ML102220170

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IR 05000272-10-003, 05000311-10-003; 04/01/2010 - 06/30/2010; Salem Nuclear Generating Station, Unit Nos. 1 and 2; Inservice Inspection and Maintenance Effectiveness
ML102220170
Person / Time
Site: Salem, University of New Mexico
Issue date: 08/10/2010
From: Arthur Burritt
Reactor Projects Branch 3
To: Joyce T
Public Service Enterprise Group
BURRITT, AL
References
IR-10-003
Download: ML102220170 (50)


See also: IR 05000272/2010003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD

KING OF PRUSSIA, PA 19406-1415

I*

August 10, 2010

Mr. Thomas P. Joyce

President and Chief Nuclear Officer

PSEG Nuclear LLC - N09 I

P.O. Box 236

Hancock's Bridge, NJ 08038 I

SUBJECT: SALEM NUCLEAR GENERATING STATION, UNIT NOS. 1 AND 2-

NRC INTEGRATED INSPECTION REPORT 05000272/2010003 and

05000311/2010003

Dear Mr. Joyce:

On June 30,2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

the Salem Nuclear Generating Station, Unit Nos. 1 and 2. The enclosed integrated inspection

report documents the inspection results discussed on July 8, 2010, with Mr. Fricker and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

The report documents one NRC-identified finding and one self-revealing finding of very low

significance (Green). One of these two findings was determined to involve a violation of NRC

requirements. Additionally, one licensee-identified violation of very low safety significance is

listed in this report. However, because of the very low safety significance of these two violations

and because they were entered into your corrective action program (CAP), the NRC is treating

these findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC

Enforcement Policy. If you contest any NCV in this report, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United

States Nuclear Regulatory CommisSion, Washington, DC 20555-0001; and the NRC Resident

Inspector at the Salem Nuclear Generating Station. In addition, if you disagree with the cross-

cutting aspect assigned to any finding in this report, you should provide a response within 30

days of the date of this inspection report, with the basis of your disagreement, to the Regional

Administrator, Region I, and the NRC Resident Inspector at Salem Nuclear Generating Station.

T. Joyce 2

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).

Arthur L. Burritt, Chief

Projects Branch 3

Division of Reactor Projects

Docket Nos: 50-272; 50-311

License Nos: DPR-70; DPR-75

Enclosure: Inspection Report 05000272/2010003 and 05000311/2010003

w/Attachment A: Supplemental Information

Attachment B: TI 172 MSIP Documentation Questions Salem Unit 1

cc w/encl: Distribution via ListServ

T. Joyce 2

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).

Sincerely.

IRA!

Arthur L. Burritt, Chief

Projects Branch 3

Division of Reactor Projects

Docket Nos: 50-272; 50-311

License Nos: DPR-70; DPR-75

Distribution w/encl.

M. Dapas, Acting RA (R10RAMAIL Resource) C. Douglas, DRP

D. Lew, Acting DRA (R10RAMAIL Resource) A. Turilin, DRP

J. Clifford, DRP (R1DRPMAIL Resource) D. Schroeder, DRP, SRI

D. Roberts, DRS (R1DRSMail Resource) K. McKenzie, DRP, OA

P. Wilson, DRS (R1DRSMaii Resource) L. Trocine, RI, OEDO

A. Burritt, DRP RidsNrrPMSalem Resource

L. Cline, DRP RidsNrrDorlLpl1-2Resource

ROPreportsResource@nrc.gov

DOCUMENT NAME: G:\DRP\BRANCH3\lnspection\Reports\lssued\SAL 1003.docx

SUNSI Review Complete: LC (Reviewer's Initials) ML102220170

After declaring this document "An Official Agency Record" it will be released to the Public.

To receive a copy 0 this document, indicate in the box: "C n= CODY without attachment/enclosure "En = CoDV with attachment/enclosure *N" = No copy

OFFICE mmt RIIDRP I RIIDRP I RIIDRP I I

NAME DSchroederl LCline/LC ABurritvALB

DATE 07/30/10 08/06/10 08/10/10

OFFICIAL RECORD COPY

1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos: 50-272, 50-311

License Nos: DPR-70, DPR-75

Report No: 05000272/2010003 and 05000311/2010003

Licensee: PSEG Nuclear LLC (PSEG)

Facility: Salem Nuclear Generating Station, Unit Nos. 1 and 2

Location: P.O. Box 236

Hancocks Bridge, NJ 08038

Dates: April 1, 2010 through June 30, 2010

Inspectors: D. Schroeder, Senior Resident Inspector

H. Balian, Resident Inspector

D. Johnson, Acting Resident Inspector

S. Ibarrola, Acting Resident Inspector

J. Furia, Senior Health PhysiCist

M. Patel, Reactor Inspector

1. O'Hara, Reactor Inspector

Approved By: Arthur L Burritt, Chief

Projects Branch 3

Division of Reactor Projects

Enclosure

2

TABLE OF CONTENTS

SUMMARY OF FI NDINGS ......................................................................................................... 3

REPORT DETAILS .................................................................................................................... 5

1. REACTOR SAFETy ............................................................................................................... 5

1R01 Adverse Weather Protection ................................................................................... 5

1R04 Equipment Alignment ............................................................................................. 6

1R05 Fire Protection ........................................................................................................ 7

1R07 Heat Sink Performance ......................................................................... " ............... 8

1R08 Inservice Inspection (lSI) ........................................................................................ 8

1R11 Licensed Operator Requalification Program .............................. " ...... " .. " .............. 12

1R12 Maintenance Effectiveness ................................................................................... 13

1R13 Maintenance Risk Assessments and Emergent Work Control .. " .......................... 15

1R15 Operability Evaluations .. " ........... ,.............................................. " ......................... 16

1R18 Plant Modifications ............................................................................................... 16

1R19 Post-Maintenance Testing .............................................. " .................................... 17

1R20 Refueling and Other Outage Activities ...................................... " .......... " .......... " .. 18

1R22 Surveillance Testing ............................... " ............................................................ 20

1EP6 Drill Evaluation .. " ....................................................................... " .................... " .. 20

2. RADIATION SAFETY .................................................................................................." ....... 21

2RS1 Radiological Hazard Assessment and Exposure Controls .... " .............................. 21

2RS2 Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls23

4. OTHER ACTIVITIES .......................... " ............................. " ............................................. " .. 23

40A 1 Performance Indicator (PI) Verification .......................... " ................................ " ... 23

40A2 Identification and Resolution of Problems ............................ " .... " ................ " ....... 24

40A3 Event Follow-up ............................................................. ,..................................... 25

40A5 Temporary Instruction (TI) 2515/172 .................. " ...................... " ......................... 26

40A6 Meetings, Including Exit ................................................. " ...................... " ............. 27

40A7 Licensee Identified Violations ................................................................................ 27

ATTACHMENT A: SUPPLEMENTAL INFORMATION ............................................................. 27

ATTACHMENT B: T1172 MSIP DOCUMENTATION QUESTIONS SALEM UNIT 1 ........ " ...... 27

SUPPLEMENTAL INFORMATION ..........................................................................................A-1

KEY POI NTS OF CONTACT ................................................. " .......... " .................................. "A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED .................................................... ".A-1

LIST OF DOCUMENTS REVIEWED ......................................................................... " .......... "A-1

LIST OF ACRONYMS ...........................................................................................................A-17

TI 172 MSIP Documentation Questions Salem Unit 1.. .................................. " .......... " ............ B-1

Enclosure

3

SUMMARY OF FINDINGS

IR 05000272/2010003, 05000311/2010003; 04/01/2010 - 06/30/2010; Salem Nuclear

Generating Station Unit Nos. 1 and 2; Inservice Inspection and Maintenance Effectiveness.

The report covered a three-month period of inspection by resident inspectors, and announced

inspections by a regional radiation specialist and reactor engineers. One Green non cited

violation (NCV) and one Green finding were identified. The significance of most findings is

indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter (lMC)

0609, "Significance Determination Process" (SOP) and the cross-cutting aspect of a finding is

determined using IMC 0310, "Components Within the Cross-Cutting Areas." Findings for which

the SOP does not apply may be Green or be assigned a severity level after NRC management

review. The NRC's program for overseeing the safe operation of commercial nuclear power

reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated

December 2006.

Cornerstone: Initiating Events

  • Green. A self-revealing finding of very low safety significance was identified on January

21, 2010, because a control system short circuit caused the 21 steam generator feed

pump (SGFP) to trip. This caused a turbine runback and ultimately an automatic Unit 2

reactor trip due to low water level in one of four steam generators (SGs). The short

circuit occurred because technicians did not use the correct procedure to repair

degraded insulation on the barrel of a connector lug that was identified in the 21 SGFP

control system in November 2009. PSEG repaired the short circuit prior to restart of Unit

2 on January 23, 2010. The issue was entered into the corrective action program as

notification 20448229. PSEGs immediate corrective actions for this issue included

repairing the degraded insulation, fixing lug alignment and performing extent of condition

inspections on the other Unit 2 SGFP panels for degraded insulation. No other

deficiencies were identified.

This performance deficiency is more than minor because it is associated with the human

performance attribute of the Initiating Events cornerstone, and it adversely affected the

cornerstone objective to limit the likelihood of events that upset plant stability and

challenge critical safety functions. Specifically, not following PSEG procedure SC.DE-

TS.ZZ-2039 on November 11, 2009, caused the 21 SGFP trip and subsequent

automatic reactor trip due to low SG water level on January 21,2010. The finding was

evaluated under IMC 0609, Attachment 4. The inspectors determined that the finding is

of very low safety significance because it does not contribute to both the likelihood of a

reactor trip and the likelihood that mitigation equipment or functions will not be available.

The inspectors determined that this finding has a cross-cutting aspect in the area of

human performance because PSEG personnel did not follow procedure requirements

while repairing plant equipment. Specifically, technicians applied electrical tape to the

21 SGFP pressure switch connector lug barrel on November 11, 2009, which did not

meet PSEG procedure SCDE-TS.ZZ-2039 requirements. (HA (b)) (Section 1R12)

Enclosure

4

Cornerstone: Mitigating Systems

/

  • Green. The inspector identified an NCV of very low safety significance for PSEG's

failure to perform auxiliary feedwater (AFW) discharge piping system pressure tests on

buried piping components as required by 10 CFR 50.55a(g)(4) and the referenced

American Society of Mechanical Engineers Code (ASME),Section XI, paragraph IWA-

5244 for Salem Unit 1. The required tests are intended to demonstrate the structural

integrity of the buried piping portions of the system. PSEG entered this condition into

the corrective action program (notification 20459689) and replaced the affected Unit 1

AFW piping.

This performance deficiency is more than minor, because, if left uncorrected, it would

have resulted in a more significant safety concern. Specifically, the inspectors

determined that based on the degraded condition of the coating and piping discovered

during excavation on Unit 1, without performance of the required pressure test, an

undetected failure of the piping would have resulted due to continued, undetected

corrosion. The finding impacts the Mitigating Systems cornerstone. Using IMC 0609,

Attachment 4, the finding was determined to be of very low safety significance because it

was not a design or qualification deficiency, did not result in an actual loss of safety

function, and was not potentially risk significant for external events. No cross cutting

Aspect is assigned to this violation because this condition began in 1988, more than 3

years ago, and is not indicative of current performance. (Section 1R08)

Other Findings

  • One violation of very low safety significance was identified by PSEG and has been

reviewed by the inspectors. Corrective actions taken or planned by PSEG have been

entered into PSEG's corrective action program (CAP). This violation and its corrective

action tracking numbers are listed in Section 40A7 of this report.

Enclosure

5

REPORT DETAILS

Summary of Plant Status

Salem Nuclear Generating Station Unit 1 (Unit 1) began the period at full power. On April 2,

operators reduced power to 89 percent because heavy river water detritus prevented adequate

cooling of the main condenser. On April 3, operators shut down Unit 1 to begin the twentieth

refueling outage (RFO) (S1 R20). On April 29 the RFO ended when operators synchronized the

main generator to the grid. On May 1, operators returned Unit 1 to full power. On June 15,

operators reduced power to 3 percent and removed the main turbine from service due to erratic

operation of the 13 steam generator (SG) feed regulating valve (FRV). Operators synchronized

Unit 1 to the grid again on June 16, but because the 12 SG FRV was not adequately controlling

12 SG water level, operators removed the main turbine from service on June 17. Operators

synchronized Unit 1 to the grid on June 17 and returned the unit to full power on June 18. Unit

1 remained at or near full power for the remainder of the inspection period.

Salem Nuclear Generating Station Unit 2 (Unit 2) began the period at full power. On April 1,

operators reduced power to 83 percent because heavy river water detritus prevented adequate

cooling of the main condenser. On April 2, operators reduced power to 69 percent because

heavy river water detritus prevented adequate cooling of the main condenser. On April 5,

operators began power ascension and reached full power on April 7. Unit 2 remained at or near

full power for the remainder of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity and Emergency

Preparedness

1R01 Adverse Weather Protection (71111.01 - 1 sample)

.1 Summer Readiness of Offsite and Alternate AC Power Systems

a. Inspection Scope

The inspectors completed one adverse weather inspection sample to evaluate the

readiness of offsite power to the Salem units prior to the summer season when electrical

grid stability can be most challenged. The inspectors verified that PSEG provided

procedure requirements or guidance to monitor and maintain availability and reliability of

the offsite AC Power (OSP) system prior to and during adverse weather conditions.

Specifically, the inspectors verified that the procedures addressed:

  • The actions to be taken when notified by the electrical system operations center

(ESOC) of the PJM interconnection that the posHrip voltage of the OSP system at

Salem will not be acceptable to assure the continued operation of the safety-related

loads without transferring to the emergency diesel generators (EDGs);

  • The compensatory actions to be performed if ESOC cannot predict the post-trip

voltage;

  • The re-assessment of plant risk for maintenance activities that could affect grid

reliability or OSP system availability to the Salem units; and

Enclosure

6

  • Communication requirements between Salem and the ESOC regarding plant

changes that could impact the transmission system, or the capacity of the

transmission system to provide adequate aSP.

The inspectors also reviewed PSEG's seasonal readiness preparations for the summer

season specific to the main power transformers and the asp system. The inspectors

interviewed engineering and work control personnel and reviewed work orders and

completed portions of WC-AA-107, Seasonal Readiness, to verify that PSEG took

measures to ensure the reliability of the main transformers and the asp system during

the summer season. The documents reviewed during this inspection are listed in the

Attachment A.

b. Findings

No findings of significance were identified.

1 R04 Equipment Alignment (71111.04 - 3 samples; 71111.04S -1 sample)

.1 Partial Walk down

a. Inspection Scope

The inspectors completed three partial system walk down inspection samples. The

inspectors walked down the systems listed below to verify the operability of redundant or

diverse trains and components when safety equipment was inoperable. The inspectors

focused their review on potential discrepancies that could impact the function of the

system and increase plant risk. The inspectors reviewed applicable operating

procedures, walked down control systems components, and verified that selected

breakers, valves, and support equipment were in the correct position to support system

operation. The inspectors also verified that PSEG properly utilized its corrective action

program to identify and resolve equipment alignment problems that could cause initiating

events or impact the capability of mitigating systems or barriers. Documents reviewed

are listed in the Attachment A.

unavailability of the 11 SW header;

  • Unit 2, 21 component cooling (CC) heat exchanger (HX) with 22 CC HX out-of-

service (OOS); and

Enclosure

7

.2 Complete Walk down

a. Inspection Scope

The inspectors conducted one complete walk down inspection sample of the Unit 1

safety injection (SI) system on June 28 through 30, 2010. The inspectors independently

verified the alignment and status of SI pump and valve electrical power, labeling,

hangers and supports, and associated support systems. The walk down also included

evaluation of system piping and equipment to verify pipe hangers were in satisfactory

condition, oil reservoir levels were normal, pump rooms and pipe chases were

adequately ventilated, system parameters were within established ranges, and

equipment deficiencies were appropriately identified. The inspectors interviewed

engineering personnel and reviewed corrective action evaluations associated with the

system to determine whether equipment alignment problems were identified and

appropriately resolved. Documents reviewed are listed in the Attachment A.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05Q - 6 samples)

.1 Fire Protection - Tours

a. Inspection Scope

The inspectors completed six fire protection quarterly inspection samples. The

inspectors walked down the systems listed below to assess the material condition and

operational status of fire protection features. The inspectors verified that combustibles

and ignition sources were controlled in accordance with PSEG's administrative

procedures; fire detection and suppression equipment was available for use; that

passive fire barriers were maintained in good material condition; and that compensatory

measures for out of service (OOS), degraded, or inoperable fire protection equipment

were implemented in accordance with PSEG's fire plan. Documents reviewed are listed

in the Attachment A.

  • Unit 1, auxiliary building, 84' elevation inside the charging pipe alley;
  • Unit 1, electrical penetration, 78' elevation;
  • Unit 1, AFW pumps area, 84' elevation;
  • Unit 1, diesel fuel oil storage area, 84' elevation;
  • Unit 2, diesel fuel oil storage area, 84' elevation; and
  • Unit 1, containment during the RFO.

b. Findings

No findings of significance were identified.

Enclosure

8

1R07 Heat Sink Performance (71111.07A-1 sample)

a. Inspection Scope

The inspectors completed one annual heat sink performance inspection sample. The

inspectors reviewed performance data and interviewed the NRC Generic Letter (GL) 89-

13 program manager to verify that potential HX or heat sink deficiencies were identified

and PSEG adequately resolved heat sink performance problems. Specifically, the

inspectors reviewed 12B component cooling water (CCW) HX data. Inspectors

evaluated trending data and verified that equipment would perform satisfactorily under

design basis conditions. The method of performance monitoring was compared to the

guidance provided in NRC GL 89-13, "Service Water System Problems Affecting Safety-

Related Equipment," and Electric Power Research Institute NP 7552, "HX Performance

Monitoring Guidelines." Documents reviewed are listed in the Attachment A.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection (lSI) (71111.08P -1 sample)

a. Inspection Scope

The inspector observed a selected sample of nondestructive examination (NOE)

activities in process. Also, the inspector reviewed the records of selected additional

samples of completed NOE and repair/replacement activities. The sample selection was

based on the inspection procedure objectives and risk priority of those components and

systems where degradation would result in a significant increase in risk of core damage.

The observations and documentation reviews were performed to verify that the activities

inspected were performed in accordance with the American Society of Mechanical

Engineers (ASME) Boiler and Pressure Vessel Code requirements.

The inspector reviewed the licensee's performance of a visual inspection (VT) of the Unit

1 reactor vessel closure head (RVCH) and the installed upper head penetrations. The

inspector reviewed the visual procedure, the qualifications of the personnel and

reviewed the inspection report documenting the inspection results. The inspector also

reviewed the data sheets for the penetrant tests completed on three of the penetration

welds of the RVCH.

The inspector reviewed records for ultrasonic testing (UT), visual testing (VT), penetrant

testing (PT) and magnetic particle testing (MT) NDE processes. PSEG did not perform

any radiographic testing (RT) during this outage. The inspector reviewed inspection

data sheets and documentation for these activities to verify the effectiveness of the

examiner, process, and equipment in identifying degradation of risk significant systems,

structures and components and to evaluate the activities for compliance with the

requirements of ASME Code,Section XI.

Enclosure

9

Steam Generator Inspection Activities

The inspectors reviewed a sample of the Unit 1 steam generator eddy current testing

(ECT) tube examinations, and applicable procedures for monitoring degradation of

steam generator tubes to verify that the steam generator examination activities were

performed in accordance with the rules and regulations of the steam generator

examination program, Salem Unit 1 steam generator examination guidelines, NRC

Generic Letters, 10CFR50, technical specifications for Unit 1, Nuclear Energy Institute

97-06, EPRI PWR steam generator examination guidelines, and the ASME Boiler and

Pressure Vessel Code Sections V and XI. The review also included the Salem Unit 1

steam generator degradation assessment and steam generator Cycle 21 and 22

operational assessment. The inspector also verified the individual certifications for

personnel participating in the SG ECT inspections during the 1 R20 refueling outage. The

inspector reviewed PSEG's efforts in identifying wear degradation to the tubing in the

four SGs at Unit 1. The majority of the identified wear indications were attributed to anti

vibration bar (AVB) wear in the u bend regions of the four SGs. The inspector reviewed

the analyses and evaluations that determined that a total of 14 SG tubes would be

removed from service by plugging.

Boric Acid Corrosion Control Program Activities

The inspector reviewed the PSEG boric acid corrosion control program. The resident

inspectors observed PSEG personnel performing boric acid walkdown inspections,

inside containment, and in other affected areas outside of containment, at the beginning

of the Unit 1 refueling outage. The inspectors reviewed the notifications generated by

the walkdowns and the evaluations conducted by Engineering to disposition the

notifications. Additionally, the inspector reviewed a sample of notifications and

corrective actions completed to repair the reported conditions.

Section XI Repair/Replacement Samples:

AFW System Piping. Control Air & Station Air: The inspectors reviewed PSEG's

discovery, reporting, evaluation and the repair/replacement of Unit 1 AFW piping that

was excavated for inspection during the April 2010 Unit 1 refueling outage (1R20).

PSEG conducted this inspection in accordance with PSEG's Buried Piping Inspection

Program. Additionally, the inspectors reviewed the UT testing results performed to

characterize the condition of the degraded Unit 1 buried AFW piping.

The inspector also reviewed the repair/replacement work orders and the 50.59 screening

and evaluation for the AFW, CA and SA piping. The inspectors reviewed the fabrication

of the replacement piping, reviewed the documentation of the welding and NDE of the

replacement piping and reviewed the pressure tests used to certify the replacement

piping. Additionally, the inspector reviewed the specified replacement coating, the

application of the replacement coating and the backfill of the excavated area after the

piping had been tested.

The inspector reviewed the finite element analysis (FEA) results from PSEG's past

operability analysis on the affected Unit 1 buried AFW piping completed by the licensee

Enclosure

10

in order to demonstrate past operability at a reduced system pressure of 1275 psig. The

design pressure of the AFW system is 1950 psig.

The inspector also reviewed the UT testing results (approximately 400) performed on

portions of the Unit 2 AFW buried piping, in response to the conditions observed on

Unit 1 AFW buried piping to determine if degradation existed on the Unit 2 buried AFW

piping.

Rejectable Indication Accepted For Service After Analysis:

The inspector reviewed the Notification and the UT data report of a rejectable wall

thickness measurement on the #11 SG feedwater elbow during 1R20. The inspector

reviewed the additional wall thickness data taken to further define the condition and

reviewed the finite element analysis (FEA) which verified that sufficient wall thickness

remained to operate the component until the next refueling outage when it will be

replaced.

b. Finding

Introduction. The inspector identified a Green non-cited violation (NCV) of 10 CFR

50.55a(g)(4) and the referenced American Society of Mechanical Engineers (ASME)

Code,Section XI, paragraph IWA-5244 for PSEG's failure to perform required pressure

tests of buried AFW components for Salem Unit 1.

Description. Portions of the Unit 1 and Unit 2 AFW system piping is buried piping and

has not been visually inspected since the plant began operation in 1977 for Unit 1 and

since 1979 for Salem Unit 2. This piping is safety related, 4.0" ID, ASME Class 3,

Seismic Class 1 piping. In April 2010, approximately 680 ft. (340 ft. of the #12 SG AFW

supply and 340 ft. of the #14 SG AFW supply) of piping between the pump discharge

manifold and the connection to the main feedwater piping to the affected SGs was

discovered to be corroded to below minimum wall thickness (0.278") for the 1950 psi

design pressure of the AFW System. The discovery was noted by PSEG during a

planned excavation implementing their buried pipe inspection program. The lowest wall

thickness measured in the affected piping was 0.077". The affected Unit 1 piping was

replaced. Although no leakage was evident as a result of the corrosion, the inspector

questioned PSEG about whether the IWA-5244 periodic pressure tests had been

conducted on this underground piping.

10 CFR 50.55(a)(g)(4)(ii) requires licensees to follow the in-service requirements of the

ASME Code,Section XI. Paragraph IWA-5244 of Section XI requires licensees to

perform system pressure tests on buried components to demonstrate the structural

integrity of the tested piping. The system pressure test required by IWA-5244 is

considered to be an inservice inspection and is part of Section XI.Section XI and IWA-

5244 do not specify other non-destructive examinations (NDE) on buried components to

demonstrate structural integrity other than a flow test if the system pressure test cannot

be performed. PSEG had not performed the required tests for Unit 1 since 1988. Thus,

PSEG did not perform the inservice inspection provided by the ASME Code,Section XI,

intended to demonstrate the structural integrity of this safety related buried piping.

Enclosure

11

PSEG was aware of the need to perform these required tests because they sought relief,

from the NRC, from the previous Code required pressure testing in 1988 for Unit 1 only.

Relief was granted to PSEG, by the NRC, to perform an alternate flow test in 1991 for

Unit 1. However, PSEG did not perform the proposed alternate flow tests for Unit 1

since 1988. Thus, PSEG had a chance to foresee and correct this performance

deficiency, but missed the opportunity at the time of processing the final results of the

relief request. PSEG replaced the affected Unit 1 buried piping during the refueling

outage in April/May 2010. The required pressure tests were successfully completed

after the replacement of the Unit 1 buried piping. PSEG determined that the buried

portions of AFW maintained structural integrity because the AFW system functioned as

required during the plant shutdown prior to the start of 1R20 (April 2010) and based

upon the results of a finite element analysis PSEG conducted using as-found UT

readings of excavated portions of the Unit 1 piping.

As part of the extent of condition for the testing issue identified on Unit 1, PSEG

reviewed the status of lSI testing for Unit 2 AFW and determined that the testing had not

been performed since 2001. PSEG currently plans to excavate the Unit 2 buried piping

for inspection during the Unit 2 refueling outage scheduled for the spring of 2011. PSEG

also completed an operability determination and risk assessment to justify continued

operation until the next refueling outage. These evaluations determined that the

condition was acceptable for continued operation until spring 2011. At present, it was

not feasible to conduct the system pressure test or alternate flow test while at power,

and to date there has been no detected degradation of the coating or piping on the Unit

2 buried AFW piping.

Analysis. Visual inspections and UT measurements completed by PSEG on Unit 1 AFW

buried piping in April 2010 identified degraded pipe coating and wall thinning on a

portion of the excavated pipe. Considering the effect of this identified degradation, not

performing the ASME Code,Section XI, paragraph IWA-5244 required pressure test at

the required frequency for this normally inaccessible buried piping would result in an

undetected loss of structural integrity for buried Unit 1 AFW discharge piping. The

inspectors determined this was a performance deficiency.

This performance deficiency was more than minor because, if left uncorrected, it would

have resulted in a more significant condition. Specifically, in light of the as-found

degraded conditions of the coating and the piping discovered during excavation in Unit

1, an undetected failure of the piping would have resulted due to further continued,

undetected corrosion, and continued pipe wall degradation eventually resulting in the

loss of structural integrity and inoperability of the Unit 1 AFW system.

The inspector screened this performance deficiency using IMC 0609, Attachment

0609.04, "Phase 1 Initial Screening and Characterization of Findings." This finding

impacts the Mitigating Systems cornerstone by adversely affecting the secondary, short

term decay heat removal capability. Because the finding was not a design or

qualification defiCiency, did not result in an actual loss of safety function, and was not

potentially risk significant for external events, the inspector determined that the finding

screened to Green, very low safety significance for Unit 1.

Enclosure

12

The inspector determined that a cross cutting aspect did not exist because the issue was

not indicative of current performance because the condition existed since 1991, more

than 3 years ago. Specifically, the failure to perform these pressure tests began in 1988

when PSEG requested relief from the requirement and did not incorporate the actions of

the relief into the plant inservice inspection program when it was granted in 1991.

Enforcement. 10 CFR 50.55a(g)(4) states, in part: "Throughout the service life of a

boiling or pressurized water-cooled nuclear power facility, components which are

classified as ASME Code Class 1, Class 2 and Class 3 must meet the requirements, set

forth in Section XI of editions of the ASME Boiler and Pressure Vessel Code".

Paragraph IWA-5244, Buried Components, of Section XI says, in part:

"(b) For buried components where a VT-2 visual examination cannot be

performed, the examination requirement is satisfied by the following: (1) The system

pressure test for buried components that are isolable by means of valves shall consist of

a test that determines the rate of pressure loss. Alternatively, the test may determine

the change in flow between the ends of the buried components. "

Contrary to these requirements, PSEG did not perform the required pressure tests of the

buried AFW piping to the #12 SG and #14 SG at Salem Unit 1. Specifically, from

February 1988 to April 2010 the required pressure tests were not performed to

demonstrate structural integrity on the affected buried Unit 1 AFW piping during the 2 nd

In Service Inspection Interval (2/27/88 to 5/19/01) and during the 1st (5/19/01 to 6/3/04)

and 2nd (6/24/04 to 5/20/08) periods of the 3'd In Service Inspection Interval (5/19/01 to

5/19/11 ).

Because PSEG entered this condition for Salem Unit 1 into the corrective action process

(Notification 20459686) and because it is of very low safety significance (Green), it is

being treated as a non-cited violation consistent with Section VI.A.1 of the NRC

Enforcement Policy. NCV 50-272/2010003-01, Buried AFW Discharge Piping Not

Tested In Accordance With 10 CFR 50.55a.

1R11 Licensed Operator Regualification Program (71111.11Q -1 sample)

.1 Regualification Activities Review by Resident Staff

a. Inspection Scope

The inspectors completed one quarterly licensed operator requalification program

inspection sample. Specifically, the inspectors observed a scenario administered to a

single crew during an emergency preparedness drill on May 18, 2010. The scenario

included a crane damaging the AFW storage tank, a small reactor coolant leak, a rod

ejection that resulted in a small break loss-of-coolant accident, and a rupture to

containment spray piping that resulted in a loss of containment integrity.

The inspectors reviewed operator implementation of the abnormal and emergency

operating procedures. The inspectors examined the operators' ability to perform actions

associated with high risk activities, the Emergency Plan, previous lessons learned items,

and the correct use and implementation of procedures. The inspectors observed and

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13

verified that deficiencies were adequately identified, discussed, and entered into the

CAP, as appropriate. Documents reviewed are listed in the Attachment A.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12Q - 3 samples)

a. Inspection Scope

The inspectors completed three quarterly maintenance effectiveness inspection

samples. The inspectors reviewed performance monitoring and maintenance

effectiveness issues for the three systems listed below. The inspectors reviewed

PSEG's process for monitoring equipment performance and assessing preventive

maintenance effectiveness. The inspectors verified that systems and components were

monitored in accordance with the Maintenance Rule Program requirements. The

inspectors compared documented functional failure determinations and unavailability

hours to those being tracked by PSEG to evaluate the effectiveness of PSEG's condition

monitoring activities and to determine whether performance goals were being met. The

inspectors reviewed applicable work orders, corrective action notifications, and

preventive maintenance tasks. The documents reviewed are listed in the Attachment A.

  • Unit 1 and Unit 2, radiation monitors;

b. Findings

Introduction: A self-revealing finding of very low safety significance was identified on

January 21, 2010, because a control system short circuit caused the 21 SGFP to trip.

This caused a turbine runback and ultimately an automatic Unit 2 reactor trip due to low

water level in one of four SGs. The short circuit occurred because technicians did not

use the correct procedure to repair degraded insulation on the barrel of a connector lug

that was identified in the 21 SGFP control system in November 2009. PSEG repaired

the short circuit prior to restart of Unit 2 on January 23, 2010. The issue was entered

into the corrective action program as notification 20448229.

Description: On January 21,2010, the 21 SGFP tripped due to a short circuit between

the normally closed and normally open terminals for the 21 SGFP low suction pressure

trip switch. The short circuit caused a false low suction pressure trip signal that tripped

the 21 SGFP, which caused a turbine run back to 66%. This run back was designed to

lower the steam flow demanded from the SGs to within the capacity of the SGFP that did

not trip. However, on January 21, the reduction in power was not rapid enough and

Salem Unit 2 automatically tripped from 78% power due to low steam generator water

level.

Following the trip technicians identified that the electrical short that caused the trip had

developed between a connector lug barrel and an adjacent wire terminal due degraded

Enclosure

14

wire insulation on the lug barrel. The technicians also determined that this same short

was previously identified as the cause of the difficulty that operators had resetting the 21

SGFP on November 11, 2009, during the Unit 2 startup after the S2R17 refueling

outage. To address the condition identified in November 2009, the technicians covered

the affected connector lug barrel with electrical tape. This allowed operators to restore

the 21 SGFP to service and continue the Unit 2 start-up. The reset problems for the 21

SGFP repeated again on January 5, 2010, during the Unit 2 plant startup after the

January 3, 2010 plant trip. However, troubleshooting in early January did not identify a

cause for the trip and the 21 SGFP was ultimately successfully reset and restored to

service with no corrective actions completed.

PSEG conducted a root cause investigation after the January 21,2010, trip and

determined the root cause was poor work practices during initial component installation

and subsequent maintenance activities. Specifically, improper orientation of the lug put

the lug barrel and wire terminal in contact with one another, which subsequently caused

the lug barrel insulation to degrade ultimately resulting in the short circuit.

The inspectors determined that the corrective actions taken by technicians when they

originally identified the short between the lug barrel and wire terminal in November 2009,

were not adequate. As stated above, to correct the short, technicians covered the

affected insulation with electrical tape. The inspectors reviewed PSEG procedure

SC.DE-TS.ZZ-2039, "Cable Termination Methods at Salem Generating Station," and

determined that applying tape to the barrels of lugs was not permitted. Therefore, the

corrective actions taken by technicians to address the degraded condition identified in

November 2009, did not meet PSEG procedure requirements and resulted in the

21 SGFP trip that cause the Unit 2 reactor trip on January 21,2010.

PSEGs corrective actions following the January 21, 2010 included performing extent of

condition inspections on the other Unit 2 SGFP panels for degraded insulation no other

deficiencies were identified. Following completion of the root cause analysis additional

extent of condition inspections for connector lug orientation were specified. Unit 1

inspections were completed in April 2010 and no deficiencies were identified. Unit 2

inspections are scheduled for the next refueling outage in 2011. PSEG entered

corrective action issues for this event into the corrective action program as NOTF

20448229.

To improve the reliability of the plant operations in response to a single SGFP trip,

PSEG installed an automatic plant run back feature in the 1990s. The inspectors

confirmed that this feature was not credited in the plant's accident analysis, and

therefore, determined that the failure of the runback to prevent a reactor trip after the 21

SGFP tripped on January 21 was not a safety concern. PSEG's plans to review the

causes of the ineffective runback as part of the response to correction action program

NOTF 20448229.

Analysis: Not performing repairs to the affected 21 SGFP pressure switch lug barrel in

accordance with PSEG SCDE-TS.ZZ-2039, "Cable Termination Methods at Salem

Generating Station," resulted in a short circuit that caused a 21 SGFP trip that resulted in

a Unit 2 reactor trip due to low SG water level. This was a performance deficiency. The

inspectors determined that the performance deficiency was more than minor because it

Enclosure

15

was associated with the human performance attribute of the Initiating Events

cornerstone, and it adversely affected the cornerstone objective to limit the likelihood of

events that upset plant stability and challenge critical safety functions. Specifically, not

following PSEG procedure SC.DE-TS.ZZ-2039 on November 11, 2009, caused the 21

SGFP trip and subsequent automatic reactor trip due to low SG water level on January

21, 2010. The finding was evaluated under IMC 0609, Attachment 4, "Phase 1 - Initial

Screening and Characterization of Findings." The inspectors determined that the finding

is of very low safety significance because it does not contribute to both the likelihood of a

reactor trip and the likelihood that mitigation equipment or functions will not be available.

The inspectors determined that this finding has a cross-cutting aspect in the area of

human performance because PSEG personnel did not follow procedure requirements

while repairing plant equipment. Specifically, technicians applied electrical tape to the

21 SGFP pressure switch connector lug barrel on November 11, 2009, which did not

meet PSEG procedure SC.DE-TS.ZZ-2039, "Cable Termination Methods at Salem

Generating Station," requirements. (HA (b))

Enforcement: Enforcement action does not apply because the performance deficiency

did not involve a violation of a regulatory requirement: FIN 05000311/2010003-02, 21

Steam Generator Feed Pump Trip.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 5 samples)

a. Inspection Scope

The inspectors completed five maintenance risk assessment and emergent work control

inspection samples. The inspectors reviewed the maintenance activities listed below to

verify that the appropriate risk assessments were performed as specified by 10 CFR

50.65(a)(4) prior to removing equipmentfor work. The inspectors reviewed the

applicable risk evaluations, work schedules, and control room logs for these

configurations. PSEG's risk management actions were reviewed during shift turnover

meetings, control room tours, and plant walkdowns. The inspectors also used PSEG's

on-line risk monito~(Equipment OOS workstation) to gain inSights into the risk

associated with these plant configurations. The inspectors reviewed notifications

documenting problems associated with risk assessments and emergent work

evaluations. Documents reviewed are listed in the Attachment A.

  • Unit 1 and Unit 2, planned unavailability of Unit 1 control room emergency air

conditioning system to support planned maintenance on the 1A 125 VDC electrical

bus on April 7;

  • Unit 1, planned unavailability of the 1A EDG and 14 station power transformer during

a RFO on April 8;

  • Unit 1, contingency measures to provide alternate power to the 12 spent fuel pool

(SFP) pump during unavailability of the 1B 4kV vital bus on April 12;

  • Unit 1, unplanned unavailability of the 1C 4kV vital bus concurrent with planned

unavailability of the 1B EDG and 11 SW header on April 16;

  • Unit 2, planned unavailability of the 2A EDG with station blackout Unit 3 out of

service on May 27.

Enclosure

16

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15 - 8 samples)

a. Inspection Scope

The inspectors completed eight operability evaluation inspection samples. The

inspectors reviewed the operability determinations for degraded or non-conforming

conditions associated with:

  • Unit 1 and Unit 2 EDGs given potential degradation of shutdown relays SDR, SR and

SRA;

  • Unit 1 boration flowpath following unplanned unavailability of the 1C 4kV vital bus

while in Mode 6;

  • Unit 1 SW system given early installation of restraints on pipe support SWPS-5;

of the 12NB CCW HX;

  • Unit 1 AFW piping following discovery of wall thinning of buried piping;
  • Unit 2 AFW piping following the discovery of wall thinning of Unit 1 AFW piping;
  • 22 SW 122 air operated valve (AOV) following the failure of the 21 SW 122 AOV;

and

  • 11 SW 122 AOV following the failure of the 21 SW 122 AOV.

The inspectors reviewed the technical adequacy of the operability determinations to

ensure the conclusions were justified. The inspectors also walked down accessible

equipment to corroborate the adequacy of PSEG's operability determinations.

Additionally, the inspectors reviewed other PSEG identified safety-related equipment

deficiencies during this report period and assessed the adequacy of their operability

screenings. Documents reviewed are listed in the Attachment A.

b. Findings

No findings of significance were identified.

1R18 Plant Modifications (71111.18 - 4 samples)

.1 Permanent Modifications

a. Inspection Scope

The inspectors completed two permanent plant modification inspection samples by

reviewing the key characteristics associated with the two permanent plant modifications

described below. The inspectors' review verified that the design bases, licensing bases,

and performance capability of the affected systems were not degraded by the

modifications. The inspectors verified the new configuration was accurately reflected in

the design documentation and that the post-modification testing was adequate to ensure

the structures, systems, and components affected would continue to function properly.

Enclosure

17

The inspectors' also interviewed plant staff and reviewed issues that were entered into

the GAP to assess whether PSEG was effective at identifying and resolving problems

associated with the modification process. The 10 GFR 50.59 screening associated with

these permanent plant modifications were also reviewed. The documents reviewed are

listed in the Attachment A.

  • The inspectors reviewed the modification package used to replace the section of

buried Unit 1 AFW discharge header piping located between the Unit 1 auxiliary and

containment buildings. PSEG replaced this section of piping because significant

coating degradation and external corrosion and wall thinning was identified on the

piping during inspections conducted in preparation for license renewal.

  • The inspectors reviewed the modification package used to replace the Unit 1 PS-1

pressurizer spray valve internals. The purpose of the new design was to provide

better flow control characteristics and reduce the valve's susceptibility to sticking.

b. Findings

No findings of significance were identified .

.2 Temporarv Modifications

a. Inspection Scope

The inspectors completed two plant modification inspection samples by reviewing the

key characteristics associated with the two temporary plant modifications described

below. The inspectors verified that the design bases, licensing bases, and performance

capability of the affected systems were not degraded by the temporary modifications.

The 10 GFR 50.59 screen associated with each modification were also reviewed.

Documents reviewed for this inspection are listed in the Attachment A.

  • The inspectors reviewed the modification package used to supply temporary power

to the 12 SFP pump. The modification moved the 12 SFP pump power supply from

the 1 B 460 VAG vital bus to the 1A 460 VAG vital bus to provide SFP cooling

capacity from both the 11 and 12 SFP pumps while the 1B 460 VAG vital bus was

de-energized for planned maintenance.

  • The inspectors reviewed the modification package used to plug a Unit 1 feedwater

flow control valve (13BF19) air supply regulator weep hole in order to ensure that full

pressure was used to position the air-operated valve.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19 - 6 samples)

a. Inspection Scope

The inspectors completed six post-maintenance testing (PMT) inspection samples. The

inspectors observed portions of and/or reviewed the PMT results for the maintenance

Enclosure

18

activities listed below. The inspectors verified that the effect of testing on the plant was

adequately addressed by control room and engineering personnel; testing was adequate

for the maintenance performed; acceptance criteria were clear, demonstrated

operational readiness and were consistent with design and licensing basis

documentation; test instrumentation calibration was current and the appropriate range

and accuracy for the application; tests were performed, as written, with applicable

prerequisites satisfied; and equipment was returned to an operational status and ready

to perform its safety function. Documents reviewed are listed in the Attachment A.

  • Work order (WO) 30156599, preventive maintenance of the 1A vital instrument bus

inverter;

122;

122;

  • WO 60088790, temporary repair of an oil leak on 21 SI pump outboard bearing.

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)

a. Inspection Scope

Unit 1 RFO (S1 R20). The inspectors completed one refueling outage activity inspection

sample. The inspectors observed or reviewed the following RFO activities to verify that

operability requirements were met and that risk, industry experience, the fatigue rule,

and previous site specific problems were considered. Documents reviewed are listed in

the Attachment A.

The inspectors reviewed the schedule and risk assessment documents associated with

S1 R20 to confirm that PSEG appropriately considered risk, operating experience, and

site specific problems in developing and implementing a plan that ensured maintenance

of defense-in-depth systems and barriers. Prior to S1 R20, the inspectors reviewed

PSEG's outage risk assessment to identify risk significant equipment configurations and

determine whether planned risk management actions were adequate. During S1 R20,

the inspectors verified that PSEG managed the outage risk in accordance with the

outage plan.

The inspectors observed portions of the shutdown and cool down processes and

monitored PSEG controls over the outage activities. The inspectors also verified that

cool down rates were within technical specification (TS) limitations. The inspectors

entered containment at the start of the refuel outage to check for evidence of previously

unidentified reactor coolant leakage. Throughout S1 R20, the inspectors made additional

containment entries to inspect for indications of unidentified leakage, damaged

equipment, foreign material control, radiation worker work practices and fire prevention.

Enciosure

19

The inspectors observed portions of refueling activities from the refueling bridge in

containment and the SFP to verify refueling gates and seals were properly installed and

verify that foreign material exclusion boundaries were established around the reactor

cavity. Core offload and core reload activities were periodically observed from the

control room and refueling bridge to verify operators adequately controlled fuel

movements in accordance with approved procedures.

The inspectors verified that tagged equipment was properly controlled and equipment

configured to safely support maintenance work. Specifically, inspectors observed the

control of work activities in the auxiliary building during reduced inventory to verify that

the risk of unplanned equipment unavailability was minimized. Equipment work areas

were periodically observed to determine whether foreign material exclusion boundaries

were adequate.

During control room tours, the inspectors verified that operators maintained adequate

reactor coolant system (RCS) level and temperature and that indications were within the

expected range for the operating mode.

The inspectors verified that offsite and onsite electrical power sources were maintained

in accordance with TS requirements and consistent with the outage risk assessment.

Periodic walk downs of portions of the on-site electrical buses and the EDGs were

conducted during risk significant electrical configurations.

The inspectors verified through routine plant status activities that the decay heat removal

safety function was maintained with the appropriate redundancy as required by TS and

consistent with PSEG's outage risk assessment. During core offload, the inspectors

periodically verified that the fuel pool cooling system was performing in accordance with

plant design parameters and consistent with PSEG's risk assessment for the RFO.

The inspectors observed the Unit 1 RCS draining to a reduced inventory condition on

April 19, 2010. RCS inventory controls and contingency plans were reviewed by

inspectors to verify that they met TS requirements and provided for adequate inventory

control. The inspectors reviewed procedures and observed portions of activities in the

control room when the unit was in reduced inventory modes of operation. The

inspectors verified that level and core temperature measurement instrumentation were

installed and operational. Calculations that provided time to boil information were also

reviewed for RCS reduced inventory conditions as well as the SFP during increased

heat load conditions.

Inspectors verified that PSEG managed fatigue of outage workers by reviewing a

sampling of waiver requests, self declarations, and fatigue assessments that were

available near the end of the RFO. PSEG scheduled covered workers such that

minimum days off for individuals working on outage activities were in compliance with

the fatigue rule. In addition, control room staff for Unit 2 remained on operating unit work

hour controls.

Containment status and procedural controls were reviewed by the inspectors during fuel

offload and reload activities to verify that TS and procedure requirements were met for

containment. Specifically, the inspectors verified that during fuel movement activities,

Enclosure

20

personnel, materials, and equipment were staged to close containment penetrations as

specified in the licensing basis.

The inspectors conducted a thorough walk down of containment prior to reactor startup.

Areas of containment where work was completed were inspected for evidence of

leakage and to ensure debris that could block containment sump screens was removed.

The condition of equipment used for fire detection, prevention, and suppression were

inspected for operability and functionality. Portions of mode changes and reactor startup

were observed and reviewed for compliance with applicable procedures and TS.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22 - 9 samples)

a. Inspection Scope

The inspectors completed nine surveillance testing inspection samples. The inspectors

observed portions of and/or reviewed results for the surveillance tests listed below to

verify, as appropriate, whether the applicable system requirements for operability were

adequately incorporated into the procedures and that test acceptance criteria were

consistent with procedure requirements, the TS requirements, the updated final safety

analysis report (UFSAR), and American Society of Mechanical Engineers (ASME)

Section XI for pump and valve testing. Documents reviewed are listed in the Attachment

A.

  • S1.0P-ST.MS-0003, Steam Line Isolation and Response Time Testing;
  • S1.0P-ST.TRB-0002, Turbine Protection System - Full Functional Test;
  • S1.0P-ST.SJ-0015, Intermediate Head Hot Leg Throttling Valve Flow Balance

Verification;

Switches;

  • S1.0P-ST.AF-0007, 13 AFW Pump Full Flow Test;
  • S2.0P-ST.SJ-0001, Inservice Testing of 21 Safety Injection Pump;
  • S1.0P-LR.FP-0001, Type C Leak Rate Test for 1FP147 and 1FP148; and
  • S1.0P-LR.CVC-0003, Type C Leak Rate Testfor 1CV116, 1CV284, and 1CV296.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06 - 1 sample)

a. Inspection Scope

The inspectors completed one drill evaluation inspection sample. On May 18, 2010, the

inspectors observed a drill from the control room simulator during an evaluated

Enclosure

21

emergency preparedness drill. The inspectors evaluated operator performance relative

to developing event classifications and notifications. The inspectors referenced Nuclear

Energy Institute (NEI) 99-02, "Regulatory Assessment Performance Indicator (PI)

Guideline," Revision 6, and verified that PSEG correctly counted the evaluated

scenario's contribution to the NRC PI for drill and exercise performance.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Radiation Safety - Public and Occupational

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

a. Inspection Scope

Radiological Hazard Assessment

The inspectors reviewed any changes to plant operations that may result in a significant

new radiological hazard for onsite workers or members of the public. The inspectors

verified PSEG had assessed the potential impact of these changes and implemented

periodic monitoring, as appropriate, to detect and quantify the radiological hazard.

The inspectors reviewed a sample of two completed radiological surveys of selected

plant areas. The inspectors verified that the thoroughness and frequency of the surveys

were appropriate for the given radiological hazard.

The inspectors conducted walk downs of the plant that included radioactive waste

processing, storage, and handling areas to evaluate material conditions and potential

radiological conditions.

The inspectors selected radiological risk-significant work activities that involved

exposure to radiation and were performed during Unit 1's RFO. Activities selected

included: primary steam generator work including eddy current testing, secondary steam

generator work including foreign object search and retrieval, and replacement of the #14

reactor coolant pump motor. The inspectors verified that appropriate pre-work surveys

were performed and were appropriate to identify and quantify the radiological hazard

and to establish adequate protective measures. The inspectors evaluated the

radiological survey program to determine if the following hazards were properly

identified:

  • Identification of hot particles;
  • The presence of alpha emitters;
  • The potential for airborne radioactive materials, including the potential

presence of transuranics and/or other hard-to-detect radioactive materials;

  • The hazards associated with work activities that could suddenly and severely

increase radiological conditions; and

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22

  • Severe radiation field dose gradients that can result in non-uniform exposures

to the body.

The inspectors selected three to five air sample survey records and verified that samples

were collected and counted in accordance with PSEG procedures. The inspectors

observed work in potential airborne areas and verified that air samples were

representative of the breathing air zone. The inspectors verified that PSEG has a

program for monitoring levels of loose surface contamination in areas of the plant with

the potential for the contamination to become airborne.

Radiological Hazards Control and Work Coverage

During tours of the facility and review of ongoing work selected in Section 2 (above), the

inspectors evaluated ambient radiological conditions. The inspectors verified that

existing conditions were consistent with posted surveys, radiation work permits (RWPs),

and worker briefings, as applicable.

During job performance observations, the inspectors verified the adequacy of

radiological controls, such as required surveys, radiation protection job coverage, and

contamination controls. The inspectors evaluated PSEG's means of using electronic

pocket dosimeters in high noise areas as high radiation area (HRA) monitoring devices.

The inspectors verified that radiation monitoring devices were placed on the

individual's body consistent with the method that PSEG has employed to

monitor dose from external radiation sources. The inspectors verified that the dosimeter

was placed in the location of highest expected dose or that PSEG was properly

employing an NRC-approved method of determining effective dose equivalent.

For high-radiation work areas with significant dose rate gradients (a factor of 5 or

more), the inspectors reviewed the application of dosimetry to effectively monitor

exposure to personnel. The inspectors verified that PSEG's controls were adequate.

The inspectors reviewed three to five RWPs for work within airborne radioactivity areas

with the potential for individual worker internal exposures. The inspectors evaluated

airborne radioactive controls and monitoring, including potentials for significant airborne

contamination. For these selected airborne radioactive material areas, the inspectors

verified barrier integrity and temporary high-efficiency particulate air ventilation system

operation.

The inspectors examined PSEG's physical and programmatic controls for highly

activated or contaminated materials stored within spent fuel and other storage pools.

The inspectors verified that appropriate controls were in place to preclude inadvertent

removal of these materials from the pool.

The inspectors conducted selective inspection of posting and physical controls for HRAs

and very high radiation areas, to the extent necessary to verify conformance with the

Occupational PI.

Enclosure

23

b. Findings

No findings of significance were identified.

2RS2 Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls

(71124.02)

a. Inspection Scope

Radiological Work Planning

The inspectors obtained from PSEG a list of work activities ranked by actual or

estimated exposure that were in progress and selected three work activities of the

highest exposure significance (listed in Section 2RS1 above).

The inspectors reviewed the ALARA work activity evaluations, exposure estimates, and

exposure mitigation requirements. The inspectors determined that PSEG had

reasonably grouped the radiological work into work activities, based on historical

precedence, industry norms, and/or special circumstances.

The inspectors verified that PSEG's planning identified appropriate dose mitigation

features, considered alternate mitigation features, and defined reasonable dose goals.

The inspectors verified that PSEG's ALARA assessment had taken into account

decreased worker efficiency from use of respiratory protective devices and or heat stress

mitigation equipment. The inspectors determined that PSEG's work planning considered

the use of remote technologies as a means to reduce dose and the use of dose

reduction insights from industry operating experience and plant-specific lessons learned.

The inspectors verified the integration of ALARA requirements into work procedure and

RWP documents.

The inspectors compared the results achieved with the intended dose established in

PSEG's ALARA planning for these work activities. The inspectors compared the person-

hour estimates provided by maintenance planning and other groups to the radiation

protection group with the actual work activity time requirements, and evaluated the

accuracy of these time estimates. The inspectors determined the reasons for any

inconsistencies between intended and actual work activity doses. The inspectors

focused on those work activities with planned or accrued exposure greater than 5

person-rem.

The inspectors determined that post-job reviews were performed and that identified

problems were entered into PSEG's CAP.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

40A 1 Performance Indicator (PI) Verification (71151 - 6 samples)

Enclosure

24

a. Inspection Scope

The inspectors reviewed PSEG submittals for the Unit 1 and Unit 2 initiating events

cornerstone performance indicators discussed below. To verify the accuracy of the PI

data reported during this period the data was compared to the PI definition and guidance

contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline,"

Revision 5.

Cornerstone: Initiating Events

  • Unit 1 and Unit 2 unplanned scrams;
  • Unit 1 and Unit 2 unplanned scrams with complications; and

The inspectors verified the accuracy of the data by comparing it to CAP records, control

room operators' logs, the site operating history database, and key performance indicator

summary records.

b. Findings

No findings of significance were identified.

40A2 Identification and Resolution of Problems (71152 - 1 annual sample; 1 trend sample)

.1 Review of Items Entered into the Corrective Action Program

As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"

and in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a daily screening of all items entered into

PSEG's CAP. This was accomplished by reviewing the description of each new

notification and attending daily management review committee meetings. Documents

reviewed are listed in the Attachment A.

.2 Semi-Annual Review to Identify Trends

a. Inspection Scope

As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"

the inspectors performed a review of PSEG's CAP and associated documents to identify

trends that could indicate the existence of a more significant"safety issue. The

inspectors' review was focused on repetitive equipment and corrective maintenance

issues, but also considered the results of daily inspector CAP item screening discussed

in Section 40A2.1. The review included issues documented in system health reports,

corrective maintenance WOs, component status reports, site monthly meeting reports

and maintenance rule assessments. The inspectors' review nominally considered the

six-month period of December 2009 through May 2010, although some examples

expanded beyond those dates when the scope of the trend warranted. The inspectors

compared and contrasted their results with the results contained in PSEG's latest

integrated quarterly assessment report. Corrective actions associated with a sample of

Enclosure

25

the issues identified in PSEG's trend report were reviewed for adequacy. The inspectors

also evaluated the trend report specified in SPP-3.1, Corrective Action Program.

Documents reviewed are listed in the Attachment A.

b. Assessment and Observations

No findings of significance were identified.

The inspectors noted a trend of low level issues entered into the CAP related to

equipment reliability. There were multiple issues with service water flow control valves

and issues with the Unit 1 steam generator flow control regulating valves. The

inspectors also noted deficiencies with the scope, planning, and implementation of long

term equipment preventive maintenance. Some of the preventive maintenance

deficiencies have been corrected through implementation of a performance centered

maintenance plan. PSEG is aware of the issues identified through this trend review and

is appropriately addressing these issues .

.3 Annual Sample: Transformer Load Tap Changer Failures

a. Inspection Scope

The inspectors reviewed PSEG's actions to investigate and identify the cause of the 12

station power transformer load tap changer failure that resulted in a reactor trip on

December 28, 2007. The inspectors also reviewed PSEG's action towards identification

and completion of corrective actions. The inspectors reviewed PSEG's procedures,

vendor documents, notifications, orders, corrective actions, and root cause evaluations

to understand the equipment functions and operational history, as well as the

identification, evaluation, and corrective actions associated with the load tap changer

failures. System engineers and other PSEG staff were interviewed to gain additional

insights on the failures. Documents reviewed are listed in the Attachment A.

b. Findings and Observations

No findings of significance were identified.

The inspectors found that PSEG appropriately identified degraded conditions associated

with load tap changer failures and entered them into the CAP. PSEG's root cause

investigation determined the cause of the load tap changer failure to be inadequate

scope of maintenance procedures on load tap changer internal components and

insufficient performance monitoring of degraded load tap changer conditions. The

investigations revealed severe coking of the selector switch components, Which included

damage to four of the six collector rings, and melted contacts. Inspectors determined

that the evaluations of degraded conditions were thorough and included considerations

for extent of condition. The inspectors reviewed PSEG's corrective actions and

determined that they were appropriate to adequately address identified deficiencies.

40A3 Event Follow-up (71153 - 1 sample)

.1 (Closed) LER 05000311/2010-002-01, Automatic Reactor

Enclosure

26

Trip Due to 21 Steam Generator Feedwater Pump (SGFP) Trip and Steam Generator

Low Level

On January 21, 2010, at 1818 hours0.021 days <br />0.505 hours <br />0.00301 weeks <br />6.91749e-4 months <br />, the 21 SGFP tripped. A turbine runback

automatically initiated as expected and steam generator level in all four steam

generators (SG) lowered. The 22 SG reached the SG low level reactor trip setpoint at

1820 hours0.0211 days <br />0.506 hours <br />0.00301 weeks <br />6.9251e-4 months <br /> resulting in an automatic reactor trip. The turbine runback function initiated

by the loss of 21 SGFP did not prevent a reactor trip as designed; however, this feature

was not credited in the Salem accident analysis and, therefore, was not required to

operate to maintain plant safety. All control rods fully inserted on the trip. All three

AFW pumps started in response to the low SG water level and decay heat was removed

by the steam dumps to the main condenser. Operators entered the emergency

procedures for the plant trip and stabilized the plant in Mode 3.

The cause of the 21 SGFP trip was an internal wiring short in the SGFP control circuit

that resulted in a false low suction pressure trip signal. The cause for the wiring short

was the result of poor work practices. Corrective actions consist of lug inspections,

document changes, training analysis, and evaluation of the integrated plant response to

a SGFP from full power and implementing changes as appropriate. The inspectors

completed a review of this LER and identified one finding of very low safety significance

as documented in Section 1 R12. This LER is closed.

b. Findings

The finding for this event is documented in Section 1R12.

40A5 Temporarv Instruction (TI) 2515/172

a. Inspection Scope

The Temporary Instruction (TI), 2515/172 provides for confirmation that owners of

pressurized-water reactors (PWRs) have implemented the industry guidelines of the

Materials Reliability Program (MRP) -139 regarding nondestructive examination and

evaluation of certain dissimilar metal welds in the RCS containing nickel based Alloys

600/82/182.

During 1R20 PSEG inspected the dissimilar metal weld on the 1" reactor vessel drain

piping with no detected indications. Salem Unit 1 has dissimilar metal welds in the eight

reactor coolant system piping to reactor vessel nozzle safe end welds. No additional

inspections or MSIP applications were performed during 1R20.

This TI requires documentation of specific questions in an inspection report. The

questions and responses are included in this report as Attachment B. I*

I

b. Findings

No findings of significance were identified.

Enclosure

27

40A6 Meetings, Including Exit

The inspectors presented the inspection results to Mr. C. Fricker and other members of

PSEG management at the conclusion of the inspection on July 8, 2010. The inspectors

asked PSEG whether any materials examined during the inspection were proprietary.

No proprietary information was identified.

40A7 Licensee Identified Violations

The following violation of NRC requirements was identified by PSEG. It was determined

to have very low significance (Green) and to meet the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as a non-cited violation.

PSEG identified general corrosion that reduced the wall thickness of the safety related

piping to less than the design minimum wall thickness of 0.278" for the system design

pressure of 1950 psig. The lowest measured wall thickness was 0.077"; however, a

finite element analysis for the degraded piping demonstrated past operability at a

reduced operating pressure of 1275 psig.

10 CFR 50, Appendix B, Criterion III, Design Control requires in part that measures shall

be established to assure that applicable regulatory requirements and design bases are

correctly translated into specifications, drawings, and instructions and that these

measures shall include provisions to assure the proper selection and review for

suitability of application of materials, parts, equipment, and processes. During pipe

excavation and inspections conducted as part of PSEGs buried piping program PSEG

identified that it did not provide an effective protective coating for the buried section of

AFW piping on Unit 1.

This finding was associated with the mitigating systems cornerstone, specifically the

short term decay heat removal capability. The finding was determined to be Green

because it was a design or qualification deficiency that was confirmed not to result in

loss of operability of the AFW system. PSEG entered this condition into the corrective

action program as notification 20456999.

ATTACHMENT A: SUPPLEMENTAL INFORMATION

ATTACHMENT B: T1172 MSIP DOCUMENTATION QUESTIONS SALEM UNIT 1

Enclosure

A-1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel:

C. Fricker, Site Vice President

E. Eilola, Plant Manager

L. Rajkowski, Engineering Director

R. DeSanctis, Maintenance Director

J. Garecht, Operations Director

R. Gary, Radiation Protection Manager

J. Higgins, System Engineer

F. Hummel, System Engineer

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened/Closed

05000272/2010003-01 NCV Buried AFW Discharge Piping Not Tested In

Accordance With 10 CFR 50.55a

(Section 1 R08)05000311/2010003-02 FIN 21 Steam Generator Feed Pump Trip.

(Section 1R12)

Closed

05000311/2010-002-01 LER Automatic Reactor Trip Due to 21 SGFP

Trip and Steam Generator Low Level

(Section 40A3.2)

LIST OF DOCUMENTS REVIEWED

In addition to the documents identified in the body of this report, the inspectors reviewed the

following documents and records:

Section 1R01: Adverse Weather Protection

Procedures

SC.OP-AB.ZZ-0001 (0), Adverse Environmental Conditions, Revision 12

SC.OP-PT.ZZ-0002(0), Station Preparations for Seasonal Conditions, Revision 11

Notifications

20377404 20415043 20437093 20437117 20446050 20449579

20465389

Attachment A

A-2

Orders

30120734 30180434 60053920 60081317 60081770 60083588

60083540 60083588 60087645 60087770 60088526 60089636

60090176

Other Documents

2010 Salem Summer Seasonal Readiness Affirmation

WC-AA-107, Seasonal Readiness, Revision 10

Section 1R04: Equipment Alignment

Procedures

S1.0P-SO.CC-0002, 11 & 12 Component Cooling Heat Exchanger Operation, Revision 26

S1.0P-SO.SW-0002, 11 Nuclear Service Water Header Outage, Revision 26

S1.0P-ST.ZZ-0004 (a), 92 Day Locked Valve Verification, Revision 3

S2.0P-SO.DG-0005, Preparation for Removing a Diesel Generator from Service, Revision 5

S2.0P-SO.SW-0005, Service Water System Operation, Revision 40

Drawings

224342 207482 207483 205236 AF-1-2B AF-1-3A

AF-1-2A 205234

Notifications

20458147 20458148 20468758

Other Documents

Tagging Work List 4263810, 12 SW HDR Hardening (11 OUTAGE) 1R20, 04/12/2010 @ 22:09

Section 1R05: Fire Protection

Procedures

FRS-II-433, Salem - Unit 1 (Unit 2) Pre-fire Plan, Auxiliary Feed Water Pumps Area Elevation

84'-0", Revision 6

FRS-II-435, Salem - Unit 1 (Unit 2) Pre-fire Plan, Diesel Fuel Oil Storage Area Elevation 84'-0",

Revision 5

FRS-II-511, Salem - Unit 1 (Unit 2) Pre-fire Plan, Electrical Penetration Area Elevation 78'-0",

Revision 5

Section 1 R07: Heat Sink Performance

Procedures

ER-AA-340, GL 89-13 Program Implementing Procedure, Revision 4

ER-AA-340-1001, GL 89-13 Program Implementing Instructional Guide, Revision 6

ER-AA-340-1003, GL 89-13 Program Pis, Revision 2

Attachment A

A-3

Section 1 ROB: I nservice Inspection

Notifications:

20457869, Control Air Piping Leak'

20462034, Basis AFW Discharge Line Design Pressure'

20461785, Untimely retrieval of Design Documents'

20461255, U2 Containment Liner Blisters'

20459259, U2 Containment Liner Blisters'

20459689, failure to do IWA-5244 pressure tests'

20456999, Guided Wave (GW) pipe wall loss 20% to 44%', in Equipment Apparent Cause

Evaluation (EQ;ACE) Charter

20457854, see Equipment Apparent Cause Evaluation (EQ: ACE) Charter

20457869, Air Line Leak, in Equipment Apparent Cause Evaluation EQ: ACE Charter

20458147, see Equipment Apparent Cause Evaluation (EQ: ACE) Charter

20458148, see Equipment Apparent Cause Evaluation (EQ: ACE) Charter

20458568, see Equipment Apparent Cause Evaluation (EQ: ACE) Charter

20458554, 11 CA HDR Line In Fuel Xfer Area Degraded'

20458761, 1R20 CA Buried Pipe Coating Repair'

20458925, 1R20 SA Buried Pipe Coating Repair'

20457262, (88) 1R20 AF Buried Pipe Inspection Results'

20460624, Need Heat Trace on AF lines in FFT Area

20457877, U1 Containment Liner Corrosion at 78' EI.'

20459259, U1 Corrosion on Containment Liner'

20459303, #14 AF pipe damaged penetration seal'

20459304, #12 AF pipe damaged penetration seal'

20459454, Request for Additional UT Data, 4/18/10 (due to 0.077" reading)'

20344017, Inspect steel liner in 1R19

20235636, NRC noted water running down containment wall

20459189, Question on location of RFO-14 location of a PZR shell weld

20290560, Replace section of 15B FWH shell-S1-R18

20457879, (184) 1R20 FAC(N18) 14# elbow below Tmin

20456828, (66) valve has visible boron buildup 1R20

20459232, Heavy Dry White Boron Vlv Packing (1R20)

20456834, Heavy Dry White Boron Vlv Packing (1 R20)

20456840, Medium Dry White Boron Vlv Packing (1 R20)

20456839, Medium Dry White Boron Vlv Packing (1 R20)

20389147, Recordable lSI Indications on CVC Tank

20344017, Inspect Steel Liner in 1R19 @ Containment Sump

20235636, NRC Noted Water Running Down Containment Wall

20392631, ARMA From lSI Program Audit 2008

20460624, Need Heat Trace on AF lines in FTT Area

20333050, Response to NRC NOV EA-07-149

20322039, 2 nd Interval lSI NRC Violation

20397518, A1CVC-1CV180 Chk Vlv Stuck Open - PI&R review

20444514, Boric Acid Leak from Drain Line - PI&R review

20445314, boron leak - PI&R review

20448241, Minor Packing Leak - BAC - PI&R review

20435861, 21SJ313 Has Boric Acid Leakage - PI&R review

20417331, Boric Acid Leak at 11 CV156 - PI&R review

20411151, Tubing leak on 1SS653 - PI&R review

Attachment A

A-4

20414343, 12 Charging Pump seal inj. Line - PI&R review

20395346, 12 Bat PP Seal Leak - PI&R review

20450330, Containment Liner Corrosion - PI&R review

20385733, Severe Corrosion on FP Valve - PI&R review

20438320, (217) Op Eval. Of Containment Corrosion - PI&R review

20387897, Significant outlet pipe corrosion - PI&R review

20397225, MIC Corrosion Causing Through Wall Leak - PI&R review

20436836, Repair Cracks in Battery Cells - PI&R review

20392145, Update U1 lSI Relief Request Book - PI&R review

20449447, Update Salem Unit 1 ISI10 Yr Plan - PI&R review

20449744, Update Salem Unit 1 Containment lSI 10 Yr Plan - PI&R review

20449442, Update Salem Unit 2 Containment ISI10 Yr Plan - PI&R review

20449554, Salem U2 RF018 lSI Scope - PI&R review

20416605, INPO PSIRV Alloy 600 Program - PI&R review

20404057, Unit 2 lSI (MSIP) - PI&R review

20392631, ARMA FROM lSI PROGRAM AUDIT 2008 - PI&R review

20388065, Water leaking in decon room - PI&R review

20439023, 23 CFCU Head Leakage - PI&R review

20439022, SW Header Leakage 23 CFCU - PI&R review

20389148, 1R19 lSI Weld Exam Limitations - PI&R review

20416605, INPO PSIRV Alloy 600 Program - PI&R review

20449442, Update Salem 2 Containment ISI10 yr. Plan - PI&R review

20449554, Salem Unit 2 RF018 lSI Scope - PI&R review

20449747, Update Salem 2 lSI 10 Yr. Plan - PI&R review

20401542, Perform lSI BMV Exam on RPV Upper Head - PI&R review

20449063, SA U1 Service Inspec - lSI & U1 TI 2515 - PI&R review

20389147, Recordable lSI Indications on CVC Tank - PI&R review

20392145, Update U1 lSI Relief Request Book - PI&R review

20449744, Update Salem U1 Containment ISI10 Yr. Plan - PI&R review

20409943, NRC RIS 2009-04 SG Tube Insp Rqmts - PI&R review

20459851,Section XI Exams Limited to 90% or Less - PI&R review

20450520, Recoat Affected Areas of Liner 2R18 - PI&R review

20457388, Excavation Issues - PI&R review

'Denotes this Notification was generated as a result of this inspection

Section XI Repair/Replacement Samples:

W.O. 60079414, 14" carbon Steel Elbow FAC indication below minimum wall

W.O. 60084266, Salem U1 AF Buried Piping Inspection

W.O. 60089561, 80101381: Replace Aux FW U/G Piping

W.O. 60064104, Repair 15B FWH Area

W.O. 60084375, BACC Program repair to 1PS1

W.O. 60089612, BACC Program repair to S1CVC-14CV392

W.O. 60089615, BACC Program repair to S1 SJ-13SJ25

W.O. 60089848, 80101382 Advanced Work Authorization #2 FDA Replace Aux. Feedwater

Pipe

W.O. 60089561,80101381 Advanced Work Authorization - Replace Aux. FW U/G Piping,

4/9/10

Attachment A

A-5

Non-Code Repair

W.O. 60089848, Repair Non-nuclear, safety related CA Pipe, Unit 1 FTTA

W.O. 60089757, Test Non-nuclear, safety related CA Pipe Repair, Unit 1 FTTA

Miscellaneous Work Orders:

W.O. 60089917, Penetrations for CA & SA Lines, 4/23/10

W.O. 941017262, Activity 04, Excavate and Examine Auxiliary Feedwater Piping, Unit 2,12/94

W.O. 941017262, Activity 03, Excavate and Examine Auxiliary Feedwater Piping, Unit 2,12/94

W.O. 941017262, Activity 02, Excavate and Examine Auxiliary Feedwater Piping, Unit 2, 12/94

W.O. 941017262, Activity 01, Excavate and Examine Auxiliary Feedwater Piping, Unit 2, 12/94

W.O. 60089561, Flush New AFW piping 12 and 14

Drawings & Sketches:

205236A8761-54, Salem Nuclear Generating Station, Unit No.1, Auxiliary Feedwater

Salem Unit 1 Aux Feed Piping, Allan Johnson, 4/10/10

80101381RO, Buried Pipe, Replaced AFW Piping Arrangement

207483A8923-11, Salem Nuclear Generating Station, Unit No.1 - Reactor Containment

Auxiliary Feedwater, Plans & Sections - Elev. 78' 10" & 100' 0", Mechanical

Arrangement, Revision 8, 9/31/86

207483A8923-28, Sheet 1 of 4, Salem Nuclear Generating Station, Unit No.1 - Reactor

Containment Auxiliary Feedwater, Plans & Sections - Elev. 84',Mechanical

Arrangement, Revision 8, 9/31/86

207483A8923-31, Sheet 2 of 4, Salem Nuclear Generating Station, Unit No.1 - Reactor

Containment Auxiliary Feedwater, Plans & Sections - Elev. 84', Mechanical

Arrangement, Revision 8, 9/31/86

207483A8923-28, Sheet 3 of 4, Salem Nuclear Generating Station, Unit No.1 - Reactor

Containment Auxiliary Feedwater, Plans & Sections - Elev. 84',Mechanical

Arrangement, Revision 8, 9/31/86

207483A8923-30, Salem Nuclear Generating Station, Unit No.1 - Reactor

Containment Auxiliary Feedwater, Plans & Sections - Elev. 84',Mechanical

Arrangement, Revision 8, 9/31/86

20761 OA8896-12, Salem Nuclear Generating Station, Unit No.1 - Auxiliary Building & Reactor

Containment Compressed Air Piping, Aux. Building EI. 84 East & React. Contain. EI. 78,

Mechanical Arrangement, Revision 8, 9/31/86

Design Change Packages/Equivalent Change Packaqes

80101382, Revision 2, Replace Salem Unit 1 AFW Piping from the Unit Mechanical Penetration

Area EI. 78'-0" to the Unit 1 Fuel Transfer Tube Area EI. 100'-0"

80101381, Revision 1, Replace in-kind the Salem Unit 1 AF Piping that runs underground from

the Unit 1 Fuel Transfer Tube Area to the Unit 1 Main Steam Outer Penetration Area

50.59 Applicability Reviews, Screenings & Evaluations

80101382; Salem Unit 1 12/14 AF Piping Reroute; 4/24/10

Attachment A

A-6

System & Program Health Reports & Self-Assessments:

Salem Boric Acid Corrosion Control Program Focused Area Self-Assessment, 1/2010

70106830, Salem S1R20 NRC lSI Inspection Check-In Self Assessment

70095327, Salem Boric Acid Corrosion Control Program Focused Area Self-Assessment,

4/29/09

Program Documents

PSEG Nuclear Salem Units 1 & 2, Alloy 600 Management Plan, Long Term Plan (LTP),

Revision 2, Integrated Strategic Plan For Long Term Protection from Primary Water

Stress Corrosion Cracking (PWSCC), 10/15/09

ASME,Section XI, 1998 Edition, 2000 Addenda, IWA-5244 Buried Components

OAR-1, Owner's Activity Report, #S1 RF019, 1/15/09

Procedures

DETAILED AND GENERAL, VT-1 AND VT-3 VISUAL EXAMINATION OF ASME CLASS MC

AND CC CONTAINMENT SURFACES AND COMPONENTS

SH.RA - AP.ZZ - 8805(Q) - Revision 4, 8/31/06; Boric Acid Corrosion Management Program

ER - AP - 331, Revision 4, Boric Acid Corrosion Control (BACC) Program

ER - AP - 331 - 1001, Revision 2, Boric Acid Corrosion Control (BACC) Inspection Locations,

Implementation And inspection Guidelines

ER - AP - 331 - 1002, Revision 3, Boric Acid Corrosion Control (BACC) Program Identification,

Screening, and Evaluation

ER - AP - 331 - 1003, Revision 1, RCS Leakage Monitoring And Action Plan

ER - AP - 331 - 1004, Revision 2, Boric Acid Corrosion Control (BACC) Program Training and

Qualification

ER - AA - 330 - 001, Revision 7, SECTION XI PRESSURE TESTING

LS - AA - 125, Revision 13; Corrective Action Program (CAP) Procedure

LS - AA - 120, Revision 8; Issue Identification And Screening Process

SH.RA-IS.zZ-0005(Q)-Revision 6; VT-2 Visual Examination Of Nuclear Class 1, 2 and 3

Systems

SH.RA-IS.zZ-0150(Q) - Revision 8, 10/19/04; Nuclear Class 1, 2, 3 and MC Component

Support Visual Examination

OU-AP-335-043, Revision 0; BARE METAL VISUAL EXAMINATION (VEl OF CLASS 1 PWR

COMPONENTS CONTAINING ALLOY 600/82/182 AND CLASS 1 PWR REACTOR

VESSEL UPPER HEADS

OU-AA-335-015, Revision 0; VT 2 - VISUAL EXAMINATION

Areva NP, Inc., Engineering Information Record 51-9118973-000; Qualified Eddy Current

Examination Techniques for Salem Unit 1 Areva Steam Generators, 10/15/09

AREVA NP 03-9123233, Revision 000,10/13/09; Salem Unit 2 RVCH Flange Repair

SC.MD-GP.ZZ-0035(Q) - Revision 9, PRESSURE TESTING OF NUCLEAR CLASS 2 AND 3

COMPONENTS AND SYSTEMS, 02/02/10

SH.MD-GP.ZZ-0240(Q) - Revision 10, SYSTEM PRESSURE TEST AT NORMAL OPERATING

PRESSURE AND TEMPERATURE, 7/29109

S2.0P-AF-0007(Q)-Revision 20, 12/23/09; INSERVICE TESTING AUXILIARY FEEDWATER

VALVES, MODE 3

ER-AA-5400-1002, Revision 1, BURIED PIPING EXAMINATION GUIDE

Specification No. S-C-MPOO-MGS-0001; Piping Schedule SPS54, Auxiliary Feedwater,

Revision 6

PSEG Test Procedure 10-H-8-R1, Unit 2 Auxiliary Feedwater 2100/2150 Hydro; 9/21/78

Attachment A

A-7

NDE Examination Reports & Data Sheets

003753, VT-10-113, PRV nozzle sliding support

003754, VT-1 0-114, RPV nozzle sliding support

006325, UT-10-041 , PZR longitudinal shell weld J (100%)

007500, UT-10-132, PZR surge line nozzle (100%)

007901, UT -10-028, 13 SG lower head to tubesheet weld (67%)

006073, VE-10-026, CRDM TO VESSEL PENETRATION WELD, 4/12/10

008001, VE-10-027, 31-RCN-1130-IRS

008026, VE-10-028, 29-RCN-1130-IRS

009070, VE-10-030, 12-STG Channel Head Drain (100%)

033300, UT-10-027, 4-PS-1131-27 (100%)

033200, UT-10-029, 4-PS-1131-26 (100%)

033100, UT-10-032, 4-PS-1131-25 (100%)

032300, UT-10-033, 4-PS-1131-17 (100%)

031700, UT-10-040, 4-PS-1131-12 (100%)

032600, UT-10-034, 4-PS-1131-20 (100%)

047600, UT-10-045, 29-RC-1140-3 (100%)

051200, UT-10-048, 29-RC-1120-3 (100%)

203901, UT-10-047, 32-MSN-2111-1 (100%)

204001, UT-10-046, 16-BFN-2111-1 (70.64%)

210586, UT-10-025, 14-BF-2141-19 (100%)

210588, UT-10-024, 14-BF-2141-20 (100%)

836300, IWE: VT-10-338, PNL-S1-343-1

836400, IWE: VT-10-333, ALK-S1-100-tubing

840000, IWE: Vert Leak Channels 1 -14

006073, VE-10-026, RPV Upper Head Inspection

006051, PT-10-004, CRDM Housing Weld Exams, penetrations #66, 67, and 72

Salem Unit 1, VT-2, Visual Examination Record, 12/14 AF FDA, W.O. 60089848, 4/26/10 (VT)

Salem Unit 1, VT-2, CA Repair Snoop Test, W.O. 60089575, 4/27/10

Salem Unit 1, UT, W.O. 60084266, Yard AF, 4/18/10

Salem Unit 2, UT, W.O.60089851, Exam of containment liner

Salem Unit 1, UT 1-SGF-31-L2 FW elbow below min. wall

Salem Unit 1, UT, W.O. 30176541, 1-SGF-31-L2 FW elbow below min. wall

Salem Unit 1, UT, W.O. 60084266, AFW .

Order 50113214, ST 550D, Surveillance: lSI Perform PORV Check

Order 50118090, ST 550D, Surveillance: OPS Perform PORV Check

W.O. 60089848, VT-2 Visual Examination Record, 12/14 AFW in FDA, 4126/10

W.O. 941017262, Activity 02; Salem Unit 2, Excavate and Examine Auxiliary Feedwater Piping,

12/2/94

W.O. 60084266, UT Unit 1 AFW (thinnest area), 4/20/10

UT Analysis, Component 1-SGF-31-L2 (14" FW Elbow below Minimum wall), 4/10/10

W.O. 60089851, Unit 2 Containment Liner blister UT measurements, 4/21/10

W.O. 60086175, Unit 1 Containment corrosion 78' elevation

W.O. 60084266, Unit 1 AFW piping UT measurements, 4/12/10

W.O. 30176541, Unit 1 AFW piping UT measurements, 4/12/10

W.O. 60084266, Unit 1 AFW piping UT measurements, 4/7/10

W.O. 60084266, Unit 1 AFW piping UT measurements, 4/5/10

W.O. 60084266, Unit 1 AFW pipe UT measurements at supports, 4/18/10

W.O. 30176541, Unit 1 CA piping UT measurements in FDA

401600, VE-04-198; Hope Creek system pressure test CST to HPCI/RCIC and Core Spray,

Attachment A

A-8

11/5/04

VT-2, Salem Unit 1 AF 12 & 14 Pressure Test, 4/25/10

W.O. 60089661, UT measurements, Unit 2 AFW Piping #24 in FTTA, 4/25/10

W.O. 60089661, UT measurements, Unit 2 AFW Piping #22 in FTTA, 4/26/10

Eddy Current Testing Personnel Qualification Records

A2421 2509981330193 L8267

B8731 K5858 F3453

B0500 1007951330114 T5616

B5127 L9168 R9311

B5128 L4332 G4943

B2576 F7460 C5542

F3961 F0037 F0075

C1560 3107943330158 F6623

D7895 6206070744 F3453

D9573 6507061922 G4943

D6502 1803983330125 G1311

H2039 2709977301226 H7791

K5380 P5304 J9141

M9460 P4006 M0950

E0427 R4201 M2665

M6664 R6452 M7006

B4260 R8002 M9459

A3502 S7752 M7007

J9815 T8251 M9082

P5436 V3197 N7035

M6042 R4142 N9952

B8589 R6279 R9311

B4014 G3380 . S9098

G2573 B3720 T5616

V8530 R6900 T5565

W3368 A9608 W2639

M4305 N2574 W7912

B4052 13805 K6975

C2028 T2170 G3910

C4596 N4815 H0268

C3340 M0945 L3025

D3858 P2963 P1465

H6267 M9715 B8079

H0282 K1903 G1756

14048 D5318 C8071

J1978 W6070 6410058746

2010983302133 M5096 B5371

P6459 J1945 H2131

R0830 L4588 2909965330076

R1164 C8042

S0608 N5330

Attachment A .

A-9

Engineering Analyses & Calculations & Standards

Calculation 6S0-1882, Revision 1, 8/30/96; Qualification of Safety-Related Buried Commodities

For Tornado Missle and Seismic Evaluation

Calculation No. S-C-AF-MDC-1789; Salem Auxiliary Feedwater Thermal Hydraulic Flow Model,

10/4/00

70087436, Steam Generator Degradation & Operational Assessment Validation, Salem Unit 1

Refueling Outage 18 (1R18) & Cycles 19/20, 9/2008

51-9052270-000, Update - Salem Unit 1 SG Operational Assessment At 1R18 For Cycles 19

and 20, 10/1/08

51-9048311-002, Salem Unit 1 SG Condition Monitoring For 1R18 And Preliminary Operational

Assessment For Cycles 19 and 20, 10/30/07

701086998-0050, Maximum Pressure in Underground Auxiliary Feedwater Piping

60089575-130, Past Operability Determination for the leak in the one inch air line to air operated

valves in Unit 1 South Penetration Area

70109233/20459231; Boric Acid evaluation of leakage from S1 CVC-1 CV277

70109232/20459230; Boric Acid evaluation of leakage from S1 CVC-1 CV2

70109230/20459228; Boric Acid evaluation of leakage from S2RC-1 PS1

70109234/20459232; Boric Acid evaluation of leakage from S1SJ-13SJ25

70108698/30, Operating Experience Report for degraded Unit 1 AFW piping

51-9135923-000, AREVA; Salem unit 1 SG Condition Monitoring For 1 R20 and Preliminary

Operational Assessment For Cycles 21 And 22, 4/20/10

SA-SURV-201 0-001, Revision 1; Risk Assessment of Missed Surveillance - Auxiliary

Feedwater discharge line underground piping pressure testing, 4/23/10

CQ9503151526; SCI-94-0877, EXCAVATED AUXILIARY PIPING WALKDOWN/DISPOSITION

OF COATING REQUIREMENTS; 12/16/94

Specification No. S-C-M600-NDS-019, COATINGS INTERIOR/EXTERIOR SURFACES

CARBON STEEL SERVICE WATER PIPING, NO. 12 COMPONENT COOLING HEAT

EXCHANGER ROOM AUXILIARY BUILDING (ELEVATION 84)

Structural Integrity Associates, Inc. Calculation File No.1 000494.301, Evaluation of Degraded

Underground Auxiliary Feedwater Piping (Between Unit 1 FTTA and OPAl, 4/23/10

Technical Evaluation 60089575-0140, Acceptability of CA Piping in the Fuel Transfer Area,

4/29/10

Technical Evaluation 60089848-0960, Auxiliary Feedwater Piping Missle Barrier Exclusion,

4/29/10

Structural Integrity Associates, Inc. Calculation File No.1 000498.301, Evaluation of Thinned

Feedwater Elbow, 4/22/10

Technical Evaluation 70108698-0050, Maximum Pressure in Underground Auxiliary Feedwater

Piping, 4/29/10

SPECIFICATION NO. S-C-MPOO-MGS-0001, Piping Schedule SPS54 AUXILIARY

FEEDWATER, Revision 6

OpEval. #10-005, Salem Unit 2 Operability Evaluation, Received 5/18/10

Technical Evaluation 60084266-105-20, Alternative Exterior Coatings for Buried Piping, AF, CA,

SA and Pipe Supports Under W.O. 60084266, 4/2/10

Technical Evaluation H-1-EA-PEE-1871, Hope Creek Service Piping Coatings Alternatives,

80075587, Revision 0,10/15/04

PSEG Nuclear, LLC, Technical Standard, Coating Systems and Color Schedules, Revision 5,

4/3/06

Attachment A

A-10

Weld Records AFW Piping Repair (W.O. #'s 60084266. 60089561, 60089798, 60089848)

Multiple Weld History Record: 74626

Multiple Weld History Record: 74556

Multiple Weld History Record: 74557

Multiple Weld History Record: 74558

Multiple Weld History Record: 74559

Multiple Weld History Record: 74560

Multiple Weld History Record: 74561

Multiple Weld History Record: 74562

Multiple Weld History Record: 74563

Multiple Weld History Record: 74564

Multiple Weld History Record: 74565

Multiple Weld History Record: 74566

Multiple Weld History Record: 74567

Multiple Weld History Record: 74627

Multiple Weld History Record: 74569

Multiple Weld History Record: 74599

Multiple Weld History Record: 74623

Multiple Weld History Record: 74600

Multiple Weld History Record: 74630

Multiple Weld History Record: 74622

Multiple Weld History Record: 74578

Multiple Weld History Record: 74596

Multiple Weld History Record: 74601

Multiple Weld History Record: 74602

Multiple Weld History Record: 74603

Multiple Weld History Record: 74604

Multiple Weld History Record: 74605

Multiple Weld History Record: 74598

Multiple Weld History Record: 74606

Multiple Weld History Record: 74607

Multiple Weld History Record: 74608

Multiple Weld History Record: 74609

Multiple Weld History Record: 74610

Multiple Weld History Record: 74611

Multiple Weld History Record: 74612

Multiple Weld History Record: 74613

Multiple Weld History Record: 74614

Multiple Weld History Record: 74615

Multiple Weld History Record: 74597

Multiple Weld History Record: 74616

Multiple Weld History Record: 74579

Multiple Weld History Record: 74580

Multiple Weld History Record: 74581

Multiple Weld History Record: 74582

Multiple Weld History Record: 74583

Multiple Weld History Record: 74595

Multiple Weld History Record: 74584

Multiple Weld History Record: 74585

Attachment A

A-11

Multiple Weld History Record: 74586

Multiple Weld History Record: 74587

Multiple Weld History Record: 74588

Multiple Weld History Record: 74589

Multiple Weld History Record: 74590

Multiple Weld History Record: 74591

Multiple Weld History Record: 74592

Multiple Weld History Record: 74593

Multiple Weld History Record: 74577

Multiple Weld History Record: 74625

Multiple Weld History Record: 74574

Multiple Weld History Record: 74624

Multiple Weld History Record: 74573

Multiple Weld History Record: 74572

Multiple Weld History Record: 74570

Multiple Weld History Record: 74571

Multiple Weld History Record: 74623

Multiple Weld History Record: 74622

Multiple Weld History Record: 74621

Multiple Weld History Record: 74537

Multiple Weld History Record: 74538

Multiple Weld History Record: 74537

Welder Stamp Number: P-664

Welder Stamp Number: P-65

Welder Stamp Number: P-466

Welder Stamp Number: P-57

Welder Stamp Number: E-64

Welder Stamp Number: P-710

Welder Stamp Number: P-207

Welder Stamp Number: P-666

Welder Stamp Number: P-708

Welder Stamp Number: E-89

Welder Stamp Number: P-84

Welder Stamp Number: P-228

Surface Exam Record: 60089561-0041

Surface Exam Record: 60089848-0001

Surface Exam Record: 60089848-0001

Surface Exam Record: 60089561-0041

Surface Exam Record: 60089561-0860

Miscellaneous Documents

Salem Unit 1 & Salem Unit 2 Technical Specification, 3.4.11 STRUCTURAL INTEGRITY, ASME

CODE CLASS 1, 2 AND 3 COMPONENTS

Electric Power Research Institute (EPRI), Steam Generator Integrity Assessment Guidelines,

Technical Report 1012987, Revision 2, July 2006

NRC Letter dated 3/11/91; FIRST TEN-YEARINSPECTION INTERVAL, INSERVICE

INSPECTION PROGRAM RELIEF REQUEST, SALEM NUCLEAR GENERATING

STATION, UNIT 1 (TAC NOS. 66013 AND 71101)

Attachment A

A-12

PSEG Nuclear, Salem Unit 1 & 2 Alloy 600 Management Plan, Long Term Plan (LTP), Revision

2,10/15/09

Salem Unit 1 - Buried Piping Risk Ranking

MPR Associates Report, Technical Input To Operability of Potential Containment Liner

Corrosion, Revision 0, 10/30109

Transmittal of Design Information #S-TODI-201 0-0005, 4/20/2010

Transmittal of Design Information #S-TODI-201 0-0004, 4/16/2010

00950315126, PSEG Itr. Dated 12/16/94; Excavated Auxiliary Feedwater Piping

Walkdown/Disposition of Coating Requirements

PSEG letter LR-N07-0224 dated 9/13/2007; REPLY TO NOTICE OF VIOLATION EA-07-149

UNTAGGING WORKLIST 4274446, 14 AF Underground Piping 1R20, 4/30/10

UNTAGGING WORKLIST 4274351, 12 AF Underground Piping 1 R20, 4/30/10

Section 1 R 11: Licensed Operator Regualification Program

Procedures

TO-AA-301, Simulator Configuration Management, Revision 13

2-EOP-TRIP-1, Reactor Trip or Safety Injection, Revision 27

2-EOP-TRIP-2, Reactor Trip Response, Revision 27

Section 1R12: Maintenance Effectiveness

Procedures

ER-AA-310, Implementation of the Maintenance Rule, Revision 7

ER-AA-310-1001, Maintenance Rule - Scoping, Revision 4

ER-AA-310-1003, Maintenance Rule - Performance Criteria Selection, Revision 4

ER-AA-310-1004, Maintenance Rule - Performance Monitoring, Revision 7

ER-AA-310-1005, Maintenance Rule - Dispositioning Between (a)(1) and (a)(2), Revision 7

Notifications

20442453 20456501 20465774 20416718 20409963 20406324

20447948 20373131 20382756 20417863 20377572 20437243

20381571 20444082 20409557

Orders

70104875 70106673 70108607 70108825 70108907 70097082

Other Documents

Salem Nuclear Generating Station Maintenance Rule System Function and Risk Radiation

Monitoring Report, dated May 26, 2010

Salem 1 Narrative Log, dated May 26, 2010

Salem 2 Narrative Log, dated May 26, 2010

Salem 1 and Salem 2, System Health Report (04-2009), Radiation Monitoring System

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

S1.0P-S0.4KV-0002, 1B 4KV Vital Bus Operation, Revision 33

S1.0P-SO.SF-0002, Spent Fuel Cooling System Operation, Revision 20

OU-AA-103, Shutdown Safety Management Program, Revision 12

Attachment A

A-13

SC.OM-AP.ZZ-0001, Shutdown Safety Management Program - Salem Annex, Revision 4

ER-AA-600-1016, ORAM-Sentinel and Paragon Tool Update, Revision 6

S1.0P-ST.4KV-0001, Electrical Power Systems 4KV Vital Bus Transfer, Revision 13

S1.0P-AB.4KV-0003, Loss of 1C 4KV Vital Bus, Revision 8

S1.0P-AB.460-0003, Loss of 1C 460/230V Vital Bus, Revision 7

S1.MD-FR.SF-0001, Alternate Power Source for No. 11 & 12 Spent Fuel Pool Cooling Pumps,

Revision 6

Drawings

203049 203110 203111 203112 203113 203072

Notifications

20458435 20459055 20459059

Other Documents

Salem Unit 1 Shutdown Risk Status Sheet, April 5, 2010 @ 17:00

SGS Unit 2 PRA Risk Evaluation Form for Work Week 014 (March 28 to April 3, 2010), Revision

2

SGS Unit 2 PRA Risk Evaluation Form for Work Week 015 (April 4 to 10, 2010), Revision 0

Salem Unit 1 Shutdown Risk Status Sheet, April 8, 2010 @ 17:00

Tagging Work List 4265994,12 SFP Pump Alt Feed 1R20, April 12, 2010 @ 19:11

SOD-201 0-013, Salem Operations Directive re: Mid-loop Operations, dated April 16, 2010

Salem 1 Narrative Log, dated April 16, 2010

Section 1R15: Operability Evaluations

Procedures

S1.0P-ST.CVC-0008, Reactivity Control Systems - Boration, Revision 7

S1.0P-ST.CVC-0009, Reactivity Control Systems - Boration, Revision 18

S1.MD-ST.SW-0002, Service Water Bays 1 and 3 Outage Inspection and Repair, Revision 4

S1.0P-ST.4KV-0001, Electrical Power Systems 4KV Vital Bus Transfer, Revision 13

S1.0P-AB.4KV-0003, Loss of 1C 4KV Vital Bus, Revision 8

S 1. OP-AB.460-0003, Loss of 1C 460/230V Vital Bus, Revision 7

S1.0P-AB.SG-0001(Q), Steam Generator Tube Leak, Revision 19

S2.0P-PM.CC-0021(Q), 21 Component Cooling Heat Exchanger High Flow Flush and

Alignment, Revision 19

Drawings

223678 223677 223676

Notifications

20435078 20456624 20456318 20153925 20457213 20457563

20457677 20459689 20462034 20461785 20459454 20459204

20458761 20458925 20463859 20463695 20460078 20460278

20464903 20460285

Orders

70108864 70110454 70109482 70108698 70109522

Attachment A

A-14

Other Documents

Calculation Number 267747, Service Water Pumphouse Piping - Bay 1, Revision 9

SWPS-0005, Design Calculation for SWPS-5, Revision 2

SA-SURV-201 0-001, Risk Assessment of Missed Surveillance - Auxiliary Feedwater Discharge

Line Underground Piping Pressure Testing, Revision 1

Section 1R18: Plant Modifications

Procedures

S1.MD-FR.SF-0001, Alternate Power Source for No. 11 & 12 Spent Fuel Pool Cooling Pumps,

Revision 6

Design Changes

Design Change No. 80098748, Modify Pressurizer Spray Valve Internals, Revision 0

Notifications

20458361 20466937

Drawings

D-401193, Revision 1 D-401194, Revision 5

Orders

70104696 80101774

Other Documents

S2010-183, 50.59 Screening for TCCP 1ST-012, Revision 0

TCCP 1ST1 0-012, Plug 13BF19-AO Air Supply Regulator Weep Hole, Revision 0

Section 1R19: Post-Maintenance Testing

Procedures

MA-AA-716-012, Post Maintenance Testing, Revision 14

SC.MD-PM.115-0001, 10/12 KVA Vital Instrument Bus Inverter Preventive Maintenance,

Revision 12

S1.0P-ST.4KV-0002, Electrical Power Systems AC Distribution, Revision 22

S2.0P-PM.CC-0022(Q), 22 Component Cooling Heat Exchanger High Flow Flush and

Alignment, Revision 16

SC.MD-PM.SW-0010(Q), Disassembly, Inspection and Repair of Masoneilan Butterfly Valve

Mark # AA-103, Revision 2

S2.0P-PM.CC-0021 (Q), 21 Component Cooling Heat Exchanger High Flow Flush and

Alignment, Revision 19

SH.IC-GP.ZZ-0003(Q), Removal and Installation of Masoneilan Domotor Actuator, Revision 2

S2.0P-ST.AF-0002(Q), Inservice Testing - 22 Auxiliary Feedwater Pump, Revision 18

S2. OP-ST.SJ-0001 (Q), Inservice Testing - 21 Safety Injection Pump, Revision 19

Notifications

20296405 20463859 20464983 20463639 20463658

Orders

30156599 30152753 60090391 60090348 60088790

Attachment A

A-15

Drawings

A-6207

Other Documents

1A VIB Inverter, Rectifier Inverter Parts Replacement & Test Plan

1A VIB Inverter, Regulator & Static Switch Parts Replacement & Test Plan

Salem 2 Narrative Log, dated May 10, 2010

Salem 2 Narrative Log, dated May 19, 2010

Prompt Investigation Report, 21 CC Heat Exchanger Unexpected Low Flow during High Flow

Flush

Salem 2 Narrative Log, dated May 21,2010

PMI Tool, Template for 21 SW122

Section 1 R20: Refueling and Outage Activities

Procedures

S1.0P-SO.RC-0006(Q), Draining the Reactor Coolant System <101 Ft. Elevation with Fuel in

the Vessel, Revision 26

S1.0P-IO.ZZ-0005(Q), Minimum Load to Hot Standby, Revision 18

S1.0P-IO.ZZ-0006(Q), Hot Standby to Cold Shutdown, Revision 33

Notifications

20453674 20461909 20460492 20460347 20460313 20453797

Orders

70107017

Other Documents

Fatigue Assessments and Waivers, January 1, 2010 - April 21, 2010

ORAM Contingency Plan, RCS at Mid-Loop Post-Refueling

1R20 Outage Risk Assessment Report, Initial Schedule Approval, Revision 0

Salem 1R20 Level 2 with Operations Testing Chart

Salem 1R20 Major Work Scope List

Section 1R22: Surveillance Testing

Procedures

S1.0P-ST.RHR-0005, Residual Heat Removal Valves and Orifices, Revision 6

S1.0P-ST.MS-0003, Steam Line Isolation and Response Time Testing, Revision 9

S1.0P-ST.TRB-0002, Turbine Protection System - Full Functional Test, Revision 17

S1.0P-ST.MS-0002, Inservice Testing - Main Steam and Feedwater Valves, Revision 11

ER-AA-321, Administrative Requirements for Inservice Testing, Revision 10

S1.0P-ST.SJ-0015, Intermediate head Hot Leg Throttling Valve Flow Balance Verification,

Revision 18

S1.MD-AP.ZZ-0012, Salem Mode Change Requirements, Revision 14

SC.MD-DC.RC-0003, Calibration of Pressurizer Safety Relief Valve Indicating Switches,

Revision 5

S1.0P-LR.FP-0001(Q), Type C Leak Rate Test 1FP147 and 1FP148, Revision 0

S1.0P-LR.CVC-0003(Q), Type C Leak Rate Test 1CV116, 1CV284 and 1CV296, Revision 0

S2.0P-ST.SJ-0001(Q), Inservice Testing - 21 Safety Injection Pump, Revision 19

S1.0P-ST.AF-0007(Q), Inservice Testing Auxiliary Feedwater Valves Mode 3, Revision 19

Attachment A

A-16

S1.RA-ST.AF-0007(0), Inservice Testing Auxiliary Feedwater Valves Mode 3 Acceptance

Criteria, Revision 7

Drawings

EHC-1: Simple EHC, Revision2

Notifications

20321206 20460597 20461042 20458712 20457236 20458026

20444513 20462371 20462544 20456929

Other Documents

PR #971003209, MSIV Emergency Hydraulic Override Not Tested

Salem 2 Narrative Log, dated April 24, 2010

Salem 2 Narrative Log, dated May 8,2010

Adverse Condition Monitoring and Contingency Plan, 21 Safety Injection Outboard Bearing

Housing Oil Leak Rate

Section 1EP6: Drill Evaluation

Procedures

NC.EP-EP-0102, Emergency Coordinator Response, Revision 14

1-EOP-TRIP-1, Reactor Trip or Safety Injection, Revision 26

Other Documents

Emergency Preparedness NRC Graded Exercise S1 0-03 Critique Report

Salem Event Classification Guides

SGS EALIRAL Technical Basis, Salem Generating Station Emergency Action Level/Reporting

Action Level Technical Basis Document, Revision 8

S10-03, Salem Graded Exercise Scenario Synopsis

Section 2RS1: Radiological Hazard Assessment and Exposure Controls

Other Documents

Radiation Work Permit #1 Tasks: 4040; 1210404; 23; 27

Section 2RS2: Occupational ALARA Planning and Controls

Other Documents

Daily ALARA Dose Summary Reports, 1 R20, dated April 12-16, 2010

ALARA Reviews: 1/4040; 1/1210404; 1/23; 1/27

Section 40A1: Performance Indicator Verification

Other Documents

Salem 1 and Salem 2, 10/2010 Performance Indicators, Unplanned Scrams per 7000 Critical

Hrs

Salem 1 and Salem 2,10/2010 Performance Indicators, Unplanned Power Changes per 7000

Critical Hrs

Salem 1 and Salem 2,10/2010 Performance Indicators, Unplanned Scrams with Complications

Attachment A

A-17

Section 40A2: Identification and Resolution of Problems

Procedures

SC.MD-PM.13-0003(Q), Westinghouse 13/4KV Power Transformers 11,12 & 21 Preventive

Maintenance, Rev. 4

Notifications

20329373 20330305 20342653 20350143 20370234 20430448

20443177 20443537

Orders

70078697 70101758

Other Documents

Nuclear Oversight Assessment Report, January thru April 2010

Salem Top Ten Low Margin Issues List, Approved June 9, 2010

Salem Critical Component Failure Clock, dated June 18, 2010

Level 1 - 4 Notifications List, December 2009 - May 2010

Salem Top 10 Equipment Issues List, dated May 4, 2010

Salem Units 1 and 2 40 Non-Outage List, dated June 18, 2010

LIST OF ACRONYMS

ADAMS Agency-wide Documents Access and Management System

AFW Auxiliary Feedwater

ALARA As Low As Reasonably Achievable

AOV Air Operated Valve

CAP Corrective Action Program

CC Component Cooling

CCW Component Cooling Water

CFR Code of Federal Regulation

EDG Emergency Diesel Generator

ESOC Electrical System Operations Center

GL Generic Letter

HRA High Radiation Area

HX Heat Exchanger

IMC Inspection Manual Chapter

NCV Non-cited Violation

NEI Nuclear Energy Institute

NRC Nuclear Regulatory Commission

OSP Off-site power

OOS Out-of-Service

PARS Publicly Available Records

PI Performance Indicator

PMT Post-Maintenance Testing

PSEG Public Service Enterprise Group Nuclear LLC

RCS Reactor Coolant System

RFO Refueling Outage

RWP Radiation Work Permit

Attachment A

A-18

SDP Significance Determination Process

SFP Spent Fuel Pool

SW Service Water

TS Technical Specifications

WO Work Order

Attachment A

8-1

Attachment 8

T1172 MSIP Documentation Questions Salem Unit 1

Introduction:

The Temporary Instruction (TI), 2515/172 provides for confirmation that owners of

pressurized-water reactors (PWRs) have implemented the industry guidelines of the

Materials Reliability Program (MRP) -139 regarding nondestructive examination and

evaluation of certain dissimilar metal welds in the RCS containing nickel based Alloys

600/82/182. This TI requires documentation of specific questions in an inspection report.

The questions and responses for MSI P for the IR 05000311/2009005 section 40A5 are

included in this Attachment.

In summary the Salem Units 1 and 2 have MRP-139 applicable Alloy 600/82/182 RCS

welds in the four hot and four cold leg piping to reactor pressure vessel nozzle

connections for each plant.

For Unit 1 during the 1R20 refueling outage in April 2010 PSEG inspected one dissimilar metal

weld, a SG channel head drain line weld. No indications were reported from this inspection.

PSEG plans on replacing this valve, and the dissimilar metal weld, during refueling outage

1R22.

T12515/172 requires the following questions to be answered for MRP-139 MSIP inspections:

Question 1: For each mechanical stress improvement used by the licensee during the Salem U1

1R20 outage, was the activity performed in accordance with a documented qualification report

for stress improvement processes and in accordance with demonstrated procedures?

Response Question 1: No MSIP activities were conducted on U1 during 1R20.

Question d.1: Are the nozzle, weld, safe end, and pipe configurations, as applicable, consistent

with the configuration addressed in the stress improvement (SI) qualification report?

Response - Question d.1: No MSIP activities were conducted on U1 during 1R20.

Question d.2.: Does the SI qualification report address the location radial loading is applied, the

applied load, and the effect that plastic deformation of the pipe configuration may have on the

ability to conduct volumetric examinations?

Response Question d.2: No MSIP activities were conducted on U1 during 1R20.

Question d.3.: Do the licensee's inspection procedure records document that a volumetric

examination per the ASME Code,Section XI, Appendix VIII was performed prior to and after the

application of the MSIP?

Response: Question d.3.: No MSIP activities were conducted on U1 during 1 R20.

Attachment 8