Bailey logic modules listed in WO 60061175 with new logic modules. As a result, a

logic module (H1PB-1PBXIS-DC652010302) for the D vital bus was not replaced during

1R15, and failed due to age on December 19, 2013, causing a loss of the vital bus and an

entry into the associated 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> Technical Specification Action Statement (TSAS) 3.8.3.1

for Onsite Power Distribution Systems. PSEGs corrective actions included replacement of

the failed logic module, performance of an extent of condition inspection to ensure other

similar logic modules and relays were replaced, and reinforcement of proper maintenance

practices with the individuals involved in the completion of WO 60061175.

The performance deficiency was determined to be more than minor because it was

associated with the human performance attribute of the Initiating Events cornerstone, and

adversely affected the cornerstone objective to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. Specifically, not following the work order instructions resulted in an extended

service duration and failure of a component that resulted in a loss of power to the D vital

bus on December 19, 2013. Similarly, this performance deficiency was also similar to

examples 2.g and 4.b of NRC IMC 0612, Appendix E, in that PSEG is required to follow

their procedures per TS 6.8.1, and ultimately led to a safety impact given the failure of the

logic module causing a loss of power to the 10A404 vital bus. The inspectors determined

the finding to be of very low safety significance (Green) in accordance with Exhibit 1 of NRC

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,

dated June 19, 2012, because the finding involved the loss of a support system that

contributes to the likelihood of an initiating event (Loss of an AC Bus), but did not affect

mitigation equipment. The inspectors determined that there was no cross-cutting aspect

associated with this finding because the cause of the performance deficiency occurred

more than three years ago, and was not representative of present plant performance.

(Section 1R13)

Green. A self-revealing finding of very low safety significance (Green) was identified when

PSEG failed to ensure that appropriate contingency actions were in place prior to the

performance of A MS emergency level controller tuning as required by WC-AA-105, Work

Activity Risk Management. Specifically, the decision to tune the emergency level controller

without appropriate contingencies in place led to a turbine trip on high A MS level and

subsequent reactor scram on December 5, 2013. PSEGs corrective actions included

conducting performance management with the individuals involved with the tuning evolution

and revising the moisture separator drain tank level tuning procedure to require an

individual at the normal and emergency controllers when performing emergency level

controller tuning.

This finding was more than minor because it was associated with the human performance

attribute of the Initiating Events cornerstone, and adversely affected the cornerstone

objective to limit the likelihood of events that upset plant stability and challenge critical safety

functions during shutdown as well as power operations. The inspectors determined that this

finding was of very low safety significance (Green) using Exhibit 1 of NRC IMC 0609,

Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated

June 19, 2012, because the finding did not cause both a reactor trip and the loss of

mitigation equipment relied upon to transition the plant from the onset of the trip to a stable

shutdown condition (e.g. loss of condenser, loss of feed water). The inspectors determined

that the finding had a cross cutting aspect in the Human Performance area associated with

Work Management, because PSEG personnel did not implement a process of planning,

Enclosure

5

controlling, and executing work activities such that nuclear safety is the overriding priority.

Specifically, technicians were only stationed at the emergency level controller during the

tuning, when having technicians at both controllers would have provided more time to

recover from a high level condition in the A MS, and may have prevented the turbine trip

and subsequent reactor scram on December 5, 2013. [H.5] (Section 4OA3)

Cornerstone: Mitigating Systems

Green. The inspectors identified a Green NCV of TS 6.8.1.a, Procedures because PSEG

procedures HC.OP-AR.ZZ-0006 and HC.OP-AR.ZZ-0022 could potentially complicate an

internal flooding event and adversely affect assumptions in Hope Creeks flood design.

Specifically, the procedures did not ensure operator response would not communicate the

high pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) watertight

rooms and potentially render two safety-significant single train systems inoperable. In

addition to entering the issue into the corrective action program (CAP) as NOTFs

20646334, 20646335 and 20620653586, PSEGs corrective actions include a planned

revision of the annunciator response procedures and issuance of a standing order to the

Operations department staff.

The performance deficiency is more than minor because it was associated with the

procedure quality attribute of the Mitigating Systems cornerstone and adversely affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences (i.e., core damage).

Specifically, PSEG procedures HC.OP-AR.ZZ-0006 and HC.OP-AR.ZZ-0022 could

potentially complicate an internal flooding event and adversely affect assumptions in Hope

Creeks flood design, since the procedures did not ensure operator response would not

communicate the HPCI and RCIC watertight rooms and potentially render multiple trains of

safety-related SSCs inoperable. This performance deficiency was also similar to examples

3.j and 3.k of NRC IMC 0612, Appendix E, in that communicating the two watertight rooms

created a reasonable doubt of operability of the HPCI and RCIC systems. PSEG plans to

perform a detailed technical evaluation to evaluate the impact of internal flood propagation

in the HPCI and RCIC rooms. The finding was evaluated in accordance with Exhibits 2 and

4 of NRC IMC 0609, Appendix A, The SDP for Findings At-Power, dated June 19, 2012.

Since opening the watertight door during an internal flooding event could bypass the flood

protection feature and potentially degrade two or more trains of a multi-train system or

function, a detailed risk assessment was performed. The finding was determined to be of

very low safety significance (Green). Since the change in core damage frequency was

sufficiently low, no further evaluation for large early release was required. The inspectors

determined that the finding had a cross cutting aspect in the Human Performance area

associated with Training, in that PSEG did not provide adequate training and ensure

knowledge transfer to maintain a knowledgeable, technically competent workforce and instill

nuclear safety values. Specifically, operator training did not ensure operator response to

internal flooding would not result in communicating two watertight rooms containing safety

significant single-train systems. [H.9] (Section 1R06)

Enclosure

6

Cornerstone: Barrier Integrity

Green. The inspectors reviewed a Green self-revealing NCV of Title 10 of the Code of

Federal Regulations (10 CFR) Part 50, Appendix B, Criterion III, Design Control, for

PSEGs failure to effectively implement the design change process. Specifically, PSEGs

design change package (DCP) 4EC-3662 failed to reclassify the purchase classification

(PC) of the main control room (MCR) chiller pressure control valve (PCV) positioner from

non-safety related (PC4) to safety related (PC1). Because of the incorrectly assigned PC,

PSEG did not track the shelf life of replacement positioner diaphragms, which led to the

failure of the A MCR positioner on December 20, 2013. PSEGs corrective actions included

replacement of the failed positioner and changing the purchase classification for the chiller

PCV positioners to safety-related (PC1). Since the implementation of DCP 4EC-3662 in

1997, the DCP procedures have been enhanced to ensure the completion of a purchase

class evaluation of procured materials that are implemented in the design change process.

The inspectors determined that the performance deficiency was more than minor because

it is associated with the design control attribute of the Barrier Integrity cornerstone, and

adversely affected the cornerstone objective of maintaining the radiological barrier

functionality of the control room. In accordance with Exhibit 3 of NRC IMC 0609, Appendix

A, The Significance Determination Process (SDP) for Findings at Power, issued June 19,

2012, the inspectors determined that this finding is of very low safety significance (Green)

because the performance deficiency represents a degradation of only the radiological barrier

function provided for the control room. The inspectors determined that there was no cross-

cutting aspect associated with this finding because the cause of the performance deficiency

occurred more than three years ago, and was not representative of present plant

performance. (Section 4OA3)

Other Findings

A violation of very low safety significance that was identified by PSEG was reviewed by the

inspectors. Corrective actions taken or planned by PSEG have been entered into PSEGs

corrective action program. This violation and corrective action tracking number are listed in

Section 4OA7 of this report.

Enclosure

7

REPORT DETAILS

Summary of Plant Status

Hope Creek Generating Station began the inspection period at full rated thermal power (RTP).

On April 1, 2014, Hope Creek conducted a planned down power to 50 percent of RTP to

support power suppression testing (PST), main turbine valve testing and main condenser water

box cleaning. The unit was returned to full RTP on April 4, 2014. On May 14, 2014, the B

reactor recirculation pump (RRP) speed unexpectedly rose to its maximum value. Operators

took manual control of the pump and reduced the pump speed to less than reactor recirculation

flow TS requirements. On May 23, 2014, operators reduced power to 98 percent to perform B

RRP speed control circuit corrective maintenance. Operators returned the unit to full power on

the same day. On May 28, 2014, Hope Creek conducted a planned down power to 50 percent

of RTP to support main turbine valve testing and main condenser water box cleaning. The unit

was returned to full RTP on May 31, 2014, and remained at or near full RTP for the remainder of

the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01 - 2 samples)

.1 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

The inspectors performed a review of PSEGs readiness for the onset of seasonal high

temperatures. The review focused on the safety auxiliaries cooling system (SACS) and

station service water (SSW) system. The inspectors reviewed the Updated Final Safety

Analysis Report (UFSAR) and TS to determine what temperatures or other seasonal

weather could challenge these systems and to ensure PSEG personnel had adequately

prepared for these challenges. The inspectors reviewed station procedures, including

PSEGs seasonal weather preparation procedure and applicable operating procedures.

The inspectors performed walkdowns of the selected systems to verify that no

unidentified issues existed that could challenge the operability of the systems during hot

weather conditions. Documents reviewed for each section of this inspection report are

listed in the Attachment.

b. Findings

No findings were identified.

.2 External Flooding

a. Inspection Scope

During the week of May 24, 2014, the inspectors performed an inspection of the external

flood protection measures for Hope Creek. The inspectors reviewed procedures, design

documents, and the UFSAR, Chapters 2.4.2, Floods, and 3.4, Water Level (Flood)

Design, which described the design flood levels and protection areas containing safety-

Enclosure

8

related equipment to identify areas that may be affected by flooding. The inspectors

also reviewed the limiting conditions for operations and the surveillance requirements in

TS 3.7.3, Flood Protection. The inspectors review focused on the Hope Creek Unit 1

areas, which protect Unit 1 equipment, that are susceptible to external flooding.

Specifically, the inspectors walked down the south, east and west walls of the reactor

building 102, 77, and 54 elevations. The inspectors inspected the condition of the

walls and ensured that any outside penetrations susceptible to external flooding were

flood protected. The inspectors also inspected the flood doors present in that area,

which are listed in TS Table 3.7.3-1, Perimeter Flood Doors. The inspectors verified

that the doors were in conformance with plant maintenance procedures and drawings.

The inspectors reviewed the preventive maintenance activities performed on these doors

with the responsible system engineer. The inspectors also conducted a walkdown of

these doors to verify that the doors were in conformance with the design basis

requirements in the UFSAR, the TS, and plant procedures and drawings. Additionally,

the inspectors reviewed the abnormal operating procedure, HC.OP-AB.MISC-0001,

Acts of Nature, for mitigating external flooding during severe weather to determine if

PSEG had planned or established adequate measures to protect against external

flooding events.

b. Findings

No findings were identified.

1R04 Equipment Alignment

Partial System Walkdowns (71111.04 - 3 samples)

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems:

RCIC during HPCI booster pump planned maintenance on May 2, 2014

D emergency diesel generator (EDG) area ventilation system tornado dampers

during A EDG planned maintenance the week of May 6, 2014

A, B, and D SSW pumps during C SSW pump planned maintenance on June 2,

2014

The inspectors selected these systems based on their risk-significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors reviewed

applicable operating procedures, system diagrams, the UFSAR, technical specifications,

work orders, condition reports, and the impact of ongoing work activities on redundant

trains of equipment in order to identify conditions that could have impacted system

performance of their intended safety functions. The inspectors also performed field

walkdowns of accessible portions of the systems to verify system components and

support equipment were aligned correctly and were operable. The inspectors examined

the material condition of the components and observed operating parameters of

equipment to verify that there were no deficiencies. The inspectors also reviewed

whether PSEG staff had properly identified equipment issues and entered them into the

corrective action program for resolution with the appropriate significance

characterization.

Enclosure

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b. Findings

No findings were identified.

1R05 Fire Protection

.1 Resident Inspector Quarterly Walkdowns (71111.05Q - 5 samples)

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material

condition and operational status of fire protection features. The inspectors verified that

PSEG controlled combustible materials and ignition sources in accordance with

administrative procedures. The inspectors verified that fire protection and suppression

equipment was available for use as specified in the area pre-fire plan, and passive fire

barriers were maintained in good material condition. The inspectors also verified that

station personnel implemented compensatory measures for out of service, degraded, or

inoperable fire protection equipment, as applicable, in accordance with procedures.

Review of compensatory measure fire watch for 10C467 fire protection panel power

supply failure on April 17, 2014

FRH-II-415, Revision 4, Hope Creek Pre-Fire Plan, drywell pad torus area on April

21, 2014

FRH-II-412, Revision 3, Hope Creek Pre-Fire Plan, RCIC pump and turbine room

and electrical equipment room, on May 20, 2014

FRH-II-532, Revision 6, Hope Creek Pre-Fire Plan, lower control equipment room, on

May 23, 2014

FRH-II-542, Revision 9, Hope Creek Pre-Fire Plan, control equipment mezzanine, on

May 23, 2014

b. Findings

No findings were identified.

.2 Fire Protection - Drill Observation (71111.05A - 1 sample)

a. Inspection Scope

The inspectors observed an unannounced fire brigade drill scenario conducted on

April 7, 2014, that involved a fire in the Hope Creek radwaste area, room 3351. The

inspectors evaluated the readiness of the plant fire brigade to fight fires. The inspectors

verified that PSEG personnel identified deficiencies; openly discussed them in a self-

critical manner at the post-drill debrief; and took appropriate corrective actions as

required. The inspectors evaluated specific attributes as follows:

Proper wearing of turnout gear and self-contained breathing apparatus

Proper use and layout of fire hoses

Employment of appropriate fire-fighting techniques

Sufficient fire-fighting equipment brought to the scene

Effectiveness of command and control

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Search for victims and propagation of the fire into other plant areas

Smoke removal operations

Utilization of pre-planned strategies

Adherence to the pre-planned drill scenario

Drill objectives met

The inspectors also evaluated the fire brigades actions to determine whether these

actions were in accordance with PSEGs fire-fighting strategies.

b. Findings

No findings were identified.

1R06 Flood Protection Measures (71111.06 - 1 sample)

Internal Flooding Review

a. Inspection Scope

The inspectors reviewed the UFSAR, the site flooding analysis, and plant procedures to

assess susceptibilities involving internal flooding. The inspectors also reviewed the

corrective action program to determine if PSEG identified and corrected flooding

problems and whether operator actions for coping with flooding were adequate. The

inspectors also focused on the A residual heat removal (RHR) pump room (4113), the

B RHR pump room (4109), the C RHR pump room (4114), the HPCI pump and turbine

room (4111), and the RCIC pump and turbine room (4110) to verify the adequacy of

penetration seals located below the flood line, watertight door seals, common drain lines

and sumps, and room level alarms.

b. Findings

Introduction. The inspectors identified a Green NCV of TS 6.8.1.a, Procedures

because PSEG procedures HC.OP-AR.ZZ-0006 and HC.OP-AR.ZZ-0022 could

potentially complicate an internal flooding event and adversely affect assumptions in

Hope Creeks flood design. Specifically, the procedures did not ensure operator

response would not communicate the HPCI and RCIC watertight rooms and potentially

render two safety-significant single train systems inoperable.

Description. During a review of flood protection measures for the 54 foot elevation of the

reactor building, inspectors questioned whether execution of flooding procedures could

impact the assumption of the flood analysis, which assumes that the A, B, and C

RHR pump rooms, the HPCI pump and turbine room, and the RCIC pump and turbine

room are protected. Specifically, inspectors determined that in response to a room

flooding alarm, the procedures directed operators to enter the rooms to investigate the

flooding and assess the extent of flooding, an action which could allow communication

between two watertight rooms.

Hope Creeks UFSAR section 3.6, Protection Against Dynamic Effects Associated with

the Postulated Rupture of Piping, states in part that, The postulated failure of a

Enclosure

11

moderate energy line can at most affect only the operations of one train of a redundant

safety-related system due to the provisions for physical separation of redundant trains.

Inspectors reviewed procedural actions that would be taken in response to flood alarms

for the HPCI pump and turbine room (Room 4111) and the RCIC pump and turbine room

(Room 4110). The alarm response procedures for the HPCI and RCIC room flood

alarms direct operators to dispatch an equipment operator to the applicable room to

investigate and confirm the floor level alarm and enter HC.OP-EO.ZZ-0103/4, Reactor

Building and Radioactive Release Control. HC.OP-EO.ZZ-0103/4 provides an entry

condition of any reactor building room floor level above 1 inch, which is also the setpoint

of the level alarm. The procedure directs operators to use all available sump pumps and

isolate all systems discharging into the room.

Since the procedures direct operators to investigate and confirm flooding, the inspectors

assessed the ability of operators to enter the room without affecting equipment in an

adjacent room. Each of the ECCS/RCIC rooms are separated by large watertight doors

with no window or portal to monitor conditions on the other side of the door without

opening the door. The inspectors noted that the alarm response procedures for a high

level alarm in the A and B RHR pump rooms direct control room operators to dispatch

an equipment operator to enter the RHR pump rooms at their upper levels (77 foot

elevation) to determine the cause of the alarm. This procedural direction would prevent

flood propagation to the adjacent HPCI and RCIC electrical rooms.

The HPCI and RCIC rooms are located next to one another and are connected by a

watertight door. For a flood in the HPCI room, since both doors to the room open into

the adjacent rooms (i.e., water pressure would aid in opening the door), once the door

was unlatched, the water would force the door open and flood the adjacent room. The

inspectors noted that the alarm response procedures for potential flooding in the HPCI

and RCIC rooms do not provide direction on where to access the HPCI and RCIC rooms

when investigating for a potential flood condition. Therefore, when executing the

procedure to respond to flooding in the HPCI room, operators could propagate an

internal flood to two watertight rooms if they were to access the HPCI room through the

door connecting HPCI and RCIC.

The inspectors interviewed the Hope Creek emergency operating procedure (EOP)

coordinator regarding operator actions in response to indications of a flood in the HPCI

and RCIC rooms and the HC.OP-EO.ZZ-0103/4 procedure. Interviews with the EOP

coordinator indicated that operator knowledge would ensure proper access to the HPCI

and RCIC rooms when investigating a potential flood. However, no operator training

could be found that specified that operators should not access the HPCI and RCIC

rooms using the connecting watertight door when responding to a potential flood

condition.

The inspectors interviewed a senior reactor operator and two equipment operators about

their response to alarms for a potential flood in the HPCI room. The senior reactor

operator did not indicate that he would direct which door to access the HPCI room. The

equipment operators indicated that they would access the HPCI room from the door to

the RCIC room because the floor drains in the RCIC room would better drain any flood

water.

In the absence of further engineering evaluation, there was reasonable doubt of the

operability of the HPCI and RCIC systems. Specifically, internal flood propagation from

Enclosure

12

the design internal flood in the HPCI room could result in a water level that calls the

operability of RCIC into question. PSEG plans to perform a detailed technical evaluation

to evaluate the impact of internal flood propagation in the HPCI and RCIC rooms in

response to the inspectors questions (Order 70167153). PSEG entered the issue into

the CAP as NOTFs 20646334, 20646335, and 20653586. PSEGs corrective actions

include a planned revision of the annunciator response procedures and issuance of a

standing order to the Operations department staff.

Analysis. The inspectors determined that PSEGs failure to provide adequate procedural

guidance to respond to a HPCI/RCIC room flood alarm was a performance deficiency

that was within PSEGs ability to foresee and correct, and should have been prevented.

The performance deficiency is more than minor because it was associated with the

procedure quality attribute of the Mitigating Systems cornerstone, and adversely affected

the cornerstone objective to ensure the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences (i.e., core

damage). Specifically, PSEG procedures HC.OP-AR.ZZ-0006 and HC.OP-AR.ZZ-0022

could potentially complicate an internal flooding event and adversely affect assumptions

in Hope Creeks flood design, since the procedures did not ensure operator response

would not communicate the HPCI and RCIC watertight rooms and potentially render

multiple trains of safety-related SSCs inoperable. This performance deficiency was also

similar to examples 3.j and 3.k of NRC IMC 0612, Appendix E, in that communicating the

two watertight rooms created a reasonable doubt of operability of the RCIC system.

PSEG plans to perform a detailed technical evaluation to evaluate the impact of internal

flood propagation in the HPCI and RCIC rooms. The finding was evaluated in

accordance with Exhibits 2 and 4 of NRC IMC 0609, Appendix A, The SDP for Findings

At-Power, dated June 19, 2012. Since opening the watertight door during an internal

flooding event could bypass the flood protection feature and potentially degrade two or

more trains of a multi-train system or function, a detailed risk assessment was

performed.

The condition was modeled using the Hope Creek SPAR model version 8.18 along with

SAPHIRE version 8.09. As a bounding analysis, the condition was assumed to exist for

greater than one year and the flooding was assumed to require a reactor shutdown,

which results in a plant transient with failure of HPCI and RCIC due to flood impacts.

The flooding initiating event frequency was derived from the Hope Creek Internal Flood

Report, HC-PRA-012, Revision 2. The resulting change in core damage frequency was

substantially less than 1E-7. The dominant sequences included a transient with a failure

to depressurize along with RCIC and HPCI failures. Since the change in core damage

frequency was sufficiently low, no further evaluation for large early release was required.

The inspectors determined that the finding had a cross-cutting aspect in the Human

Performance area associated with Training, in that PSEG did not provide adequate

training and ensure knowledge transfer to maintain a knowledgeable, technically

competent workforce and instill nuclear safety values. Specifically, operator training did

not ensure operator response to internal flooding would not communicate the HPCI and

RCIC watertight rooms and potentially render multiple trains of safety-related SSCs

inoperable. [H.9].

Enforcement. TS 6.8.1.a, Procedures and Programs, requires in part, that written

procedures recommended in Appendix A of Regulatory Guide (RG) 1.33, Revision 2,

shall be established, implemented, and maintained. RG 1.33, Revision 2, Appendix A,

Enclosure

13

Section 5, requires that each safety-related annunciator should have its own written

procedure, which should normally contain the immediate operation action. PSEG

procedures HC.OP-AR.ZZ-0006 and HC.OP-AR.ZZ-0022 provide direction for operator

response to indications of high level in the HPCI and RCIC rooms. Contrary to the

above, until implementation of Operations Department Standing Order 2014-26 on

May 24, 2014, PSEG procedures HC.OP-AR.ZZ-0006 and HC.OP-AR.ZZ-0022 were

inadequate in that actions directed in the procedures could complicate an internal

flooding event and potentially adversely affect assumptions in Hope Creeks flood

design. In addition to entering the issue into the CAP as NOTFs 20646334, 20646335,

and 20653586, PSEGs corrective actions include a planned revision of the annunciator

response procedures and issuance of a standing order to the Operations department

staff. Because this violation was of very low safety significance (Green), and PSEG

entered this issue into their CAP, this violation is being treated as an NCV, consistent

with Section 2.3.2 of the Enforcement Policy. (NCV 05000354/2014003-01, Inadequate

Procedural Guidance for Responding to an Internal Flooding Event in the HPCI

and RCIC Rooms)

1R11 Licensed Operator Requalification Program (71111.11Q - 2 samples)

.1 Quarterly Review of Licensed Operator Requalification Testing and Training

a. Inspection Scope

The inspectors observed licensed operator simulator training on April 28, 2014, that

included an A RRP trip, reactor water cleanup (RWCU) system leak, loss of main

condenser vacuum, and an anticipated transient without scram. The inspectors

evaluated operator performance during the simulated event and verified completion

of critical tasks, risk significant operator actions, including the use of abnormal and

emergency operating procedures. The inspectors assessed the clarity and effectiveness

of communications, implementation of actions in response to alarms and degrading plant

conditions, and the oversight and direction provided by the control room supervisor. The

inspectors verified the accuracy and timeliness of the emergency classification made by

the shift manager. Additionally, the inspectors assessed the ability of the training staff to

identify and document crew performance problems.

b. Findings

No findings were identified

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

a. Inspection Scope

The inspectors observed a planned down power to support PST to locate a potential fuel

defect and the conduct main turbine valve testing on April 1, 2014. The inspectors

observed reactivity manipulations to verify that procedure use and crew communications

met established expectations and standards. The inspectors observed pre-job briefings

to verify that the briefings met the criteria specified in OP-AA-101-111-1004 Operations

Standards, Revision 4, and HU-AA-1211, Pre-Job Briefings, Revision 11. Additionally,

the inspectors observed the performance of turbine valve testing surveillance test,

HC.OP-ST.AC-0002, on April 1, 2014, to verify that procedure use, crew

Enclosure

14

communications, and coordination of activities between work groups similarly met

established expectations and standards.

b. Findings

No findings were identified

1R12 Maintenance Effectiveness (71111.12Q - 3 samples)

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of

maintenance activities on structure, system, or component (SSC) performance and

reliability. The inspectors reviewed corrective action program documents (notifications),

maintenance work orders (orders), and maintenance rule basis documents to ensure

that PSEG was identifying and properly evaluating performance problems within the

scope of the maintenance rule. As applicable, the inspectors verified that the SSC was

properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and verified

that the (a)(2) performance criteria established by PSEG staff was reasonable; for SSCs

classified as (a)(1), the inspectors assessed the adequacy of goals and corrective

actions to return these SSCs to (a)(2); and, the inspectors independently verified that

appropriate work practices were followed for the SSCs reviewed. Additionally, the

inspectors ensured that PSEG staff was identifying and addressing common cause

failures that occurred within and across maintenance rule system boundaries.

A MS drain and dump valve functional failure determinations for December 1 and 5,

2013, scrams (Order 70161698)

Salem Unit 3 (gas turbine generator) scoping in Hope Creek maintenance rule

program (NOTF 20502118)

RCIC nuclear management and control leak detection system card failure and

replacement on May 23, 2014 (Order 60113250)

b. Findings

Introduction. A self-revealing finding of very low safety significance (Green) was

identified for PSEGs failure to evaluate an identified deficiency in accordance with

PSEG procedure LS-AA-125, Corrective Action Program. Specifically, PSEG failed to

take self-recommended actions in NOTF 20447050 to evaluate the B MS dump valve

performance after failing to operate as designed during B MS drain valve trouble-

shooting on January 11, 2010. As a result, PSEG did not identify and correct a potential

design flaw associated with thermal binding of the MS dump valves, which was

determined to be the cause of the A MS dump valve failing to stroke open on

December 1, 2013, causing a reactor scram from 100 percent power.

Description. Hope Creek utilizes two horizontal non-reheat MS vessels that remove

moisture in the steam from the high pressure turbine exhaust before it enters the low

pressure turbine which prevents damage to the low pressure turbines. The condensate

that is collected in the MS is drained to the 5A, 5B, and 5C feed water heaters where it

eventually drains to the condenser. If the water level in the MS becomes too high and

the normal MS level control drain valves are not able to drain it, then the dump valve

opens draining the water in the MS directly to the condenser.

Enclosure

15

At 6:07 am on December 1, 2013, while operating at 100 percent power, the A MS

normal drain level reached a maximum allowed value of 70 percent allowing the MS

dump valve to cycle to control level. After six minutes (~15 cycles of the A dump valve

going open and shut) of successfully controlling MS level in the dump valve range, the

A MS dump closed and failed to re-open causing high level in the A MS, a turbine trip

and a reactor scram.

On December 5, 2013, a second reactor scram occurred at 75 percent power during A

MS dump valve tuning with the normal A MS drain valves failed closed to support

emergency level controller tuning. The A MS dump valve again failed to stroke open

when expected causing high MS level.

PSEG conducted a root cause evaluation (Order 70161698) to determine the cause of

the A MS drain and dump valve issues leading to the December 1 and December 5,

2013, scrams. PSEG determined that the A MS dump valve experienced thermal

binding because both PSEG and the valve manufacturer did not recognize the potential

for these valves to experience thermal binding. The results from PSEGs evaluation

concluded that the A MS dump valve design is susceptible to internal binding due to

differential expansion, resulting in the valve plug sticking in the valve cage.

During the timeline review for the A MS root cause evaluation, PSEG discovered that

the B MS dump valve did not open as expected on January 11, 2010, when trouble-

shooting B MS drain valve control issues. The dump valve had cycled multiple times

prior to PSEG removing air to reopen the B MS dump valve when MS level was rising

during drain valve control troubleshooting and the dump valve did not open for 12

minutes. The condition of the B MS dump valve not operating as expected was

documented under NOTF 20447050. The NOTF documented that the B MS dump

valve had cycled several times prior to the failure to open and recommended that the

B MS dump valve performance be evaluated and implement corrective actions as

necessary. This NOTF was not properly allocated to the equipment apparent cause

evaluation (EQACE) that was created (Order 70105948) to evaluate the B MS drain

valve control troubleshooting and therefore was never evaluated. PSEG created NOTF

20640526 to document the missed opportunity to troubleshoot B MS dump valve

performance and identify the thermal binding issue when the valve is cycled at normal

reactor power and pressure.

LS-AA-125, Corrective Action Program, Revision 12, Section 3.5.6 (effective on

January 11, 2010) states to ensure that the corrective action identified have been

agreed upon by the assignees and that the corrective actions are appropriately entered

into the CR database. Based on this information, the inspectors concluded that PSEG

failed to ensure that EQACE 70105948 addressed the identified issue in NOTF

20447050 recommending that the B MS dump valve performance on January 11, 2010,

be evaluated and corrected. PSEG has entered the above concerns into the CAP as

20640526. PSEGs corrective actions include a design change to the MS emergency

level control system that eliminates dump valve cycling on high MS level.

Analysis. PSEGs failure to ensure evaluations addressed identified issues in

accordance with PSEG procedure LS-AA-125, Corrective Action Program, was a

performance deficiency which was reasonably within PSEGs ability to foresee and

correct and should have been prevented. The performance deficiency was determined

Enclosure

16

to be more than minor because it was associated with the equipment performance

attribute of the Initiating Events cornerstone, and adversely affected the cornerstone

objective to limit the likelihood of events that upset plant stability and challenge critical

safety functions during shutdown as well as power operations. The inspectors

determined that this finding was of very low safety significance using Exhibit 1 of NRC

IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-

Power, dated June 19, 2012, because the finding did not cause both a reactor trip and

the loss of mitigation equipment relied upon to transition the plant from the onset of the

trip to a stable shutdown condition (e.g. loss of condenser, loss of feed water). The

inspectors determined that there was no cross-cutting aspect associated with this finding

because the cause of the performance deficiency occurred more than three years ago,

and was not representative of present plant performance.

Enforcement. This finding does not involve enforcement action because no violation of a

regulatory requirement was identified. Since this finding does not involve a violation and

is of very low safety significance (Green), it is identified as a FIN. (FIN

05000354/2014003-02, Failure to Evaluate an Identified Issue with the Moisture

Separator Dump Valve Performance)

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 5 samples)

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the

maintenance and emergent work activities listed below to verify that PSEG performed

the appropriate risk assessments prior to removing equipment for work. The inspectors

selected these activities based on potential risk significance relative to the reactor safety

cornerstones. As applicable for each activity, the inspectors verified that PSEG

personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the

assessments were accurate and complete. When PSEG performed emergent work, the

inspectors verified that operations personnel promptly assessed and managed plant risk.

The inspectors reviewed the scope of maintenance work and discussed the results of

the assessment with the stations probabilistic risk analyst to verify plant conditions were

consistent with the risk assessment. The inspectors also reviewed the technical

specification requirements and inspected portions of redundant safety systems, when

applicable, to verify risk analysis assumptions were valid and applicable requirements

were met.

Unplanned de-energization and loss of the D vital bus on December 19, 2013

Planned high risk activity to perform main turbine combined intermediate valve

testing on April 2, 2014

Planned high risk activity to perform power suppression testing to locate a fuel defect

on April 2, 2014

B RRP isolator replacement due to un-demanded speed changes on May 22, 2014

B RHR system and F filtration, recirculation, and ventilation system recirculation

fan planned maintenance on June 11, 2014

b. Findings

Introduction. A Green self-revealing NCV of TS 6.8.1.a, Procedures and Programs,

was identified for PSEGs failure to follow procedure MA-AA-1000, Maintenance

Enclosure

17

Standards and Practices, during the replacement of Bailey logic modules associated

with the D vital bus (10A404). Specifically, during the spring 2009 refueling outage

(1R15), PSEG failed to follow a WO requiring the replacement of all Bailey logic modules

listed in WO 60061175 with new logic modules. As a result, a logic module (H1PB-

1PBXIS-DC652010302) for the 10A404 vital bus was not replaced during 1R15, and

failed due to age on December 19, 2013, causing a loss of the 10A404 bus and an entry

into the associated 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> TSAS 3.8.3.1 for Onsite Power Distribution Systems.

Description. The PSEG Class 1E AC power distribution system provides a reliable

source of power for all Class 1E loads and distributes power at 4.16 kilovolt (kV), 480

volt (V), and 208/120 V. The system is divided into four independent channels and each

channel supplies power to loads in its own load group. Each of the four vital buses is

provided with connections to the two offsite power sources through two in-feed breakers

(40401 and 40408). One of these breakers is designated as the normal source and the

other as the alternate source for the bus. In addition to these two connections to offsite

power, each of the vital buses is connected to its dedicated EDG. These EDGs serve as

the standby electric power source for their respective channels in case both the normal

and alternate power supplies to a bus are lost.

At 3:11 pm on December 19, 2013, PSEG was performing a normally planned swap of

the 10A404 in-feed breakers from 40408 to 40401, when both in-feed breakers tripped

open and de-energized the 10A404 bus. PSEG stabilized the plant, entered the

associated 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> TSAS 3.8.3.1, conducted troubleshooting, performed component

replacements, and returned the 10A404 vital bus to service at 5:01 pm on December 19,

2013.

Following the restoration of the 10A404 vital bus on December 19, 2013, PSEG

conducted an EQACE documented under order 70162013. This EQACE determined

that the apparent cause of the 10A404 vital bus loss was an age-related failure of a logic

module (H1PB-1PBXIS-DC652010302) that was not replaced, but mistakenly

documented as being replaced in 2009 per WO 60061175. PSEG determined that the

independent peer check verification performed for both the LM removal and LM

installation failed to ensure that the serial number for the removed LM (H1PB-1PBXIS-

DC652010302) was not reinstalled into the system. Because this logic module was not

replaced in 2009, and remained in the system for 4 years past its vendor recommended

lifetime of 20 years, PSEG determined that it failed due to age and could not provide an

output to allow the 10A404 bus 40408 in-feed breaker to trip normally during the planned

in-feed breaker swap on December 19, 2013.

The inspectors reviewed PSEGs procedures for conducting the 10A404 in-feed breaker

swaps, operations narrative logs, and the completed EQACE 70162013 for the

December 19, 2013, event. PSEG procedure MA-AA-1000, Section 3.0, Maintenance

Standards and Practices, states in part, that all work on plant SSCs will be performed

using appropriate documentation such as work orders, notifications, or applicable

troubleshooting process control forms. Both the current revision of this procedure

(Revision 14) and the revision in use during 1R15 (Revision 7) have this language

requiring all work be performed in accordance with the appropriate documentation.

The inspectors determined that PSEG failed to follow this procedure by not complying

with WO 60061175 for the replacement of Bailey cards for the 10A404 in-feed breakers

during 1R15. This WO stated, in part, to Replace all Logic Modules listed with new

modules, and the list contained included the 10A404 in-feed breaker logic module

Enclosure

18

(H1PB-1PBXIS-DC652010302 LM 4.16 KV MAIN BKR 52-40401). Contrary to this,

PSEGs review of the serial number on the failed logic module and WO 60061175

showed that the original logic module was re-installed following its removal during the

conduct of maintenance. As part of the extent of condition for PSEGs EQACE, a review

of all other similar logic modules found them replaced as documented.

PSEG initiated NOTF 20639519 and EQACE 70162013 in the CAP to replace the failed

logic module, identify other similar logic modules and relays that may not have been

replaced or may not have an associated maintenance plan, and reinforce proper

maintenance practices to the individuals involved in the completion of WO 60061175.

Analysis. PSEGs failure to follow procedure MA-AA-1000 for Maintenance Standards

and Practices during the replacement of a Bailey logic module associated with the

10A404 vital bus represented a performance deficiency that was reasonably within

PSEGs ability to foresee and correct and should have been prevented. The

performance deficiency was determined to be more than minor because it was

associated with the human performance attribute of the Initiating Events cornerstone,

and adversely affected the cornerstone objective to limit the likelihood of events that

upset plant stability and challenge critical safety functions during shutdown as well as

power operations. Specifically, not following the work order instructions resulted in an

extended service duration and failure of a component that resulted in a loss of power to

the D vital bus on December 19, 2013. Similarly, this performance deficiency was also

similar to examples 2.g and 4.b of NRC IMC 0612 Appendix E, in that PSEG is required

to follow its procedures per TS 6.8.1, and ultimately led to a safety impact given the

failure of the logic module causing a loss of power to the 10A404 vital bus. The

inspectors determined the finding to be of very low safety significance (Green) in

accordance with Exhibit 1 of NRC IMC 0609, Appendix A, The Significance

Determination Process for Findings At-Power, dated June 19, 2012, because the finding

involved the loss of a support system that contributes to the likelihood of an initiating

event (Loss of an AC Bus), but did not affect mitigation equipment.

The inspectors determined that there was no cross-cutting aspect associated with this

finding because the cause of the performance deficiency occurred more than three years

ago, and was not representative of current plant performance.

Enforcement. TS 6.8.1.a, Procedures and Programs, requires in part, that written

procedures recommended in Appendix A of RG 1.33, Revision 2, shall be established,

implemented, and maintained. Section 9.a of RG 1.33, Revision 2, Appendix A, requires

that maintenance that can affect the performance of safety-related equipment should be

properly preplanned and performed in accordance with written procedures, documented

instructions, or drawings appropriate to the circumstances. Section 3.0 of PSEG

procedure MA-AA-1000, Maintenance Standards and Practices, states in part, that all

work on plant SSCs will be performed using appropriate documentation such as work

orders, notifications, or applicable troubleshooting process control forms.

Contrary to the above, on April 16, 2009, PSEG failed to follow this procedure during the

replacement of a Bailey logic module associated with the 10A404 vital bus. Specifically,

PSEG failed to follow WO 60061175 which required the replacement of all Bailey logic

modules listed in the WO with new logic modules. As a result, a logic module for the

10A404 vital bus was not replaced in 2009, and failed due to age on December 19,

2013, causing a loss of the 10A404 bus and an entry into the associated 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> TSAS

Enclosure

19

3.8.3.1 for Onsite Power Distribution Systems. PSEGs corrective actions included

replacement of the failed logic module, performance of an extent of condition inspection

to ensure other similar logic modules and relays were replaced, and reinforcement of

proper maintenance practices with the individuals involved in the completion of WO

60061175. Because this violation was of very low safety significance (Green) and was

entered into PSEGs CAP as NOTF 20639519 and EQACE 70162013, the violation is

being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000354/2014003-03, Failure to Follow Procedure Resulting in the Loss of a

Vital 4kV Bus)

1R15 Operability Determinations and Functionality Assessments (71111.15 - 5 samples)

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or non-

conforming conditions:

Minimum Allowable Wall Thickness Evaluation of 4 D RHR Piping (Order

80108395)

C EDG operability with lost parts potentially in the main lube oil sump on April 7,

2014 (NOTF 20645519)

Standby liquid control event report #49909 retraction on April 15, 2014 (NOTFs

20647199 and 20643229)

B RRP undemanded speed changes on May 14, 2014 (NOTF 20651102)

Revision 3 of Masterpact Breaker failure analysis operability evaluation on May 28,

2014 (NOTF 20652187 and Order 70163760)

The inspectors selected these issues based on the risk significance of the associated

components and systems. The inspectors evaluated the technical adequacy of the

operability determinations to assess whether technical specification operability was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and UFSAR to

PSEGs evaluations to determine whether the components or systems were operable.

Where compensatory measures were required to maintain operability, the inspectors

determined whether the measures in place would function as intended and were

properly controlled by PSEG. The inspectors determined, where appropriate,

compliance with assumptions in the evaluations.

b. Findings

No findings were identified.

Enclosure

20

1R18 Plant Modifications (71111.18 - 2 samples)

.1 Temporary Modifications

a. Inspection Scope

The inspectors reviewed the temporary modification listed below to determine whether

the modification affected the safety functions of systems that are important to safety.

The inspectors reviewed 10 CFR 50.59 documentation to verify that the temporary

modification did not degrade the design bases, licensing bases, and performance

capability of the affected systems.

Temporary Configuration Change Package (TCCP) 4HT-14-005 - Temporary

Repairs to the Condensate Storage Tank Dike Drain Line

b. Findings

No findings were identified.

.2 Permanent Modifications

a. Inspection Scope

The inspectors evaluated a modification to the RWCU system implemented by DCP

80111754, Masterpact Breaker Add Aux Contact with Close Coil. This DCP wires an

existing breaker auxiliary contact in series with the internal close coil to allow the close

coil to be de-energized after the breaker has closed rather than be continuously

energized. The existing configuration with the breaker close coil continuously energized

is allowing an intermittent failure of these breakers where they lock up and fail to re-

close when required per design. The inspectors verified that the design bases, licensing

bases, and performance capability of the affected systems were not degraded by the

modification. In addition, the inspectors reviewed modification documents associated

with the upgrade and design change, including the breaker operation. The inspectors

also reviewed revisions to the control room alarm response procedure and interviewed

engineering and operations personnel to ensure the procedure could be reasonably

performed.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19 - 7 samples)

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed

below to verify that procedures and test activities ensured system operability and

functional capability. The inspectors reviewed the test procedure to verify that the

procedure adequately tested the safety functions that may have been affected by the

maintenance activity, that the acceptance criteria in the procedure was consistent with

the information in the applicable licensing basis and/or design basis documents, and that

the procedure had been properly reviewed and approved. The inspectors also

Enclosure

21

witnessed the test or reviewed test data to verify that the test results adequately

demonstrated restoration of the affected safety functions.

HPCI oil supply pressure gauge replacement on October 10, 2013 (Order 60113238)

B control room chilled water pressure control valve positioner and diaphragm

replacement on April 23, 2014 (Order 60116090)

10C467 fire protection panel power supply replacement on May 9, 2014 (Order

30269527)

B RRP pump speed controller card replacements on May 22, 2014 (Order

60117312)

RCIC nuclear management and control leak detection system card replacement on

May 23, 2014 (Order 60113250)

Service air compressor oil leak repair on June 5, 2014 (Order 60117447)

B RHR system relay replacements on June 11, 2014 (Orders 30098613 and

30098617)

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22 - 9 samples)

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data

of selected risk-significant SSCs to assess whether test results satisfied technical

specifications, the UFSAR, and PSEG procedure requirements. The inspectors verified

that test acceptance criteria were clear, tests demonstrated operational readiness and

were consistent with design documentation, test instrumentation had current calibrations

and the range and accuracy for the application, tests were performed as written, and

applicable test prerequisites were satisfied. Upon test completion, the inspectors

considered whether the test results supported that equipment was capable of performing

the required safety functions. The inspectors reviewed the following surveillance tests:

HC.OP-ST.AC-0002, Turbine Valve Testing quarterly surveillance on April 1, 2014

HC.OP-ST.KJ-0003, Emergency Diesel Generator 1CG400 Operability Test on

April 7, 2014

HC.OP-IS.BJ-0001, HPCI Main and Booster Pump Set - 0P204 and 0P217 -

In-service Test on April 9, 2014 (in-service test)

HC.MD-ST.PB-0003, Class 1E 4.16 kV Feeder Degraded Voltage Monthly

Instrumentation Channel Functional Testing of the B vital bus on April 15, 2014

HC.OP-IS.BC-0004, DP202, D Residual Heat Removal Pump In-Service Test on

April 22, 2014 (in-service test)

HC.OP-DL.ZZ-0026, Drywell floor drain leakage monitoring on May 1, 2014 (RCS

leakage)

HC.FP-ST.KC-0009, Diesel Driven Fire Pump Operability Test on May 6, 2014

HC.OP-IS.BC-0002, CP202, C Residual Heat Removal Pump In-Service Test on

June 25, 2014 (in-service test)

HC.OP-ST.KJ-0001, Emergency Diesel Generator 1AG400 Operability Test on

June 30, 2014

Enclosure

22

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (71114.06 - 1 sample)

Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a routine PSEG emergency drill on June 24,

2014 to identify any weaknesses and deficiencies in the classification, notification, and

protective action recommendation development activities. The inspectors observed

emergency response operations in the technical support center to determine whether the

event classification, notifications, and protective action recommendations were

performed in accordance with procedures. The inspectors also attended the drill critique

to compare inspector observations with those identified by PSEG staff in order to

evaluate PSEGs critique and to verify whether the PSEG staff was properly identifying

weaknesses and entering them into the corrective action program.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151)

Reactor Coolant System (RCS) Specific Activity and RCS Leak Rate (2 samples)

a. Inspection Scope

The inspectors reviewed PSEGs submittal for the RCS specific activity and RCS leak

rate performance indicators for the period of April 1, 2013, through March 31, 2014. To

determine the accuracy of the performance indicator data reported during those periods,

the inspectors used definitions and guidance contained in NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 7. The inspectors

also reviewed RCS sample analysis and control room logs of daily measurements of

RCS leakage, and compared that information to the data reported by the performance

indicator. Additionally, the inspectors observed chemistry personnel taking and

analyzing an RCS sample.

b. Inspection Findings

No findings were identified.

Enclosure

23

4OA2 Problem Identification and Resolution (71152 - 1 sample)

.1 Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure 71152, Problem Identification and Resolution, the

inspectors routinely reviewed issues during baseline inspection activities and plant

status reviews to verify that PSEG entered issues into the corrective action program at

an appropriate threshold, gave adequate attention to timely corrective actions, and

identified and addressed adverse trends. In order to assist with the identification of

repetitive equipment failures and specific human performance issues for follow-up, the

inspectors performed a daily screening of items entered into the corrective action

program and periodically attended condition report screening meetings.

b. Findings

No findings were identified.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a semi-annual review of site issues, as required by Inspection

Procedure 71152, Problem Identification and Resolution, to identify trends that might

indicate the existence of more significant safety issues. In this review, the inspectors

included repetitive or closely-related issues that may have been documented by PSEG

outside of the corrective action program, such as trend reports, performance indicators,

major equipment problem lists, system health reports, maintenance rule assessments,

and maintenance or corrective action program backlogs. The inspection also reviewed

PSEGs corrective action program database for the period of January 2014 to May 2014

to assess the notifications written as well as individual issues identified during the NRCs

daily condition report review (Section 4OA2.1). The inspectors reviewed the Hope

Creek station performance improvement integrated matrix (PIIM), conducted under

procedure LS-AA-125-1006, Performance Improvement Integrated Matrix, to verify that

PSEG personnel were appropriately evaluating and trending adverse conditions in

accordance with applicable procedures.

b. Findings and Observations

No findings were identified during this trend review.

The inspectors noted that PSEG personnel identified the following trends and entered

them into the corrective action program: an adverse trend in Appendix J leakage

(NOTFs 20632747, 20632748, 20632749); an adverse trend in design change package

quality (NOTFs 20642767 and 20644539); and an adverse trend in critical component

failures (NOTF 20638889). The inspectors also reviewed the 2013 third cycle Hope

Creek PIIM and the performance improvement action plan developed to improve station

performance in the areas of equipment reliability, decision making, and risk

management.

Enclosure

24

The inspectors noted a trend in the stations failure to perform cross-system

maintenance rule screenings:

When the feedwater crosstie valve (AE-HV-4144) failed, it was screened as not

a functional failure against the feedwater system. The condition was not

screened against the feedwater sealing functions of HPCI and RCIC.

The DD-411 battery room temperature was found above acceptance criteria. A

maintenance rule functional failure screening was performed for the functions of

the 1E 125 volt direct current (DC) system, but not for the auxiliary building

diesel area ventilation system.

As found setpoint failures of safety relief valves were screened against the

automatic depressurization system functions, but not against any of the main

steam system functions.

The inspectors determined this observation was not more than minor in accordance with

IMC 0612, because the observations did not result in any of the systems requiring

additional monitoring per 10 CFR 50.65(a)(1).

Based on the review of PSEGs trending, the inspectors concluded that PSEG was

appropriately identifying and entering issues into the corrective action program,

adequately evaluating the identified issues, and appropriately identifying adverse trends

before they become more safety significant problems.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153 - 6 samples)

.1 Plant Events

a. Inspection Scope

For the plant event listed below, the inspectors reviewed plant parameters, reviewed

personnel performance, and evaluated performance of mitigating systems. The

inspectors communicated the plant events to appropriate regional personnel, and

compared the event details with criteria contained in IMC 0309, Reactive Inspection

Decision Basis for Reactors, for consideration of potential reactive inspection activities.

As applicable, the inspectors verified that PSEG made appropriate emergency

classification assessments and properly reported the event in accordance with 10 CFR

Parts 50.72 and 50.73. The inspectors reviewed PSEGs follow-up actions related to the

events to assure that PSEG implemented appropriate corrective actions commensurate

with their safety significance.

B RRP un-demanded speed change due to a failure in the speed controller, causing

a momentary increase in reactor power above the thermal power limit on May 15,

2014 (NOTF 20651102)

b. Findings

No findings were identified.

.2 Event Notification49909 Retraction, Standby Liquid Control System (SLC) Sample

Concentration Outside Technical Specification Limits

Enclosure

25

At 10:27 pm on March 12, 2014, PSEG was in the process of returning the SLC system

to service following planned maintenance on the B SLC pump when the MCR received

a SLC tank high level alarm (>4880 gallons). The MCR informed the equipment

operator conducting the SLC system restoration of the unexpected SLC tank high level

alarm and the operator closed a valve that had just been opened, which stopped the rise

in SLC storage tank level at 4926 gallons. PSEGs sample analysis of the SLC system

tank yielded a sodium pentaborate concentration outside the TS limits, rendering both

subsystems inoperable. The concentration was found to be at 13.598% by weight,

below the required concentration of 13.6% by weight. As part of the corrective actions,

PSEG restored the concentration to within TS limits and conducted an apparent cause

evaluation.

This condition was reported under 10 CFR 50.72(b)(3)(v)(D) on March 13, 2014, as

a condition that could have prevented the fulfillment of a safety function required to

mitigate the consequences of an accident (EN 49909). On April 14, 2014, PSEG

retracted EN 49909 stating that a subsequent review of the analytical data has

determined that the SLC tank sample met the TS requirement for operability (13.6

weight percent) and therefore, there was no reportable condition. The inspectors

reviewed PSEGs EN and EN retraction, apparent cause evaluation report, supporting

documentation including multiple NOTFs and technical evaluation (Order 70166989),

station procedures, and interviewed several members of station staff and management

regarding the event. No findings were identified during this review.

.3 (Closed) Licensee Event Report (LER) 05000354/2013-007-00, As-Found Values for

Safety Relief Valve Lift Set Points Exceed Technical Specification Allowable Limit

On November 22, 2013, PSEG received test results indicating that the as-found lift

setpoints for 5 of 14 main steam safety relief valves (SRVs) failed to open within the

required TS actuation pressure setpoint tolerance. TS 3.4.2.1 provides an allowable

pressure band of +/- 3 percent for each SRV. All five of the SRVs opened above the

required pressure band. PSEG determined that the apparent cause for the A, D, F,

K, and L SRV setpoint failures was corrosion bonding/sticking between the mating

surfaces of the pilot disc. These issues were placed into the CAP as NOTF 20631351.

The pilot assembly for each of the 14 SRVs has been replaced with a fully tested spare

assembly. Additionally, this LER stated PSEGs corrective actions include plans to

replace the currently installed SRVs with a new design that eliminates setpoint drift

events exceeding TS requirements and improves SRV reliability. Although this LER

reports the inoperability of five SRVs, this event did not result in a loss of system safety

function based on engineering analyses. These analyses showed that the SRVs would

have functioned to prevent a reactor vessel over-pressurization and that postulated

piping stresses would not exceed allowable limits. The enforcement aspects of this

finding are discussed in Section 4OA7. This LER is closed.

.4 (Closed) LER 05000354/2013-008-00 and LER 05000354/2013-008-01, Automatic

Actuation of the Reactor Protection System Due to a Main Turbine Trip

On December 1, 2013, Hope Creek Unit 1 automatically scrammed from 100 percent

rated thermal power due to a main turbine trip. The main turbine trip was due to high

level in the A MS. As a result of the scram, both RRPs tripped and three SRVs opened.

The plant was stabilized in hot shutdown, Operational Condition 3.

Enclosure

26

This condition is reportable under 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted

in an automatic actuation of the reactor protection system. The inspectors reviewed

PSEGs LER and LER revision, root cause evaluation report (Order 70161698),

supporting documentation, station procedures, and interviewed several members of

station staff and management regarding the event. One finding was identified and is

discussed in Section 1R12 of this report. These LERs are closed.

.5 (Closed) LER 05000354/2013-009-00 and LER 05000354/2013-009-01, Automatic

Actuation of the Reactor Protection System Due to a Main Turbine Trip

a. Inspection Scope

On December 5, 2013, during tuning of the A MS emergency level controller, the

reactor automatically scrammed from 75 percent power due to a main turbine trip.

During the tuning activities, the A MS dump valve cycled repeatedly and subsequently

failed closed, resulting in high level in the A MS and subsequent turbine trip. The

automatic reactor scram resulted in a trip of both RRPs, as designed. During the

recovery of the RRPs, the digital electro-hydraulic control system was mis-operated

which caused the turbine bypass valves to cycle. This caused reactor level to swell

above Level 8 then shrink below Level 3, resulting in a second actuation of the reactor

protection system.

This condition is reportable under 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in

an automatic actuation of the reactor protection system. The inspectors reviewed

PSEGs LER, root cause evaluation report (Order 70161698), supporting documentation,

station procedures, and interviewed several members of station staff and management

regarding the event. Two findings were identified and are discussed below. These

LERs are closed.

b. Findings

.1 Failure to Use Approved Method of Post-Scram Reactor Pressure Control

The mis-operation of the digital electro-hydraulic control system following the reactor

scram on December 5, 2013, has been previously evaluated. A self-revealing Green

NCV of TS 6.8.1.a (NCV 05000354/2014002-06) for Failure to Use Approved Method of

Post-Scram Reactor Pressure Control is documented in NRC Inspection Report

05000354/2014002.

.2 Inadequate Implementation of Contingency Actions During Moisture Separator

Emergency Level Controller Tuning

Introduction. A self-revealing finding of very low safety significance (Green) was

identified when PSEG failed to ensure that contingency actions were appropriate for

the activity being performed prior to A MS emergency level controller tuning on

December 5, 2013. Specifically, the decision to tune the emergency level controller

without appropriate contingencies in place led to a turbine trip and subsequent reactor

scram on high A MS level.

Description. On December 5, 2013, maintenance technicians were tuning the A MS

emergency level controller following its replacement in accordance with PSEG

procedure HC.IC-LC.AF-00007, Moisture Separator Drain Tank Level Tuning.

Enclosure

27

During the tuning evolution, the A MS dump valve failed closed, causing a turbine trip

due to high A MS level and automatic reactor scram.

The moisture separators improve the quality of the steam from the high pressure turbine

exhaust, and minimize erosion of the low pressure turbines due to excessively moist

steam. The levels in the A and B MSs are maintained through a normal drain path

through three drain valves on each MS to the #5 feedwater heaters. The position of the

drain valves is controlled by the MS normal level controller. When the level in the MS

is above the normal drain control level, a high level emergency dump valve (one per MS)

directs flow from the MS to the condenser. The emergency level dump valve is normally

closed and is controlled by the MS emergency level controller.

PSEG procedure HC.IC-LC.AF-00007, Moisture Separator Drain Tank Level Tuning,

raises MS level into the emergency dump range to tune the emergency level controller

by manually closing the normal drain valves. This evolution was evaluated and

determined to be a high risk evolution in accordance with WC-AA-105, Work Activity

Risk Management. A risk management plan was developed for the high risk activity.

WC-AA-105 requires that the risk management plan be presented for approval by a risk

management challenge board prior to performance of the high risk activity.

This plan was initially reviewed by a risk management challenge board and was not

approved. An action from the risk management challenge board included ensuring that

during the tuning, one person is to be stationed at the normal level controller and one at

the emergency level controller. The risk management challenge board directed that both

people would need to be prepared to respond in case the MS drain tank level rises

during the tuning evolution. A second risk management challenge board was held to

review the risk management plan. The contingency action for stationing maintenance

technicians at each controller was not implemented.

The second challenge board failed to ensure that contingency actions were appropriate

for the activity being performed as specified by PSEG procedure WC-AA-105. A

heightened level of awareness (HLA) brief was performed prior to performance of the

high risk activity. Having a maintenance technician at the normal and emergency level

controllers was discussed. Contrary to the direction of the risk management challenge

board and the HLA brief, a maintenance technician was not stationed at the normal level

controller during the tuning of the emergency level controller. PSEGs corrective actions

included conducting performance management with the individuals involved with the

tuning evolution, and revising the moisture separator drain tank level tuning procedure to

require an individual at the normal and emergency controllers when performing

emergency level controller tuning.

Analysis. The inspectors determined that PSEGs failure to ensure that the contingency

actions were appropriate for the activity being performed prior to A MS emergency

level controller tuning was a performance deficiency that was within PSEGs ability to

foresee and correct, and should have been prevented. Specifically, a contingency action

specified by the risk management challenge board and the HLA brief prior to the high

risk tuning activity was not performed. As a result, the technicians were unable to

restore air to the drain valves in time to reduce the A MS level before the high level

caused a turbine trip and reactor scram.

Enclosure

28

This finding was more than minor because it was associated with the human

performance attribute of the Initiating Events cornerstone, and adversely affected the

cornerstone objective to limit the likelihood of events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. The

inspectors determined that this finding was of very low safety significance (Green) using

Exhibit 1 of NRC IMC 0609, Appendix A, The Significance Determination Process

(SDP) for Findings At-Power, dated June 19, 2012, because the finding did not cause

both a reactor trip and the loss of mitigation equipment relied upon to transition the plant

from the onset of the trip to a stable shutdown condition (e.g. loss of condenser, loss of

feed water). The inspectors determined that the finding had a cross-cutting aspect in the

Human Performance area associated with Work Management, because PSEG

personnel did not implement a process of planning, controlling, and executing work

activities such that nuclear safety is the overriding priority. Specifically, technicians were

only stationed at the emergency level controller during the tuning, when having

technicians at both controllers would have provided more time to recover from a high

level condition in the A MS, and may have prevented the turbine trip and subsequent

reactor scram on December 5, 2013. (H.5)

Enforcement. This finding was not a violation of NRC requirements because no violation

of regulatory requirements was identified. Since this finding does not involve a violation

and is of very low safety significance (Green), it is identified as a FIN. (FIN

05000354/2014003-04, Inadequate Implementation of Contingency Actions During

Moisture Separator Emergency Level Controller Tuning)

.6 (Closed) LER 05000354/2013-010-00, Loss of Both Main Control Room Chillers

a. Inspection Scope

On December 20, 2013, at 1:03 pm, while the B MCR chiller was out of service in

support of maintenance, the A MCR chiller was manually secured due to excessive

fluctuations in load. The TSAS (TS 3.7.2.2 Action a.2) for both MCR air conditioning

subsystems inoperable was entered. At 9:20 pm, the B control area ventilation train

and chiller were placed in service for post maintenance testing, returned to an operable

status, and the TS action statement was exited.

This condition is reportable under 10 CFR 50.73(a)(2)(v)(D) as an event or condition that

could have prevented the fulfillment of the safety function of structures or systems that

are needed to mitigate the consequences of an accident. The inspectors reviewed

PSEGs LER and LER revision, apparent cause evaluation (Order 70162284),

supporting documentation, station procedures, and interviewed several members of

station staff and management regarding the event. One finding was identified and is

discussed below. These LERs are closed.

b. Findings

Introduction. A Green self-revealing NCV of 10 CFR 50, Appendix B, Criterion III,

Design Control, was identified for PSEGs failure to effectively implement the DCP

process. Specifically, PSEGs DCP 4EC-3662 failed to reclassify the PC of the MCR

chiller PCV positioner from non-safety related (PC4) to safety related (PC1). Because of

the incorrectly assigned PC, PSEG did not track the shelf life of replacement positioner

diaphragms, which led to the failure of the A MCR positioner on December 20, 2013.

Enclosure

29

As a result, while the B MCR chiller was inoperable following planned maintenance, the

A MCR chiller had to be manually secured due to excessive fluctuations in load caused

by the failed positioner, and led to both MCR chillers being inoperable.

Description. The control room envelope (CRE) heating, ventilation and air conditioning

(HVAC) systems are designed to ensure habitability during any design basis radiological

accident. Redundant HVAC systems are provided to control the ambient conditions for

safety-related equipment to ensure operating temperature limits are not exceeded. The

A and B MCR chillers provide the accident function of maintaining the temperature of

the CRE for equipment performance and operator comfort.

On December 20, 2013, at 1:03 pm, while the B MCR chiller was out of service in

support of maintenance, the A MCR chiller was manually secured due to excessive

fluctuations in load. TS action statement 3.7.2.2.a.2 for both MCR chillers being

inoperable was entered. This condition was reportable per 10CFR50.72(b)(3)(v)(D), as

an event or condition that could have prevented the fulfillment of the safety function of

structures or systems that are needed to mitigate the consequences of an accident,

PSEG submitted an eight-hour event notification (#49671) for concurrent inoperability of

both MCR chillers. At 9:20 pm (~8 hours into the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> TS action statement), the B

MCR chiller was placed in service for post maintenance testing and returned to an

operable status, allowing PSEG to exit the TS. Throughout the time both chillers were

inoperable, the MCR temperature was maintained below the TS limit of 90 degrees

Fahrenheit.

PSEG conducted an equipment apparent cause evaluation (EQACE 70162284) and

determined the A MCR chiller excessive load fluctuations were the result of an

inoperable chiller condenser PCV. The positioner for the PCV, which provides cooling

water flow to the chiller condenser, failed due to a leak in the positioner's internal relay

assembly, which is made up of a series of diaphragms. This positioner had failed

previously due to a missing roller bearing and C clip, and was replaced at the end of

2011. The replaced positioner that failed on December 20, 2013, had only been

installed for 2 years. The damaged diaphragm in the positioners relay assembly

allowed an internal leakage path for the air, resulting in the failure of the positioner to

operate properly. This failure was determined to be age-related caused by a legacy

issue with the implementation of DCP 4EC-3662 in 1997. The chiller PCV has an active

safety function in the open position to provide cooling water flow to the MCR chiller. On

a loss of instrument air, the chiller PCV was originally designed to fail open, but this DCP

installed backup air bottles to supply the chiller PCV, preventing the PCV from failing

open so that the chiller would not trip on low evaporator refrigerant pressure. This

design change resulted in the PCV becoming self-modulating, changing the

classification of the PCV positioner from nonsafety-related to safety-related. PSEGs

evaluation of this DCP in the EQACE concluded that the DCP failed to identify that the

PC of the positioner for the PCV should have been changed from nonsafety-related to

safety-related and as a result, the PC was not changed. If the PC of the positioner had

been changed to PC1, a positioner that had been on the shelf for more than 20 years

would not have been installed into a safety-related system. But because the PC was not

changed, PSEG determined that the shelf life of the in-stock replacement positioners

was not tracked, leading to the installation of a positioner in 2011 that had been

manufactured 21 years before.

Enclosure

30

PSEGs determined that the MCR chiller PCV positioner failed to operate because of

internal relay leakage caused by damaged diaphragms. These diaphragms failed due to

the positioners age exceeding the vendor recommended lifetime of 4 years. PSEG has

entered this issue into the CAP as NOTF 20642546. As part of PSEGs corrective

actions the site has replaced the failed positioner and changed the purchase

classification for the chiller PCV positioners to safety-related (PC1).

Analysis. PSEGs failure to effectively implement the DCP process for DCP 4EC-3662

was a performance deficiency that was within the licensees ability to foresee and

correct, and should have been prevented. Specifically, because of the incorrectly

assigned PC, PSEG did not track the shelf life of replacement positioner diaphragms,

which led to the failure of the A MCR positioner on December 20, 2013. The inspectors

determined that the performance deficiency was more than minor because it is

associated with the design control attribute of the of the barrier integrity cornerstone, and

adversely affected the cornerstone objective of maintaining the radiological barrier

functionality of the control room Exhibit 3 of IMC 0609, Appendix A, The Significance

Determination Process (SDP) for Findings at Power, issued June 19, 2012, the

inspectors determined that this finding is of very low safety significance (Green) because

the performance deficiency represents a degradation of only the radiological barrier

function provided for the control room. Since the implementation of DCP 4EC-3662, the

DCP procedures have been enhanced to ensure the completion of a purchase class

evaluation of procured materials that are implemented in the DCP process.

The inspectors determined that there was no cross-cutting aspect associated with this

finding because the cause of the performance deficiency occurred more than three years

ago, and was not representative of current plant performance.

Enforcement. 10 CFR 50, Appendix B, Criterion III, Design Control, states, in part, that

measures shall be established to assure that applicable regulatory requirements and the

design basis for structures, systems, and components shall be correctly translated into

specifications, drawings, procedures, and instructions.

Contrary to this, PSEGs implementation of DCP 4EC-3662 in 1997, failed to reclassify

the PC of the MCR chiller PCV positioner from nonsafety-related to safety-related.

Because of the incorrectly assigned PC, PSEG did not track the shelf life of replacement

positioner diaphragms, which led to the failure of the A MCR positioner on

December 20, 2013. PSEGs corrective actions include replacement of the failed

positioner and changing the PC for the MCR PCV positioners to safety-related.

Because of the very low safety significance (Green) and because the issue was entered

into the CAP as notification 20642546, this violation is being treated as an NCV,

consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV

05000354/2014003-05, Inadequate Evaluation of a Main Control Room Chiller

Design Change)

4OA5 Other Activities

Temporary Instruction (TI) 2515/182, Phase II, Underground Piping and Tank Integrity

(1 sample)

Enclosure

31

a. Inspection Scope

The licensees buried piping and underground piping and tanks program was inspected

in accordance with paragraph 03.02.a of the TI. It was confirmed that activities which

correspond to completion dates specified in the program, which have passed since the

Phase 1 inspection was conducted, have been completed.

Additionally, the licensees buried piping and underground piping and tanks program was

inspected in accordance with paragraph 03.02.b of the TI and responses to specific

questions found in http://www.nrc.gov/reactors/operating/ops-experience/buried-pipe-ti-

phase-2-insp-req-2011-11-16.pdf were submitted to the NRC headquarters staff.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

On July 10, 2014, the inspectors presented the inspection results to Mr. Paul Davison,

Hope Creek Site Vice President, and other members of the PSEG staff. The inspectors

verified that no proprietary information was retained by the inspectors or documented in

this report.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which meets the criteria of the NRC

Enforcement Policy, for being dispositioned as a NCV:

In Modes 1, 2, and 3, Hope Creek TS 3.4.2.1, "Safety Relief Valves," requires that

13 of the 14 SRVs open within of +/- 3 percent of the specified code safety valve

function lift settings or else be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in Mode 4 within the

next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Contrary to this requirement, on November 22, 2013, PSEG identified

that five of the fourteen SRVs were determined to have their as-found setpoints in

excess of the TS allowable tolerance, thus leaving nine operable SRVs. The pilot

assembly for each of the fourteen SRVs has been replaced with a fully tested spare

assembly. Additionally, LER 2013-007 stated PSEGs proposal to replace the SRVs

is being considered through the plant modification process. PSEG entered this issue

into their CAP as notification 20631351. The inoperability of the five SRVs did not

result in a loss of system safety function based on engineering analyses that showed

that postulated piping stresses would not exceed allowable limits. Therefore, this

finding is of very low (Green) safety significance based on an SDP issue screening,

because the SRVs would have functioned to prevent a reactor vessel over-

pressurization. The closure of the LER associated with this event was documented

in Section 4OA3.

ATTACHMENT: SUPPLEMENTARY INFORMATION

Enclosure

A-1

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

P. Davison, Site Vice President

E. Carr, Plant Manager

P. Bellard, Program Engineering

S. Bier, EOP Coordinator

M. Biggs, Hope Creek Maintenance Rule Coordinator

M. Cardile, Fire Protection Supervisor

J. Carlin, Fire Protection Superintendent

S. Connelly, System Engineer

A. DiEgidio, Chemistry Technician

T. Headman, Emergency Preparedness Technical Specialist

W. Hickey, Work Week Manager

C. Johnson, Senior Program Engineer

E. Martin, Senior Program Engineer

J. Master, Chemistry Technician

M. Meltzer, Chemistry

T. Morin, Regulatory Assurance Engineer

M. Reeser, System Engineer

M. Rooney, System Engineer

R. Smith, System Engineer

K. Timko, System Engineer

A. Tramontana, Program Engineering Manager

M. Tudisco, Nuclear Maintenance Supervisor

K. Wichman, System Engineer

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

Opened/Closed

05000354/2014003-01 NCV Inadequate Procedural Guidance for Responding

to an Internal Flooding Event in the HPCI and

RCIC Rooms (Section 1R06)05000354/2014003-02 FIN Failure to Evaluate an Identified Issue with the

Moisture Separator Dump Valve Performance

(Section 1R12)05000354/2014003-03 NCV Failure to Follow Procedure Resulting in the Loss

of a Vital 4kV Bus (Section 1R13)05000354/2014003-04 FIN Inadequate Implementation of Contingency

Actions During Moisture Separator Emergency

Level Controller Tuning (Section 4OA3)

Attachment

A-2

05000354/2014003-05 NCV Inadequate Evaluation of a Main Control Room

Chiller Design Change (Section 4OA3)

Closed

05000354/2013-007-00 LER As-Found Values for Safety Relief Valve Lift Set

Points Exceed Technical Specification Allowable

Limit (Section 4OA3)

05000354/2013-008-01 LER Automatic Actuation of the Reactor Protection

System Due to a Main Turbine Trip (Section

4OA3)

05000354/2013-009-01 LER Automatic Actuation of the Reactor Protection

System Due to a Main Turbine Trip (Section

4OA3)

05000354/2013-010-00 LER Loss of Both Main Control Room Chillers (Section

4OA3)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

ER-HC-310-1009, HCGS - Maintenance Rule Scoping, Revision 10

HC.MD-GP.ZZ-0037, Plant Bulkhead Doors Overhaul, Revision 5

HC.MD-PM.ZZ-0007, Missile Resistant and Watertight Doors Preventative Maintenance,

Revision 9

HC.OP-AB.MISC-0001, Acts of Nature, Revision 23

HC.OP-DL.ZZ-0014, Monday Shift Routine Log, Revision 34

HC.OP-GP.ZZ-0003, Station Preparations for Winter Conditions, Revision 29

OP-AA-108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 9

WC-AA-107, Seasonal Readiness, Revision 13

Other Documents

2013 Summer Readiness Hope Creek Critique

2014 Hope Creek Summer Readiness Affirmation Certification Letter, dated May 1, 2014

Notifications (*NRC-identified)

20546153 20562816 20610276 20612823 20613802 20615133

20649147 20650908 20650999 20652771* 20652918* 20654490

20654491 20654493 20654495 20654496

Maintenance Orders/Work Orders

30236406 60092591 60104126 60112815 60112948 60114177

60115861 70159564 80107747 80110867

Attachment

A-3

Drawings

A-0203-0, General Plant Floor Plan Level 3 - Elevation 102, Revision 19

Section 1R04: Equipment Alignment

Procedures

HC.OP-ST.BD-0001, RCIC Piping and Flow Path Verification - Monthly, Revision 14

HC.OP-ST.EA-0001, Service Water Flow Path Verification - Monthly, Revision 11

OP-AA-108-116, Protected Equipment Program, Revision 9

OP-HC-108-115-1001, Operability Assessment and Equipment Control Program, Revision 27

Notifications (*NRC-identified)

20529358 20529359 20529360 20529362 20636088 20636089

20647011 20648223 20649406* 20649407* 20649408* 20649409*

Maintenance Orders/Work Orders

30255253 50165993 70127188 70129996

Drawings

E-0485-0, Electrical Schematic Auxiliary Building - Diesel Area Switchgear Room Coolers and

Air Dampers, Sht. 3, Revision 8

M-10-1, Sheet 1, Service Water, Revision 54

M-10-1, Sheet 2, Service Water, Revision 43

M-49-1, Reactor Core Isolation Cooling, Revision 30

M-50-1, RCIC Pump Turbine, Revision 29

Miscellaneous

HCGS PRA Risk Evaluation Form for Work Week #1418, Revision 3, dated May 2, 2013

MP 192355

NRC IN 96-06, Design and Testing Deficiencies of Tornado Dampers at Nuclear Power Plants

OE 33769

PM 30255253

Protected Equipment Log for HPCI Sight Glass Repair, dated May 2, 2014

Section 1R05: Fire Protection

Procedures

FP-AA-014, Fire Protection Training Program, Revision 1

FP-AA-015, Compensatory Measure Firewatch Program, Revision 5

FP-AA-028-1001, Emergency Response Safety and Risk Management Plan, Revision 0

FP-HC-004, Actions for Inoperable Fire Protection - Hope Creek Station, Revision 1

FRH-II-332, Service & Radwaste Area, Elevation: 102-0, Revision 4

FRH-II-412, Hope Creek Pre-Fire Plan, RCIC Pump and Turbine Room, RHR Pump and Heat

Exchanger Rooms, and Electrical Equipment Room, Elevations 54, Revision 3

FRH-II-415, Hope Creek Pre-Fire Plan, Dry Well Pad Torus Area, Elevations: 54-0 &77-0,

Revision 4

FRH-II-522, Hope Creek Pre-Fire Plan, Cable Spreading Room, Elevation: 77-0, Revision 6

FRH-II-532, Hope Creek Pre-Fire Plan, Lower Control Equipment Room, Elevation: 102-0,

Revision 6

Attachment

A-4

FRH-II-542, Hope Creek Pre-Fire Plan, Control Equipment Mezzanine, Elevations: 117-6 &

124-0, Revision 6

FRH-II-551, Hope Creek Pre-Fire Plan, Battery Rooms & Cable Chases, Elevations: 146-0 &

150-0, Revision 6

HC.OP-IS.BD-0001, Reactor Core Isolation Cooling Pump - OP203 - Inservice Test, Rev 58

SH.FP-EO.ZZ-0002, Fire Department Fire Response, Revision 3

Notifications (*NRC identified)

20632422 20633801 20639488 20642920 20644734 20644822

20646267 20646330 20646361 20647111 20647263* 20647351*

20651472

Maintenance Orders/Work Orders

0158901 50165299 70143862 70161457

Drawings

M-50-1, P&ID RCIC Pump Turbine, Revision 29

Miscellaneous

Fire Protection Impairment Permit 11760, dated April 16, 2014

Section 1R06: Flood Protection Measures

Procedures

EP-HC-111-130, HC EAL Wall Chart - All Conditions, Revision 1

HC.OP-AR.ZZ-0004, Overhead Annunciator Window Box A6, Revision 18

HC.OP-AR.ZZ-0006, Overhead Annunciator Window Box B1, Revision 25

HC.OP-AR.ZZ-0022, CRIDS Computer Points Book 3 D2880 Thru D3257, Revision 19

HC.OP-EO.ZZ-0103/4, Reactor Building and Radioactive Release Control, Revision 9

HC.OP-EO.ZZ-0103/4-CONV, Hope Creek Emergency Operating Procedure Conversion

Document, Revision 9

HC.OP-EO.ZZ-0103/4-FC, Reactor Building and Radioactive Release Control Flow Chart,

Revision 9

Notifications (*NRC identified)

20643688* 20643694* 20643696* 20643885* 20643886* 20643887*

20646334* 20646335* 20653586* 20656703*

Drawings

A-4641-1, Reactor Building Unit 1 Floor Plan at El. 54-0, Revision 6

J-25-0, Sheet 5, Logic Diagram Plant Leak Detection, Revision 6

M-25-1, Sheet 1, Plant Leak Detection, Revision 8

M-97-1, Sheet 2, Building and Equipment Drain Reactor Building, Revision 18

Other Documents

Calculation Number 11-0092, Reactor Building Flooding - Elevation 54 and 77, Revision 5

Calculation Number BC-0031, ECCS Pump Rooms Flood Level Alarm Set Point, Revision 1

HC-PRA-012, Internal Flood Evaluation Summary and Notebook, Revision 2

HC-PRA-017, Internal Flood Walkdown Notebook, Revision 0

Attachment

A-5

Section 1R11: Licensed Operator Requalification Program

Procedures

CY-AB-120-340, Offgas Chemistry, Revision 8

HC.OP-AB.IC-0001, Control Rod, Revision 16

HC.OP-FT.AC-0002, Main Turbine Functional Test Monthly, Revision 31

HC.OP-FT.AC-0005, Turbine Overspeed Protection System Operability Test - Quarterly,

Revision 13

HC.OP-ST.AC-0002, Turbine Valve Testing - Quarterly, Revision 49

HU-AA-1211, Pre-Job Briefings, Revision 11

NF-AA-400-1000, Fuel Integrity Monitoring, Revision 4

NF-AA-400-1700, BWR Fuel Reliability Indicator (FRI) Calculation and Transmittal, Revision 1

NF-AA-430, Failed Fuel Action Plan, Revision 8

OP-AA-101-111-1004, Operations Standards, Revision 4

OP-AA-108-111, Attachment 1, Adverse Condition Monitoring and Contingency Plan, Revision 7

OP-AA-300, Reactivity Management, Revision 6

OP-AB-300-1001, BWR Control Rod Movement Requirements, Revision 6

OP-AB-300-1003, BWR Reactivity Maneuver Guidance, Revision 11

Notifications

20543906 20566308 20644437

Maintenance Orders/Work Orders

50163804 70140638 80110856

Other Documents

HC 14-01, OTDM for Turbine Overspeed Protection System Operability Test - Quarterly,

February 11, 2014

HC 14-008, ACM for Fuel Reliability Parameters used to Monitor Fuel Defect indicate potential

fuel failure, March 25, 2014, Revision 0

Hope Creek Long Term Trends - 2014 for Failed Fuel Monitoring (NOTF 20644437)

Hope Creek Failed Fuel Monitoring Team Meeting on March 15, 2014

REMA 2014-0022, April 2014 TVT and PST Downpower REMA, Revision 0

Miscellaneous

Scenario Guide (SG)-644, Reactor Recirc Pump Trip / RWCU Leak / Loss of Main Condenser

Vacuum / ATWS dated April 24, 2014

Section 1R12: Maintenance Effectiveness

Procedures

ER-AA-10, Equipment Reliability Process Description, Revision 1

ER-AA-310, Implementation of the Maintenance Rule, Revision 11

ER-AA-310-1001, Maintenance Rule - Scoping, Revision 6

ER-AA-310-1004, Maintenance Rule - Performance Monitoring, Revision 10

ER-AA-310-1005, Maintenance Rule - Dispositioning Between (a)(1) and (a)(2), Revision 9

ER-HC-310-1009, Maintenance Rule System Function and Risk Significant Guide, Revision 10

ER-SA-310-1009, Salem Generating Station - Maintenance Rule Scoping, Revision 4

HC.DE-PS.ZZ-0041, Hope Creek Station Blackout Program, Revision 3

Attachment

A-6

HC.IC-CC.SK-0002, RCIC - Division 4 Steam Leak Detection Temperature Monitor H1SK-

1SKXR-11503, Revision 14

HC.IC-DC.SK-0001, NUMAC Leak Detection Setup and Trip Selection, Revision 11

HC.OP-AB.ZZ-0135, Station Blackout // Loss of Offsite Power // Diesel Generator Malfunction,

Revision 39

LS-AA-125, Corrective Action Program, Revision 17

MA-AA-716-004, Conduct of Troubleshooting, Revision 12

MA-AA-716-012, Post Maintenance Testing, Revision 19

MA-AA-716-210-1005, Predefine Change Process, Revision 3

S1.OP-AB.LOOP-0001, (Salem) Loss of Off-site Power, Revision 29

WC-AA-111, Predefine Process, Revision 8

Notifications

20335737 20413574 20447050 20502118 20570839 20619184

20623712 20638460 20640526 20645207 20651951

Orders

60113250 70073704 70105948 70121525 70124871 70157974

70161698 80110856

Miscellaneous

HC 10-03, License Amendment Request for Extending the Allowed Outage Time for the A and

B EDGs from 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> to 14 days

HC 13-015, OTDM for Continued Operation of the Moisture Separator without a Root Cause for

the Dump Valve Failing to Control Level, dated December 6, 2013

NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear

Power Plants, Revision 4

NRC Correspondence, HCGS - Issuance of Amendment Re: Emergency Diesel Generators A

and B Allowed Outage Time Extension, dated March 25, 2011

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

HC.CH-SA.HA-0002, Sampling Offgas System from 00-C-963 Panel, Revision 8

HC.OP-AB.RPV-0001, Reactor Power, Revision 13

HC.OP-FT.AC-0005, Turbine Overspeed Protection System Operability Test - Quarterly,

Revision 13

HC.OP-IO.ZZ-0006, Power Changes During Operation, Revision 57

HC.OP-SO.BB-0002, Reactor Recirculation System Operation, Revision 98

HC.OP-SO.PB-0001, 4.16KV System Operation, Revision 29

HC.OP-ST.PB-0002, AC Power Supply Transfer Functional Test - 18 Months, Revision 11

HC.OP-ST.ZZ-0001, Power Distribution Lineup - Weekly, Revision 36

MA-AA-1000, Conduct of Maintenance Manual, Section 3.0 - Maintenance Standards and

Practices, Revision 7 and 14

NC.CH-RC.ZZ-2525, Gamma Spectroscopy Analysis Using CAS, Revision 4

NF-AB-431, Power Suppression Testing, Revision 6

WC-AA-101, On-Line Work Management Process, Revision 22

WC-AA-105, Work Activity Risk Management, Revision 2

Attachment

A-7

Notifications (*NRC identified)

20465881 20521256 20585982 20593568 20600597 20627730

20632023 20634061 20637967 20638221 20639498 20639519

20644437 20645095 20645435 20645701* 20645705 20650898

20650904 20651102 20651204 20651430 20651432 20651876

20653142

Maintenance Orders/Work Orders

30098613 30098617 30243196 30265556 60061175 60114688

60117312 70046681 70072347 70097158 70110518 70142932

70155514 70162013

Miscellaneous

DCP 4-HC-0170

HC-14-006, OTDM for B Reactor Recirculation MG Set Speed Control, dated May 17, 2014

HCGS Operations Narrative Logs, May 14-15, 2014

HCGS PRA Risk Evaluation Form for June 8, 2014, through June 14, 2014, Revision 0

Protected Equipment Log -F FRVS Recirc Fan, dated June 8, 2014

HRE 2014-0023, Mid-Cycle 19 Standing REMA, from May 9-30, 2014, Revision 3

NRC RIS 2007-21, Adherence to Licensed Power Limits, Revision 1

REMA 2014-0022, April 2014 TVT and PST Downpower REMA, Revision 0

Troubleshooting Data Sheet - NOTF 20630902 for B RRP Speed Demand, dated

November 15, 2013

Troubleshooting Work Sheet - NOTF 20651102 for Proper Indication and Control of the B RRP

Speed Control Loop, dated May 14, 2014

WC-AA-105-F3, Form 3, Risk Management Plan - Replacement of B Isolator, Revision 1

Section 1R15: Operability Determinations and Functionality Assessments

CC-AA-309-101, Engineering Technical Evaluations, Revision 10

ER-AA-2006, Lost Parts Evaluation, Revision 8

HC.CH-CA.ZZ-0026, Boron by Mannitol Titration, Revision 18

HC.OP-AB.RPV-0001, Reactor Power, Revision 13

HC.OP-IO.ZZ-0006, Power Changes During Operation, Revision 57

HC.OP-IS.BH-0004, Standby Liquid Control Pump - BP208 - Inservice Test, Revision 12

HC.OP-SO.BB-0002, Reactor Recirculation System Operation, Revision 98

HC.OP-SO.KJ-0001, Emergency Diesel Generators Operation, Revision 70

HC.OP-SO.PB-0001, 4.16KV System Operation, Revision 29

HC.OP-ST.KJ-0003, Emergency Diesel Generator 1CG400 Operability Test - Monthly,

Revision 76

HC.OP-ST.PB-0002, AC Power Supply Transfer Functional Test - 18 Months, Revision 11

HC.OP-ST.ZZ-0001, Power Distribution Lineup - Weekly, Revision 36

HU-AA-1212, Technical Task Risk/Rigor Assessment, Pre-Job Brief, Independent Third Party

Review and Post-Job Brief, Revision 8

MA-AA-1000, Conduct of Maintenance Manual, Section 3.0 - Maintenance Standards and

Practices, Revision 7 and 14

WC-AA-101, On-Line Work Management Process, Revision 22

Attachment

A-8

Notifications (*NRC identified)

20221500 20439888 20442565 20442566 20465881 20521256

20585982 20593568 20600597 20616574 20627730 20632023

20634061 20637967 20638221 20639498 20639519 20640696

20643229 20643322* 20644637 20645519 20645994 20647199*

20650611* 20650701* 20650788* 20650831* 20650856* 20650858*

20650898 20650904 20651102 20651204 20651430 20651432

20651876 20652187 20652199 20653142 20653635*

Drawings

M-52-1, Core Spray, Revision 31

M-52-1, Sheet 1, Residual Heat Removal, Revision 45

M-52-1, Sheet 2, Residual Heat Removal, Revision 40

Maintenance Orders/Work Orders

30098613 30098617 30243196 50165850 60061175 60087495

60087534 60087538 60087539 60087540 60087541 60089905

60114688 60117312 70046681 70072347 70097158 70110518

70142932 70149472 70155514 70157453 70162013 70163760

70164628 80079629 80079863 80108395 80111752 80111754

Miscellaneous

10855-D3.33, Design, Installation and Test Specification for Standby Liquid Control System for

the Hope Creek Generating Station, Revision 5

22A7641, Design Specifications for SLC System, Revision 1

ASTM E29-13, Standard Practice for Using Significant Digits in Test Data to Determine

Conformance with Specifications

C-0001, Wall Thickness Calculation for Piping, Revision 9

Calculation 1SC-BH-0001, SLC System Tank 10T-204 Level, Revision 0

DCP 4-HC-0170

DCP 4HM-0136, Change Standby Liquid Control Tank Sodium Pentaborate Concentration from

13.4 to 14.0 Weight Percent, dated December 17, 1987

HC-14-006, OTDM for B Reactor Recirculation MG Set Speed Control, May 17, 2014

HCGS Operations Narrative Logs, May 14-15, 2014

HRE 2014-0023, Mid-Cycle 19 Standing REMA, from May 9-30, 2014, Revision 3

LD-042-MASTERPACT-1, Masterpact Issues, Revision 1

NLR-N87131, Request for Amendment Facility Operating License NPF-57 Hope Creek

Generating Station Docket No. 50-354, dated July 14, 1987

NRC RIS 2007-21, Adherence to Licensed Power Limits, Revision 1

Part 9900: Technical Guidance, Standard Technical Specifications Section 3.0 Acceptable

Measurement Tolerances for Technical Specification Limits, dated October 1, 1978

PM018Q-0499, Vol. 1, Operation and Maintenance Manual for Colt Industries Diesel Generator,

Revision 25

Troubleshooting Data Sheet - NOTF 20630902 for B RRP Speed Demand, dated November

15, 2013

Troubleshooting Work Sheet - NOTF 20651102 for Proper Indication and Control of the B RRP

Speed Control Loop, dated May 14, 2014

WC-AA-105-F3, Form 3, Risk Management Plan - Replacement of B Isolator, Revision 1

Attachment

A-9

Section 1R18: Plant Modifications

Procedures

CC-AA-102, Design Input and Configuration Change Impact Screening, Revision 23

CC-AA-103, Configuration Change Control for Permanent Physical Plant Changes, Revision 15

CC-AA-112, Temporary Configuration Changes, Revision 13

CC-AA-112-1001, Temporary Configuration Change Implementation T&RM, Revision 2

OP-AA-115-101, Operator Aid Postings, Revision 3

Notifications

20439888 20639161 20640696 20651205 20652187

Maintenance Orders/Work Orders

60115429 70163760 80107203 80111298 80111754

Drawings

M-08-0, Sheet 1, Condensate & Refueling Water Storage & Transfer, Revision 34

Miscellaneous

DCP 80111754, Masterpact Breaker Add Aux Contact with Close Coil, Revision 1

H-1-ZZ-EGS-0043, Hope Creek Generating Station GE AKR Circuit Breaker Replacement

Project

LD-042-MASTERPACT-1, Revision 1

OPEVAL 14-002, Masterpact Breaker Model NW with Locked in Close Signal, Revision 3

Temporary Configuration Change Package Tracking Log, dated June 10, 2014

Section 1R19: Post-Maintenance Testing

Procedures

CC-AA-309-101, Engineering Technical Evaluations, Revision 10

HC.IC-CC.SK-0002, RCIC - Division 4 Steam Leak Detection Temperature Monitor H1SK-

1SKXR-11503, Revision 14

HC.IC-DC.SK-0001, NUMAC Leak Detection Setup and Trip Selection, Revision 11

HC.IC-DC.ZZ-0011, Device/Equipment Calibration Bailey, Characterizable Pneumatic

Positioner, Type AP2, Revision 5

HC.OP-AB.COMP-0001, Instrument and/or Service Air, Revision 5

HC.OP-AB.RPV-0001, Reactor Power, Revision 13

HC.OP-IO.ZZ-0006, Power Changes During Operation, Revision 57

HC.OP-IS.BJ-0001, HPCI Main and Booster Pump Set - OP204 and OP217 - Inservice Test,

Revision 62

HC.OP-SO.BB-0002, Reactor Recirculation System Operation, Revision 98

HC.OP-ST.BC-0005, LPCI Subsystem B ECCS Time Response Functional Test - 18 Months,

Revision 16

HC.OP-ST.ZZ-0001, Power Distribution Lineup - Weekly, Revision 36

HU-AA-1212, Technical Task Risk/Rigor Assessment, Pre-Job Brief, Independent Third Party

Review and Post-Job Brief, Revision 8

MA-AA-716-012, Post Maintenance Testing, Revision 19

MA-AA-1000, Conduct of Maintenance Manual, Section 3.0 - Maintenance Standards and

Practices, Revision 7 and 14

SM-AA-410, Control of Purchased Material, Equipment and Services Program, Revision 6

WC-AA-101, On-Line Work Management Process, Revision 22

Attachment

A-10

Notifications (*NRC identified)

20454035 20465881 20521256 20619184 20623712 20623802

20629385 20632023 20642546 20642950 20647111 20650904

20651102 20651430 20651872 20651951 20652010 20652012

20652232 20652238 20652321 20652339 20652702 20653142

20653572* 20653872*

Maintenance Orders/Work Orders

30098613 30098617 30240742 30269527 50163142 60113238

60113250 60116090 60117312 70125746 70155514 70157974

70163994 70166194

Drawings

PN11-E11-1040-0383, Sheet 3, Residual Heat Removal System, Revision 15

PN11-E11-1040-0383, Sheet 12, Residual Heat Removal System, Revision 18

PN11-E11-1040-0383, Sheet 13, Residual Heat Removal System, Revision 10

PN11-E11-1040-0383, Sheet 22, Residual Heat Removal System, Revision 17

Miscellaneous

HC-14-006, OTDM for B Reactor Recirculation MG Set Speed Control, dated May 17, 2014

HCGS Operations Narrative Logs, May 14-15, 2014

HCGS PRA Risk Evaluation Form for April 20, 2014 through April 26, 2014

HRE 2014-0023, Mid-Cycle 19 Standing REMA, from May 9-30, 2014, Revision 3

NRC RIS 2007-21, Adherence to Licensed Power Limits, Revision 1

Troubleshooting Data Sheet - NOTF 20630902 for B RRP Speed Demand, dated

November 15, 2013

Troubleshooting Work Sheet - NOTF 20651102 for Proper Indication and Control of the B RRP

Speed Control Loop, dated May 14, 2014

WC-AA-105-F3, Form 3, Risk Management Plan - Replacement of B Isolator, Revision 1

Section 1R22: Surveillance Testing

Procedures

CC-AA-309-101, Engineering Technical Evaluations, Revision 10

ER-AA-2006, Lost Parts Evaluation, Revision 8

FP-HC-004, Actions for Inoperable Fire Protection - Hope Creek Station, Revision 1

HC.FP-ST.KC-0009, Diesel Driven Fire Pump Operability Test, Revision 20

HC.IC-CC.SK-0016, Radiation Monitoring - Channel D Monitor H1SK-1SKLY-4930 Drywell

Leak Detection Sump Monitoring System (DLD-SMS), Revision 22

HC.IC-GP.ZZ-0004, Thermocouples (T/C) and Resistance Temperature Detectors (RTD),

Revision 8

HC.MD-ST.PB-0003, Class 1E 4.16 kV Feeder Degraded Voltage Monthly Instrumentation

Channel Functional Test, Revision 26

HC.OP-DL.ZZ-0026, Surveillance Log, Revision 139

HC.OP-FT.AC-0002, Main Turbine Functional Test Monthly, Revision 31

HC.OP-FT.AC-0005, Turbine Overspeed Protection System Operability Test - Quarterly,

Revision 13

HC.OP-IS.BC-0002, CP202, C Residual Heat Removal Pump In-Service Test, Revision 43

HC.OP-IS.BJ-0001, HPCI Main and Booster Pump Set - 0P204 and 0P217 - Inservice Test,

Revision 62

Attachment

A-11

HC.OP-SO.KJ-0001, Emergency Diesel Generators Operation, Revision 70

HC.OP-ST.AC-0002, Turbine Valve Testing - Quarterly, Revision 49

HC.OP-ST.KJ-0001, Emergency Diesel Generator 1AG400 Operability Test - Monthly,

Revision 76

HC.OP-ST.KJ-0003, Emergency Diesel Generator 1CG400 Operability Test - Monthly,

Revision 78

HC.OP-ST.SK-0001, Alternate RCS Leakage Determination, Revision 9

HU-AA-1211, Pre-Job Briefings, Revision 11

HU-AA-1212, Technical Task Risk/Rigor Assessment, Pre-Job Brief, Independent Third Party

Review and Post-Job Brief, Revision 8

OP-AA-101-111-1004, Operations Standards, Revision 4

OP-AA-108-101, Control of Equipment and System Status, Revision 7

OP-AA-300, Reactivity Management, Revision 6

Notifications

20504658 20629522 20630428 20630429 20640032 20645519

20645994 20646319 20648114 20648751 20649201 20649292

20649425 20649905 20649906 20654936

Maintenance Orders/Work Orders

30199753 50163804 50164408 50164695 50165664 50165690

50165691 50165850 50166624 50167441 50169340 60026593

60058122 60097901 60107882 70008407 70023178 70097767

70122058 70127960 70139509 70145982 80111752

Calculations

SC-SK-0118, Drywell Leak Detection SMS (Floor Drain Unidentified Leakage), Revision 2

Miscellaneous

HC 14-01, OTDM for Turbine Overspeed Protection System Operability Test - Quarterly, dated

February 11, 2014

HCGS PRA Risk Evaluation Form for April 6, 2014, through April 12, 2014

PM018Q-0499, Vol. 1, Operation and Maintenance Manual for Colt Industries Diesel Generator,

Revision 25

REMA 2014-0022, April 2014 TVT and PST Downpower REMA, Revision 0

Section 1EP6: Drill Evaluation

Procedures

EP-AA-122, Drills and Exercises, Revision 3

EP-AA-122-1001, Drill and Exercise Scheduling, Development and Conduct, Revision 3

EP-AA-125-1002, NRC Drill and Exercise Performance (DEP) Indicator Guidance, Revision 3

EP-HC-111-121, Fission Product Barrier Table, Revision 1

EP-HC-111-230, Use of Fission Product Barrier Table, Revision 0

NC.EP-EP.ZZ-0102, Emergency Coordinator Response, Revision 18

NC.EP-EP.ZZ-0404, Protective Action Recommendations (PARS) Upgrades, Revision 4

Notifications

20654844

Attachment

A-12

Miscellaneous

DEP Observation Checklist for FAD-HC14-02, dated June 24, 2014

Section 4OA1: Performance Indicator Verification

Procedures

HC.OP-DL.ZZ-0026, Surveillance Log, Revision 136

HC.OP-DL.ZZ-0026, Surveillance Log, Revision 137

HC.OP-DL.ZZ-0026, Surveillance Log, Revision 138

HC.OP-DL.ZZ-0026, Surveillance Log, Revision 139

HC.RA-IS.ZZ-0010, Containment Isolation Valve Type C Leak Rate Test, Revision 15

LS-AA-2090, Monthly Data Elements for NRC Reactor Coolant System Activity, Revision 5

LS-AA-2100, Monthly Data Elements for NRC Reactor Coolant System Leakage, Revision 6

LS-HC-1000-1001, Hope Creek Generating Station Surveillance Frequency Control Program

List of Surveillance Frequencies, Revision 4

NC.CH-RC.ZZ-2525, Gamma Spectroscopy Analysis Using CAS, Revision 4

NC.CH-SA.RC-0002, Operation of the Reactor Building/RHR Sample Stations, Revision 18

Calculations

SC-SK-0119, Drywell Leak Detection SMS - Equipment Drain Sump, Revision 1

Notifications

20650305

Maintenance Orders/Work Orders

50137021 50149686 50162608

Miscellaneous

Daily Dose Equivalent Iodine-131 Sample Data

Daily Surveillance Log Data

Monthly Data Elements for NRC Reactor Coolant System Leakage Data Sheets

Section 4OA2: Problem Identification and Resolution

Procedures

ER-AA-2003, System Performance Monitoring and Analysis, Revision 9

ER-AA-3002, Component Cross-System Monitoring & Component Health Reporting, Revision 3

LS-AA-125, Corrective Action Program, Revision 17

LS-AA-125-1006, Performance Improvement Integrated Matrix (PIIM), Revision 5

LS-AA-1006, NRC Cross-Cutting Analysis and Trending, Revision 2

Notifications (*NRC identified)

20615843 20619913 20632801 20632802 20632361 20632641

20632746 20632747 20632748 20632749 20633058 20633338

20633339 20634028 20635871 20636138 20638889 20639772

20642767 20644539

Orders

70144876 70158815 70161953 70162269 80109029 80110809

80110866

Attachment

A-13

Miscellaneous

Hope Creek Engineering PIIM Report 1st Cycle 2013 Presentation, dated 8/31/13

Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion

Procedures

CC-AA-102, Design Input and Configuration Change Impact Screening, Revision 23

CC-AA-103, Configuration Change Control for Permanent Physical Plant Changes, Revision 15

ER-HC-310-1009, Maintenance Rule System Function and Risk Significant Guide, Revision 10

HC.IC-DC.ZZ-0140, Device/Equipment Cal. Masoneilan Pressure Temperature Controller,

Revision 4

HC.IC-LC.AF-0007, Moisture Separator Drain Tank Level Tuning, Revision 2

HC.OP-AB.RPV-0001, Reactor Power, Revision 13

HC.OP-AR.ZZ-0008, Overhead Annunciator Window Box C1, Revision 45

HC.OP-DL.ZZ-0026, Surveillance Log, Revision 140

HC.OP-SO.BB-0002, Reactor Recirculation System Operation, Revision 98

HC.OP-SO.GJ-0001, A(B) K400 Control Area Chilled Water System Operation, Revision 60

HU-AA-1211, Pre-Job Briefings, Revision 11

LS-AA-125-1003, Attachment 2, Equipment Apparent Cause Evaluation Guide, Revision 13DCP

4EC-3662

MA-AA-716-004, Conduct of Troubleshooting, Revision 12

SM-AA-300, Procurement Engineering Support Activities, Revision 7

WC-AA-105, Work Activity Risk Management, Revision 2

Notifications (*NRC identified)

20454035 20521256 20528822 20529153 20567269 20570629

20630857 20631351 20631820 20631940 20632542 20638799

20640526 20642546 20642767 20643301 20644017 20645207

20647829 20650346* 20650904 20651102 20651876 20652180

20652182 20652183 20652184 20652185 20652186 20652188

20653024 20653142

Maintenance Orders/Work Orders

60114285 60114286 70041898 70110518 70115711 70119769

70128407 70129670 70140751 70142556 70159686 70161353

70161698 70162284

Miscellaneous

10855-d3.33, Design, Installation and Test Specification for Standby Liquid Control System for

the Hope Creek Generating Station, Revision 5

22A7641, Design Specifications for SLC System, Revision 1

ASTM E29-13, Standard Practice for Using Significant Digits in Test Data to Determine

Conformance with Specifications

Calculation 1SC-BH-0001, SLC System Tank 10T-204 Level, Revision 0

DCP 4-HC-0170

DCP 4HM-0136, Change Standby Liquid Control Tank Sodium Pentaborate Concentration from

13.4 to 14.0 Weight Percent, December 17, 1987

HC-14-006, OTDM for B Reactor Recirculation MG Set Speed Control, dated May 17, 2014

HCGS Operations Narrative Logs, May 14-15, 2014

HRE 2014-0023, Mid-Cycle 19 Standing REMA, from May 9-30, 2014, Revision 3

Attachment

A-14

LER 2013-009-00, Automatic Actuation of the Reactor Protection System Due to a Main Turbine

Trip

LER 2013-009-01, Automatic Actuation of the Reactor Protection System Due to a Main Turbine

Trip

NLR-N87131, Request for Amendment Facility Operating License NPF-57 Hope Creek

Generating Station Docket No. 50-354, dated July 14, 1987

NRC RIS 2007-21, Adherence to Licensed Power Limits, Revision 1

Part 9900: Technical Guidance, Standard Technical Specifications Section 3.0 Acceptable

Measurement Tolerances for Technical Specification Limits, October 1, 1978

PM018Q-0499, Vol. 1, Operation and Maintenance Manual for Colt Industries Diesel Generator,

Revision 25

Troubleshooting Data Sheet - NOTF 20630902 for B RRP Speed Demand, dated

November 15, 2013

Troubleshooting Work Sheet - NOTF 20651102 for Proper Indication and Control of the B RRP

Speed Control Loop, dated May 14, 2014

WC-AA-105-F3, Form 3, Risk Management Plan - Replacement of B Isolator, Revision 1

Section 4OA5: Other Activities

Condition Reports

20650822 20650823 20652896

Procedures

ER-AA-5400, Underground Piping Program Guide, Revision 4

ER-AA-5400-1002, Underground Piping Examination Guide, Revision 3

SA-AA-117, Industrial Safety, Excavating Trenching, and Shoring, Revision 13

Miscellaneous

Cathodic Protection System Health Report for Hope Creek, Q1-2014

Cathodic Protection System Health Report for Salem U1, Q2-2014

Hope Creek Underground Piping Inspection Plan, Revision 3

LR-ISG-2011-03, Aging Management Program XI.M41, "Buried and Underground Piping and

Tanks"

NACE SP0169-2007, Control of External Corrosion on Underground or Submerged

Metallic Piping Systems, Revision 0

NEI-09-14, Guideline for the Management of Underground Piping and Tank Integrity

Location Sketch for Cathodic Protection of Salem U1 and U2 Structures, Revision 3

Program Health Report for the Salem Plant Underground Piping Program, P1-2014

Program Health Report for the Hope Creek Plant Underground Piping Program, P1-2014

Salem Underground Piping Inspection Plan, Revision 3

Underground Piping Inspection and Evaluation Report for Hope Creek line 0-DB-003, Liquid

RadWaste Discharge, dated February 22,2013

Underground Piping Inspection and Evaluation Report for Salem line SC-LW-0001-12-01, liquid

waste, Steam Generator Blowdown, dated September 11, 2012

Underground Piping Inspection and Evaluation Report for Salem lines S1-SG-1031-10 and S2-

SG-1111-10, dated September 17-20, 2012

UT report on Hope Creek component HODB-0-DB-V013, dated June 20, 2013

Attachment

A-15

LIST OF ACRONYMS

10 CFR Title 10 of The Code of Federal Regulations

ADAMS Agencywide Documents Access and Management System

CAP corrective action program

CCE common cause evaluation

CFR The Code of Federal Regulations

CRE control room envelope

DCP design change package

EDG emergency diesel generator

EN event notification

EQACE equipment apparent cause evaluation

ER Environmental Report

HCGS Hope Creek Generating Station

HLA heightened level of awareness

HPCI high pressure coolant injection

HVAC heating, ventilation and air conditioning

IMC Inspection Manual Chapter

kV kilovolt

LER licensee event report

LM logic module

MCR main control room

MS moisture separator

NACE National Association of Corrosion Engineers

NCV non-cited violation

NEI Nuclear Energy Institute

NOTF notification

NRC Nuclear Regulatory Commission

NRR Nuclear Reactor Regulation

PARS Publicly Available Records

PC purchase classification

PCV pressure control valve

PI performance indicator

PIIM performance improvement integrated matrix

PSEG Public Service Enterprise Group Nuclear, LLC

PST power suppression testing

RCIC reactor core isolation cooling

RCS reactor coolant system

RG Regulatory Guide

RHR residual heat removal

RRP reactor recirculation pump

RTP rated thermal power

RWCU reactor water cleanup

SACS safety auxiliaries cooling system

SDP Significance Determination Process

SLC standby liquid control

SRV safety relief valve

SSC structure, system, or component

SSW station service water

Attachment

A-16

TCCP temporary configuration control package

TI Temporary Instruction

TS technical specifications

TSAS technical specification action statement

U1 Unit 1

U2 Unit 2

UFSAR Updated Final Safety Analysis Report

UT ultrasonic testing

V volt

WO work order

Attachment